ML18010A964

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Insp Rept 50-400/92-27 on 921024-1120.Violation Noted.Major Areas Inspected:Plant Operations,Radiological Controls, Security,Fire Protection,Surveillance Observation,Maint Observation,Design Changes & Mods & Outage Activities
ML18010A964
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 12/08/1992
From: Christensen H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010A962 List:
References
50-400-92-27, NUDOCS 9212290074
Download: ML18010A964 (18)


See also: IR 05000400/1992027

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,G EDR G IA 30323

M. Shanno

dent Inspector

Approved by:

H

Chri tensen,

Section Chief

Division of Reactor Projects

Report No.:

50-400/92-27

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Condu

d:

October

24 - November 20,

1992

Inspectors:

J.

Tedrow,

Seni

Resident

Inspector

Licensee

No.:

NPF-63

D

e

i ned

/4

D te Signed

/2 g gz

Da e

igned

SUMMARY

Scope:

This routine inspection

was conducted

by two resident

inspectors

in the areas

of plant operations,

radiological controls, security, fire protection,

surveillance observation,

maintenance

observation,

design

changes

and

modifications,

outage activities, refueling activities, safety system

walkdown, licensee

event reports

and licensee

action

on previous inspection

items.

Numerous facility tours were conducted

and facility operations

observed.

Some of these tours

and observations

were conducted

on backshifts.

Results:

One violation with three

examples

was identified:

Failure to properly

establish/implement

plant procedures,

paragraphs

2.c.(2), 3.a,

and 3.b.

Two non-cited violations were identified:

Failure to obey

a radiography

posting,

par agraph 2.c.(1);

and failure to properly move fuel in accordance

with fuel transfer data sheets,

paragraph

8.b.

A weakness

was identified regarding

implementation of the equipment clearance

program,

paragraph

2.a.

92i2290074 92i208

PDR

ADOCK 05000400

Q

PDR

2

A weakness

was also identified regarding

temporary test procedure

adequacy,

paragraph

3.c and 5.

Another weakness

was identified regarding the reviews performed for the fuel

transfer data sheets,

paragraph

S.a.

,

Persons

Contacted

REPORT DETAILS

Licensee

Employees

  • J. Collins, Manager,

Operations

  • J. Cribb, Manager, guality Control

C. Gibson,

Manager,

Programs

and Procedures

  • C. Hinnant,

General

Manager,

Harris Plant

D. Knepper,

Project Engineer,

Nuclear Engineering

Dept.

B. Meyer,

Manager,

Environmental

and Radiation Monitoring

  • T. Morton, Manager,

Maintenance

J. Moyer, Manager,

Project Assessment

  • J. Nevill, Manager,

Technical

Support

C. Olexi k, Manager,

Regulatory

Compliance

A. Powell,

Manager,

Harris Training Unit

  • W. Seyler,

Manager,

Outages

and Modifications

H. Smith,

Manager,

Radwaste

Operation

  • G. Vaughn,

Vice President,

Harris Nuclear Project

W. Wilson, Manager,

Spent Nuclear Fuel

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

2.

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Review of Plant Operations

(71707)

The plant began this inspection period in the defueled condition.

On

October 30,

1992, refueling operations

(Mode 6) were

commenced.

The

core

was reloaded into the reactor vessel

at 5: 19 a.m.

on November 3.

At 10:55 p.m.

on November

12, the reactor vessel

head

studs

were

tensioned

and the plant entered

the cold shutdown

(Mode 5) condition.

The plant remained

in cold shutdown for the duration of this inspection

period.

a ~

Shift Logs and Facility Records

The inspector reviewed records

and discussed

various entries with

operations

personnel

to verify compliance with the Technical

Specifications

(TS)

and the licensee's

administrative procedures.

The following records

were reviewed:

Shift Supervisor's

Log;

Outage Shift Manager's

Log; Control Operator's

Log; Night Order

Book; Equipment Inoperable

Record; Active Clearance

Log; Grounding

Device Log; Temporary Modification Log; Chemistry Daily Reports;

Shift Turnover Checklist;

and selected

Radwaste

Logs.

In

addition, the inspector

independently verified clearance

order

tagouts.

The inspectors

found the logs to be readable,

well organized,

and

provided sufficient information on plant status

and events.

Licensee

personnel

identified several

deficiencies related to

equipment

clearances

during this refueling outage.

Although the

deficiencies

were all minor, they involved several different

aspects

of generating

and removing equipment clearances

including:

miscommunication,

improper clearance

tag installation,

improper

initial positioning of tagged

components,

subsequent

operation of

tagged

components,

removal of tagged

components

from a system,

and

premature

clearance

removal prior to work completion.

Although

none of these deficiencies resulted

in safety-related

equipment

damage

or personnel

injury, they indicated

a potential

problem

which could have serious

consequences if not corrected.

The

inspector identified six different ACR's related to equipment

clearance

problems

and questioned

licensee

personnel if an adverse

trend

had

been identified.

Although an adverse

trend

had not

previously

been identified, licensee

personnel

reviewed the ACR's

identified by the inspector

and agreed that

an adverse

trend

was

indicated.

During the previous refueling outage

an adverse

trend regarding

equipment clearance utilization was also identified.

An

evaluation of this trend identified

a lack of verbatim compliance

with the clearance

procedure

as the root cause.

The licensee

implemented corrective actions,

such

as procedural

revisions

and

training, in an effort to reverse

the trend.

These actions

were

not sufficient to preclude the events

which resulted

in the ACR's

identified during this assessment

period.

The licensee

has

concluded that additional

measures

are

needed to prevent

recurrence

of these

types of problems.

The licensee is presently

investigating these

events to determine appropriate corrective

action.

The inspector will review the licensee's

corrective

action regarding

equipment clearance

problems

under violation

400/92-27-02,

(paragraph 2.c.(2)).

Since the inspector

had to prompt the adverse

trend declaration

by

the licensee,

the corrective action trending program

was

considered

to be weak in this case.

Facility Tours

and Observations

Throughout the inspection period, facility tours were conducted

to

observe

operations,

surveillance,

and maintenance activities in

progress.

Some of these

observations

were conducted

during

backshifts.

Also, during this inspection period, licensee

meetings

were attended

by the inspectors

to observe

planning

and

management activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence;

control

room;

emergency diesel

generator building; reactor

auxiliary building; reactor containment building; waste processing

building; turbine building; fuel handling building; emergency

service water building; battery rooms; electrical

switchgear

rooms;

and the technical

support center.

During these tours,

the following observations

were made:

(4)

Monitoring Instrumentation

- Equipment operating status,

area

atmospheric

and liquid radiation monitors, electrical

system lineup, reactor operating

parameters,

and auxiliary

equipment operating

parameters

were observed to verify that

indicated parameters

were in accordance

with the

TS for the

current operational

mode.

Shift Staffing - The inspectors verified that operating

shift staffing was in accordance

with TS requirements

and

that control

room operations

were being conducted

in an

orderly and professional

manner.

In addition, the inspector

observed shift turnovers

on various occasions

to verify the

continuity of plant status,

operational

problems,

and other

pertinent plant information during these turnovers.

Plant Housekeeping

Conditions

- Storage of material

and

components,

and cleanliness

conditions of various

areas

throughout the facility were observed to determine

whether

safety and/or fire hazards

existed.

Radiological Protection

Program

- Radiation protection

control activities were observed routinely to verify that

these activities were in conformance with the facility

policies

and procedures,

and in compliance with regulatory

requirements.

The inspectors

also reviewed selected

radiation work permits to verify that controls were

adequate.

The licensee

started early boration of the

RCS during plant

shutdown to lower the

PH chemistry.

This action

was

intended to dissolve corrosion products

so they could

be

removed

by the purification system.

Hydrogen peroxide

was

then

added to aid in corrosion product removal.

This

process

was effective in lowering the dose rate in several

RCS pipe locations

and resulted

in approximately

700 curies

of corrosion products

being removed.

Security Control

- The performance of various shifts of the

security force was observed

in the'conduct of daily

activities which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and retrieval; escorting of visitors;

patrols;

and compensatory

posts.

In addition, the inspector

observed

the operational

status of closed circuit television

monitors,

the intrusion detection

system in the central

and

secondary

alarm stations,

protected

area lighting, protected

and vital area barrier integrity,

and the security

organization interface with operations

and maintenance.

(6)

Fire Protection

- Fire protection activities, staffing and

equipment

were observed to verify that fire brigade staffing

was appropriate

and that fire alarms,

extinguishing

equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

The inspectors

found plant housekeeping

and material condition of

safety related

components

to be good.

The licensee's

adherence

to

radiological controls, security controls, fire protection

requirements,

and

TS requirements

in these

areas

was satisfactory.

Review of Nonconformance

Reports

Adverse Condition Reports

(ACRs) were reviewed to verify the

following:

TS were complied with, corrective actions

and generic

items were identified and items were reported

as required

by

10 CFR 50.73.

(1)

ACR 92-529 reported that two licensee

employees

had violated

the radiological

boundaries

established

for radiography.

One employee

had intentionally crossed

the radiography

posting

and boundary rope to access

a stairwell.

The other

individual

had attempted to warn the first employee to exit

the area

when they were noticed

by health physics personnel.

The two individuals were then escorted

from the area

and

an

investigation

conducted.

The investigation determined that

the radiography

source

was retracted

during this time frame.

This was confirmed by measuring

the personnel

exposure of

the two individuals (less

than

20 millirem).

The inspector reviewed the licensee's

procedure

governing

this activity, AP-507,

Radiography Guidelines,

and the

training provided to the two individuals before this event.

The inspector determined that appropriate training and

administrative controls

had

been

implemented

before the

event occurred.

The inspector also reviewed radiation

survey records of the radiography

boundary

and found it to

be satisfactory.

The licensee's

corrective action following

the event included terminating

employment of the individual

who intentionally violated the radiography

boundary

and

counseling of the second individual.

The event

was further

discussed

between

the inspector

and regional health physics

experts.

This violation will not be subject to enforcement

action because

the licensee's

efforts in identifying and

correcting the violation meet the criteria specified in

Section VII.B of the Enforcement Policy.

NCV (400/92-27-01):

Failure to obey

a radiography posting.

(2)

ACR 92-570 reported that

on November 6,

1992, the "A"

emergency diesel

generator

experienced

a generator

differential trip when it was started following maintenance.

The licensee's

investigation into this event disclosed that

electrical

grounding straps

were still installed

on the

generator

from previous work.

A review of equipment

clearances

and the grounding device log indicated that the

grounding straps

had

been installed in accordance

with

procedures

AP-024,

Grounding Device Control,

and AP-020,

Clearance

Procedures.

However,

when the equipment clearance

was authorized to be removed,

the grounding straps

had

inadvertently

been left in place.

Procedure

AP-020, step

5.7. 1, requires that installed ground devices

be removed

following maintenance.

Section

6 of the clearance

form had

been

signed indicating that electrical

grounds

had

been

removed

on November 6,

1992,

even though the grounds

were

still in place.

Failure to properly implement procedure

AP-

020 is contrary to the requirements

of TS 6.8. l.a and is

considered

to be

a violation.

(3)

Violation (400/92-27-02):

Failure to properly

establish/implement

plant procedures.

ACR 92-596 reported that

on November ll, 1992, the licensee

discovered

the tubing between

the governor oil booster

and

the "A" emergency diesel

governor

was installed incorrectly.

The governor oil booster provides oil pressure

to fully open

the diesel

generator

fuel racks

on

a diesel start signal,

which helps to decrease

the starting time of the diesel.

Although the "A" diesel

had longer starting times than the

"8" diesel, it was still able to meet its maximum starting

time of 10 seconds.

The tubing was subsequently

connected

to the correct governor port and the diesel

was tested

satisfactorily.

It appeared

that the incorrect tubing

connection

was

made during initial factory installation.

A

review of starting data indicated that with low starting air

flask pressures

the diesel

may not have

been

able to meet

its

10 second starting time requirement

and it appeared

that

previous

slow start valid failures were probably caused

by

the incorrect tubing connection.

Surveillance

Observation

(61726)

Surveillance tests

were observed to verify that approved

procedures

were

being used; qualified personnel

were conducting the tests;

tests

were

adequate

to verify equipment operability; calibrated

equipment

was

utilized;

and

TS requirements

were followed.

The following tests

were

observed

and/or data reviewed:

~ OST-1013

lA-SA Emergency Diesel

Generator Operability Test

Monthly Intervals

~ OST-1091

Containment

Closure Test Weekly Interval During Core

Alterations

and Movement of Irradiated

Fuel

Inside

Containment

~ OST-1817

Refueling Machine (Manipulator Crane) Operability Modes:

100 Hours Prior to Fuel

Movement in Pressure

Vessel

~ OST-1818

Auxiliary Hoist Operability Modes:

All 100 Hours Prior to

Drive Rod Movement in Pressure

Vessel

~ OST-1833T Temporary Procedure for the Completion of OST-1813

(Remote

Shutdown

System Operability,

18 month) Retest

Requirements

~ HST-I0072 Train A 18 Month Annual

Manual Reactor Trip Solid State

Protection

System Actuation Logic

E Master Relay Test

~ HST-I0127 Hain Steam Line Pressure,

Loop

1 (P-0476) Operational

Test

~ HST-I0163 Nuclear Instrumentation

System

Power

Range

N41 Operational

Test

~ HST-I0169 Nuclear Instrumentation

System Source

Range

N31 Operational

Test

~ MST-I0170 Nuclear Instrumentation

System

Source

Range

N32 Operational

Test

~ HST-H0011

Emergency Diesel

Generator

Crankshaft

Web Deflection

and

Thrust Clearance

Check

~ MST-H0014 Emergency Diesel

Generator

Cold Compression

and

Maximum

Firing Pressure

Checks

~ EST-209

Type

B Local

Leak Rate Tests

~ EPT-032T

Component

Cooling Water System

Pressure

Test

~ EPT-146

Emergency Diesel

Generator

Post-Maintenance

Operation

The performance of these

procedures

was found to be satisfactory with

proper use of calibrated test equipment,

necessary

communications

established,

notification/authorization of control

room personnel,

and

knowledgeable

personnel

having performed the tasks.

The local leak rate

tests

on the

RHR valve chambers

were performed following the removal of

mud and debris which was found to have clogged the chamber drain lines.

The tests

were completed satisfactory indicating the drain valves would

have provided satisfactory

pressure

barriers.

'a ~

Following the measurements

taken in accordance

with procedure

HST-

M011, the "A" emergency diesel

was started.

Shortly after

startup,

licensee

personnel

discovered that the cylinder petcocks

had

been left open.

The petcocks

are generally closed during

7

diesel

operation

and opened to check for cooling water inleakage

into the cylinders

when the engine is barred over.

The inspectors

noted that the system engineer

was assisting

the craft in

performance of the engine inspection

and that steps

in procedure

HST-M011 required the engine

be barred over with a hydraulic

device.

When licensee

maintenance

personnel

encountered

resistance

during the engine barring, the system engineer

directed

the petcocks

be opened.

The maintenance

procedure

did not provide

specific guidance for barring the engine.

Subsequently,

the

petcocks

were not returned to the closed position following the

barring.

The inspectors

noted that operating

procedures

contained

clear guidance

on barring the engine which contained

independent

verification that the petcocks

be closed.

However, the operating

procedure

was not implemented

since the barring

had already

been

performed

by operating

personnel

within the previous four hours.

Furthermore,

the inspectors

found that the scope of work performed

on the diesel

engine,

while under

an equipment

clearance,

was not

discussed

between the craft and operating

personnel

to determine

appropriate testing or valve lineups

needed to restore

the engine

to operable status.

This event is considered

to be another

example of the violation discussed

in paragraph

2.c.(2) of this

report.

On November 8,

1992, during the performance of procedure

EST-212

on penetration

H-7,

CVCS Normal

Letdown, approximately

50 gallons

of contaminated

water was spilled in the reactor auxiliary

building.

To pressurize

the penetration,

a local leak rate

monitor was connected

through drain valves

1CS-12

and

1CS-13 which

were opened.

Following the completion of the test,

the system

was

refilled with water by opening the isolation valve.

When the

isolation valve was opened,

licensee

personnel

discovered that the

drain valves

had inadvertently

been left open.

Section

6 of

Attachment

1 to procedure

EST-212,

contains specific steps to

restore

the penetration to service following testing

and requires

that the drain valves

be shut before opening the isolation valves

to refill the system.

Failure to properly implement procedure

EST-212 is considered

to be another

example of the violation

discussed

in paragraph

2.c.(2) of this report.

During the performance of procedure

OST-1833T

on November

12,

1992, licensee

personnel

observed

several

transfer relays to be

smoking.

This procedure

was performed to retest

components

which

had failed during the previous test of the auxiliary control

panel.

Licensee

personnel

determined that the cause for the

burned relays

was

an inadequate test procedure

in that power

supply fuses

had not been

removed which caused

the transfer relays

to cycle excessively.

The failed relays

were subsequently

replaced

and

a revised test procedure

performed satisfactory.

The

inspector considered

the procedure

generation

process

to be weak

in this case

as the mistake to remove all the power supply fuses

was not detected

during reviews.

4.

Haintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify that

correct equipment clearances

were in effect; work requests

and fire

prevention work permits,

as required,

were issued

and being followed;

quality control personnel

were available for inspection activities

as

required;

and

TS requirements

were being followed.

Haintenance

was observed

and work packages

were reviewed for the

following maintenance activities:

~

Inspection of valve

1CS-751 in accordance

with procedure

CH-H0198,

Kerotest Series

9900 "Y"-Type Globe Valve Disassembly,

Inspection,

Reconditioning

and Reassembly.

Inspection

and non-destructive

examination of the "B" emergency

diesel

generator cylinder block in accordance

with procedures

HPT-

H0030,

Emergency Diesel

Generator Cylinder Block Inspection,

and

CH-H0150,

Emergency Diesel

Generator

Cylinder Head

Removal,

Disassembly,

and Reassembly.

Inspection of the camshaft

lobes

on the "A" emergency diesel

generator

in accordance

with procedure

HPT-H009,

Emergency Diesel

Generator

Camshaft

Lobe/Bearing

and Tappet Assembly Inspection.

~

Repair of the static inverters in accordance

with procedures

CH-

E0020,

Replace Oil Filled and Electrolytic Capacitors

and/or

Ferro-Resonant

Transformer Assembly in Westinghouse

7.5

KVA Static

Inverters

and PIC-E051,

Class

IE 7.5

KVA Westinghouse

Inverter.

The performance of work was satisfactory with proper documentation

of

removed

components

and independent verification of the reinstallation.

a

~

b.

A routine preventative

maintenance

(PH) task to replace the gate

and synchronization

board

and the gate driver assembly

in all four

vital inverters

was performed during this refueling outage.

'Following the component

replacements,

inverters

I and II began

experiencing

problems.

Inverter II tripped off line after

operating

several

days

and inverter I experienced

a loss of output

following reenergization.

The output

SCRs in both inverters

were

found faulted

and the

SCR supply fuses

were blown.

The licensee

replaced

the damaged

SCRs

and fuses,

removed the

new gateing

and

synchronization

board,

and reinstalled the old boards.

The

inverters

were subsequently

placed

back into operation with no

further problems.

There

appeared

to be

a problem with the

replacement

boards received

from the spare parts warehouse.

The

licensee

is evaluating the cause of the board failures with the

manufacturer

and will take appropriate

actions.

The "A" emergency diesel

generator

camshaft

inspection

was

performed following identification of spalling

and wear

on the "B"

emergency diesel

generator

camshaft discussed

in NRC Inspection

Report 50-400/92-23.

Very minor surface

spots

were noted which

indicated the potential

beginning of spalling.

The indications

were not serious

enough to require camshaft

replacement,

however.

The camshaft will be reinspected

during the next scheduled

diesel

inspection in refueling outage

number six.

Design

Changes

and Modifications (37828)

Installation of new or modified systems

were reviewed to verify that the

changes

were approved in accordance

with 10 CFR 50.59, that the changes

were performed in accordance

with technically adequate

and approved

procedures,

that subsequent

testing

and test results

met acceptance

criteria or deviations

were resolved

in an acceptable

manner,

and that

appropriate

drawings

and facility procedures

were revised

as necessary.

This review included selected

observations

of modifications and/or

testing in progress.

~

PCR-2512

Service Air Regulators to Chiller Expansion

Tank

~

PCR-5534

ESCWS Expansion

Tank Improvements

~

PCR-6547

Alternate Mini-Flow Redesign

~

PCR-6575

Reactor

Vessel

Stuck Stud

~

PCR-6584

EDG Starting Air/Control Air Contamination

~

PCR-6605

Pre-Heater

Bypass

Line Replacement

~

PCR-6630

Containment

Closure for AFW Pipe Replacement

While performing the post modification testing for PCR-6547,

on

November 6,

1992,

an

SSPS logic relay actuated

which satisfied the

initiation signal for an automatic

swapover of the

RHR and

CT suction

valves to the containment

sump.

The valves did not reposition

and

dump

the

RWST to containment

because

the shift supervisor

had conservatively

turned off the breaker

power supply earlier.

Although this event did

not actually cause

a spill in containment,

the procedural

controls were

considered

to be weak.

During the removal of reactor vessel

closure

studs in preparation of

core offload,

one stud

was found to be stuck in its reactor vessel

flange hole.

The licensee

performed

an engineering

evaluation to leave

the stud in place during refueling activities.

The stuck stud did not

interfere with the fuel manipulator.

The evaluation

concluded that the

stuck stud could still be tensioned

normally along with the other

closure studs

and not have to be removed until

ASME Section

XI

examinations

were required.

The inspector considered

the licensee's

actions to be appropriate.

Modification PCR-6630

was implemented to allow core alterations

during

auxiliary feedwater pipe replacement.

This temporary modification

10

installed

and removed blank flanges

on the

AFW piping for containment

closure requirements.

The inspector

was satisfied that containment

closure requirements

were met during refueling activities.

Modification PCR-6605 replaced

the pre-heater

bypass piping from the

main feedwater

system to the auxiliary feedwater

system.

This piping

showed evidence of accelerated

erosion rates

when tested ultrasonically

for pipe wall thinning.

The

new piping was fabricated

from chrome-moly

material

which should

be less susceptible

to erosion.

The inspectors

reviewed the post-modification testing for this maintenance

and the

maintenance

on the auxiliary feedwater piping which was replaced

in

containment.

Radiography

was performed

on the weld repairs

and

a system

inservice pressure

test performed.

The inspector

checked

the testing

performed to the requirements

contained

in ASME Section

XI and found it

to be acceptable.

Safety Systems

Walkdown (71710)

The inspector

conducted

a walkdown of various safety

systems

in

containment to verify that the lineups were in accordance

with license

requirements for system operability and that the system drawings

and

procedures

correctly reflected "as-built" plant conditions.

No violations or deviations

were identified.

Outage Activities (71707)

Major activities performed during this scheduled

refueling outage

included

a 20 percent

eddy current inspection

on the three

steam

generators,

inspection of service water piping and components,

testing

of motor operated

valves,

teardown/overhaul

of the "B" emergency diesel

generator

and reconstitution of fuel rods.

Also, feedwater pipe erosion

inspections

prompted significant pipe replacement/modifications

in the

auxiliary feedwater/pre-heater

bypass

system.

The results of the steam generator

eddy current inspection revealed

no

indications that steam generator

tubes

needed to be plugged.

The inspector

reviewed the licensee's

risk assessments

for emergent

work

activities during the outage.

The licensee recently implemented

a

revision to procedure

PLP-700,

Outage

Management,

which required that

all outage activity additions receive

an initial risk assessment

to

determine if the activity potentially affected

key safety functions or

the planned defense-in-depth.

Specifically schedule

changes

involving

the removal of the "B" SFP normal

power supply

and the repair of the "A"

EDG during continuing maintenance

on the "B" ESCWS were reviewed to

verify appropriate

evaluations

had

been

made or

PNSC approval

obtained.

The inspector considered

the process

to be effective.

s.

Refueling Activities (60710)

ll

The inspectors

witnessed

several shifts of fuel handling operations

and

verified that the refueling was being performed in accordance

with TS

requirements

and approved

procedures.

Areas inspected

included

containment integrity, housekeeping

in the refueling area, shift

staffing during refueling, surveillance testing,

and periodic monitoring

of plant status

during refueling operations.

In addition, the following

procedures

were reviewed:

~

PLP-616

Fuel Handling Operations

~

FHP-010

Core Mapping Following Fuel

Loading

~

FHP-014

Fuel

and Insert Shuffle Sequence

~

FHP-020

Fuel Handling Operations

~

OST-1091

Containment

Closure Test Weekly Interval During Core

Alterations

and Hovement of Irradiated

Fuel Inside

Containment

~

OST-1817

Refueling Machine (Manipulator Crane) Operability

~

OST-1818

Auxiliary Hoist Operability

~

NST-10169

Nuclear Instrumentation

System

Source

Range

N31

Operational

Test

~

HST-10170

Nuclear Instrumentation

System Source

Range

N32

Operational

Test

The inspectors

found procedure

implementation to be satisfactory.

The

water clarity and lighting in the refueling cavity was excellent.

During the core offload on October 2,

1992, operators

received

several

manipulator crane

underload interlock actuations

while

moving fuel assemblies.

Although the interlock actuation

temporarily halted crane

movement,

fuel movement

was possible in-

between actuations.

During the first nine assemblies

moved,

operators

encountered

four underload interlock conditions.

The

manipulator crane

has four load switch settings for selection

depending

on the weight of the fuel assembly

and insert.

The fuel

transfer data sheets

specified which switch setting to select.

The purpose of the underload interlock is to prevent lowering an

assembly

which comes

in contact with an adjacent

assembly

and

"hangs-up".

In this case

the load settings specified in the fuel

transfer data sheets

were in error,

but conservative,

causing

premature interlock actuation.

Licensee

personnel

compared

the load settings specified

on the

fuel transfer sheets

with original calculations of assembly weight

12

b.

and found that most of the switch positions specified

were

incorrect.

Fuel

movement

was halted until the transfer sheets

could be revised with correct load settings.

The licensee's

investigation of this event revealed that the transfer sheet

data

was incorrectly transposed

from the fuel assembly weight

calculations.

Since the fuel transfer data sheets

receive several

different independent

reviews prior to implementation,

the

inspector considered this effort to be weak for not previously

identifying this error.

During fuel reload

on October 30,

1992, licensee

personnel

discovered that

a fuel assembly

had

been

moved out of sequence.

The first step of the fuel transfer data sheets

specified the

first assembly for reload to be from spent fuel rack location A-

B2C4.

The refueling operator mistakenly latched

and

moved the

fuel assembly

located in the adjacent

rack location A-A2C4.

The

incorrect fuel assembly

was placed in the upender

and transferred

to the containment refueling cavity.

This error was noticed

by

licensee

personnel

during the next step in the fuel transfer data

sheet

when the refueling operator

was noticed

by another operator

to be over the incorrect rack location.

Fuel

movement

was then

stopped

and the first fuel assembly

was transferred

back from

containment to the spent fuel rack location.

Refueling operations

were suspended

until shift briefings were conducted

which

reinforced attention to detail principles.

Future fuel movement

proceeded

without incident indicating that the licensee's

corrective action

was appropriate.

This violation will not be

subject to enforcement

action because

the licensee's

efforts in

identifying and correcting the violation meet the criteria

specified in Section VII.B of the Enforcement Policy.

NCV (400/92-27-03):

Failure to properly move fuel in accordance

with fuel transfer data sheets.

Review of Licensee

Event Reports

(92700)

The following LERs were reviewed for potential generic

impact, to detect

trends,

and to determine

whether corrective actions

appeared

appropriate.

Events that were reported

immediately were reviewed

as

they occurred

to determine if the

TS were satisfied.

LERs were reviewed

in accordance

with the current

NRC Enforcement Policy.

a 0

b.

(Closed)

LER 90-03:

This

LER reported that

a train of essential

services chilled water was inoperable

due to air intrusion into

the system.

This item was previously discussed

in

NRC Inspection

Report 50-400/92-02.

During this outage the licensee

has

completed modifications to improve system cleanliness

and provided

new regulators for expansion

tank pressure

control.

(Closed)

LER 91-08:

This

LER reported that the high head safety

injection system

was inoperable

due to

a failure of the system's

alternate miniflow lines.

This event

was previously discussed

in

13

NRC Inspection

Report 50-400/92-17.

The licensee

issued

a

supplement

to the

LER dated October

13,

1992,

which documented

additional testing performed

on the system

and system

modifications to prevent recurrence of the event.

During this

outage

the licensee

implemented modification PCR-6547 to remove

the relief valves

and install flow orifices to regulate

recirculation flow.

(Closed)

LER 91-16:

This

LER reported the lifting of several

component cooling water relief valves during

a pump start.

This

event

was previously discussed

in NRC Inspection

Report 50-400/92-

07.

The licensee

has finished modification PCR-5741,

CCW to SFP

Coolers

Low Flow Alarm, which upgraded

the design pressures

of the

excess

letdown heat

exchanger

and reactor coolant drain tank heat

exchanger,

In conjunction with increasing

the relief valve

setpoint to 190 psig, this action enabled

the restoration of the

CCW system to

a normal lineup.

(Closed)

LER 92-04:

This

LER reported that

a single failure could

render the entire radiation monitoring system inoperable.

This

matter

was previously discussed

in

NRC Inspection

Report 50-

400/92-08.

Operating

and test procedures

have

been revised to

reflect the

new slide switch positions.

A revision to the

FSAR

has

been

made

and will be submitted in the next

FSAR update

package.

(Closed)

LER 92-09:

This

LER reported

a manual reactor trip which

was initiated following the loss of the running main feedwater

pump.

This event

was previously discussed

in

NRC Inspection

Report 50-400/92-15.

The licensee

has

completed real-time

training alerting operating

personnel

on the causes

for this

event.

(Closed)

LER 92-11:

This

LER reported that the emergency

bus

undervoltage logic circuitry was inadequately

tested.

This event

was previously discussed

in

NRC Inspection

Report 50-400/92-15.

The licensee

has revised the permanent test procedures

to correct

the deficiency.

(Closed)

LER 92-13:

This

LER reported that

a TS surveillance

requirement to sample the fuel oil day tank was not performed

following emergency

diesel

operation.

This event

was previously

discussed

in NRC Inspection

Report 50-400/92-17.

The licensee

has

completed training applicable

personnel

and has revised

administrative

procedures

to clarify procedure

step annotations.

The individuals involved in this deficiency were counseled.

(Open)

LER 92-14:

This

LER reported

pipe wall thinning in the

auxiliary feedwater

and main feedwater

systems

caused

by flow

erosion.

This matter was previously discussed

in NRC Inspection

Report 50-400/92-23.

The licensee

has replaced

those sections of

piping which exhibited extensive erosion.

The licensee is

14

presently evaluating the effectiveness

of the computerized

pipe

wall thinning program

and is investigating the cause for the

accelerated

rate of erosion.

10.

Licensee Action on Previously Identified Inspection

Findings

(92702

&

92701)

a.

(Closed)

IFI 400/91-26-01:

Follow the licensee's

activities to

increase

the charging

pump flow margin

and evaluation of quarterly

pump testing acceptance

criteria.

This matter

was previously discussed

in NRC Inspection

Report

50-302/91-27 during which the quarterly

pump testing

was

considered

to be satisfactory.

The licensee

has reanalyzed

the

minimum safety injection flow limit during

a loss of coolant

accident

and

has determined that only 348 gpm is necessary.

This

value constitutes

an additional

30 gpm available for design

margin.

A change to the

TS was subsequently

requested

and issued

on November

10,

1992.

b.

(Closed) Violation 400/92-13-01:

Failure to maintain

gC inspector

certification.

The inspector reviewed

and verified completion of the corrective

actions listed in the licensee's

response letter dated August 28,

1992.

The licensee

has

enhanced

the

gC inspector recertification

system to provide

a two week notification prior to expiration

dates.

c.

(Closed)

IFI 400/92-23-01:

Review the licensee's

activities to

repair preheater

bypass

and auxiliary feedwater piping due to

erosion.

The licensee

has

issued

LER 92-14 describing the corrective

actions

taken for this event.

For record purposes

the IFI will be

closed

and further action tracked

by the

LER.

ll.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1) at the conclusion of the inspection

on November 23,

1992.

During

this meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violation, Non-cited Violations,

and Inspector Follow-up Item

addressed

below.. The licensee

representatives

acknowledged

the

inspector's

comments

and did not identify as proprietary

any of the

materials

provided to or reviewed

by the inspectors

during this

inspection.

No dissenting

comments

from the licensee

were received.

Item Number

400/92-27-01

400/92-27-02

400/92-27-03

Acronyms

and Initialisms

Descri tion and Reference

NCV:

Failure to obey

a radiography

posting,

paragraph 2.c.(l).

VIO:

Failure to properly

establish/implement

plant

procedures,

paragraph 2.c.(2).

NCV:

Failure to properly move fuel

in accordance

with fuel transfer

data sheets,

paragraph

S.b.

ACR

AFW

ASHE

CCW

CFR

CT

CVCS

EDG

EPT

ESCWS-

EST

FHP

FSAR

GPH

IFI

LER

HPT

HST

NCV

NRC

OST

PCR

PLP

PH

PNSC

PSIG

QC

RCS/RC-

RHR

RWST

SCR

SFP

SSPS

TS

VIO

Adverse Condition Report

Auxiliary Feedwater

American Society of Hechanical

Component Cooling Water

Code of Federal

Regulations

Containment

Spray

Chemical

Volume Control

System

Emergency Diesel

Generator

, Engineering

Performance

Test

Essential

Services Chilled Wate

Engineering Surveillance

Test

Fuel Handling Procedure

Final Safety Analysis Report

Gallons

Per Hinute

Inspector

Follow-up Item

Licensee

Event Report

Haintenance

Performance

Test

Haintenance

Surveillance Test

Non-Cited Violation

Nuclear Regulatory

Commission

Operations

Surveillance Test

Plant

Change

Request

Plant

Program

Procedure

Preventive

Haintenance

Plant Nuclear Safety Committee

Pounds

Per Square

Inch Gage

Quality Control

Reactor Coolant System

Residual

Heat

Removal

Refueling Water Storage

Tank

Silicon Controlled Rectifier

Spent

Fuel

Pump

Solid State Protection

System

Technical Specification

Violation

Engineers

r System