ML18025B407

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IE Insp Repts 50-259/81-03,50-260/81-03 & 50-296/81-03 on 810101-31.Noncompliance Noted:Secondary Containment Not Maintained & Radioactive Contaminated Ladder Found in Clean Area
ML18025B407
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 03/09/1981
From: Cantrell F, Chase J, Paulk G, Sullivan R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18025B408 List:
References
50-259-81-03, 50-259-81-3, 50-260-81-03, 50-260-81-3, 50-296-81-03, NUDOCS 8103270104
Download: ML18025B407 (20)


See also: IR 05000259/1981003

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

.'EGION II

'01

MARIETTAST., N.W., SUITE 3100

ATLANTA,GEORGIA 30303

Report Nos.

50-259/81-03,

50-260/81-03

and 50-296/81-03

Licensee:

Tennessee

Valley Authority

500A Chestnut Street

Tower II

Chattanooga,

TN

37401

Facility:

Browns Ferry Nuclear Plant

Docket Nos.

50-259,

50-260 and 50-296

License Nos'.'PR-33,

OPR'-52 and DPR-68

'nspection

at Browns Ferry Site near Athens,

Alabama

Inspectors:

. F. Sulli an,

S

ior Resident Inspector

z-z- P/

Date Signed

J.

W. Cha~

,

Re

dent Inspector

Res dent inspector

1

G. L. Pau

Appr.oved by.- ~~

. S. Cantrell,

Sec-.>o

f, RRPI Division

SUMMARY

~

1

e

'Inspection on'anuary-31',

1'981

Date Signed

Z-3'-Z

Date Signed

ate

Signed

Areas Inspected

This routine inspection

involved

203 resident

inspector-hours

in the

areas

of

operational

safety,

reportable

occurrences,

maintenance,

fuel handling,

plant

physical,'adiation

protection,

reactor trips,

surveillance

testing,

emergency

procedures

and scram discharge

header monitoring.

Results

Of the

10 areas

inspected,

no violations or deviations

were found in

7 areas,

five violations were found in

3~ .areas;

(.Violation - Welding performed

on safety

related

equipment

and the welder's qualifications can't

be determined, paragraph

.5; Violation. -. Secondary

containment

not.. maintained,

paragraph

5;. Violation .-..

Radioac

ive contamina.ed,.ladder

found in

a. clean area,.'aragraph

6; Violation-

Personnel

working in

a high radiation

area without

a dose rate meter,

paragraph

6; Violation - Workers

not kept informed of the radiation levels in areas

they

Pp

I

0

I

E

DETAILS

Persons

Contacted

Licensee

Employees

H. L. Abercrombie,

Power Plant Superintendent

J.

L. Harness, Assistant

Power Plant Superintendent

(Maintenance)

J.

R. Bynum, Assistant

Power Plant Superintendent

(Operations)

J.

B. Studdard,

Operations Supervisor

R...Hunkapil lar, Assistant Operations. Supervisor

" ":"'A,"'L'.'-Burnett,':Assistant Op'era'ticins'Supervis'or'Outage)

~

'J.-A;-

Teague,'aintenance

Supervisor,

ETectr'ical'.

A. Haney, Maintenance

Supervisor,

Mechanical

J.

R. Pit man, Maintenance Supervisor,

Instruments

R. G. Metke, Results Section Supervisor

R. T. Smith, gA Supervisor

J.

E. Swindell, Outage Director

8. Howard, Plant Health Physicist

R. E. Jackson,

Chief, Public Safety

R. Cole,

gA Site Representative

Office of Power

R. E. Burns, Instrument Engineer

T. L. Chinn, Compliance Staff Supervisor

Other " licensee:

employees'. contacted'nc.luded

.licensed

senior

reactor

'operators

and

reactor

. operators,

auxiliary

operators,

craftsmen,

technicians,

public safety'fficers,- gA personnel

and engineering personnel..

2.

Management Interviews

,-.....-: Site management,interviews

weee, conducted. on.January

9, 16,.23

and .30,

1981,

'with 'the Pow'er'lant 'S'u'perintendent

and/or hi's Assi'stant'Superint'endents

and

'other selected

members of his staff.

The inspectors

summarized

the

scope

,, and,findings of their. inspection. activities..TNe

licensee

was informed of

'he five app'arent violations identified during this report

period.'.

Licensee Action on Previous Inspection Findings

(Closed)

Unresolved

Item (259/77-20-02)

References

in the

nondestructive

examination

procedures

on welds were outdated.

The procedures

were replaced

with new ones.

4.

Unresolved

Items

There were no new unresolved

items identified during the report period.

.'5'.

'pe'rational Safety.:

The inspectors

kept informed

on

a daily basis of the overall plant status

and. any

signi fi cant. safety .matters

rel a ted

to plant;. ooerati ons.

Daily.

.discussions

were held each morning with plant management

and various

members.

of the plant operating staff.'

0

The inspectors

made frequent visits to the control

room such that each

was

visited at least daily when

an inspector

was

on site.

Observations

included

instrument readings,'etpoints

and recordings;

status of operating

systems;

status

and

alignments

of emergency

standby

systems;

purpose

of temporary

tags

on equipment

controls

and

switches;

annunciator

alarms;

adherence

to

procedures;

adherence

to limiting conditions

for operations;

temporary

alterations

in effect; daily journals

and data

sheet entries;

and control

room manning.

This inspection

activity also

included

numerous

informal

discussions with operatoi s and their supervisors.

General..planttours,

were conducted

on at least

a weekly basis.

Portions of

the tu'rbi'ne'building; .each'eactor'ui

l'ding';and outside

areas'were

visited;

Observations

'included

valve" positi'ons

and

system

alignment;

snubber

and

'anger

conditions;

instrumen

readings;

housekeeping;

radiation

area

controls;

tag controls

on equipment;

work ac.ivities in progress; vital area

controls; personnel

badging,

personnel

search

and escort;

and vehicle search

and escort.

Informal discussions

were held with selec

ed plant personnel

in

their functional areas during these tours.

On January

8,

1981 at

1:20 p.m., while observing

the 'inspection

of the

control rod drive accumula or level switches

on Unit 3,

an inspector

noted

reactor

building eauipment air lock inside door open while .he outside

air lock door

was

open.

This resulted

in

a loss of secondary

containment

while primary containment

was not being maintained.

The loss of secondary

.-containment'was

due.to.personnel

not adhering to administration.instructi.ons

posted

by the doors which 'requires, that

a

second

person

be. posted

at

one

door to ensure it remains

shut while opening

the other door.

On this date,

no second

person

was posted at the door which was to remain shut.

When the

person

opened

the

outside air'ock door,

the positive

pressure

in the

,,, turbine,,bui1ding...blew ..open..the;:inside.,

door.

On. January.,9,

1981,

.an

inspector

observed that

an indiviBual'n'Unit'Z faiTed to follow the poste'd

administr'ative instructions but on this occasion

did not result in a loss of

secondary

contai'nment.

I

The violation of secondary

containment

while primary containment

was

not

maintained

was identified to

the

Plant

Superintendent

as

an

apparent

violation (296/81-03-01)

of technical specification 3.7.C. 1.

The

Plant

Superintendent

accepted

the apparent violation and stated that

he would take

disciplinary action

on these individuals who did not adhere

to the require-

ments for passage

through the reactor building equipment air lock doors.

On January

15, 1981, prior to startup of Unit 3 after

a refueling outage,

an

inspector

reviewed

work

plan

7779R1,

Enstallation

of

Hydrogen-Oxygen

Monitoring Panel.

At the

time

of. this review,

the

wor k plan

had not yet

been. reviewed

by. the ',plant. quality.,assurance

office..: The review by the

~

.

-.'nspector

indicated'th'at;a

minimum of 70'elds

an thi s safety-relat'ed

system

were made.

The welder

who made these

welds could not be identified in the

work plan. thus his qualifications to do the welding can not be determined.

.. The'icen'see:.i.ssued

.Corrective Action Reports

(CAR) 81-13 and, 81-15 in which

the failure to identify the. welder was addressed

as

a significant condition

adverse to quality;

The 'licensee also reviewed all the weld'od check out

'

7'

. ~

.I

0

3

h

forms to ensure that only qualified welders

checked

out weld rods for these

work plans.

No problems

were identified:as a result of these

reviews.

Oye

penetrant testing

and

hydrostatic testing

has been performed

on the welds.

The lack of documentation

to prove that qualified welders

performed

the

welding was'dentified

as

an

apparent

violation of

10 CFR 50 Appendix

8

Criterion IX and Topical Report

TVA - TR75-1, paragraph

17.2.9. to the plant

superintendent

on January

16, 1980. (296/81-03-05).

Health Physics

'

'-".Bur'ing 'the'"ihspe'cti'on."'p'e'riod

the"'inspectors

made "'frequent- inspections ot

-;:.;::. ""-

contami'nated 'storage

and work 'areas';. radiation

and high 'radiation areas

a'nd'

='bserved

work in areas

where

a special

work permit

(SWP) was necessary.

This

inspection

was conducted

to assure

that adherence

to the requirements

on the

SWP was being followed and to verifying that the

SWP

was properly filled

out.

On January

29,

1981,

the licensee

informed an inspector that a pile of scrap

which was being readied for transport

to TVA's local

dump, contained

a metal

ladder

which

had

been

cut

up into four pieces

and

was radioactively

contaminated

to levels of 150,000

dpm direct reading

and

2000

dpm smearable.

En addition,

the metal scaffolding in the bed of a truck being readied for

transport to the cooling water towers

had radioactive contamination

levels

...of. 800,dpm smearable.

,These

items, were. in a clean

zone

and were discovered

,during,.the.,required

radiation

survey, made. before

,the material. leaves

the

.

plant protected area.

The levels of contamination

on these

items are below the limits listed in 10

. CFR .20, however.plant. procedure .Radiological. Control Instruc .ion (RC1)-1,.

"-"requ'ir'es"th'at'TT i'tems'eavi'ng'

'i egulated'rea

to a"clean"'zone

"sha'1T

be

surveyed

by the plant health physics

personnel

and shall not be released

to

'a

clean

zone if the

item

has

greater

than

.200

dpm contamination.

On

January

30,- 1981,

inspector'nformed

the

Plant

Superintendent

that'his

incident was

an apparent violation of technical specification 6.3.A.7 which

requires that radiation control procedures

shall

be adhered to.

The Plant

Superintendent

stated

that

this

incident

would

be

discussed

with all

personnel

in the

outage

organization

by February

4,

1981.

(259/81-03-01,

260/81-03"01, 296/81"03-02).

On January

14,

1981, while observing

the installation of the scram discharge

header,transducers

for monitoring water level

on unit

3 east

header,

an

inspector

observed

three

TVA personnel

and one

GE representative

working in

a high radiation area without a dose rate meter.

The inspector

determined

tilat;the.'special;workpermit

(SMP) required" that

a dose. rate, meter

be used

..

because

the general: area survey,'ndicated'adi:ation

level. of 300 mr/hr.

A .

radiation

survey of the area

where the personnel

were working was determined

to be

100 to 500 mr/hr.

The inspector

informed TVA's instrument

engineer

who.was.at-the:job.site

of..the, requirements-

on the.SWP:

The, engineer

had

~

~

8

4

the

personnel

in the high radiation area

leave the area until

a dose rate

meter

could

be obtained.

The engineer

stated

he

was

aware

of the

the

requirements,

and

had used

a dose rate meter at

a previous job site but had

forgotten to have the dose rate meter at this job site.

Radiological Control Instruction (RCI) - 10 requires that for any work in a

high radiation

area (greater

than

100 mr/hr),

a dose rate meter will be with

the individual or group of individuals who enter

the area.

The Plant Super-

intendent

was

informed

on January

16,

1981, that failure to follow the

requirements

of the

SWP and RCI-10 was

an apparent

violation of Technical Specification 6.3.A.0.7 which requires that radiation control procedures

be

~ .'- "--adhered:to:'(296/81-03'-'03).'-

':.

-., - - *;

-".'

': .

" '

~

While making

a tour of unit

3 reactor building

on January

15,

1981,

the

inspectors

observed

carpenters

on the west

scram discharge

header

(SOH)

north

end

removing scaffolding.

The inspector

questioned

the

foreman

in

charge

of the job as

to the requirements

of his

SWP

since

the

area

the

workers were in was posted

as

a high radiation area

and

no dose rate meter

was

observed

in the

area.

The

foreman

stated

that

the

health

physics

technician did not require

a dose rate meter

nor did the

SWP which

he

was

told to use.

The inspector

reviewed the

SWP No. 01-3-37187

and found that

it had

been

issued

for general

work and cleanup.

The general

area

was

t

documented

at

40 mr/hr and that

no rate

meter

was required.

The health

physics technician

who authorized

the

use of that

SWP by the workers stated

that tpe. job was .only 5 or, 10 minutes. long,

so

he cautioned

the workers. to,

. stay clear. of the,SDH pipin'g,and that

he also

was "keeping

an eye"

on them.

The

general

area

where

the

workers

were

removing

the

scaffolding

was

surveyed

by plant health physics

personnel

and found to vary from 60 mr/hr

to

150 mr/hr.

The inspector

noted also that the health physics technician

was approximately

200 feet from the work area

and his view of this area

was

'

obstructed

by equi'pment.'The'- two"worker'nthis area received'an

exposure,'s'registered

by their dosimeters of 7mrem and

10 mrem.

The Plant. Super intendent

was

informed

by the

inspector

that failure to

inform workers of the radiation

levels

in which they were working was

an

apparent violation of 10 CFR 19. 12 which requires that workers

to

be kept

informed of radiation

in portions of restricted

area

in which they are in

(296/81-03-04)

.

Reactor Trips

The inspectors

reviewed activities associated

with the below listed reactor

trips during this report

period.

. The

review included

determination

of

cause,

safety

significance,

performance

of personnel

and

systems,

and

corrective action.

The inspectors.examined

instrument recordings,

computer

.:pr'intouts, opera ion..journal en'ies,

scram. reports. arid had discussions

with

operations,

maintenance

and engineering

support personnel

as appropriate.

0

5

On January

3,

1981,

Unit 2 tripped at 11:24 a.m.

from 100.o power due to

a

turbine trip caused

by failure of the generator

bus tie breaker.

Four

main

steam relief valves actuated

to relieve reactor high pressure.

No emergency

core cooling was initiated.

Systems

performed

as designed.

Inspector Followup Items

The inspectors

followed up on the Confirmation of Action letter

issued

on

November

10,

1980,

as

a result of the Health Physics Appraisal

inspection

performed

on

October 20-31,

1980.

The

Confirmation

of Action letter

addressed

four

items

in

which

.TVA was

to

take

action

to alleviate

defici'encies:"'i:n'- the.'-'p'ersonnel'.."contamination"

monitoring

program.'-'-- The '.

'*

~ '

.

" inspectors"rev'iewed'ach

-area:-to

ensure:that" the proper action

had

been'aken.

a.

Plant

instructions

were

revised

on

November 7,

1980,

to

require

individuals exiting

a contamination

zone to have

a whole body contami-

nation survey performed prior to donning personal clothing.

b.

On November

5, 1980, the Plant Superintendent

informed all employees

by

memorandum

tha

they must

use the hand

and foot monitors

when exiting

regulated areas.

c.

TVA has

increased

the

frequency

of functional

checks

on

personnel

,friskers to,.three. times..per. week.

P

'I ~ S

d.

equality

Assurance

has

performed

and is performing

surveillance

of

personnel

contamination monitoring to evaluate the effectiveness

of the

actions taken.

" No v'iolation"or'eviations wer'e ide'ntffied

within

'the areas

inspected.

9.

Reportable Occurrances

The below listed licensee

event reports

(LER's) were reviewed to determine

if the information provided

met

NRC reporting

requirements.

The determi-

nation included adequacy of event description

and corrective action taken or

planned,

existance

of potential

generic

problems

and

the relative

safety

significance of each event.

Additional inplant reviewed and discussion with

plant personnel

as appropriate were conducted for those reports

indicated

by

an asterisk.

LER No.

"259-8025

"259-.8057.

259-8073

259 8074

t

~'259.-8079

Gate

4/11/80

8/80/80 .::....

10/9i80

10/23/80

11/21/80-.'vent

.

RHR injection valve failed to close

.Technical Specification 4.6.G.6 testing not..

performed..

River delta T exceeded 5'.

Seismic monitor inoperable.

Electric'al ground in HPCI oumo

'-6

11/12/80

12/30/80

12/31/80

1/8/81

FSV-84-19 solenoid coil not environmental ly

qualified.

POIS-75-28 was found at outside technical

specification limits.

1C diesel generator tie br eaker tripped

Reactor water level switch was found set out

of technical specification limits.

Continuous air monitor was inoperable.

Drywell hydrogen monitor was inoperable.

"259-8081

259-8087

-'259-8088

259-8089

"259-8090

259-8091

1/8/81

1/15/81

4/8/80

"260"8016

, "260-8037

"260"8040 '." ""'IO/14'/80

10/21/80

10/27/80

11/6/80

Loaded fuel with control rod withdrawn

MSIV's exceeded

allowable leakage rate

"260"8041

260-8042

"260-8043

260-8044

Scram accumulator level switches inooerable

Refueling zone inboard isolation time delay

relay was out of tolerance.

Instrument line was missing internals for

excess

flow check valve.

Inadequate dilution of water to environment

Drywell pressure

transmitter not qualified

Leak rate testing exceeded

technical

specification

Intermedi.ate:-range

monitors did not respond

during initial startup..

11/10/80

11/24/80

"260-8046

  • 260"8047

260-8048

260-8049

"260-8050

1)/20/80

11/28/80

12/3/80

-12/-IZ/80

12/12/80

260-8051

Level switch did not operate within technical

specification limit

3 gallon SOIV level switch did not operate

..,Leak-,in.ZC.RHR heat. exchanger

'Main 'st'earn'relief,valves

did 'not'i'ft within

IX of set pressure.

CS discharge

pressure

switch was found set

outside technical specification limits.

Reactor water level switch was found set out

side technical specification limits.

MS line low pressure

switches were found set

outside technical specification limit.

SOIV level switches,

25 gallon inoperable

SOIV level switch was inoperable

Cooling water flow to 30 diesel

was

inadequate

Turbine first stage pressure

switch setpoint

drifted

.'

"-3A diesel generator would not trip .

~'B diesel generator

lube oil circulating jump

inoperable

Orywell high pressure

setpoint drifted

Flow-bias circuitry for APRM's was inoperable

3-PS-1-76 setpoint drifted

260-8052

12/12/80

,,260-8053.

- ,, 1/2/81 -:.,

"260-8054'

'

.12/10/81

I/6/81

1/6/81

1/13/81

260-8055

260"8056

260-8057

260-8058

260-8101

"296-8016

1/19/81

1/15/81

6/11/80

9/5/80

296-8030

"296"8036 ;;,'

'9/29/80

"296-.8040,

'

1/7/80

11/14/80

11/17/80

, 12/1/80

296-8042

~296-8043

296-8045

MS line sensing

1 ine blocked

9/26/80, Fuel. assemblies

mi sorientated

" ma'in'team'rel i'ef valves* fail'ed 'to actuate

within '1%. '-'. "

It

4 '

I

'I t

7;.

296-8046

11/28/80

  • 296-8047

12/1/80

296-8048

12/5/80

"296-8049

296-8050

296-8051

296-8052

"296-8054

12/11/80

'2/11/80

12/15/80

12/15/80

1/8/81

'"296-'8055. -'"""I/8%81'".':

'-'296"8057'

" .

1/1G/81'96-80581/6/81

SLC pump inoperable

3B&D core spray

room cooler had inadequate

cool ing flow.

EECW to 3B RHR seal

heat exchanger

had

inadequate

flow.

3D RHR pump tripped

3B SLC pump breaker tripped

Orywell H2 sensor would not calibrate

3-PS-68-95 setpoint drifted

8 MSRV's failed to actuate within 1:o of

setpoint.

CAM-3"RM'-90-:250'as'noperable

CAM-3-'RM-90-.251'as inoperable

'SIV's

exceeded

leakage criteria

Within the areas

inspected

no violations or deviations were identified.

10.

Scram Discharge

Header Monitoring

Efforts

to

make

the

G.E.

supplied

continuous

monitoring

system

(CMS)

operational

continued into January with G.E. engineers

on site.

Testing of

the

new

system

was

performed

on unit

3 which was

in cold

shutdown for

refueling.

The original monitoring system which required

30 minute

checks

of the local

sensor

recording strip charts

were maintained

in service for

aperating

uni.ts. 1.and.2,

When. unit. 3..resumed .,operati.on,

the. old. system

was

pl.aced in. sery.ice.

As

a result of the

on site effort,

an

improvement in sensor

response

was

attained by optimizing transducer

locations

The vendor further decided that

changes

..to. the circuit design. were desirable..

The, vendor.

committed to TVA

.

"

. tiiat thpdate'd

drawings"and'pa'res "required"for'he modified'yste~ would

'e

provided by January

30, 1981.

TVA notified the

NRC by l'etter to the Director, Region II, dated January

20,

1981, that problems were encountered

and the revised

schedule for having the

CMS operable.

The schedule

showed that the

system would be operable

on unit

3 within three

days of receipt of material

from the vendor.

Modifications

to units

1

and

2 would then

be completed

in another

week.

Region II found

the'revised

schedule

accepta'ble.

Aside

from

the

vendors

efforts,

TVA pursued

another

approach

toward

providing

a monitoring system with alarms

in the control room.

TVA utilized

'the

same

type

UT monitor

used

in 'the'reviously

installed

system

in

combination with the .vendor

supplied

transducer

and equipment to transmit

~

.and annunciate'information.in

the: control. room..'he. control

room operator

was. pr'ovided: with .an

alarm 'for'.high'ater

level

and another for loss of

'ocal

power

to the

UT monitor.

By the

end of the

month

TVA had design

approval of their system

and

had installed

and tested

the system

on unit 3.

,Plant

Operations

Review

Committee..'s..approval.

of the test results

and the

procedures

is needed to declare the system operable.

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No violations or deviations

were ident,ified during the review of the above

activities.

Scram Accumulator Level Switches

'n

November

6,

1'980,

TVA reported

to the

NRC that

17

accumulator

level

switches

out of

185 would not operate

on unit

2

and

the

same

number

was

reported

on January

27, 1981, for unit 3.

These

switches

sense

leakage

from

the water

side of the

scram accumulator

to the nitrogen side

and cause

an

alarm to actuate

in the control

room and locally when leakage

is detected.

investigation. by

TVA into. the large failure rate

revealed

no conclusive

"evidence'to"'supp'or't

-why.".'the'"twit'ches'fa'i'led'..".Ihspectio'n

of'ome 'of the ".=

" 'ailedev'el'witches," showed'hatsome

had

an adhesive

type'ubstance

on

the

spring which could

have

prevented

the

switch

from opera.ing;

but it

could

not

be

concluded

that . this

caused

all

34 failures.

Where this

adhesive

substance

came

from could not be determined

other

than

to

assume

from either the lubricant

on the accumulator

"0"ring which separates

the

water

from nitrogen

or

from the lubricant

used

on

the

threads

of the

switches.

The possible

cause

for the large

number of failures

also being

considered

is

an

inadequate

test

procedure.

Electrical

Maintenance

Instruction (EMI)-50 which tests

the level switches did not require venting

the test

pump prior to hookup.

This could allow for the introduction of air

into the level switch housing which would not allow the switch to function

properly.

TVA is continuing their investigation

by revising

EMI-50 to

ensure

the, test, pump is. vented prior-.to, hookup. to .the

scram accumulator:.and..

by,testing, the .accumul:ator

leve)

switches

on .unit

1

as conditions

permit

under

the revised

EMI to

see if the venting of the test

pump

solved the

problem.

., Within.the areas,.(nspected.no..items

of nopcomp1..iance

.were identified.

12.

Plant Physical

Protection'uring

the 'course

of routine inspection activities,

the

inspectors

made

observations

of certain

plant

physical. protection

activities.

These

included personnel

badging,

personnel

search

and escort,

vehicle

search

and

escort,

communications

and vital area access control.

Turnstiles,

one

on either

side of the enclosed

guard station at the west

gatehouse,

were installed

and placed in service

on January

12,

1981.

This

addition provides improved control for access

to the protected area.

No violations or deviations were identified within the areas

inspected:

.'. -'3...-.. Maintenance

~

I

The inspector

made direct observation

of the installation of a replacement

water accumulator for rod drive 34-27, unit 2,

on January

8,

1981.

The rod

was declared

inoperahle

as'. required. by: Technical. Specifications.

Within the areas

inspected 'no.violation. or deviati'ons were identified.

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14.

Surveillance Testing

The inspector

observed

the conduct of surveillance testing for the Standby

Liquid Control System, Surveillance Instruction (SI) 4.4.A. 1,

on January

19,

1981,

on unit 3.

The completion of the surveillance satisfied

the require-

ment for monthly loop functional testing.

On January

14,

1981,

an

inspector

observed

the

conduct

of surveillance

testing

on

the

reactor

high

pressure

scram

switches,

Surveillance

Instruction (Sl) 4. 1.A.S.

The surveillance

test

was performed in accordance

with the instruction...All

gauges

and

meters. were in calibration, all the

"'Tat'est: revi'si'ons'-were 'entered'n

'the

instruc'ti'on - and" the 'instrume'nt

technician.'ere

"knowledgeable" of the

procedure

and

the 'effects

this

surveillance

had on the plant.

No violations. or deviations were identified within the areas

inspected.

15.

Special

Test

The inspector

on January '2,

1981 observed

the performance of Special

Test

168,

Inspection

for Missing

Tags,

in the unit

1

fuel

pool.

The test

required the movement of fuel bundles,

dechanneling

of fuel assemblies,

and

the

search

of fuel

racks

to locate

missing. identification tags

which had

fallen into the fuel pool in May 1979.

Within the. areas

inspected,.ne violations or deviations were.identi.fied.

16.

Emergency Procedures

on Antisipated Transient Without Scram

(ATWS)

. A review was made of. pl.ant,,operati.ng.,and.emergency

procedures,

to. verify that

condi t'ions of concern relating. t'o"a'n

ATWS event were adequately" addressed

in'he

procedures.

The'eview

included

a

range

of potential

control

rod

problems

from single

rod malfunction to all rods fai ling to scram.

Also

included'i.n the r'eview was, failure of a scram to be initiated when required

and the initiation of the

standby liquid control

system

when

needed.

A

total of five procedures

were reviewed.

The inspector determined that the

conditions of interest

were addressed

in the procedures;

however,

some minor

changes

appeared

advisable

to more clearly define desired operator

action.

The licensee

implemented these procedure

changes

on January

27, 1981.

No violations or deviations were identified within the areas

inspected.

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