ML18005A580
| ML18005A580 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 08/31/1988 |
| From: | Hale M, Watson R CAROLINA POWER & LIGHT CO. |
| To: | NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
| References | |
| HO-880184-(O), NUDOCS 8809140289 | |
| Download: ML18005A580 (9) | |
Text
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cS'CC SION NBR:8809140289 DOC.DATE: 88/
NOTARIZED:
NO DOCKET FAC,IL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH.NAME AUTHOR AFFILIATION HALP,M.
Carolina Power 6 Light Co.
WATSON,R.A.
Carolina Power a Light Co.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
Monthly operati t for Aug 1988 for Harris Nuclear Power Plant Unit 1. /88090 ltr.
DISTRIBUTION CODE:
IE24D OPIES RECEIVED:LTR
(
ENCL /
SIZE:
TITLE: Monthly Operating Report (per Tech Specs)
NOTES:Application for permit renewal filed.
D 05000400 RECIPIENT ID CODE/NAME PD2-1 LA BUCKLEY,B INTERNAL: ACRS AEOD/DSP/TPAB NRR/DLPQ/PEB 11 EP RPB 10 REPTILE Ol EXTERNAL EGStG WILLIAMSg S NRC PDR COPIES LTTR ENCL 1
0 1
0 10 10 1
1 1
1 1
1 1
1 1
1 1
1 RECIPIENT ID CODE/NAME PD2-1 PD AEOD/DOA ARM TECH ADV NRR/DOEA/EAB 11 NUDOCS-ABSTRACT RGN2 LPDR NSIC COPIES LTTR ENCL 5
5 1
1 2
2 1
1 1
1 1
1 1
1 1
1
/
h h
D TOTAL NUMBER OF COPIES REQUIRED:
LTTR 31 ENCL 29
DOCKET NO.:
050-400 UNIT:
Harris Unit 1
DATE:
August 1988 COMPLETED BY:
Mark Hale OPERATIONS
SUMMARY
Harris Unit 1 operated at a 0.0 percent Availability Factor for the month of August with a -1.66 percent capacity factor.
There was one continued offline refueling outage, the refueling outage is in progress.
Details are provided on the Unit Shutdowns and Power Reduction Sheet.
I There are 157 fuel assemblies and 52 new fuel assemblies in the Harris Unit 1
spent fuel pool and 0 assemblies in the new fuel pool.
Fuel insert shuffle completed and fuel reload is in progress.
157 fuel assemblies will be reloaded into the reactor and 52 assemblies will remain in the Harris Unit 1 spent fuel pool for storage.
8809i40289 88083i PDR ADOCK 050004DO R
PNU MEM/DATAREPa/1/OS1
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" RUN DA'fE 09/06/88 RUN TIME 08: 43: 33 F'LANT F'ERFQRMANCE DATA SYSTEM OF'ERAT ING DATA REF'ORT HARRIS UNIT PAGE RPD36-000 OF'ERAT IHG STATUS DOCKET HO. 050-400 COMF'LETED BY MARK M.
HALE TELEF'HOHE (919)362-2944 3.
4 ~
I 4
6.
7.
8.
UNIT NAME:
I.IARRIS UNIT I
NOTES I
REF'ORT ING F'ER lOD:
AUGUST 88 I
LICENSED THERMAL F'OWER (MMT): 2775 Fuel insert shuffle completed and HAMEF'LATE RATING (GROSS MWE): 950.9 I <<el <<l-d in p<<S<<ss.
ELECTRICAL RATIN(
( HET MWE )
~
9QQ Q
I assemblies will be reloaded into MAX DEF'ENDABLE CAF'ACITY (GROSS MME): 920.0 I t"e ~~~~t~~ and
~2 will remain I
MAX DEPENDABLE CAPACITY (NET MWE): 860.0 IF Cl-IAHGES OCCUR ZN CAF'ACITY RATINGS
( ITEMS 3 THRU 7)
SINCE LAST REF'ORT, GIVE REASONS:
N/A 18.
F'OWER LEYEL TO WlIICI I RESTRICTED IF ANY
( NET MWE):
None REASONS FOR RESTRICTION IF ANY:
N/A Tl-IIS MONTH YR TO DATE CUMUL ATIVE 33.
14.
15.
f6.
17.
f8.
.l Q 4
4 J
23m HOURS IH REPORTING PERIOD NUMBER OF I-IQURS REACTOR CRITICAL REACTOR RESERVE SHUTDOWN HRS HOURS GENERATOR ON LINE UNIT RESERYE SHUTDOWN HOURS GROSS Tl-IERMAL ENERGY GEH.
(MWH)
GROSS ELEC.
ENERGY GEN.
(MWH)
HET ELEC.
ENERGY GENERATED (MMH)
UNIT SERYICE FACTOR UNIT AVAILABILITYFACTOR UNIT CAP.
FACTOR (USING MDC NET)
UNIT CAF'.
FACTOR (USING DER HET)
UNIT FORCED OUTAGE RATE SHUTDOWHS SCI-IED.
OYER NEXT 6 MONTHS None 744.00
.08
.00
.00
.00
.00
.00
-18689.88
.00
.08
-3.66
-1.58
.00 (TYF'E, DATE, 5855.00 4877.65
.00 4865.05
.00 33106387 AD )6 4396889.00 4184219.88 83.09 83.09 81.5$
77.89 3.98 AND DURATION 33732.88 9327.54
.00 9188.65
.80 24256532.52 8862(87.88 7483048.00 78.46 78.46
- 74. 2'9 70.99
- 7. 33 QF EACH):
- 25. IF SHUTDOWN AT END OF REF'ORT F'ERIOD, ESTIMATED DATE OF START UP: 10/03/SS UNITS lN TEST STATUS (F'RIOR TO COMMERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION MEN/DATAREPa/2/OSl
)C CPKL. CO' RL~H DATE RUH TIHE 09/OE)/88 08:44:12 PLANT F'ERFORHAHCF DATA SYSTEH APF'EHDIX B
AVERAGE DAILY POWER LEVEL I-IARRIS l3N IT F'AGE RPD39-006 AUGU, T 1988 DAY AVG. DAILY F'OWER LEVEL (HWE-NET) l)9 DOCKET NO. e5e-4ee COHF'I ETED BY HARK W.
HALL=.
TELEPHONE (919)362-2944 DAY AVG. DAILY F'OWER LEVEL (HWE-HET)
-30
-18
')5 30
.)7 28 1.16 8
MEM/DATAREPa/3/OS1
i(
~ t
UNIT SHUTDOWNS AND POWER REDUCTION DOCKET NO,:
050-400 UNIT NAME:
Harris DATE:
9/6/88 COMPLETED BY:
M. W. Hale TELEPHONE:
(919) 362-2944 REPORT MONTH:
AUGUST 1988 No, Date Duration (Hours)
R Method of Shutting Down Reactor Licensee Event Report /f System Code 4
Component Code 5
Cause II, Corrective Action to Prevent Recurrence 88-017 880730 744,00 88-018 ZZ ZZZZZZ Unit ramped down to off line for refueling outage During the ramp down the running mainfeed Pump (1B) tripped on low flow due to a recirc valve failing to open on load decrease, As a result, both motor driven AFW pumps started as required'he cause of the mainfeed pump (IB) trip was determined to be a
low setpoint on the recirculation flow s~itch.
The flow switch had drifted out of calibrations Corrective action includes:
recalibration and a more frequent calibration frequency to prevent recurrence, F:
Forced S:
Scheduled Reason:
A-Equipment Failure (Explain)
B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training 4 License Examination F-Administrative G-Operational Error (Explain)
H-Other (Explain)
Method:
I-Manual 2-Manual Scram 3-Automatic Scram 4-Continued 5-Reduced Load 6-Other Exhibit G-Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161 )
Exhibit I - Same Source
" Corrective action to prevent recurrence as per the License Event Report
V l
1
CRQE Carolina Power & Light Company HARRIS NUCLEAR PROJECT P. 0.
Box 165 New Hill, North Carolina 27562 SEP Q 8 )988 File Number,'SHF/10-15505 Letter Number.'O-880184 (0)
Document Control Desk United States Nuclear Regulatory Commission Washington, D.C.
20555 HARRIS NUCLEAR PROJECT DEPARTMENT UNIT NO ~
1 DOCKET NO. 50-400 LICENSE NO. NPF"63 MONTHLY OPERATIONS REPORT
Dear Sirs:
In accordance with Technical Specifications 6.9.1.5 for the Harris Nuclear Power Plant, Unit No.
1, Carolina Power
& Light Company herewith submits the report of operation statistics and shutdown experience for the month of August 1988.
Yours very truly, R. A. Watson Vice President Harris Nuclear Project MWH'tbb Enclosure cc'Dr. J. Nelson Grace (NRC)
Messrs.
J.
M. Taylor (NRC)
G. F. Maxwell (NRC-SHNPP)
R.
G. Oehl (DOE)
MEM/MoOperRep/1/OS1