ML18010B156

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Insp Rept 50-400/93-12 on 930515-0618.Violation Noted.Major Areas Inspected:Plant Operations,Radiological Controls, Security & Fire Protection
ML18010B156
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 07/02/1993
From: Christensen H, Darrell Roberts, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010B153 List:
References
50-400-93-12, NUDOCS 9308050063
Download: ML18010B156 (24)


See also: IR 05000400/1993012

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

++*++

Report No.;

50-400/93-12

Licensee:

Carolina

Power and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

Hay 15 - June

18,

1993

Inspectors:

J.

Te row, Senior

Resi

t

pector

D. Roberts,

esident

Ins

ctor

Approved by:

H.

ristensen,

C ief

Reactor Projects Section

lA

Division of Reactor

Projects

Licensee

No.:

NPF-63

D

e

igne

v i//W

Date Signed

7

z.

Date Signe

SUMMARY

Scope:

This routine inspection

was conducted

by two resident

inspectors

in the areas

of plant operations,

radiological controls, security, fire protection,

review

of nonconformance

reports,

surveillance observation,

maintenance

observation,

safety

system walkdown, followup of onsite events,

outage activities,

adverse

weather operations,

licensee

event reports,

and licensee

action

on previous

inspection

items.

Numerous facility tours were conducted

and facility

operations

observed.

Some of these tours

and observations

were conducted

on

backshifts.

Results:

Three violations were identified:

Failure to maintain

an electrical

containment penetration

conductor overcurrent protection

device operable,

paragraph 2.c.(1);

Failure to properly implement plant procedures for the

control of locked valves

and for the oper ation of electrical

switchgear,

paragraphs

2.c.(3)

and 6;

and Failure to verify design

accuracy of auxiliary

feedwater recirculation piping, paragraph

10.

Weaknesses

were noted in the areas of scaffolding control, paragraph

2.b.(7)

and in the documentation of a boric acid leakage

inspection,

paragraph

7.

9308050063

930702

PDR

ADOCK 05000400

8

PDR

2

More problems

were experienced

with 480 volt Asea

Brown Boveri

LK Circuit

breakers,

paragraph 2.c.(2).

Good pre-planning

and

use of equipment

mockups

were evident for containment

work, paragraph

7.

In addition, the simulator was utilized to provide plant

startup/shutdown

training and potential transients.

Also, simulator training

was provided for the conduct of an infrequent turbine test,

paragraph

3.

REPORT DETAILS

Persons

Contacted

Licensee

Employees

D. Batton,

Manager,

Work Control

J. Collins, Manager, Training

  • C. Gibson,

Manager,

Programs

and Procedures

H. Hamby, Manager,

Regulatory Compliance

D. HcCarthy,

Manager,

Regulatory Affairs

T. Morton, Manager,

Maintenance

  • J. Hoyer, Manager, Site Assessment

J; Nevill, Manager,

Projects

  • W. Robinson,

General

Manager,

Harris Plant

  • W. Seyler,

Hanager,

Outages

and Modifications

H. Smith,

Manager,

Radwaste

Operation

  • D. Tibbitts, Manager,

Operations

G. Vaughn, Vice President,

Harris Nuclear Project

  • B. White, Manager,

Environmental

and Radiation Control

W. Wilson, Manager,

Spent Nuclear Fuel

  • L. Woods,

Manager,

Technical

Support

  • A. Worth, Principal

Engineer,

Nuclear Engineering

NRC Representatives

  • J. Johnson,

Deputy Director, Division of Reactor Projects

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

"Attended exit interview

Acronyms

and initialisms used throughout .this report are listed in the

last paragraph.

Review of Plant Operations

(71707)

The plant began this inspection period in power operation

(Mode 1).

At

12:07 a.m.,

on Hay 22,

1993,

a plant shutdown

was performed to repair

steam generator

blowdown valve 1BD-8 located inside containment.

The

plant was placed in the hot standby condition

(Hode 3) at 12:44 a.m. to

effect repairs.

Following completion of these repairs,

a reactor

startup

was

commenced

and criticality achieved at 3:19 a.m.,

on Hay 22.

Power operation

was resumed

at 1:30 p.m.,

on Hay 23.

The plant

continued in power operation for the remainder of this inspection

period.

'a ~

Shift Logs and Facility Records

/

The inspector reviewed records

and discussed

various entries with

operations

personnel

to verify compliance with the Technical

Specifications

(TS)

and the licensee's

administrative procedures.

2

The following records

were reviewed:

shift supervisor's

log;

control operator's

log; night order book; equipment

inoperable

record; active clearance

log; grounding device log; temporary

modification log; chemistry daily reports; shift turnover

checklist;

and selected

radwaste

logs.

In addition, the inspector

independently verified clearance

order tagouts.

The inspectors

found the logs to be readable,

well organized,

and

provided sufficient information on .plant status

and events.

Clearance

tagouts

were found to be properly implemented.

During a

review of the shift supervisor's

log, the inspector noted

an entry

for June

7,

1993,

where the shift supervisor

had identified an

expired working copy of procedure

OP-. 126

(Main Steam,

Extraction

Steam,

and

Steam

Dump Systems)

during

a tour of the steam tunnel

area.

Selected

controlled copies of procedures

are maintained at

local operating stations to assist

operators

in system/component

operation.

The expired procedure

was subsequently

replaced with a

current controlled copy of the procedure.

The inspector toured plant areas

and verified that the procedures

at local operating stations

were properly controlled.

Areas

inspected

included the steam tunnel,

emergency diesel

generator

building, fuel handling building,

and auxiliary control

room.

No

discrepancies

were identified.

Also, the licensee's

periodic

audits of controlled procedures

in these

areas

were reviewed.

The

audit reports indicated that these

procedures

were generally well

maintained.

No violations or deviations

were identified.

Facility Tours

and Observations

Throughout the inspection period, facility tours were conducted to

observe operations,

surveillance,

and maintenance activities in

progress.

Some of these observations

were conducted during

backshifts.

Also, during this inspection period, licensee

meetings

were attended

by the inspectors

to observe

planning

and

management activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence;

control

room;

emergency diesel

generator building; reactor

auxiliary building; waste processing

building; turbine building;

fuel handling building; emergency service water building; battery

rooms; electrical

switchgear

rooms; the technical

support center;

and the emergency operations facility.

During these tours, the following observations

were made:

(I)

Monitoring Instrumentation

- Equipment operating status,

area atmospheric

and liquid radiation monitors, electrical

system lineup, reactor operating

parameters,

and auxiliary

equipment operating

parameters

were observed to'verify that

indicated parameters

were in accordance

with the

TS for the

current operational

mode.

Shift Staffing - The inspectors verified that operating

shift staffing was in accordance

with TS requirements

and

that control

room operations

were being conducted

in an

orderly and professional

manner.

In addition, the inspector

observed shift turnover s on various occasions

to verify the

continuity of plant status,

operational

problems,

and other

pertinent plant information during these turnovers.

Plant Housekeeping

Conditions - Storage of material

and

components,

and cleanliness

conditions of various areas

throughout the facility were observed to determine

whether

safety and/or fire hazards

existed.

Radiological Protection

Program - Radiation protection

control activities were observed routinely to verify that

these activities were in conformance with the facility

policies

and procedures,

and in compliance with regulatory

requirements.

The inspectors

also reviewed selected

radiation work permits to verify that controls were

adequate.

Security Control - The performance of various shifts of the

security force was observed

in the conduct of daily

activities which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and retrieval; escorting of visitors;

patrols;

and compensatory

posts.

In addition, the inspector

observed

the operational

status of closed circuit television

monitors, the intrusion detection

system in the central

and

secondary

alarm stations,

protected

area lighting, protected

and vital area barrier integrity,

and the security

organization interface with operations

and maintenance.

Fire Protection

- Fire protection activities, staffing and

equipment

were observed to verify that fire brigade staffing

was appropriate

and that fire alarms,

extinguishing

equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

Between January

and June

1993, significant amounts of

scaffolding had

been erected

in the

190 foot elevation of

the reactor auxiliary building in the vicinity of the "A"

residual

heat removal

(RHR) and containment

spray

pumps,

and

above safety-related

system piping, electrical junction

boxes,

conduits,

and the area

HVAC unit.

The scaffolding

had been erected to support the correction of problems which

have occurred

due to ground water intrusion

(See

NRC

Inspection

Report 50-400/92-04).

'Concurrently

on Hay 19,

1993, the licensee

performed

a maintenance

outage to repair

several

small deficiencies in "B" safety train components

including the "C"- CSIP,

"B" RHR,

CCW,

and

ESW pumps.

The

inspector questioned

the wisdom of placing the "B" RHR

system under

an equipment clearance

which rendered it

inoperable at the

same time that scaffolding was erected

around the "A" RHR pump

and system piping.

The inspector

discussed

this situation with licensee

management.

Although

the licensee

had established

a program for the control of

scaffolding,

no seismic evaluations for erected-scaffolding

were required

by the implementing procedure.

The inspector reviewed

PLP-401

(Ladder, Scaffold,

and

Equipment

Use

and Storage)

and noted specific exclusions for

the erection of scaffolding over redundant safety trains

simultaneously.

The intent of this step

was to prohibit the,

loss of both safety trains due solely to the failure of

scaffolding.

Regulatoi y Guide 1.29 discusses

the "two-over-

one" situation where nonsafety-related

structures

whose

continued function is not required,

but whose failure could

reduce the functioning of any safety-related

equipment,

should

be seismically designed

and constructed.

The

inspector

noted that procedure

PLP-401 did not require

a

seismic evaluation of erected scaffolding over safety-

related

components;

particularly when scaffolding is erected

over the only available train of safety-related

systems,

as

was the case

on May 19.

The inspector related this concern to licensee

management,

who concurred with the inspectors

comments

and directed

a

seismic evaluation

be performed for the "A" RHR and

- containment

spray

pump room.

This evaluation

concluded that

the scaffolding would not damage safety-related

components

during

a seismic event.

While the evaluation yielded favorable results for the

scaffolding erected

over the "A" RHR system,

the inspectors

concluded that the licensee's

controls over this situation

were weak, in that the evaluation

should

have

been

done

prior to the removal of the "B" RHR system from service

on

Nay 19.

The inspectors

noted that the licensee

has taken

administrative

measures

to ensure that scaffolding is

no'onger

erected

over safety-related

equipment until the

procedure is enhanced

to include better controls.

The inspectors

found plant housekeeping

and material condition of

components

to be satisfactory.

The licensee's

adherence

to

radiological controls, security controls, fire protection

requirements,

and

TS requirements

in these

areas

was satisfactory.

Review of Nonconformance

Reports

Adverse Condition Reports

(ACR) were reviewed to verify the

following:

TS were complied with, corrective actions

and generic

items were identified and items were reported

as required

by

10 CFR 50.73.

(2)

ACR 93-220 reported that the electrical

containment

penetration for the Integrated

Reactor Vessel

Head

(IRVH)

bridge hoist was not provided with a secondary

overcurrent

protection device

as specified in plant control wiring

drawings. 'uring

a walkdown of these circuit breakers

used

to provide overcurrent protection

on Hay 25,

1993, the

licensee

discovered that only one breaker provided power to

the bridge hoist located inside containment.

The other

breaker

specified

on the dr awings

was found to be

disconnected

from the circuit.

When notified of this

condition, plant operators

deenergized

the circuit by

establishing

an equipment clearance

in accordance

with TS 3.8.4.l.a.

The inspector verified the clearance

tagout in

the field.

Although the tags were found to be on the

specified

components,

the inspector noted that

one of the

breakers. which were tagged

(1D12-7BR) was labeled

as

a

"spare" instead of a power source for the bridge hoist.

This spare

breaker coincided with the one which was not

terminated to the circuit.

The licensee's

investigation

into this matter concluded that this wiring deficiency

had

existed since initial plant construction.

The licensee

has experienced

previous

problems with these

types of electrical penetrations.

On Harch 14,

1990,

licensee

personnel

discovered

a discrepancy

in the amperage

rating for a circuit breaker providing overcurrent

protection.

The licensee

issued

LER 90-08 reporting this

condition.

The corrective actions associated

with this

LER

included

a review of the calculations of similar circuits

. and

a field verification that breakers

used

as protection

, devices

were properly identified/verified.

These actions

were completed in Nay 1991.

This matter was considered

to

be

a licensee identified violation in NRC Inspection

Report

50-400/90-06

(NCV 400/90-06-01).

Although the condition reported

by ACR 93-220 was identified

by the licensee,

corrective actions

performed for the

previous deficiency should

have identified the labeling

problem for breaker

1D12-7BR and the inability of this

secondary

breaker to perform its function.

Therefore, this

matter is considered

to be

a violation of TS 3.8.4.a.

Violation (400/93-12-01):

Failure to maintain the

IRVH

bridge hoist electrical

containment penetration

conductor

overcurrent protective device operable.

ACR 93-205 reported that on Hay 17,

1993, the

RAB normal

exhaust

fan E-18 could not be secured

from the control

switch in the main control room.

Auxiliary operators

noted

locally that the fan's circuit breaker

was still closed

and

an electrical

burning smell

was present.

The breaker

subsequently

automatically tripped open after two

unsuccessful

manual

attempts.

Troubleshooting of this Asea

Brown Boveri LK-16 circuit breaker revealed that the trip

coil had burned

up and the breaker

had mechanically

bound in

the, closed position.

Although this application of the LK-16

breaker

was in nonsafety-related

equipment,

many safety-

related

components

receive electrical

power through

LK-16

breakers.

Several

previous failures of these

types of breakers

have

occurred in the past.

As reported in LER 92-09,

a failure

of the E-18 supply breaker contributed to a reactor trip on

July 15,

1992.

As mentioned in NRC Inspection

Reports

50-

400/92-26,

50-400/92-13,

and 50-400/90-13,

the licensee

has

performed

numerous corrective actions to improve breaker

reliability including breaker

physical modifications

(PCR-

3510,

480 volt Drawout Breakers

used

as Contacters)

and

periodic preventive maintenance

checks.

Although this

action reduced

the number of breaker failures, additional

failures

have occurred

even

on the modified breakers

(the E-

18 breaker

had

been previously modified in November 1990).

The licensee

plans to replace this switchgear beginning in

the next refueling outage

scheduled for March 1994

(PCR-

6526,

Frequently Cycled

LK Breakers;

PCR-6714,

Frequently

Cycled Non-Safety

LK Breakers;

PCR-6715, Train "B" Load

Centers

LK Breakers

Replacement;

and

PCR-6896,

Non-Safety

Train "B" and General

Services

Bus Section

1 Breaker

Replacement).

Until then the licensee

developed

interim

corrective action.

The licensee

determined that

a

significant number of the failures were from a few heavily

cycled breakers.

These

breakers

are being identified and

"retired".

In addition, the preventive maintenance

frequency for the heavily cycled breakers will be increased

to ensure

breaker reliability.

On May 30,

1993, while attempting to deenergize

nonsafety-

related

MCC 1-481 to perform LK-16 circuit breaker

modifications per PCR-3510, plant operators

could not open

the 480 volt feeder breaker for this bus.

Alternatively,

the operators

opened

the corresponding

6.9

KV supply breaker

to the

MCC.

Troubleshooting of this Asea

Brown Boveri LK-42

feeder breaker revealed similar problems to those

found on

the LK-16 circuit breakers.

The breakers

are very similar

in design.

The licensee

had already increased

the scope of

modification PCR-3510 to include all the

LK breakers (i.e.,

LK-8, LK-16, LK-25, LK-32 and LK-42).

Approximately 200 of

the

243

LK circuit breakers

have

been modified.

The

modification was subsequently

performed

on this feeder

breaker.

The failure of this circuit breaker differ ed from

previous failures in that the feeder breaker did not

experience

many cycles

and was not anticipated to exhibit

the

same

problems

as the heavily cycled breakers.

As

discussed

in paragraph

6, another failure mechanism for LK

breakers

involves the closing coils.

The inspectors will

continue to monitor the licensee's

progress

in correcting

these

breaker problems.

ACR 93-237 reported that the lock for the circuit breaker

for valve 1CT-95, Containment

Spray

Pump

1B-SB Recirculation-

Valve, was not installed

as required

by Operations

Management

Manual procedure

OMM-011, Control of Locked

Valves.

Valve 1CT-95 is

a

normally closed motor-operated

containment isolation valve whose breaker is required to be

locked/off during normal plant operating conditions,

as

described

in the plant

FSAR. 'uring performance of

surveillance

procedure

OST-1119,

Containment

Spray

Operability Train

B quarterly Interval,

on June

2,

1993,

operators

were required to remove the lock and close the

breaker.

This would allow for the manipulation of valve

1CT-95 to support surveillance testing of the "B"

containment

spray

pump.

Section 7.3, step

48 of the

procedure

requires

operators

to turn off and lock the

breaker to valve

1CT-95 following the

pump test.

There are

two sign-off steps

in the procedure for this action,

one for

the operator performing the step

and another for an

independent verifier.

Interviews with'he involved

personnel

revealed that while performing the step,

the

operator turned the breaker off but failed to re-install the

lock as required.

Additionally, both sign-off steps

were

initialed by the operator

and the independent verifier

indicating that the lock had

been installed

and verified to

be in place.

The individuals involved indicated that the

error was due to oversight

and that they simply did not read

the procedure

step completely.

The inspectors

concluded

that this was not

a case of record falsification.

While this incident was identified by the licensee, it is

the latest of several

examples of plant performance

where

either self-checking or independent verification were

lacking.

On April 28,

1993, operations

personnel

went to

the wrong breaker cubicle during efforts to swap safety

trains.

This resulted in an inadvertent start of the "B"

CCW pump.

In the past,

NRC violations have

been

issued

(Violations 400/91-27-01

and 400/91-09-01) for incidents

involving inadequate

self-checking or independent

verification.

One involved a mispositioned

NI comparator

switch which rendered

the

gPTR alarm inoperable in January

1992.

The other involved instrument process

tubing for,a

differential pressure

switch in the

EDG fuel oil system,

which was neither

reconnected

nor properly verified to be

connected prior to returning the instrument to service in

April 1991.

This latest

example involving the failure to

properly implement procedure

OST-1119 is contrary to the

requirements 'of TS 6.8.l.a

and is being cited because

violations have

been previously identified by both the

NRC

and the licensee

in the areas of procedural

adherence

and

independent verification, indicating

a need for additional

management

attention in those

areas.

Violation (400/93-12-02):

Failure to properly implement

plant procedures

as required

by TS 6.8. I.a.

3.

Surveillance Observation

(61726)

Surveillance tests

were observed to verify that approved

procedures

were

being used; qualified personnel

were conducting the tests;

tests

were

adequate

to verify equipment operability; calibrated

equipment

was

utilized;

and

TS requirements

were followed.

The following tests

were

observed

and/or data reviewed:

OST-1007

OST-1039

OST-1079

OST-1081

HST-I0137

HST- I0138

HST- I0151

EST-222

EPT-126T

CVCS/SI System Operability quarterly Interval

Calculation of quadrant

Power Tilt Ratio, Meekly

Interval

(With Alarm Operable)

Containment Isolation Valves ISI Test quarterly

Interval

Containment Visual Inspection

When Containment

Integrity is Required

Hain Steam/Feedwater

Flow Loop 2 (F-0485/F-0486)

Operational

Test

Hain Steam/Feedwater

Flow Loop 3 (F-0494/F-0497)

Operational

Test

Steam Generator

C Narrow Range

Level

Loop (L-0496)

Operational

Test

Procedure for the Type

B LLRT of the Personnel

Air

Lock Barrel

Turbine Volumetric Test

4.

The performance of these

procedures

was found to be satisfactory with

proper

use of calibrated test equipment,

necessary

communications,

established,

notification/authorization of control

room personnel,

and

knowledgeable

personnel

having performed the tasks.

The inspectors

noted good use of the plant simulator for performing practice runs

on

procedure

EPT-126T.

", This allowed operators

to smoothly execute

the

actual test,

which was

an infrequently used procedure that had the

potential for introducing unwanted plant transients if not performed

correctly.

No violations or deviations

were observed.

Haintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify that

correct equipment clearances

were in effect; work requests

and fire

prevention work permits were issued

and

TS requirements

were being

followed.

Haintenance

was observed

and work packages

were reviewed for

the following maintenance activities:

~

Preventive

maintenance

on the startup transformer feeder breaker

to auxiliary bus

1E (breaker

121) in accordance

with procedure

PH-

E006,

6.9

KV 3000

Amp Air Circuit Breaker

PM.

~

Repair nitrogen leak on the actuator for the "A" main feedwater

isolation valve

1FW-159 in accordance

with procedure

CM-H0059,

Feedwater

Isolation Valve Actuator Disassembly

and Maintenance,

Pilot Check Valve Shim Replacement

and Fill/Bleed Procedure.

~

Replacement

of bent yoke that actuates circuit breaker

122

mechanism

operated cell switch.

~

Troubleshooting/calibration

of the nitrogen pressure

switch for

the "C" main feedwater isolation valve

1FW-217 in accordance

with

procedure

PIC-I100,

Pressure

and Differential Pressure

Switch

Inspection

and Calibration.

~

Repair of the "A" steam generator

blowdown flow control valve

1BD-

8 in accordance

with procedure

CM-H0033,

ITT 'Hamel

Dahl

V500

Series

Cage Trim Valves Disassembly

and Maintenance.

4

~

Troubleshooting

the failure of the "B" chilled water

pump breaker

to close in accordance

with procedures

EPT-033,

Emergency

Safeguards

Sequencer

System Test,

and

PH-E0012,

480

VAC Load

Center Breaker

and Cubicle

PH.

The performance of work was satisfactory with proper documentation of

removed

components

and independent verification of the reinstallation.

No violations or deviations

were identified.

Safety Systems

Walkdown (71710)

The inspector

conducted

a walkdown of portions of the fire protection

system to verify that the lineup was in accordance

with license

requirements

for system operability and that, the system drawing and

procedure correctly reflected "as-built" plant conditions.

The inspector noted that the material condition of components

in the

valve pit area adjacent to the motor driven fire, pump was poor.

The

corresponding

area near the diesel

engine driven fire pump was in a much

better material condition.

The inspector discussed this observation

with licensee

personnel

and discovered that efforts were already

underway to upgrade

the material condition of the motor driven fire pump

components

as

had been recently done to the engine driven fire pump

components.

r

From a review of plant drawings the inspector

noted that no drawing

existed for the fuel oil supply tank and delivery system to the diesel

engine driven fire pump.

Although only a few valves existed in this

system

(one flow isolation valve,

one tank drain valve,

and two level

indicator isolation valves),

the inspector considered

the lack of a flow

10

drawing to be unusual.

Licensee

personnel

stated that they would review

this matter to determine if a drawing was appropriate.

No violations or deviations

were identified.

Followup of Onsite Events

(93702)

At 5:32 p.m.,

on Hay 23,

1993, the

1B-SB emergency

bus

was inadvertently

deenergized

which caused

an automatic start of the "B" emergency diesel

generator.

A power increase

was in progress

follow'ing the outage.

When

operators

attempted to transfer

AC electrical

power from the Startup

Transformers

(SUT) to the Unit Auxiliary Transformers

(UAT) a circuit

breaker malfunctioned which caused auxiliary bus lE to be supplied from

both the

UAT and

SUT.

Operators

proceeded

to manually open the

SUT

feeder breaker

(121) to restore

the electrical lineup to the desired

configuration.

The auxiliary contacts

associated

with the

UAT feeder

breaker

(122) were not properly engaged

due to a damaged

actuating

mechanism

and provided

a false breaker

open signal to the

1B-SB

emergency

bus feeder breaker

(125)

even though breaker

122 was actually

closed.

When breaker

121 was manually opened,

feeder breaker

125 was

provided with open signals

from both breakers

121'nd

122 and

automatically

opened

as designed.

This action deenergized

the

1B-SB

emergency

bus

and the emergency diesel

generator

started

on

a low bus

voltage signal.

Haintenance

was performed

on breaker

122 to replace the

actuating

mechanism for the auxiliary contacts

which were found to be

bent.

The licensee

believes

the damage to the actuating

mechanism

occurred

when the breaker

was previously racked in during the October

1992 refueling outage.

At 7:54 a.m.,

on Hay 24, the emergency diesel

generator

was secured

and the electrical distribution lineup returned to

the desired configuration with the

UAT supplying auxiliary bus lE.

During this event,

the auxiliary feedwater

system actuated

as designed

and

a containment ventilation isolation signal

was generated

due to

losing power to the containment

system radiation area monitors.

With

the exception of the "B" chilled water

pump which failed to start, plant

equipment

operated

properly.

The licensee

investigated

the problem and

determined that the closing coil on the LK-16 circuit breaker for this

pump had failed.

The closing coil was subsequently

replaced

and the

pump was tested satisfactory.

The licensee

has experienced

several

previous

problems with proper

engagement

of 6.9

KV breaker

secondary

contacts.

As discussed

in NRC

Inspection

Report 50-400/92-04,

closing problems

have

been identified

for these

types of breakers.

On October 1,

1988,

a similar event to

this one occurred.

While in a refueling outage,

power was inadvertently

interrupted to the lA-SA emergency

bus during an attempt to realign-the

electrical distribution system to backfeed electrical

power through the

main transformers.

In this event the

SUT feeder breaker to auxiliary

bus

1D failed to open

when the

UAT feeder breaker

was closed.

'When

operators

manually opened the

SUT feeder breaker the

1A-SA feeder

breaker automatically

opened

and deenergized

the emergency

bus.

Troubleshooting for this condition also revealed that the actuating

mechanism for the auxiliary contacts

on the

UAT feeder breaker

were

bent.

Corrective action to prevent recurrence of this event included

a

repair to the actuating

mechanism,

and procedural

guidance

provided to

operators

to prevent actuating

mechanism

damage

when racking 6.9

KV

breakers

into the connected position.

Operating procedure

OP-156.02,

AC

Electrical Distribution,

wa's revised to provide

a note alerting

operators

to visually ensure that the cell switch is properly aligned

with the actuating

mechanism.

The failure to properly implement procedure

OP-156.02 (i.e., verify the

alignment of the circuit breaker actuating

mechanism with the cell

switch when the breaker

was placed into service during the previous

refueling outage)

is contrary to the requirements

of TS 6.8. l.a and is

considered to be another

example of the violation discussed

in paragraph

2.c.(3) of this report.

Outage Activities (71707)

Hajor work performed during this planned

outage

included repairs to

steam generator

blowdown valve IBD-8, oil addition to the "B" reactor

coolant

pump, repair, of nitrogen leaks

on the operators for valves

1FW-

159 and

1FW-217, replacement of the motor for the "A" heater drain pump,

and repair of through-wall leaks

on the seal

water supply piping for the

"B" condensate

booster

pump.

As mentioned in

NRC Inspection

Report 50-400/93-08,

containment

sump

inleakage

had increased

and

a temporary modification had

been installed

to valve

1BD-8 to backseat

the valve and reduce

secondary

system

inleakage to the

sump.

During this inspection period,

a gradual

increase

in sump inleakage

occurred.

Licensee

management

decided to

take the unit off line and repair this valve prior to the upcoming

summer peak load period.

Significant planning activities included the use of a spare

"mockup"

valve

and actuator for the lBD-8 work and

a spare reactor, coolant

pump

motor for the oil addition.

The simulator was uti'iized to provide

operators

with unit shutdown

and startup training,

as well as potential

transients

which could be expected

during these plant evolutions (i.e.,

feedwater transient

and premature reactor criticality).

The inspector

found this pre-planning to be effective and the actual evolutions were

performed without mishap.

Additional activities performed

by the licensee

during the outage

included

a containment visual inspection to identify fibrous air filters

or other sources of fibrous material in accordance

with NRC Bulletin 93-

02, Debris Plugging of Emergency

Core Cooling Suction Strainers,

and

a

visual inspection of the reactor coolant pressure

boundary for boric

acid leakage.

No fibrous material

and only minor boron residue

was

found.

Work tickets were generated

to correct the boric acid leakage

during the next refueling outage.

12

The inspector

requested

the documented

inspection results for the boric

acid leakage

inspection.

The inspector

was informed that the results

were not well documented.

Procedure

PLP-600,

Boron Corrosion

Program,

and inspection

procedure

OPT-1519,

Containment Visual Inspection for

Boron Leakage

Every Outage

Shutdown, specified that

a walkdown

inspection

be performed prior to cooldown in Hode 3.

Since

a plant

cooldown was not commenced,

the inspection procedure,

which included

an

attachment

specifying areas

to be inspected

and results,

was not

implemented.

After the inspector discussed this matter with licensee

management,

the data sheets

were filled out with the results for the

areas

inspected.

The inspector considered

the licensee's

documentation

of the boric acid leak inspection to be poor.

Adverse Weather Operations

(71707)

On June 4,

1993,

a tornado warning was issued for Wake County.

The

inspector reviewed the licensee's

preparations

performed in response

to

this warning.

No tornadoes

approached

the plant

and

no plant damage

occurred during the adverse

weather conditions.

The inspector reviewed

the provisions contained in the licensee's

emergency

plan for handling

these situations

and also reviewed procedure

AP-301, Adverse Weather

Operations.

The licensee's

emergency

plan requires

the declaration of

an Unusual

Event if a tornado crosses

the exclusion area

boundary,

and

if sustained

wind speeds

exceed

90

HPH then

an

ALERT would be declared.

If a tornado

impacts the power block and sustained

winds exceed

100

HPH

then

a site emergency

would be declared.

Procedure

AP-301 contains

provisions to ensure

the plant is placed in hot standby

(Hode 3) at

least

two hours prior to the anticipated arrival of sustained

winds in

excess

of 73 HPH.

For the tornado warning issued

on June 4, loose

material

was

removed from exposed

areas,

acc'ess

doors closed,

safety

lines fixed,

and emergency

equipment

was verified to be available.

The

inspector

found that the licensee's

emergency

plan and procedures

were

properly implemented.

Review of Licensee

Event

Repo} ts (92700)

The following LERs were reviewed for potential generic

impact, to detect

trends,

and to determine whether corrective actions

appeared

appropriate.

Events that were'reported

immediately were reviewed

as

they occurred to determine if the

TS were satisfied.

LERs were reviewed

in accordance

with the current

NRC Enforcement Policy.

a ~

(Open)

LER 93-05:

This

LER reported

an entry into TS 3.0.3

on

April 28,

1993 during an in-service stroke test

on two CSIP

discharge

cross

connect valves.

As discussed

in NRC Inspection

.

Reports

50-400/93-08

and 50-400/93-10,

the "B" CSIP rotating

assembly

was replaced following a shaft failure.

Following the

return to service for this pump, valves'CS-218

and

1CS-220 were

stroke tested to satisfy

IST requirements.

These valves isolate

the "A" CSIP from the normal high head safety injection flow path

when closed.

The valves'troke

times were approximately ten

seconds

each

and they were closed for a total of less than

one

13

b.

minute.

On April 29, it was determined that the "B" CSIP had not

yet been demonstrated fully operable

and that both

ECCS flow paths

were inoperable for the seconds

that the valves were closed.

This

constituted

a TS 3.0.3 entry.

The "C" CSIP was subsequently

placed into service

and the

"B", CSIP was declared

inoperable.

The licensee attributed this event to several

causes,

all stemming

from personnel

error.

Inadequate

evaluation

and review of the "B"

CSIP test data coupled with a lack of understanding

on the use

and

restrictions of the

JCO process

were cited as reasons

for the

premature declaration of the

pump to be operable.

The licensee

will train appropriate plant personnel

on this event

and the

proper

use of JCOs,

Engineering Evaluations,

Technical

Specifications,

and other processes

applicable to this event.

Additionally, the "B" CSIP will now remain inoperable until

conditions permit full flow testing to verify the pump's ability

to meet vendor

and

TS runout limits.

This

LER will remain

open

pending completion of the above actions.

(Open)

LER 93-06:

This

LER reported

two separate

incidents

where

the requirements

of TS 4. 11. l. 1. 1 were not met.

Specifically,

on

Hay 17 and Hay 31,

1993, it was determined that the automatic

sampling device

on the Secondary

Waste

Sample

Tank

(SWST) effluent

line had malfunctioned during releases

from the

SWST.

Technical

Specification'.11. 1.1.1 requires

continuous

sampling of the

SWST

effluent during releases

to provide

a weekly radioactivity

composite.

The composite

sample

would be used

as

a backup to the

normal radiation monitor in the event it became

inoperable.

This

composite

sample is typically discarded

when the radiation monitor

is operable.

In both instances

the

SWST releases

were immediately

secured

and the in-line radiation monitor was used to verify that

no detectable

levels of radioactivity existed.

The sampling device malfunctions were caused

by a failure in, the

unit's electronic counter .

After the second failure, the licensee

consulted with the vendor who attributed the cause of both

failures to inadequate

surge protection in the counter

power

supply.

Immediate corrective actions

were taken to replace the

automatic

sampling device with a modified version which included

enhanced

surge protection for the counter power supply.

Long-term

corrective actions

are to include developing test procedures

to

more thoroughly test

or calibrate the composite

sampling units.

This

LER will remain

open pending completion of the procedure,

development.

10.

Licensee Action on Previously Identified Inspection

Findings

(92702

K

92701)

(Closed)

URI 400/93-10-01:

Review calculations

and licensee

actions

regarding the seismic qualification of AFW piping.

0

14

As discussed

in NRC Inspection Report 50-400/93-10,

the inspectors

identified two valves in the

AFW system,

1AF-5 and lAF-24, which

appeared

to be installed without adequate

supports.

These two-inch

motor-operated

valves are in the recirculation lines from the two motor-

driven

AFW pumps to the condensate

storage

tank..

The valve bodies

are

installed horizontally in the piping with big Limitorque motor operators

attached

to their sides.

The motor operators

had

no additional

supports

other than the small two-inch piping,

and

seemed

to impose

a significant

bending

moment

on that piping.

The inspectors

brought this observation

to the licensee's

attention

who researched

the original design

calculations for that section of piping and discovered

a modeling error

in the centers of gravity for the two valves.

Specifically, Stress

Analysis Calculation 71-1,

"AF Piping From Mass Points

66 and 453 at

Floor (flevation 261') to Steam Generator Auxiliary Feedwater

Pumps

Discharge

Nozzles

and Anchor Point 4903 at Wall", incorrectly applied

the mass of the composite valve body/motor operator

assemblies

at the

center of gravity of the valve bodies

themselves

for valves

lAF-5 and

IAF-24, and not at the cente} of gravity of the composite valve

assemblies.

Stress

calculations resulting from this modeling error

incorrectly yielded stress

figures which wer e within the design

basis

allowable stress criteria as referenced

in the

FSAR, Table 3.9.3-11.

Recalculations

of the actual

pipe stresses

imposed

by the unsupported

motor operators yielded stress

values of approximately

33 ksi.

This

figure exceeded

the allowable value for the emergency condition (which,

as defined

by FSAR Table 3.9.3-7,

included the safe

shutdown earthquake

in its loading combination)

by 6 ksi.

This rendered that section of the

seismic class I AFW system outside of its original design allowable

str ess limits.

Upon discovering this, the licensee

performed

an

immediate operability determination

as allowed by the guidelines of NRC Generic Letter 91-18, "Information to Licensees

Regarding

Two NRC

Inspection

Manual Sections

on Resolution of Degraded

and Nonconforming

Conditions

and

on Operability" and the licensee's

own Design Guide No.

DG-II.20,

Design Guide for Civil/Structural Operability Reviews".

The

design guide incorporated

more recent rules for calculating .stress

limits as specified in Appendix

F of the Appendices to ASME Boiler &

Pressure

Vessel

Code,Section III, 1986 edition.

Specifically,

a stress

limit of two times the material yield stress. of 36 ksi, or 72 ksi, could

be used in determining the short-term structural integrity of the

AFW

recirculation piping.

Based

on the actual

stresses

being calculated at

33 ksi, the system

was considered

operable in the short-term.

Stress

Analysis Calculation 71-1, which contained

the center of gravity

modeling error was originally developed in 1974 by the plant,'s architect

engineer.

The calculation received

reviews by the licensee

in 1986 in

accordance

with the guidelines established

in NRC Bulletin 79-14,

"Seismic Analyses for As-Built Safety-Related

Piping Systems"..

However,

those reviews failed to identify the modeling'rror which resulted in

that section of AFW piping being outside of its design basis.

The

failure to perform adequate

measures

to ensure

the accuracy of design

with respect to this seismic class I system is considered to be

a

violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control.

15

Violation (400/93-12-03):

Failure to establish

adequate

measures

to

verify that designs

were technically accurate

with respect to the design

basis for the

AFW system.

In accordance

with the requirements

of NRC Generic Letter 91-18 and the

licensee's

design guide,

an engineering evaluation which will document

the current,

short-term operable condition,

as well as

a modification

which will restore the system to long-term acceptable

status,

are being

developed

by the licensee.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted in paragraph

1) at the conclusion of the inspection

on June

21,

1993.

During this

meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violations addressed

below.

The licensee representatives

acknowledged

the inspector's

comments

and did not identify as

proprietary

any of the materials

provided to or reviewed

by the

inspectors

during this inspection.

No dissenting

comments

from the

licensee

were received.

Item Number

Descri tion and Reference

400/93.-12-01

400/93-12-02

400/93-12-03

Acronyms

and Initialisms

VIO:

Failure to maintain the

IRVH bridge

hoist electrical

containment. penetration

conductor overcurrent protective device

operable,

paragraph 2.c.(l).

VIO:

Failure to properly implement plant

procedures

as required

by TS 6.8.l.a.,

paragraphs

2.c.(3)

and 6.

VIO:

Failure to establish

adequate,

measures

to verify that designs

were

technically accurate with respect to the

design basis for the

AFW system,

paragraph

10.

ACR

AFW

AP

ASNE

CCW

CFR

CSIP

CVCS

ECCS

EDG

EPT

Adverse Condition Report

Auxiliary Feedwater

Administrative Procedure

American Society of Hechanical

Engineers

Component Cooling Water

Code of Federal

Regulations

Charging Safety Injection

Pump

Chemical

Volume Control System

Emergency

Core Cooling System

Emergency Diesel Generator

Engineering

Performance

Test

EST

ESW

FSAR

HVAC

IRVH

ISI

IST

JCO

KV

KSI

LER

LLRT

HCC

HPK

NCV

NRC

OPT

OST

PCR

PLP

PH

QPTR

RAB

RHR

SI

SUT

SWST

TS

UAT

URI

VAC

VIO

16

Engineering Surveillance Test

Emergency Service Water

Final Safety Analysis Report

Heating, Ventilation and Air Conditioning

Integrated

Reactor

Vessel

Head

Inservice Inspection

Inservice Testing

Justification for Continued Operation

Kilovolt

Kilopounds per square

inch

Licensee

Event Report

Local Leak Rate Test

Hotor Control Center

Miles Per Hour

Non-Cited Violation

Nuclear Regulatory

Commission

Operations

Performance

Test

Operations

Surveillance

Test

Plant

Change

Request

Plant Procedure

Preventive

Maintenance

Quadrant

Power Tilt Ratio

Reactor Auxiliary Building

Residual

Heat

Removal

Safety Injection

Startup Transformers

Secondary

Waste

Sample

Tank

Technical Specification

Unit Auxiliary Feedwater

Unresolved

Item

Volt Alternating Current

Violation