05000296/LER-1979-006-03, During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated

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During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated
ML18024B089
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 11/07/1979
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18024B090 List:
References
LER-79-006-03L, LER-79-6-3L, NUDOCS 7911140353
Download: ML18024B089 (4)


LER-1979-006, During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated
Event date:
Report date:
2961979006R03 - NRC Website

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" Tennessee Valley Authority Brown.; Ferry Nuclear Plant II Form BF-17 Bs'5.2 1/10/79 I.ER SUPPLEMENTAL INFORMATION BFI40-50 296 /

796 Technical Specification Involved 3.7.H.

iteportad Under Tcchnical Specifiration 6~7.2.b(2 Dat,e of Occur) <<nc>>

5/7/79 Time of Occurrence 1100 Unit 3

7 Identification and l)esci iption of Occui'rene>>:

Operations personnel observed erratic indications on the torus hydrogen sensor H2M-76-38.

The system was declared inoperable.

Conditions Prior to Occurrence:

Normal operation.

Action specified in the Technical Specification Surveillance Requirements met duo I.

tao~arable a

~ui ment.

Describe.'

30-day operating limit was established in accordance with T.S. 3.7.H.4.

A~)arent Cause of Occurrence:

Defective hydrogen sensor.

~Anal sis of Occurrence:

None

Corrective Action

Replaced hydrogen sensor.

Design change request.

1194 will replace the General Electric hydrogen monitoring system with a system whose sensors are external to the primary containment.

Primary containment modification is being completed on unit 3 during the present refueling outage.

F:iiluvu D'tta:

259/7815 and 259/7820

~Ret'ntion:

eriod - Lifetime; Responsibility - Administrative Superv'isor

~:Revision:

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