ML18010A941

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Initial SALP Rept 50-400/92-20 for 910602 - 920926
ML18010A941
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 11/25/1992
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010A940 List:
References
50-400-92-20, NUDOCS 9212080240
Download: ML18010A941 (39)


See also: IR 05000400/1992020

Text

ENCLOSURE

INITIAL SALP

REPORT

U. S.

NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT

OF

LICENSEE

PERFORMANCE

Inspection

Report

Number

50-400/92-20

Carolina

Power

and Light Company

Shearon Harris

June

2,

1991 to September

26,

1992

92i2080240 92ii25

PDR

ADOCK 05000400

PDR

I.

INTRODUCTION

II.

SUMMARY OF

RESULTS

III.

CRITERIA

IV.

PERFORMANCE ANALYSIS

TABLE OF

CONTENTS

~

~

2

3

~

~

3

A.

B.

C.

D.

E.

F.

G.

Plant Operations

Radiological Controls

.

Maintenance/Surveillance

Emergency

Preparedness

Security

4

~

~

~

~

~

~

~

~

~

Engineering/Technical

Support

Safety Assessment/guality

Veri

~

~

~

~

~

~

fication

~

~

3

5

8

11

12

14

16

V.

SUPPORTING

DATA AND SUMMARIES

.

19

A.

B.

C.

D.

E.

F.

G.

H.I.

Licensee Activities .

Direct Inspection

and Review Activities

.

Escalated

Enforcement Action

Significant Licensee

Conferences

Held Duri

Period

Confirmation of Action Letters

Reactor Trips

.

Review of Licensee

Event Reports

(LERs)

.

Licensing Activities

Enforcement Activity

ng

~

~

~

~

~

~

~

~

The Appraisal

19

.

20

.

20

20

.

21

.

21

.

21

.

22

.

22

INTRODUCTION

The Systematic

Assessment

of Licensee

Performance

(SALP) program is

an

integrated

NRC staff effort to collect available observations

and data

on

a periodic basis

and to evaluate

licensee

performance

on the basis of

this information.

The program is supplemental

to normal regulatory

processes

used to ensure

compliance with NRC rules

and regulations.

It

is intended to be sufficiently diagnostic to provide

a rational basis

for allocation of NRC resources

and to provide meaningful

feedback to

licensee

management

regarding the

NRC's assessment

of their performance

in each functional area.

An

NRC SALP Board,

composed of the staff members listed below,

met on

November 4,

1992, to review the observations

and data

on performance

and

to assess

licensee

performance

in accordance

with Manual

Chapter

NRC-

0516,

"Systematic

Assessment

of Licensee

Performance."

The Board's

findings and recommendations

were forwarded to the

NRC Regional

Administrator for approval

and issuance.

This report is the NRC's assessment

of the licensee's

safety performance

at Shearon

Harris for the period June

2,

1991 through September

26,

1992

'he

SALP Board for Shearon

Harris was

composed of:

E.

W.

B. S.

C. A.

D.

M.

J.

E.

E.

G.

N.

B.

Merschoff, Director, Division of Reactor Projects

(DRP), RII

(Chairperson)

Mallett, Deputy Director, Division of Radiation Safety

and

Safeguards,

RII

Julian, Chief, Engineering

Branch, Division of Reactor Safety,

RII

Verrelli, Chief, Reactor Projects

Branch

1,

DRP, RII

Tedrow, Senior Resident

Inspector,

Shearon Harris,

DRP, RII

Adensam,

Director, Project Directorate II-1 (PD II-1), Office of

Nuclear Reactor Regulation

(NRR)

Le, Project Manager,

PD II-l, NRR

Attendees

at

SALP Board meeting:

H. 0. Christensen,

Chief, Reactor Projects

Section

1A,

DRP, RII

D. J. Roberts,

Project Engineer,

Project Section

1A,

DRP, RII

SUMMARY OF

RESULTS

During the assessment

period,

Shearon Harris continued to be operated

in

a safe

and effective manner.

Maj or strengths

were identified in the

areas of security,

emergency

preparedness,

engineering/technical

support

and radiological controls.

Weaknesses

were identified in the safety

assessment/quality

verification section.

Good management

involvement in plant operations activities

and site

walkdowns contributed to the overall safe operation

and good material

condition of the plant.

However, inconsistent

performance

by operators

during transient

and routine operations

resulted

in a declining trend.

Implementation of the radiation protection

program was good.

Efforts to

control radiation exposure

were noteworthy

and effective

as were those

efforts to reduce

contaminated

areas.

Strengths

were noted in the preventative

maintenance

program

and

improvement

was noted in the area of post-maintenance

testing.

Additionally, management

involvement in maintenance activities

was also

exhibited.

Some weaknesses

in the performance of maintenance activities

was observed

including one which caused

a reactor trip.

Strengths

were noted in the emergency

preparedness

area,

specifically

during two annual

graded

emergency

exercises.

Good management

support

was also noted in the area of simulator configuration control

and the

maintenance

of emergency

response facilities and equipment.

Implementation of the security program was good.

Hardware

changes,

training and good management

involvement in this area contributed to

this successful

implementation.

Engineering

and technical

support continued to be good.

Strong

engineering

support

was demonstrated

through refueling activities, the

system engineering

program

and engineering

evaluations

associated

with

plant modifications.

However,

a weakness

was noted for an inadequate

post-trip review.

Licensee

performance

in the area of safety

assessment

and quality

verification was less effective than during the previous cycle.

Weakn'esses

were noted in the corporate

self-assessment

function.

Overall, the licensee's

performance

was considered

to be superior.

Overview

Performance

ratings for the last rating period

and the current period

are

shown below.

Functional

Area

Rating Last Period

Rating This Period

~l

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency

Preparedness

Security

and Safeguards

Engineering/Technical

Support

Safety Assessment/equality

Verification

1

1

2

1

1

1

1

1 (declining)

1

2 (improving)

1

1

2

III.

CRITERIA

The evaluation criteria which were used to assess

each functional

area

are described

in detail in

NRC Manual Chapter 0516, which can

be found

in the Public Oocument

Room.

Therefore,

these criteria are not repeated

here,

but will be presented

in detail at the public meeting held with

the licensee

management.

IV.

PERFORMANCE ANALYSIS

A.

Plant

0 erations

~Anal sis

This functional

area

addresses

the control

and performance

of activities directly related to operating the facility,

including fire protection.

The plant was operated

in a safe

and conservative

manner

during the assessment

period.

Four reactor trips occurred

from power operation

and one Reactor Protection

System

actuation occurred while the plant was shutdown.

There were

no reactor trips during the last assessment

period.

Two of

the reactor trips this period involved component failure,

one occurred during the performance of a maintenance

calibration procedure,

and

a manual reactor trip was

inserted

when

a main feedwater

pump tripped following

deenergization

of an electrical

bus for a breaker failure.

Three of the four reactor trips occurred during

a one week

period.

The plant had

an excellent continuous

run of 271

days which set

a plant record.

The plant was managed

conservatively

as evidenced

by the decision to shutdown

and

repair boric acid leakage

on

a reactor coolant system

temperature

detector

bypass line even though leakage

was

well below regulatory limits.

Operating activities were generally conducted

in a

professional,

dedicated,

and conscientious

manner.

Shift

turnovers

and the performance of operator

rounds

were

considered

to be good.

Good attention to detail

was

exhibited

by an operator during the performance of rounds to

identify an improper flange

on the turbine-driven auxiliary

feedwater

pump lube oil cooler.

Also, operator

performance

to control

a plant transient during troubleshooting

on the

digital electric hydraulic control

system

was good.

Operator performance

during plant transients

was

inconsistent,

however,

as evidenced

by poor control of steam

generator

level

and steam pressure

which both resulted

in

unnecessary

safety

system actuations.

In addition,

instances

were noted during routine operations

indicating

a

lack of attention to detail.

In one instance

operators

failed to detect

a mispositioned

switch which rendered

the

quadrant

power tilt alarm inoperable.

In another,

operators

failed to notice

a low oil condition in a safety injection

pump.

Operator actions which failed to properly identify

and document several

adverse

conditions resulted

in three

violations.

Administrative controls regarding plant operations

were

considered

to be effective.

A new program was developed to

control infrequent tests

and evolutions.

The additional

management

involvement, planning,

and interdepartmental

communication which resulted

from this program

had

a

definite benefit to safe plant operation.

However,

areas

in

need of improvement were also noted.

Boric acid system

temperature

monitoring alarm response

procedures

for

radwaste

personnel

did not provide sufficient guidance.

Additionally, the operating

procedure

for removing

a hose

from a demineralizer filter was weak which resulted in

personnel

and area contamination.

Plant housekeeping

was considered

to be good.

Progress

was

made in a new paint and labeling program which was initiated

during this assessment

period.

The practice of weekly

management

inspections

of areas

inside the power block and

specific outside

areas

was continued.

This effort was

effective in identifying housekeeping

deficiencies.

The licensee reinstituted the practice of rotating licensed

personnel

to other departments/work

groups.

Several

licensed

operators

were rotated to the operations

procedure

writers group,

work scheduling

group, real-time trainer

position,

and the load dispatcher's

office.

The licensee

maintains extra licensed

personnel

on shift in excess of TS

requirements.

Additionally, licensed

operators

have

been

transferred

to the training department

and the Nuclear

Assessment

Department

(NAD) to increase

the technical

expertise

in these

areas.

2.

Formal

communication

was observed

between control

room

operators

and between control

room personnel

and auxiliary

operators

in the field.

Use of repeat

backs

was

common.

Day-to-day communications

between shift operating

personnel

and technical

support

system engineers/managers

and

maintenance

managers

was evident.

Operations

management

was

routinely observed

monitoring several

of the planned

shutdowns

and startups.

Control

room drawings

were found to correctly reflect plant

conditions.

However, the

NRC identified deficiencies

in

updating

one set of drawings to accurately depict

modifications which had

been

performed

on the

CCW system.

Operator logs were found to be organized,

and usually

provided sufficient information on plant status

and events.

However,

one instance

was noted where

a deficiency regarding

a service water valve was not adequately

addressed.

The fire brigade duties were assigned

to radwaste

operating

personnel.

A licensed operator

was also assigned

to the

brigade

as

an advisor.

This action allowed less

impact on

main control

board personnel

and allowed more detailed fire

fighting training to be provided.

The fire brigade

response

to several

minor fires was considered

to be satisfactory.

During this assessment

period six violations were cited.

Performance

Ratin

3.

Category:

1

Trend:

Declining

Board Recommendations

The Board determined that there

was

a decline in performance

during this period

as evidenced

by inconsistent

operator

performance

during transients

and

a lack of attention to

detail during routine operations.

Even though performance

remained superior,

in this area,

management

attention to

this trend is considered

appropriate.

Radiolo ical Controls

~Anal sis

This functional

area

addresses

activities related to

radiological controls, radioactive waste

management,

environmental

monitoring, water chemistry,

and

transportation of radioactive materials.

The licensee

continued,to maintain stable

and well qualified

radiological controls staffing.

Sufficient numbers of

qualified technicians

were available to support both outage

and non-outage activities,

and the licensee

ensured

a

favorable return rate for contractor technician

support for

the

1992 refueling outage.

The technician continuing

training program was considered

comprehensive

and included

plant systems

overview and performance related training.

In

addition, the licensee actively supported

technician

certification by the National Registry of Radiation

Protection Technicians,

and certified twelve radiation

control personnel.

Hands-on-training facilities utilized

radiation detector simulation to reinforce

ALARA concepts.

The licensee

took steps to improve performance

in the area

of self-assessment

during the period.

In particular,

increased

management

attention to the feedback reporting

system

was evident

by the implementation of causal

factor

trending

and close-out of old action items.

Overall, the licensee

continued to effectively manage

collective dose expenditure

during the assessment

period.

Collective dose for the period was approximately

82 person-

rem.

This dose level

was good since it reflected

expenditure primarily for operating conditions

and spent

fuel operations with 28 outage

days during the period.

The

licensee

also

began refueling outage activities thirteen

days prior to the end of the period.

The licensee

effectively managed

dose for significant activities

including an unplanned

outage to repair

a resistance

temperature

detector valve.

The dose for this activity was

considered

low at approximately 7.4 person-rem.

Licensee

personnel

exhibited effective

ALARA planning which limited

personnel

exposure.

For example,

detailed pre-planning for

work (adding oil to reactor coolant

pumps, repairing valves,

and cleaning waste storage

tanks)

included conservative

power reductions,

mockup training on spare

equipment,

and

the

use of video cameras

and dose rate instruments for

remote monitoring of job performance.

The licensee

also

actively decreased

radiation sources

in the plant by

cleaning waste tanks.

Licensee

planning

and preparation for the

1992 refueling

outage

was thorough,

and the established

goal of 165 person-

rem appeared

aggressive

relative to the scope of work.

The licensee's

contamination control

and housekeeping

practices

were considered

excellent.

The average

contaminated

surface

area continued to trend downward with

respect

to previous

assessment

periods.

The licensee

also

actively tracked valves which exhibited leakage of

contaminated liquid so that appropriate

management

attention

could be applied.

Personnel

contamination

events for the

year

1991

and through September

26,

1992,

were

131

and 44,

respectively.

This is about the

same level

as that observed

during previous single outage

and non-outage

periods.

One

isolated

poor practice

was identified late in the assessment

period associated

with trash frisking operations.

Immediate

corrective actions

were implemented,

and the licensee

initiated actions to evaluate

the need for long-term

training and procedural

improvements.

Improvements

in both radiological

and chemical controls

associated

with fuel stored in the spent fuel pools were

noted during this assessment.

As mentioned in the previous

assessment

report,

the licensee

removed

a significant amount

of crud from the bottom of the spent fuel pools.

Licensee

management

decided to halt any further clean-up of crud

as

a

method of reducing

dose to plant personnel.

Thus,

crud

management for spent fuel continues to provide

a challenge

for contamination control.

Issues

regarding technician training for the operation of

the Post Accident Sampling

System

and the development of a

procedure to remove

an undiluted

sample

from a shielded

container

were resolved.

Although significant progress

has

been

made,

some operability problems identified during the

last assessment

continued.

The licensee

was implementing

corrective actions to resolve those problems.

The plant water chemistry program was effectively

implemented,

maintaining chloride, fluoride, dissolved

oxygen

and dose equivalent iodine well within their

respective

TS limits.

A sampling

system

was installed for

in-line monitoring of chemistry conditions in the secondary

side of the plant.

The system

was undergoing testing at the

end of the assessment

period.

Secondary

chemistry

was very

good

as evidenced

by steam generator

sludge lancing results

with less than

50 pounds of sludge per generator for each of

the last two operating cycles.

The liquid and gaseous

effluents

program

was

managed

effectively.

During this period, the licensee

continued to

have

some effluent radiation monitors declared

inoperable

for periods greater

than

30 days.

The licensee

made

a

concerted effort to return effluent radiation monitors to

operable status.

This effort was successful

as the number

of inoperable monitors

was reduced

by the end of the period.

Two non-routine

gaseous

releases

were recorded during this

period.

Liquid and gaseous

effluents for the 12-month

period from mid-1991 to mid-1992 were well within regulatory

limits.

The maximum whole body dose

was less

than five

percent of the allowable limit.

2.

The Radiological

Environmental Monitoring Program

was

implemented effectively.

Collection stations

were

calibrated

and well maintained.

Licensee

sample results

compared favorably with those of the State of North

Carolina.

Overall, the radiological

environmental

data

indicated that plant operations

had

no significant impact on

the environment or public health

and safety.

Shipping

and handling of radwaste

were efficient, reflecting

the competence,

training,

and experience

of the staff.

In

general,

shipping documentation

was in compliance with

requirements.

During this assessment

period,

no violations were cited.

Performance

Ratin

3.

Category:

I

Board Recommendations

None

Maintenance Surveillance

~Anal sis

This functional

area

addresses

those activities related to

equipment condition, maintenance,

surveillance

performance,

and equipment testing.

Performance of maintenance

and surveillance activities

continued to be effectively performed.

For the majority of

activities observed,

performance of work was good with

proper documentation of removed or replaced

components

and

independent verification of their reinstallation.

Maintenance efforts to decrease

air lock leakage

were

effective.

However,

instances

of inattention to detail

were

also noted.

One reactor trip occurred during the

performance of a maintenance

surveillance test

when

a

pressure

pulse occurred

on the

common leg of the three

reactor coolant flow detectors

while a flow transmitter

was

being returned to service.

One

AFW system actuation

was

reported while troubleshooting

a steam generator level

instrument.

The cause

was attributed to

personnel

error.

An additional

weakness

was noted where licensee

personnel

failed to properly reference

the equipment technical

manual

during an oil addition to the turbine driven auxiliary

feedwater

pump.

The resultant

improper oil level could have

caused

pump damage if not corrected.

Good pre-planning to reduce

personnel

exposure,

equipment

down time,

and avoid plant transients

was evident for

several

maintenance activities.

This planning included

utilization of spare

equipment for mock-up training, pre-

evolution briefings with operations

personnel,

and

contingency planning.

This demonstrated

supervisory

involvement in these activities.

Specialized

vendor training programs,

the continuing

training program,

hands-on training facilities,

and

a low

turnover rate

have

enhanced

the craft skills and knowledge.

A full-time dedicated

crew of instrumentation

and control

technicians

was maintained to perform testing

and

troubleshooting

associated

with RPS

and

ESF instrumentation.

This has provided consistency

in job performance

and

resulted

in fewer problems

associated

with the testing

and

maintenance

performed

on these

systems.

The backlog of maintenance

work was relatively constant.

Plant management

assigned

an additional

IKC crew which

started to reduce the backlog at the end of this assessment

period.

The overall material condition of the plant was good.

However, specific deficiencies,

such

as oil leaks

on the

safety injection pumps

and several

safety injection valve

motor operators,

needed

improvement.

Sodium hydroxide

leakage

was noted

on several

transmitters

associated

with

the containment

spray additive system.

Also,

a few

emergency

service water vent and drain valves

had signs of

general

corrosion.

The licensee

took action to correct

these deficiencies

and significant improvements

were noted,

especially in the area of. boric acid and sodium hydroxide

leakage control.

The licensee

continued the preventive maintenance

program

for large

pumps

and motors by completing inspections

on the

normal service water pumps.

This program

has

been effective

in ensuring the reliability of this type of equipment.

Strengthening

of the licensee's

predictive maintenance

activities

was demonstrated

during this assessment

period

due to improvements in the vibration and lube oil analyses

programs.

These

included the completion of monthly

vibration tests for normally operating safety-related

equipment,

with more frequent testing

as

needed,

and the

adoption of an expanded list of equipment requiring lube oil

testing.

Vibration analyses

detected

problems with the

jockey fire pump

and

a main feedwater

pump enabling repairs

before

pump failure.

Thermography

was utilized to detect

hot spots

in large motors,

process

instrumentation

cabinets,

rod drive cabinets,

and the switchyard.

10

As discussed

in the previous

SALP report, efforts to improve

post-maintenance

testing were in progress.

The licensee

has

expanded

the planner's test matrix, completed training on

the

new matrix,

and enhanced

the Automated Haintenance

Management

System database

to improve the post-maintenance

testing process.

Improvement

was noted during this

assessment

period.

The licensee

developed

a formal program for the conduct of

infrequent tests

and evolutions to strengthen

the

communication

and pre-planning

between

maintenance

and

operations

personnel.

Industry guidance

on the conduct

and

substance

of pre-job briefings, training,

and procedures

to

be utilized,

was included.

Likewise, the licensee

developed

a troubleshooting

procedure

incorporating risk-oriented

reviews

by management.

Strong supervisory

and management

involvement was noted for

several

work activities.

Work involving the entry into TS

action statements

received

management

attention.

Haintenance

managers

were observed daily in the control

room

communicating with operations

personnel

on equipment

problems.

Hanagement

was also involved in on-the-job-

training and qualification of personnel.

This action

contributed to improved procedural

compliance.

The surveillance test scheduling

program continued to

perform well.

The reports

generated

from this system

allowed management

to focus attention

on potentially overdue

tests.

No scheduled

tests

were overdue or missed.

However,

on one occasion,

boric acid

pump testing periodicity was not

increased

as required.

The licensee's

approved inservice

inspection (ISI) program continued to be satisfactory.

ISI

program procedural

requirements

and responsibilities

were

clearly defined.

Technical

and supervisory

personnel

were

generally

knowledgeable

in their areas of responsibility.

During the assessment

period, four violations were cited.

Performance

Ratin

Category:

2

Trend:

Improving

Board Recommendations

None

11

Emer enc

Pre aredness

~Anal sis

This functional

area

addresses

activities related to the

implementation of the

Emergency

Plan

(EP)

and procedures,

support

and training of onsite

and offsite emergency

response

organizations,

and licensee

performance

during

emergency

exercises

and evaluated

actual

events.

Good management

support for the

EP program was demonstrated.

The licensee carried out several drills to test alternates

for response

positions, initiated

an auto-dial call-out

system

and relocated

the Operational

Support Center

(OSC) in

an effort to protect workers from potential radiation

plumes.

The licensee

continued to provide effective

Emergency

Response

Organization training .hroughout the assessment

period.

With one exception, all personnel

had completed

the

required training.

The licensee

maintained

emergency

response facilities and

equipment in a state of readiness

through equipment

surveillance

and functional testing.

Two equipment

operability problems did occur.

One problem involved

inadequate

maintenance

of the gross failed fuel detector

and

the other was the inoperability of some

Emergency

Response

Facility Information System

(ERFIS) terminals.

Both issues

were corrected,

with the latter resulting in improved

ERFIS

reliability.

The licensee's

audit and critique program

was effective in

identifying routine

and exercise conditions requiring

corrective actions.

Hanagement

reviewed these findings and

.

verified that corrective actions

were taken.

The licensee

implemented its Emergency

Plan in response

to

one event this period.

The event

was correctly classified

as

a Notification of Unusual

Event, with offsite

notifications performed in a timely manner.

'arris

demonstrated

good response

capability for dealing

with site emergency situations during graded exercises

in

September

1991

and August 1992.

During the exercises,

the

licensee

demonstrated it could implement the

Emergency

Plan

and its implementing procedures,

as well as take suitable

actions to mitigate the consequences

of the accident

scenarios.

Emergency classifications

were timely as the

scenarios

progressed,

and operation of the emergency

response facilities and equipment

was good.

Performance

strengths

observed

during the exercises

included good

12

2.

teamwork

and aggressive

play of participants.

Improvement

was noted in the involvement of the accident

assessment

team

and casualty control

team from the

OSC.

The

command

and

control exhibited

by the Technical

Support Center

(TSC)

and

Emergency Operations Facility (EOF)

Emergency Directors

and

the licensee's

critique process

were also exercise

strengths.

All substantive

findings were documented for

review and corrective actions.

Although no exercise

weaknesses

were identified,

some minor problems

were noted

in the areas of notification messages

to offsite authorities

and issuance

of dosimetry to TSC and

EOF personnel.

During the assessment

period,

one violation was cited.

Performance

Ratin

3.

Category:

1

Board Recommendations

None

~Secure it

~Anal sis

This functional

area

addresses

those security activities

related to protection of vital plant systems

and equipment,

and special

nuclear material.

The licensee

implemented

and managed

an effective security

program.

Security management

at both the site

and corporate

level

was skilled and highly visible in program activities.

The licensee

revamped

the training program for supervisors

to enhance

communications.

Many program improvements

implemented

since the last assessment

show site

and

corporate

management's

strong support.

Examples of these

included

enhanced

alarm stations

and assessment

capabilities,

and patrol

and response

personnel

effectiveness.

The security force was professionally

and effectively

staffed,

equipped,

and trained to do their assigned

duties.

The security training staff was dedicated

and knowledgeable.

The licensee

has initiated several

programs that have

enhanced

the security force's professionalism.

The most

effective items were the creation of an improved combat

stress

course

using

new rifles and the purchasing of a new

security radio system that has encryption capabilities.

The licensee

continued to identify and implement methods to

better perform the security program.

The licensee

enhanced

13

2.

their protected

area patrol capabilities

by obtaining

several

security patrol vehicles.

This improved the

effectiveness,

efficiency,

and morale of the security

personnel

by providing weather protection

and increasing

the

patrol

and response

speed of the security officers.

The

acquisition

and issuance

of new smaller

and lighter

semiautomatic rifles have also

improved the response

capabilities of the response

force.

The licensee

has

replaced

the older tube driven closed-circuit television

(CCTV) cameras

with new solid state

cameras,

which has

improved picture quality and coverage.

Alarm

stations'ssessment

capabilities

were enhanced

by the addition of a

Video Capture

system with a new video switcher

and larger

CCTV monitors.

To further enhance

the alarm

stations'ssessment

proficiency,

a Computer Aided Lighting Analysis

program was

used to upgrade

and identify illumination

deficiencies within the protected

area.

Licensee

management

continued to provide trend data to

system engineers

and maintenance

personnel

in order to

maintain security equipment at

an acceptable

level.

The licensee's

Physical Security,

Contingency

and Training

and gualification Plan revisions submitted during this

period were consistent

with 10 CFR 50.54(p),

and were timely

and adequately

coordinated with the

NRC.

The licensee's

staff,

who coordinated security plan revisions

and technical

specification

changes,

were knowledgeable of regulatory

requirements.

During this assessment

period,

no violations were cited.

Performance

Ratin

3.

Category:

1

Board Recommendations

None

En ineerin

Technical

Su

ort

~Anal sis

This functional

area

addresses

those activities associated

with the design of plant modifications,

engineering

and

technical

support for operations,

outages,

maintenance,

and

operator training.

Overall, engineering

continued to provide effective

technical

support to the operation of the facility.

Strong

engineering

support

was demonstrated

through refueling

14

activities; the predictive maintenance

and repetitive

failure analysis

programs;

the system engineering

program

and engineering

evaluations

associated

with plant

modifications.

High levels of corporate

engineering

onsite involvement

during modification development

and implementation

were

evident.

The licensee's

administrative controls for

ensuring reliable decay heat

removal during outages

was

noteworthy.

These controls included provisions for

identification of higher risk evolutions

and

key safety

functions, defense-in-depth

contingency planning, training,

and outage risk assessment

reviews.

In addition, this

information was emphasized

during outage

meetings to help

reduce

the potential for loss of shutdown cooling events

during outage activities.

Furthermore,

the refueling outage

plan did not include mid-loop operating conditions.

Excellent technical

support

was evidenced

by reactivity

management for planned

power reductions

and outages.

This

action

was effective in controlling axial flux peaking.

The

power ascension

test

program,

which was created

following a

nuclear instrumentation miscalibration event,

was utilized

to control plant startups without any further mishaps.

Additionally, technical

support personnel

were actively

involved in maintenance activities such

as troubleshooting

the

ATWS Mitigation System Actuation Circuitry and the

emergency

service water screen

wash

pumps.

Another example

of good performance

was the analysis of self-identified

weaknesses

in secondary

side performance monitoring which

resulted

in the installation of a computer workstation that

would access all Emergency

Response

Facility Information

System database

points

and provide real-time display of

secondary

and primary side data.

Some weaknesses

were identified in the area of technica'l

support.

These

included

an inadequate

post-trip review

which did not identify the potential for reactor trip

breaker failure based

on previous industry events,

inadequate

design control of pipe supports

in the boric acid

system

and emergency diesel

generator

lube oil system,

inadequate

incorporation of manufacturers'ecommendations

into procedures for periodic heat trace

panel calibration,

and the omission of several

required

items in the

PM program

for the turbine driven auxiliary feedwater

pump.

The

licensee

recognized

the problems with the

PM program

and

implemented

a technical

manual

review process

to identify

similar items.

Engineering

and technical

support organizational

involvement

in the outage planning process

was

an identified strength.

There were several

system engineers

designated

as

coordinators for various major outage activities including

15

steam generator

work and electrical

bus outages.

These

individuals were knowledgeable

and organized

as reflected

by

the efficient completion of their assigned

work activities.

In addition to these

designated

coordinators,

many other

system engineers

were involved in other aspects

of outage

planning activities which contributed to the overall outage

efficiency.

The licensee's

system engineering

program

was effective.

System Engineers

took ownership of their systems.

Their

level of knowledge of both system. history and performance

was

commendable.

System engineers

were actively involved in

troubleshooting,

performance monitoring,

and the

coordination of corrective actions.

An example

was

a

containment

temperature

monitoring change initiated to

provide data for equipment qualification concerns.

The

modification involved the installation of resistance

temperature

detectors

at various locations throughout

containment to verify that local temperature

conditions did

not exceed technical specification limitations.

Additionally, the licensee

continued to foster strong

communications

and effective working relationships

between

engineering

and other plant organizations that was evident

during previous

SALP periods.

Hodifications

and engineering

evaluations

generally

contained clear safety reviews

and were considered

to be

technically sound

and acceptable.

Examples

included

modifications to the reactor cavity seal ring instrument air

piping to allow component testing

and calibration prior to

use inside containment,

and annunciator setpoint

changes

to

prevent spurious

alarms

and to more accurately reflect main

feedwater flow limits.

However,

a plant change

request

to

return the component cooling water system to its normal

configuration following a relief valve lifting event failed

to accomplish its purpose

due to lack of interdepartmental

communications.

A lack of progress

to modify emergency

diesel

generator starting air quality was

an example of

inadequate

modification prioritization.

The temporary

modification process

was strengthened

by the inclusion of

jumpers

and lifted leads

as temporary modifications.

A motor-operated

valve testing

and surveillance

program

had

been

developed

which adequately

addressed

most of the

recommendations

of Generic Letter 89-10.

Strengths

in the

program included the use of state-of-the art diagnostic

systems,

knowledgeable

and well trained personnel,

extensive

licensee

involvement in industry groups,

and effective

programmatic incorporation of industry experience

and vendor

information.

However, several

concerns

were noted.

The

concerns primarily involved

a potential reduction of the

scope of differential pressure

testing,

the use of static

16

2.

rather than dynamic flow testing to demonstrate

design basis

acceptability,

and the potential for non-conservative

sizing

and thrust calculations

due to failure to incorporate rate-

of-loading effects.

The licensed operator training program continued to be

effective as evidenced

by a

100% pass rate

on the Generic

fundamentals

Examination Section

and initial examinations.

Improvement of weaknesses

identified during the last

assessment

period

was evidenced

by improved communications

among crew members

during an initial examination

administered to eight candidates

this assessment

period.

The requalification program

was found to be satisfactory

when all twenty operators

passed

the NRC-administered

requalification examination.

The licensee

adequately

evaluated its operators.

However, inconsistencies

were

noted in the performance of evaluators

during walkthroughs.

The simulator was

used effectively for training.

The

licensee

has

implemented corrective actions to alleviate

simulator deficiencies identified during examination

administration.

The licensed

operator training staff has

been

supplemented

by three licensed

operators

which should

strengthen

the technical

expertise of the department.

During the assessment

period,

no violations were cited.

Performance

Ratin

3.

Category:

1

Board Recommendations

None

Safet

Assessment

ualit

Verification

~Anal sis

This functional

area

addresses

those activities related to

licensee

implementation of safety policies;

amendments;

exemptions

and relief requests;

responses

to Generic

Letters; Bulletins and Information Notices; resolution of

safety issues;

reviews of plant modifications performed

under

10 CFR 50.59; safety review committee activities;

and

use of feedback

from self-assessment

programs

and

activities.

Licensee

performance

in the area of safety

assessment

and

quality verification was satisfactory.

However,

as

mentioned in the previous

assessment

report,

the licensee

had not achieved

the desired results

from its first level

assessment

process,

which included individual self-checks,

17

management

supervision,

independent

verification> post-

maintenance

testing

and corrective action program trending.

With regard to onsite self assessment,

plant management

continued to perform frequent inspections

and tours of

various plant areas

focusing

on the general

cleanliness

and

material condition of equipment.

These activities

had

a

positive effect on plant housekeeping.

Nanagement

involvement

was evidenced

by the coaching of personnel,

the

conduct of infrequent activity pre-evolution briefings,

and

direct observation of critical work involving TS equipment

inoperability.

The Adverse Condition Report system

has

been fully

implemented.

Due to the lower threshold for reporting

problems than with the previous

system,

the data

base

has

grown considerably

which has allowed more meaningful

problem

trending.

Self-identification of problems continued to be

a

strength in this assessment

area.

However, four violations

were cited regarding the failure to adequately identify,

document,

and correct deficiencies,

as mentioned

in the

Operations

and Engineering/Technical

Support sections of

this report.

Good participation

and advance

preparation

by plant nuclear

safety committee

members for those

items discussed

in

committee meetings

was noted.

Minutes from the meetings

contained

accurate

documentation of the committee's

activities.

Corporate responsibilities

included quality verification

surveillances

and independent

evaluations.

In contrast to

the good on-site self assessment

effort, corporate

activities were initially found to be deficient in several

areas.

For most of the rating period, little change

was

noted in the minimal involvement of the guality Verification

(gV) organization.

This organization

had recently

begun to

assist

the plant organizations

in self-assessment

field

surveillances

during which

a

gV inspector is temporarily

assigned

to the other group,

observes

a work activity, and

reports discrepancies

to the area

manager.

Although two

self-assessment

field surveillances

were found to be of high

quality, only two were performed.

Near the end of this

assessment

period,

gV involvement was increased

and the

licensee

hired two additional

personnel

so that field

surveillances

could

be continued throughout the outage.

The initial performance of onsite quality assessments

was

considered

to be poor.

Audits were found to be fragmented

and lacked sufficient documentation

to draw meaningful

conclusions

or measure

effectiveness.

Audits were not

always forwarded to senior licensee

management

in a timely

18

manner.

The licensee

made extensive efforts to correct the

violations

and weaknesses.

Improvement

was noted near the

end of this assessment

period

as to the adequacy of audit

documentation

and timeliness of submittal to higher

management.

The

amendment

requests

for changes

to TS were adequate

in

providing "no significant hazards

considerations"

evaluations.

Licensee

management's

involvement in

interacting with the staff during meetings,

site visits,

and

the review of licensing/technical

issues,

and in the timely

submittal of license

amendment

requests

remains effective.

One exception

was noted

when the licensee failed to submit

a

timely request for a TS change

regarding surveillance

requirements for the emergency

core cooling system.

No

emergency

TS changes

were requested

during this period.

Some licensee

strengths that were observed

in the last

SALP

were sustained

during this assessment

period.

The licensee

was effective

and pro-active in identifying potential

safety

problems during their review of documentation

related to

license

amendment activities

and generic industry

communications.

When

a safety concern

was identified, the

licensee

addressed

all aspects

of the issue to satisfy all

regulatory

as well as plant safety aspects.

Examples

included the identification of a discrepancy

involving the

safety injection switch-over time from cold leg to hot leg

recirculation during the long-term cooling phase of a loss

of coolant accident

and implementation of the Station

Blackout Rule.

The licensee's

responses

to Bulletins and Generic Letters

had

bee'n timely and met staff requirements.

The licensee

demonstrated

a conservative

approach

to issues

and

had

placed

a high priority on the assessment

of industry

experience

to improve plant safety

and performance.

Plant

management

conservatively

decided to shut the unit down in

response

to boric acid leakage

from valves in the reactor

coolant

system

even though leakage

was well within TS

limits.

Industry experience

was shared with all on-site

managers

and system engineers

and programs

were established

to address

industry concerns

which included the main turbine

emergency trip system,

fuse control

and replacement,

and

solenoid valve reliability.

During this assessment

period, longstanding deficiencies

in

the design

and testing of the high head safety injection

system were resolved

by design

changes.

The

10 CFR 50.59 review process

at Harris was consistent

with approved industry guidance

and

was considered

to be

a

strength

because

trained, tested,

and experienced

reviewers

19

were maintained

by technical discipline;

and the. necessary

procedures

were in place.

In addition,

two independent

reviewers routinely performed the required evaluation to

confirm the conclusions.

During this assessment

period, five violations were cited.

2.

Performance

Ratin

3.

Category:

2

Board Recommendations

II

The Board continued to be concerned

over the lack of

Corporate activities

on self assessment

and field

surveillance efforts.

Management attention in this area is

warranted.

SUPPORTING

DATA AND SUMMARIES

A.

Licensee Activities

The plant began

the assessment

period at

100 percent

power.

On

June 7,

1991, the plant was shutdown to perform additional post-

maintenance

testing

on

a reactor trip switch.

Full power

operations

resumed

on June 9,

1991.

On March 6,

1992, the reactor

was

shutdown to repair leaking valves

on the

C

RTD bypass

manifold.

This outage

ended

a record continuous

run of 271 days.

The plant returned to normal

power operations

on March 12,

1992.

The plant was shutdown for refueling outage

No.

4 on September

12,

1992.

B.

Significant management

changes

occuring this

SALP period included

the creation

and filling of the

new President/Chief

Operating

Officer position who reports directly to the existing Chief

Executive Officer.

In addition,

a new Site Vice President

was

assigned.

A new Chemistry Manager

was also assigned

during the

period.

Direct Ins ection

and Review Activities

During the assessment

period,

one special

audit,

31 routine

and

five special

inspections

were performed at the Harris facility by

the

NRC staff.

The special

audit and inspections

were:

June 3-7,

1991; Inspection of Activities Associated with

Reactor Trip Breaker Failure Following the June 3,

1991 Trip

September

23-26,

1991;

Emergency

Preparedness

Program

Review

October

21 - November

16,

1991;

Program

Review for Changes

to Plant Environs

20

~

April 6 - 10,

1992; Motor-Operated

Valve Inspection

~

August

3 - 7,

1992; Audit of the High Head Safety Injection

Alternate Miniflow System

and Related

Issues

~

August

31

- September

4,

1992;

Emergency Operating

Procedures

Followup Inspection

Escalated

Enforcement Action

Orders

None.

2.

Civil Penalties

(CP)

Severity Level III problem

(EA 91-076) for improper

maintenance activities which led to one channel

of the

reactor protection

system being inoperable

($50,000 CP).

CP issued for activities which occurred during

SALP cycle 9.

Si nificant Licensee

Conferences

Held Durin

The

A

raisal

Period

During the assessment

period there

were seven significant

management

conferences

with the licensee.

These

were:

~

June

12,

1991;

Management

Meeting to discuss Harris'elf-

assessment

(cycle 9).

~

July 3,

1991;

Enforcement

Conference to discuss

improper

maintenance activities which rendered

one Reactor Trip

System instrumentation

channel

inoperable

(cycle 9).

~

August 1,

1991;

Management

Meeting to present results of

SALP cycle

9 assessment.

~

June

9,

1992;

Management

Meeting to discuss Harris'elf-

assessment

(cycle 10).

~

August 20,

1992;

Management

Meeting to discuss

technical

and

management

issues

associated

with the high head safety

injection (HHSI) alternate miniflow system.

~

September

10,

1992;

Management

Meeting to discuss

the

Harris'PEEE submittal

schedule.

~

October

14,

1992;

Enforcement

Conference

to discuss

apparent

inadequate

corrective actions

associated

with the

HHSI

alternate miniflow system.

Confirmation of Action Letters

21

Confirmation of Action Letters

None.

Reactor Tri s

The unit experienced

four reactor trips at power during this

assessment

period

and

one reactor protection

system actuation

occurred

on July 13,

1992, while the plant was in the hot standby

condition.

The trips were:

~

June 3,

1991; Automatic reactor trip from full power while

performing

a maintenance

calibration procedure

on

a reactor

coolant system flow transmitter.

~

July 12,

1992; Automatic reactor trip from full power due to

a failed main condenser

boot seal

and resultant

low

condenser

vacuum.

~

July 15,

1992;

Hanual reactor trip from 30 percent

power due

to the loss of the main feedwater

pump following

deenergization

of an electrical

bus for breaker removal.

~

July 17,

1992; Automatic reactor trip from full power due to

a failed main condenser

boot seal

and resultant

low

condenser

vacuum.

Review of Licensee

Event

Re orts

LERs

During the assessment

period,

22

LERs were analyzed.

Special

reports

were submitted during the period by the licensee

but are

not included in the table.

The distribution of these

events

by

cause,

as determined

by the

NRC staff,

was

as follows:

Cause

Component Failure

Design/Procedures

Construction/Fabrication

Installation

Personnel

-Operating Activity

-Maintenance Activity

-Testing/Calibration Activity

-Other

Other

Totals

22

Licensin

Activities

22

During this

SALP period,

30 licensing activities were resolved.

This included nine license

amendments,

and

14 other licensing

actions.

Review was also completed for seven multiplant

activities.

The most significant of these

were

NRC Bulletin 88-08

and the Station Blackout Analysis to meet

10 CFR 50.63,

which is

due to be implemented

in 1994.

Enforcement Activit

FUNCTIONAL

AREA

NO.

OF VIOLATIONS IN SEVERITY LEVEL

I

II

III

IV

V

DEV

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency

Preparedness

Security

Engineering/Technical

Support

Safety Assessment/

guality Verification

TOTAL

1*

4

1

1*

15

1

  • This violation, issued during this period,

was discussed

in the

previous

SALP.