ML17348A586

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Insp Repts 50-250/90-30 & 50-251/90-30 on 900804-31. Violation Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety & Plant Events
ML17348A586
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 09/21/1990
From: Butcher R, Crlenjak R, Schnebli G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17348A585 List:
References
50-250-90-30, 50-251-90-30, NUDOCS 9010120033
Download: ML17348A586 (14)


See also: IR 05000250/1990030

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-250/90-30

and 50-251/90-30

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami, FL'3102

Docket Nos.:

50-250

and 50-251

License 'Nos.:

DPR-31

and

DPR-41

Facility Name:

Turkey Point

3 and

4

Inspection

Conducted:

.August 4,

1990 through August 31,

1990

Inspector:

R.

C.

u cher,

Senior Resident

Inspector

Dat

Si

ned

Approved

y:

. A. Sc

b i, Res dent Inspector

R.

. Cr enja Section

ief

Division of Reactor Projects

Dat

Signed

qz( po

ate Signed

SUMMARY

Scope:

This routine resident

inspector

inspection

entailed direct inspection at the

site

in the

areas

of monthly surveillance

observations,

monthly maintenance

observations,

operational

safety,

and plant events.

Results:

Within the

scope

of this

inspection,

the

inspectors

determined

that

the

licensee

continued to demonstrate

satisfactory

performance

to ensure

safe plant

operations.

One violation was identified.

50-250,251/90-30-01,

Violation.

Failure

to incorporate

revised

instrument

setpoint into instrument calibration data sheet.

REPORT'ETAILS

Persons

Contacted

Licensee

Employe'es

T. V.

  • L. W.
  • T. A.

R. J.

S. T.

K. N.

'E.

F.

R.

G.

V. A.

J.

A.

G. L.

R.

G.

"L. W.

~D.

R.

K. L.

C.

V.

G.

M.

R.

N.

J.

C.

F.

R.

  • M. B.

J.

D.

A. T.

Abbatiello, guality Assurance

Supervisor

Bladow, guality Manager

Finn, Assistant Operations

Superintendent

Gianfrencesco,

Assistant

Maintenance

Superintendent

Hale, Engineering Project Supervisor

Harris, Senior Vice President,

Nuclear Operations

Hayes,

Instrumentation

and Controls Supervisor

Heisterman,

Assistant Superintendent

of Electrical Maintenance

Kaminskas,

Operations

Superintendent

Labarraque,

Senior Technical Advisor

Marsh,

Reactor Supervisor

Mende, Operations

Supervisor

Pearce,

Plant Manager,

Nuclear

Powell, Superintendent,

Plant Licensing

Remington,

System

Performance

Supervisor

Rossi,

equality Assurance

Supervisor

Smith, Service

Manager,

Nuclear

Steinke,

Chemistry Supervisor

Strong, Mechanical

Department Supervisor

Tirmons, Site Security Superintendent

Wayland, Maintenance

Superintendent

Webb, Assistant Superintendent

Planning

and Scheduling

Zielonka, Technical

Department Supervisor

Other

licensee

employees

contacted

included

construction

craftsman,

engineers,

technicians,

operators,

mechanics,

and electricians.

  • Attended exit interview on August 31,

1990

Note;

An alphabetical

tabulation

of acronyms

used

in this report is

listed in paragraph

10.

Followup on Items of Noncompliance

(92702)

A review

was

conducted

of the following noncompliances

to assure

that

corrective actions

were adequately

implemented

and resulted

in conformance

with regulatory

requirements.

Verification of corrective

action

was

achieved

through

record

reviews,

observation,

and

discussions

with

licensee

personnel.

Licensee

correspondence

was evaluated

to ensure

the

responses

were timely and corrective actions

were

implemented within the

time periods specified in the reply.

(Closed)

Violation 50-250,251/89-43-03.

This violation concerned

an

inadequate

clearance

resulting

in the

disassembly

of

a valve in

a

pressurized

system

which resulted

in

a personnel

injury.

The licensee

determined

the root cause for this event

was

inadequate

training for the

-'task.

Corrective

actions

accomplished

included

the following:

The

accounts

of this

event

were

described

in plant safety'eetings;

Supervision

was reinstructed

to clearly communicate their job scope

and

clearance

requirements

to the control

room, includihg re-evaluation

each

time the job scope

changes;

Procedures

O-GME-102.8,

102.9,

and 102.10,

addressing

MOV operator

inspection

and overhaul,

have

been

revised

to

include

a precaution

and caut'.ons

in the body of the procedure to address

. the removal of the stem lock nut or upper bearing

housing with thrust load

'applied

or if the valve is

under

pressure;

and electrical. department-

personnel

assigned

to work on valve actuators

were'rained

on methods,to

render

a pressurized

valve actuator

safe for disassembly.

The inspector

considers

the actions

taken

were

adequate

to prevent

recurrence.

This

item is closed.

Followup on Previous

Inspection

Findings

(92701)'Closed)

URI 50-250,251/90-25-02.

Concerning

the

improper setpoint for

Unit 4

CCW pump automatic start pressure

switch.

On January

6,

1988, the

setpoints

for PC-3/4-611

were

changed

from 75.0 psig

+ 1.5 psig to 60.0

psig

+ 1.5 psig in accordance

with Administrative Procedure

AP 0140.2,

=

"Changing Setpoints,"

which required

a

10 CFR 50.59 safety evaluation

and

subsequent

review by the

PNSC.

This setpoint

change

was

deemed

necessary

to prevent

nuisance

automatic starts

of the

standby

CCW pump(s)

due to

flow transients

when

switching

from two

pump to

one

pump operation.

Single

pump operation results

in

CCW pump discharge

header

pressures

close

to

75.0

psig.

On

January

19,

1988,

PC-3-611

and

PC-4-611'ere

recalibrated

to 60.0

psig

+ 1.5 psig.

Calibration of these

pressure

controllers

was performed under

a

PWO using the setpoint

change

package

as

guidance.

The master

instrument calibration data

sheet for PC-3/4-611

should

have

been

revised

to reflect the

new low pressure

set point and

attached

to the

PWOs at this time.

This administrative

task

was not

performed.

During the Unit 4, Cycle

12 refueling outage,

PC-4-611

had to

be

moved

due to mechanical

interference

with the

CCW heat

exchanger

tube

bundle

replacement.

Upon reinstallation,

PC-4-611

was calibrated to 75.0

psig

+ 1.5 psig using the instrument calibration data sheet

as guidance in

lieu of 60.0 psig

+ 1.5 psig because

the data sheets

had not been revised

to the

new setpoint.

TS 6.8. 1 requires

that written procedures

and

administrative policies shall

be established,

implemented

arid maintained

that meet or exceed

the requirements

and

recommendations

of Appendix

A of

USNRC Regulatory

Guide

1.33

and Sections

5.1

and 5.3 of ANSI N18.7-1972.

ANSI N18.7-1972,

Section

5. 1 requires

that administrative

policies

be

provided to control

the

issuance

of documents,

including changes,

that

prescribe

activities affecting safety-related

structures,

systems,

or

components.

On July 26,

1990, the Unit 4A

CCW pump automatically started

due to pressure

switch

PC-4-611

being set at the wrong value,

75

+ 1.5

psig in lieu of the required

60

+ 1.5 psig.

The root cause for the

improper setpoint of the switch

was inadequate

administrative controls to

ensure

that

revisions

to setpoints

were

incorporated

into instrument

calibration

data

sheets.

This

item

is

identified

as

violation

50-250,251/90-30-01.

4.

(Closed)

IFI 250,251/87-07-03.

Generation of Electrical

Breaker Setpoint

Document.

The status

of this item was reviewed in a telephone

conference

between

Region II Division of Reactor

Safety

(Operational

Programs

Section) staff

and

the licensee

on September

7,

1990.

The licensee

is

tracking

completion

of this

item

.on the

Integrated

Schedule

and

has

established

a

completion

goal

of

May 1991.

The Integrated

Schedule

provides

a tracking vehicle; therefore', this IFI is considered

closed.

Onsite

Followup

and In-Office Review of Written Reports

of Nonroutine

Events

and

10 CFR Part 21 Reviews

(90712/90713/92700)

The Licensee

Event Reports

and/or

10 CFR Part 21 Reports

discussed

below

were reviewed.

The inspectors

verified that reporting requirements

had

been

met, root cause

analysis

was

performed,

corrective actions

appeared

~

appropriate,

and generic applicability had

been considered.

Additionally,

the inspectors

verified the licensee

had reviewed

each

event,

corrective

actions

were

implemented,

responsibility for corrective actions not'fully

completed

was clearly assigned,

safety

questions

had

been

evaluated

and

resolved,

and

violations of regulations

or

TS conditions

had

been

identified.

When applicable,

the criteria of 10 CFR 2, Appendix C, were

applied.

~ (Closed)

LER 50-250/89-01.

Concerning

the

3A

ICW being declared

OOS while

performing operability tests

of the

8

EDG.

This issue

was previously

discussed

in detail in IR 50-250,251/88-40.

This

LER is closed.

(Closed)

LER 50-250/89-02.

Concerning

a reactor

shutdown required

by TS

due to

a

RCS leak at the seal table.

This issue

was previously identified

as IFI 50-250,251/88-40-03

and subsequently

closed in IR 50-250,251/89-52.

This

LER is closed.

(Closed)

LER 50-250/89-03.

Concerning

the automatic isolation of control

room ventilation

system

during testing.

This

issue

was

previously

discussed

in detail in IR 50-250,251/88-40.

This

LER is closed.

(Closed)

LER 50-250/89-09.

Concerning

Appendix

R safe

shutdown analysis.

This issue

was previously discussed

in IR '50-250,251/89-18.

This

LER is

closed.

(Closed)

LER 50-250/89-10.

Concerning

a

loss

of power to the vital

instrument

rack

and automatic isolation of control

room and containment

ventilation.

This event

was discussed

is detail

in IR 50-250,251/89-27.

This

LER is closed.

(Closed)

LER 50-250/89-11.

Concerning

two safeguards

actuations

due to

personnel

error.

This

event

was

previously identified

as Violation

50-250,251/89-27-04

which was subsequently

closed in IR 50-250,251/89-54.

This

LER is closed.

(Closed)

LER 50-250/89-14.

Concerning

CCW flow rates

to the

ECCs

being

below design

basis

accident

requirements

due to inadequate

administrative

controls.

This issue

was discussed

in detail in IR 50-250,251/89-43

and

identified as

NCV 89-43-01.

This

LER is closed.

(Closed)

LER 50-250/89-20.

Concerning

corrosion of the terminal

blocks

for the NSIVs.

This issue

was previously discussed

in IR 50-250,251/89-54=

and

was identified as Violation 89-54-02.

Close out of this issue will be

accomplished

when closing out the violation.

This

LER is closed.

(Closed).

LER 50-250/89-21.

Concerning

the

use

of

a

high integrity

container

not authorized

in the process

control

program.

This issue

was

previously discussed

in

IR 50-250,251/89-35

and

was identified

as

NCY

89-35-02.

This

LER is closed.

(Closed)

LER 50-251/89-01.

Concerning

the

A

EOG inoperable with 4B

RHR

pump

00S

due

to miscommunication

between

personnel.

This

issue

was

previously discussed

in

IR 50-250,251/89-06

and identified

as

an'NCV.

This

LER is closed.

(Closed)

LER 50-251/89-02.

Concerning

a

safeguards

actuation

due to

personnel

error while installing fuses in the safeguard

racks.

This issue

was

previously

identified

as

Violation

50-250,251'/89-18-01

and

subsequently

closed in IR 50-250,251/89-52.

This LER is closed.

(Closed)

LER

50-251/89-03.

Concerning

a

reactor trip during

the

performance

of

SG protection

channel

test.

This issue

was previously

identified as Violation 50-250,251/89-24-01

and subsequently

closed in IR

50-250,251/90-04.

This

LER is closed.

(Closed)

LER 50-251/89-04.

Concerning

the

loss of alternate

hot leg

injection flow path

due to hydraulic locking of the injection valve.

This

event

was

previously

identified

as

IFI

50-250,251/89-24-05

and

subsequently

closed in IR 50-250,251/89-27.

This

LER is closed.

(Closed)

LER 50-251/89-05.

Concerning

the

4A accumulator

level

TS not

being

met

due to wrong level transmitter identified

as malfunctioning.

This event

was previously discussed

in IR 50-250,251/89-34

and identified

as

NCV 50-251/89-34-01.

This

LER is closed.

(Closed)

LER 50-251/89-06.

Concerning

degraded

ICW flow to

CCW heat

exchangers

due to valve failure.

This event

was previously discussed

in

IR 50-250,251/89-34.

This

LER is closed.

(Closed)

LER

50-251/89-08.

Concerning

the

CS

pump

being

00S for

maintenance

longer

than

the

TS allowed period

due to increased

motor

vibration.

This event

was previously discussed

in IR 50-250,251/89-40.

This

LER is closed.

(Closed)

LER 50-251/89-12.

Concerning

the

A loop of containment

wide

range level indication being de-energized

longer than the

TS allowed time

period.

This issue

was previously discussed

in IR 50-250,251/89-45

and

identified as

NCV 89-45-04.

This

LER is closed.

(Closed)

LER 50-251/89-13.

Concerning

a missed

surveillarice

on

ICW to

.

TPCW isolation valves

due to personnel

error.

This issue

was previous y

1

identified

as

URI

50-250,251/89-45-05

and

later

as

NCV

50-250,251/89-52-07.

This

LER is closed.

(Closed)

LER 50-251/90-07.

Concerning

the improper setpoint for Unit 4

CCW

pump automatic start

pressure

switch.

This

issue

was

previously

identified as

URI 50-250,251/90-25-02

and is discussed

in paragraph

3 of

this report.

This

LER is closed.

5.

Monthly Surveillance

Observations

(61726)

The inspectors

observed

TS required surveillance

testing

and verified:

the test

procedure

conformed

to the requirements

of the TS; testing

was

~

performed in accordance

with adequate

procedures;

test, instrumentation

was

calibrated; limiting 'conditions for operation

were met; test re'suits

me't

acceptance criteria requirements

and were reviewed

by personnel

other than

the

individual directing

the test;

deficiencies, were identified,

as

appropriate,

and

were

properly

reviewed

and

resolved

by

management

ersonnel

and

system restorati.on

was adequate.

For completed tests,

the

inspectors verified testing

frequencies

were met and tests

were performe d

by qualified individuals.

The

inspectors

witnessed/reviewed

portions

of

the

following test

activities:

6.

OP 1604. 1, Full Length

RCC - Periodic Exercise

OP 4004.2,

Safeguard

Relay

Rack Train A,B - Periodic Test

O-OSP-022.4,

EDG Fuel Oil Transfer

Pump Inservice Test

O-ADM-716, Infrared Thermography

(For

EDG Fuel Oil Transfer

Pumps)

The inspectors

determined that the above testing activities were performed

in

a satisfactory

manner

and

met

the

requirements

of the

TS.

No

violations or deviations

were identified in the areas

inspected.

Monthly Maintenance

Observations

(62703)

Station

maintenance

activities of safety-related

systems

and

components

were observed

and

reviewed to ascertain

they were conducted in accordance

with approved

procedures,

regulatory guides,

industry codes

and standards,

and in conformance with TS.

The following items

were considered

during this review,

as appropriate:

LCOs were

met while

components

or systems

were

removed

from service;

approvals

were

obtained

prior

to initiating work; activities

were

accomplished

using

approved

procedures

and were inspected

as applicable;

procedures

used

were

adequate

to control

the activity; troubleshooting

activities

were controlled

and repair records

accurately

reflected

the

maintenance

performed;

functional

testing

and/or

calibrations

were

performed prior to returning

components

or systems

to service;

gC records

were

maintained;

activities

were

accomplished

by qualified personnel;

parts

and materials

used

were properly certified; radiological controls

were properly

implemented;

gC hold points

were established

and

observed

where

required;

fire prevention

controls

were

implemented;

outside

contractor

force activities

were

controlled

in

accordance

with the

approved

gA program;

and housekeeping

was actively pursued.

The inspectors

witnessed/rev'iewed

portions of the following maintenance

activities in progress:

Troubleshooting

No.

3 Blackstart

Diesel

High Level Transfer

Switch

Failure.

Cleaning of 48

TPCW Heat Exchanger.

Repair of 4A Heater Drain Pump Seal.

For those

maintenance

activities observed,

the inspectors

determined that,.

the activities'ere

conducted

in a satisfactory

manner

and that the work

was

properly

performed

in accordance

with approved

maintenance

work

orders.

No violations

or deviations

were identified in the

areas

inspected.

7.

Operational

Safety Verification (71707)

The inspectors

observed

control

room operations,

reviewed applicable logs,

conducted

discussions

with control

room

operators,

observed

shift

turnovers,

and confirmed operability of instrumentation.

The inspectors

verified

the

operab'ility

of

selected

emergency

systems,

verified

maintenance

work orders

had

been

submitted

as

required,

and verified

followup and prioritization of work

was

accomplished.

The inspectors

reviewed

tagout

records,

verified compliance

with

TS LCOs,

and verified

the return to service of affected

components.

By observation

and direct interviews, verification

was

made that

the

physical security plan was being implemented.

Plant

housekeeping/cleanliness

conditions

and

implementation

of

radiological controls were observed.

Tours of the intake structure

and diesel, auxiliary, control,

and turbine

buildings

were

conducted

to observe

plant equipment conditions

including

potential fire hazards,

fluid leaks,

and excessive

vibrations.

The inspectors

walked

down accessible

portions of the following safety

related

systems

to verify operability and proper valve/switch alignment:

A and

B Emergency Diesel

Generators

Control

Room Vertical Panels

and Safeguard's.Racks

'

'

Intake Cooling Water Structure

4l60 Volt Buses

and 480 Volt Load and Motor Control Centers

Unit 3 and

4 Feedwater

Platforms

Unit 3 and

4 Condensate

Storage

Tank Area

Auxiliary Feedwater

Area

Unit 3 and

4 Main Steam Platforms

Auxiliary Building

On August

28,

1990,

at I:20

pm,

th'e licensee

secured

the Uni't 4

SFP

cooling sy'tem to determine

the

SFP

heatup rate.

This special

test

was'onducted

per

TP-642

in preparation

for

the

upcoming

SFP

system

modifications scheduled

to start later this year.

The inspectors

reviewed

the licensee's

safety evaluation for adding additional

temper'ature

probes

for the test.

Initial SFP heater

temperature

was approximately

98 degrees

Fahrenheit.

The inspectors,

as

a result of routine plant tours

and various operational

observations,

determined

that

the

general

plant

and

system

material

conditions

were

being satisfactorily

maintained,

the

plant

security

program

was

being effective,

and

the overall

performance

of plant

operations

was

good.

No violations or deviations

were identified in the

areas

inspected.

Plant Events

(93702)

The following plant event

was

reviewed to determine facility status

and

the

need for further followup action.

Plant

parameters

were evaluated

during transient

response.

The significance of the event

was evaluated

along with the

performance

of the appropriate

safety

systems

and

the

actions

taken

by the licensee.

The inspectors

verified that required

notifications were

made to the

NRC.

Evaluations

were performed relative

to the

need for additional

NRC response

to the event.

Additionally, the

following issues

were

examined,

as

appropriate:

details

regarding

the

cause of the event;

event chronology; safety system performance;

licensee

compliance

with approved

procedures;

radiological

consequences,

if any;

and proposed corrective actions.

On August

12,

1990,

at 4:28

pm, with Unit 4 at

100K,

a reactor trip

occurred

due to low-low level

in the

A steam generator.

The event

was

caused

by

the

4B condensate

pump tripping

on overcurrent

which

was

immediately followed by

a trip of the

4A feedwater

pump.

The trip of the

feedwater

pump initiated

a turbine

runback to less

than

60 percent

power

as designed.

Steam generator

levels

dropped

below

15 percent

narrow range

due to shrink

caused

by the

combined effects of a partial

loss of feed

flow, turbine runback,

and subsequent

reactor trip.

The trip of a running

condensate

pump will normally start

the standby

condensate

pump

and not

trip the

SGFW

pump if the

swap

occurs within five seconds.

The five

seconds

is timed

by an Agastat relay in the

SGFW

pump breaker trip logic.

Upon investigation it was

discovered

that the Agastat relay

was set at

9.

10.

0. 15 seconds

in lieu of the required five seconds.

The low setting of the

'elay did not allow enough

time for the 'start of 'the standby

condensate'-'ump

to be sensed

by the breaker trip logic and therefore

a

SGFW

pump trip . "..

signal

was generated.

The relay was reset to 5.0 sec

+ 10% for the

A SGFW

pump

and

the relay for the

B

SGFW

pump was also reset after testing found

it to be set at 3.3 seconds.

The

ERT is currently trying to determine

the

cause for the

low setpoint

on the relay

and provide

a method of control.

The unit was

subsequently

returned

to service at 4:43

am

on August

14,

1990.

'

'No 'violations'or deviations

were identified in the areas

inspected.

Exit Interview (30703)

The

inspection

scope

and

findings

were

summarized

during -management

interviews held throughout

the reporting period with the Plant Manager-

Nuclear

and selected

members

of his staff.

An exit meeting

was conducted

on

August

31,

1990.

The

areas

requiring

management

attention

were

reviewed.

No proprietary

information

was

provided to the inspectors

during the reporting period.

The inspectors

had the following findings:

50-250,251/90-30-01,

Violation.

Failure to incorporate

revised

instrument

setpoint into instrument calibration data sheet.

Acronyms

and Abbreviations

ADM

AFW

AP

ASME

CCW

CFR

CS

DP

ECC

EDG

ENS

ERDADS

ERT

FPL

FSAR

GME

HHSI

ICW

IE

IFI

IR

LCO

LER

LIV

Administrative

Auxiliary Feedwater

Administrative Procedures

American Society of Mechanical

Engineers

Component

Cooling Water

Code of Federal

Regulations

Containment

Spray

Differential Pressure

Emergency

Containment

Coolers

Emergency

Diesel

Generator

Emergency Notification System

Emergency

Response

Data Acquisition Display System

Event Response

Team

Florida

Power

& Light

Final Safety Analysis Report

General

Maintenance Electrical

High Head Safety Injection

Intake Cooling Water

Inspection

Enforcement

Inspector

Followup Item

Inspection

Report

Limiting Condition for Operation

Licensee

Event Report

Licensee Identified Violation

LOCA

MP

MOV

MSIV

NCR

NCV

NPO

NPSH

NRC

ONOP

OOS

OP

OTSC

PC/M

PNSC

PSN

PSP

QA

QC

RCC

RCO

RCP

.RCS

RHR

SFP

SFW

SG

SNPO

SRO

TPCW

TS

TSA

URI

Loss of Coolant Accident

Maintenance

Procedures

Motor Operated

Valve

Main Steam Isolation Valve

Non-conformance

Report

Non-Cited Violation

Nuclear Plant Operator

Net Positive Suction

Head

Nuclear Regulatory

Commission

Off Normal Operating

Procedure

Out of Service

'perating

Procedure

On the Spot Change

Plant Change/Modification

Plant Nuclear Safety Committee

Plant Supervisor

Nuclear

Physical Security Procedures

Quality Assurance

Quality Control

Rod Control Cluster

Reactor Control Operator

Reactor Coolant

Pump

Reactor

Coolant System

Residual

Heat

Removal

Spent

Fuel Pit

.Standby

Feedwater

Steam Generators

Senior Nuclear Plant Operator

Senior Reactor Operator

Turbi.ne Plant Cooling Water

Technical Specification

Temporary

System Alteration

Unresolved

Item