ML17348B233

From kanterella
Jump to navigation Jump to search
Operational Readiness Assessment Team Insp Repts 50-250/91-38 & 50-251/91-38 on 910909-13.Violations Noted. Major Areas Inspected:Licensee Overall Operational Readiness Following Recent Outage
ML17348B233
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 10/18/1991
From: Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17348B231 List:
References
50-250-91-38, 50-251-91-38, NUDOCS 9111200219
Download: ML17348B233 (41)


See also: IR 05000250/1991038

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

U. S.

NUCLEAR REGULATORY COMMISSION

REGION II

OPERATIONAL READINESS ASSESSMENT

TEAM (ORAT)

INSPECTION

1

Report Nos.:

50-250/91-38

and 50-251/91-38

Licensee:

Florida Power

and Light Company

9250 West Flagler Street

Hiami,

FL

33102

4

Docket Nos.:

50-250/91-38

and 50-251/91-38

License

Nos:

DPR-31

and

DPR-41

Facility Name:

Turkey Point

3 and

4

Inspection

Conducted:

September

9-13,

1991

Inspector:

T. A. Peebles,

Team Leader

Date Signed

Accompanying Personnel:

R. Auluck,

NRR Project

Manager

H. Ernstes,

Operator

Licensing Examiner

G. Galletti,

Human Factors

Engineer

R. Moore, Reactor

Inspector

G. Schnebli,

Resident

Inspector

H. Scott,

Resi'dent

Inspector

D. Thompson,

Security Inspector

Approved by:

A.

. Gibson, Director

Date Signed

" Division of Reactor Safety

91

1 3 r"'00~'

C7 9 ) 3 0 ) 8

PDR

ri DQCI( 05000'?lia

0

E'D;-<

EXECUTIVE SUMMARY

The

objective

of the

inspection

was

to

determine

the

licensee's

overall

. operational

readiness

following the recent

outage,

including whether

the

new

equipment

had

been

integrated

into overall plant operations.

The outage

was

intended to separate

the two units'lectrical

busses

and to add two emergency

diesel

generators.

The following were the major items

added =-or replaced

on both units:

-Emergency

Bus

Load (safeguards)

Sequencer;

-Anticipated Transient

Without Scram

(ATWS) Mitigating System Actuation

Circuitry (AHSAC);

-RTD bypass

removal

and instrumentation

upgrade

(Eagle 21);

-Battery chargers

3Al, 3A2,4A1,4A2,3B1,

3B2,

4B1,

and 4B2;

-Spare battery

D5Z and spare

charger

D51;

-480 Volt Motor Control Centers,

3K, 3L, 3H,

4D, 4J,

4K, 4L,

and

4H;

-480 Volt Load Centers

3H and

4H;

-4160 switch gear

3D and

4D (swing buses

and transfer switches);

-Emergency diesel

generators

(EDG)

4A and

4B;

and

EDG 3A and

3B upgrade.

During the outage period, Turkey Point had numerous other inspections.

The team

independently

assessed

the

operability

and

usability

of the

major

system

modifications,

the

procedural

changes,

and

the

newly

implemented

Technical

Specifications.

This included

an assessment

of the operators'eadiness

for the

startup

and their familiarity with the

new equipment'nd

procedures.

Management's

involvement and oversight of the outage

was readily apparent.

The

thoroughness

of the major system tests

and the lack of discrepancies

found during

the tests

are attributable to this attention.

The team findings in the area of

major modifications were minor and,

due to the complexity of the outage,

many

management

cross-checks

were

implemented

and were the reason for the excellent

progress

toward the quality and timely completion of the outage.

Deficiencies

were

corrected

prior to

system

turnover

to operations.

This

required tracking all deficiencies

to closure.

Identification and tracking of

all outstanding

items for each

system provided plant management

with detailed

status information and maintained accountability for resolution of deficiencies.

The

team

found

an

inadequately

implemented

design

change.

The

inadequate

implementation of the initial design intent was not detected

during the design

process

due primarily to

inadequate

independent

review

and

inadequate

post

modification testing.

The operating procedures

developed to implement the back-

up cooling water flow to the charging

pumps would have misdirected the operator.

Therefore,

the back-up function would not have performed properly.

System

engineers

reviewed all

5500

open Plant

Work Orders to determine if the

work

was

required

to

be

accomplished

prior to turning

over

the

system

to

Operations

Department.

The disposition

was agreed

upon by both Maintenance

and

Operations.

The team reviewed the open

PWOs for the Safety Injection, Residual

Heat

Removal,

and

Component

Cooling Water

systems

and

agreed with their final

disposition.

Executive

Summary

2

Approximately 310 Plant Change/Hodifications

were planned to be accomplished

and

22 of these

were cancelled.

The team reviewed the deleted

PC/Hs and agreed that

they did not impact plant safety.

Eleven of the cancelled

PC/Hs were replaced

by 14 other

PC/Hs that the licensee

considered

to be more important.

Shift manning. was found to have experienced

personnel

in the shift supervision

positions

but

22 of 24 of the control

board operators

comprising the current

crews were licensed for less than

a year with few actual plant start ups and shut

downs.

Operations

management

required experienced

operators in the proximity of

control board operations

at all times,

and personally provided oversight in the

control

room.

The Normal and Off-normal operating procedures

were in general

agreement with the

writer's guide.

Some

procedures

were

walked

down with operations

staff

and

particular emphasis

was placed

on reviewing the modifications to the Unit 3 and

Unit 4 Emergency Diesel Generator controls.

The team found that the procedures

were adequately detailed

and the operations staff was capable of performing the

activities described

in the procedures.

Inspectors

observed

the fill and

vent of the Unit

3 Reactor

Coolant

System.

Operators did a good job in monitoring plant conditions

and keeping the evolution

coordinator

and shift supervision

informed of the plant status.

A sample of valve lineup attachments

associated

with Safety Injection, Component

Cooling Water and Emergency Diesel Generators

were reviewed and walked down.

The

team

found system configurations

consistent

with the documented

valve lineups

except 'for

a

few minor labelling discrepancies

and

a broken valve handwheel.

Control of locked valves

was adequate

with a few problems noted.

The team reviewed the incorporation of new Technical Specification requirements

into operation,

calibration

and

surveillance

procedures.

Additionally, the

mechanisms

which identify and track TS operability requirements for Hode change

and

routine

operating

conditions

were

reviewed.

The

team

found

good

incorporation of the

new TS.and

good oversight of changing plant conditions.

The security facilities and staff were found capable of supporting the restart

of Units

3 and 4, with minimal'mpact

on operations.

Simulation of the

new electrical

systems

and

the

sequencer

soft

and

hardware

(switches,

indicator, etc.)

have

been installed

and trained

on in the control

room simulator by the operators

that will perform the upcoming Unit 3 startup.

Electrical maintenance

personnel

were trained

on the

new equipment with the aid

of actual

equipment

installed

at

the training

center.

The

use

of actual

equipment in the training process

was

a positive point in the inspection.

In summary,

the

team determined

that the outage

was accomplished

in

a quality

manner,

and the plant

was staffed

by competent

personnel

who were capable

of

starting-up

and operating

the plant safely.

However; the team identified that

one design

change

was not properly implemented

such that the intended function

would not have

been

performed,

Executive

Summary

TABLE OF

CONTENTS

~Pa

e

1.0

INSPECTION

SCOPE

AND OBJECTIVES.................'..........

1

2.0

FACILITY MANAGEMENT ASSESSMENT.............................1

2. 1.

Review of the

Company

Nuclear

Review

Board

(CNRB)

Assessment

of

Turkey Point Operational

Readiness

2.2.

Review of management efforts for proper prioritization of activities

to assure

completion of required

items

on schedule

3.0

CONFIGURATION CONTROL MANAGEMENT .....

I

~

~

~

~

~

~

~

~

~

~

~

~ t 1

3. 1

Review of control of new equipment

by operations

3.1

~ 1

PC/H Control

3. 1.2

Walkdown of New Equipment

3. 1.3

New Equipment Drawings

and Procedures

3.2

Review of changeover

of preoperational

deficiencies

to plant work

orders

3.3

Minor Plant

Change Modification (PC/H)

Package

Reviews

3.4

Review Backlog of PWOs for Effect on Operational

Readiness

3,4. 1

Review of PC/Ms which had not been

accomplished.

3.5

Drawing Control for new equipment in Control

Room and

TSC

4,

OPERATIONS..........................

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

o 9

5.

4.1

Shift Manning

4.2

Review of Operating

Procedures

and

Human Factor Walkdown

4.3

Review of Major Operations Activities

4.4

Independently

performed

system walkdowns/Line

up Verifications

4.5

Balance of Plant maintenance

to prevent inadvertent transients

TECHNICAL SPECIFICATIONS (TS) ADHERENCE........... ~...........12

5, 1

New TS requirements

Incorporated

in Operating

Procedures

5.2

Specific

TS Operability Procedure

Review

5.3

Tracking Plant Activities

Equipment

Out of Service Controls

Limiting Conditions for Operation

(LCO)'racking

Tracking Haintenance

and Surveillance Activities

6.

SECURITY

6.1

Hanagement

Support

6.2

Security

Program

Plans

16

6.3

Protected

and Vital Area Access Control of Personnel,

Packages,

and

Vehicles

6.4

Alarm Station

and Communications

6.5

Security Training and gualification

6.6

Vital Areas

7.

ENGINEERING AND TECHNICAL SUPPORT..........................19

7. 1

Operator

and Technical Training

7.2

Temporary Alterations/Hodifications Control

7.3

Human Factors

Review of Control

Room and Local Control

Panel

Changes

7,4

EOP Follow-up Inspection (Inspection Report No.50-250

& 50-251/91-33)

7.4

System Pre-Operability Checklist Process

8.

EXIT HEETING t

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~ 21

APPENDIX A - ABBREVIATIONS AND ACRONYHS

APPENDIX 8

PROCEDURES

REVIEWED

APPENDIX

C -

DRAWINGS REVIEWED

APPENDIX D - EXIT ATTENDANCE

INSPECTION

SCOPE

AND OBJECTIVES

The ORAT assessed

overall plant readiness for startup with respect to: the major

system modifications,

procedural

changes,

and the newly implemented

Technical

Specifications.

The team also assessed

the operators'eadiness

for the startup

and their familiarity with the

new equipment

and procedures.

This special,

announced

inspection

was conducted

in the areas of management

of

outage

activities,

configuration

control

management,

operations,

Technical

Specification

adherence,

security,

engineering

and technical

support.

Within

these areas,

the inspection consisted of selected examinations of newly installed

equipment,

review

and

walkdown of procedures,

inter views with personnel

and

observation of activities in progress.

2.

FACILITY HANAGEHENT ASSESSHENT

e

2. 1

Review of the Company Nuclear Review Board

(CNRB) Assessment

of Turkey Point

Operational

Readiness

In Hay of 1991, the President of the Nuc'lear Division of FP&L gave

a charter to

the

CNRB.

The charter

was,

in addition to the Nuclear Plant Hanager's

overall

responsibility to assure

the plant is ready for restart, for the

CNRB to review

and approve the overall plant re-start program and provide oversight activities.

A review of the activities 'of the

CNRB and its individual members'ite visits

showed that the overview function was, fulfilled.

A discussion

with the

CNRB

Chairman

and

a review of appropriate

minutes of CNRB meetings

showed that the

review and approval of the plant re-start

program were also achieved.

The team found that this oversight of outage

completion

and readiness

for re-

start

was

an important contributer to the re-start

program

and its success.

2.2

Review of management

efforts for proper prioritization of activities to

assure

completion of required

items

on schedule

The team attended

several of the planning meetings that the licensee periodically

held

and reviewed the multilayered oversight for work planning

and completion.

These

programs

are detailed later in this report.

During the outage planning,

the

licensee

determined

that,

due

to

the

complexity of the

outage,

many

management

cross-checks

were required

and assured their implemention.

The team

concluded that this oversight

was the reason for the excellent progress

toward

the quality and timely completion of the outage.

3.

CONFIGURATION CONTROL HANAGEHENT

3. 1

Review of control of new equipment

by operations

3.1.1.

PC/H Control

The

System

Acceptance

Turnover

(SAT) group

was

led

by the Technical

Support

Department

and provided closeout of the dual unit outage

PC/Hs.

The

SAT staff

had dropped

from 28 people

down to eight

as

the outage

was

coming to

an

end.

This staff was supported

by other groups in the closure effort particularly plant

gC, engineering,

document control, startup test,

and construction.

Documents reviewed, that provided control to assure

PC/H implementation to closure

during the outage

were:

gI 3-PTN-1

Design Control, revision date 6/25/91

0-ADM-708

Maintenance Department

PC/H Guidelines, revision date 10/27/87

TS 3. 1

Design

Change

Verification

and

Document

Turnover,

revision

date

1/31/91

The team conducted

interviews

and reviewed records with PC/H closeout

personnel

in the SAT group, engineering,

and plant gC.

These interviews demonstrated

that

the

licensee

had:

a

functioning-

close'out

methodology;

controlled

records/documentation

that

supported

their

closeout

system;

and

completed

packages

to support the installed

systems

and components.

The

SAT group

and others

involved in the

PC/H closure

system

had

been

given

enough

independence

and authority

by- licensee

management

to insure

a proper

product,

The team reviewed the final closure documentation

package for PC/H

90-071,

Load

Center

and Switchgear

Rooms Chilled Water Air Con'ditioning System.

This system

supplied cooling for the safety-related

load centers'ooms

and was powered from

vital bussing.

Members of the

SAT group discussed

the package

in detail

and

supplied support documents for the review.

During package closure, construction,

engineering,

gC,

and

startup

documents

were

compared

to

separate

listing

documents (e.g., drawings,

PC/H revisions,

Design change Notices,

Change Request

Notices,

Nonconformance

Reports, etc.) that were maintained in document control

as

the official quality

assurance

records

during

package

installation

and

testing.

The package

was complete

and the paper trail which supported

the

PC/M

package

closure

was plain.

No violations or deviations

were identified.

3. 1.2.

Walkdowns of New Equipment

The

new

equipment

was

mainly installed

and

complete.

At the

time of the

inspection,

Unit 3

had

gone

from Node

6 to Mode 5.

Operations

had filled the

primary system

on Unit 3 and was making preparation for Mode 4.

Unit 4 was still

defueled.

New equipment

was in the following states:

The sequencer,

AMSAC, and most of the motor control centers

and electrical

busing were complete;

RTD loop calibration with the vendor present

was ongoing;

The spare

battery

and charger

were being tested

by startup

and were not

needed for either unit power operation (turnover completion was scheduled

for September

19,

1991);

and

=

The

EDGs

were

complete

except for minor segments

of six

PC/Hs

(87-257,

258,

263,

264,

265,

and

266) that were in process

to be closed out.

The

EDG addition was supported

by 27 dual outage

PC/Ms and was the largest single

work package.

The Unit 3 EDGs had also been modified during the outage receiving

upgrades

such

as air start

enhancements

and idle start

panels.

Much of the

electrical modification testing was observed

by the

NRC as indicated in previous

Inspection Reports, (e.g., 50-250,251/91-22).

The licensee stated that all minor

diesel

work (e.g.,

fireproofing addition)

to complete

the

packages

would

be

accomplished prior to entry into Mode 4.

Operations

walked systems

down during the. turnover process,

when performing the

valve lineups prior to returning the system to normal.

The

PSN is required to

verify for each

SATS that all system; valves, switches,

and breakers

are aligned

in accordance

with the appropriate

operating

procedures

and that the equipment

is operable

as defined in TS or the system/component

is entered

the

EOOS log.

Deficiencies identified during performance of the valve lineups were documented

in the remarks section of the procedure

and

PWO's were generated,

as required.

The system engineers

performed

a walkdown of their assigned

system to identify

deficiencies.

These

walkdowns were documented

on

a check list which was

a part

of the

System

Readiness

for Restart

System

book.

This checklist

included:

deficiencies

identified

and corrective

actions

taken;

missing

or mislabeled

equipment tags;

drawing discrepancies;

and equipment that was

OOS.

The licensee

performed

system

readiness

tests for a number of primary and

BOP

systems prior to returning the system to normal service.

Special test procedures

were written to perform selected

portions of OSPs to run pumps,

cycle valves,

etc.,

in order to find major problems prior to returning the system to service.

This program identified several

problems with pumps

and valves before they were

needed,

which allowed early repair

and prevented

additional delays.

The team performed

walkdowns with system engineers

and/or operations

personnel

of selected

new equipment.

The majority of the system engineers

had participated

in the startup testing of portions of the new equipment under their supervision.

The

non-licensed

operators

who

would control

the

equipment

and

line-up the

equipment during normal operation did participate in the initial testing of the

equipment

and had training on the equipment.

All licensee

personnel

involved in

the walkdowns displayed

a working understanding of the systems

and modifications

that 'had

been

performed.

During the walkdowns,

the construction

was complete,

functional,

and in good working order.

The support drawings for the equipment

which

had

been

generated

from the

PC/Ms or altered

during the

PC/M process

matched

the

equipment

and

agreed

with existing

system

conditions

with

few

exceptions.

During team / licensee jointly performed detailed

system walkdowns of piping on

the 3A and

4A

EDG air start

and lube oil piping,

some minor discrepancies

were

noted.

Overall, the systems

matched the lineup instructions.

Air start system

discrepancies

found during the walkdown were

as follows:

3A

EDG

gage

isolation

valve

(3-70-441A)

appeared

on the

valve lineup

procedure,

but was not on the print;

3A EDG two way manifold valves

(two valves in one valve body/block) 3-70-

303A, 317A, 419A, 420A were identified by only a valve tag for their globe

valve instrumentation

isolation side

and not the vent valve side;

valves 3-70-314A (3A EDG), 3-70-537A (4A EDG) and 3-70-538A (4A EDG) were

not the=valve type specified'on

the piping drawing.

The first discrepancy

noted

above

was generated

during

a intermediate

drawing

.revision that inadvertently

removed

the valve from the drawing.

The operator

performing the lineup had no problem locating the actual valve.

With the second

discrepancy,

the operator

was faced with the problem of deciding which of the

valves in the common body or block was the isolation valve.

He reasoned

out the

correct

valve

but future manipulations

could

be

questionable

and

a

missed

manipulation

could vent the line, which at the most,

could cause

an erroneous

alarm.-

With the third discrepancy,

the Unit 4

EDG skid vendor

had indicated

a

ball type valve on his bill of materials while the installed valve was

a globe.

The Unit

3 portion of the third discrepancy

occurred

as

a drawing error in

translating

the bill of materials to the drawing.

The licensee

evaluated

the

above

discrepancies

and

took immediate corrective

actions.

For the first discrepancy,

the

441A valve

was

reinstated

to the

appli,cable

drawing,

For the

second

discrepancy,

the applicable

drawing

was

modified to use

a manifold valve symbol

instead of a single globe valve symbol

on all four valves;

operations

had

each

valve

handle

tagged

separately

for

identification purposes.

For the third discrepancy, after the licensee performed

a more detail

walkdown of the air start

systems

to insure there were'no other

types of valves in error, the applicable

drawings

were changed to indicate the

proper type.

The team reviewed the corrective actions

(CRN-H-5442 and

DCR-TPH-

91-389) prior to the

end of the inspection.

Due to the minor nature of the

discrepancies

and

the

immediate

corrective

actions

taken,

no additional

NRC

action

was warranted,

as allowed under the

NRC enforcement policy.

No violations or deviations

were identified.

3. 1.3

New Equipment Drawings

and Procedures

In preparing

for the

use

of the

new equipment,

the

licensee

has

added

new

procedures

and

drawings

to

the

document

control

system.

The

drawings

in

particular have had many changes

due to the many PC/Hs involved and the multiple

revisions to the PC/Hs.

At the point in time of the inspection,

only some minor

changes

were expected

to the critical plant drawings

used to operate

the plant.

All changes

were to be completed prior to Hode

4 operation.

To determine

the state

of control

over the

drawing

program,

the

team

cross

checked

the drawings

a number of ways.

As noted elsewhere

in this report, the

plant drawings

were

used

in plant walkdowns to ensure correlation

between

the

drawings

and the actual

systems.

A comparison

was

made between the PC/H content

and the actual drawing revision.

Then

a comparison

was made between the drawing

targeted for distribution and those in the plant.

Except for some minor points,

the program

was intact.

The team obtained copies of the

POD section from the 27 dual outage

PC/Hs for the

EDGs.

This section details, the revision level

and the drawing impacted

by the

PC/Hs.

Those

drawings stated

to

be

"POD 1" were to

be issued

to support

the

e

plant prior to startup.

From this population of critical drawings,

a comparison

was

made

between

the

drawing

indicated

PC/Hs

and

those

located

in document

control.

The

PC/Hs

and drawings

sampled

are

as follows:

drawing

sheet

Revision

PC/H

drawing type

5610-T-E-4536

1

22

5610-T-E-4536

3

6

5614-H-736

1

1

5614-H-736

2

1

5610-E-0855

C3

284

  • piping and instrumentation

diagram

87-263

86-155

87-263

87-263

91-071

P&ID*

P&ID

P&ID

P&ID

breaker list

A

comparison

was

made

between

document

control

records

regarding

drawing

distribution.

From the population

sampled,

the correct revision for drawings

required to be in the control

room and Technical

Support Center

(TSC) were found

as listed in Appendix C.

Also, drawings for new equipment

were checked

in the

control

room 'and the

TSC with good results.

The

licensee

stated

that

the

drawing

system

is

changing

further.

Per

a

relatively new Architect/Engineer contract with Stone

and Webster, all Piping and

.Instrument Diagrams

(P&ID) would be redrawn under

a common numbering system.

The

new

drawings

would rid

the

existing

drawings

of

an

existing

problem

of

e

conflicting symbology

caused

by the

use of at least

three different drawing

developers

in the past.

Additionally, the

new drawings would combine three to

'our existing drawing types

such that the

new drawings would show Environmental

gualification requirements,

code boundaries,

etc.

Approximately 40 percent of

the

P&ID drawings

were stated

to

have

been

changed

and

were existing in the

drawing control system.

Redrawing completion was scheduled for the end of 1991.

The change

should not impact the current startup.

Support

drawings

(other

than

"POD

1" critical drawings)

were

not evaluated.

These were being handled

on a expeditious

schedule with a scheme of required due

.dates

up to 180 days.

"POD 1" drawings would be turned around in one day at the

plant site.

The team

was

shown graphical

presentations

of the backlog of the

lower priority drawings that

showed

the

backlog

close

to

be

being

completed

within schedule.

e

Procedures

for the

new equipment

have

been

issued to support the startup.

These

new

procedures

were

generated

as

a part of the

PC/H process

with specific

signoffs

by the affected

departments.

These

procedures

will change

as

more

information and experience presents itself but the procedures

were largely intact

for the startup.

Reviewed

procedures

are listed in Appendix

8 and they were

found to be complete

and

no problems

were identified.

No violations or deviations

were identified,

3.2

Review of changeover

of preoperational

deficiencies

to plant work orders

Although

in

the

past it

was

common

policy

for

the

licensee

to

convert

preoperation deficiencies

to their normal

PWO system,

the current philosophy is

to correct all deficiencies prior to unit startup,

Regional

based

and resident

0

inspectors witnessed

numerous preoperational

tests throughout the current outage

and

observed

that all deficiencies

identified during the testing

phase

were

corrected.

Test

deficiencies

were

documented

on

a

TER for the

specific

preoperational

test

procedure

being

performed.

The.

TER

then

provided

a

disposition to correct the deficiency and determine the appropriate retest.

The

retest normally required the reperformance of applicable portions of the original

test procedure or in some instances

required the performance of a new procedure

written

-for

the

specific

deficiency.

Deficiencies

identified

after

preo'perational

tes,'ting

and turnover to operations

department for returning the

system/component

to service

would

be identified

by the licensee's

normal

PWO

process

and corrected

under this system.

In order to ensure all deficiencies, identified during the outage were documented

and closed out, the licensee established

'a System Readiness

for Restart

Program.

This program identified approximately

50 systems,

per unit which included all

nuclear plant systems

and those

secondary

systems

considered

by the licensee

as

important to safety

and plant reliability.

The systems

were assigned their own

unique

notebook

which was sub-divided into about

30 subtopics

which included:

open clearances,

surveillance to be performed,

equipment listed in the

EOOS log,

PH,'s

to

be

accomplished,

outstanding

PWOs,

PHT required,

training,

system

lineups,

PC/H's open,

system walkdowns, NCR's, etc.

open items identified in each

subtopic were listed on a master

punch list by system, responsibility,

due date,

and the Node the item must

be cleared

by.

Closure of the open items was'racked

at the daily meetings to ensure all required items were corrected or accomplished

prior to allowing

a Hode change.

For example,

there

were over 800

punch list

items that were required to be completed prior to entering Hode 6.

The books and

punch list for each

system were reviewed

and signed for by each department

head

and approved

by the

PNSC and Plant Hanager.

The team considered this extensive

effort to identify all outstanding

items for a specific system to be beneficial,

in that it provided plant management

with a detailed status of each

system.

It

should be noted this program which was established for the outage

was in addition

to the licensee's

normal

process

for ensuring all required

work was

complete

prior to restart.

No violations or deviations

were" identified.

3.3

Hinor Plant

Change Hodification (PC/H)

Package

Reviews

The team accomplished

a detailed review of PC/H 91-064 which was developed

and

implemented

under

the

Hinor Engineering

Package

program.

The

HEP

program

provides guidance for developing minor design changes.

The selected

PC/H was to

the charging

pump reduction

speed drive system.

The charging

pumps are positive

displacement

pumps with variable

speed

control

achieved

through the hydraulic

coupler.

The purpose of the hydraulic oil cooler is to maintain the hydra'ulic

coupling oil within its operating

range.

The

reviewed

PC/H's intent

was to

provide

an alternate

source

of cooling water to the

A and

C charging

pumps'ydraulic

coupling oil coolers (its

normal

cooling water

source

is

CCW)

and

prevent overheating of the oil in the hydraulic coupling should

CCW be lost.

The

B charging

pump for both Units received

a similar modification in 1976.

Design deficiencies identified in this PC/H by the team demonstrated

deficiencies

in

the

HEP

program.

Primarily,

these

deficiencies

were

related

to

the

independent

review and post modification testing

aspects

of the design

change

process

as applied to minor design changes.,The

package appropriately addressed

hardware

installation

and

procurement.

The

package

did not provide

adequate

calculation, analysis, testing or procedural

guidance to demonstrate that service

water could supply adequate

cooling for the hydraulic oil which was the design

intent of the modification.

Additionally, piping design. pressures

given in the

documentation

indicated the

CCW piping would experience

pressures

greater

than

design

when the service water supply was provided.

These deficiencies

were not

identified by the independent

reviews.

Although the hardware

was appropriately modified, the incorporation of design

information into the appli,cable operating procedures

was incorrect, resulting in

establishment

of inadequate

flow for the service

water through

the coolers.

Additionally, the parameters

monitored,

by procedure, direction, would not have

alerted the operators if the oil temperature

was approaching limiting conditions.

The procedure directed the operator to adjust the inlet service water valve to

the heat

exchanger

to prevent overflow of the, floor drain to which the outlet

flow was directed.

Due to the flow restriction provided by the drain screen this

would

have

been

considerably

less

than full service

water flow or normal

CCW

flow.

This flow condition was not tested

or analyzed to determine if adequate

cooling was provided.

The procedure,

ONOP-030, Malfunction of CCW, directed the operator to monitor the

temperature of the service water outlet flow from the cooler.

No instrumentation

was installed for measuring this temperature.

The procedure stated

a 150 degree

F

upper limit.

During

the

modification

walkdown

the

operator

stated

the

temperature

would be verified by operator tactile sensitivity; i.e., finger in

. the flowstream.

Due to the variable

and unspecified

flow rate this would not

provide

a reliable verification that the oil was not exceeding its temperature

limits even if operator tactile sensitivity was accurate to 150 degrees

F.

The

design

change

package

did state

the oil inlet temperature

to the cooler should

be monitored

however this information was not incorporated

into the applicable

procedures.

Existing

instrumentation

was

available

to

measure

oil inlet

temperature.

The above design deficiencies

challenge the effectiveness

of this design

change

to

accomplish its intent.

The

design

review process

and

post modification

testing, if adequately

performed,

are

mechanisms

which should

have identified

these

deficiencies

or

verified

the

design

intent

was

achieved

by

the

modification.

The failure of the

HEP design

change

process

to provide adequate

design control is identified as violation 91-38-01.

The service water back-up cooling capability provided

by this modification was

taken credit for in improving the licensee's

PRA for preventing

core

damage

in

specified

accident

scenarios.

The modification specifically reduced

the core

melt probability for the unmitigated

RCP Seal

LOCA scenario

where

CCW is assumed

to fail.

Either

CCW or charging flow is required to maintain

RCP seal

cooling

and

CCW is required for continued operation of the charging

pumps

and the High

and

Low

Head

Safety

Injection

Pumps.

Therefore,

to

prevent

unacceptable

consequences

from loss of CCW,

an alternate

source of cooling to the charging

pumps

was developed.

The short-term operability impact of this specific

PC/H deficiency is minimal

'because

the

added

service

water cooling is

a

back-up

function.

A similar

capability on the

B charging

pumps, installed since

1976,

has

never

been

used.

The primary importance of this issue is the design

change

process

programmatic

deficiency

demonstrated.

The licensee's

corrective

action

discussed

in the

following

paragraph

addresses

the

potential

operability

impact

of

other

modifications

accomplished

under

the

HEP program.

The

HEP program at Turkey

Point was initiated in March,

1991;

91

HEPs

had

been issued

as of September

12,

1991.

I

Upon

notification of this

finding,

the

licensee

initiated

the

following

corrective actions'hich

were to be completed prior to entering

Mode 4:

2

~

All

dual

unit

outage

HEPs

will

be

reviewed

to

ensure

post

modification testing

and procedural

interfaces

are satisfactory.

The

HEP process

at Turkey Point

was modified to:

1) include Site

Engineering

Manager

sign-off

of

the

MEP

package

prior

to

implementation,

and

2) include

a joint pre-implementation

walkdown

with the

design

engineer,

system

engineer

and

appropriate

plant

operations

and maintenance

personnel.

3.

All site engineering

personnel will be trained

on the changes to the

HEP process.

4.

The

PNSC will be "resensitized" to the need for a thorough review of

post modification testing

requirements

on all

design

changes it

reviews.

The licensee further prohibited use of the

HEP process

at Turkey Point until the

above

items are completed.

3.4

Review backlog of PWOs for effect

on Operational

Readiness

As previously stated,

outstanding

PWO's

are identified

as

a subtopic

in the

System

Readiness

for Restart

Books.

For this portion of the

program,

the

licensee

reviewed all open

PWOs for each

system

and included

a printout of each

one

in this

section

of

the

book.

This

required

reviewing

a

total

of

approximately

5500

PWOs.

The

respective

system

engineer

reviewed

the

PWOs

associated

with his system

and determined if the work described

in the

PWO was

required

to

be

accomplished

prior to turning

over

the

system

to Operations

Department.

The

system

engineer's

disposition for each

PWO was

reviewed

and

agreed

upon

by both Maintenance

and Operation

Departments,

If the work was

required to be accomplished prior to turnover it was

added to the master

punch

list and assigned

a Mode to be completed by.

The team reviewed the open

PWOs for

the SI,

RHR,

and

CCW systems,

and

agreed with the final disposition for those

PWOs 'determined

as not required prior to system turnover.

The team considered

the licensee's

review of the

open

PWOs to be comprehensive

as it included all

open

PWOs

and not just trouble

and

breakdown

PWOs.

0

3.4. 1

Review of PC/Hs which had not been

accomplished.

For this

DUO approximately

310

PC/Hs were planned to be accomplished

and

22 of

these

were canceled.

In order for the licensee

to delete

an activity that was

initially planned for the outage, it had to

be

recommended

by the applicable

Department

Head,'echnical'epartment

Supervisor,

Outage

Manager,

Operations

Superintendent,

and Plant Manager,

and approved

by the Site Vice President.

The

recommendations

and approval

are documented

on Attachment

3 of O-ADH-003, Outage

Management.

The team reviewed

the

22

PC/Hs that were deleted

and

agreed that

they 'did not

impact plant safety.

The

canceled

PC/Hs

ranged

from modifying

components

for system

enhancement

to installing removable

hand rails at the

containment

equipment hatch area.

Eleven of the canceled

PC/Hs were replaced

by

14 other

PC/Hs that

the

licensee,

considered

to

be

more

important

than

the

original

PC/H.

For example,

PC/Hs90-301,

304,

and

305,

to modify

11 pipe

supports,

were traded to procure, install, and test the Hydrogen Recombiner.

In

addition, the canceled modifications were added

as candidates for either the "Top

20" or "Top 30" lists.

These lists were recently implemented

by the licensee to

control the number of modifications being installed in the plant.

In order for

a

modification

to

be

installed it

must

be

listed

on

the

"Top

20 List"

(modifications scheduled for the next outage) or the "Top 30 List" (modifications

that

can

be accomplished

on-the-line or during short notice outages).

For

a

modification to be added to the lists there must be room for it or a modification

currently on the list must be canceled

and the new modification added.

The team

considered

this

an

excellent

method

of controlling

the

number

of

changes

occurring in the plant at any one time.

No violations or deviations

were identified.

, 4.

OPERATIONS

4. 1 Shift Manning

Shift manning

was found to have experienced

personnel

in the shift supervision

positions

but

22 of 24 of the control

board operators

comprising the current

crews were licensed for less than

a year with few actual plant start ups and shut

downs.

Through discussions

with Operations

management, it was agreed that there

would be experienced

operators

in the proximity of control

board operations

at

all times.

These

experienced

operators fill the positions of PSN,

APSN,

and

Watch

Engineer.

Operations

management

personally

provided oversight

in the

control

room.

No violations or deviations

were identified.

4.2

Review of Operating

Procedures

and

Human Factors

Walkdown

The team reviewed

a sample of the

OPs

and

ONOPs to ensure that the procedures

adequately

incorporated

human factors considerations

and that the Turkey Point

operations staff clearly understood

and could use the procedures

as written.

The

review consisted of: (1)

a review of the procedure writer'-guide ADM-101; (2)

comparison of the procedures

against the administrative guidelines for procedural

development;

and

(3) plant

walkdowns of selected

procedures

with operations

e

10

staff.

The procedures

reviewed are listed in Appendix

B to this report.

k

The team reviewed the licensee's

procedures writer's guide

(ADM-101) to ensure

that it adequately

addressed

the

previous

concerns

identified

during

the

Emergency Operating Procedures

Inspection (IR 50-250/89-53)

and incorporated the

human

factors

principles

as

described

in

NUREG-0899,

"Guidelines

for

the

Preparation

of Emergency Operating

Procedures."

The licensee

has incorporated

revisions to the procedure writer's guide in response to the inspection findings.

Most significantly, the writer's guide

has

been

expanded

to include all

OPs,

ONOPs,

and

EOPs.

This is

a good practice

and should help to ensure

consistency

and standardization

in the preparation

and formatting of procedures.

The procedures

reviewed

(Appendix B) generally

agreed with the requirements

of

the writer's guide.

Several

of the

OPs

contained

minor deviations

from the

writer's guide with regard to the format 'and terminology for transition steps,

referencing

and branching steps,

and the use of highlighting.

These deviations

reflect

a lack of verification of the procedures

against the procedure writer'

guide.

The licensee

was appraised of these

concerns

and will continue to review

the procedures

to ensure

consistency

with the writer's guide.

A sample of the procedures

reviewed

were walked

down with operations staff to

determine the adequacy of the procedures,

and to ensure that appropriate controls

and indications were presented.

Particular emphasis

was placed

on reviewing the

modifications to the Unit 3 and Unit 4

EDG controls.

The team found that the

procedures

were

adequately

detailed

and the operations staff were

capable

of,

performing the activities described in the procedures.

In general,

the equipment

nomenclature

used

in the

procedures

matched

the

label identification

on the

equipment.

In those

cases

where labelling discrepancies

were identified, the

licensee

took

the

appropriate

administrative

actions

to

correct

the

discrepancies.

No violations or deviations

were identified.

4.3 Review of major operations activities

Unit 3 Containment

was not yet ready for closeout during this inspection period.

Inspectors

observed

from the control

room,

the fill and vent of the

Reactor

Coolant System.

An off-shift operator

served

as coordinator of the evolution.

He

was

responsible

for the fill and

vent leaving

the

APSN free to monitor

operations of the entire plant.

The coordinator

gave the pre-brief concerning

the

evolution

to

the

shift

during

the

shift

turnover.

There

were

no

discrepancies

observed

during

the

evolution.

Operators

did

a

good job in

monitoring plant

conditions

and

keeping

the

evolution coordinator

and

APSN

informed of the plant status.

During the fill of the Reactor

Coolant

System,

a conservative

value for boron

concenti ation of the water used for make-up to the Volume Control Tank was used

to ensure that

no dilution occurred while filling the Reactor

Coolant System.

No violations or deviations.

were identified,

0

4.4

Independently

performed

system walkdowns/Line

up Verifications

Com onent Coolin

Water

s stem

and

Emer enc

Diesel

Generators

A sample of valve lineup attachments

associated

with the Component Cooling Water

system

and

Emergency

Diesel

Generators

was

reviewed

to verify that

system

configurations

were consistent

with the documented

lineups

and to ensure that

there

was

adequate

control of locked valves.

The

team

found that the

system

configurations

were consistent

with the documented

valve lineups.

A few minor

labelling discrepancies

and

a

broken

valve

handwheel

were identified.

The

licensee

implemented

the appropriate

administrative

actions

to correct

these

discrepancies.

Control of locked valves was generally adequate with some exceptions

noted on the

Component Cooling Water system.

Inspectors

walked down selected

Enclosures

and

Attachments of OSP-205,

"Control of Locked Valves".

All valves were found locked

in their proper position.

This

procedure

calls for color coding of safety

related valves

so that

a color coded

key will open all the locks of that color.

There were three valves

on Unit three

CCW heat exchangers=that

had blue locks,

which are Unit 4 locks.

The facility subsequently

changed these locks to conform

with the procedure,

It should be noted that the check list includes checking the

color of the lock.

Enclosure

2 of the procedure

had omitted one page of valves

during the last revision.

The facility issued

a

new revision to the procedure

that included the correct

pages.

The team also identified several

discrepancies

between the plant system drawings

and the

new plant equipment,

A detailed discussion

of these

discrepancies

is

presented

in paragraphs

3. 1.

Safet

In 'ection

The

team conducted

a system

walkdown of the

SI

system to ensure

proper valve

alignment,

This was accomplished utilizing 3-0P-062, Operating Procedure for the

Safety

Injection

System,

and. 5610-T-E-4510,

sheet

1

and

2,

Rev.

106,

dated

September

6,

1991, Operating

Diagram Unit 3 and

4 Safety Injection and Residual

Neat

Removal

Systems

Inside

and Outside

Containment.

The

team verified the

following;

all valves, in the

system

were in the correct position with power

available

and valves

locked if required;

valves

in the

system

were correctly

installed and did not exhibit signs of gross packing leakage,

bent stems, missing

hand

wheels,

or

improper

labeling;

system

lineup

procedures

matched

plant

drawings

and as-built configuration; local

and

remote position indication

was

compared

and functional;

and

system

components

were properly labeled.

Several

minor

discrepancies

were

identified

and

brought

to

the

attention

of the

Operations

Supervisor for correction.

In addition, the team reviewed the valve

lineups performed

by the licensee

on the

AFW,

CCW, and

RHR systems.

All lineups

reviewed

were found to be satisfactory with deficiencies

noted in the remarks

section

,of the

applicable

procedures.

Deficiencies

requiring

re'pair

were

identified w'ith the respective

PWO number listed,

No violations or deviations

were identified.

12

4.5

Balance of Plant

(BOP) maintenance

to prevent inadvertent transients

The

team

reviewed

and

discussed

with the licensee their efforts

and

actions

concerning their preventative

maintenance

programs with the secondary

systems

during the outage.

It was determined that the licensee

had taken major action

to ensure the secondary

systems

are functioning to support

a long term run after

re-start.

In support of Unit 83, the licensee

completed the following:

High pressure

turbine overhaul

(5 year inspection);

Generator

Rotor Rewind/Stator

Inspection/Repair;

Cross-under

Piping Ultrasonic Inspection/Repair

Program;

Turbine Control Valve Inspection/Overhaul

Condenser

Hotwell Inspection/Repair

Program

Extraction

Steam

Expansion Joint Inspection/Repair

Turbine Plant Cooling Water Heat Exchanger

Retubing

Steam Generator

Feed

Pump Motor Upgrade

Steam Generator

Feed

Pump Exhaust

Fan Modification

Condenser

Water

Box 100 percent

ECT Program

Replace

Atmospheric

Dump Valves

Moisture Separator

Reheaters

A<B<C<0 Inspect/Repair

on Shellside/Tubeside

Over haul all Turbine Oil Pumps

Relief Valve Testing/Overhaul

Program

Valve Packing

Program

Actuator and Valve Overhaul

Program

Replace

Condenser

Water Box Expansion Joint

Turbine Generator

High Pressure

Oil Flush

and Cleanup

Condensate

Pump Overhaul/Motor

Intake Traveling Screen

Overhaul

Circulating Water

Pump Overhaul

(5 year plan)

5.

Technical

S ecification

TS

Adherence

5. 1

New TS requirements

Incorporated

in Operating

Procedures

The team reviewed the incorporation of the

new TS requirements

into operations,

calibration and surveillance procedures.

Additionally, the licensee's

mechanisms

which identify and track TS operability requirements for Node change

and routine

operating conditions

were reviewed.

A sample

of requirements

was

selected

from the

new

TS for verification of

appropriate

implementation in procedures,

The sample focussed

on criteria which

were

new or changed

from the previous

TS.

The general

areas

included

ECCS

and

reactor

trip

setpoints,

fire

protection,

ECCS

equipment

and

battery

surveillances.

5,2

Specific Technical Specification Operability Procedure

Review

1.

TS

3. 1.2.3 - Charging

pumps operability,

Reviewed

operating

procedure

4

-

OSP

-

047,

"Charging

Pump/Valves

13

Inservice Test" for consistency

with the applicability and surveillance

requirements

from the

TS including action statements.

Comments:

Acceptable

TS 4.8. 1. 1.2.b.

Fuel transfer

pump operability.

Reviewed

procedures

3-0SP-022.4,

"EDG Fuel

Oil Transfer

Pump

and

Valve

Inservice Test",

and 3-OSP-023. 1,",DG Operability Test" for operability of

fuel transfer

pump to 'start

automatically

and transfer

fuel

from the

storage

system to the day tank.

Comments:

Acceptable

TS 4.8. 1. 1.2.d

Removal

of accumulated

water

from fuel oil storage

tanks.

Reviewed procedure

O-OSP-022.6,

"Diesel Fuel oil storage

tank accumulated

water removal" for consistency with the

TS requirements

and also reviewed

the results of the surveillance

completed

in Hay. 1991.

Comments:

Acceptable.

TS 4.8. 1. 1.2.c

Removal

of accumulated

water

from the

day

and skid-

mounted fuel tanks (Unit 4 tank only)

Reviewed

procedure

0-OSP-022-6

for

compliance

with

the

surveillance

requirements.

Comments:

Acceptable.

TS 4.8. 1. 1.2.i.(1) - Draining and cleaning of fuel oil storage

tank.

Reviewed procedure

O-PHA-022.6 "Diesel oil storage tank cleaning"

and the

results of the cleaning

performed during 1987.

Comments:

Acceptable

TS 4.8.2. l.a.(3) - D.

C. Battery

and Charger Surveillance.

Reviewed

procedure

O-SHE-003.7

"

125

VOLT

DC startup

Battery

Weekly

Haintenance" for consistency

with the

TS surveillance

requirements.

Comments:

Procedure

and

TS were not updated to reflect the

new proposed

requirements

issued

on August 26,

1991.

Florida Power

and Light Company

indicated that their documents

are in the

process

of being

updated

and

will be completed

by September

13,

1991.

TS 4.8.2. I.a(1)

Table 4.8.2 Battery surveillance

requirements.

Reviewed

procedure

O-SHE-003.7

for

compliance

with

the

pilot cell

verification

and rotation

schedule

requirements

including reference

to

8.

9

R.G.

1. 129 and

IEEE recommendations.

Comments:

Acceptable

TS 4.7.2.a - Component

Cooling Water System.

Reviewed procedures

O-ADH-513," Duties

and responsibilities of the STA",

and

3-0SP-019-4,"

Component

Cooling

Water

Heat

Exchanger

Performance

Monitoring" for consistency

with the surveillance

requirements.'omments:

Acceptable

TS 4.7..2.b(2)

CCW heat

exchanger

performance test.

Reviewed

procedure

3-0SP-030.6,

"Component

Cooling Water Heat

exchanger

performance test".

Comments:

New surveillance requirements

were issued

as part of a license

amendment

dated

August

26,

1991.

As of September

12,

1991,

procedures

were not updated

to reflect the

new requirements,

nor were the

TS pages

changed,

FPKL indicated that the changes

were in the process

and will be

completed

by September

13,

1991.

~

~

~

~

10.

TS 4.7.9. I.c Fire Rated Assemblies

Reviewed procedure

0-SHE-0163.

"Fire barrier penetration

seal inspection"

for

compliance

with

the

surveillance

requirements

and

Appendix

R

requirements.

Reviewed the last surveillance

performed in June

1991.

Comments:

Acceptable.

TS 4.7.8. 1. I.d - Fire Water

and Distribution System

Reviewed procedure

O-SMM-016.1, "Fire suppression

system annual flush" for

compliance with the TS surveillance requirement

and also reviewed the test

performed in February

1991.

Comments:

Acceptable.

12.

TS 4.7.8. 1. l.g - Fire Protection

System

Reviewed Procedure

O-OSP-016029,

"Fire Hain three year Hydraulic gradient

flow test" for compliance

with

TS surveillance

requirements

and

also

serviced

the results of the tests

performed in 1989.

Comments:

Acceptable.

A few exceptions

were

noted

above,

but were corrected

immediately.

The

team

concluded

the

new

TS

had

been

appropriately

incorporated

into

operation,

calibration

and surveillance

procedures.

No violations or deviations

were identified.

5.3

Tracking Plant Activities

15

- Equipment

Out of Service Controls

- Limiting Conditions for Operation

(LCO) Tracking

- Tracking Maintenance

and Surveillance Activities

The licensee's

mechanism for identifying and tracking

Mode change operability

requirements

encompassed

a computer data

base

and the software to generate

TS

surveillance

requirement

schedules

and reports.

This data

base

and software

accomplished

the tasks which were previously performed manually.

The new system

was being

used to identify and track

Mode change

requirements

for the current

Mode

5 to 4 transition.

The

computer

data

base,

which

was

established

during the'resent

outage,

identified all TS surveillance requirements, their Mode application, performance-

,

. responsibility, frequency,

and other pertinent .data for tracking and performance.

The team reviewed the

Mode change report generated

by the software

program for

the current plant conditions to verify applicable

requirements

from the

TS for

Mode

4 had

been identified.

No discrepancies

were identified by the team.

A

Mode change report for Mode

2 was similarly reviewed to verify, by sample, that

appropriate

TS requirements

were identified by the system for entry into Mode

2

from Mode 3.

No discrepancies

were identified.

Based

on this sample,

the team

concluded the licensee's

mechanism for identification of Mode change requirements

was adequate.

The Mode change report

was tracked in the control

room by the Plant Supervisor

Nuclear.

This document

was initialed and dated for each surveillance

as it was

completed.

Discussions

with

the

on-shift

PSN

demonstrated

the staff

was

knowledgeable

of the

process

and

current

status

of outstanding

surveillance

requirements.

The operating procedure for Mode change,

3-GOP-503,

Cold Shutdown

to

Hot

Standby,

dated

August

30,

1991,

contained

verification

sign-offs

referencing completion of the Mode change report.

Based

on this review, the team

concluded

the

licensee's

mechanism

for tracking

performance

of

Hode

change

requirements

was adequate.

The team additionally reviewed the application of the new computer based

process

to routine

TS surveillance activity.

A daily task

sheet

is generated

which

identifies

TS surveillances

due within a current

7 day window.

This information

is carried

in the

Plan

of the

Day which receives

daily

management

review.

Surveillance requirements

entering the grace period or separately listed in the

POD for increased

management

attention.

Responsibility

for administrative

control of the surveillance tracking program were

assigned

and

personnel

were

knowledgeable

of their duties

and responsibilities.

Equipment out of service

documentation

was

routed

through

the

surveillance

coordinator,

facilitating

verification that

appropriate

TS operability requirements

were

met prior to

declaring the equipment operable.

The team reviewed the

PODs during the week and

verified the currently iidentified surveillances

applicable

in this 'Mode were

being tracked.

Based

on this review,

the

team

concluded that the licensee's

mechanism for identification and tracking of routine TS surveillance requirements

was adequate.

No violations or deviations

were identified.

16

6.

~Securit

Through observation,

testing,

review of documentation,

and evaluation of the

licensee's

organization

and staffing, security plan,

access

control function,

alarm response,

communications,

and training, it was determined that the security

function was capable of supporting the restart of Units

3 and 4.

6. 1

Management

Support

Review of the security program functions and observation of security operational

activities revealed that the program

was effectively managed

and that -security

resources

were

being utilized in

an efficient

manner.

The security

force

provided

by Security

Bureau,

Incorporated,

consisted

of approximately

270

personnel

assigned

to

two shifts

that

provide

security

protection

for the

facility on

a 24-hour basis.

The contract security force includes

a supervisor

and administrative

elements

to support the security shift operations.

Based

on observation

and discussion with security personnel

during the course of

the inspection, it appeared that the security organization

was adequately

managed

and that communication

between plant management

and the contract security force

was sufficient to ensure

the maintenance

of good working relations,

morale,

and

motivation of the security force.

Support of the security

program

by senior

plant management

was evident.

6.2

Security

Program

Plans

Review of current

security

plans

and

discussions

with security

management

determined

that

security

operational

activities

were

being

performed

in

accordance

with the

provisions

of Revision

0 to the

Turkey

Point

Physical

Security Plan,

placed in effect

on July 1,

1991.

The licensee

had established

implementing procedures for use by the security force to facilitate adherence

and

compliance

with the

security

plan

commitments.

Review

confirmed

that

the

security

plan

and

implementing

procedures

were current

and

provided

adequate

guidance for security force implementation of regulatory requirements.

Although

the central/secondary

alarm station

(CAS/SAS)

procedures

were

developed,

the

licensee

continues

to update

the

CAS/SAS procedures

as the total alarm systems

are integrated.

e

17

6.3

Protected

and

Vital

Area

Access

Control

of Personnel,

Packages,

and

Vehicles

Observation

of personnel,

package,

and vehicle

access

control activities

at

personnel

access portals

and vehicle gates revealed that positive access

control

procedures

have been established

to provide control of access

into the protected

and vital

areas.

Personnel

are

issued

security

badges

wh'.ch

includes

an

electronic

key card

and

are

searched

either

by processing

through

metal

and

explosive detection

equipment or

a hands-on

search

by security personnel

prior

to being granted

access

into the protected

area.

Access into the protected

area

is

accomplished

by

passage

through

electronically

controlled

turnstiles.

Security

personnel

positioned

within bullet-resistant

enclosures

have

the

capability of locking

down the turnstiles

to preclude

entry to the protected

area.

access

to vital areas

is controlled by key card

and intrusion detection

equipment.

Security personnel

provide response to attempted unauthorized entry.

All hand-carried

items are

scanned

by X-ray equipment prior to access

into the

protected

area.

guestionable

items are hand-searched.

Routine vehicle access

into the protected

area is accomplished

at

a vehicle gate

located

on the south side of the site.

Vehicles entering the protected

area are

enclosed

within a vehicle

entrapment

area

where

they are

searched

and

access

authorization verified prior to entry.

Observation of vehicle access

and search

activity during the period of the inspection did not identify any discrepancies

or deficiencies

in the control of vehicle access.

6.4

Alarm Station

and Communications

Observation

of routine security

operational

activities

in the

Central

Alarm

Station/Secondary

Alarm Station

(CAS/SAS) during regular

and non-regular

hours

confirmed

that

the

alarm

station

was

equipped

with

appropriate

alarm,

surveillance,

and communications capability in accordance with commitments of the

approved

Physical

Security Plan.

The alarm station

was continuously

manned

by

trained

and experienced

operators

and was independent

and diverse to the extent

that

no single act could remove the security force's capability of calling for

assistance

or otherwise

responding

to

a threat.

There

were

no

operational'ctivities

observed

in the

CAS that

would interface

with the

execution

of

assessment

and response

functions.

The alarm station demonstrated

the ability

to communicate with all security personnel

assigned to armed response

duties

and

fixed posts.

On

September

10,

1991,

the

team

discussed

with the

licensee

and

contractor

personnel

the status

of the computer

and its capability to support the site's

alarm system,

All personnel

present

indicated that they believed that:

1,

As

of this

date,

the

computer

system

would

support

the

site

exterior/interior alarm system,

2.

Other than those

zones

and vital doors

which are not operational,

the intrusion alarm system would cause

an alarm when

a zone or door

alarm was generated.

18

3

There were

no concerns that when all alarm points are tied in, that

the

computer

would overload

or not

be

capable

of functioning

as-

designed.

The

system

cannot

be altered

without the

knowledge of other site

personnel.

6.5

Security Training and gualification

Discussion

with

security

management

and

observation

of

personnel

during

,performance

of their duties,

confirmed

that

the

security

force

had fully

implemented

and

was

in

compliance

with

provisions

of

the

Training

and

gualification

Plan'.

The training

program

is

administered

by

a proprietary

training

supervisor,

assisted

by contractor

training

personnel.

Based

on

observation

of security

operational

activities

and

discussion

with several

members

of the

security

force, it appeared

that

personnel

were

adequately

trained,

motivated,

and capable of providing an acceptable

level of protection

for the power plant facility and vital resources.

6.6

Vital Areas

In addition to the above areas,

the team observed

the licensee's

security force

efforts

on September

11,

1991, to search,

test,

and secure

the protection aids

to support the vital equipment required for Node 4.

The vitalization began at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br />,

and concluded at approximately

1645 hours0.019 days <br />0.457 hours <br />0.00272 weeks <br />6.259225e-4 months <br />.

At the conclusion of the efforts on September

11, 1991,

one compensatory

post was

established

due to door equipment

problems,

and one other compensatory

post was

established

because

of

a barrier

opening

that

exceeded

the

96

square

inch

criteria.

The auxiliary building was vitalized on September

12,

1991,, or prior

to Mode 4.

It was noted that the licensee

decided

not to 'search existing high

radiation

areas

prior to vitalization of the auxiliary building to preclude

exposing security personnel

to radiation.

No violations or deviations

were identified.

7.

ENGINEERING AND TECHNICAL SUPPORT

7. 1

Operator

and Technical Training

The

inspectors

interviewed

training

department

management

to

determine

the

licensee's

program for incorporating

system

and

procedure

changes

into the

licensed

operator requalification

and initial training programs.

Changes

to a

particular

system

were

found to

have

been effectively reviewed for training

requirements.

Changes

requiring

additional

training. were

included

in the

training program.

This included shift training, requalification training

and

initial training.

Procedure

changes

are analyzed

by the training department

to determine training

requirements,

Those changes that are of a minor nature are incorporated into the

required reading list.

The current initial class

was found to be up to date

on

the required reading list.

19

As a subset of the new equipment walkdown, the team observed training tools that

had

been

set

up

by the

licensee

on

the

new

equipment.

The following was

observed.

The training staff

had

a working

sequencer

installed

in the training

building that had been utilized in actual training of Instrumentation

and

Control

and operations

personnel.

The training staff had installed

a partially working panel of the Unit 4

EDG start

control

panel

in

the. training

building.

The

electrical

maintenance

staff

had

trained

on

the

unit

and will requalify

on it

periodically.

The licensee

stated

that within the next year,

a

small

diesel

which was already

on site would be hooked

up to the Unit 4 training

EDG control

cabinet

in the training building to

more closely

simulate

actual

operation.

It is noted that the Un'it 3 and Unit 4 control panels

were similar but not identical.

Recognizing this, the operations staff

had

relied

on .in-plant

EDG training of its

licensed

and

nonlicensed

operators,

During the course of startup testing,

the Unit 4 diesels

were

started

35- times

and

the Unit

3 diesels

were started

in excess

of

25

times.

The Unit 4

EDGs

have

been operated

over 300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br />

each.

Additionally in the training building, the training staff has installed

new breakers of the

same type as those recently installed in the new load

center positions

and motor controller positions.

These

have

been

used for

plant staff familiarization.

For the

new dual unit

RTD instrument modifications,

the control cabinet

has

been installed in the control

room simulator.

The operators

normally

disable/re-enable

bistables

in .their protection

equipment

as required.

The

bistables

have

not

been

available

for installation

in

the

RTD

simulator rack but this was intended.

Simulation

of the

new electrical

systems

and

the

sequencer

soft

and

hardware (switches, indicator, etc.)

have been installed and trained

on in

, the control

room simulator by the operators that will perform the upcoming

Unit 3 startup.

In summary,

the team considered that the use of actual

equipment in the training

process

was

a positive point in the inspection,

No violations or deviations

were identified.

7,2

Temporary Alterations/Modifications Control

Inspectors

reviewed the log of Temporary

System Alterations

(TSA) and found it

maintained in accordance with 0-ADM-503. All TSAs for the required

Mode changes

had

been

completed,

Efforts were being reasonably

made to review and minimize

the number of TSAs.

No violations or deviations

were identified.

is

20

7.3

Human Factors

Review of Control

Room and Local Control

Panel

Changes

The team reviewed the control

room and local control panel revisions associated

with the Emergency

Power System

(EPS)

Enhancement

Project.

The review consisted

of:

(1)

an

evaluation

of

the

documentation

supporting

the

control

panel

modifications;

(2) review of the modifications through plant

and control

room

walkdowns of the affected

panels with operations staff;

and

(3) review of the

resolutions to the

human engineering discrepancies

(HEDs) identified during the

design process.

The

team

reviewed

the

licensee's

documentation

(Appendix

8)

supporting

the

control panel modifications to ensure the design process

adequately incorporated

human factors

engineering

principles described

in NUREG-0700,

"Guidelines for

Control

Room Design Reviews."

The. team-found that the licensee

had implemented

an adequate

process to: identify important operator actions associated

with .the

EPS,

identify controls

and

indications

necessary

for

those

actions,

and

incorporate

accepted

human factors principles into the'esign

of the control

panel modifications.

The

team

reviewed

the control

room

and local

control

panel

modifications to

ensure that the operations staff recognized

and understood the modifications,

and

to ensure that the appropriate

controls

and indications necessary

for operator

activities had been incorporated into the modifications.

The team found that the

operations staff recognized

and understood

the modifications,

and were capable

of performing the activities associated

with the affected control panels.

The

team

found that

indications

and

controls

were

adequate

for performing

the

required activities.

The team reviewed the resolutions to the HEDs identified during the control panel

design

and validation process.

In most

cases

the licensee

has

incorporated

adequate

design modifications to resolve the HEDs identified, and had adequately

documented

the resolutions.

However, the licensee did not adequately

address

the

one major control panel

HED identified during the performance validation process

(PA-SEI-EPS.02,

Discrepancy ¹I) related

to distinguishing

between

the diesel

"emergency start"

and "rapid start" controls.

The team reviewed the discrepancy

with the licensee,

and

the licensee

initiated the appropriate

administrative

controls to resolve

the

concern.

In 'addition,

resolutions

to several

minor

discrepancies

identified

in the validation

report

(PA-SEI-EPS.02)

were

not

documented.

The licensee

stated

that they will document

the resolutions for

these

minor discrepancies.

No violations or deviations

were identified.

7.4

EOP Follow-up Inspection

(Inspection

Report

No. 50-250

5 50-251/91-33)

The team

ass'essed

the licensee's

corrective actions

associated

with the

human

factors findings from the Emergency Operating Procedures

follow-up Inspection (IR

No. 50-250

5. 50-251/91-33),

dated

September

3,

1991.

The licensee

implemented

~

~

~

procedural

revisions

and

control

panel

modifications

in

response

to

the

inspection

report

findings.

The

team

found

that

the

licensee

adequately

C

21

addressed

the minor discrepancies

identified in Section

7 of IR No. 50-250

8 50-

251/91-33,

these

items are therefore

considered

closed.

With regard to the inspection team finding related to the actions taken to verify

containment integrity following a phase

A or phase

B isolation (IR 50-250 850-

251/91-33,

Section

2),

the

licensee

is

incorporating

additional

procedural

guidance into the

EOPs to help ensure

appropriate

operator actions to allow for

local or manual isolation of the affected containment penetrations.

This is more

consistent

with actual. isolation

methodology.

The

team

finds

the

proposed

actions to be adequate.

No violations or deviations

were identified.

8.

EXIT MEETING

On September

13,

1991,

the team conducted

an exit meeting at the Turkey Point

site.

The licensee

and

NRC personnel

attending

this meeting

are listed in

Appendix D.

The licensee did not provide any materials identified as proprietary

to the team.

During the exit, the team summarized

the scope

and findings of the

inspection.

There were no dissenting

comments from the licensee of the findings.

APPENDIX A

ABBREVIATIONS AND ACRONYHS

ADM

AFW'PSN

BOP

CCW

CNRB

DUO

ECCS

EDG

EOOS

EOP

FP&L

HEP

NCR

OOS

ONOP

OP

OSP

PC/H

PH

PHT

PNSC

POD

PSN

PWO

RHR

SAT

SATS

SI

TER

Administrative Procedure

Auxiliary Feedwater

Assistant

Plant Supervisor

Nuclear

Balance of Plant

Component

Cooling Water

Company Nuclear Review Board

Dual Unit Outage

Emergency

Core Cooling System(s)

Emergency Diesel

Generator

Equipment out of Service

Emergency Operating

Procedure

Florida Power 5 Light

Minor Engineering

Package

Nonconformance

Reports

Out of Service

Off Normal Operating

Procedure

Operating

Procedure

Operations

Surveillance

Procedures

Plant Change/Modification

Preventive

Maintenance

Post Maintenance

Testing

Plant Nuclear Safety Committee

Plant Operation

Document

Probabilistic Risk Assessment

Plant Supervisor

Nuclear

Plant Work Order

Residual

Heat

Removal

System Acceptance

Turnover group

System Acceptance

Turnover Sheet

Safety Injection

Test Exception Report

References

for Para ra

h 3.1

APPENDIX

B

PROCEDURES

REVIEWED

Procedures

for the new equipment

have been issued to support the startup.

Aside

from the

EDG surveillance

procedures

(OP-023),

the sequencer

tests

(OSP-24.2),

and procedures specifically mentioned other places in this report, the following

procedures

were sampled for completeness

and not content:

0-PME-003. 1,

DC Load Center Undervoltage

Relay Maintenance,

9/8/88

3-OP-005',

4160

Buses A,B, and

D, 8/27/91

4-0P-005,

4160

Buses

A, B,

and

D, 8/27/91,

0-OP-003. 1,

125 Vital

DC System,

8/30/91

3-0P-023,

Emergency Diesel

Generator,

8/16/91

4-0P-023,

Emergency Diesel Generator,

8/16/91

O-OP-024,

Emergency

Bus

Load Sequencer,

8/16/91

O-OSP-024.2,

Emergency

Bus

Load Sequencer

Manual Test,

8/16/91

0-PMI-024. 1,

Emergency

Bus

Load Sequencer

18 Month Maintenance,

8/22/91

MI 59-010,

AMSAC Cabinet Calibration

and Test Instruction,

2/4/91

3-OP-49. 1,

ATWS Mitigating System Actuation Circuitry (AMSAC),6/26/91

4-OP-49. 1,

ATWS Mitigating System Actuation Circuitry (AMSAC), 6/26/91

The above

procedures

were complete

and

no problems

were identified.

References

for Para

ra

h 4.2

0-ADM-101

O-OP-003.4

0-OP-24

3-OP-023

3-ONOP-004

3-ONOP-030

3-OP-030

4-OP-050

4-GOP-301

4-OP-023

~ 2

Procedure Writer's Guide

Auxiliary 120 Volt AC System

Emergency

Bus

Load Sequencer

Emergency Diesel

Generators

Loss of 3A 4KV Bus

Component

Cooling Water Malfunction

Component

Cooling Water System

Residual

Heat

Removal

System

Hot Standby to Power Operation

Emergency Diesel

Generators

8/06/91

8/30/91

8/16/91

8/16/91

7/09/91

6/19/91

7/09/91

8/19/91

8/09/91

8/16/91

References

for

ara ra

h 7.3

0-ADM-006

PTN-90-0381

PA-ESI-EPS. 01

PA-ES I-EPS. 02

FL0-53-20.5006

Human Factors

Review Program,

3/07/91

Turkey Point - Unit

3

8

4

EDG

Enhancement

Project

Nuclear

Safety Related Transmittal of Minutes of Meeting, 4/04/90

EPS

Enhancement

Project

Human

Factors

Engineering

Review,

Preliminary Review, Revision 0, 8/31/90

EPS

Enhancement

Project

Human

Factors

Engineering

Review,

Performance

Validation Final Report,

Revision 0, 6/30/91

EPS

Enhancement

Project

Human

Factors

Engineering

Package,

Revision 2, 8/06/91

APPENDIX C

DRAWINGS REVIEWED

A

comparison

was

made

between

document

control

records

regarding

drawing

distribution.

The team obtained

copies of the following:

controlled document status file (line number listings) - this was the

gA

record total population of "POD 1" drawings;

immediate distribution

acknowledgement list - this listed

the

drawing

distributed

to various departments/locations

which

was

a subset

of the

above;and,

W

drawing index control

system,

operation

and logic diagrams,

5610-T-D-l,

revision

27 - this was the index for drawing deemed critical to the plant

that is found in the control

room and listed

a subset of drawings from the

immediate distribution list.

The population

sampled

was

as follows:

drawing

sheet

revision

component

5610-E-0855

5610-E-0855

5610-T-E-1591

5610-T-E-4501

5610-T-Li

5610-T-Li

5610-T-Li

5610-T-Li

5613-T-Li

5613-T-Li

5614-T-L i

5614-T-Li

B2

196

1

1

9C1

9Dll

12A

33A

33B

33A

33B

284

285

9

97

2

1

20

12

0

Unit 3

0

Unit 3

0

Unit 4

0

Unit 4

breaker list

II

electrical distribution

reactor coolant

system

EDG

sequencer

ANSAC

Except

as

noted

below,

drawings for ne'w equipment

were

checked

in the control

room

and the

TSC with good results.

The

above listed drawings

also

had the

appropriate

revisions.

The list four drawings listed above were for the AHSAC.

These drawings were not

filed chronologically in the control room and in the TSC due to the fact that the

index drawing 5610-T-D-1

had not but updated

to reflect these

new drawings in

their expected order.

Additionally, there was misfiling error between

two of the

control room binders of drawings regarding these

same

ANSAC drawings.

The filing

clerks

wee uncertain

as to where to file the

new 5613

and

5614 series

drawings.

Additionally, the old telemand transfer drawing (5610-T-Li 28A and 29A) that was

replaced

by the

new sequencer

and

new

EDGs equipment

and drawings

were still

listed in the index drawing.

After finding the swapped

sheet drawings for ANSAC

as

a quick check, operations did a audit of their control room drawings per their

e

distribution list with no negative results,

Appendix

C

The above mentioned discrepancies

were considered

minor in light of the massive

changes that have occurred to the drawing files.

By September

27,

1991,

Design

Change

Request

TPH-91-221 will provide disposition for drawing 5610-T-D-l, the

drawing index, that will either declassify,

remove, or reorganize the drawing as

agreed to by engineering

and operations.

APPENDIX

D

EXIT ATTENDANCE

Licensee .Employees

at Exit on September

13,

1991

T.

L.

T.

R.

G.

S.

D.f.

D.

R.

A.

S.

D.

D.

J.

D.

R.

J.

H.

J.

J.

V.

f. Plunkett,

Vice President

W. Pearce,

Plant Manager

Abbatliello, Supervisor

gA

E.

Rose,

Design Control Supervisor

E. Hollinger, Operator Training Supervisor

Salamon,

License Supervisor

Sisk,

Reactor Licensing Engineer

R. Timmons, Security Superintend

J. Davis, Security

L. Teuteberg,

JPN

T. Zielonka, Technical

Department Supervisor

T. Hale, Plant Engineering

Manager

C. Poteralski,

Manager,

Nuclear fuel

W. Haase,

ISEG Chairman

D. Lindsey,

HP Supervisor

R. Powell, License Superintend

J. Earl,

gC Superintend

E. Crockford, Operations

Support Supervisor-

B. Wayland,

Maintenance

Supervisor

Arias, Jr. Technical Advisor to Vice President

D. Webb,

Planning

8

Sch

A. Kaminskas,

OPS Superintendent

NRC Representatives

at Exit

S.

J.

T.

K.

H.

R.

G.

R.

Rubin, RII

Hilhoan, RII, Deputy Regional Administrator

Peebles,

RII

Landis, RII

Ernstes,

RII

Butcher,

Senior Resident

Inspector

.

A. Schnebli,

Resident

Inspector

Auluck,

NRR

G. Galletti,

NRR

L.

R. Moore, RII

Trocine,

Resident

Inspector

Scott,

Resident

Inspector

L.

H.

0