ML18010A388

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Insp Rept 50-400/91-18 on 910720-0823.No Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Security,Fire Protection,Surveillance Observation, Maint Observation,Safety Sys Walkdown & LERs
ML18010A388
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 09/06/1991
From: Christensen H, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010A385 List:
References
50-400-91-18, NUDOCS 9109240392
Download: ML18010A388 (12)


See also: IR 05000400/1991018

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/91-18

Licensee:

Carolina

Power and Light Company

P. 0. Box-1551

Raleigh,

NC 27602

Docket No.:

50-400

License No.:

NPF-63

Facility Name:

Harris

1

Inspection

Conducted:

July 20 - August 23,

1991

Lead Inspector:

J.

edrow,

Sensor

Resident

Ins

ctor

Other Inspectors:

M.

S annon,

Resident

Inspector

Approved by:.

hristensen,

Section Chief

Division of Reactor Projects

Da

e

Soigne

Date Signed

SUMMARY

Scope:

This routine inspection

was

conducted -by two resident

inspectors

in .the areas

of plant

operations,

radiological

controls,

security,

fire protection,

surveillance

observation,

maintenance

observation,

safety

system

walkdown,

licensee

event reports

and licensee self assessment.

Numerous facility tours

were

conducted

and facility operations

observed.

Some of these

tours -and

observations

were conducted

on backshifts.

Results:

Two violations

were identified;

Failure

to approve

and

forward Technical

Specification

required

audits within 30 days,

Paragraph

7

and;

Failure to

document corrective actions,

Paragraph

7.

One weakness

was identified:

Because

the documentation for the audit program

is

scattered

through

various

reports, it was difficult to deterII,ine

the

= effectiveness

of the

program

as required

by 10 CFR 50, Appendix B, Criterion

XYIII, Paragraph

7.

One unresolved

item was identified:

Improper Crosby relief valve blowdown ring

settings,

Paragraph

2.d.

9109'240392

910906

PDR

ADOCK 05000400

G

REPORT

DETAILS

1.

Persons

Contacted

Licensee

Employees

  • P. Beane,

Manager, guality Control

  • J. Collins, Manager,

Operations

  • G. Forehand,

Manager,

Management/Organization

  • C. Gibson,

Manager,

Programs

and Procedures

C. Hinnant,

General

Manager, Harris Plant

  • D. McCarthy, Manager, Site Engineering

B. Meyer, Manager,

Environmental

and Radiation Monitoring

T. Morton, Manager,

Maintenance

J. Nevill, Manager,

Technical

Support

C. Olexik, Manager,

Regulatory Compliance

A. Powell, Manager, Harris Training Unit

R. Richey, Vice President,

Harris Nuclear Project

H. Smith, Manager,

Radwaste

Operation

  • N. Wallace, Sr. Specialist,

Regulatory Compliance

E. Willett, Manager,

Outages

and Modifications

W. Wilson, Manager,

Spent Nuclear

Fuel

  • L. Woods,

Manager,

System Engineering

Other

licensee

employees

contacted

included

office,

operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

Acronyms

and initialisms used

throughout this report are listed in the

last paragraph.

"

2.

Review of Plant Operations

(71707)

The plant continued in power operation

(Mode 1) for the duration, of this

inspection period.

a

~

Shift Logs and Facility Records

The inspector

reviewed

records

and discussed

various entries

with

operations

personnel

to verify compliance

with the

Technical

Specifications

and the licensee's

administrative

procedures.

The following records

were reviewed:

Shift Supervisor's

Log; Control

Operator's

Log; Night Order Book; Equipment Inoperable

Record; Active

Clearance

Log; Jumper

and Wire Removal

Log; Temporary Nodification

Log; Chemistry Daily Reports; Shift Turnover Checklist;

and selected

Radwaste

Logs.

In addition,

the inspector

independently verified

clearance

order tagouts.

No violations or deviations

were identified.

'

b.

Facility Tours

and Observations

Throughout

the inspection

period, facility tours

were conducted

to

observe

operations,

surveillance,

and

maintenance

activities

in

progress.

Some

of

these

observations

were

conducted

during

backshifts.

Also, during this inspection period,

licensee

meetings

were attended

by the inspectors

to observe

planning

and management

activities.

The facility tours

and

observations

encompassed

the

following areas:

security perimeter fence; control

room;

emergency

diesel

generator

building;

reactor

auxiliary building;

waste

processing

building;

turbine

building; fuel

handling

building;

emergency

service

water

building;

battery

rooms;

electrical

switchgear

rooms;

and the technical

support center.

During these tours,

the following observations

were made:

( I)

Monitoring Instrumentation

- Equipment operating

status,

area

atmospheric

and liquid radiation monitors, electrical

system

lineup, reactor

operating

parameters,

and auxiliary equipment

operating

parameters

were

observed

to verify that indicated

parameters

were

in accordance

with the

TS ,for the current

operational

mode.

(2)

Shift Staffing - The inspectors

verified that operating shift

staffing was in accordance

with TS requirements

and that control

room

operations

were

being

conducted

in

an

orderly

and

professional

manner.

In addition,

the inspector

observed shift

turnovers

on various occasions

to verify the -continuity of plant

status,

operational

problems,

and

other

pertinent

plant

information during these

turnovers.

(3)

Plant

Housekeeping

Conditions

-

Storage

of material

and

components,

and

cleanliness

conditions

of various

areas

throughout

the facility were

observed

to determine

whether

safety and/or fire hazards

existed.

(4)

Radiological

Protection

Program - Radiation protection control

activities

were

observed

routinely to verify that

these

activities

were in conformance with the facility policies

and

procedures,

and in compliance with regulatory requirements.

The

inspectors

also

reviewed

selected

radiation

work permits

to

verify that -controls were adequate.

(5)

Security

Control - In the

course

of monthly activities,

the

inspector

included

a review of the licensee's

physical security

program.

The

performance

of various shifts of the security

force

was

observed

in the

conduct of daily activities which

included:

protected

and vital area

access

controls;

searching

of personnel,

packages,

and

vehicles;

badge

issuance

and

retrieval;

escorting

of visitors; patrols;

and

compensatory

posts.

In addition,

the inspector

observed

the operational

status

of

Closed

Circuit Television

(CCTY) monitors,

the

Intrusion Detection

system

in the central

and

secondary

alarm

stations,

protected

area

lighting, protected

and vital area

barrier integrity, and the security organization interface with

operations

and maintenance.

(6)

Fire Protection

- Fire protection activities, staffing

and

equipment were observed

to verify that fire brigade staffing was

appropriate

and

that fire alarms,

extinguishing

equipment,

actuating

controls,

fire

fighting

equipment,

emergency

equipment,

and fire barriers

were operable.

No violations or deviations

were identified.

Review of Nonconformance

Reports

Adverse

Condition

Reports

(ACRs)

were

reviewed

to veri fy the

following:

TS were complied with, corrective actions

as identified

in the reports

were

accomplished

or being

pursued

for completion,

generic

items were identified and reported,

and items were reported

as required

by the TS.

No violations or deviations

were identified.

CCW Inventory Loss

On August 8,

1991, at 8:21 a.m.,

a second

CCW pump

was started

in

order to support

troubleshooting

of the

"A" RHR Heat Exchanger

CCW

Outlet

Flow Indicator FI-688A.

The operators

immediately noted

a

decreasing

CCW surge

tank level

and manually maintained

CCW tank

level.

Additional operators

were dispatched

to find the cause of the

leakage

and it was subsequently

determined that various relief valves

had lifted.

A control board operator then initiated

CCW flow through

the

RHR heat exchanger

to reduce

system pressure

from 140

PSIG to 120

PSIG,

but leakage

continued until the

second

running

CCW

pump

was

secured.

A second

test

run

was started

at 12:20

p.m. to verify which

CCW

relief valves

had lifted and

to

determine

the correct

system

configuration to prevent further relief valve lifting. It was found

that four relief valves lifted following the

second

CCW

pump start.

It was also

determined

that if CCW system

pressure

was maintained

less

than

95

PSIG,

no relief valves

would lift when the

second

CCW

pump started.

Flow is presently

being maintained

through

the

RHR

heat

exchanger

to maintain

system

pressure

below 95

PSIG until this

deficiency is adequately

resolved.

Discussions

with operations

personnel

indicated that

on previous

CCW

pump starts,

minor

CCW

head

tank level

decreases

had

been

noted.

These

decreases

had been attributed to placing

a cold

CCW system into

operation.

The

CCW system

may

have

been

spi king high

enough

on

previous

pump starts

to cause relief valve lifting but the valves

reset with little head tank loss.

Further investigation

found that the

CCW relief valves

had incorrect

nozzle ring settings

which resulted

in a lower- reset

pressure

than

the

135

PSIG specified

in the vendor test

data reports. 'any of

these

valves

had

been

tested for proper relief setting

during the

1991

refuel-ing

outage.

The

cause

of the incorrect

nozzle ring

settings

has

not

been

determined.

Following a maintenance

history

review it was found that the suspect

valves

had

been disassembled

and

worked

on prior to initial startup in 1986.

It appeared

that during

the

1986 corrective maintenance activities,

the valve blowdown rings

were improperly set prior to returning the valves

back to service.

Further review found that procedural

guidance

was lacking

on

how to

set

the

blowdown rings; specific training

on

how to measure

the

blowdown ring setting

was not adequate;

and the manufacturer's

design

data

and technical

manual

were difficult to interpret,

leading to

different interpretations

in

how to set

the

blowdown rings.

It

appeared

that operator

actions

were correct

and timely in addressing

this

event.

The relief valve deficiency

has

the potential

for

causing

a loss of both

CCW systems

and it also

has the potential for

causing

other safety

systems

to

become

inoperable.

The improper

setting of various

Crosby relief valve blowdown rings is- considered

to

be

an

unresolved

item

pending

NRC review of the licensee's

engineering resolution.

URI

(400/91-18-01):

Improper

Crosby relief valve

blowdown ring

settings.

No violations or deviations

were identified.

3.

Surveillance Observation

(61726)

Surveillance

tests

were observed

to verify that approved

procedures

were

being

used;

qualified personnel

were

conducting

the tests;

tests

were

adequate

to verify equipment

operability;

calibrated

equipment

was

utilized; and

TS requirements

were followed.

The following tests

were observed

and/or data reviewed:

PN-N0057

Terry Turbine Annual Bolt Retorquing

NST-I0123 Pressurizer

Pressure

Protection

Set II Operational

Test

NST-I0125 Main Steam Line Pressure

Loop

1 Operational

Test

NST-I0400 Spent

Fuel

Pool North Monitor, RN-*1FR-3567B-SB Operational

Test

The

maintenance

personnel

were

found

to

be

knowledgeable

of the

procedures,

used calibrated test equipment,

properly notified the control

room,

maintained

communications,

and followed the applicable

procedure

steps,

therefore

these

procedures

were performed .satisfactory.

No violations or deviations

were identified.

4.

Maintenance

Observation

(62703)

The inspector

observed/reviewed

maintenance

activities to verify that

correct

equipment

clearances

were

in effect;

work requests

and fire

prevention

work permits,

as

required,

were

issued

and

being followed;

quality control

personnel

were available for inspection activities

as

required;

and

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the following

maintenance

(WR/JO) activities:

On July 24,

1991 the "B" spent fuel

pump was disassembled

in order to

perform

pump

seal

replacement.

Due to the

high contamination

.potential,

as

a result of Brunswick fuel storage,

special

health

physics

precautions

were

required.

The

maintenance

personnel

received

constant

HP coverage,

followed maintenance

procedures,

had

the required tools,

were properly dressed,

and appeared

to be very

knowledgeable

of

the

assigned

task,

the

job

was

performed

expeditiously with no observed deficiencies.

The inspector

also witnessed

the

replacement

of FI-0688A,

CCW flow

indicator,

per

WR/JO 91-ALI(1.

The maintenance

technicians

properly

followed corrective

maintenance

procedure,

CM-I0084, Methodology of

Scale

Replacement

for

VX2 52 Indicators,

=used

appropriate

tools,

obtained

correct

replacement

parts

and

therefore

performed

an

acceptable

replacement of FI-0688A.

'o

violations or deviations

wer e identified.

5.

Safety Systems

Walkdown (71710)

The inspector

conducted

a walkdown of the service water system to verify

that the lineup

was in accordance

with license

requirements

for system

operability and that the system

drawing and procedure correctly reflected

"as-built" plant conditions.

It was

found that the

system

was lined up

according

to applicable

system lineup procedures,

components

were clearly

identified,

system

drawings

were correct,

and the

system

appeared

to be

well maintained.

No violations or deviations

were identified.

6.

Review of Licensee

Event Reports

(92700)

The following LERs were reviewed for potential

generic

impact, to detect

trends,

and to determine

whether corrective actions

appeared

appropriate.

Events that

were reported

immediately

were reviewed

as they occurred to

determine if the

TS were satisfied.

LERs were reviewed in accordance

with

the current

NRC Enforcement Policy.

r

a.

(Closed)

LER 90-01:

This

LER reported

a violation regarding

response

time testing of an engineered

safety featurechannel.,This

matter

was previously discussed

in

NRC Inspection

Report 50-400/90-02

and

was

the subject of a non-cited violation

(NCV 400/90-02-06).

The

licensee

has completed testing of the omitted channel

instrumentation

and

has

incorporated

controls into appropriate

procedures

used in

writing and approving procedure

changes.

b.

(Closed)

LER 91-14:

This

LER reported that cooling water flow to the

"A" residual

heat

removal

pump

was

inadvertently

isolated

for

approximately

15 minutes.

The licensee

has

completed

corrective

actions

to include the cooling water throttle valves into the locked

valve program

and has

reviewed the event with maintenance

personnel.

Evaluation of Licensee Self Assessment

(40500)

In January

1991, the licensee

made organizational

changes

which eliminated

the

guality

Assurance

Department

(gA)

and

reassigned

the

gA

responsibilities

to the Nuclear Assessment

Department (NAD).'n order to

evaluate

the

new organization,

assessments

performed

by

NAD were reviewed

to ensure

Technical

Specification

requirements

were being met.

Various

deficiencies

were noted.

The

licensee

is

required

to perform various

Technical

Specification

required

audits

at various

frequencies.

The licensee's

reorganization

changed

the audit process

to assessments

and three

1991

assessments

were

performed

'to meet specific audit requirements.

TS 6.5.4.4 requires that

audit reports

shall

be

prepared,

approved

by the

manager

gA/NAD, and

forwarded within 30 days after completion of the audit to the Executive

Vice

President,

Power

Supply

and

Senior

Vice

President,

Nuclear

Generation.

The inspector

found that the fire protection assessment

which

was conducted

February 8-22,

1991,

was not approved until July 16,

1991;

the maintenance

and

E&RC assessment

which'as

conducted April 1-19,

1991,

,was

not

approved

until

June

26,

1991;

and

the

outage

management/

modification assessment

which was

conducted

May 9-17

and

June 14,'991,

was not approved until July 30,

1991.

This is contrary to TS 6.5.4.4 in

that the

licensee failed to approve

and forward these

audits within 30

days.

It was also

found that the licensee failed to forward the

(1991)

fire protection,

maintenance

and

E8RC,

and outage management/modification

assessments

to the executive. and senior vice presidents

as required.

The

licensee's

failure to approve

and forward these

audits within 30 days to

the appropriate

levels of management

is contrary to

TS 6.5.4.4

and is

considered

to be

a violation.

Violation (400/91-18-02):

Failure to approve

and- forward

TS required

audits within 30 days.

The inspector

performed

an indepth review of Assessment

91-02, Maintenance

and

ESRC,

and it was

found that various

adverse .conditions

noted

on the

observation

reports

were not documented

ip the inspection report.

The

following are

examples

of field observations

which were not noted in the

assessment

report or resolved

on the observation

sheets:

It

Seven out of 26 individuals did not review the

RWP prior to filling

out "CHITS" to begin work in an

RWP area.

Older work packages

did not require

PMT when

asked

on the work

request

sheet,

regular

packing

was

replaced

with live load packing

without any testing,

and

two valves

were disassembled

and inspected

but no

PMT was recorded.

I

A pipe

rack is

being

used

to store

several

different types of

material.

This rack contains

both stainless

steel

and carbon

pipe.

Some of the pipe is marked 9-List and

some

ends of the pipe are not

capped

nor taped.

The individuals involved didn't have

much experience with this task,

and

attempted

to install

the

(cavi,ty seal)

rings

in the

wrong

direction around

the

head.

This took extra 'rigging time and delayed

the job a couple of hours.

'Temporary

power feed to battery chargers

was not tied off properly to

prevent accidental

short, if pulled.

An instrumentation line leading

from valve

1BD-133 was

supported

by

several

wraps of duct tape

attached

to

a mechanical

snubber/strut

assembly.

Possible

binding of the snubber

may have occurred.

Contract

worker exited containment

via step-off

pad but failed to

frisk hands

and feet, quickly frisked at

a second frisker,

and did

not monitor through portal monitor before exiting area.

10 CFR 50 Appendix

B Criteria XVIII and the licensee-'s

accepted

quality

Assurance

Program,

Corporate

equality

Assurance

Program

Manual

Rev.

14,

collectively

require

that

the

corrective

actions

for significant

conditions

adverse

to quality be documented.

gA Manual, paragraph

12.4.2

also requires

that if the condition is not confirmed,

the initiating

document

shall

be

canceled,

the

basis

for cancellation

noted

on the

document,

and the

document shall

be placed in a permanent file.

Contrary

to the

above

requirement,

the previous

adverse

conditions

were noted

on

various'bservation

sheets

but the resolution of the adverse

conditions

were not documented

or retained.

The fai lure to properly document

the

resolution

to adverse

conditions is contrary to

10 CFR 50 Appendix

B and

the licensee's

accepted

gA program

and is considered

to be

a violation.

Violation (400/91-18-03).:

Failure to document corrective actions.

~

'

The

licensee

is required

by

TS 6.5.4.1

to perform audits

of unit

activities

on

a periodic basis.

10 CFR'0,

Appendix

B Criteria XVIII

requires

that

a comprehensive

system of periodic audits shall

be carried

out to verify compliance with all aspects

of the guality Assurance

Program

and to determine

the effectiveness

of the

program.

After an extensive

review of applicable

assessments,

gA reports,

and observations, it was

concluded that sufficient documentation of inspection activities may exist

to

show

conformance

to the

TS required

audits.

However,

the audit

activities for specific audit

requirements

are

fragmented

throughout

.

various reports

and therefor e it was difficult to draw

a conclusion that

the audited

areas

were satisfactory.

It was also noted that the licensee

in

some

cases

did not

document

a conclusion for specific

TS required

audits.

The audits

need sufficient documentation

to

show that audited

areas

were adequately

reviewed to justify conclusions

in audit reports.

Fragmented

documentation

made it difficult to determine

the effectiveness

of the program

and is considered

a program weakness.

Two violations were identified.

8.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1)

at'he

conclusion

of the inspection

on August 23,

1991.

During this

meeting,

the

inspectors

summarized the

scope

and

findings of the

inspection

as

they are detailed

in this report, with particular

emphasis

on the Violations

and

Unresolved

Item addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify

as

proprietary

any of the materials

provided

to or reviewed

by the

inspectors

during this inspection.

Item Number

Descri tion and Reference

400/91-18-01

400/91-18-02

400/91-18-03

9.

Acronyms

and Initial i sms

URI:

Improper Crosby relief valve blowdown ring

settings.

(Paragraph

2.d.)

VIO:

Failure to approve

and forward TS required

audits within 30 days.

(Paragraph

7).

VIO:

Failure to document correcti ve actions

(Paragraph

7).

ACR

CCTV

CCW

CFR

ESRC

HP

Adverse Condition Report

Closed Circuit Television

Component Cooling Water

Code of Federal

Regulations

Environmental

5 Radiation Control

Health Physics

LER

MST

NCV

NAD

NRC

PMT

PSIG

QA/QC

RHR

RWP

TS

URI

VIO

WR/JO

Licensee

Event Report

Maintenance Surveillance Test

Non-Cited Violation

Nuclear Assessment

Department

Nuclear Regulatory

Commission

Post Maintenance

Test

Pounds

per Square

Inch Gage

Quality Assur ance/Quality Control

Residual

Heat

Removal

Radiation

Work Permit

Technical Speci'fication

Unresolved

Item

Violation

Work Request/Job

Order