ML18030B228
| ML18030B228 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 03/20/1986 |
| From: | Brooks C, Cantrell F, Patterson C, Paulk G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18030B226 | List: |
| References | |
| 50-259-86-06, 50-259-86-6, 50-260-86-06, 50-260-86-6, 50-296-86-06, 50-296-86-6, NUDOCS 8604080275 | |
| Download: ML18030B228 (19) | |
See also: IR 05000259/1986006
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
ATLANTA,GEORGIA 30323
Report Nos.:
50-259/86-06,
50-260/86-06,
and 50-296/86-06
Licensee:
Valley Authority
6N38 A Lookout Place
1101 Market Street
Chattanooga,
TN
37402-2801
Docket Nos.:
50-259,
50-260
and 50-296
License Nos.:
DPR"33,
and
Facility Name:
Browns Ferry Nuclear Plant
0
C. A.
atterson,
Resi
C.
R. Brooks, Resident,
pe
or
Approved by:
F.
.
antrell, Sectio
'ef
Division of Reactor
Prospects
spc or
Inspection
Conducted:
February
1-28,
1986
Inspectors:
G.
L. Paulk,
Senior
e
d
Inspector
Da
e Signed
z.d
Date Signed
se
Date
igned
'
g
Date Signed
SUMMARY
Scope:
This routine,
inspection
involved
240 resident
inspector-hours
in the
areas
of operational
safety,
maintenance
observation,
reportable
occurrences,
unresolved
items,
surveillance
observation,
previous
enforcement
activity,
housekeeping,
and facility modifications.
Results:
Two violations:
Technical Specification 6.3 for inadequate
procedures,
fai lure to
follow procedures,
and control procedure
changes
of six examples:
b.
C.
d.
e.f.
Failure
to
have
an
adequate
procedure
for fire protection
surveillance.
Changing
a procedure
using
a temporary non-intent
change
instead
of a procedure
revision.
Failure to follow procedure
during chemistry
sample.
Failure
to
have
adequate
proc'edure
due
to not incorporating
a
previous non-intent
change.
Failure to follow procedure
for locking valves.
Failure to properly control clearance
tags.
8604080275
86040k
ADOCN 05000259
8
2.
Technical Specification 3.5.C.7
for failure to satisfy
the
minimum
required
Residual
Heat
Removal
Service
Water
(RHRSW)
Pump
Limiting
Condition for Operation
(LCO).
REPORT DETAILS
Licensee
Employees
Contacted
W.
C. Bibb, Site Director
T.
F. Ziegler, Assistant to the Site Director
R.
L. Lewis, Plant Manager
E. A. Grimm, Assistant to the Plant Manager
J.
E. Swindell, Superintendent
- Operations/Engineering
T.
D. Cosby,
Superintendent
Maintenance
J.
H. Rinne, Modifications Manager
D,
C. Mims, Engineering
Group Supervisor
R.
M. McKeon, Operations
Group Supervisor
C.
G. Wages,
Mechanical
Maintenance
Supervisor
J.
C. Crowell, Electrical Maintenance
Supervisor
R.
E. Burns,
Instrument Maintenance
Supervisor
A,
W. Sorrell, Health Physics Supervisor
R.
E. Jackson,
Chief Public Safety
J.
R. Clark, Chemical Unit Supervisor
B.
C. Morris, Plant Compliance Supervisor
A. L. Burnette, Assistant Operations
Group Supervisor
R.
R. Smallwood, Assistant Operations
Group Supervisor
S.
R. Maehr, Planning/Scheduling
Supervisor
W.
C. Thomison,
Engineering
Section Siipervisor
C.
E. Burke,
Radwaste
Group Controller
Other
licensee
employees
contacted
included
licensed
reactor
operators,
auxiliary operators,
craftsmen,
technicians,
public safety officers, quality
assurance,
design
and engineering
personnel-.
Exit Interview
(30703)
The inspection
scope
and findings were
summarized
on February
28,
1986, with
the
Plant
Manager
and Assistant
Plant
Managers
and other
members
of his
staff.
The licensee
acknowledged
the findings and took no exceptions,
The licensee
did not identify as proprietary
any of the materials
provided to or reviewed
by the inspectors
during this inspection.
Licensee Action on Previous
Enforcement Matters (92702)
(Closed)
Violation
(296/82-24-03)
The
response
to this violation
was
reviewed
and
the
inspector
has
no
further
questions.
A
more
recent
violation
was
issued
in Inspection
Report
85-36
concerning
failure to
conduct
post
maintenance
testing
on
a control
rod drive hydraulic unit.
This item is closed.
(Closed)
Open
Item (260/82-24-04)
Administrative errors
in
scram reports
were
noted
in Report 85-25.
There are
no
new reports to review due to all
the units being
shutdown nearly
one year.
Any future
scram reports will be
reviewed
as part of the routine inspection
program.
This item is closed.
(Closed)
Unresolved
Item (259/260/296/85-36-06)
The inspector
reviewed the
revision to Licensee
Event Report 260/85-04
R1 concerning
the
low pH in Unit
two reactor
and has
no further questions.
This item is closed.
(Closed)
Violation (259/260/296/83-33-03)
The inspector
reviewed the plant
drawings to verify the corrected
instrument setpoints.
This item is closed.
(Closed)
Open Item (296/85-15-09)
No definite reason
for the high pressure
coolant injection
minimum flow orifice bolted joint being
loose
could
be
found.
No similar conditions
were
found
on
the
other units.
The plant
records
showed
that
the last
time
the joint was
worked
the bolts were
torqued
per plant Mechanical
Maintenance
Instruction
MMI 143,
Torquing of
Mechanical
Bolted Joints.
The
procedure
requires
a quality control
inspector's
signature
for verification of the
torquing.
One
unconfirmed
explanation
for the loose connection
was due to plant personnel
lcosing the
connection
due to pipe
hanger
work in the
area.
The
cognizant
engineer
stated
the loose connection
was believed not due to vibration.
This item is
closed.
(Closed)
Violation (259/260/286/84-23-01)
The inspector
reviewed the
licensee's
corrective action
and
Licensee
Event
Report
25984-22
Rl.
This
addresses
the violation
concern
for inadequate
prompt corrective
action
dealing with a non-conformance
report.
Long tern resolution of the design
problem will be tracked
under Violation 259/260/296/84-20-01
which is still
open.
This item is closed.
(Closed)
Unresolved
Item (260/85-57-01)
The licensee
determined
that the
weld distortion was
due to excessive
weld material
and not due to any forces
exerted
on
the
restraint.
Calculations
were
performed
to verify the
structural
integrity of the
support.
No modifications
were
recommended
based
on the original plant design.
This support
has
not
been
evaluated
under Bulletin 79-14 which may require possible modifications.
This item is
closed.
(Closed)
Violation
(259/260/296/83-60-03)
The
inspector
reviewed
a
revision to Operating
Instruction
01-64,
System,
which
contained
updated
instrument inspection list and
has
no further questions.
This item is closed.
(Closed)
Open
Item (259/84-07-06)
The licensee
reported
the problems with
the
EECW air release
valves in Licensee
Event Report 259/84-13.
This report
was
closed
in Inspection
Report
84-10.
The door to the
RHRSW/EECW
pump
rooms continue to remain partially open to prevent possible
flooding due to
a valve failure.
A security guard is permanently
stationed at the entrance
to the
pump
rooms
and routinely observed
by the inspectors.
This item is
closed.
(Closed)
Violation (259/260/296/84-15-01)
The
licensee
response
to this
violation
was
reviewed
and
the
inspector
has
no
fur the<
questions.
Increased
emphasis
has
been
placed
on control of system valve alignments
by
operations'upervision.
This item is closed.
(Closed)
Open
Item (259/84-10-02)
The
inspector
reviewed
the Operating
Instruction for the
standby
gas
treatment
system.
Several
revisions
have
been
made to system lineup checklists.
This item is closed.
(Closed)
Open
Item
(296/84-44-04)
The
diesel
generator
failures
are
addressed
in Violation 259/260/296/85-45-08 'his
item is
closed.
(Closed)
Open
Item
(259/260/296/82-15-01)
The
inspector.
reviewe~
the
revised
drawing update
on the core spray
system.
Interviews with operators
revealed
no
apparent
problems
with the
core
spray
system
high pressure
permissive
keylock
hand
switch
on
Although Unit
3 switch
was
physically installed different
than
the
other
two units,
no operational
problems
have
been identified during testing.
This item is closed.
Unresolved
Items" (92701)
There
are
three
unresolved
items
in paragraph
five concerning
seismic
qualification of control
rod drive "insert
and
withdraw lines,
seismic'-
qualification of various venti lati.on
systems,
and
an
unanalyzed
condition
regarding diesel
generator
loading criteria.
In paragraph
10,
there is
an
unresolved
item concerning installation of instrument lines.
Operational
Safety
(71707,
71710)
The
inspectors
were
kept informed
on
a daily basis
of the overall plant
status
and
any significant
safety
matters
related
to plant operations.
Daily discussions
were held with plant management
and various
members of the
plant operating staff.
The inspectors
made frequent, visits to the control
rooms
when
an inspector
was
on
site.
Observations
included
instrument
readings,
setpoints
and
recordings;
status of operating
systems;
status
and alignments of emergency
standby
systems;
onsite
and offsite emergency
power sources
available for
automatic
operation;
purpose
of temporary
tags
on
equipment
controls
and
switches;
alarm status;
adherence
to procedures;
adherence
to
limiting conditions for operations;
nuclear
instruments
temporary
alterations
in effect; daily journals
and
logs;
stack
monitor recorder
traces;
and control
room manning.
This inspection activity also
included
numerous
informal di scussions
with operators
and their supervi sors.
"An Unresolved
Item is
a matter about which more information is required to
determine
whether it is acceptable
or may involve
a violation or deviation.
General
plant tours were conducted
on at least
a weekly basis.
Portions of
the turbine building, each reactor building and outside
areas
were visited.
Observations
included
valve positions
and
system
alignment;
and
hanger
conditions;
containment
isolation alignments;
instrument
readings;
housekeeping;
proper
power supply
and breaker;
alignments;
radiation
area
controls;
tag controls
on equipment;
work activities in progress;
radiation
protection
controls
adequate;
vital
area
controls;
personnel
search
and
escort;
and vehicle search
and escort.
Informal discussions
were held with
selected
plant
personnel
in their functional
areas
during
these
tours.
Weekly verifications of system
status
which included major flow path valve
alignment,
instrument'lignment,
and
switch
position
alignments
were
performed
on the high pressure fire protection
systems'
complete
walkdown of the
accessible
portions
of the diesel
generator
systems
was
conducted
to verify system operability.
Typical of the
items
checked during the walkdown were: lineup procedures
match plant drawings
and
the as-built configuration,
hangars
and
supports
housekeeping
adequate,
electrical
panel
interior conditions,
calibration
dates
appro-
priate,
system
instrumentation
on-line,
valve position
alignment
correct,
valves
locked as appropriate
and system indicators functioning proper'ly.
Control
Rod Drive (CRD) Insert
and Withdraw Lines Not Seismically
Qualified
The licensee
reported that the
CRD insert
and withdraw lines
do not
meet
seismic qualification.
The original design
by Reactor
Controls
appeared
adequate
based
on techniques
at the time of design
but the
pipe hangers
were designed
by TVA and field installed not in accordance
with drawings.
The
problem is applicable
to all three units.
This,
will remain
an unresolved
item pending further review of the
problem.
(259/260/296/86-06-01).
b.
Inadequate
Design of HVAC System
On February
21,
1986,
the licensee
reported the original design of the
reactor
building
and
control
bay
heating,
ventilation,
and air-
conditioning
(HVAC) systems
was inadequate
and the structural integrity
could not be assured
during
a seismic. event.
This was contrary to
requirements
5.3.2
and
10. 12.3 which state
that the reactor building
and control
bay
HVAC system
are Class
1 structures.
The design
report
listed the potential
consequences
as loss of cooling capability in all
safety-related
plant
areas
(main control
rooms,
auxiliary
instrument
rooms,
residual
heat
removal
and
rooms,
and
shutdown board
rooms.
Also the ability to maintain
secondary
containment
could
be
compromised
by failure of
standby
gas
treatment
ducts
and
reactor
building isolation ducts.
Off gas
stack dilution ducts
may also
be
affected.
This
item will remain
unresolved
pending further review.
(259/260/296/86-06-02).
c.
Unanalyzed
AC Auxiliary Power System
Load Configuration
Through
informal
discussions
with licensee
personnel,
the
resident
inspector
became
aware of a condition which could result in overloaded
Diesel
Generator s.
Continuing discussions
revealed
that the condition
. was
documented
in Significant Condition
Report
(SCR)
BFNEEB8511 dated
8/2/85.
The
SCR documents
that electrical
calculation
on the
Browns
Ferry
AC Auxiliary Power
System
are
based
on
the
"as-designed"
configuration of the plant.
Modifications which have
been
implemented
out
of
sequence
and
undocumented
temporary
loads
have
created
an
"as-constructed"
plant configuration which has
not been
analyzed for
compliance
with General
Design Criterion
17.
The
states
that
system failure modes
cannot
be determined until the system is analyzed
for the
"as-constructed"
cont1guration.
The
licensee
was
awaiting
analysis of the "as-constructed"
configuration prior to determining the
reportabi lity of thi s unanalyzed
condition .
This item is
a potential
violation of 10 CFR 50, Appendix B, Criterion III, Design Control,
and
will be tracked
as
an Unresolved
Item (259/260/296/86-06-03)
pending
completion of the Diesel Generator
Load Study.
The
Diesel
Generator
Load
Study
has
been
ongoing for years.
The
licensee
has
been reanalyzing diesel
loading in each of the postulated
16 modes of operation related to various accident
scenarios
and loss of
off site
power.
A TVA memorandum
dated July 3,
1985,
documented that-
the preliminary load analysis
resulted
in potential
overloads
of the
diesel
generators
and
480V
shutdown
transformers.
The
memorandum
requested
that Design Services
review the load study to verify that the
study accurately
reflects
the anticipated
loading at
Browns
Ferry.
While in the
process
of this
review the
discussed
above
was,
incorporated into the load study and field walkdowns were initiated to
determine
the as-built condition of the plant for use in completing the
diesel
load study.
Resolution
of the potentially overloaded
diesels
will be tracked along with the Unresolved
Item discussed
above for the
6.
'Maintenance
Observation
(62703)
Plant maintenance
activities of selected
safety-related
systems
and
components
were observed/reviewed
to ascertain
that they were conducted
in
accordance
with requirements.
The following items
were considered
during
this
review:
the limiting conditions for operations
were
met; activities
were
accomplished
using
approved
procedures;
functional
testing
and/or
calibrations
were
preformed prior to returning
components
or
system
to
service;
quality control
records
were
maintained;
activities
were
accom-
plished
by qualified personnel;
parts
and materials
used
were
adhered
to;
Technical
Specification
adherence;
and radiological
controls
were
imple-
mented
as required.
Maintenance
requests
were
reviewed to determine
status of outstanding
jobs
and
to
assure
that priority
wa's
assigned
to
safety-related
equipment
maintenance
which'might affect plant safety.
The inspectors
observed
the
below listed maintenance activities during this report period:
Emergency
Diesel Generator
3EC,
Cracked
Housing
While performing
the
vendor
recommended
3,
6,
and
12 year
diesel
maintenance,
the
licensee
discovered
cracks
on the diesel
accessory
drive housing
assembly
which supports
various shaft-driven
pumps.
The
cracks
on the drive housing
are between
the bolt holes
and housing.
The
bolt holes
have
a steel
insert that is press fit into the
assembly.
The
cracks
were
not
observed
on
the four Units
1
and
2
diesels
or the
3EB
and
3ED diesels.
The
housing
was
replaced
on the
3EC diesel
and the
3EA diesel
remains to be inspected.
Tagout Clearance
Procedures
Many problems with the control of clearance
tags were identified during
this report period.
On February 9,
1986,
the inspector
found Tag No.
4
of Clearance
No.
85-1304
improperly installed.
This clearance
was to
provide electrical isolation of two circuits exiting fuse block FBI on
Reactor
Protection
System
on
Unit 2.
The
fuse
block
contains
one
fuse
and
a shorting link.
The
tag
was to isolate
the
circuits by pulling the fuse
on one circuit and lifting the lead
on the
other circuit containing
the shorting link.
The inspector
found that
the fuse
was pulled
and tagged;
however,
the circuit containing the-
shorting link was intact.
The lifted lead that
was
tagged
was
a lead
in the fused circuit so that the fused circuit was double isolated but
the
circuit with the shorting link remained
intact.
Clearance
No.
85-1304
had similar tags
hung
on Panels 9-84, 9-85 and 9-86.
Although
some of the tags
were
hung properly,
Tag
No.
5 and
Tag No.
7 for fuse
blocks
in
and
9-86 respectively
were
found in the
same
inadequate
condition as
Tag
No. 4.
On February
12,
1986,
two additional
problems
were found with clearance
tags
on fuses.
Tag
No.
12 of Clearance
No.85-949 was issued to
remove'use
13A-F23 on Panel 9-33 of Unit 2.
This fuse is in the Reactor
Core
Isolation
Cooling
System.
The
plant
practice
for setting
up
a
clearance
boundary
by pulling
a fuse is to
remove
the
fuse
from the
fuse clip and install
a
wooden
dowe).
This is to prevent inadvertent
replacement
of the fuse.
Tag No.
12 was found laying on the bottom of
Panel 9-33 with no dowel
attached.
Although fuse
13A-F23 was
removed
from the
fuse clip,
no dowel
was installed
in its place.
Also
on
February
12,
1986,
Tag
No.
8 of Clearance
No. 85-1517
and
Tag
No.
6 of
Clearance
No.85-949 were
found attached
to
a wire way.
Both of these
tags were
supposed
to be installed
on
a wooden
dowel placed in the fuse
clip for fuse
on Unit 2.
Although fuse
was
pul 1 ed,
the
tags
wer e
not properly control ling the
cl earance
boundary.
During a daily tour on February
17,
1986, yet another
clearance
problem
was
noted.
Tag
No.
11
on Clearance
No.85-510
was attached
to the
Limitorque valve
operator
hand
wheel
for valve
2-FCV-74-77
in the
Residual
Heat
Removal
(RHR)
system
on Unit 2.
This valve operator
had
been
removed
from the valve
and
was laying
on the floor with the tag
attached.
The
valve itself
had
also
been
removed
from the
system.
Work on this valve
had
been
allowed to proceed
even
through it was
established
as
a clearance
boundary for work on different valves in the
system.
Discussion
with
licensee
representatives
indicated
that
although this type of activity was not specifically prohibited by the
clearance
procedures,
a
breakdown
in
the
coordination
of
the
two
competing maintenance activities
had occurred.
The tag
was subsequently
authorized to be removed
by the Shift Engineer.
In all of the above cases,
the clearance
discrepancies
were immediately
reported, to the responsible shift engineer or assistant
shift engineer
who took prompt corrective action.
Each
instance
was
discussed
with
members
of the plant
management
during
the
routine daily meeting.
These
are also
included
as
examples
of
a violation for failure to
adhere to procedures
(259/260/296/86-06-04).
7.
Surveillance
Testing Observation
(61726)
The
inspectors
observed
and/or
reviewed
the
below listed
surveillance
procedures.
The inspection
consisted
of
a
review of the
procedures
for
technical
adequacy,
conformance to technical
specifications,- verification of
test instrument calibration, observation
on the conduct of the test,
removal
from service
and return to service of the
system,
a review of test data,
limiting condition for operation
met,
testing
accomplished
by qualified
personnel,
and
that
the
surveillance
was
completed
at
the
required
frequency.
Fire Protection Surveillance
The
inspector
observed
part of the
annual
Surveillance
Instruction,
S. I.4. 11.A. l.e, Testing of Fixed Water Nozzles for Blockage.
Over the
course
of several
days,
four non-intent
changes
were
necessary
to
complete
the procedure.
( I)
Observation
on 2/5/86
After several
people
were
assembled
in the reactor building, the
surveillance
was
immediately
stopped
because
the craft personnel
recognized that the procedure did not require isolation of all the
necessary
valves.
This portion of the
procedure
tests
the
dry
pipe
in the
reactor
building
by blowing air through
the lines
while the
nozzle outlets
are
checked
for passage
of air.
The
surveillance
was
being
performed
in
the
unit three
reactor
building for zones
3C
3D - 3E
3F.
A non-intent
change
made
on
1/29/85
had left only
one
isolation
valve for these
zones.
Although Units I and
2
had previously
been
tested prior to the
1
inspector's
observations,
a
change
was
not
made for those units.
If the
procedure
was followed, -only
one
valve
was
isolated
to
perform the test.
The valves
are
closed
to prevent
inadvertent
initiation of the
deluge
valve
and
spraying
down
the
reactor
building.
After a non-intent
change
was
made
the test continued
in the afternoon for zones
3C - 3D - 3E - 3F which were isolated
by shutting
valves
3-26-993
and
3-26-1162.
Next the inspector
observed
testing
on
zones
3A and
3B
which
were
isolated
by
shutting valves 3-26-992
and 3-26-1165.
Upon further review of the procedure
the inspector
noted several
inconsistencies
and
problems.
The non-intent
change
performed
1/29/86
changed
the valve isolated for 20 valves
from isolating
the individual deluge valve for a zone of nozzles
to isolating
a
valve in the line which isolated
several
zones.
Although
the deluge valve was listed by number
and the deluge valve listed
as
the
isolation,
this
valve
is
not isolated.
Other
isolations
are
closed
to isolate
the deluge
valve but were not
specified
by valve
number.
Also,
16 header
valves were deleted.
This was
a major revision to the procedure affecting nearly all of
the valves
and the
number of fire protection nozzle
zones .isolated
at
one
time.
The
inspector
reviewed
the definition of intent
changes
and non-intent
changes
defined in Browns Ferry Standard
Practice
1.3.
One of the -definitions applicable
to this
change--
was change
in scope,
technique,
or sequential
order of instruction
steps that would affect the result or nuclear safety.
Also noted
was that the fire protection
engineer
had
reviewed
the original
procedure
but the non-intent
change
was
not reviewed
even
though
changes
to the
amount of fire pr~tection
equipment
taken
out of
service at one time were
made.
(2)
Review of Fire Protection
Equipment
Removal
From Service Permits
In addition,
the inspector
reviewed the Fire Protection
Equipment
Removal
From Service
Permits
in the procedure
package at the job
site.
Permit
197 for zones
3N
3g -
3P
had
expired
at
2400
2/4/86 but had not been
signed
as being returned to service
as of
2/5/86.
The craft personnel
discussed
this with the
foreman
who
stated
the master
copy in the control
room had been
extended.
The
inspector verified that the permit
which originally started
at
0700
on 1/29/86
had
been
extended
to 2400
on 2/6/86.
Later review
found the permit extended
again to 2400
on February 7,
1986.
The
inspector
noted that although permit
201
was for zones
3D - 3E-
3F that the method of isolating the zones
using the header
valves
isolated
3C
3d
3E - 3F.
No permit could be found for 3C zone.
Likewise,
no permit could be found for zones
3A 3B.
Discussion
with the fire protection
engineer
revealed
that
the
procedure
allows for equipment
to
be
removed
from service
for one
hour
without
a permit but the
procedure
was
being revised
and plant
personnel
had
been
instructed
to notify the fire protection
engineer
any time equipment
was
removed
from service.
The fire
protection
engineer
stated
the
following permits
had
been
completed:
199
Unit One
Zones
A, B, C,
D,
E,
F
198
Unit Two
Zones
P,
R,
N,
Q
200
Unit Two
Zones J,
K.
L
The
method
of
using
the
permits
appeared
to
be
totally
inconsistent.
Oelay oi 2/7/86
The test
was again delayed
on 2/7/86 for another non-intent
change
necessary
for testing
the
nozzles
in the high pressure
coolant
injection room.
The original procedure
required that
a test
hose
be
connected
for the air supply but the non-intent
change
was
necessary
since there
was
no test connection
and
a nozzle
had to
be
removed to connect
the air supply.
The inspector
noted
the
non-intent
changes
made
on 2/7/86
and 2/5/86 were
made
such that
a
historical
record of the change
might be lost.
On the non-intent
change
form a block is designated
"Change to Read" but instead of"
identifying
the
pages
or
procedure
step
changed,
the
block
contained
the words
"See attached".
If the
staple
was
removed
from the cover
sheet it would be difficult to tell what had been
changed
and
a historical record of the transaction
would be lost.
Observations
on 2/10/6
The
inspector
observed
the test for the Unit
3
high
pressure
coolant
injection
room.
After
completion
of
the
test
the
inspector
questioned
what
the
signature
in
the
procedure
represented.
The
procedure
was
nearly
completed
at this time.
The foreman stated
the
signatures
were for verifying the
nozzles
were
not obstructed
and
second
party verification was required.
However, the inspector
recalled. that the inspection
performed
on
2/5/86
had
only
a
single
person
in the
overhead
to verify the
nozzles
not blocked.
Also, due to the format of the data
sheet it
appeared
that the craft personnel
were signing for the test
hose
completion
and removal but not for verifying the nozzles
were not
obstructed.
The
column
heading
entitled
"nozzles
not blocked,
initials/date", aligned with the
second party signature
blank for
the test
hose,
but the
same
person
had
signed
in this vertical
column
indicating
the
signatures
were
for
the
test
hose
installation
and
removal.
No signature
could
be
found for the
nozzles.
The inspector
noted
the last time the surveillance
was
completed
using
a different data
sheet
format the
nozzles
were
10
verified twice as not blocked.
The cognizant engineer
stated that
a space
was
on the data
sheet for the signature
but the block had
no line for
a signature
like the
other
signature
blocks.
The
craft
people
were
instructed
to
now
go
back
and
sign for the
nozzles "not blocked" in the
space.
The double verification was
stated to not be required.
(5)
Review of Past Surveillances
The inspector
reviewed the completed Surveillance Instructions for
4. 11.A. l.e
performed
on 6/9/85,
6/18/84,
and
5/31/83.
The
procedure
was basically the
same
as the procedure
used before the
non-intent
changes
were
made but was performed without difficulty
and
no major revisi~n.
Failure to have
an adequate
procedure for the non-intent
change
on
1/29/86 which was used for Unit
1 and Unit
1 testing
and failure
to
have
a
data
sheet
with adequate
format
such that
personnel
could tell what the signatures
signified were given as
an example
of a violation against
T.
S. 6.3, (259/260/296/86-06-04).
Likewise,
making
a
temporary
change
to the
procedure
for the
non-intent
change
1/29/86 which was
an intent
change
was another
example of the violation against T.S.6.3,
(259/260/296/86-06-04).-
b.
Chemistry Surveillance
Three
samples
were observed
during this surveillance
The first sample
observed
was for the performance
of Surveillance
Instruction,
S. I. 4.8.B.2-3a
Airborne
Effluents
(Weekly
Gamma
Isotopic)
for
the
radwaste
building
monitor
0-RE-90-252
on
February
5,
1986.
The -S. I. referenced
Chemistry Instruction
430
and Section
430.3
was
used for the
sample.
During collection of
the
sample,
using
a marinelli beaker,
the
red alarm light on top
.
of the
monitor
was
received.
The technicians
stated
this
was
normal
and it was
a low flow alarm due to sampling.
The inspector
noted that the flow light on the side of the monitor was not lit
and the procedure
contained
no note that this should occur.
Next the
sample
was
taken to the chemistry
count
room where the
sample
was
placed into the counter.
The technician
had initiated
the
counting
from
a
computer
terminal
and
was waiting
as
the
sample
was
counted.
However,
another
technician
in
the
Lab
cautioned
the technician
that the
wrong terminal
was
being
used
for the
counter.
Although Chemistry
Instruction- 701,
Acquisition and Data Reduction,
Section
VI, Step
B. 1. requires
a
check for the
proper detection
and terminal, this step
was not
11
performed.
The inspector
was particularly concerned
that
a count
of air
could
have
been
taken
without detection.
Thi s
sample
routinely has
a count rate
near
background
and
an error
such
as
this could easily overlook
a real
problem.
Next,
the
sample
was
counted
using
the correct
terminal
and
detectors.
One 'step in the
computer
program
asked for the stack
monitor count rate
in counts
per
second
(CPS)
and
a value of 17
was entered.
However, another technician
said the value should
be
around
6
or
7
CPS.
The
technician
determined
that
the
stack
flowrate of 17,000
in units of cubic feet
per
minute
had
been
entered
instead of the count rate in units of CPS.
The technician
stated this part of the
program
was irrelevant to the procedure
but data
had to be entered
to <<ake the program run.
The cognizant
engineer
was called to determine if the error could affect the
results
and if
a
recount
was
necessary.
The
stack
monitor
controls
were determined
irrelevant to the results
and
the test
proceeded.
Later,
the
cognizant
engineer
stated
the
software
needed
improvements
(2)
During the test
some discussion
occurred with the technician
about
the value of the marinelli beaker
as to whether it was
one liter
or two liters.
After the test it was
learned
that
the
beaker
volume
was
1240
and
was specially calibrated.
The
geometry
was
such that the inside of the beaker
was
recessed
to fit over
the detector
probe for better
counting
geometry.
The inspector
noted that this volume was listed
on the computer
output sheet
and
the technicians
seemed
unfamiliar with their test equipment.
This
procedure
is performed routinely avery week.
This
same
procedure
was
observed
in the past
and is discussed
in
Inspection
Report
84-10.
A violation with
seven
examples
was
issued
for procedural
problems
at that
time.
An
example
of
a
violation
against
Technical Specification 6.3 for failure
to
follow
procedure
was
given
for
this
observation.
(259/260/296/86-06-04).
The
second
sample
observed was'or
the Turbine/Reactor
Building
combined exhaust
and
no problems
were noted.
(3)
The third sample
observed
was for the plant stack.
Taking of the
sample
was attempted
on February
5,
1986,
but
had to
be
stopped
pending
interpretation
of procedural
inadequacies.
The
sample
procedure,
BF CI 466.51, if performed
as written would have left
the continuous monitor inoperative after the
sample
was taken
due
to closing of valves
90-305A
and
90-282N.
Upon investigation it
was
noted
that
an
attempt
to correct this condition
had
been
previously
conducted
with
a
non-intent
change
drafted
during
November,
1985,
but the non-intent
change
had not
been
properly
12
implemented
in that it was absent
from both the chemist's
copy and
the copy that the inspector obtained
from the master file in the
drawing control center.
The procedure
was again revised
and stack
sample
was
resumed
on
February
6,
1985,
and
completed
with
no
further
incident.
Failure
to
have
an
adequate
procedure
is
another
example
of
the
violation
against
T.S.
6.3
(259/296/296/86"06-04).
c.
Electrical Surveillance
On February 4,
1986,
the resident
observed
surveillance,
S. I. 4.9.A.2a
(Auxiliary Electrical
Equipment - Battery Check).
The surveillance
was
satisfactorily
completed
on the
"A" and "B" shutdown
boar'd
250 V.D.C.
batteries.
Several
minor
def>ciencies
were
~ointed
out
to
the
cognizant engineer
including:
( 1)
The
"B" shutdown
board battery
was
being maintained
at
a float
potential
greater
than that
recommended
by the
procedure,
2.25
volts/cell,
due
to
three
jumpered
cells.
The
licensee
had
previously received
vendor
concurrence
to exceed
2.25 volts/cell,
up to
a
maximum of 2.33 volts/cell for
a
one year time frame.
However, this time limit had
been
exceeded
and
no administrative
controls
had been
implemented to address
this occurrence.
(2)
The
data
sheet
was deficient
in that individual battery
pre-
requisite
and precaution
signoffs were not included.
Other minor
data
sheet
deficiencies
were pointed out to ease
in technician
procedural clarification.
(3)
The associated
battery chargers'nternal
cabinets
and the battery
rooms
were
observed
to be deficient in regards
to proper
house-
keeping requirements.
d.
System
On
February
10,
1986,
the
inspector
observed
the
performance
of
Surveillance
Instruction,
S. I.4.4.C.3
Standby
Liquid Control System-
Boron Concentration.
The surveillance
requires that the
SLC System
be
sampled
per
Chemistry
Instruction
(C. I.)
463. 1,
Sampling
Pentaborate
from the
Storage
Tank.
Prior to
sampling,
air
is
sparged
through
the
storage
tank for
15 minutes
to obtain
a
representative
sample.
After the air lineup is isolated,
Step
VI.C
requires
that the air. supply valves
be verified locked.
Data
Sheet
S. I. 4.4.C.3
provides
sign off spaces
that
valve
63-536
is
locked
closed
and second
person verification that the valve is locked closed.
When
the
chemistry
technician
noted
that
no
locking
device
was
installed
on valve 2-63-536,
he engaged
in
a discussion
with the valve
operator
who assured
him that
an air isolation valve upstream of valve
2-63-536
was locked closed
and therefore
no locking device
was
needed.
13
Both the valve operator
and chemistry technician
then initialed on the
S. I. 4.4.C.3
Data Sheet that valve 2-63-536
was locked closed.
This is
another
example
of
a violation for failure to follow to procedures.
(259/260/296/86-06-04).
Diesel Generator
Testing
On February 21;
1986,
the inspector
observed
the
performance
of S.I.
4.9.A. l.b,
Diesel
Generator
Emergency
Load
Acceptance
Test.
The
surveillance
involved close coordination
between operations,
electrical
maintenance
and
Power Systems
Operations
(PSO).
The procedures
upgrade
engineer
responsible
for revising
the
procedure
also
observed
the
surveillance
in order to gain first hand
knowledge of the procedure
and
interview the
personnel
performing the test.
One typogra, hical error
and
many procedure
enhancements
were identified.
The surveillance
was
carefully controlled by the Assistant Shift Engineer
and was completed
without incident.
Reactor Building Ventilation Radiation Monitors
While
performing
Surveillance
Instruction,
S.I.
4.2.A-10,
Reactor
Building Ventilation Radiation Monitors,
on February
15,
1986,
on Unit
2
equipment,
the
logic circuit
was
found
to
deviate
from
the
as-constructed
drawings'his
deviation
was discovered after the
S.
I'as
revised
such that jumpers
used in the test were placed in different
locations
than
in previous test performances.
Specifically,
a contact
of the
Reactor
Zone
Exhaust
Radiation
Monitor upscale
trip relay
( 16A-K61A
shown
on
drawing
730
E
927
SH
18)
was installed
in
a
different location from that
shown
on <he, drawing.
Licensee
personnel
evaluated
the discrepancy
and determined
that the circuit would still
perform its intended
function.
A Drawing
Discrepancy
was
issued
to
revise
the
drawing
such
that it would
match
the as-built
plant
configuration.
(Drawing
Discrepancy
No.
730
E
927
SH
18,
dated
2/15/86).
The
inspector
questioned
whether
this
would
be
the
appropriate
corrective action
as
opposed
to re-wiring the contacts
to
match
the plant drawings.
The
same
drawing is applicable to all three
units,
however,
the deviation
is only present
on Unit 2.
Initial
discussions
with licensee
representatives
resulted
in an agreement
that
the plant configuration should
be changed
to agree with the drawing and
that
a Discrepancy
Report would be
issued to accomplish this.
Later,
licensee
representatives
stated
that
the
Standard
Practice
which
controls
the Drawing Discrepancy
program included sufficient checks to
ensure
that in cases
like this,
drawings
are
not blindly revised
to
match
the plant configuration,
but that
a proper evaluation
of the
required corrective 'ction is performed.
The plant will continue
to
track the deviation through the Drawing Discrepancy
program
as
opposed
to
issuing
a
Discrepancy
Report.
An
Inspector
Followup
Item
(259/260/296/86-06-05) will'e
opened
to
follow this
particular
deviation
through
resolution
as
well
as
to investigate
the
generic
potential that hardware deviations
may be resolved
by drawing changes.
14
8.
Reportable
Occurrences
(90712,
92700)
The below listed licensee
events
reports
(LERs) were reviewed to determine
if the
information
provided
met
NRC
requirements.
The
determination
included:
adequacy
of event
description,
verification of compliance with
technical
specifications
and
regulatory
requirements,
corrective
action
taken,
existence
of potential
generic
problems,
reporting
requirements
satisfied,
and the relative safety significance
of each
event.
Additional
in-plant reviews
and discussion
with plant personnel,
as appropriate,
were
conducted
for those
reports
indicated
by
an
asterisk.
The
following
licensee
event reports
are closed:
LER No.
259/86-01
Date
1/07/86
Event
Stack
Gas Monitoring
Recorder
"296/86-02
l/16/86
Inadvertent
Diesel Start During
Performance
of a Plant Instruction
Due to Personnel
Error.
260/85-19
"260/85-18
12/13/85
-
Inadvertent
Containment Isolation
11/06/85
'-
Creation of a Potential
to
Violate Secondary
Containment
260/85-04
"296/86-04
6/11/85
2/21/86
Reactor Mater Chemistry-Low
pH
Removal of Diesel Generator
From
Service
Leads to Prohibited
Configuration
was reviewed to determine if the event satisfied the criteria
of
a licensee
identified violation pursuant
to
Appendix
C.
A
compliance
engineer
identified that
the
plant
failed to satisfy
the
requirements
of Technical Specification 3.5.C.7
about
5
days after
the
occurrence.
A one-hour
report
was
made
to
the
NRC pursuant
to
on
January
30,
1986
and
the
followup
LER was
submitted
on
February
21,
1986.
A Notice of Violation will be
issued for this event
(296/86-06-06),
however,
since this violation could reasonably
be
expected
to
have
been
prevented
by the licensee's
corrective
action for
a previous
violation.
Violation 259/260/84-26-02
was issued
on October
17,
1984.
This
violation followed
an
enforcement
conference
conducted
on August 30,
1984,
during which the
NRC Regional Administrator
expressed
his concerns that the
licensee's
Technical Specification
must be clear
and understandable
and that
the
licensee
should
make
a
concerted
effort to
upgrade
the
Technical
Specification to eliminate confusion
and ambiguity.
LER 296/86-04 indicated
that
once
again
several
interrelated
TSs
were
involved and contributed
to
the
complexity of the event
assessment.
This
LER additionally failed .to
15
indicate that the prior violation (reported in
was
a previous
similar event.
A licensee
representative
indicated that the precious
LER
was considered,
but was judged
not to
be
similar.
Without
a
review of
corrective action for previous violations,
there
can
be
no confidence that
corrective
action instituted
as
a result
of the
recent
event
wi 11
be
effective.
The
NRC judges
these
two event to be similar for the following reasons:
a.
Both events resulted
in plant operation outside the limiting
condition for operation
( LCO) for
RHRSW as
specified in the Technical
Specifications.
b.
Both events
were contributed
Co by ambiguous
wording in the Technical
Specifications
dealing with RHRSW pump requirements
and the definition
of equipment operability
as it related
to the onsite
emergency
power
source (diesel
generators)
and
RHRSW pumps.
C.
The
cause
of both events
has
been attributed
to personnel
error.
In
response
to Violation 259/260/84-26-02,
the licensee
stated that "plant
personnel
misinterpreted
Technical
Specification
1.C.2".
This is the
LCO definition as it related to operability of offsite or diesel
power
sources.
For the recent'vent,
the
licensee
stated
in
that "the
cause
of the
event 'is attributed
to oversight
by
shift'ersonnel
in determining all system operability requirements."
This item was discussed
in detail during
a routine daily meeting with
plant management
on February
25,
1986.
9.
Housekeeping
Observation
An inspector
toured
the
Reactor
and Control Buildings for the
purpose
of
determining
the status
of plant housekeeping,
General
cleanliness
was poor
and conditions
observed
indicated lack of effort to perform indepth cleaning
other
than routine surface cleaning.
Hard to get to areas
such
as crevices,
cabinet foundations,
cable trays, penetrations,
etc., did not
show adequate
cleaning effort.
Specific examples
of areas
of concern
are
as follows:
Many electrical
and
pipe penetration
areas
in Reactor
Buildings were
dirty.
Cables
in cable
trays
in Reactor
Building were dirty, Plant
Stack
ground floor, mesanine,
and
sample
areas
were dirty.
Ground floor had
large
amount of loose materials lying around.
Area inside
MOV Board
BD3D cabinets
was dirty.
Units
1 and
2 shared
shutdown
board battery chargers
contained
a thick
coat
of lint
and dirt within the
cabinets.
One of the
cabinets
contained
a large
amount of stripped
electrical
insulation
material
16
that
had
not
been
cleaned.
up from
a previous electrical
termination
activity. Additionally, the
two battery
charger
cabinets
appeared
to
have incorrect unit identification labels.
Cable spreading
areas
were dirty.
Units
1
and
2
shutdown
board battery
rooms
were dirty inside.
All
cells in both batteries
require external
cleaning.
a
damaged
battery
cell terminal
was lying on floor (the associated
cell
had
been
jumpered
over one year prior).
Several
sections of flexible conduit associated
with the battery rooms'entilation
fans
and dampers
were observed to
have loose connections.
The above conditions existed in spite of the fact that all three units were
in cold
shutdown with
a
minimum of outage activities in progress.
It does
not appear
that
the
licensee's
housekeeping
program,
as
implemented,
is
fully effective.
10.
Facility Modification (37701)
This
supplemental
inspection
was
conducted
to determine
whether facility
modifications that require prior review
and approval
from the
Commission
pursuant
to
are completed .in conformance with requirements
in
the facility license,
technical
specifications,
and
applicable
industry
codes
and
standards.
Specifically, work associated
with the replacement
of
certain
Reactor
Protection
System
and
Emergency
Core
Cooling
System
mechanical
type instrumentation
switches with analog transmitter/trip unit
(ATTU) instrumentation
was observed.
Engineering
Change
Notice
(ECN)
P0126
implements
the modification for Unit 2.
The.
ECN is scheduled for completion
prior to startup.
The actual
work is divided into
some
48 work packages
which
include
cable,
conduit,
and
junction
box
installation;
panel
installation;
panel
internal wiring; transmitter
installation;
instrument
piping installation;
cable
pulling;
and
post modification testing.
The
current
status
of work packages
is
as
follows:
4-complete,
6-not yet
written, 2-in approval cycle, 36-working.
The inspector
observed
work being
performed
under
Work Plan
No.
2040-85,
Install piping/tubing and supports for ins'trument
sensing
lines for the
new
trensmitters
at panel
25-5A, 25-6-1
and
new panels
25-5C,
25-5D, 25-6c,
and
25-6D.
This work plan requires
instrument lines to be installed
per General
Construction
Specification
No.
G-60
Rev.
1.
The preface to this construc-
tion specification states
that the Revision
1 issue of this specification is
applicable to Bellefonte Nuclear Plant only. Licensee representatives
stated
that this specifidation
was being
used for work at Browns Ferry since there
is
no existing
specification
applicable
to
Browns
Ferry.
The
licensee
intends to revise Specification
G-60 to make it applicable to Browns Ferry.
This will be tracked
as
an Inspector
Followup Item (259/260/296/86-06-07)
to
ensure
that
any
technical
revisions
that
may
be
needed
to
make
the
specification
applicable
to Browns Ferry are
reviewed for compliance with
the physical
work already completed.
17
Section
3.3.1
of Specification
G-60 requires
instrument lines to have
a
downward
slope of I inch per'o'ot
except
where this is impractical
due to
equipment
location or piping geometry.
In that
case,
the line could
be
sloped
as
much
as
possible,
but not
less
than
1/8
inch
per foot.
The
inspector
observed
many instrument
sensing
lines installed
under
the work
plan
which
had
minimal
slope
with
no
apparent
interference
which would
prevent
achievement
of
a full inch per foot slope.
Personnel
involved in
the installation
stated
that lines
were built to obtain
a 1/8 inch slope.
Modifications managers
were contacted
and
agreed
that
the intent of the
construction
specification
was
not
being
met.
A walkdown of the
work
located
one
section
of piping which did not satisfy the
minimum 1/8 inch
slope.
All other instrument lines would be considered
acceptable
based
upon
the minimum slope criteria.
Future work plans
wi 11 explicitly require
a
1
iach
per
foot
slope
to
be
attained
unless
the
cognizant
engineer
is
contacted
and gives approval for using the
minimum slope criteria
when the
geometry
prevents
attainment
of the
nominal
slop'e.
This
item will be
tracked
as
an
Unresolved
Item
(259/260/296/86-06-08)
pending
necessary
rework and final closeout
and acceptance
of the work plan.