ML18011A613

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Insp Rept 50-400/94-21 on 940903-28.Two Apparent Violations Noted.Major Areas Inspected:Plant Operations,Review of Nonconformance Repts,Maint Observation,Surveillance Observation,Design Changes & Mods & Fire Protection
ML18011A613
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 10/07/1994
From: Christensen H, Elrod S, Darrell Roberts, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18011A612 List:
References
50-400-94-21, NUDOCS 9411010163
Download: ML18011A613 (22)


See also: IR 05000400/1994021

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Report No.:

50-400/94-21

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Licensee

No.:

NPF-63

Facility Name:

Harris

1

Inspection

Conduc ed:

September

3 - 28,

1994

Inspectors:

J.

e row, Senio

esi

nt Inspector

Da e Signed

S

o

, Senior

esi

nt Inspector

CJ

Da e Signed

D

obert

,

s

ent

nspector

Approved by:

H. Christensen,

Section Chief

Division of Reactor Projects

Dat

Signed

/

Date

igned

SUMMARY

Scope:

This routine inspection

was conducted

by the resident

inspectors

in the areas

of plant operations,

review of nonconformance

reports,

maintenance

observation,

surveillance observation,

design

changes

and modifications, plant

housekeeping,

radiological controls, security, fire protection,

and licensee

action

on previous inspection

items.

Numerous facility tours were conducted

and facility operations

observed.

Some of these

tours

and observations

were

conducted

on backshifts.

Results:

One apparent violation was identified involving inadequate

design control

measures

resulting in a single failure vulnerability affecting the

charging/safety

injection pumps,

paragraph

4-;c.(1).

A second

apparent violation was identified which involved incomplete or

inaccurate

information provided to the

NRC in response

to a generic letter

~

~

~

~

regarding single failure reviews associated

with the

ESW system,

paragraph

4.c.(2).

PDR

0163 94i007

941 10'DOCK 05000400

PDR

2

An unresolved

item was identified involving cell-to-cell resistance

measurements

exceeding

maximum Technical Specification values for the IA

Emergency Battery,

paragraph

3.a.

An unresolved

item was also identified concerning

improper implementation of

procedure

MST-E0010,

1E Battery Weekly Test,

paragraph

3.b.

Another example of improper implementation or resolution of vendor manual

recommendations

was identified, paragraph

4.b.

The content of operator logs regarding entry into

a TS

LCO action statement

was deficient,

paragraph

2.a.( I).

Management

involvement in radiation worker activities was considered

to be

beneficial to overall radiation control program,

paragraph

5.b.

Improvement

was noted in technical

support center

command

and control,

dispatch of damage control

teams

from the operations

support center,

and

timeliness

and content of offsite notifications during the annual

emergency

exercise,

paragraphs

S.e, 5.f.(2)

and 5.f(3).

REPORT DETAILS

1.

Persons

Contacted

Licensee

Employees

D., Batton,

Hanager,

Work Control

  • D. Braund,

Hanager,

Security

B. Christiansen,

Hanager,

Haintenance

  • J. Collins, Hanager,

Training

J.

Dobbs,

Hanager,

Outages

  • J. Donahue,

General

Hanager,

Harris Plant

R. Duncan,

Hanager,

Technical

Support

H. Hamby,

Hanager,

Regulatory Compliance

D. HcCarthy,

Hanager,

Regulatory Affairs

  • R. Prunty,

Hanager,

Licensing

5 Regulatory

Programs

  • W. Robinson,

Vice President,

Harris Plant

  • G. Rolfson,

Hanager,

Harris Engineering

Support Services

H. Smith, Hanager,

Radwaste

Operation

B. White, Hanager,

Environmental

and Radiation Control

"A. Williams, Acting Hanager,

Operations

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

S.

A. Elrod arrived

on site September

19,

1994 to relieve J.

E. Tedrow

of his duties

as Senior Resident

Inspector.

This

NRC personnel

change

became effective on September

22,

1994.

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

2.

,

Operations

a 0

Plant Operations

(71707)

The plant continued in power operation

(Hode 1) for the duration

of this inspection period.

(1)

Shift Logs

and Facility Records

The inspector

reviewed records

and discussed

various entries

with operations

personnel

to verify compliance with the

Technical Specifications

(TS)

and the licensee's

administrative procedures.

The following records

were

reviewed:

shift supervisor's

log; control operator's

log;

night order book; equipment

inoperable record; active

clearance

log; grounding device log; temporary modification

log; chemistry daily reports; shift turnover checklist;

and

selected

radwaste

logs.

In addition, the inspector

independently verified clearance

order tagouts.

In general,

the inspectors

found the logs to be readable,

well organized,

and provided sufficient information on plant-

status

and events.

However, the inspector

found the shift

supervisor's

log to be incomplete regarding

a

7 day

LCO that

was entered

at 10:57 p.m.,

on September

19,

1994.

The

LCO

was entered for the "A" steam generator

PORV, valve INS-58,

which had

been declared

inoperable

due to problems with its

hydraulic system.

The inspector identified on September

20

that the shift supervisor's

log did not contain

an entry for

this

LCO.

This information was available

from other sources

including the onshift operators

and the

RO logs.

This

comment follows similar statements

contained

in

NRC

Inspection

Report 400/94-15 regarding

incomplete control

room logs.

Clearance

tagouts

were found to be properly

implemented.

No violations or deviations

were identified.

Facility Tours

and Observations

Throughout the inspection period, facility tours were

conducted to observe activities in progress.

Some of these

observations

were conducted

during backshifts.

Also, during

this inspection period, licensee

meetings

were attended

by

the inspectors

to observe

planning

and management

activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence; control

room;

emergency diesel

generator building; reactor auxiliary

building; waste processing

building; turbine building; fuel

handling building; emergency

service water building; battery

rooms; electrical

switchgear

rooms;

and the technical

support center.

During these tours,

observations

were

made regarding

monitoring instrumentation

which included equipment

operating status,

electrical

system lineup, reactor

operating

parameters,

and auxiliary equipment operating

parameters.

Indicated parameters

were verified to be in

accordance

with the

TS for the current operational

mode.

The inspectors

also verified that operating shift staffing

was in accordance

with TS requirements

and that control

room

operations

were being conducted

in an orderly and

professional

manner.

In addition, the inspector

observed

shift turnovers

on various occasions

to verify the

continuity of plant status,

operational

problems,

and other

pertinent plant information during these turnovers.

The

licensee's

performance

in these

areas

was satisfactory.

No violations or deviations

were identified.

b.

Review of Nonconformance

Reports

(71707)

Adverse Condition Feedback

Reports

(ACFR) were reviewed to verify

the following:

TS were complied with, corrective actions

and

generic

items were identified and items were, reported

as required

by 10 CFR 50.73.

No violations or deviations

were identified.

Maintenance

a ~

Maintenance

Observation

(62703)

The inspector observed/reviewed

maintenance

activities to verify

that correct equipment

clearances

were in effect; work requests

and fire prevention work permits were issued

and

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the following maintenance activities:

Clean boric acid buildup from the

"C" CSIP inlet flange

and

retorque bolts to between

100 -

197 ft~lbs.

Install lube oil sample taps

on "C" CSIP components

in

accordance

with PCR 6103,

SI Lube Oil Sample

Taps.

Jumper out cell

87 from the IA emergency battery

and jumper

in spare cell in accordance

with CM-E0024, Safety/Non-Safety

Spare Battery Cell Connection.

The spare cell

was installed in the IA emergency battery

following discovery of some deformities

on the non-

contacting surface of a battery post

on cell 87.

After

installation of the spare cell

and removal of cell

87 on

September

15, the inspector noted that

no post-maintenance

testing occurred other than items contained

in a'M

procedure

which had

been

performed

on the individual spare

cell prior to its installation (i.e, temperature

and

specific gravity readings).

The inspector

asked

maintenance

personnel

whether

any other post maintenance activities

would be done

on the newly connected

battery cell.

Licensee

personnel

indicated that

no other activities were referenced

in the work ticket or the

PCR which was implemented for the

spare cell installation.

After the inspector left the job

site,

the maintenance

crew took cell-to-cell resistance

readings

between

the newly connected

spare cell

and

a cell

on the tier to which it was connected.

These

readings

were

taken to obtain baseline

data

so that trending could

be

performed during subsequently

scheduled

surveillance tests.

Cell-to-cell resistance

readings of 182 micro-ohms were

obtained

which exceeded

a connection resistance

value of 150

micro-ohms referenced

in TS 4.8.2. 1.

.This information was

documented

in ACFR 94-2887.

The battery

had

been declared

operable

at 9:30 a.m.,

on

September

15 following installation of the spare cell.

It

was declared

inoperable nearly

9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> later at 6:07 p.m.,

based

on engineering

reviews of the above resistance

data.

The'spare cell was then

removed from the battery

and cell

//7

was reinstalled.

The licensee

conducted

an operability

determination

which concluded that the battery would remain

operable with cell

0'7 reinstalled

based

on its post

deformation occurring

on

a non'-contacting

side

and that

no

corrosion existed

on the contacting sides of the post.

The

operability determination

also concluded that cell P7's

capacity

was not affected

by it having been

removed from the

battery

and uncharged for approximately

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

The

licensee

then initiated an event review team tasked with

conducting

an engineering

review to determine

whether the

ability of the battery to perform its intended safety

function was jeopardized

during the

9 hour1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> period in which

the spare cell

was installed.

This review would also

include

a root cause

determination

as to why the attribute

of connection resistance

was missed during development of

the

PCR and/or implementing procedures

which installed the

spare cell.

The licensee

issued

an internal

memorandum

on September

21,

1994,

which concluded that the battery was capable of

performing its intended function with the spare cell

installed

and with cell-to-cell resistance

readings of 182

micro-ohms.

The inspectors later reviewed

a preliminary

licensee

interpretation of TS 4.8.2.1.c.3

which concluded

that the requirement

contained

in Technical Specifications

was intended for resistance

measurements

at individual

connections (i.e between

post

and connecting

bar)

and not

for resistance

values of inter-tier jumpers or cell-to-cell

assemblies,

as

had

been

measured

on September

15.

The

inspectors

informed licensee

personnel

that

an independent

NRC review of the intent behind the

TS requirement

and of

the licensee's

final event review team findings would be

conducted

and tracked

as

an unresolved

item.

Unresolved

Item (400/94-21-03):

Determine the intent of TS 4.8.2.l.c.3

and review the licensee's

operability

determination for the IA Emergency Battery.

In general,

the performance of work was satisfactory with proper

documentation of removed

components

and independent verification

of the reinstallation.

No violations or deviations

were

identified.

Surveillance Observation

(61726)

Surveillance tests

were observed

to verify that approved

procedures

were being used; qualified personnel

were conducting

the tests;

tests

were adequate

to verify equipment operability;

calibrated

equipment

was utilized;

and

TS requirements

were

followed.

The following tests

were observed

and/or data reviewed:

~

MST-E0010

IE Battery Weekly Test

~

OST-1079

Containment Isolation Valves ISI Test quarterly

Interval

The physical

performance of these

procedures

was found to be

satisfactory with proper

use of calibrated test equipment,

necessary

communications

established,

initial

notification/authorization of control

room personnel,

and

knowledgeable

personnel

having performed the tasks.

Post-completion

procedure

review of MST-0010 by the inspector

found that battery cell temperature

had exceeded

the procedure's

administrative

range but the control

room had not been notified as

required

by the procedure.

Also, the procedure

referenced

vendor

technical

manual

"PAA" or C8D manual

12-800,

Standby Battery,

Flooded Cell, Installation

and Operating Instructions.

Though the

vendor manual

was approved,

the local procedures

did not seem to

implement the various requirements

such

as torque values

upon

installation or semi-annual

retorque at

a lower value prior to

taking inter-cell resistance

readings.

These

items are unresolved

pending completion of the

NRC technical

review.

Unresolved

Item 400/94-21-04:

Adequacy of procedures

and

procedure

adherence

in the area of battery surveillance.

c.

Licensee Action on Previously Identified Maintenance

Findings

'92902)

(Closed) Violation 400/94-13-03:

Failure to calibrate high

voltage probe measuring

device.

The inspector

reviewed

and verified completion of the corrective

actions listed in the licensee's

response letter dated August 24,

1994.

Licensee

personnel

have revised applicable surveillance

test procedures

to require the use of calibrated

high voltage

probes

and

have trained technicians

on using this test equipment.

The high voltage probes

used in the example cited were verified to

meet accuracy requirements

and included in the licensee's

calibration program.

Engineering

Design/Installation/Testing

of Modifications (37551)

Plant

Change

Requests

(PCR) involving the installation of new or

modified systems

were reviewed to verify that the changes

were

reviewed

and approved

in accordance

with 10 CFR 50.59, that the

changes

were performed in accordance

with technically adequate

and

approved

procedures,

that subsequent

testing

and test results

met

approved

acceptance

criteria or deviations

were resolved

in an

acceptable

manner,

and that appropriate

drawings

and facility

procedures

were revised

as necessary.

In addition,

PCR's

documenting engineering

evaluations

were also reviewed.

The

following modifications and/or testing in progress

was observed.

~

PCR 6103

Safety Injection Lube Oil Sample

Taps

~

PCR 7379

Reportability Determination of

ESW to "B" CSIP

No violations or deviations

were identified.

System Engineering

(37551)

The inspector reviewed information contained

in a vendor manual

for ITT Barton Hydramotor actuators.

During

a tour on August 8,

1994,

the inspector

noted that these

actuators

were employed

on

various plant valves

and dampers

including auxiliary feedwater

flow control valves from both the motor driven and turbine driven

auxiliary feedwater

pumps.

The technical

manual listed

maintenance

recommendations

for the actuators

which included

an

item to stroke the actuators

a minimum of 10 times per 90 days.

The inspector

knew that the

AFW flow control valves were not

routinely stroked at that frequency

and inquired with engineering

personnel

on the subject.

According to the engineer,

the

recommendation

had not been translated

into any maintenance

or

surveillance

procedure.

The engineer

indicated that this

nonconformance

was missed during the licensee's

technical

manual

review conducted

in 1991

and 1992.

As

a result of the inspector's

finding, engineering

personnel

contacted

the actuator manufacturer

who indicated that periodic stroking was only a recommendation

for

Hydramotor actuators

with an older type seal that historically

exhibited leakage

problems.

The. Hydramotors

used for the

AFW flow

control valves

had

been

upgraded with a seal that did not exhibit

the problem.

On August ll, this information was

added to the

review forms which had already

been initiated for the vendor

manual

in question.

Further discussions

with licensee

personnel

indicated that this particular vendor recommendation

had

been

addressed

several

years

ago when the valves were included in the

licensee's

Eg program.

It was determined during correspondence

with the vendor then that the maintenance

recommendation

only

applied to those actuators that

had the older type seal installed.

However, that information was not well documented

as the valves

were ultimately removed

from the

Eg program.

The cognizant

engineer

indicated that

he would initiate an

ESR to have the

vendor manual

updated.

Licensee Action on Previously Identified Engineering

Inspection

Findings

(92703)

(

(1)

(Closed)

Unresolved

Item 400/94-17-04:

Examine the

licensee's

design review of the

ESW system cooling water

supply to the

CSIP oil coolers

and development of a better

test method.

This item was previously discussed

in

NRC Inspection

Report

50-400/94-17.

The licensee

and the

NSSS vendor have subsequently

completed

a design review of the postulated

failure-to-open of valve

1SW-270,

"ESW header

"A" return valve."

The design review

considered

the effect on the CSIPs,

and also the increased

service water temperature

effects

on

ESW system piping.

The

review concentrated

on the "8" train CSIPs, i.e., the "8"

CSIP or the

"C" CSIP aligned to the "8" train.

The "A" CSIP

was

assumed

not to be available during the single failure

scenario

due to valve

1SW-270 being

on the "A" ESW discharge

header.

The review analyzed

both the long standing

ESW

valve lineup with all valves

open

such that both

ESW trains

supplied all three

CSIPs,

and the temporary

ESW valve lineup

existing from July 1-18,

1994,

in which the opposite train

ESW isolation valves from the oil cooler outlets

were

closed.

The licensee

documented

the following review

results

in

PCR 7379, "Reportability Determination

of,ESW to

nBn CSIP

n

For the long-standing

ESW valve lineup with all the

valves

open

such that both

ESW trains supplied all

three

CSIPs, it was concluded that, if a safety

injection signal

was initiated concurrently with a

loss of offsite power,

"A" train valve

1SW-270 failing

to open would result in cooling water with temperature

exceeding

270 degrees

Fahrenheit

reaching the "8"

train CSIP oil coolers

in 10 minutes

and

26 seconds.

This would result in failure of the only available

CSIP.

For the temporary

ESW valve lineup that existed

from

July 1-18,

1994, in which the opposite train

ESW

isolation valves

on the oil cooler outlets were

closed,

the time for this increased

temperature

water

to reach the "8" train CSIP oil coolers

was reduced to

9 minutes

and

13 seconds.

This would result in

quicker failure of the only available

CSIP.

The design review further concluded that operator

'ction

would be required within the above time frames

to prevent

CSIP failure.

~

The

NSSS vendor also concluded that the integrity of

the

ESW piping in the

CSIP rooms,

which would be

challenged

by expansion

from temperatures

exceeding

the design,

could not be assured

unless

operator

action was taken within the

above time frames.

This vulnerability existed

from initial power operations

in

Janua'ry

1987, until July 18,

1994,

when the opposite train

ESW supply valves to the

CSIP oil coolers

were shut.

This,

in conjunction with previously shutting the opposite train

oil cooler discharge

valves on'uly I, 1994,

accomplished

total train separation

of the

ESW headers

to and from the

CSIPs.

The licensee

considered

the current lineup (opposite

train supply

and discharge

valves shut) to be both the short

and long term corrective action to eliminate the single

failure vulnerability.

The inspectors

reviewed the engineering evaluation,

various

flow and temperature profile calculations,

and

correspondence

between

the licensee

and its

NSSS vendor.

Based

on flow models developed to support the evaluations,

the increased

temperature vulnerability was setup

by the

single failure of valve

ISW-270 followed by an increase

in

the "A" discharge

header

pressure

due to continued operation

of the "A" ESW booster

pump.

This increase

in discharge

header

pressure

would cause

a reverse

flow path in which

preheated

ESW water would flow back through the "A" EDG

jacket water cooler,

which provides

a significant heat input

during the loss of offsite power scenario.

Heated

ESW water

would then flow through the CSIP oil coolers.

Because of

the lack of train separation

before July 18 and the

significantly higher "A" train header

pressure,

the "B"

ESW

header

would not provide sufficient cooling water flow to

the

CSIP oil coolers during the postulated

scenario

absent

operator action.

The inspectors

had originally questioned

why the "B" ESW

header

was not vulnerable to the comparable

single failure

of "B" train header

discharge

valve ISW-271.

The licensee's

flow model considered this.

The study concluded that the

"B"

ESW booster

pump was located

downstream of the

CSIP oil

cooler lines such that it did not create

the

same

high

pressure/reverse

flow gradients that the "A" train failure

did.

The inspectors

reviewed the design basis of the

ESW system

contained

in the licensee's

FSAR section 9.2. 1, Service

Water System.

It stated that the service water system is

designed to provide

a heat sink for essential

loads

assuming

a single active failure in conjunction with a loss of

offsite power.

Essential

loads referenced

in Table 9.2. 1-1

of the

FSAR included the charging

pump oil coolers.

As

referenced

in Table 9.2.1-13 of the

FSAR,

a failure analysis

was performed prior to plant operations

to support the

statement

that service water to essential

cooling loads

would be assured

despite

any active failure in the system.

That analysis

only considered

the active failures of the

ESW

pumps,

booster

pumps,

one emergency electric power train,

and non-essential

header isolation valves.

It did not

consider the failure of any other motor operated

valves in

the system.

In 1989, following industry events

involving service water

systems,

the

NRC issued

Generic Letter 89-13, Service Mater

System

Problems Affecting Safety-Related

Equipment.

One of

the actions

requested

by the Generic Letter was that

licensees

conduct

a review to confirm that the service water

systems

would perform their intended safety 'functions in the

event of the failure of a single active component.

Following recent

concerns with the Harris

ESM system

involving the above-described

scenario

and the recent

discovery of Asiatic clams in the

ESW intake structures

(IFI

400/94-17-02),

the inspectors

reviewed the licensee's

earlier actions regarding the generic letter.

The licensee

provided

a draft single failure analysis

which discussed

the

consequences

of the failure modes of every active component

in the

ESW system.

The analysis for valve- 1SW-270

concluded,

in summary, that

no immediate corrective actions

were required

and that control

room annunciation

and

redundant train flow would be available.

The reverse

flow

and elevated

temperature

scenario

was never considered.

According to licensee

personnel,

this draft single failure

analysis

was the only one completed to address

the generic

letter.

t

10 CFR 50 Appendix A, Criterion 44, requires that

a system

to transfer heat from systems

and components

to an ultimate

heat sink be provided which will perform the intended safety

function assuming

a single failure.

10 CFR 50, Appendix B,

Criterion III, requires that measures

be established

to

assure that applicable regulatory requirements

and the

design basis

are correctly translated

into specifications,

drawings,

procedures,

and instructions.

The single failure

vulnerability described

above,

and the lack of adequate

design

measures

both prior to plant operation

and during the

Generic Letter 89-13 review are contrary to these

requirements

and are considered

to be

an apparent violation.

Apparent Violation (400/94-21-01):

Failure to establish

adequate

design

measures

to prevent/identify single failure

vulnerability associated

with ESW=valve

1SW-270.

10

As mentioned

above,

the single failure vulnerability was

immediately corrected

by shutting the opposite train's

ESW

supply

and discharge

valves.

However, at the conclusion of

the inspection period, the licensee

had not completed

a root

cause investigation into why the design deficiency was

missed.

It should

be noted that while this postulated

failure is based

on theory, various flow characteristics

assumed

in the licensee's

flow analyses

were substantiated

by field walkdowns

and the results of surveillance tests.

As a mitigating factor, the licensee

conducted .validation

scenarios

on the plant simulator to demonstrate

that

operators

on six crews would have taken steps

to restore

adequate

ESW flow within the

9 minute time frame (i.e.,

opening

ISW-270, stopping the "A" ESW booster

pump, etc.)

using existing procedures

and relying on control

room

annunciation.

These

scenarios

were conducted,

however,

assuming that offsite power was available.

The licensee

indicated that its root cause investigation

and

any

recommendation

of corrective actions

would be completed

by

the end of September

1994.

As noted

above,

the inspectors

reviewed the licensee's

actions taken in response

to Generic Letter 89-13.

This

Generic Letter requested,

among other actions,

that

licensees

confirm that the service water system would

perform its intended function in accordance

with the

licensing basis for the plant.

The confirmation was to

include

a single failure review for every active component

in the system

and

a recent

system walkdown.

In a letter to

the

NRC dated January

26,

1990,

the licensee

committed to

conduct the review and walkdown prior to startup

from the

next scheduled

refueling outage.

In a followup response

to

the

NRC dated

June

17,

1991, the licensee

stated that the

Harris plant

had completed,

as of the Hay 20,

1991, plant

startup date

(from refueling outage

0'3), the initial

activities, testing,

and establishment

of the continuing

program to which CPLL committed.

Following the recent discovery of Asiatic clams

and the

single failure vulnerability associated

with ISW-270, the

inspectors

reviewed

a copy of the single failure analysis

conducted

to support the generic letter.

This review

contained

a failure analysis for each of the active

components

as requested

by the letter.

However, the

information provided to the inspectors

was in draft form.

Licensee

personnel

informed the inspectors that they were

unable to track down

a finalized copy of the failure

analysis,

but they were able to locate internal

memorandums

issued

from the offsite engineering

organization during the

time frame in which the single failure review was conducted.

These

memos discussed

the status of the draft single failure

analysis.

One

memorandum

dated

Hay 22,

1991, stated that

the single failure review would remain in draft to'allow

incorporation of plant comments.

The Hay 7 memo stated that

after cleaning

up of editorial

comments,

the single failure

reviews would be transmitted onsite for inclusion into

packages

being prepared for future

NRC inspection.

The

licensee

was unable to find any further internal

correspondence

indicating that the si'ngle failure review was

finalized prior to Hay 20,

1991,

as indicated in its

response

to the

NRC.

10 CFR 50.9,

Completeness

and Accuracy of Information,

requires,

in part, that information provided to the

Commission

by a licensee

or information required

by the

Commission's regulations,

orders,

or license conditions to

be maintained

by the licensee

shall

be complete

and accurate

in all material

respects.

The .licensee's

actions regarding

the incomplete single failure review or the absence

of

documentation

in plant records containing

a finalized single

failure review is in contrast to statements

contained

in the

licensee's

response

to the

NRC dated

June

17,

1991.

The

licensee's

activities in this regard

are contrary to

10 CFR 50.9

and are considered

to be

an apparent violation.

Apparent Violation (400/94-21-02):

Failure to provide

complete

and accurate

information regarding service

water'eviews.

'Closed)

Inspector

Followup Item 400/94-15-01:

Follow the

licensee's

actions to determine

the adequacy of

ESW flow to

the

ESCWS chillers while aligned to the main reservoir at

the minimum TS level.

Licensee

personnel

have completed engineering calculation

SW-0078 to determine the minimum flowrates for the

ESW

system

when aligned to take

a suction from the main

reservoir.

The licensee

performed this calculation in

conjunction with the single failure analysis of 1SW-270

described

in paragraph 4.c.(1) of this report.

The

calculation

assumed

a minimum main reservoir level of 205.7

feet

and considered

single failures of active components.

This calculation revealed that the minimum calculated

flowrates for all major

ESW-cooled

components,

including the

ESCWS chillers, were above their respective limits.

The

minimum flowrate values for the "A" and

"B" ESCWS chillers

were calculated to be 2,258

GPH and 2,288

GPH respectively

compared to the minimum limit of 2, 175

GPH.

(Closed) Violation 400/94-12-03:

Failure to properly review

and approve

a change to modification acceptance

testing.

The inspector

reviewed

and verified completion of the

corrective actions listed in the licensee's

response letter

12

dated July 14,

1994.

Licensee

personnel

reviewed the actual

acceptance

testing performed for the modification and found

it to be satisfactory.

Field revision

88 was issued to

modification PCR-6105,

EDG Start

Time Recorder,

to document

the testing performed.

Training was provided to appropriate

licensee

engineering

personnel.

5.

Plant Support

a.

Plant Housekeeping

Conditions

(71707)

- Storage of material

and

components,

and cleanliness

conditions of various areas

throughout

the facility were observed to determine whether safety and/or fire

hazards

existed.

b.

C.

Radiological

Protection

Program

(71750)

- Radiation protection

control activities were observed to verify that these activities

were in conformance with the facility policies

and procedures,

and

in compliance with regulatory requirements.

The inspectors

also

verified that selected

doors which controlled access

to very high

radiation areas

were appropriately locked.

Radiological

postings

were likewise spot checked for adequacy.

While observing

maintenance

associated

with the

"C" CSIP on

September

12, the inspectors

noted that several different jobs

involving 5 or 6 workers were occurring simultaneously.

All of

the jobs involved breaching the area

around the

pump baseplate

which had

been

posted

as

a contaminated

area listing only gloves

as

a dress

requirement.

The inspector

considered

the number of

people working in this small

area to represent

a higher than

normal potential for spreading

contamination,

especially in the

absence

of a health physics technician.

This concern

was

discussed

with the appropriate

management

personnel

who had also

observed

the working condition

and

had already initiated steps to

correct it.

When the inspector returned to the work site,

he

noted that

a health physics technician

was present

and the size of

the posted

area

had

been

increased

so that better controls could

be implemented for equipment

being taken from the

pump baseplate

area.

The inspector considered

licensee

management's

aggressiveness

in addressing

this matter to be beneficial to the

plant's overall

implementation of the radiological protection

program.

Security Control

(71750)

- The performance of various shifts of

the security force was observed

in the conduct of daily activities

which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and

retrieval; escorting of visitors; patrols;

and compensatory

posts.

In addition,

the inspector'bserved

the operational

status of

closed circuit television monitors,

the intrusion detection

system

in the central

and secondary

alarm stations,

protected

area

lighting, protected

and vital area barrier integrity,

and the

security organization interface with operations

and maintenance.

13

Fire Protection

(71750)

- Fire protection activities, staffing and

equipment

were observed to verify that fire brigade staffing was

appropriate

and that fire alarms,

extinguishing equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

During plant tours,

areas

were

inspected

to ensure fire hazards

did not exist.

Emergency

Preparedness

(71750)

- Emergency

response

facilities'ere

toured to verify availability for emergency

operation.

Duty

rosters

were reviewed to verify appropriate staffing levels were

maintained.

As applicable,

emergency

preparedness

exercises

and

drills were observed to verify response

personnel

were adequately

trained.

On September

13,

1994, the annual

emergency drill was conducted

by

the licensee

to verify the effectiveness

of the Radiological

Emergency

Response

Plan

and implementing procedures.

In contrast

to comments

contained

in

NRC Inspection

Report 50-400/94-13

concerning

a practice dril1, no problems

were identified in the

area of command

and control from the

TSC.

Additionally, open

items identified during previous

annual

exercises

involving

timeliness

and content of offsite notifications

and delays in

dispatching

damage control

teams

from the

OSC were closed

as

indicated in paragraphs

5.f.(2)

and 5.f.(3) below.

Licensee Action on Previously Identified Plant Support Inspection

Findings

(92904)

(1)

(Closed) Violation 400/94-05-02:

Failure to implement

adequate

corrective actions to prevent recurrence

of

deficiencies.

The inspector

reviewed

and verified completion of the

corrective actions listed in the licensee's

response letter

dated April 8,

1994.

The following actions

were completed:

~

For the temperature

maintenance

of boron injection

piping, the licensee

completed modification PCR-6259

which installed replacement

room heaters

in the boric

acid transfer

pump valve gallery.

In addition,

placards

were installed near the heater

power panels

alerting personnel

to their importance.

The auxiliary

operator

rounds guidance

was also

changed

indicating

. the importance of the heaters

and compensatory

action

required if they are found to be functioning

improperly.

~

For the degraded

ERFIS

SPDS function, the licensee

revised operating

procedures

and generated

an

operational

check procedure to verify proper operation

of ERFIS.

Operating logs were revised to periodically

check that key ERFIS functions are working properly.

14

A long term plan was also developed for ERFIS

reliability enhancements.

(2)

(Closed)

Inspector

Followup Item 400/92-16-03:

Review

licensee's

corrective actions for improving notification

content

and timeliness to offsite emergency

agencies.

The licensee's

recent training for emergency

communicators

emphasized

message

content .and timeliness.

Additionally,

with the

EOF now assembling for activation at

an alert

classification,

the responsibility for notification of the

State

and Counties

was turned over to the

EOF from the

control

room.

This simplified the turnover process

by

eliminating the interim steps of turnover from the control

room to the

TSC and then from the

TSC to the

EOF.

The

emergency notification messages

1 thru

10 reported during

the September

13,

1994,

emergency 'exercise

were reviewed for

message

content

and timeliness.

All messages

were timely

and contained

the significant events

which affected the

response

of the State

and Counties.

(3)

(Closed)

Inspector

Followup Item 400/93-18-01:

Exercise

Weakness:

Damage Control

Team

(DCT) with top priority

mission took approximately

two hours to be dispatched

from

the

OSC.

The licensee

had increased

the level of management

authority

in the

OSC by re-locating the emergency repair director from

the

TSC to the

OSC.

The SEC's priorities for DCT's were

thereby

implemented

by the

ERD in the responsible

emergency

facility.

Other changes

included selected

OSC personnel

being partially dressed-out

in advance to expedite

team

response.

Noted improvements

were observed

in the September

13,

1994 emergency

exercise with the timely dispatch of top

priority teams

being emphasized.

The inspectors

found plant housekeeping

and material condition of

components

to be satisfactory.

The licensee's

adherence

to

radiological controls, security controls, fire protection

requirements,

emergency

preparedness

requirements

and

TS

requirements

in these

areas

was satisfactory.

No 'violations or

deviations

were identified.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1) at the conclusion of the inspection

on September

28,

1994.

During

this meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violations addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify as

proprietary

any of the materials

provided to or reviewed

by the

15

inspectors

during this inspection.

No dissenting

comments

from the

licensee

were received,

however,

regarding the response

to Generic Letter 89-13 discussed

in paragraph 4.c.(2),

the licensee

believed that

the Generic Letter technical

review was completed

and that any

incompleteness

involved administrative concurrence.

Item Number

Descri tion and Reference

400/94-21-01

Apparent Violation:

Failure to establish

adequate

design

measures

to prevent/

identify single failure vulnerability

associated

with

ESW valve

1SW-270.

400/94-21-02

400/94-21-03

400/94-21-04

Acronyms

and Initialisms

Apparent Violation:

Failure to provide

complete

and accurate

information

regarding

a service water review.

Unresolved

Item:

Determine the intent of

TS 4.8.2. l.c.3 and review the licensee's

operability determination for the

1A

Emergency Battery.

Unresolved

Item:

Adequacy of procedures

and procedure

adherence

in the area of

battery surveillance.

ACFR

AFW

CFR

CPKL

CSIP

DCT

EDG

EOF

EQ

ERD

ERFIS-

ESCWS-

ESW

FSAR

GPM

IFI

ISI

LCO

NRC

NSSS

OSC

PORV

RO

SI

Adverse Condition Feedback

Report

Auxiliary Feedwater

Code of Federal

Regulations

Carolina

Power

and Light

Charging Safety Injection

Pump

Damage Control

Team

Emergency Diesel

Generator

Emergency Operations Facility

Environmental Qualification

Emergency

Response

Director

Emergency

Response

Facility Information System

Essential

Services Chilled Water System

Emergency Service

Water

Final Safety Analysis Report

Gallons

Per Minute

Inspector

Followup Item

Inservice Inspection

Limiting Condition for Operation

Nuclear Regulatory

Commission

Nuclear Steam

System Supplier

Operational

Support Center

Power Operated Relief Valve

Reactor Operator

Safety Injection

SPDS

TS

TSC

16

Safety Parameter

Display System

Technical Specification

Technical

Support Center

0