ML17347B167

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Insp Repts 50-250/89-24 & 50-251/89-24 on 890429-0526. Violations Noted.Major Areas Inspected:Monthly Surveillance Observations,Maint Observations,Esf Walkdowns,Operational Safety & Plant Events
ML17347B167
Person / Time
Site: Turkey Point  
Issue date: 06/28/1989
From: Butcher R, Crlenjak R, Mcelhinney T, Schnebli G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17347B164 List:
References
50-250-89-24, 50-251-89-24, NUDOCS 8907120302
Download: ML17347B167 (34)


See also: IR 05000250/1989024

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

'EGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Repor t Hos.:

50-250/89-24

and 50-251/89-24

Licensee:

Florida Power

and Light Company

9250 West Flagler Street

Niami,

FL

33102

Docket Nos.:

50-250

and 50-251

License Nos.:

DPR-31

and

DPR-41

Facility Name:

Turkey Point

3 and

4

Inspection

Conducted:

April 29,

1989 through

Nay 26,

1989

Inspectors:

L~Xt'

. ~M

R.

C. Butcher, Senior Resident

Inspector

~

.1c~

'

Da

e Signed

T.

F. Ncflhinney, Resident

Inspector

c.. P~

G. A.

Sc

neb i, Resident

Inspector

Approved by:

R

V. Crlenj

,

ection

Ch'

Division of Reactor Proje

s

Date Si

ned

Dat

Signed

at

Sig ed

SUNNARY

Scope:

This routine resident

inspector

inspection

entailed direct inspection at the

site in the

areas

of monthly surveillance

observations,

monthly maintenance

observations,

engineered

safety

features

walkdowns,

operational

safety

and

plant events.

Results:

One violation with two examples

was identified:

Failure to follow procedure

resulting in an inadvertent

drop of Rod N-8, paragraph

5.

Failure to follow

procedure resulting in a reactor trip during surveillance testing,

paragraph

10.

One non-cited violation was identified regarding

the use of the wrong calibra-

tion curves during

RTD calibration,

paragraph

10.

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Two unresolved

items** were identified:

Determine

the

cause of inadequate

clearance

control, paragraph

5.

Resolution of document control discrepancies,

paragraph

8.

Two Inspector

Followup Items

were identified:

Followup on concerns

with the

control

and

storage

.of hydrogen

on site,

paragraph

8.

Followup

on

the

resolution to correct the failure of MOV-4-751, paragraph

10.

.

    • Unresolved items

are matters

about

which more information is required to

determine

whether they are acceptable

or may involve violations or deviations.

REPORT DETAILS

1.

Persons

Contacted

2,

Licensee

Employees

  • J.

W. Anderson, guality Assurance

Supervisor

J. Arias, Assistant to Plant Manager

  • L. W. Bladow, Plant guality Assurance

Superintendent

  • J. E. Cross,

Plant Manager-Nuclear

  • R. J. Earl, guality Control Supervisor

T. A. Finn, Training Supervisor

S. T. Hale, Engineering Project Supervisor

K. N. Harris, Site Vice President

  • R. J. Gianfrancesco,

Maintenance

Superintendent

  • V. A. Kaminskas,

Reactor

Engineering Supervisor

J.

A. Labarraque,

Senior Technical Advisor

R.

G. Mende, Operations

Supervisor

L. W. Pearce,

Operations

Superintendent

  • S. guinn, Acting Radiochemist
  • F. H. Southworth, Assistant to Site

VP

  • R. Steinke,

Chemistry Supervisor

J..C. Strong, Mechanical

Department

Supervisor

  • K. Van Dyne, Acting Regulatory

and Compliance Supervisor

M. B. Wayland, Electrical

Department

Supervisor

J.

D. Webb, Operations

- Maintenance

Coordinator

~

~

Other

licensee

employees

contacted included

construct~on

craftsman,

engineers,

technicians,

operators,

mechanics,

and electricians.

  • Attended exit interview on May 26,

1989.

Note

An Alphabetical

Tabulation of acronyms

used

in this report is

listed in paragraph

13.

Followup on Pr'evious

Inspection

Findings

{92702)

e followin

noncompliances

to assure

that

A review

was

conducted

of the

g

d

lted in conformance

if'i

f corrective aetio

wa

s were

ade uately implemented

an

resu

e

i

with regulatory

require ments.

Ver

ica

on

o

ion and discussions

with licensee

achieved

through record r'eviews, observat

on an

s

c

nnel.

Licensee

correspondence

was

evaluated

to ensure

a

e

d th t

rrective actions

were implemented within

responses

were timely an

a

corr

the time periods specified in the r'eply.

-251 83-39-04,

Failure to

remove old seal

1

d fl

t

'tt

transmitters.

This concern

invo ve

ow

drawing

5610-T-E-4503,

Reactor

Coolant

Pump

11

d

The licensee

generated

PC/M 84-104,

Details,

but were still insta

e

.

e

RCP

Seal

Leakoff No.

1 Instrumentation,

which removed

the flow trans-

mitters.

The

PC/M was

completed

and turned over to plant operations

on

September

5, 1986.

This item is closed.

Followup on Inspector

Followup Items

( IFIs)

(Closed)

IFI 50-250,251/85-37-03.

Contr'ol

Room Noise Level

Increase

due

to Ceiling Insulation

Removal.

The licensee

installed

a carpet in the

control

room to aid in noise reduction.

Engineering

recommended

a carpet

with specifications

on weight, height

and Noise. Reduction Coefficient.

However,

the

carpet

installed

did not

completely

meet

engineerings

specifications.

Therefore,

a noise reduction effect study

was

performed

in March

1988

by

a contractor.

The study determined

that the carpet

reduced

the

noise

level

by approximately

3 decibels

(db).

The noise

levels

measured

during

normal plant operation

were

found slightly below

the

NRC criterion of 65 db maximum.

This item is closed.

(Closed)

IFI 50-250,251/85-02-04.

Engineering

to Evaluate

the Monitoring

of Loss of Control Voltage at the Emergency

Diesel

Generators

(EDGs).

The

licensee

generated

Plant Change/Modification

(PC/H)86-185, Annunciation

In Hain Control

Room

On

Loss of

EDG Control

Power,

due to concerns

addressed

in

LER 50-250,251/85-02.

This

PC/M added

annunciation

in the

main control

room for the

A and

B

EDGs starting circuitry.

In order to

reduce

the probability of blowing fuses,

the non-resistored

indicating

lights were replaced

with resistored

indicating lights at the

A and

B

EDG

engine panels.

The

PC/M was

implemented

on March 14,

1989 and March 21,

1989, for A and

B EDGs respectively.

This item is closed.

Onsite

Followup

and

In-Office Review of Written Reports of Nonroutine

Events

(92700/90712)

The

Licensee

Event

reports

(LERs)

discussed

below

were

reviewed

and

closed.

The inspectors

verified that reporting requirements

had

been met,

root

cause

analysis

was

performed,

corrective

actions

appeared

appropriate,

and generic applicability had

been considered.

Additionally,

the

inspectors

verified that

the

licensee

had

reviewed

each

event,

corrective actions

were implemented, responsibility for corrective actions

not fully completed

was clearly assigned,

safety

questions

had

been

evaluated

and resolved,

and violations of regulations

or TS conditions

had

been identified.

When applicable,

the criteria of 10 CFR 2, Appendix C,

were applied.

(Closed)

LER 50-250/89-05,

Automatic

AFW Pump Actuation Following Attempt

to Start Steam Generator

Hain Feedwater

Pump.

This event

was discussed

in

detail in Inspection

Report 50-250,251/89-06

and the corrective actions

required are complete.

This

LER is closed.

(Closed)

LER 50-250/89-04,

Reactor Trip Due to Defective Procedure

During

Steam

Generator

Protection

Channel

Testing.

The event discussed

in this

LER was identified previously as Violation- 50-250,251/89-06-02

and will be

followed through closeout of the violation.

This

LER is closed.

5.,Monthly Surveillance Observations

(61726)

The inspectors

observed

TS required

surveillance

testing

and verified:

That the test

procedure

conformed to the requirements

of the TS, testing

was performed in accordance

with adequate

procedures,

test instrumentation

was calibrated,

limiting conditions for operation

(LCO) were met, test

results

met

acceptance

criteria

requirements

and

were

reviewed

by

personnel

other than the individual directing the test, deficiencies

were

identified,

as appropriate,

and were properly reviewed

and resolved

by

management

personnel

and that

system

restoration

was

adequate.

For

completed tests,

the inspectors verified that testing frequencies

were met

and tests

were performed

by, qualified individuals.

The

inspectors

witnessed/reviewed

portions

of

the

following test

activities:

4-PMI-028.3

RPI Hot Calibration,

CRDM Stepping Test,

and

Rod

Drop Test.

TP-522

Unit 4 Alternate

Shutdown

Panel

Performance

Test.

0

4-0SP-075.1

Auxiliary Feedwater

Train

1 Operability

Verification.

On

May 7,

1989,

the licensee

experienced

an unexpected

drop of Rod

M-8.

The licensee

was performing 4-PMI-028.3,

RPI Hot Calibration,

CRDM Stepping Test and

Rod Drop Test, revision dated 3/30/89, Section

6.3,

CROM Stepping

Test for

Rod

H-12,

when

Rod

M-8 dropped.

Investigation

by the

ISC department

found that .the moveable coil fuse

for rod M-8 was pulled, while stepping

rod H-12, which caused

rod M-8

to drop unexpectedly.

A review of Section 6.3 did not identify any

provision for removing the moveable

gripper coil fuse for any

CRDMs

during the performance of this section.

However, the next section of

the procedure,

Section 6.4,

Rod Drop Test, did provide for removal of

these

fuses for the bank under test,

which included both rods M-8 and

H-12.

Discussion with personnel

involved in the test indicated that

miscommunication

between

personnel

in the Control

Room and the Motor

Control

Center

(where the fuses

were pulled) caused

the personnel

to

mistakenly

proceed

into the rod drop section of the procedure

which

caused

the event.

TS 6.8.1 requires

that written procedures

and

administrative

policies

shall

be

established,

implemented

and

maintained that meet or exceed

the requirements

and recommendations

of Appendix A of USNRC Regulatory

Guide 1.33

and Sections

5.1 and 5.3

of ANSI N18.7-1972,

'Contrary to the above,

licensee

personnel

failed

to follow procedure

4-PMI-028.3

by proceeding

to Section 6.4 of the

procedure,

prior to

completing

Section

6.3,

resulting

in

an

inadvertent

drop of Rod M-8.

This is identified as the first example

of Violation 50-250,251/89-.24-01.

b.

The inspectors

witnessed

the performance

of TP-522, Unit 4 Alternate

Shutdown

Panel

Performance

Check,

on May 24 and 25,

1989.

The test

was being performed to ensure

the unit could be shutdown from outside

the control

room utilizing the Alternate

Shutdown

Panel

and personnel

at various locations

throughout the plant to perform local operation

of various

components.

The test started

with T

AVG stable

between

545

and

550 degrees

F, being controlled

by control

room personnel.

The

normal shift complement

was

to

remain

in the control

room

throughout .the test with instructions

to abort the test

and

resume

control

of the

plant if an

abnormal

situation

developed.

An

additional shift complement

dedicated

to the test

evacuated

the

control

room and proceeded

to their assigned

stations.

At this time

control of the systems'nd

components

required to place

the plant in

a cold shutdown condition was shifted to the Alternate

Shutdown

Panel

and

a cooldown

was

commenced.

The initial cooldown

was conducted

by

using

"8" "Auxiliary Feedwater

Pump

and

dumping

steam

to the

atmosphere.

When attempting to place

the plant on

RHR to cooldown to

less, than

300 degrees

F, MOV-4-751

(RHR suction isolation valve from

~

loop

"C" hot leg)

would not open.

The test

was

terminated

and

control

of the

plant

was

returned

to

the

control

room

where

conditions

were maintained

stable until the

problem with MOV-4-751

was

resolved

and testing

could

be

resumed.

See section 10,'Plant

Events,

for

a discussion

on 'this valve

problem

on

May 23,

1989.

Testing

was

resumed

on May 24,

1989,

and the plant was cooled

down to

less

than

300 degrees

F, using the

RHR system.

At that time the test

was completed satisfactorily

and control

was returned to the control

room.

The inspectors

consider that the test went very well with all

systems

and components

functioning as required, with the exception of

MOV-4-751.

Minor deficiencies

were noted

by the inspectors

and the

licensee

and were

documented

in PTN-OPS-89-154,

dated

May 30,

1989,

with the appropriate corrective actions to be taken

as assigned

to the

responsible

departments.

co

On

May 22,

1989,

the

licensee

performed

4-0SP-075.1,

Auxiliary

Feedwater

Train

1 Operability Verification Test, after repairs

were

made

on

Flow Control

Valves

(FCV)

2817

and

2818.

The test

was

unsatisfactory

due to

FCV-2818 failing the test.

The test

was

reperformed after

I&C worked

on the valve.

During the test the

C

Steam

Generator

(SG) did not receive

AFW flow.

Investigation

by the

licensee

revealed

clearance

4-89-5-149

was not released

by I&C.

This

clearance

isolated

FCV'-2818, which feeds

the

C SG.

The licensee

was

investigating

the

cause of this event at the

end of the inspection

period.

Therefore,

this

item will be tracked

as

Unresolved

Item

50-250,251/89-24-04.

-

6.

Engineered

Safety Features

Walkdown (71710)

The inspectors

performed

an inspection

designed

to verify the operability

of the

Emergency

Diesel

Generators

and the Safety Injection System to

support

reactor

startup.

The

following

cr iteria

were

used,

as

appropriate,

during this inspection:

~4 H.

WP ~~

(

g~p g

a.

System

lineup

procedures

matched

plant

drawings

and

as built

configuration.

b.

Housekeeping

was adequate

and-appropriate

levels of cleanliness

were

being maintained.

c.

Valves in the

system

were correctly installed

and did not exhibit

signs of gross

packing

leakage,

bent

stems,

missing

handwheels

or

improper 'labeling.

d.

e.

Hangers

and supports

were

made

up properly and aligned correctly.

Valves in the flow paths

were in the correct position

as required

by

the

applicable

procedures

with power available

and

valves

were

locked/lock wired as required.

Local

and

remote

position

indication- were

compared

and

remote

instrumentation

was functional.

7.

g.

Major system

components

were properly labeled.

No violations or deviations

were identified in the areas

inspected.

Monthly Maintenance

Observations

(62703)

Station

maintenance

activities

on safety related

systems

and

components

were

observed

and

reviewed

to ascertain

that

they were

conducted

in

accordance

with approved

procedures,

regulatory guides,

industry codes

and

standards,

and in conformance with TS.

The following items

were considered

during this review,

as appropriate:

That

LCOs were met while components

or systems

were

removed

from service;

approvals

were

obtained

prior to initiating work; activities

were

accomplished

using

approved

procedures

and were inspected

as applicable;

procedures

used

were

adequate

to control

the activity; troubleshooting

activities

were controlled

and repair records

accurately

reflected

the

maintenance

performed;

functional

testing

and/or

calibrations

were

performed prior to returning

components

or systems

to service;

gC records

were maintained;

activities

were

accomplished

by qualified personnel;

parts

and materials

used

were properly certified; radiological controls

were properly implemented;

gC hold points

were established

and observed

where

required;

fire prevention

controls

were

implemented;

outside

contractor

force activities

were controlled

in accordance

with the

approved

gA program;

and housekeeping

was actively pursued.

The inspectors

witnessed/reviewed

portions of the following maintenance

activities in progress:

Troubleshooting

LT-4-474 and LT-4-475, "A" Steam Generator

Level

Channels After Failure.

Troubleshooting

of

PORV

PCV-4-456,

to

determine

cause

of

spurious

opening.

Replacement

of

FCV-4-489

and

FCV-4-499,

"B" and

"C"

Steam

Generator

Feedwater

Bypass

Valves.

Troubleshooting

MOV-4-751 failure to open.

See

section

10,

Plant Events,

dated

May 23,

1989.

Troubleshooting

Unit 4

AFW Flow Control Valves.

No violations or deviations

were identified in the areas

inspected.

8.

Operational

Safety Verification (71707)

The inspectors

observed

control

room operations,

reviewed applicable logs,

conducted

discussions

with control

room

operators,

observed

shift

turnovers

and confirmed operability of instrumentation.

The inspectors

verified the operability of selected

emergency

systems,

verified that

maintenance

work orders

had

been

submitted

as required

and that followup

and prioritization of work was

accomplished.

The inspectors

reviewed

tagout records,

verified compliance with TS

LCOs and verified the return

to service of affected

components.

By observation

and direct interviews, verification was

made that

the

physical security plan

was being implemented.

Plant

housekeeping/cleanliness

conditions

and

implementation

of

radiological controls were observed.

Tours of the intake structure

and diesel, auxiliary, control'nd turbine

buildings were

conducted

to observe

plant equipment conditions

including

potential fire hazards, fluid leaks

and excessive vibrations.

The inspectors

walked

down accessible

portions of the following safety

related

systems

to verify operability and proper valve/switch alignment:

A and

B Emergency Diesel

Generators

Control

Room Vertical Panels

and Safeguards

Racks

Intake Cooling Water Structure

4160 Volt Buses

and 480 Volt Load and Motor Control Centers

Unit 3 and

4 Feedwater

Platforms

Unit 3 and

4 Condensate

Storage

Tank Area

Auxiliary Feedwater

Area

Unit 3 and

4 Main Steam Platforms

a ~

In response

to

NRC Information Notice 89-44,

Hydrogen Storage

on the

Roof 'of the .Control

Room,

the resident

inspectors

were requested

to

canvass their facilities to determine:

Distance

from the

hydrogen

storage facility to the nearest

safety-related

structure or air intake.

Maximum volume of gaseous

or liquid hydrogen

stored

on site in

standard

cubic feet or gallons respectively.

The residents

obtained

the

above

information from the licensee

and

forwarded it to the region

as requested.

Based

on the information

collected

and

concerns

previously

expressed

to the licensee,

the

following concerns

with hydrogen

storage

and control of hydrogen

on

site will be followed up for resolution

as Inspector

Followup Item

50-250,251/89-24-02.

( 1)

Administrative controls

or limits have

not

been

established

on the

amount of hydrogen that could

be located in the identi-

fied hydrogen storage

areas.

(2)

The

back-up

hydrogen

storage trailer location is within 5 feet

of the Unit

3

RWST and about

55 feet from the Unit 4

RWST.

Based

on the resident

inspectors

concerns,

the back-up hydrogen

storage

trailer

was

previously

removed

from this location.

However,

there

were

no administrative

controls

to

prevent

locating the hydrogen trailer in this location.

(3)

The

Gas

House,

which stores

hydrogen

gas cylinders, is within 14

feet of the safety injection

pump suction line from the

RWST for

both Unit 3 and Unit 4.

The

Gas

House is also about

15 feet

from the Unit 3

RWST and

45 feet from the Unit 4

RWST.

(4)

An administrative limit on the quantity of hydrogen that could

be brought

on site

has not been established.

b.

While preparing'o

inspect controlled

documents for completeness

and

the latest revision, the inspectors

determined

there

was insufficient

information available

from document control to identify the drawings

required

at

a

given location

and their latest

revision

number.

Subsequently,

document control

developed

a list of drawings required

at controlled drawing stations

with the latest revision number.

The

inspectors

checked

various

procedures

and

drawings

at

the

TSC,

Control

Room,

and

IKC Department

to determine if.they

were complete

and

up to date.

The following results

were -found:

(1)

The following discrepancies

were found at the TSC.

AP 0103.18

and

AP 0103.36 were missing.

OP-0204.2

had revisions

dated July 26,

1988

and April 26,

1989 in the file.

HP 11550.70

was in the file but has

been superseded.

(2)

The

following discrepancies

were

found

in drawing

control

document

No.

10 in the control

room.

Drawing 5610-T-E-4062,

sheet

3,

had revisions

57

and

58

filed, in the book.

Drawing

5610-T-E-4062/R18,

sheet

5,

revision

1,

and

5610-T-E-4534,

sheet

1, revision

39 were missing.

The following obsolete

red line drawings

were still in the book

along with the current drawing.

5610-T-E-4501/R74,

sheet

1, Rev. 0;

5610-T-E-4505/R25,

sheet

1, Rev. 0.

5610-T-E-4505/R3,

sheet

5, Rev. 0.

5610-T-E-4512/R68,

sheet

1, Rev. 2.

5610-T-E-4512/R25,

Sheet 2, Rev.

1.

5610-T-E-4531/R48,

sheet

1, Rev. 0.

5610-T-E-4534/R18,

sheet

2, Rev.O.

5610-T-E-4535/Rll, sheet

1, Rev.O.

Drawing 5610-T-E-4532,

sheet

1,

had revision

7 and

8 filed

in the book.

(3)

The inspector

examined

the

back log of unfiled documents

in the

ISC Department

and found documents

dating back to February

1989

that

had not been filed nor had the cover sheet

been returned to

document control.

Administrative

Procedure

(AP)

0190.86,

Document

Control,

dated

October 27,

1988,

provides instructions for the control of documents

(drawings

and

procedures).

AP 0190.86,

paragraph

5.5,

states

the

holder of

a controlled

document

is responsible

for the

proper

updating

and maintenance

of controlled

documents

in their custody,

the

prompt return of dated

and signed receipt

acknowledgement

cover

letters,

and

superseded

controlled documents.

Paragraph

8.1.7 of AP

0190.86

requires

the

document

holder complete

the cover letter

and

return it to Document Control within 30 days

along with superseded

documents.

The findings

noted

above

indicate this is not being

accomplished.

guality Instruction (gI) 6-PTN-1,

Document Control, dated

March 22,

1988,

applies

to all

controlled

documents

except

drawings.

f16-PTN-2, is for dr'awing control but has not been

issued

to date.

QI6-PTN-1,

paragraph

5.3.5,

states if the

document

cover letter is

not received

by document control within 30 days,

and if the followup

letter is not received

by document control within 10 days,

document

control

shall

retrieve

the holder's

document

and

remove it from

distribution list if not updated

immediately.

This action

has

not

been

implemented.

QI6-PTN-1,

paragraph

5.4,

states

document control shall

prepare

a

quarterly status

report of controlled documents

specifying the latest

revision

to

be

sent

to

each

holder.

Holders shall verify the

currentness

of their documents

and request

updates.

This action

has

not been

implemented.

'I6-PTN-. 1, paragraph

5.7, states

that document control shall perform

an annual

review of all controlled

documents

(that have their master

maintained

in document control) and problem areas

shall

be corrected,

documented,

and reported to the holders

manager.

This action

has not

been

implemented.

The Quali'ty Assurance

(QA)

group

has

an audit in progress,

Audit

QAO-PTN-89-988, that covers

the

areas

of document control in which

discrepancies

were noted

by the inspectors.

The resolution of Document

Control

discrepancies

will

be

followed

as

Unresolved

Item

50-250,251/89-24-03,

pending completion of the

QA audit.

No violations or deviations

were identified in the areas

inspected.

9.

Plant Startup from Refueling

(71711)

(61709) '(61710)

The

inspectors

witnessed/reviewed

selected, activities

related

to the

Unit 4 Startup

From Refueling Cycle XII.

These

reviews

were

performed

to verify that

the

licensee

properly restored

systems

effected

during

the

outage

and

to ascertain

whether

plant startup

and

core

physics

tests

were conducted

in accordance

with approved plant procedures.

a ~

The

inspectors

performed

a walkthrough of the

Emergency

Diesel

- Generators

(EDG)

and

the

Safety

Injection

System

(SIS).

The

following completed

procedures

were

reviewed to verify that these

systems

were restored

properly:

O-OSP-023.1

Diesel

Generator

Flowpath Verification.

4-OP-062

Safety Injection.

The

inspectors

did not identify any discrepancies

in .the

areas

reviewed.

b.

The inspectors

witnessed

the licensee's

approach

to initial criti-

cality on

May 19,

1989.

Operating

Procedure

(OP) 0204.3, Initial

Criticality After Refueling,

dated

March 24,

1989,

contained

the

instructions

for achieving initial criticality, establishing

the

upper limit of the neutron flux level for zero

power testing

and to

verify proper operation of the reactivity computer.

10

Based

on this determination,

in order to ensure

the reactor

was operated

below nuclear

heating,

the test

range

was established

in the next lower

decade. 'he

reactivity computer

was

then

checked

and calibrated

in

accordance

with Appendix

B of the procedure

and the acceptance

criteria

was successfully

met for the positive and negative

period checks.

Test

personnel

performed

a statistical

check

of the

source

range

instruments

in accordance

with Appendix

D of OP 0204.3.

The licensee

used

the Chi-Squared

method with an acceptance

criteria of between

16 and 45.7.

The results for Source

Range

Nuclear Instruments

(SRNIs)

31 and

32 were

35.68

and 39.735 respectively.

The testing

was

commenced

by withdrawing the control

rods until Control

Bank

(CB)

D was at

160 steps.

The

RCS

was then diluted at

100

gpm until

the reactor

was approximately

2X shutdown.

Thereafter,

the dilution rate

was

decreased

to 50

gpm.

The Inverse

Count Rate Ratio

( ICRR) was plotted

versus

the primary 'water added until the

ICRR was approximately 0. 10.

The

dilution was terminated at this time.

Criticality was not achieved

during

the subsequent

mixing, therefore,

the operators

withdrew control

bank

D in

15 step

increments.

The r'eactor

went critical at 3:50 p.m.

on

May 19,

1989 with

D bank at

190 steps

and boron concentration at 1520

ppm.

Test personnel

next established

the upper limit of neutron flux level for

all

zero

power physics testing.

Appendix

A of the procedure

provided

instructions for the determination

of the nuclear

heating

range.

The

results

were as follows:

Reactivity Computer

Intermediate

Range

Channel

N-35

Intermediate

Range

Channel

N-36

3.4lx10-7

amps

4.54x10-7

amps

4.77xl0-7

amps

C.

Operating

procedure

0204.5,

Nuclear Design Check Tests

During Startup

Sequence

After Refueling,

dated

March 24,

1989, specified

the Refuel-

ing

Outage

Test

Sequence

from initial criticality to full power

operation.

The inspectors

witnessed/reviewed

the

low power tests

which were completed prior to the end of this inspection period.

The

remaining tests will be reviewed during .escalation

of power.

The

tests

reviewed included:

Determination of All Rods Out

(ARO) Critical Boron Concentration.

Determination of the Isothermal

Temperature Coefficient.

Determination of Control

Rod Group Worths.

Determi nati on of Differenti al

Boron Worth.

(a)

The

boron endpoint

on

Bank

D was performed in accordance

with

Appendix

A of

the

procedure.

The

ARO critical

boron

concentration

was

measured

at

1538

ppm,

which

was

34

ppm

different

from the

design

value.

This

met

the

acceptance

criteria of +50

ppm difference.

(b)

The

Isothermal

Moderator

Temperature

Coefficient

(ITC)

was

determined

in accordance

with Appendix

B of the procedure.

The

measured

ITC was -.880

pcm/degrees

F which met the acceptance

criteria of +2 pcm/degrees

F of the

design

value -1.7

pcm/

degrees

F.

The Moderator

Temperature

Coefficient

(MTC)

was

determined

to

be +.92

pcm/degrees

F which met the

acceptance

criteria of +5 pcm/degres

F.

(c)

The rod worths

were determined

in accordance

with Appendix

D,

Rod Worth Verification by

Rod

Swap Method.

The design report

determined

Control

Bank

(CB)

C

had

the

greatest

worth,

'herefore,

this bank was the reference

bank.

The integral worth

of

CB

C

was

measured

as

1329

pcm which met the

acceptance

criteria of +10 percent difference from the predicted

integral

worth.

The integral worths of each

bank were measured

and the

acceptance

criteria of +15 percent difference from the. predicted

integral worth was met.

The

sum of all the control rod worths

was

measured

as

5861

pcm/degrees

F, which met the acceptance

criteria of +10 percent of the predicted value.

(d)

The Hot 2ero

Power

(H2P) Differential Boron Worth was calculated

using

Control

Bank

C

as

recommended

by

Step

8.7 of the

procedure.

The differential

boron worth was

measured

at 9.6

pcm/ppm which was the

same

as the predicted value.

No violations or deviations

were identified in the areas

inspected.

10.

Plant Events

(93702)

The following plant events

were reviewed to determine facility status

and

the

need for further followup action.

Plant

parameters

were evaluated

during transient

response.

The significance of the event

was evaluated

along with the 'performance

of the appropriate

safety

systems

and

the

actions

taken

by the licensee.

The inspectors

verified that required

notifications were

made to the

NRC.

Evaluations

were performed relative

to the

need for additional

NRC response

to the event.

Additionally, the

following issues

were

examined,

as

appropriate:

details

regarding

the

cause of the event;

event chronology; safety

system performance;

licensee

compliance

with approved

procedures;

radiological

consequences, if any;

and proposed corrective actions.

12

On May 3,

1989, at 1:45 p.m., with Unit 3 in Mode

5 and Unit 4 in Mode 3,

a

loss

of the

Emergency Notification System

(ENS)

communications

was

identified.

The licensee notified the

NRC in accordance

with 10 CFR 50.72

(b)( 1)(v).

The local

phone

company

was contacted

concerning

the failure

and the required

communications

were re-established

at 2:45 p.m.

On May 4, 1989, at 4:50 p.m., with Unit 4 in Mode 3,

PORV PCV-4-456 opened

momentarily then reclosed

causing

a

45 psig reduction

in

RCS pressure.

RCS pressure

was at 2235 psig which was well below the

PORV setpoint of

2335 psig.

The

RCO closed

the

PORV block valve

(MOV-4-535) and

removed

power to it as

directed

by ONOP-1208.1.

Subsequent

troubleshooting

determined

the

spurious

valve actuation

was

caused

by

a failure. of

PC-4-445A,

a setpoint

comparator

in the

PORV's control loop.

The faulty

comparator

was

replaced

and

the valve

was

returned

to service.

The

licensee

is currently conducting

root cause

analysis

to determine

the

cause of the failure..

On

May 5,

1989,

at

1:52 a.m., with Unit 4 in Mode 3,

and with control

banks

C

8

D withdrawn,

a Reactor Protection

System

(RPS) trip occurred.

While performing 4-SMI-071.4,

Steam

Generator

Protection

Set III Analog

Channel

Test,

the

Reactor

Trip .Breakers

(RTBs)

open'ed

when bistable

BS-4-446-1

was placed in the Test position in accordance

with step 6.2.3.1

of the

procedure.

This

simulated

a reactor

power greater

than

10K

enabling the

P7 trips.

The

RTBs opened

due to the presence

of the Turbine

Stop Valves Closed signal

which was introduced

due to leads

being lifted

to the

Stop

Valve limit switches.

All systems

functioned

as

designed.

The

sequence

of events

was repeated

and the

same results- were obtained.

The procedure

was

stopped,

notification was

completed

per

10 CFR 50.72

(b)(2)(ii),,and

an

Event

Response

Team

(ERT)

was

convened

to review the

incident.

Although the turbine

stop

valves

were

open

as required

by

procedure

4-SMI-071.4,

the lifted leads

(4T10

and 4Tll) prevented

the

"Turbine Stop

Valve Closed" contacts

in the

RPS= circuitry from closing.

This in turn gave

th'e

RPS

a false signal indicating that the turbine stop

valves

were closed.

When bistable

BS-4-446-1

was placed in the tripped

position,

indicating

power

greater

than

10K, with the

stop

valves

indicating closed,

a reactor trip occurred.

The

ERT formed

a task

team to

determine.

the

root

cause

for the li.fted leads

not

being

relanded.

However,

the

team could find no documentation

or information identifying

that the leads

were lifted. 'S 6.8. 1 requires that written procedures

and

administrative policies shall

be established,

implemented

and maintained

that meet or exceed

the requirements

and'econmendations.

of Appendix A of

USNRC Regulatory

Guide 1.33

and Sections

5.1

and 5.3 'of 'ANSI N18.7-'1972.

O-GME-102.1, Troubleshooting

and Repair Guidelines,

step 3. 1 requires that

a

PWO shall

be

issue'd prior to commencing

work and step 6.2.7 requires

that all lifted leads

be

documented

and

independently verified.

Steps

6.2.9

and 6.3 .8 require all lifted leads

be reconnected

and independently

verified.

O-ADM-715, Maintenance

Procedure

Usage,

steps- 5.5.2

and 5.5.3,

provide instructions for independent. verification of lifting and relanding

13

leads.

Contrary to the

above,

leads

to the turbine stop valve limit

switches

were lifted without adequate

controls which resulted

in a reactor

trip during surveillance'esting.

This is identified

as

the

second

example of Violation 50-25,251/89-24-01.

On May 8,

1989, at 6:00 p.m., with Unit 4 in Mode 3, the unit was placed

in Technical Specification 3.0. 1 due to both the "B" and

"C" loop

T AVG

Resistance

Temperature

Detectors

(RTDs)

being

out of service.

The

elements

(TE-422

and

TE-432)

were

placed

out of service

when the

IKC

department

discovered

that

the

wrong calibration

data

was

used

to

calibrate

the

RTDs.

The Plant Supervisor-Nuclear

placed

the unit in TS 3.0. 1

as required

by Table 3.5-2,

item 1.5, which requires

the High Steam

Flow in two-out-of-three

steam lines with Low T

AVG or Low Steam

Line

Pressure

channels

be functional.

The bistables for TE-422 and TE-432 were

tripped in accordance

with ONOP-208. 14

and

the

NRC

was notified of the

event

as required

by 10 CFR 50.72(b)(l)(i)(A).

The licensee's

investiga-

tion into the

event

determined

that

PC/M 88-234,

performed

during the

current Unit 4 outage,

required that the

RCS temperature

RTDs

be replaced.

When the

new

RTDs were received

on site,

the

new response

curves for the

RTDs to be installed in Unit 4 were obtained

and included into procedures

to assure

the data

was readily available

when required for testing after

installation.

During pre-installation

testing

of the

RTDs it was

determined'hat

three of them did not meet the acceptance

criteria and

NCR

89-0250

was initiated to document

the deficiency.

The

NCR was disposi-

tioned

by allowing the

use of three

RTDs that were to be used in Unit 3.

.However,

the calibration

curves for the Unit 3

RTDs that were

used

in

place of the defective Unit 4 RTDs were not included into the calibration

procedures.

Therefore,

when

the

RTDs

were calibrated,

they

were

calibrated

to the

wrong curves.

The licensee

took prompt corrective

action

when

the discrepancy

was identified

and corrected

the affected

procedures.

Westinghouse

verified that the

new curves

contained

in the

updated

procedures

were for the. specific

RTDs installed

and the circuitry

was

recalibrated

to the

new curves.

Westinghouse

has

reviewed

the

assumptions

contained

in the Safety Analysis against-the

calibration data

of the installed

RTDs.

This review concluded

that the installation

correction

values for the

RTDs were within the assumptions

contai.ned

in

the Safety Analysis.

Therefore,

the "8" and

"C" loop

RPS

T AVG indication

was

not Out-of-Service

due to being Out-of-Calibration.

Based

on this

information it was

concluded

no Technical

Specification

(TS) violation

existed

and

TS 3.0.1

need

not to

have

been

entered.

The evolution

described

above constitutes

a violation of TS 6.8.1 in that

procedures

were not adequately

implemented

or maintained to ensure

that the correct

RTD calibration

curves

were

included

in the appropriate

procedures.

It was determined this violation meets

the criteria of 10 CFR 2, Appendix

C, therefore,

no notice of violation will be issued,

This item is identi-

fied as non-cited violation (NCV) 250,251/89-24-06.

14

On

May 9,

1989, with Unit 4 in Mode 3, the unit experienced

a feedwater

isolation which was reported to the

NRC under

10 CFR 50.72(b)(2)(ii).

The

unit was in the process

of cooling

down from Mode

3 to Mode 4 with one

level

channel

(LT-4-475) for the

"A" steam generator

out of service, with

its bistables

tripped,

due to

a level deviation of greater

than

10'K.

During the

cooldown

an additional

channel

for the

"A" steam

generator

(LT-4-474) failed high which made

up the necessary

two out of three .logic

to

cause

a

feedwater

isolation signal for steam

generator

"A".

All

systems

functioned

as required.

Subsequent

troubleshooting of the level

transmitters

indicated the sensing

lines contained

some sludge which was

flushed

from

the

lines

and

the

transmitters

were

successfully

recalibrated.

The licensee

considers

the

sludge

was

caused

by 'sludge-

lancing of the

steam

generators

during the outage

and not performing

a

flush of lines

coming

from the

steam

generator.

The licensee

stated

future sludge-lancing

evolutions

would require

an adequate

flush of the

lines.

On May 11,

1989,

the licensee

conducted

a cooldown of Unit 4 from Mode 3

to

Mode 4, to facilitate repair of FCV-4-489

8 and

C,

steam

generator

feedwater

bypass

valves.

During operation

in Mode

3 the operators

noted

that seat

leakage

past the valves

was excessive

and they felt it would be

impossible

to control temperature

within the narrow band required during

the

upcoming

post refueling

low power physics testing.

Therefore,

the

licensee

cooled

down the unit to less

than

350 degrees

F and replaced

the

valves.

The valves

were

replaced

due to

damaged

internal

valve

body

threads

which retain

the internal throttling cage

assembly.

These

same

internal

threads

were previously repaired

by weld buildup and remachining

in accordance

with NCR 86-083 in March of 1986.

On

May 14,

1989,

the

licensee

experienced

another

loss of Emergency

Notification System

(ENS)

communications.

The event

occurred

at

1:32

a.m.,

when

a

4A Primary Water

Pump Motor fault occurred which tripped the

"D" MCC Breaker

Number 0832,

removing incoming power from the

MCC.

This

in turn caused

a loss of power to lighting panel

Number 33A de-energizing

Breaker

Number 9, which removed

power

from the

ENS phone.

The licensee

reported

the event in accordan'ce

with 10 CFR 50.72(b)(l)(v) upon discovery

of the loss of ENS.

On

May 23,

1989,

during the

performance

of TP-522,

Unit 4 Alternate

Shutdown

Panel

Performance

Check,

MOV-4-751

(RHR suction isolation valve)

failed to

open.

The

licensee

made

a significant event report in

accordance

with 10 CFR 50.72(b)(2)(ii'i)(B).

After the valve failed to

open

due to the

breaker tripping

on thermal

overload,

two additional

attempts

were

made with identical

results.

The licensee

then

shut

MOV-4-750 (the

upstream

isolation

valve to

MOV-4-751) to

reduce

the

differential pressure

across

MOV-4-751.

A final attempt

was

made to open

the valve and it again tripped on thermal overload.

Maintenance

personnel

then partially opened

the valve manually,

which was very hard to operate

until the valve disc partially cleared

the seats,

indicating the valve was

15

binding during the inital porti'on of travel.

The valve

was then

MOVATS

tested

successfully

and

cycled

several

times with

no

problems

being

identified.

The inital indication is that

the valve

may

have

been

"pressure

bound",

a

phenomenon

by which pressure

is induced

between

the

discs of the valve.

This, in turn,

causes

the discs

to exert greater

pressure

against

the seats.

This causes

the valve to bind until the discs

partially clear

the

seat

area

during opening.

This would allow the

internal

pressure

between

the discs

to be relieved thus eliminating the

"pressure

binding".

The licensee

is currently performing tests

on the

valve

and discussing

the event with the

vendor

and other utilities to

determine

the root cause

of the failure and possible corrective actions to

be taken.

The resolution to correct the failure of MOV-4-751 will be

tracked

as Inspector

Followup Item 50-250,251/89-24-05.

Management

Meeting (94702)

On May 10,

1989,

the bi-monthly NRC/FPL Management

Meeting

was conducted

at the site.

This meeting

was

the eleventh

in

a series

of management

meetings

following issuance

of Confirmatory Order 87-85 in October

1987.

The meeting

was attended

by

NRC Regional

and Headquarters

Management

and

FPL Site

and

Corporate

Management.

The topics of discussion

included

overall plant status,

recent operational

events,

engineering,

maintenance,

and security initiatives.

Exit Interview (30703)

The

inspection

scope

and

findings

were

summarized

during

management'nterviews

held throughout the reporting period with the Plant

Manager

Nuclear

and selected

members of his staff.

An exit meeting

was conducted

on

May 26,

1989.

The areas

requiring management

attention

were reviewed.

No proprietary

information

was

provided to the inspectors

during the

reporting period.

The inspectors

had the following findings:

50-250,251/89-24-01,

Violation.

Failure to meet the requirements

of TS 6.8.1,

two

examples:

Failure

to follow procedure

resulting

in

an

inadvertent

drop of Rod M-8; and failure to follow procedure resulting in

a reactor trip during surveillance testing.

(paragraph

5 and 10).

50-250,251/89-24-02,

Inspector

Followup

Item.

Followup

on

concerns

identified with the storage

and control of hydrogen

on site

(paragraph 8).

50-250,251/89-24-03,

Unresolved

Item.

Resolution of document

control

discrepancies.

(paragraph 8).

50-250,251/89-24-04,

Unresolved

Item.

Determine

the cause

of inadequate

clearance

control.

(paragraph

5).

50-250,251/89-24-05,

Inspector .Followup Item.

Followup on the resolution

to correct the failure of MOV-4-751,

(paragraph

10).

16

5O-250,251/89-24-06,

non-cited

violation with

no written notice

of

violation regarding

the

use

of the

wrong

RTD calibration

curves.

{paragraph 10).

Acronyms and Abbreviations

ADM

ANSI

AP

ARO

ASME

CB

CCW

CCTV

CFR

CS

DP

ENS

ERT

FPL

FSAR

HHSI

ICRR

ICW

!EB

IFI

ITC

LCO

LER

LIV

LOCA

MP

MTC

NCR

NPSH

NRC

ONOP

OOS

OP

OTSC

PA

PC/M

pcm

ppm

PNSC

PSN

PSP

gA

Administrative

American National Standards Institute

Administrative Procedures

all rods out

American Society of Mechanical

Engineers

Control

Bank

Component Cooling Water

Closed Circuit Television

Code of Federal

Regulations

Containment

Spray

Differential Pressure

Emergency Notification System

Event Response

Team

Florida Power

5 Light

Final Safety Analysis Report

High Head Safety Injection

Inverse

Count Rate Ratio

Intake Cooling Water

Inspection

and Enforcement Bulletin

Inspector

Followup Item

Isothermal

Temperature

Coefficient

Limiting Condition for Operation

Licensee

Event Report

L'icensee Identified Violation

Loss of Coolant Accident

Maintenance

Procedures

Moderator Temperature Coefficient

Non-conformance

Report

Net Positive Suction

Head

Nuclear Regulatory

Commission

Off Normal Operating

Procedure

Out of. Service

Operating

Procedure

On the Spot

Change

Protected

Area

Plant Change/Modification

Percent Millirho

Parts

Per Million

Plant Nuclear Safety Committee

Plant Supervisor

Nuclear

Physical Security Procedures

guality Assurance

17

QC:

RCO

RCP

RCS

RHR

RPS

RTD

RTB

SRNI

SRO

T AVG

TS

TSA

URI

Quality Control

Reactor Control Operator

Reactor

Coolant'Pump

Reactor Coolant System

Residual

Heat

Removal

Reactor Protection

System

Resistance

Temperature

Detectors

Reactor Trip Breaker

Source

Range Nuclear Instrument

Senior Reactor Operator

Average Reactor. Coolant Temperature

Technical Specification

Temporary System Alteration

Unresolved

Item