ML18009A749
| ML18009A749 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 11/30/1990 |
| From: | Hale M, Richey R CAROLINA POWER & LIGHT CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| HO-903043-(O), NUDOCS 9012190116 | |
| Download: ML18009A749 (14) | |
Text
,. ACCELERATED D TRIBUTION DEMONS TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR: 9012190116 DOC. DATE: 90/11/30 NOTARIZED:
NO FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina AUTH.NAME AUTHOR AFFILIATION HALE,M.
Carolina Power
& Light Co.
RICHEY,R.B.
Carolina Power
& Light Co.
RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000400
SUBJECT:
Monthly operating rept, for Nov 1990 for Harris Unit 1.N/
901214 ltr.
DISTRIBUTION CODE: IE24D COPIES RECEIVED:LTRI ENCL SIZE:
TITLE: Monthly Operating Report (per Tech Specs)
NOTES:Application for permit renewal filed.
05000400 RECIPIENT ID CODE/NAME PD2-1 LA BECKER, D INTERNAL: ACRS AEOD/DSP/TPAB N
.L~L B10 EG FILE 01 EXTERNAL: EG&G BRYCE,J.H NSIC COPIES LTTR ENCL 3
3 1
1 10 10 1
1 1
1 1
1 1
1 1
1 RECIPIENT ID CODE/NAME PD2-1 PD AEOD/DOA IRM TECH ADV NRR/DOEA/OEAB RGN2 NRC PDR COPIES LTTR ENCL 1
1 1
1 2
2 1
1 1
1 1
1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 26 ENCL 26
R C
Carolina Power 8 Light Company P. O. Box t65 ~ New Hill,N. C. 27562 R. B. RICHEY Vice President Harris Nuctear Project C
1 y ~ggo HARRIS NUCLEAR PROJECT P. 0.
Box 165 New Hill, North Carolina 27562 File Number'SHF/10-15505 Letter Number'HO-903043 (0)
Document Control Desk United States Nuclear Regulatory Commission Washington, DC 20555 HARRIS NUCLEAR PROJECT DEPARTMENT UNIT NO.
1 DOCKET NO. 50-400 LICENSE NO NPF-63 MONTHLY OPERATIONS REPORT Dear Sirs In accordance with Technical Specification 6.9.1.5 for the Harris Nuclear Power Plant, Unit, No.
1, Carolina Power 6 Light Company herewith submits the report of operation statistics and shutdown experience for the month of November 1990.
Yours very truly, C.H R. B. Richey Vice President Harris Nuclear Project MWH:smh Enclosure cc:
Mr. S.
D. Ebneter (NRC-RII)
Mr. R.
G. Oehl (DOE)
Mr. J.
E. Tedrow (NRC-SHNPP)
. 9012190116 901130 PDR ADOCK 05000400 R
~ n.rq Q Q MFM/DATAREPa/1/OS4 IJ t4
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W
DOCKET NO.:
UNIT:
DATE COMPLETED BY:
050-400 Harris Unit 1
November 1990 Mark Hale OPERATIONS
SUMMARY
Harris Unit 1
operated at a 35.17 percent Availability Factor for the referenced month and a
29.55 percent Capacity Factor.
There were two events.
Details are provided on the Unit Shutdowns and Power Reduction Sheet.
There are 157 fuel assemblies in the reactor vessel and 410 spent fuel assemblies in the Spent Fuel Pools.
306 of the spent fuel assemblies are BWR and were shipped to Harris from CP&L's Brunswick Plant.
MEM/DATAREPa/1/OS4
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, Cf)b,L CO
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PLANT PERI-'GRHANCE DA'I'A~"TFH
-" HUH "DArE 12/<</ve M
ul'EliArxHG DArA REr~
RUN TXHE 09:44:80 HARRIS UNIT I PAGE I'<PD36-eee OPERA'I'lHG STATUS Docl<L'r Nu. e58-4ee COHPLETED K<Y HARI< M.
HALE rELEPHGHE
<919>36 944 1. 'UNXT NAHE:
I.IARR1S UNIT
". REroRrING r.ERxoD:
HQVEHDER 90 3.
LXCEHSED Tl-IERHAL POMER
<HMT): 2775 5
- 6 ~
7 8.
NAHEPLATE RATlNG (GROSS HME>: 950.9 DESIGN El ECTRXCAI RATXNG (NET HWE): 980.8 HAX DEPENDABLI= CAPACXTY (GROSS HWE>: 920.0 HAX DEPENDABLE CAPACITY <NE'1'WE):
860 '
Xl'= CIHAHGES OCCUR XH CAPACXTY RATXNGB (XTEHB GlVE REASONS:
N/A I
HOTES There are 157 fuel assem-I blies in the reactor vessel and I 410 spent fuel assemblies in the I Spent Fuel Pools.
306 of the I spent fuel assemblies are BWR and I were shipped from Brunswick.
I 3
THI
BXNCE LAST REPORT) 9.
18.
I'OWER LEVEL TO Wl-IXCH RES'IRICTED XI= AHY (NET HWE):
No f<EASQNS FQR RESTRICTION XF AHY:
N/A Tl<XB HONTI-I YR ru DATE CUHUL ATXVE 11*
4 A
13.
14.
15.
16.
17.
18.
19.
21 *
)') t')
) 4 4
23.
I-IOURS 1N REPORfxNG PERXGD NUHBEIX OF IHOURB REACTOR CRXTXCAL REACTOR RESERVE BIIUTDGMN I.IRB HOURS GEHERAroR QN LINE UNX'1'EBERVF Bl-lUTDGWN IHOURB GROSS TIIERHAL ENERGY GEN.
(HWIR)
GROSS ELEC.
ENERGY GEN.
(HMI-I)
NET El EC.
ENLRGY GEHI=RATED (HMIH)
UHXT SERVlCE FACTOR UNIr AVAXLADXLX'rYFAcTOR UHXT CAP.
FACTofk <USING HDC NET)
UNXT CAP.
FACTOR (UBXHG DER HET>
UNIT FofICED OUTAGE RATE SIHUTDOMHB BCIIED ~
OVLR HEXT 6 HONTI-IB 72e.ee 266.99
.ee 253.28
.88 629383.48 206946.08 183804.80 35.17 35.17 29.55
.)8
.88 (TYPE,
- DATE, 8e16
~ ee 72')'5. 96
.08 7264.48
.00 19111489.38 6334592.00 5989514.88 98.62 90.62 85'2 81.91 1 '9 AND DURATION 31417.88 "5"93 53
.00 24923.83
~ 08 65653167.78 21784854.80 20247682.08 79 33 79.33 "r4. 94 71.61 4.05 OF LACH>:
Refueling Outage, March 2nd, 1991 8 weeks.
g5 26.
XF SI IUTDOWN A'1'ND GF REPGR'1'ER1GD, EST1HATED DAl'E OF STAR'I'P: 12/89/98 UNITS XN rEBr 'rAIU (I-'l<xul~ ru CQHHl=acxAI.
ul LlcArxoH>: I-.ul<I=CABr AcllxLVLD XNXTXAI Cf<XS XCAI IS Y XNXTIAI El ECTRICXTY CQHHERCXAI QPEf<ATIQN MEM/DATAREPa/2/OS4 1.16 9
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I LANT I"El'<I=QRHANCE DA'I'A~"'I'EH
'<UN DAl'E 0 2)/ "I 0 /98
~"PENDXX B AVEBAGE DAXLY~EB LEVEI RuN TXVI:-
09:43:S8 I-IARniS uNXT PAGE RPD39'-888 NOVENBEB 1998 DOCI<ET NO. 8S8-488 CONPLETED BY MARI< W.
I-IALE TELEI~ISONE
< 91 9) 362-2944 DAY AVG. DAILY POWER LEVEL
<HWE-NET)
DAY AVG. DAXLY POWER LEVEL
<HWE-NET) 863 878
~7 I')
I'j3
-28
$ 8 85 27
-30 38
$.$ 6 "8 MEM/DATAREPa/3/OS4
II A
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V
UNIT SHUTDOWNS AND POWER REDUCTION UNIT NAME:
Harris DATE:
12/10/90 COMPLETED BY:
M. W. Hale TELEPHONE:
(919) 362"2944 REPORT MONTH:
November 1990 No.
Date Ti y
p e
Duration (Hours)
R Method of Shutting Down Reactor Licensee Event Report S
System Code 4
Component Code 5
Cause 4 Corrective Action to Prevent Recurrence 90-017 901110 466.8 N/A HTEXCH Unit removed from service to perform maintenance on steam generator "A" due to a primary to secondary tube leak.
The leak was identified by pressurizing the secondary side to 500 psig.
The leaking tube was plugged along with an adjacent tube that exhibited signs of wear.
F:
Forced S:
Scheduled Reason:
A-Equipment Failure (Explain)
B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training 4, License Examination F-Administrative G-Operational Error (Explain)
H-Other (Explain)
Method:
I-Manual 2-Manual Scram 3-Automatic Scram 4-Continued 5-Reduced Load 6-Other Exhibit G-Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161) 5 Exhibit I - Same Source MEM/DATAREPa/4/OS4
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ee
UNIT SHUTDOWNS AND POWER REDUCTION UNIT NAME:
Harris DATE:
12/IO/90 COMPLETED BY:
M. W. Hale TELEPHONE:
(919) 362"2944 REPORT MONTH:
November 1990 No.
Date Tl y
p e
Duration (Hours)
R Method of Shutting Down Reactor Licensee Event Report f System Code 4
Component Code 5
-Cause 4 Corrective Action to Prevent Recurrence 90-018 901 129 0.0 N/A HG zzzzzz Unit was operated at a reduced power
-30$, due to secondary chemistry limitations.
The chemistry was allowed to return to specification and the unit was ramped to 905 power.
F:
Forced S:
Scheduled Reason:
A-Equipment Failure (Explain)
B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training 8, License Examination F-Administrative G-Operational Error (Explain)
H-Other (Explain)
Method:
I-Manual 2-Manual Scram 3-Automatic Scram 4-Continued 5-Reduced Load 6-Other Exhibit G-Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161) 5 Exhibit I - Same Source MEM/DATAREPa/5/OS4
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