ML18009A277

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Safety Insp Rept 50-400/89-21 on 890826-1006.Violation Noted.Major Areas Inspected:Operational Safety Verification, Surveillance Observations,Maint Observations,Onsite Followup of Events & Reactor Operator License Verification
ML18009A277
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 11/18/1989
From: Dance H, Shannon M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18009A275 List:
References
50-400-89-21, NUDOCS 8912070318
Download: ML18009A277 (11)


See also: IR 05000400/1989021

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/89-21

Licensee:

Carolina

Power and Light Company

P. 0.

Box 1551

Raleigh,

N.

C. 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

Irspector;

anno

i

Approved by:

/If~>v~

'nce,

ection

ief

Division of Reactor Projects

SUYMARY

License No.:

NPF-63

a

e

gne

ate

gne

Scope.

This routine,

safety

inspection

was

conducted

in the

areas

of operational

safety verification,

survei llance

. observations,

maintenaIice

observations,

" onsite followup of events,

and reactor operator license verification.

Results:

MiThiI'I the areas

inspected

three violations were identified,

one cited and

two

non-cited.

The cited violation involved

a failure to adequately

evaluate

the

suitability of ccmmercial

grade

items

used

in safety

grade

applications,

paragraph

7.

The

two non-cited

licensee

identified violations involved:

a

failure to install

the operatiIIg floor equipment

hatch prior to spent fuel

movement,

paragraph

P.a;

and

a failure to submit

a written report

as required

by 10 CFR 50 Appendix H, Section III.A, paragraph

5.a.

Two Inspector.

Followup Items

were identified:

emergency

service

water flow

inadequacies

versus

FSAR requirements,

paragraph

2.b;

arid contact overloading

of Potter-Brumfield relays,

paragraph

3.a.

89g2O70318

8yggO8

PLIER

ADOCK O. OOO4CIO

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FDC

'EPORT

DETAILS

1.

Persons

Contacted

Licensee

Employees

D. Braund, Supervisor,

Security

  • J. Collins, Manager,

Operations

  • G. Forehand,

Director,

OA/gC

  • C. Gibson, Director, Programs

and Procedures

.*J.

Hammond,

Manager,

Onsite Nuclear Safety

  • C. Hinnant, Plant General

Manager

  • T. Yiorton, Manager,

Maintenance

C. Olexik, Supervisor, Shift Operations

  • R. Richey, Manager,

Haris Nuclear Project Department

  • J. Sipp, Manager,

Environmental

and Radiation Monitoring

H. Smith, Supervisor,

Radwaste

Operation

D. Tibbits, Director, Regulatory Compliance

B.

Van Metre, Manager, Technical

Support

  • E. Willett, Yianager,

Outages

and Yiodifications

Other

licensee

employees

contacted

during this

inspection

included

engineers,

operators,

mechanics,

security force members,

technicians,

and

administrative personnel.

  • Attended monthly exit. interview on October 12,1989.

Acronyms

and initialisms

used

in the report

are listed in the last

paragraph.

2.

Operational

Safety Verification (71707)

The inspector

observed

control

room operations,

reviewed applicable logs,

and

conducted

discussions

with various

licensee

personnel.

The oper-

ability of various

emergency

systems,

the

adherence

to

LCO action

statements,

the

proper

return

to service of components,

and

adequate

switching

and

tagging

records

were

observed

or reviewed during routine

plant tours.

Site security

and portions of the Radiological

Protection

Program

were also evaluated

during the plant tours.

The inspector

also

attended

various plant meetings,

such

as

Maintenance,

Technical

Support,

Outage Planning,

and Morning Management;

a.

On August

27,

1989,

plant

personnel

were transferring

spent

fuel

assemblies

from the spent fuel cask to the spent fuel storage

pool,

when the operator

noted

abnormal

noise

comino from the north end of

the

fuel

handling

building.

Upon investigating

the

noise,

he

discovered

that the operating floor equipment

hatch

had

riot been

installed.

The

Shearon

Harris Unit

1

FSAR Section 9.1.4:2.3

assumes

that

no

irradiated

fuel will

be

handled

or transported

inside

the fuel

handling building unless

the operating floor equipment

hatch to the

unloading

area

is in place.

The

removal of the hatch cover could

prevent the

FHB Emergency

Exhaust

System from performing its intended

function in the event of a postulated

fuel handling accident.

The

licensee

halted

fuel

movement

and installed

the operating floor

equipment

hatch.

The licensee

also identified this in LER-89-15,

which detailed

the procedures

that would be revised

and reviewed

by

personnel.

This licensee

identified violation (89-21-04)

is not

being cited

becuase

criteria specified

in Section

Y.G.1 of the

NRC

Enforcement Policy were satisfied.

I

Emergency

Service Mater Flow Balance Inconsistencies.

Due to ongoing service water problems identified by various industry

events

and initiatives, plant management

requested

that the Onsite

Nuclear Safety

Group perform

a Service Water System Assessment.

The

assessment

was

completed

and given to plant management

on August 21,

1989.

The

assessment

contained

18 recommendations,

two concerns

questioned

whether

the

system

could supply

the required

flow to

safety related

components

and

a. third concern questioned

the

ESW pump

performance.

Due to the

recommendations,

the Technical

Support Staff was tasked

with developing

and performing

a special test to determine

system

and

pump

performance.

The test

was- performed

on

August

31

and-

September

1,

1989,

and the test results

indicated that flow values

listed in the

FSAR could not be met. "

Review of startup test data

and further reviews of FSAR sections

were

performed.

It was also

noted that when'he

ESM pump took suction

from the

main reservoir

ESW flow to the

emergency

diesels

was

abnormally low (approximately

50% of that indicated in FSAR);

Since

this placed

the emergency diesels

in ieopardy,

the operations

manager

immediately restricted

placing the

ESW suction

on the main reservoir

until this descrepancy

could

be resolved.

The licensee

continued

to investigate

the service water issues

and

performed

a

reduced

SW Flow Test to the emergency

diesels.

It was

found that

the greatly

reduced

SM flows to the

emergency

diesels

would still provide

adequate

cooling.

Additionally, further reviews

of cooling requirements for component cooling water indicated that

as

found flows were acceptable

even

though they did not meet the

FSAR

Design

Flows.

The resident

reviewed

the related test data

and noted thai TS 3.7.5,

Ultimate Heat Sink, requires

that both main and auxiliary reservoirs

must

be operable.

Therefore,

the

ESM system would have to be able to

take

a suction

from both reservoirs

and supply all safety-related

loads.

A telephone

conference

was

held

between

plant management,

'egion

II management,

and

NRR management.

Discussions

centered

on the

plants ability to adequately

supply cooling to essential

components

during

emergency situations.

By using test results

and engineering

evaluations

the licensee

could

show plant safety

was not jeopardized

and

informed

NRC

management

that

the

ESW flow issues

would

be

actively

pursued

and

resolved.

Additionally,

NRR confirmed

the

resident's

TS interpretation

concerning

ESW supply capabilities

from

both the main

and auxiliary reservoir.

The licensee

did not agree

with this interpretation

(based

on

FSAR documentation),

but indicated

that they would comply until the matter could

be formally resolved.

Subsequent

testing

was

performed

and the test results indicated that

previous test results

could

have

been in error and that flow to the

emergency

diesels

was actually greater

than previously thought.

The.

concern with the

ESW system flow balance

and the resolution of actual

system

flows versus

th~ flows detailed

in the

FSAR are identified as

an Inspector

Followup Item (89-21-02).

3.

Surveillance

Observation

(61726)

Portions of the following surveillance

inspections

and tests

required

by

the

TS were observed

or reviewed

by the inspector:

MST-I0139

EPT-33

EPT-134T

MST-0006

EPT-141T

EPT-140T

OST-1044

MST-I0205

S/G

3C Steam/feedwater

Flow Protection

Set IY

Operational

Test

Emergency

Safeguards

Sequencer

System Test

ESW Flow Balance Test

480

VAC Molded Case Circuit Breaker Test

"B" ESW Header

Flow/Pressure

Test

EDG Minimum Flow S.W. Test

ESFAS Train "A" Slave

Relay Test

Refueling Water Storage

Tank Liquid Level

Channel

II (L-991) Operational

Test

OST-1215

Emergency Service Water Sys'em Operability

The inspector verified that the surveillances

were performed in accordance

with adequate

procedures;

instrumentation

was calibrated;

limiting

conditions

were

met;

test

results

mei acceptance

criteria

and

were

reviewed

by personnel

other

than

the

individual directing

the test;

deficiencies

identi ied

during

the test

were

properly

reviewed

and

resolved

by appropriate

management

personnel;

and

personnel

conducting

the test were qualified.

On

September

11,

1989,

Engineering

Periodic

Test

EPT-33,

Emergency

Sequencer

System Test,

was

be'ing performed

by 'plant personnel.

When the

"Test Stop" pushbutton

was actuated

the

ESW Sequencer

Test Relay failed to

reset

and

ESW

Pump

1B-SB started.

The test circuit relay

is

a

Potter-Brumfield

Model

PMDR137-8.

The licensee attributed the failure to

overloading of the relay contacts.

PCR 4765

was generated

to evaluate

the

overloaded

contacts

and to verify other overloadings

do not exist in the

sequencer

circuitry.

This item is also identified by the licensee

in LER

89-16.

The inspector will continue to follow the licensee's

action

on

this

matter.

This

is

identified

as

an

Inspector

Followup

Item:

(89-21-03), Contact Overloading of Potter-Brumfield Relays.

No violations or deviations

were identified.

4.

Monthly Maintenance

Observation

(62703)

The inspector

observed/reviewed

the following'aintenance activities of

safety-related

and

non safety-related

systems

and components

to ascertain

that

they

were

conducted

in

accordance

with

approved

procedures,

regulatory

guides,

industry codes

and standards,

and were in conformance

with TS:

Molded Case

ITE Circuit Breakers

(IFI 89-13-0P)

The

inspector

continued

to follow the licence's difficulties with

molded case circuit breakers

manufactured

by Siemens

Automated,

Inc.

Further testing of 100 AflP ITE breakers

was conducted

using

a bneaker

testing

unit manufactured

by Multi-ANP Corporation.

The breaker

testing continued to show failures of the

100

ANP ITE breakers.

One

breaker test confirmed two poles tripping on instantaneous

current of

500

AMPs

and

the third pole failing to trip at

3500

ANPs.

The

acceptance

criteria for the

100

AMP breakers

is

1200 to 2000

ANPs.

Additional testing using the Multi-AMP unit was performed

on various

40-90

AMP ITE breakers.

The test results

met the instantaneous

trip

acceptance

criteria,

which at this

time indicates

the

breaker

problems

are confined to only 100

AMP ITE-480V molded

case circuit

breakers.

This item remains

open.

b.

Brown Boveri LK16 Switchgear

(IFI 89-13-01)

The inspector

continued

to follow the licensee's

difficulties with

Brown Boveri

LK16 switchgear

breakers.

During this inspection period

three additional failures to open

on

demand

occurred.

Two breakers

were used in circuits with motor controllers

and were not expected

to

have

opening

problems.

.Slight pitting of the arcing contacts

caused

by opening

under load is the primary cause of breaker failure.

Eighteen

safety

related

LK16 breakers

are installed at the Harris

Plant.

Eight are cycled quarterly to verify operation.

Ten are

supplies

for motor control

centers

and

cannot

be cycled without

affecting plant operation.

Breaker modifications are being performed

by Brown Boveri, but at

a much slower rate than originally planned.

Additional problems

have

been

noted in that the

openinq

stops

are

being

damaged

by

the

opening

force of the

breaker

contacts.

Resolution of this

problem will be closely monitored.

This item

remains

open.

c ~

Kapton Wiring Failure

The licensee

experienced

a

second failure of Kapton wiring used

on

the limit switches for the

Steam Line

PORVs.

The failure caused

a

ground

on the vital

DC bus.

During

PORV testing,

the ground

became

intermittent

and

I&C personnel

were

sent

to investigate.

After

opening the junction boxes the ground disappeared.

The Kapton wiring

was

subsequently

replaced. 'he

licensee

has

determined

that

mechanical

interaction

during installation or removal

of the limit

switch

assembly

can

cause

minor

damage

to the

insulation

and

subsequent

exposure

to moisture

can lead to an eventual

breakdown of

the insulation.

The licensee

is planning to inspect

various plant

installations

of

Kapton wiring to

determine

the extent of the

problem.

No violations or deviations

were identified.

~

~

~

~

5.

Onsite Followup of Events

(93702)

a 0

b.

On

September

3,

1988,

a material

specimen,

required

to monitor

change

. in fracture

toughness

properties

in the reactor

vessel

beltline region,

was

removed

from the reactor vessel.

A technical

report is required to be submitted within one year after the specimen

is withdrawn,

as specified

in

10 CFR 50 Appendix

H Section III.A.

Due to revisions

in the original test report,

the technical

report

was

not submitted to the

USNRC as required within one year

and the

licensee failed to request

an extension for reporting.

The licensee

informed the

Resident

Inspector

and

NRR on September

5,

1989, that

the report

was late.

The technical report

was submitted

on September

5,

1989.

This licensee identified violation (89-21-05) is not being

cited

because

criteria specified

in Section

Y.G.1 of the

NRC

Enforcement Policy were satisfied.

On September

21,

1989,

the plant experienced

an

EHC oil leak.

The

roving auxiliary operator

discovered

the leak during his rounds

and

isolated

the

broken instrument line to the

"A" EHC

pump discharge

filter differential pressure

instrument.

Approximately three gallons

of oil were lost

from .the

pencil

sized

leak.

The operator's

effectiveness

is considered

excellent

because

this item was found at

2: 15 a.m.

and could have resulted in a plant trip if not discovered.

.,a

6.

Reactor Operator

License Ver'ification.

I

In response

to

a

regional

concern

over non-qualifiation of licensed

operators

from

a varity of causes,

Resident

Action 89-34

was initiated.

The following are the findings at Harris.

a.

Reveiw of Administrative Procedures

(1)

The

on-duty Shift

Foreman

is

provided with current license

'tatus

for all watchstanders

by use of a software

program which

maintains current license. status..

I

(2)

The maximum time between

a disqualifying event

and notification

of. on shift operations

management

does

not appear

to

be

a

problem.

It was

observed

that

when

an individual failed

a

portion of the requalification examination,

he was

removed from

active status .inmediately

by telephone

and'memo.

(3)

Procedures

require

proper turnover

and

assumption

of license

duties.

Qi

b.

Two back shift supervisors

were able

to, show the up-to-the

minute

status of each watch person.

c.

A list of all persons disqualified since initial plant operations

was

obtained.

The activities of two people

on the list were reviewed

and

neither

were found to have stood

a license required watch during the

time they were not qualified.

d.

The verification of qualifications

are maintained

by the on-shift

clerk and are maintained

up to date

on

a daily basis.

e.

High failure rates

have not been

an issue at the Harris Plant

and the

shifts are adequately

staffed.

No violations or deviations

were identified.

7.

Action on Previous

Inspection

Findings

(92701)

(Closed)

URI 89-17-01, Potentially Inadequate

Commercial

to Safety

Grade

Dedication.

After further review, it was determined that

PCR 4007, which

reviewed

the acceptability of use of commercial

grade

ITE breakers

in

safety

grade

applications,

was

inadequate

in that it assumed

that

no

physical

changes

took place in the breaker.

The manufacturer

had modifed

the breaker in that the voltage rating was changed

from 600 Yac to 480 Vac

and

the

instantaneous

trip range

was

changed

from 600-1000

ANPS to

1200-2000

AMPS.

The Site Procurement

Group also 'noted that there

was

an

identifiable weight difference

between

the old model

and

new model

ITE

breakers.

'0

CFR Part

50, Appendix B, Criterion III, Design Control, requires that

measures

be established

for the selection

and review for suitability of

materials,

parts,

equipment,

and

processes

that

are essential

to the

safety-related

functions

of structures,

systems

and"

components.

Commercial

grade

ITE molded

case circuit breakers

were. installed in-

safety-related

electrical

systems

and

the

review for suitability of

equipment

by the licensee's

Engineering

Department

was

inadequate.

The

breakers

were physically

changed

by the manufacturer

and

the

seismic

qualification of the breakers

was

not verified prior to installation in

safety related

applications.

Further,

the modified breakers

were not

fully qualified

by testing

in that all of the

required critical

characteristic

tests (i.e.,

a dielectric test

between. the line and load

terminals with the breaker

open,

a full load starting current test, contact

resistance

measurement

with the

breaker

closed,

or testing

with the

breaker

properly oriented)

were not considered

or performed.

This

URI is

closed

and transferred to a,violation:

Failure to Adequately Eva'luate

the

Suitability of Commercial

Grade

Items

Used in Safety

Grade Applications

(89-21-01)

One violation and

no deviations

were identified.

8.

Exit interview

~

~

The

ins ectio

p

n

scope

and

findings

were

summarized

during

management

interviews throughout the reporting period

and

on October

12,

1989, with

those

persons

indicated in paragraph

1.

The inspection findings addressed

below and in the report

summary were discussed

in detail.

The licensee

acknowledged

the inspection findings

and did not identify as proprietary

any material

reviewed

by the inspector during the inspection.

Item Number

89-21-01'9-21-02

89-21-03

89-21-04

89-21-05

Descri tion/Reference

Paraora

h

VIOLATION -

Inadequate

Review for Suitability of

Commerical

Grade

Items in Safety

Grade Applications;

paragraph

7.

IFI

-

Emergency

Service

Water

Flow

Balance

Inconsistenicies;

paragraph

2.b.

IFI - Contact Overloading of Potter-Brumfield Relays;

paragraph

3.a.

Licensee

Identified Violation - Spent

Fuel

Movement

with

Operating

Floor

Equipment

Hatch

Removed;

paragraph

2.a.

Licensee

Identified Violation -

Failure

to

Make

Technical

Report

Within

Timeframe

of

10 CFR 50

Appendix H, III.A; paragraph

5.a.

Acronymns

and initialisms.

ALARA

AMSAC

ATWS

ECCS

EDG

EHC

ESFAS

ESW

FHB

FSAR

IFI

LCO

LER

MCB

MFP

MS

MSI V

MST

NRC

NRR'P

OST

PCR

.

PIC.

Cab

PYiTR

PORV

QA

QC

RAB

RCDT

RCS/RC

RHR

RPS

RTD

RWP

SF

SG

SIS

STA

.,SW

TFW

TS

URI

VAC

WR/JO

As Low As Reasonably

Achievable

ATWS Mitigation System Actuation Circuitry

Anticipated Transient Without Scram

Emergency

Core .Cooling System

Em rgency Diesel

Gene'rator

Electro-Hydraulic Control

Engineered

Safety Features

Actuation System

Emergency Service Water

Fuel Handling Building

Final Safety Analysis Report

Inspector

Followup Item

Limiting Condition for Operation

Licensee

Event Report

Main Control

Board

Main Feed

Pump

Main Steam

Main Steam Isolation Valve

Maintenance

Surveillance Test

Nuclear Regulatory

Commission

Nuclear Reactor

Regulation

Operating

Procedure

Operations

Surveillance Test

Plant Change

Request

Primary Instrument Control Cabinet

Post Maintenance

Test Requirements

Power Operated

Relief Valve

Quality Assurance

Quality Control

Reactor Auxiliary Building

Reactor

Coolant Drain Tank

Rea'ctor Coolant System

Radiation

Heat

Removal

System

Reactor Protection

System

Resistance

Temperature

Detector

Radiation

Work Permit

Spent

Fuel

System

Steam Generator

Safety Injection Signal

Shift Technical

Advisor

Service Water

Temperature - Feedwater

Technical Specification

Unresolved

Item

Volt A.C.

Work Request/Job

Order

1