ML17346B204

From kanterella
Jump to navigation Jump to search
Insp Repts 50-250/86-25 & 50-251/86-25 on 860414-0512. Violation Noted:Failure to Meet Requirements of Tech Spec 6.8.1 Re Maint & 10CFR50,App B,Criterion VI Concerning Accuracy of Drawings
ML17346B204
Person / Time
Site: Turkey Point  
Issue date: 06/17/1986
From: Brewer D, Elrod S, Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17346B203 List:
References
50-250-86-25, 50-251-86-25, GL-83-28, NUDOCS 8607070358
Download: ML17346B204 (32)


See also: IR 05000250/1986025

Text

~p,S Rfgg,

Mp0

Cy

nO

ip

~0

<<k*<<>>

UNITED STATES

NUCLEAR REGULATORY

COMMISSION'EGION

II

101 MAR I ETTA ST R E ET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.: 50-250/86-25

and 50-251/86-25

Licensee:

Florida Power

and Light Company

9250 West Flagler Street

Miami, Florida 33102

Docket Nos.:

50-250

and 50-251

Facility Name:

Turkey Point

3 and

4

Inspection

Conducted:

April 14

May 12,

1986

License Nos.:

DPR-31

and

DPR-41

Inspectors:

T.

.

eebles,

Senior

Resi

nt Inspector

Date Signed

D.

R.

Brew r,

esident

Inspector

Approved by: t phen A. Elrod, Section Chief

Division of Reactor Projects

Date Signed

Date

S gned

SUMMARY

Scope:

This routine,

unannounced

inspection

was

conducted

in the

areas

of

licensee

action

on previous inspection findings, annual

and monthly surveillance

observations,

maintenance

observations

and reviews,

operational

safety verifi-

cation,

engineered

safety features

walkdown,

independent

inspection,

and plant

events.

Results:

Violations

Failure to meet

the requirements

of Technical Specifica-

tion (TS) 6.8. 1., three

instances

with multiple examples,

(paragraphs

6,

7 and

8);

and failure to meet the requirements

of 10 CFR 50, Appendix B, Criterion VI,

(paragraph

8).

8607070358

860620

PDR

ADOCK 05000250

PDR

lf

g t

F

II II

li

Jl

REPORT DETAILS

Licensee

Employees

Contacted

"C.

M. Wethy, Vice President - Turkey Point

"C. J. Baker, Plant Manager-Nuclear

Turkey Point

  • F. H. Southworth, Administration Department

E. Preast,

Site Engineering

Manager

D.

W. Hasse,

Safety Engineering

Group Chairman

D.

D. Grandage,

Operations

Superintendent-Nuclear

T. A. Finn, Operations

Supervisor

"V. A. Kaminskas,

Acting Operations

Supervisor

J. Crockford, Assistant Operations

Supervisor

J.

Webb, Operations/

Maintenance

Coordinator

D. A. Chancy,

Corporate

Licensing

J. Arias, Regulation

and Compliance Supervisor

"R. Hart, Regulation

and Compliance

Engineer

~J.

W. Kappes,

Maintenance

Superintendent-Nuclear

J.,C.

Strong, Electrical Maintenance Supervisor,

R. A. Longtemps,

Mechanical

Maintenance

Supervisor

E.

F. Hayes,

Instrument

and Control (IC) Maintenance

R.

G. Mende,

Reactor Engineering

Supervisor

R.

E. Garrett,

Plant Security Supervisor

P.

W. Hughes,

Health Physics Supervisor

W.

C. Miller, Training Supervisor

J.

M. Donis, Site Engineering Supervisor

J.

M. Mowbray, Site Mechanical

Engineer

R.

H. Reinhardt,

Quality Control

(QC) Inspector

"L. W. Bladow, Quality Assurance

(QA) Superintendent

"J. A. Labarraque,

Technical

Department

Supervisor

"M. J. Crisler,

QC Supervisor

R. J. Earl,

QC Inspector

Supervisor

Other

licensee

employees

contacted

included

construction

craftsmen,

engineers,

technicians,

operators,

mechanics,

electricians

and

security

force members.

"Attended exit interview.

Exit Interview

The

inspection

scope

and

findings

were

summarized

during

management

interviews

held throughout

the reporting period with the Plant Manager

Nuclear

and selected

members of his staff.

An exit

meeting

was

conducted

on

May 14,

1986.

The

areas

requiring

management

attention

were reviewed.

Four violations were identified:

4,

,4

Failure of operations

personnel

to meet the requirements

of TS 6.8. 1.,

three

examples,

in that:

(1) Operating

Procedure

(OP)

1004.2

was not

properly implemented,

resulting in a Unit 3 reactor trip; (2)

OP 4304. 1

was

not

properly

implemented,

resulting

in

the

inadvertent

inoperability of the

"A" Emergency

Diesel Generator

(EDG); and (3)

OP

4304. 1 was not properly implemented,

resulting in the inadvertent start

of the "B" EDG (paragraph

7)(250, 251/86-25-01).

Failure to establish

an

adequate

procedure

for the operation

of the

EDGs

as

required

by

TS 6.8. 1,

in that

procedure

0-OP-023

did not

correctly address

the. positioning of several

valves (paragraph

8)(250,

251/86-25-02).

Failure

to

implement

10 CFR 50,

Appendix

B, Criterion VI, in that

drawing

5610-T-E-4536

did

not

accurately

reflect

the

as-built

configuration

of

the

EDG

auxiliary

systems

(paragraph

8)(250,

251/86-25-03).

Failure to meet the requirements

of TS 6.8. 1 in the area of maintenance

control, in that Administrative Procedure

(AP) 0190. 19 was not properly

implemented

when

a maintenance

technician

did not thoroughly document

maintenance

actions,

and

maintenance

work

was

performed

under

an

emergency

authorization

when the criteria for such work did not exist

(paragraph

6) (250/86-25-05).

Two unresolved

items were identified:

Determine

the

basis

for allowing maintenance

activities

which

can

affect

the

performance

of safety-related

equipment

to begin without

requiring that the maintenance

be preplanned

or performed in accordance

with written procedures,

documented

instructions or drawings appropriate

to the circumstances

(paragraph

6)(UNR 250, 251/86-25-06).

Determined the relationship of TS 6'.3.,

temporary

changes,

to changes

made

to

Preoperational

Procedure

(POP)

0800. 112

(paragraph

5)

(250/86"25-04).

The licensee

did not identify as proprietary

any of the materials

provided

to or reviewed

by the

inspectors

during this inspection.

The

lice'nsee

acknowledged

the

findings

without dissenting

comments.

The

licensee

indicated that

perhaps

violations

250,

251/86-25-01

and

250,

251/86-25-05

could

be

combined.

This was

subsequently

considered

by the

NRC Region II

management.

While example

2 of 86-25-05

could fit either place,

example

1

would not.

The violations remain separated.

3.

Licensee Action on Previous

Inspection

Findings (92702)

a.

Performance

Enhancement

Program

(PEP)

Summary

The construction of the Administration Building was completed

in April

1986

and

occupancy

began

in

May

1986.

The centralization

of

the

4T

administrative

offices

has

improved

the

coordination

of inter-

departmental

matters

and facilitated

communications.

Construction

of the Training Building is progressing well; work began

on the

second floor in early May.

A meeting is scheduled

for May 29 and

30 between

NRC management

and the

licensee

to discuss,

in detail,

the progress

of the

PEP

program

to

date.

The meeting will take place at the Turkey Point site to allow

NRC management

to tour the nuclear plants.

Consolidation

of the Engineering

Department

under the Site Engineering

Manager

has

facilitated

the

handling

of

engineering

issues.

Coordination

between

the

engineering

staff

and

the

Plant

Manager'

staff

has

improved.

An

improved

procedure

for the resolution

of

technical

issues

has

been

implemented.

The

procedure

is

highly

structured

and

provides

measures

for prioritization,

feedback

and

monitoring not found in previous

programs.

r

Previously Identified Items

(Cl osed)

Violation

250/84-39-01

and

251/84-40-02

-

Thi s violati on

occurred

when

the

licensee

staff

failed

to fully evaluate

the

consequences

of

a fai 1 ed

Auxi 1 iary

Feedwater

(AFW)

differenti al

pressure

(DP)

cell

during

surveillance

testing.

The

licensee

has

conducted

training

on

TS

4. 10.4

which

has

corrected

misconceptions

regarding

AFW pump operability.

The

DP cells

were

removed

from the

AFW system after being evaluated

as

not essential

for proper

system

operation.

Additionally,

the

surveillance

procedures

have

been

- revised to clarify testing

and operability requirements.

The previous

surveillance

procedure,

OP 7304. 1, which was

common to both trains for

both units,

has

been

superseded

by procedures

3/4 OSP-075. 1

and 3/4

OSP-075.2,

which are unit and train specific.

(Closed)

Violation 251/84-40-01

This violation occurred

due

to

a

misinterpretation

of

AFW TS 3.8.

During

an

AFW test

on Unit 3

a

DP

cell failure resulted

in Unit

3 entering

a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> limiting condition

for operation

(LCO).

Licensee

personnel

failed to evaluate

the

DP cell

failure with respect

to Unit 4, which was being started

up.

Due to

a

peculiarity in the wording of TS 3.8,

no

LCO existed for Unit 4,

and

a

shutdown of Unit 4 was not begun

as required.

Since

December

1984 the

licensee

has

continued

to

emphasize,

through training,

the correct

interpretation

of TS 3.8.

In addition,

on

May 7,

1986,

the licensee

submitted

to the

NRC Office of Nuclear

Reactor

Regulation

(NRR),

a

proposed

license

amendment

which clarifies the requirements

for AFW

system operability by adopting

modes of applicability consistent

with

the Standard

Technical Specifications.

Licensee letter

L-86-193, which

transmits

the

amendment

request,

was voluntarily submitted.

(Closed)

Unresolved

Item 250/84-35-04

and 251/84-36-04

This item was

determined

to

be

a violation of

NRC requirements,

in that the

Main

Steam

Isolation

Valves

were

not

tested

in

accordance

with

the

requirements

of

the

Inservice

Inspection

Program.

Violation

250, 251/85-05-01

was issued

on March 6,

1985.

Corrective

action for

the

discrepancy,

which

was

subsequently

the

subject

of

a

10 CFR 21

report (Licensee

Event Report

(LER) 250/85-20),

is in progress

and its

completion will be verified at

a later date.

(Closed)

Inspector

Followup Item (IFI) 250, 251/84-33-01

The licensee

submitted

supplemental

data describing plant capabilities with respect.

to Section

1.2 of Generic Letter (GL) 83-28.

On November 27,

1985, the

NRC completed

a safety evaluation

(TAC Nos.

53643

and

53644)

on the

data

and

information capabilities

of

the

Turkey Point plants

and

determined that the licensee's

response

was acceptable.

GL 83-28,

Item

1.2 is complete for Turkey Point Units

3 and 4.

(Closed)

IFI

250,

251/83-26-06

-

The

licensee

has

developed

and

implemented

drawing

5610-T-E-4536,

sheets

1

and

2

which correctly

identify the status

of all valves in the

EDG air start

system.

Those

valves

whose closure could prevent

EDG starting

are

kept

locked

open.

OP

4303. 1,

EDG

Normal

Standby

Condition,

has

been

superseded

by

procedure

O-OP-023,

which correctly itemizes the required positions of

the

EDG air start

valves

and

reflects

the

locked

status

of the

appropriate air valves.

(Closed)

IFI 250,

251/83-38-05 - This item documented

a concern that

the

Spent

Fuel

Pool

(SFP)

temperature

was

excessively

high during

refueling.

Inspection

Report

250,

251/85-23

subsequently

documented

that

the

SFP

was

being

operated

in

a

manner

contrary

to

the

requirements

of the Final Safety Analysis Report

(FSAR), in that the

lower cooling

pump

suction

was

being

used

instead

of the

higher

suction.

It was determined

that the total cooling flow through

the

lower suction

was significantly lower than that which could be obtained

through

the

upper suction.

The

reduced

flow resulted

in higher

SFP

temperatures,

especially

when

the entire

core

was off-loaded during

refueling.

As a result of Violation 250, 251/85-23-01,

the licensee

no

longer

uses

the

lower

cooling

suction

line.

Consequently,

SFP

temperature

has

remained

less

than

120 degrees

Fahrenheit.

Corrective

actions for the violation have

been

implemented

and will be reviewed at

a later date.

(Closed)

LER 251/85-08

This

LER documented

the licensee's

discovery

that Unit 4 containment

isolation valve

CV-4-956A, pressurizer

steam

space

vent line isolation,

was susceptible

to leakage

above the limits

established

in the inservice test program.

The potential

leakage

path

was identified during post-maintenance

testing after repairs

were

made

to the valve.

To preclude

the possibility of inadvertent

leakage via

CV-4-956A, the licensee

shut CV-4-951, which is located just inside the

containment

building

in

series

with

CV-4-956A.

CV-4-951

was

deenergized

to preclude

inadvertent

operation

90

minutes

after

the

'0

8g

E

identification of the problem.

No TS requirement or

LCO was exceeded.

Though not required,

the licensee

also shut manual

valve 997A adjacent

to

CV-4-951 'inside

containment.

This

provided

an additional

closed

valve in the flowpath through

the containment

penetration.

CV-4-956A

was

repaired

within

2

1/2 hours.

No radiological

release

occurred.

CV-4-951

remained

closed until August

1984

because

a failed position

indicator precluded reliable remote monitoring of valve position.

The

delay

in the

maintenance

repair

was justified since

the

valve is

normally closed,

infrequently operated

and located in a relatively high

radiation area while the reactor is at

power.

The valve

was repaired

during the first shutdown of opportunity.

4.

Unresolved

Items

An unresolved

item is

a matter

about which more information is required to

determine whether it is acceptable

or may involve

a violation or deviation.

Two unresolved

items identified during this

inspection

are

discussed

in

paragraphs

5 and 6.

5.

Monthly and Annual Surveillance

Observation

(61726/61700)

The inspectors

observed

TS required surveillance testing

and verified: that

the test procedure

conformed to the requirements

of the TS, that testing

was

performed in accordance

with adequate

procedures,

that test

instrumentation

was calibrated,

that limiting conditions for operation

(LCO) were met, that

test

results

met

acceptance

criteria

requirements

and

were

reviewed

by

personnel

other than the individual directing the test,

that deficiencies

were identified,

as appropriate,

and were properly reviewed

and resolved

by

management

personnel

and

that

system

restoration

was

adequate.

For

completed tests,

the .inspector verified that testing

frequencies

were

met

and tests

were performed

by qualified individuals.

The inspectors

witnessed/reviewed

portions of the following test activities:

Emergency Diesel Generator

Periodic Test

Load on 4

KV Bus

Unit 3 Auxiliary Feedwater

Flow Control Valve Stability Test

Power

Range Nuclear Instrumentation Shift and Daily Calibrations

Rod Position Indication System Monthly Test

Preoperational

Procedure

(POP)

0800. 112,

Unit 83

AFW Flow Control

Valve

Stability Test,

dated

March

21,

1986,

was

reviewed

in detail

following

implementation.

The testing

was performed to verify that flow oscillations

in the

AFW system during automatic

operation

had

been

corrected

subsequent

to

the

implementation

of Plant

Change/Modification

(PCM)85-130.

The

procedure

was

performed

by

the

Startup

Department

on

April 9,

1986,

following a reactor startup

from a month-long Unit 3 maintenance.

outage.

The

inspector

noted that

several

procedural

steps

had not

been

properly

implemented

during

the

performance

of the

test.

Step

9.4. 14 of

the

procedure

required that the time between

the start of the "A" AFW pump and

the delivery of 375 gallons per minute (gpm) flow to the

steam generators

be

'iI

verified to

be

less

than

3 minutes

with the

system

operating

in the

automatic

mode.

However, flow oscillations through flow control valve (FCV)

3-CV-2816 precluded

obtaining

an accurate

flow reading.

Consequently,

the

verification was

not performed.

Similarly, step

9.4.25 of the procedure,

which directed that the time required to obtain

561

gpm flow to the

steam

generators

be recorded,

was not done.

Steps

9.5. 14

and 9.5.25

were also

not implemented

on train

2 because

AFW

system

flow indicator

FI-3-1401B exhibited

sticky

and erratic

operation

during part of the test.

Consequently,

accurate

flow readings

were

not

possible.

Members of the Startup

Department

documented

those

areas

where they deviated

from the

requirements

of

the

procedure.

The

Engineering

Department

evaluated

the test results

and concluded that the two steps relative to the

testing

of

each

train

were

unacceptable.

However,

the

Engineering

Department

recommended

that

the

AFW system

be

accepted

"as is" for the

following reasons:

Valve CV-3-2816

was the only one of six identical

valves

to exhibit

excessive

oscillation

subsequent

to the design

change.

Therefore,

the

problem did not appear to be inherent in the trim design,

but rather in

the control

loop.

Engineering

concluded

that the valve control

loop

could be repaired

and retested

in accordance 'with

POP

0800. 112 at the

next possible opportunity.

Even

though

FI-3-1401B exhibited erratic operation

during the test,

personnel

monitoring CY-3-2831 reported that it was operating without

oscillation

and

was

open to a position that agreed with the other two

train

2 FCVs.

Engineering

considered

the visual verification of valve

stability to

be

acceptable.

FI-3-1401B

was

replaced

but applicable

portions

of

POP

0800. 112

were

not

repeated

due

to the

Engineering

comments.

The Plant Nuclear Safety Committee

(PNSC) specifically approved

POP 0800. 112

on March 21,

1986.

Section

3.2 of the procedure

specifies

the

acceptance

criteria,

stating that (1) flow control

valves

must stroke

smoothly;

(2)

within three minutes after

pump start,

the

system

must achieve

setpoint flow

to each

steam generator;

and (3) the flow controller

must maintain flow per

the flow criteria outlined in the procedure.

TS 6.8.3 requires that temporary

changes

to procedures

only be

made provided

that:

a.

The intent of the original procedure is not altered;

b.

The change is approved

by two members of the plant management

staff, at

least

one

of

whom holds

a

Senior

Operator's

license

on

the

Unit

affected;

and

e

c.

The

change

is

documented,

reviewed

by the

PNSC

and

approved

by the

Plant Manager-Nuclear within 14 days of implementation.

On April 9,

1986,

temporary

changes

were

made to Preoperational

Procedure

(POP)

0800. 112,

Unit

3

AFW

Flow Control

Valve Stability

Test,

dated

March 21,

1986,

in that several

procedural

steps

were

not performed.

The

omi ssions

included not recording the time required to achieve

required flow

rates

and

not

observing

required i flows

on

installed

flowmeters.

The

omissions

appear

to constitute

changes

to the intent of the

procedure

in

that the acceptance

criteria for control valve stability were modified to be

less restrictive

than was,.acceptable

by the

PNSC

approved

procedure.

The,

intentional

omi ssions

were

not

approved

by

two

members

of

the

plant

management staff or approved

by the Plant Manager-Nuclear within 14 days.

The relationship of TS 6.8 '

to preoperational

test procedures

is unresolved

item 250/86-25-04

pending further

NRC evaluation.

Maintenance

Observations

(62703/62700)

Station maintenance activities

on safety-related

systems

and components

were

observed

and

reviewed to ascertain

that they were conducted

in accordance

with approved

procedures,

regulatory guides,

industry

codes

and

standards

and in conformance with TS.

The following items

were

considered

during this

review,

as appropriate:

that

LCOs were

met while components

or systems

were

removed

from service;

that approvals

were obtained prior to initiating work; that activities were

accomplished

using

approved

procedures

and

were

inspected

as

applicable;

that

procedures

used

were

adequate

to

control

the

activity;

that

troubleshooting

activities

were controlled

and

repair

records

accurately

reflected

the

maintenance

performed;

that

functional

testing

and/or

calibrations

were

performed prior to returning

components

or

systems

to

service;

that

gC records

were maintained; that activities were accomplished

by qualified

personnel;

that

parts

and

materials

used

were

properly

certified; that radiological

controls

were properly implemented;

that

gC

hold

points

were

established

and

observed

where

required;

that fire

prevention

controls

were

implemented;

that

outside

contractor

force

activities were controlled in accordance

with the

approved

gA program;

and

that housekeeping

was actively pursued.

The following maintenance activities were observed

and/or

reviewed:

Replacement

of AFW Flow Indicator FI-3-1401B

(PWO 6230)

Rod Control

System Repair For Shutdown

Bank "A" (PWO 6379)

CV-3-2816

Loop Calibration

FI-3-1401B Meter Calibration

During review of these

maintenance

activities,

the inspector

noticed that

work on the rod control

system

and

AFW system

began prior to the development

of written work procedures

and without the required pre-review of the work

package

by the

gC Department.

I

Technical Specification (TS) 6.8.1

requires

that written procedures

and

administrative policies

be implemented that meet or exceed

the requirements

and recommendations

of sections

5. 1 and 5.3 of ANSI N18.7-1972

and Appendix

A of USNRC Regulatory

Guide 1.33.

Appendix

A of

USNRC

Regulatory

Guide

1.33

states

that

administrative

procedures

specifying procedure

adherence

should

be established.

AP 0190. 19,

Control of Maintenance

on Safety

Related

and Quality Related

Systems,

dated

January

8,

1986,

states

that the Plant Supervisor-Nuclear

(PSN)

may authorize

work to start prior to obtaining Quality Control

(QC)

approval

of the

Plant

Work Order

(PWO)

when

the plant is in

a

load

threatening

condition or in an Action Statement of TS 3.0. 1.

To immediately

commence

work, the

PSN shall originate

a

PWO and assign

a class

"AA" work

priority

and

sign

the

permission

to

start

work

block.

Maintenance

technicians

are

required

to thoroughly document all actions

taken

on the

PWO,

and the

PWO shall

be

made available

for subsequent

review by the

QC

Department within one day.

On April 9,

1986,

PWO 6230

was

issued

as

a priority class

"AA" work order

for maintenance

on

AFW FI-3-1401B but the maintenance

technician

did not

thoroughly

document

his

maintenance

actions.

He failed to originate

a

calibration record sheet for the flow meter

he installed.

Additionally, he

failed to indicate

on

the

PWO that

he

had

performed

the required

meter

calibration.

The licensee

re-performed

the calibration

in order to obtain

the required

QA record of the maintenance activity, and indication was found

to be within calibration tolerances.

On

May 3,

1986,

the

PSN authorized

work on the rod control

system to start

on priority class

"AA" PWO 6379 when the plant was not in a load threatening

condition or in an Action Statement

of TS 3.0. 1.

Additionally, the

PWO was

not made available for review by the

QC Department within one day.

Shutdown

bank

"A" could not

be withdrawn past

41 steps.

The bank

was

then fully

inserted

and the reactor trip breakers

were

opened.

A dirty contact

was

found in the

rod control circuitry.

The

rod control

system

performed

satisfactorily after cleaning.

These

failures

to adequately

implement

AP 0190. 19 are

a violation of

TS 6.8. 1.

This violation applies to Unit 3 only (250/86-25-05).

The licensee

has

used priority class

"AA" PWOs approximately

77 times since

January

1985.

The licensee is implementing

changes

to AP 0190. 19 to better

define

the

responsibilities

of

those

tasked

with its

implementation.

Additionally, the licensee

has

instructed

the

PSNs to rigorously adhere to

the

implementation

requirements

and avoid the

use of priority maintenance

for activities for which it was not intended.

Since

AP

0190. 19

effectively

authorizes

maintenance

to

begin

on

safety-related

equipment

prior

to

the

development

of

a

maintenance

procedure,

a concern

is raised

regarding

the

adequacy

and quality of the

maintenance.

Additionally, AP 0190. 19

may conflict with applicable

ANSI

y

1,

J'q

Standards

which require that maintenance

activities which can affect the

performance

of safety-related

equipment

be

preplanned

or

performed

in

accordance

with written procedures,

documented

instructions

or

drawings

appropriate

to the circumstances.

This concern constitutes

an Unresolved

Item pending additional

review and analysis

by both the licensee

and the

NRC

staff (UNR 250, 251/86-25-06).

Opera tiona1

Sa fety Verificati on (71707)

The inspectors

observed

control

room operations,

reviewed applicable

logs,

conducted

discussions

with control

room operators,

observed shift turnovers

and confirmed operability of instrumentation.

The inspectors

verified the

operability of selected

emergency

systems,

verified that maintenance

work

orders

had been

submitted

as required

and that followup and prioritization

of work was accomplished.

The inspectors

reviewed tagout records, verified

compliance with TS

LCOs

and verified the

return

to service

of affected

components.

By observation

and direct

interviews,

verification

was

made

that

the

physical security plan was being implemented.

Plant housekeeping/cleanliness

conditions

and implementation of radiological

controls were observed.

Tours of the intake structure

and diesel,

auxiliary, control

and turbine

buildings and Unit 4 containment

were

conducted

to observe

plant equipment

conditions

including potential fire hazards,

fluid leaks

and

excessive

vibrations.

The

inspectors

walked

down

accessible

portions

of

the

following

safety-related

systems

on Unit 3 and,

as applicable,

on Unit 4 to verify

operability and proper valve/switch alignment:

Emergency

Diesel Generators

Auxiliary Feedwater

4160 Volt and

480 Volt Switchgear

Control

Room Vertical Panels

and Safeguards

Racks

Two

examples

of

operations

personnel

failures

to properly

implement

procedures

were identified when they adversely affected plant operations.

A

third example

resulted

in the

inadvertent

start

of the

"B"

EDG.

The

requirements

for procedural

compliance

are specified below.

Technical Specification (TS) 6.8. 1 requires

that written

procedures

and

administrative policies

be implemented that meet or exceed

the

requirements

and recommendations

of sections

5. 1 and 5.3 of ANSI N18.7-1972

and Appendix

A of USNRC Regulatory Guide 1.33.

Appendix

A of

USNRC

Regulatory

Guide

1.33

states

that

administrative

procedures

specifying procedure

adherence

should

be established.

'1 i

4

r,

'lC

I

10

Administrative

Procedur e

O-ADM-201,

Upgrade

Operations

Procedur e

Usage,

dated

December

4,

1985,

requires,

in

section

5.5. 1,

that

operating

procedures

be followed exactly

and that all personnel

comply with approved

procedures

applicable to the activity or circumstance

being performed.

Operating

Procedure

(OP)

1004.2,

Reactor

Protection

System

Periodic Test

(Unit 3 Only), dated

February 7,

1986, requires,

in section 8.61, that the

operator

proceed

to protection

instrument

rack

41 to perform train

"B"

reactor trip breaker testing.

Section 8.63 directs the operator to trip the

"B" reactor trip breaker.

On May 2,

1986,

an operator failed to properly

implement

OP 1004.2,

in that

while performing step 8.61

he remained at protection instrument rack 36 and,

while performing

step

8.63,

tripped the

"A" reactor trip breaker,

thereby

inadvertently tripping the Unit 3 reactor.

OP 4304. 1,

Emergency

Diesel Generator

Periodic Test

Load on

4KV Bus, dated

April 1,

1986, requires,

in section 8.3, that the starting air supply valve

be closed for the

emergency

diesel

generator

(EDG) being tested.

Section

8.7 requires

that the starting air supply valve for the

EDG

be

reopened

after completion of sections

8.3 through 8.6,.

On

May 2,

1986,

an operator failed to properly

implement

OP 4304. 1 on two

consecutive

occasions,

in that during

an initial start

of the

"B"

EDG

section

8.7

was not implemented,

causing

the

EDG to fail to start.

While

realigning

the

"B"

EDG for

a

subsequent

start

attempt,

the

operator

improperly

implemented

section

8.3,

in that

he

closed

the

starting air

supply valve for the "A" EDG rendering the "A" EDG temporarily inoperable.

Additionally, on May 9,

1986,

an operator

again failed to properly implement

OP 4304. 1, in that

he pressed

the local start button during step 8. 11 of the

procedure

instead of pressing

the fuel priming button.

This personnel

error

resulted

in the inadvertent start of the "B" EDG.

The

EDG was immediately

secured

and was subsequently

successfully tested.

These

three

examples

of procedural

noncompliance

together

constitute

a

failure to implement

TS 6.8. 1., which is

a Violation (250, 251/86-25-01).

Engineered

Safety

Features

Walkdown (71710)

The inspector

completed

a verification of the operability of the emergency

power

system

for Units

3

and

4

begun

in

Inspection

Report

Nos.

250,

251/86-17.

Additionally, the operability

of the

"A" and

"B"

EDGs

was

verified by performing

a complete

walkdown of the accessible

portion of the

system.

The

following

specifics

were

reviewed

and/or

observed

as

appropriate:

a.

that the licensee's

system lineup procedures

matched plant drawings

and

the as-built configuration;

11

b.

that the

equipment

conditions

were satisfactory

and

items that might

degrade

performance

were identified and

evaluated

(e.g.

hangers

and

supports

were operable,

housekeeping

was adequate,

etc.);

c.

that instrumentation

was properly valved in and functioning

and that

calibration dates

were not exceeded;

d.

e.

that

valves

were

in proper position,

breaker

alignment

was correct,

power was available,

and valves were locked/lockwired as required;

local

and

remote

position

indication

was

compared

and

remote

instrumentation

was functional;

and

f.

breakers

and

instrumentation

cabinets

were

inspected

to verify that

they were free of damage

and interference.

Both

EDGs

were

determined

to

be

operable.

However,

discrepancies

were

identified in the normal lineup procedure

and the

system

drawing

was

found

to contain inaccuracies.

Technical Specification (TS) 6.8. 1 requires

that written procedures

and

administrative policies

be established

and maintained that

meet or exceed

the

requirements

and

recommendations

of sections

5. 1

and

5.3 of ANSI

N18.7-1972Property "ANSI code" (as page type) with input value "ANSI</br></br>N18.7-1972" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.

and Appendix A of USNRC Regulatory Guide 1.33.

Appendix

A of Regulatory

Guide

1.33

states

that

procedures

should

be

established

for the

startup,

operation

and

shutdown

of safety-related

equipment including instructions relative to emergency

power sources

such

as

diesel

generators.

Procedure

O-OP-023,

Emergency

Diesel

Generator,

dated

March 25,

1986,

provides

instructional

guidance

for the

startup,

normal

operation

and

shutdown of the

EDG system.

As of May 12,

1986,

0-OP-023 did not adequately

establish

procedures

for the

startup

and operation of the "A" and "B" EDGs, in that:

the procedure

did not address

the control of valves

292

and

293 for

either the "A" or "B" EDG radiator cooling water system drains

and did

not address

the drain valves for the "A" or "B" EDG fuel oil skid tank;

the

procedure

addressed

the

position

of skid tank

solenoid

valve

SV-3-3522

bypass

line isolation

valve

70-048A,

which

has

not

been

installed for the "A" EDG; and

the

procedure

did

not

address

the

control

of valve

269B for the

starting air flask drains for the "B" EDG.

The failure to establish

an adequate

procedure

as required

by TS 6.F 1 is a

Violation (250, 251/86-25-02).

3

12

10 CFR 50,

Appendix

B, Criterion VI, as

implemented

by

FPL Topical Quality

assurance

Report

(FPL-NQA-100A) Revision

8,

TQR 6.0,

Document

Control,

requires,

in part; that the distribution of controlled

documents,

such

as

drawings,

which provide guidance,

specifications

or requirements

affecting

the quality of nuclear safety-related

structures,

systems

and

components,

shall

be controlled

and that Quality Procedures

shall delineate

the control

measures

for drawings,

including direction for the review for adequacy.

t

FPL Quality

Assurance

Manual,

Quality

Procedure

(QP) 6.6,

Revision

1,

delineates

requirements

for maintaining

the

drawing

update

program

and

assuring

that

drawings reflect

the

as-constructed

configuration

of the

sa fety-rel ated

system.

Administrative Procedure

(AP) 0103.10,

Using

and Updating Plant

Drawings,

dated

March 3,

1983,

implements

the

above

requirements

and specifies

that

drawings shall

be field verified to ensure

proper accuracy.

As of

May

13,

1986,

drawing

5610-T-E-4536,

Revision

0,

sheets

1

and 2,

entitled "Diesel Generator

A" and "Diesel

Generator

B", respectively,

were

not accurate,

in that:

the drawing sheets failed to show the existence

of a fuel oil skid tank

drain valve for each

EDG;

the drawing sheets

showed that valves

292A and 292B, drains for the

EDG

radiator cooling system,

were normally closed valves

when actually they

were normally open valves;

numerous

valve numbers specified

on the drawing sheets

conflicted with

the valve

numbers utilized by approved

operating

procedure

0-OP-023;

and

drawing

sheet

1

showed

the

presence

of starting air flask drain valve

269A, which does

not exist,

and drawing sheet

2 showed

a starting air

flask drain piping configuration which was not accurate.

The failure to meet the requirements

of 10 CFR 50, Appendix B, Criterion VI

is

a Violation (250, 251/86-25-03).

9.

Independent

Inspection

During the report period,

the inspectors'outinely

attended

meetings with

licensee

management

and monitored shift turnovers

between shift supervisors,

shift

foremen

and

licensed

operators.

These

meetings

included

daily

discussions

of plant operating

and testing activities

as well as discussions

of significant problems or incidents.

As a result,

the inspectors

reviewed

potential

problem areas

to independently

assess

their importance to safety,

the

adequacy

of proposed

solutions,

improvement

and progress,

and adequacy

of corrective actions.

The inspector's

reviews of these

matters

were not

limited to the defined inspection

program.

Independent

inspection effort

was conducted

in the area of EDG loading.

"4

%

~

13

10.

Plant Events

(93702)

An independent

review was conducted of the following events.

a.

April 23,

1986

Intake Cooling Mater (ICW) Temperatures

Above Limits

The

maximum allowable

ICW temperature

to the

Turbine

Plant Cooling

Water

(TPCW)

heat

exchangers

was limited by engineering

evaluation

JPE-PTP0-86-172,

dated

February

13,

1986,

as

a result of the potential

failure of

ICM valve

CY-2201.

Engineering

evaluation

JPE-L-85-38,

Revision

1,

dated

February

16,

1986,

provided instructions

for the

operation of the

ICW system until permanent corrective actions could be

implemented.

The allowable

ICW temperature

varied with the fouling

level of the

ICM heat exchangers

and the

number of heat

exchangers

in

service,

as depicted in graphs

developed

by the Engineering

Department.

On April 23,

1986,

the

average

tube resistance

of the heat exchangers

was

0.00288

which allowed

a

maximum

ICW temperature

of 77.8 degrees

Fahrenheit

(F) for

two

heat

exchanger

operation.

The

"B"

heat

exchanger

was

removed

from operation for cleaning.

ICW temperature

was

verified to be 77.0 degrees

F.

Within three

hours the

ICW temperature

increased

to 77.5 degrees

F and the cleaning of the "B" heat exchanger

was halted

and preparations

were

made to restore its operability.

At

approximately

9:00 a.m.

the temperature limit was exceeded

and the "B"

heat

exchanger

was

not yet operable.

Restoration

of the

"B" heat

exchanger

was unexpectedly

hindered

by the discovery of

a tom cover

gasket

which

required

replacement.

This

caused

the

Maintenance

Department to exceed

the

one hour time frame in which they had

hoped to

return the heat

exchanger

to service.

The increase

in

ICW temperature

above that evaluated

in JPE-L-85-38,

Rev'ision

1,

placed

the

ICM system in an unanalyzed condition, in that

the Component

Cooling Water

(CCW) system,

which is cooled

by the

ICW

system,

was

suspected

to

be incapable of fulfillingits post accident

heat

removal

function.

TS 3.4.4

requires

that

the

CCM system

be

operable

and at 9:00 a.m.

on April 23,

1986,

the licensee

determined

that the

CCM system

was not capable of fulfillingits intended function

should

a large break loss of coolant accident coincident with a fai lure

of an

EDG and

a loss of offsite power occur.

At 10:00 a.m.

the licensee

began

a Unit 3 load reduction in preparation

for a reactor

shutdown

as required

by TS 3.0. 1.

At 10:30 a.m.

the "B"

heat

exchanger

was returned

to service

and the

ICM system

was again

operating

within

the

bounds

of

the

JPE-L-85-38,

Revision

1.

Consequently

the licensee

returned Unit 3 to full power operation.

0

( ~

kl

t

e

II

V

4

f

I

P'

t,

April 22,

1896 - Inoperability of the

Emergency Notification System

(ENS)

On April 22,

1986,

the

ENS telephone

was disconnected. in ~the.control

room to allow an additional

telephone

to

be connected

i'.n> the 'general

office building.

The

control

room

ENS

telephone

was 'returned

to

service

on April 23,

1986.

While the

ENS circuit was ',unavailable,

commercial

telephone

service

was available

and could have

been

used for

emergency notification purposes.

April 25,

1986

Failure of the "A" EDG to Close Onto the

4

KV Bus

At 9:27 a.m.,

during

a periodic test of the

"A" EDG, breaker

4AA20,

which connects

the

"A" EDG to the "4A" 4160 volt bus,

would not close

from the control

room.

The

"4B" 4160 volt bus

had

previously

been

deenergized

for routine

maintenance.

Unit

4

was

operating

in .cold

shutdown with the

"4A" Residual

Heat

Removal

(RHR)

pump operating.

Since the "A" EDG could not be connected

to the "4A" bus,

the "4A" RHR

pump did not have

a backup

power supply in the event offsite power was

lost.

Thus,

due to

a mechanical

failure, the action statement for TS 3.4. l.e. 1 was entered.

Breaker

4AA20 was returned to service following

adjustment of a type

"HH" interlock switch at 11:33 a.m.

Type

"HH" switches,

which are

common to several

4160 volt breakers,

have

caused similar problems

on previous occasions.

Modified switches

are

on order

and will be installed

when received.

Discussions

with the

licensee

regarding the adequacy of the corrective

action

and root cause

identification are still in progress

and will be addressed

and tracked

when the

LER for this event is issued.

May 2,

1986

Unit 3 Reactor Trip

Thi s

reactor trip

was

the

resul t of

per sonnel

error

during

the

performance of OP 100'4.2,

Reactor Protection

System Periodic Test.

The

plant responded

as

designed

during the post-trip transient.

However,

source

range

instrument

N-32 failed to energize

as

reactor

power

decreased

into the source

range.

Poor performance

of the source

range

instruments

has

been

a

frequent

problem.

On

November 30,

1985

and

March 5,

1986,

two previous

reactor trips occurred

during

which

one

source

range

instrument

failed to perform properly.

The failure to

follow procedures

during the implementation of OP 1004.2

was determined

to

be

one

part

of Violation

250,

251/86-25-01

as

discussed

in

paragraph

7.

The Unit 3 reactor

was returned to power

on

May 3,

1986.

May 2,

1986

"A" and "B" EDG Inadvertently

Placed out of Service

The "B" EDG was out of service during the Unit 3 reactor trip on May 2,

1986.

As

required

by

TS 3.0. 1.,

a

plant

cool

down

was

begun.

Preparations

were

made to test the

"B"

EDG to verify its return to

service.

As

a result of a personnel

error, the air start valve was not

opened

as required during the

EDG lineup for operation.

Consequently,

1

15

the

"B"

EDG failed to start

when the start

signal

was initiated,from

the control

room.

Subsequent

to correcting the lineup for the "B"

EDG

air start

system,

the

same operator

inadvertently closed

the air start

isolation valve

on the "A" EDG.

This rendered

the

"A" EDG inoperable

at

a time

when

the

"B"

EDG

had not yet

been verified to

be operable

following its maintenance.

The "A"

EDG air start valve

was quickly

opened after the air isolation resulted

in the loss of the ready start

light.

The

"A"

EDG

was

out of service

for just

a

few minutes.

Subsequent

to

these

personnel

errors,

both

EDGs

were

tested

satisfactorily.

The personnel

errors

were determined

to constitute

a

violation of

TS 6.8. 1,

which requires

that

procedures

be

properly

implemented.

The violation (250, 251/86-25-01) is further discussed

in

paragraph

7.

May 4,

1986

"D" Motor Control Center

(MCC) Automatic Transfer Design

Error

The

licensee

previously identified tha't

the

"D"

MCC could fail to

transfer

to an energized

bus during cer tain failures of equipment,

such

as

loss of the

"3B" battery.

PCM 86-041

was installed

on Unit 3 to

correct

the

problem.

During

a design

review,

the licensee

determined

that

PCM 86-041 created

the possibility that the "D" MCC could transfer

from an operable

bus to

an inoperable

bus.

An engineering

evaluation

was performed which determined that the continued

operation of Unit 3

was justified (JPE-PTP0-86-1000,

dated

May 4,

1986)

as long as the "D"

MCC

was

manually transferred

to

an

operable

bus within

20 minutes

following its

loss

of power.

Changes

were

made

to the

emergency

operating

procedures

to

incorporate

the

requirements

of

JPE-PTPO-86-1000.

The validity of the evaluation

was discussed

with

the

NRC Region II staff.

The

PNSC has since

approved

a modification to

PCM 86-041,

which provides

a timing relay to alleviate

the

problem.

The modification is to be installed in the near future.

May 9,

1986

Inadvertent

Manual Start of the "B" EDG

During preparation

for the

performance

of a periodic test

run of the

"B"

EDG,

a Turbine

Operator

failed to follow OP

4304.1

in that

he

pressed

the

diesel

start

button

instead

of

the

fuel oil

prime

pushbutton

as required

by step

8.11 of the procedure.

This personnel

error resulted

in the local start

of the

"B"

EDG.

The diesel

was

secured

and properly tested.

The failure to follow procedure

OP 4304. 1

was determined

to

be

a violation (250,

251/86-25-01)

and is further

discussed

in paragraph

7.

J

4

Ci

i'l

10(r