ML18009A636

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Insp Rept 50-400/90-13 on 900616-0720.Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Security,Fire Protection,Surveillance & Maint Observations & Review of LERs & Nonconformance Repts
ML18009A636
Person / Time
Site: Harris 
Issue date: 08/07/1990
From: Dance H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18009A635 List:
References
50-400-90-13, NUDOCS 9009050195
Download: ML18009A636 (20)


See also: IR 05000400/1990013

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/90-13

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

June

16 - July 20,

1990

Inspectors;

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Reacto

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Branch

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Division of Reactor Projects

License No.:

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SUMMARY

Scope:

This routine inspection

was conducted

by two resident

inspectors

in the areas

of plant operations,

radiological controls, security, fire protection,

surveillance observation,

maintenance

observation,

review of licensee

event

reports

and nonconformance

reports,

actions

regarding moderator dilution

accidents,

review of the reactor protection

system

manual trip, actions

'regarding

low temperature

overpressure

protection,

and licensee

action

on

previous inspection

items.

Numerous facility tours were conducted

and facility

operations

were observed.

Some of these tours

and observations

were conducted

on backshifts.

Results:

Two violations were identified:

failure to properly implement plant

procedures

during the performance of an incore/excore calibration,

paragraph

6.a;

and failure to properly perform personnel

monitoring prior to leaving

a potentially contaminated

area,

paragraph

2.b(4) (non-cited violation).

A non-cited licensee identified violation is discussed

in paragraph

5.b

regarding

inadequate

testing of the

FHB emergency

exhaust

system.

An unresolved

item is identified in paragraph

6.b regarding

review of

inservice testing data for the boric acid pumps.

REPORT DETAILS

Persons

Contacted

Licensee

Employees

  • J. Collins, Manager,

Operations

  • G. Forehand,

Manager,

gA/gC

J. Garcia-Serafin,

Sr. Reactor

Engineer

  • C. Gibson, Director,

Programs

and Procedures

  • J.

Hammond, Director,

ONS

C. Hinnant, Plant General

Manager

D. Jackson,

Electrical

Foreman - Nuclear

  • M. Jackson,

Supervisor,

Maintenance

D. McCarthy,

NED Site Principal

Engineer

J. Nevill, Manager,

Technical

Support

  • C. Olexik, Director, Regulatory

Compliance

  • A. Poland,

Manager,

ESRC Support

R. Richey,

Manager,

Harris Nuclear Project Department-

C. Rose,

Manager,

gA

J. Sipp,

Manager,

Environmental

and Radiation Monitoring

H. Smith, Manager,

Radwaste

Operation

A. Stalker,

Senior Mechanical

Engineer

R. Stewart, Principal Mechanical

Engineer

D. Tibbits, Supervisor, Shift Operations

  • B. Van Metre, Manager,

Harris Engineering

Support

E. Willett, Manager,

Outages

and Modifications

  • L. Woods,

Engineering Supervisor - Nuclear

Other licensee

employees

contacted

i.ncluded office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

2.

Review of Plant Operations

(71707)

The plant continued in power operation

(Mode 1) for the duration of this

inspection period.

a.

Shift Logs

and Facility Records

The inspector

reviewed records

and discussed

various entries with

operations

personnel

to verify compliance with the Technical

Specifications

(TS)

and the licensee's

administrative

procedures.

The following records

were reviewed:

Shift Foreman's

Log; Control

Operator's

Log; Night Order

Book; Equipment Inoperable

Record;

A'ctive Clearance

Log; Jumper

and Wire Removal

Log; Shift Turnover

Checklist;

and selected

Chemistry/Radiation

Protection

and Radwaste

Logs.

In addition, the inspector

independently verified clearance

order tagouts.

No violations or deviations

were identified.

b.

Facility Tours

and Observations

Throughout the inspection period, facility, tours were conducted

to

observe

operations

and maintenance activities in progress.

Some

operations

and maintenance activity observations

were conducted

during backshifts.

Also, during this inspection period; licensee

meetings

were attended

by the inspectors

to observe

planning

and

management activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence; control

room;

emergency

diesel

generator

building; reactor- auxiliary building; waste processing

building;

fuel handling building; emergency

service water building; battery

rooms;

and electrical

switchgear

rooms.

During these tours, the following observations

were made:

(I)

Monitoring Instrumentation

- Equipment operating status,

area

atmospheric

a'nd liquid radiation monitors, electrical

system

lineup, reactor operating

parameters,

and auxiliary equipment

operating

parameters

were, observed

to verify that indicated

parameters

were in accordance

with the

TS for the current

operational

mode.

(2)

Shift Staffing - The inspectors verified that operating shift

staffing was in accordance

with TS requirements

and that

control

room operations

were being conducted in an orderly and

professional

manner.

In addition, the inspector

observed shift

turnovers

on various occasions

to verify the continuity of

, plant status,

operations

problems,

and other pertinent plant

information during these turnovers.

(3)

Plant Housekeeping

Conditions - Storage of material

and

components,

and cleanliness

conditions of various

areas

throughout the facility were observed

to determine whether

safety and/or fire hazards

existed.

(4)

Radiological Protection

Program - Radiation protection control

activities were observed routinely to verify that these

activities were in conformance with the facility policies

and

procedures,

and in compliance with regulatory requirements.

The inspectors

also reviewed selected

RWPs to verify that the

RWP was current

and that the controls were adequate.

While performing

a plant tour on July 9, 1990, three general

contractor

personnel

were observed

to exit the south

RHR/CS

pump area without performing personnel

contamination

monitoring.

Although the area

was posted to frisk hands

and

feet prior to exiting, the three workers left the area without

frisking.

The inspector notified

HP supervision of this

failure to follow plant procedures.

Subsequently,

the three

workers were counseled,

the frisker was relocated

next to the

door,

and

a

new posting with bolder letters

was placed

on the

door.

This

NRC identified violation is not being cited because

criteria specified in Section

V.A of the

NRC enforcement policy

were satisfied.

NC5 (400/90-13-01):

Failure to follow radiological posting

requirements.

(5)

Security Control - In the course of monthly activities, the

inspectors

included

a review of the licensee's

physical security

program.

The performance of various shifts of the security

force was observed

in the conduct of daily activities, to

include:

protected

and vital area

access

controls;

searching

of personnel,

packages,

and vehicles;

badge

issuance

and

retrieval; escorting of visitors; patrols',

and compensatory

posts.

In addition, the inspector

observed

the operational

status of Closed Circuit Television

(CCTV) monitors, the

Intrusion Detection

system in the central

and secondary

alarm

stations,

protected

area lighting, protected

and vital area

barrier integrity, and the security organization interface with

operations

and maintenance.

(6)

Fire Protection - Fire protection activities, staffing,

and

equipment

were observed

to verify that fire brigade staffing

was appropriate

and that fire alarms,

extinguishing

equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

3.

Surveillance

Observation

(61726)

Surveillance tests

were observed

to verify that approved

procedures

were

being used; qualified personnel

were conducting the tests;

tests

were

adequate

to verify equipment operability; calibrated

equipment

was

utilized; and

TS requirements

were followed.

The following tests

were observed

and/or data

reviewed:

OST-1004,

Power Range

Heat Balance

OST-1013,

1A-SA Emergency

Diesel Generator Operability Test

OST-1036,

Shutdown Margin Calculation

EST-717,

Incore/Excore Detector Calibration

No violations or deviations

were identified.

4.

Maintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify that

correct equipment clearances

were in effect; work requests

and fire

prevention work permits,

as required,

were issued

and being followed;

quality control personnel

were available for inspection activities

as

required;

and,

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the

following maintenance

(HR/JO) activities:

Troubleshooting of inoperable

bank

D group

2 control rods

and post

maintenance

testing in accordance

with procedure

OST-1005,

Control

Rod Verification

Motor operated

valve testing utilizing VOTES test equipment

Troubleshooting of a failed shut steam generator

B blowdown valve

(BD-20) and temporary modification to the automatic

pressure

control

circuit PCR-5386.

No violations or deviations

were identified.

5.

Review of Licensee

Event Reports

(92700)

The following LERs were reviewed for potential

generic

impact, to detect

trends,

and to determine whether corrective actions

appeared

appropriate.

Events that were reported

immediately were reviewed

as they occurred to

determine if the

TS were satisfied.

LERs were reviewed in accordance

with the current

NRC Enforcement Policy.

'a ~

(Closed)

LER 90-15:

This

LER reported

a deficiency in the design of

the emergency

diesel

generator

sequencer

circuit.

This matter

was

previously being tracked

as

an IFI (see

paragraph

10.c of this

report).

The. inspector

reviewed

and verified the licensee's

corrective action

as stated

in the

LER.

b.

(Open)

LER 90-16:

This

LER reported

inadequate

testing of the

FHB

emergency

exhaust

system.

On March 30,

1990, during the performance

of surveillance testing

on this system,

licensee

personnel

identified

a discrepancy

with measured

system flowrate.

Due to turbulent airflow

in the region being measured,

actual

system flowrates were greater

than those

allowed by TS 4.9.12 for test performance.

The licensee

reperformed

the test procedure

which was completed satisfactorily

on

April 27.

Previous test data

was reviewed

by the licensee

and

determined

not to be in compliance with the TS.

A review of other

TS

filtration units

was performed which revealed

no similar problems.

This item is considered

to be

a licensee identified

NCY and is not

cited because

the criteria specified in section

V.G. 1 of the.NRC

Enforcement Policy were satisfied.

5

NC4 (400/90-13-02):

Failure to adequately test the

FHB emergency

exhaust

system.

The

LER will remain

open pending revisions,to test procedures

to

identify acceptable

locations for flowrate measurements

and

comparison of measured

flowrate with permanent

instrumentation.

6.

Review of Nonconformance

Reports

(71707)

Significant Operational

Occurrence

Reports

(SOORs)

and Nonconformance

Reports

(NCRs) were r'eviewed to verify the following:

TS were complied

with, corrective actions

as identified in the reports

were accomplished

or being pursued for completion, generic

items were identified and

reported,

and items were reported

as required

by the TS.

a ~

b.

SOOR 90-92 reported that nuclear instrument detector currents

were

determined

based

on improperly calculated

heat balances.

The

performance of procedure

OST-1004,

Power

Range

Heat Balance,

was

required

at= various steps

during the completion of procedure

EST-717,

Incore/Excore

Detector Calibration

on June

27,

1990.

However, while

performing procedure

OST-1004

on June

26 and 27,

blowdown was left in

service.

This action

was contrary to the requirements

of procedure

OST-1004

step

2 which required the blowdown flow control valves to be

shut.

This action in turn caused

a 1.7 percent error in the normalized

full power nuclear instrumentation currents.

During the subsequent

detector- calibrations,

operating

personnel

alertly identified the

nuclear instrument calibration error.

At this point, licensee

personnel,

without procedural

guidance,

modified the previously taken

'data

from procedure

OST-1004 to account for blowdown remaining in

service.

The program for performing the incore/excore calibration,

detailed in procedure

EST-717,

was rerun

and nuclear instruments

were

subsequently

adjusted.

Although calculatons

were technically correct,

failure to follow procedural

steps of procedure

OST-1004

and

performance of steps

not procedurally

documented

in procedure

EST-717

were collectively considered

a failure to follow plant procedures.

Violation (400/90-13-03):

Failure to follow plant procedures

during

the performance of EST-717

and OST-1004.

Although this matter

was identified by the licensee, it is being

cited due to previous

problems

the licensee

has experienced

in this

area

(90-01-01,

90-02-02).

NCR 90-08 identified improper testing of the boric acid

pumps

as

required

by the licensee's

IST program.

On October 4,

1988 the boric acid

pump impellers were inadvertently

replaced with impellers" which, when tested,

could not meet the

design flow specified in the

FSAR (75 GPH).

The impellers could,

,L

however,

provide the

TS required flow of 30

GPM and the shutdown

requirements

specified

by the

FSAR.

Following the impeller replace-

ment,

a

PCR was written to evaluate

the change in impeller diameter,

but this evaluation

had not been completed

as of May 11,

1990,

almost

two years,

when this item was identified by the

gA organization

during

a modification audit.

The plant response

to this

gA finding

is not due until July 27,

1990,

the licensee

has installed the proper

impellers.

This item is considered

unresolved

pending further

NRC

review of the licensee's

corrective action.

URI (400/90-13-04):

Failure to perform

a timely evaluation of boric

acid

pump test data.

Review of Actions Regarding

Moderator Dilution Accident

(Closed) TI-2515/94:

This inspection

was performed to verify the

licensee's

administrative controls to prevent inadvertent dilution of the

boron concentration

in the reactor coolant system.

The plant

SER

(NUREG 1038, Safety Evaluation Report Related to the Operation of Shearon

Harris

Nuclear

Power Plant, Units

1 and 2, November

1983)

and the

FSAR were

reviewed to determine

which administrative controls the licensee

had

committed to.

As stated

in the

SER, Section 15.4.6,

the licensee

committed

to lock out one reactor

makeup

pump during plant operation in the cold

shutdown condition

and to maintain

a

2 percent

shutdown margin.

The

licensee

subsequently

revised

the

TS to reflect

a variable

shutdown margin

with a minimum value of

1 percent.

This revision was accepted

by the

NRC

staff which= issued

license

amendment

P7

and safety evaluation,

dated

August 16,

1988.

The inspector

reviewed the licensee's

procedures

for

operating in the cold shutdown condition (GP-007,

Normal Plant Cooldown)

and verified that administrative controls were in place to adhere

to the

shutdown margins required

by TS and to lock out one reactor water makeup

pump.

No violations or deviations

were identified.

Review of Actions Regarding

Reactor Protection

System

Manual Trip

(Closed)

TI 2500/14:

This inspection

was performed to verify the

location. of the manual trip circuit in the reactor solid state protection

system.

The licensee's

controlled drawings correctly depicted

the

location of the manual trip circuit located

downstream of output

transistors

93 and

g4 in the undervoltage

output circuit.

No violations or deviations

were identified.

Review of Actions Regarding

Low Temperature

Overpressure

Protection

(LTOP)

(Closed) TI-2500/19:

This inspection

was performed to verify the licensee

had

an effective mitigation system to prevent

severe

pressure

transients

while at

a relatively low RCS temperature.

Reviews of the

mitigation system design,

drawings, plant specific analysis,

administra-

tive controls, operator training,

system maintenance

and modifications,

surveillance testing,

and system descriptions

in the

FSAR and

SER, were

performed.

As described

in the

FSAR, Section 5.2.2. 11, the licensee utilizes two

PORVs

(1RC-114

and

1RC-118), with automatically adjusted

opening

setpoints

that vary as

a function of RCS temperature,

to provide

LTOP.

An alarm has

been provided to alert operators

to increasing

RCS pressure

prior to

PORV actuation.

The

LTOP system is manually enabled

by

operators utilizing a switch on the main control

board

when

RCS

temperature

decreases

below 350 degrees

F.

Also,

a pressurizer

steam

bubble is utilized as

a surge

volume to help mitigate pressure

transients.

The steam bubble is used until the Node

5 (cold shutdown)

condition is approached

when the pressurizer

is filled and solid water

operation is initiated.

While in the solid water condition, pressure

is

controlled with the

CVCS system.

The inspectors

found that the

LTOP system

was appropriately

designed

to

prevent exceeding

pressure limits, had adequate

redundancy of system

components,

and system setpoints

were supported

by a plant specific

analysis.

The SER, section 8.4.8, incorrectly assumed

that the power

supplies for the

PORVs were safety related.

Although the

PORVs are

classified

as safety related

due to their function as

an

RCS pressure

boundary,

the control air system for these

valves is not safety related

or seismically qualified.

The air valve solenoids

receive

DC power from

the non-class

1E balance of plant uninterruptible

DC power supply which

is provided with a backup battery source.

Although these

systems

are not

safety related,

the inspector verified adequate

redundancy

existed

and

that the system descriptions

provided in the

FSAR were correct.

Administrative controls were adequately

addressed

by the

TS and

implemented

by plant procedures.

However, the inspector

found that the

licensee's

operation in the solid water condition did not optimize the

use of a pressurizer

nitrogen bubble which would also act as

a pressure

buffer.

System modifications

and maintenance

were reviewed.

Nodification

PCR

3241,

LTOPs Operation in Nodes

1,

2 and 3,

was

implemented

to defeat the

automatic

arming of the

LTOP system

and installed

an inhibit switch

requiring operator action to enable

the system.

This change

was

necessitated

due to

a potential

unanalyzed

condition which could occur

during

a main steam line break or steam generator

tube rupture accident.

This problem,

and associated

corrective action,

was reported to the

NRC

via

LER 88-11.

Nodification

PCR 3965,

Cycle

2

LTOP Setpoints,

changed

the system setpoints

in order to comply with new heatup/cooldown limit

curves established

in accordance

with NRC Generic Letter 88-11,

Regulatory

Guide 1.99

Rev.

2 Radiation Embrittlement of Reactor

Vessel

Naterials.

The inspector

found these modifications to be appropriate

and

post maintenance/modification

testing

adequate.

A review of the licensee's

surveillance testing of this. system revealed

that periodic surveillance tests

were being performed,

the system

was

tested

before

each cold shutdown,

and that the

PORVs were included in the

licensee's

IST program to be full. stroke tested

during cold shutdown.

In response

to

a recent reanalysis

of the steam generator

tube rupture

accident,

and

NRC Generic Letter 90-06, Resolution of Generic

Issue 70,"

Power-Operated

Relief Valve and Block Valve Reliability", and Generic

Issue

94, "Additional Low-Temperature

Overpressure

Protection for Light

Water Reactors"

pursuant

to

10 CFR 50.54(f), the licensee

is considering

upgrades

to the plant

TS and

PORVs to enhance

protection

system

availability.

In correspondence

to the

NRC dated

December

15,

1989, the

licensee

committed to upgrade

the

PORV manual actuation

components,

controls,

and

power supplies,

to safety

grade for use in the tube rupture

event.

The licensee

was encouraged

to upgrade

the

LTOP components

as

well.

No violations or deviations

were identified.

10.

Licensee Action on Previously Identified Inspection

Findings

(92702

5

92701)

a.

(Closed)

IFI 400/90-04-01:

Review the licensee's

activities to

revise

procedure

OST-1092,

1B-SB Residual

Heat

Removal

Pump

Operability,

and to improve records of corrective action.,

The licensee

has revised

procedure

OST-1092 to reflect appropriate

acceptance

criteria for pump flow and

has

changed

procedure

ISI-203,

ASt1E Section

XI Pump

and Valve Program Plan, to provide an

attachment for documenting corrective action.

b.

(Closed)

IFI 400/90-04-02:

Review the licensee's

development of

acceptance

criteria for procedure

OST-1024,

Onsite

Power

Distribution Verification.

C.

Since specific voltage criteria was not included in the

TS

acceptance

criteria, the licensee

decided to revise procedure

OST-1024 to delete it.

Instead,

the licensee

has taken credit for

this criteria in routine operator logs.

(Closed)

IFI 400/89-21-03:

Contact Overloading of Potter-Brumfield

Relays.

This matter

was previously discussed

in

NRC Inspection Report

50-400/90-10

and

was identified as

a deficiency in

NRC Inspection

Report 50-400/90-200

(item 400/90-200-06).

The licensee

has

issued

LER 90-15 describing this event

and corrective actions

taken to

prevent recurrence.

The test report (Corporate Consulting

and

Development

Company,

LTD. dated July 12,

1990)

was reviewed

by the

inspector.

For record

purposes

this item will be closed

and

possible

enforcement

action tracked

by deficiency 400/90-200-06.

l

'

d.

(Closed)

IFI 400/89-13-01:

Failure of Brown Boveri LK-16 breakers

to open

on demand.

The licensee

has

completed onsite testing,

design verification with

Brown Boveri,

and successful

overcurrent (trip and latch) testing at

20K, 40K and

50K amperes

on.two different breakers

at an independent

testing facility.

Modification PCR 3510,

480 Volt Drawout Breakers

Used

As Contactors,

which will install the required breaker design

changes,

is due for initial implementation

by July 27,

1990.

Completion of safety related

breaker modifications will be completed

at the earliest available outage.

All non safety related

breakers

will be modified prior to the completion of the

1991 refueling

outage.

The modification consists of removal of booster springs

and

torsion springs, verification of opening spring tension,

and

replacing of arcing contact

compression

springs.

Additionally, the

licensee will provide maintenance

personnel

with formalized training

by Brown Boveri

and will perform preventive maintenance

on the

breakers

at least

once per

100 breaker cycles.

This matter

was

discussed

with NRC Region II specialist

inspectors

who considered

the licensee's

action adequate

to close this item.

ll.

Exit Interview (30703)

The inspectors, met with licensee

representatives

(denoted

in paragraph

1)

at the conclusion of the inspection

on July 19,

1990.

During this

meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violation, Unresolved

Item,

and Inspector Follow-up item addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify as proprietary

any of the materials

provided to or reviewed

by the inspectors

during this inspection.

Item Number

Descri tion and Reference

400/90-13-01

400/90-13-02

400/90-13-03

400/90-13-04

NC5:

Failure to follow radiological posting requirements

(paragraph

2.b.4).

NC4:

Failure to adequately

test the

FHB emergency

exhaust

system

(paragraph

5.b).

VIO:

Failure to follow plant procedures

during the

performance

of EST-717

and

OST-1004

(paragraph

6.a).

URI:

Failure to perform

a timely evaluation of boric acid

pump test data

(paragraph

6.b).

12.'cronyms

and Initial i sms

ASME

CCTV

CFR

Ameri can Soci ety of Mechani cal

Engineers

Closed Circuit Television

Code of Federal

Regulations

10

CS'VCS

EDG

EST

FHB

FSAR

GP

GPN

HP

IFI

IST

LER

LTOP

NCR

NCV

NED

NRC

ONS

OST

PCR

PORV

QA/QC

RCS/RC

RHR

RWP

SER

SOOR

TS

URI

YIO

WR/JO

Containment

Spray

Chemical

Volume Control

System

Emergency Diesel

Generator

Engineering Surveillance Test

Fuel Handling Building

Final Safety Analysis Report

General

Procedure

Gallons per Minute

Health Physics

Inspector Follow-up Item

Inservice Testing

Licensee

Event Report

Low Temperature

Overpressure

Prot

Non-Conformance

Report

Non-Cited Violation

Nuclear Engineering

Department

Nuclear Regulatory

Commission

Onsite Nuclear Safety

Operations

Surveillance Test

Plant

Change

Request

Power Operated Relief Valve

Quality Assurance/Quality

Control

Reactor

Coolant System

.

Residual

Heat

Removal

Radiation

Work Permit

Safety Evaluation Report

Significant Operational

Occurrenc

Technical Specification

Unresolved

Item

Violation

Work Request/Job

Order

ection

e Report