ML18012A457

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Insp Rept 50-400/96-10 on 961013-1123.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering, Plant Support & Plant Status
ML18012A457
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 12/20/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18012A455 List:
References
50-400-96-10, NUDOCS 9701150050
Download: ML18012A457 (19)


See also: IR 05000400/1996010

Text

U. S.

NUCLEAR REGULATORY COHHISSION

REGION II

Docket No:

License

No:

50-400

NPF ~ 63

Report

No:

50-400/96-10

Licensee:

Carolina

Power

& Light (CP&L)

Facility:

.Shearon Harris Nuclear

Power Plant, Unit 1

Location:

5413 Shearon Harris Road

New Hill, NC 27562

Dates:

October

13

-

November

23,

1996

Inspectors:

J.

Brady, Senior Resident

Inspector

DE Roberts,

Resident

Inspector

G. HacDonald,

Project Engineer

Approved by:

N. Shymlock, Chief, Projects

Branch 4

Division of Reactor Projects

970l150050

961220

PDR

ADOCK 05000400

8

PDR

EXECUTIVE SUMMARY

Shearon Harris Nuclear

Power Plant, Unit 1

NRC Inspection Report 50-400/96-10

This integrated

inspection included aspects of licensee operations,

engineering,

maintenance,

and plant support.

The report covers

a six-week

period of resident inspection:

in addition, it includes the results of an

announced

inspection

by a regional project engineer.

O~erations

~

The conduct of operations

during the period was adequate.

(Section 01.1)

The negative trend in operator

performance

continued into this report

period with two minor errors being identified by the licensee.

(Section 04.1)

~

The System Description for the Chemical

5 Volume Control

System did not

describe the emergency boration function. (Section 02.1)

~

Self-assessment

activities were good (Section 07.1)

Maintenance

~

Maintenance

personnel

were following procedures

during maintenance

activities

and modification installation activities.

An incorrect

maintenance

procedure

had personnel

bypass

a start permissive interlock

for the running ."A" Normal Service Water

(NSW)

pump rather than the

intended

"B" NSW pump during an uncoupled motor run. (Section H1.4)

~

Surveillance

performances

were being adequately

conducted.

(Section

M2.1)

En ineerin

Engineering support for operation of the plant was good (Section E2.1)

Two violations were identified which related to the determination of a

new main reservoir water level design basis.

One related to the use of

an administrative limit to administer

the

new main reservoir level limit

without promptly submitting

a license

amendment

request to change the

Technica'I Specification value.

The other involved not providing the new

design basis

when Final Safety Analysis Report

(FSAR) Amendment 46 was

submitted.

(Section E8.1)

Plant

Su

ort

The general

control of contamination

and dose for the site was good.

The performance of a Reactor Coolant System

sample using the Post

Accident Sampling System

was good.

(Section Rl.l)

Management

commitment to the performance of the emergency

response

function was good.

(Section Pl.l)

~

The security and safeguards

activities were we1] performed.

(Section

S1.1)

Fire Protection activities were acceptable

(Section Fl.l)

Re rt Details

Summar

of Plant Status

Unit 1 maintained 100'ercent

power during this entire inspection period.

01

01.1

Conduct of Operations

General

Comments

71707

~l. 0

02

02.1

04.1

Using Inspection Procedure 71707,

the inspectors

conducted frequent

reviews of ongoing plant operations.

In general,

the conduct of

operations

was professional

and safety-conscious;

specific events

and

noteworthy observations

are detailed in the sections

below.

Operational

Status of Facilities and Equipment

En ineered Safet

Feature

S stem Walkdowns

71707

The inspectors

used Inspection

Procedure

71707 to walk down accessible

portions of the following Engineered

Safety Features

(ESF) systems:

~

High Head Safety Injection

(FSAR Section 6.3.2)

~

Chemical

8 Volume Control System

(FSAR Section 9.3.4)

Equipment operability, material condition,

and housekeeping

were

acceptable

in all cases.

The inspector

observed that the system

description for the Chemical

and Volume Control System,

SD-107.

Revision 5, did not describe the emergency boration function of the

system.

That function was described in FSAR section 9.3.4,

and in

rocedure

AOP-002,

Emergency Boration, Revision 10, which is referenced

y several

Emergency Operating Procedures.

The licensee

was taking

action to add

a description of this feature to the system description.

Operator Knowledge and Performance

General

Comments

71707

Inspection Reports 50-400/96-07

and 96-09 documented

a negative trend in

human performance

associated

with the operation of plant equipment.

During the routine review of condition reports,

the inspectors

noted

that several

operator

performance

issues

were documented indicating a

continuance of the negative trend.

One involved an inadvertent control

switch manipulation in actuating the emergency

load sequencer test

switch instead of the lamp test switch

(CR 96-03278)

and another

involved the momentary deadheading of the boric acid transfer

pump

(CR

96-03327).

In these

two situations the errors were immediately detected

by the operators

and corrected without any safety consequences.

07

07.1

08.1

Quality Assurance in Operations

Licensee

Self-Assessment

Activities

40500

Ouring the inspection period, the inspectors

reviewed multiple licensee

self-assessment

activities, including:

Plant Nuclear Safety Committee

(PNSC) meetings

on October

28,

1996

and November 22,

1996;

Nuclear Assessment

Section Audits on Harris Nuclear Plant

(HNP)

and Corporate

Nuclear

Fuels

Program

(HNAS96-213)

and on Cold

Weather Preparations

(HNAS96-224);

Condition reports.

Self-assessment

activities were good during the assessment

period.

The

inspectors

noted that the Nuclear Assessment

Section

(NAS) has reviewed

the line organization self-assessments

as part of their audits.

NAS

used the number of condition reports that the line organization

has

issued

as

an initial indicator of the quality of'he self-assessments.

This has instilled in the line organization that the writing of

condition reports is good.

Hiscellaneous

Operations

Issues

(92700,

90712)

Cl'osed

LER 50-400/95-012-00:

Containment Pre-entry Purge Valve

drifted open during Node

1 power operation.

This item was reported

due to Containment Pre-entry

Purge Valve 1CP-1

drifting open on November 10,

1995.

This was reported

as

a violation of

Technical Specification (TS) 3.6.1.7

and 3.3.2.

The method for ensuring

this valve and 1CP-7 were sealed

shut was found to be deficient.

The

air isolation valves were locked shut to prevent air from opening the

valves.

In this case the air isolation valve for

1CP-1 leaked by during

performance of a Containment Pre-Entry Purge

Fan start causing the valve

to drift open.

The Pre-Entry Purge

Fan start generates

an open signal

which pressur izes the line to the 1CP-1 air isolation valve.

That

occurred at 12:10 p.m.

on November 10,

1995.

The valve was discovered

to have drifted open at 6:00 p.m. the

same day.

The operators

took

immediate action to close

1CP-1 when they noticed intermediate

indication.

Further corrective action was to open

a vent down stream of

the air isolation valve to ensure that pressure

cannot buildup and open

1CS-1.

TS 3.6

~ 1.7 states that with a containment pre-entry purge makeup and/or

exhaust isolation valve open or not sealed

closed,

close and/or seal

closed that valve or isolate the penetration(s)

within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />,

otherwise

be in at least

Hot Standby in the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

and in cold

shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

The licensee

speculated that

the valve opened

no earlier than 12:10 p.m..

and that at 4:10 p.m. the

valve should have been shut to comply with the action statement.

The

inspector

was unable to independently verify at what time 1CP-1

came off

its closed seat.

The inspector

concluded that the licensee's

operability and reportability determinations

were appropriately

conservative

and followed the guidance in Generic Letter 91-18.

The inspector 's rev'iew of licensee

records

support the licensee's

conclusion that the root cause

was that opening air pressure

leaked by

1CP-1 isolation valve.

The licensee's

long term corrective action was

to revise procedures

to ensure the instrument air lines were

disconnected

between the air isolation valve and the valve actuators for

1CP-1

and 1CP-7.

The inspector verified that procedures

OP-16S,

Containment Ventilation and Vacuum Relief, Revision 9, OST-1029,

Containment Penetration

Outside Isolation Valve Verification, Revision

7,

and OST-1055,

Containment Pre-Entry Purge

and Exhaust Valve Inser vice

Inspection,

Revision

6 included provision to disconnect

(or verify

disconnected)

the air lines to 1CP-1

and 1CP-7.

The inspector also

field verified that the air lines were disconnected.

This

LER is

closed.

II. Maintenance

Conduct of Maintenance

General

Comments

Ins ection

Sco

e

62707

The inspectors

observed all or portions of the following work

activities:

~

WR/JO 96-AHHI2, Repair/Replace

1CH-323

TCV for AH-15A

~

WR/JO 96-AMOS 002, Inspect

"A" CSIP Oil Cooler

~

WR/JO 96-ACWJl, Fabricate

and Install Emergency Diesel Generator

(EDG) Shaft Encoder

on

EDG A.

Observations

and Findin s

The inspectors

found the work performed under these activities to be

professional

and thorough.

All work observed

was performed with the

work package

present

and in active use.

Technicians

were experienced

and knowledgeable of their assigned

tasks.

Measurement

and test

equipment

was in calibration.

The inspectors

frequently observed

supervisors

and system engineers

monitoring job progress,

and quality

control personnel

were present

whenever required by procedure.

When

applicable,

appropriate radiation control measures

were in place.

Modification Engineering Service Request

96-00114

was performed by

maintenance

personnel

with oversight by the system engineer.

The

modification was implemented

by maintenance

work package

WR/JO 96-ACWJl.

The work activity was well managed to minimize the Limiting Condition

for Operation

(LCO) time.

Post installation checks were performed with

the

EDG operating to verify proper alignment,

ensure

no leakage,

and to

verify that the transmitter provided output signals.

Post installation

checks were satisfactory.

8

NSW Pum

Re air

Ins ection Sco

e

62707

The inspectors

observed portions of the following work activity:

~ 'R/JO 96-AHYFl,

8 Normal Service Water

(NSW)

Pump Repair

Observations

and Findin s

The inspectors

observed the installation of the repaired

8

NSW pump.

The work was performed in accordance

with-work documents actively in

use.

Haintenance

personnel

were knowledgeable of their assigned

tasks.

The system engineer

. supervisors,

and Quality Control

(QC) personnel

were noted to be monitoring'he job.

The installation of the

pump was

acceptable

and the work performed was professional.

Following the installation of the 8

NSW pump and motor,

an uncoupled

motor run was scheduled

as part of post maintenance testing to verify

proper operation.

The test

was conducted

per procedure

ORT-1413,

Revision 3,

Normal Service Water

Pump Uncoupled Hotor Operation.

The

motor failed to start

and the motor breaker did not close.

The licensee

wrote condition report

(CR) 96-003353

and initiated an investigation of

the failure.

Uncoupled motor operation required bypassing start permissive interlocks

by the use of electrical

jumper wires.

The licensee

determined that the

start failure was due to an incorrect jumper placement.

Operators

installed the jumpers in accordance

with procedure

ORT-1413.

However,

the procedure

was incorrect and resulted in the technicians

bypassing

the start permissive interlock for the running A NSW pump rather than

the 8

NSW pump as required.

The inspector

reviewed the procedure

and plant drawings

and confirmed

that the procedure

was incorrect.

The jumpers were correctly installed

in panel

ARP-11 in the relay room and from observation of the jumper

terminals the inspector determined that the incorrect jumper placement

was not caused

by an operator

error or a lack of attention to detail but

due to an incor rect procedure.

If the jumper had been in a trip circuit

rather than

a star t permissive circuit,

a 'ioss of normal service water

would have resulted which would have challenged operators

and could have

caused

a plant transient.

Installation of Kirk Ke

Interlock Hodification

Ins ection Sco

e

The inspectors

observed portions of the following work activities:

WR/JO 96-AFNUP1

Install Kirk Key Interlock For Charging/Safety

Injection Pump

(CSIP)

1A Breaker

WR/JO 96-AFNUQl

WR/JO 96-AFNU1

WR/JO 96-AFNUT1

Instal.l Kirk Key Interlock For CSIP

1C Breaker

Install Kirk Key Inter lock For

Component Cooling

Water

(CCW)

Pump

1C Breaker

Install Kirk Key Interlock For

CCW Pump

1A

Breaker

Observations

and Findin s

The inspectors

observed the implementation of modification ESR No. 96-

00422,

Revision 0, regarding the installation of kirk key interlocks for

the Charging/Safety Injection Pump (CSIP)

and the Component Cooling

Water

(CCW) pumps.

The objective of the modification was to prevent

loading either two CSIP or two CCW pumps onto

a safety related

electrical

bus at the

same time.

This modification implemented

corrective action for NRC Yiolation 50-400/96-06-01.

The modification was installed by maintenance

personnel

working

individual work requests

for each breaker.

The inspectors

observed the

interlocks being installed on the 1A-SA bus,

breaker

compartments 3,5,7

and 8.

The modification consisted of installing capture

key deadbolt

lock sets to control the position of the breakers in the compartments

with two locks and one key per interlocked breaker pair.

The Kirk Key

inter lock deadbolt.

when extended.

functioned to prevent a'reaker

from

being racked into the connect position by blocking the breaker shutter

guide on the right side of the breaker which prohibited further travel.

This would permit only one breaker to be racked into the connected

position at

a time.

The inspector observed that work was performed in

accordance

with the modification package

and the individual work

documents.

QC personnel

were available

whenever

required by the work

documents.

Engineering personnel

were coordinating the installation of

the modification.

All personnel

were knowledgeable

regarding the

modification workscope

and installation requirements.

Work was

professional

and thorough.

The

LCO time was not exceeded.

Good

coordination

was noted between engineering,

maintenance,

QC and

operations

personnel.

The inspector

observed the performance of the post installation testing

of the modification.

The testing met the acceptance criteria; however,

the inspector

identified that the interlock for the swing

1C

CCW breaker

compartment

was not tested with the

1C

CCW pump breaker.

An alternate

breaker

was used to test the interlock.

The

1C

CCW breaker

was

installed in the 1B-SB switchgear

which is located in an adjacent

switchgear

room.

The door between the switchgear

rooms is equipped with

a removable curb.

Rather than disassemble

and remove the curb to allow

the

1C

CCW breaker to be rolled into the

1A switchgear

room to test the

interlock, licensee engineering

personnel

made

a conscious decision to

utilize another breaker.

This necessitated

the removal of the

compartment

1 bracket to allow an alter nate breaker into the

1C

CCW

breaker

compartment.

The inspector

questioned

the licensee to determine if they had verified

that the swing

1C

GCW breaker

shutter bracket dimensions

were the

same

as the breaker

used to test the inter lock.

The licensee

had not

verified the shutter bracket dimensions.

The swing

1C

CCW breaker

compartment

was opened

and the dimensions

were verified to be acceptable

for interlock function.

The inspector

determined that the post

installation testing verified the objective of the modification.

However, the dimensions of the swing

1C

CCW pump breaker

were not

verified 'prior to 'testing the

1C

CCW pump breaker

compartment interlock

with an alternate

breaker until questioned

by the inspector.

Conclusions

on Conduct of Haintenance

Haintenance

personnel

were following procedures

during maintenance

activities and'modification installation activities.

The test procedure

for the nonsafety-related

NSW pump motor

was inadequate

which extended

the time that the plant was operated

in reduced

equipment status.

r

Hodification installation and post installation testing

was acceptable

for the

EDG shaft encoder modification and the switchgear kirk key

interlock modification.

The dimensions of the swing

1C

CCW pump breaker

were not verified prior to testing the

1C

CCW pump breaker

compartment

inter lock with an alternate

breaker until questioned

by the inspector.

Haintenance

and Hater ial Condition of Facilities and Equipment

Surveillance Observation

Ins ection Sco

e

61726

The inspectors

observed all or portions of the following surveillance

tests:

~

EPT-250,

A Train

ESW Flow Verification/Balance,

Revision 3.

~

OST-1013,

1A-SA Emergency Diesel Generator Operability Test.

Honthly Interval

Hodes 1-2-3-4-5-6,

Revision 9/l.

Observations

and Findin s

The inspector

found that the testing

was adequately

performed.

The

Emergency Service Water

(ESW) flow to containment

fan cooler

AH-2 did

not meet acceptance criteria.

CR 96-03304

was written for the adverse

condition.

The inspector discussed

the issue with engineering

and

operations

personnel

and determined that there was still margin between

the measured

value and the flow used in the safety analysis/FSAR.

The

licensee

had already identified long term corrective action for the

upcoming refueling outage to address

containment

fan cooler

ESW flow.

C.

H8

M8.1

H8.2

The corrective actions included containment

fan cooler

ESW orifice

modifications and

ESW pump modifications.

Conclusions

The surveillance

performances

were adequately

conducted.

Hiscellaneous

Haintenance

Issues

(92700)

Closed

LER 50-400/95-14-00:

Residual

Keat Removal

(RKR) System

components

removed from service for testing while required for

operability resulting in Technical Specification violation.

This

LER was issued to report

a condition that occurred in 1994, but was

not determined to be reportable until December

14,

1995 as

a violation

of Technical Specifications.

Inservice Inspection testing of RKR check

valves

was held up during refueling outage

6 due to the good questioning

attitude of several

licensee

personnel

pertaining to performance of a

ortion of this test with the plant in mode 6 and refueling cavity level

ess than 23 feet.

The procedure

(OST-1508,

Revision 2) did not specify

that refueling cavity level

needed to be above

23 feet for this test to

be performed in,mode 6.

Condition Report 95-2468 was issued to identify

this problem.

The licensee

reviewed previous occurrences

of the

rocedure to determine if they had occurred with refueling cavity level

elow 23 feet in mode 6.

The 1994 occurrence

was discovered

and

reported.

Procedure

OST-1508,

ISI Operability Test for 1CS-167,

1CS-

294,

1CS-775,

1CS-776.

was revised to add the 23 feet as

a prerequisite

for mode 6.

The inspector verified that it was added to Revision 3

which was the current revision.

The licensee identified potential

programmatic surveillance

procedure

problems in LER 50-400/95-07

and as corrective action committed to a

comprehensive

surveillance

procedure

review program which was still

ongoing.

That review also addressed

Generic Letter 96-01, Testing of

Safety-Related

Logic Circuits.

Collectively, in the past two years the

licensee

has reported over 40 items related to surveillance

procedure

problems.

Consequently,

the generic aspects

of surveillance

procedure

program deficiencies will be reviewed during closure of LER 50-400/95-

07.

This item is closed.

Closed

LER 50-400/94-001-00:

Technical Specification surveillance

violation due to inadequate

procedure.

This event report was issued to

report that the slave relay test for relay K623 did not verify actuation

of the reactor coolant drain tank pump discharge

valve (lED-121).

The

specific corrective actions were reviewed

as documented in IR 50-400/96-

07 and found acceptable.

In that report the inspector discussed

the

comprehensive

surveillance procedure

review program that was committed

to in LER 95-07 which was still ongoing.

As discussed

above,

the

generic aspects of surveillance

procedure

program deficiencies will be

reviewed during closure of LER 50-400/95-07.

This item is closed.

III. En ineerin

E2.1

E7

E7.1

E8

E8.1

Engineering Support of Facilities and Equipment

General

Comments

37551

Engineering support for the operation of the plant was observed to be

good during the inspection period.

Operations

personnel

informed and

routinely involved the system engineer

with abnormalities

found with a

particular

system.

Several

problems with containment isolation valves

during the period resulted in significant engineering effort to achieve

resolution.

Quality Assurance in Engineering Activities

S ecial

FSAR Review

37551

A recent discovery of a licensee

operating their facility in a manner

contrary to the Updated Final Safety Analysis Report

(UFSAR) description

highlighted the need for a special

focused review that compares plant

practices,

procedures

and/or

parameters

to the

FSAR descriptions.

While

performing the inspections

discussed

in this report, the inspectors

reviewed the applicable portions of the

FSAR that related to the areas

inspected.

The licensee

made

a presentation to the

NRC on Hay 31,

1996 concerning

their corporate-wide plan for reviewing the

FSAR at the CPSL sites.

The

program has generated

a large number of condition reports at the Harris

Plant

(264 by the end of the inspection period).

Three have resulted in

LERs.

The results

from this program will be reviewed in the closure of

Unresolved

Item 50-400/96-04-04,

Tracking

FSAR Discrepancy Resolution.

The inspectors

did not find any additional discrepancies

other than

those identified by the licensee.

Miscellaneous

Engineering Issues

(92903)

Closed

Unresolved

Item 50-400/96-09-03:

Ultimate Heat Sink (UHS)/

Emergency Service Water

(ESW) Technical Specification Interpretation.

This item was unresolved

pending the inspector's

review of previous main

reservoir level history and an overall regulatory assessment.

The

inspector

reviewed previous main reservoir

levels from 1987 until

current that was documented

from performance of procedure

OST- 1021,

Daily Surveillance Requirements.

The inspector verified that the level

had never

been below 217 feet.

Inspection Report 50-400/96-09

documented that

a Technical Specification

Interpretation

(TSI) had been put in place to change the Ultimate Heat

Sink Technical Specification (TS) 3.7.5 Limiting Condition for Operation

(LCO) value to apply the action statement

at the main reservoir level of

215 feet instead of the TS value of 205.7 feet.

The TSI had been in

place since June 28,

1995 and was currently at Revision 3.

Each

revision had been reviewed by the Plant Nuclear Safety Committee

and

approved

by plant management.

The TSI was corrective action for a

problem found during performance of a Service Water System Operational

Performance

Inspection.(SWSOPI)

conducted

by the licensee.

TSI Basis

The TSI-basis

was documented in Inspection Report 50-400/96-09.

The

report documented

the inspector 's review of licensee'ngineering

Service

Requests

(ESRs),

Adverse Condition and Feedback

Reports

(ACFRs),

TSs 3.7.5

(UHS) and 3.7.4 (ESW),.and the associated

TS bases.

The licensee

discovered during the resolution of a

SWSOPI question

related to UHS temperature that although the TS 3.7.5

LCO main reservoir

level of 205.7 feet was adequate

volume to dissipate the design heat

load over

a 30-day period (stated in TS Bases),

the level

was not

adequate

for the emergency service water system to provide sufficient

flow for all components to remove the design heat generated.

Since

an

ESW pump upgrade could not be immediately accomplished to increase

flow,

an a'lternative that was immediately put in place

was to raise the limit

on reservoir level.

A calculated reservoir level of 215 feet was

determined to provide adequate

flow to maintain all components

serviced

by ESW operable.

This administrative limit was put in place through the

TSI.

The inspector 's review of PNSC meeting minutes for the TSI found

that the licensee felt the TSI required them to apply the

LCO "ear ly" as

compared to the TS value and therefore the interpretation

was more

conservative

than TS.

No discussion of a license

amendment/TS

change

was documented.

ESR 9500548,

issued August 25,

1995.

concluded that the 215 feet

elevation main reservoir administrative limit (TSI) needed to be

maintained to ensure operability of some

ESW components.

The inspector

found that later

ESRs

and design calculations

used the 215 feet

elevation

as

an assumption

and did not support retracting that limit.

The

FSAR change

markup in the

ESR did not include the 215 feet elevation

administrative limit.

The inspector

reviewed

FSAR section 2.4.11.7,

Heat Sink Dependability

Requirements,

FSAR section 9.2.1, Service Water System,

and

FSAR section

9.2.5, Ultimate Heat Sink.

None of the

FSAR sections

mentioned the main

reservoir level needing to be 215 feet to provide adequate

ESW flow for

heat removal.

These sections

were changed

by Amendment 46. submitted

April 12,

1996, to include many of the results

from the

SWSOPI question

on this issue.

ESR 9500707,

issued January

17,

1996, provided the basis

for the

FSAR changes to those sections

and included those from ESR

9500548,

but made

no mention of the 215 feet level.

The safety

evaluation for ESR 9500707 concluded that

a license

amendment

was needed

for UHS temperature.

No change

was discussed

for level.

On Hay 21,

1996, licensee

management

authorized the regulatory affairs

organization to develop

a TS change that enco'mpassed

TSI 95-003.

The

10

licensee

had not made

any meaningful progress

on the change prior to the

inspector discussing

the issue,

as documented in IR 50-400/96-09.

The

inspector

found that the licensee did not recognize that the TS did not

meet the definition of LCO in 10 CFR 50.36.

Re ulator

Im act

10 CFR 50.36 states that

LCOs are the lowest functional capability or

performance levels of equipment required for safe .oper ation of the

facility.- The inspector

found from review of the licensee's

calculation

and engineering evaluations that the TSI values were those values

required'by

10 CFR 50.36 for the TS.

The licensee initiated

administrative controls

(TSI) on June 28,

1995, that would have

pr'evented the plant from exceeding the design basis.

These controls

were in place for approximately

15 months prior to the inspector raising

this issue.

Hain reservoir

level

was never below the revised design

basis value during the life'of the plant.

10 CFR 50. Appendix B, Criterion XVI requires that conditions adverse to

quality be promptly identified and cor rected.

Procedure

AP-615,

Condition Reporting,

Revision 20, identifies non-compliance with

regulations

as

an adverse condition.

The licensee

did not promptly

submit

a change to TS 3.7.5.

Consequently,

the failure to promptly

revise

TS 3.7.5'to ensure that the

LCO was the limit for the lowest

performance

level of the ultimate heat sink and emergency service water

system is considered

a violation of 10 CFR 50, Appendix B, Criterion XVI

(50-400/96-10-01).

10 CFR 50.71(e) states that

FSARs shall

be updated annually or 6 months

after each refueling outage.

The revision must reflect all changes

up

to a maximum of 6 months prior to the date of'iling.

FSAR Amendment 46

updated the

FSAR relative to the ultimate heat sink temperature

and

emergency service water

component flows, but did not include information

relative to main reservoir level.

The minimum main reservoir level

had

been determined to be 215 feet instead of the 205.7 feet main reservoir

limit discussed

in FSAR section 2.4.11.7

and TS 3.7.5.

The 215 feet

level is important because it is the level that provides the minimum

flow required for all

ESW components to be operable.

Consequently,

the

failure to adequately

update the

FSAR for main reservoir level in

Amendment 46 is considered

a violation of 10 CFR 50.71(e)

(50-400/

96-10-02).

Licensee Corrective Actions

The inspector

found that the licensee

was adequately

pursuing corrective

action of the technical

issue

from a hardware standpoint including

modifications during the upcoming outage

(RF07) to replace the "B" ESW

pump with a larger capacity

pump and to enlarge the containment

fan

cooler orifices to allow greater flow.

The replacement of the "A" pump

is scheduled for the following outage

(RF08).

The licensee

submitted

a

TS change

request

on October 31,

1996.

and intends to revise the

FSAR to

include all the information in the TSI.

The licensee

performed

a review

of other TSIs and developed

a plan (November 12,

1996) to reduce the

total

number of TSIs to less than 10.

The licensee

also intends to

'revise the administrative controls for TSIs in procedure

AP-107.

Conclusions

The inspector

concluded that the licensee

had vigorously pursued the

design problem when it was discovered in 1995.

The licensee

promptly

ut in place the administrative limit to control main reservoir level.

owever,

a violation of 10 CFR 50 Appendix B Criterion XVI had occurred

in that

a TS change

was not promptly submitted to revise

TS 3.7.5.

In

addition,

FSAR Amendment 46 failed to identify that

UHS main reservoir

level could not go below 215 feet and

ESW perform its design function.

This was considered

a violation of 10 CFR 50.71(e) for not adequately

updating the

FSAR for main reservoir level in Amendment 46 to reflect

the current design basis of the plant.

This unresolved

item is closed.

IV~ Plant

Su

rt

R1

Rl. 1

P1

P1.1

Radiological Protection

and Chemistry

(RP&C) Controls

General

Comments

71750

The inspector

observed radiological controls during the conduct of tours

and observation of maintenance activities and found them to be

acceptable.

The general

approach to the control of contamination

and

dose for the site was good.

Teamwork between the various departments

continued to be

a major contributor to the good control of dose.

The inspector

observed the Post Accident Sampling System quarterly

sample using procedure

CRC-821, Post-Accident

RCS/RHR sampling,

Revision

18.

The drawing of the sample

by the chemistry technicians

was used

as

training.

The procedure

was followed and performance

was good.

Conduct of EP Activities

General

Comments

71750

The licensee

has evaluated their emergency

response

organization

assignments

and has

made

a number of changes.

Training drills and table

top sessions

were planned to train the personnel

in the new positions.

This indicates

a positive management

commitment to the performance of

the emergency

response

function.

The inspector

observed portions of a

training drill conducted

on November 7, 1996.

The scenario

was the

same

challenging scenario

described in Inspection Report 50-400/96-06.

These

training drills were considered

a good way for site emergency

response

personnel

to gain experience.

The inspector also attended the Harris Task Force meeting

on October 30,

1996.

The Harris Task Force consisted of representatives

from each of

the affected county governments,

state

government,

and CP8L personnel.

S1

Sl.l

F1

The task force jointly addresses

Harris site emergency

preparedness

issues that affect the local area.

Conduct of Security and Safeguards Activities

Gener al

Comments

71750

The inspector observed security and safeguards activities during the

conduct of tours, observation of maintenance activities,

and the

emergency

preparedness drill, and found them to be good.

Compensatory

measures

were posted

when necessary

and properly'onducted.

Control of Fire Protection Activities

Fl.1

General

Comments

71750

The inspector inspected fire protection equipment

and observed

activities during the conduct of tours

and observation of maintenance

activities on this equipment

and found them to be acceptable.

V. Mana ement Meetin s

X1

Exit Meeting Sugar y

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on November 26,

1996.

The licensee

acknowledged the findings presented.

The inspectors

asked the licensee

whether any of the material

examined

during the inspection should be considered proprietary.

No proprietary

information was identified.

13

PARTIAL LIST OF PERSONS

CONTACTED

Licensee

D. Alexander,

Supervisor,

Licensing and Regulatory Programs

D. Batton, Superintendent,

On-Line Scheduling

D.

Br aund,

Superintendent,

Security

B. Clark, General

Hanager,

Harris Plant

A. Cockerill, Superintendent,

IKC Electrical

Systems

J. Collins, Manager, Training

J.

Dobbs,

Manager,

Outage

and Scheduling

J.

Donahue,

Director Site Operations,

Harris Plant

R. Duncan,

Superintendent,

Hechanical

Systems

W. Gautier,

Manager,

Maintenance

W. Gurganious,

Superintendent,

Environmental

and Chemistry

H, Hamby, Supervisor,

Regulatory Compliance

H. Hill, Manager,

Nuclear

Assessment

D. HcCarthy, Superintendent,

Outage

Management

K. Neuschaefer,

Superintendent,

Radiation Protection

W. Peavyhouse,

Superintendent,

Design Control

W. Robinson,

Vice President,

Harris Plant

G. Rolfson,

Manager, Harris Engineering Support Services

S. Sewell,

Manager,

Operations

T. Walt, Hanager,

Performance

Evaluation

and Regulatory Affairs

NRC

T. Le, Harris Project Manager,

NRR

H. Shymlock, Chief, Reactor Projects

Branch 4

IP 37551:

IP 40500

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 90712:

IP 92700:

IP 92903:

14

INSPECTION

PROCEDURES

USED

Onsite Engineering

Effectiveness of Licensee Controls in Identifying, Resolving,

and

Preventing

Problems

Surveillance

Observations

Haintenance

Observation

Plant Operations

Plant Support Activities

In Office Review of Written, Reports of Non Routine Events at Power

Reactor Facilities

Onsite Followup of Events

Followup - Engineering

~Qened

50-400/96-10-01

50-400/96-10-02

Closed

ITEHS OPENED,

CLOSED,

AND DISCUSSED

VIO

Failure to Promptly Submit

a Technical Specification

Change for Hain Reservoir

Level (paragraph

E8.1)

VIO

Failure to provide an up-to-date

FSAR Amendment for

Hain Reservoir Level (paragraph

E8.1)

50-400/95-012-00

LER

Containment Pre-entry

Purge Valve Drifted Open

(paragraph

08.1)

50-400/95-014-00

LER

Residual

Heat Removal

Check Valve Testing when Valves

Required for Operability (paragraph

H8.1)

50-400/94-001-00

LER

Inadequate

Surveillance

Procedure for Slave Relay Test

(paragraph

H8 ~ 2)

50-400/96-09-03

Discussed

None

URI

UHS/ESW Technical Specification Interpretation

(paragr aph E8.1)