ML17342B168

From kanterella
Jump to navigation Jump to search
Forwards Summary of mgt-on-shift Weekly Repts,Per Commission 871019 Order
ML17342B168
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 02/10/1988
From: Woody C
FLORIDA POWER & LIGHT CO.
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
L-88-66, NUDOCS 8802190031
Download: ML17342B168 (47)


Text

3 i

t ACCELEBRATED DESI'RIBUTJON DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

DOCKET 05000250 05000251 NOTES:

ACCESSION NBR:8802190031 DOC.DATE: 88/02/10 NOTARIZED: NO FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C AUTH.NAME AUTHOR AFFILIATION WOODY,C.O.

Florida Power 6 Light Co.

RECIP.NAME RECIPIENT AFFILIATION GRACE,J.N.

Region 2, Ofc of the Director

SUBJECT:

Forwards summary of mgt-on-shift weekly repts,per Commission 871019 order.

DISTRIBUTION CODE:

D036D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: Turkey Point Management Onshift Program RECIPIENT ID CODE/NAME DRP/ADR-2 PD2-2 PD INTERNAL: AEOD NRR DEPY NRR MORISSEAU,D NRR/ADT NRR/DOEA DIR NRR/PMAS/ILRB OGC/HDS2 RGN2 FILE EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1

1 1

1.

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

RECIPIENT ID CODE/NAME NRR/DRP-1/2 EDISON,G DEDRO NRR DIR NRR/ADP NRR/DLPQ/PEB NR~R, DRRS DIR 01~)~BE NIJ EG FIL 01 NRC PDR COPIES LTTR ENCL 1

1 2

2 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 j

A TOTAL NUMBER OF COPIES REQUIRED:

LTTR 23 ENCL 23

P.

OX 14000, JUNO BEACH, FL 33408.0420 yklllg~

30 f'E8 l2 Al0: 3g L-88-66 Dr. J. Nelson Grace Regional Administrator, Region II U.S. Nuclear Regulatory Commission 101 Marietta Street, N. W., Suite 2900 Atlanta, Georgia 30323 Re:

Turkey Point Units 3 and 4

Docket Nos.

50-250 and 50-251 Mana ement-on-Shift Weekl Re ort

Dear Dr. Grace:

Pursuant to the Nuclear Regulatory Commission Order dated October 19,

1987, the, attached summary of Management-on-Shift (MOS) reports is submitted.

Should there be any questions on this information, please contact us

~

Very truly yours, Hid C.

O.

dy 8~ Execut'v Vice President COW/SDF/pw Attachment cc:

J.

Lieberman, Director, Office of Enforcement, USNRC Dr. G. E. Edison, Project Manager,

NRR, USNRC Senior Resident Inspector, USNRC, Turkey Point, Plant R. E.. Talion, President, FPL r,.88p219pppy ppggp

.DR,.

A>OCK 05000250 woS@

an FPL Group company

MANJREMENT ON SHIFT OS)

WEEKLY

SUMMARY

REPORT WEEK STARTING:

PAGE~

OF 2

Four MOS observers were on shift; John A.

Dyer, St.

Lucie Nuclear

Plant, Quality Control Department (02/01-02/07/88, Days);

Garry A.

Harris, Westinghouse Electric Corporation (02/01-02/08/88, Nights);

William C.

Miller, Turkey Point Nuclear Plant Senior Technical Advisor (02/01-02/05/88, Nights);

and Daniel E.

Meils Turkey Point Nuclear Plant Chemistry Supervisor (02/05-02/08/88, Nights).

During this reporting period, Unit 3 was returning from an outage and began the plant startup process.

Unit.

4 operated at high power levels until inoperable battery chargers on February 7,

1988 forced a plant shutdown.

No immediate safety problems were observed by the MOS observers.

The following questionable work practices were observed:

Entry into a

highly contaminated area without proper protective clothing.

Reactor operator license candidate trainees acknowledging a

few routine Control Room annunciator alarms without verbally communicating each repeat occurrence to the Control Room operator.

Over fifteen positive comments were made by MOS observers concerning good team

work, the professional environment of the Control
Room, housekeeping, conduct of shift turnover meetings and conscientious performance of duties by various plant personnel.

During the period the MOS observers made about twenty eight suggestion for improvements including:

Five suggestions for improving procedures in areas such as liquid waste

release, Auxiliary Feedwater System
testing, Residual Heat Removal valve testing and steam generator filling.

Three suggestions to help insure

complete, current procedures are always issued for field use.

Two equipment labeling suggestions.

Six suggestions for additional equipment or improvement of equipment corrections.

Three comments on the Emergency Drill conducted on February 4th.

ATTACHMENT:

MOS DAILY REPORTS

MANAGEMENT ON SHIFT +OS}

WEEK STARTING'EEKLY

SUMMARY

REPORT PAGE 2

QF 2

A MOS observer again expressed concern about the use of the current Technical Specifications and the Interim Technical Specifications.

Specifically during the event dealing with "4S" battery charger operability.

FPL understands that the use of two sets 'f Technical Specifications presents a

new learning experience to the operators and as

such, some difficulties are faced until the Interim Technical Specifications are well understood.

The issue has been discussed in a

recent meeting in Bethesda with NRC management and the issue discussed by the MOS observer should not be construed as new or different evidence.

Plant management was fully involved in the event and proper guidance was provided to the Control Room operators.

ATTACHMENT:

MOS DAILY REPORTS

0-ADM-019 management on Shift (MO+

MOS DAILYREPORT To Operations Superintendent - Nuclear Date:

From:

(I bseroer)

Shin;:

Qx Day g Night A.

Plant evolutions observed 0

Morning meeting Shift briefing days and Peak shift Review of the following procedures

- O-ADM-015.3 "Satellite Accumulation of Hazardous iVasten ADM-201 "Upgrade Operations Procedure Usage"

" OSP-075.6 nAuxililary Feedwater Train 1 Backup Nitrogen Test" Observed performance of a

portion of 4-OSP-075.6, Auxiliary Feedwater Train Backup Nitrogen Test.

B.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement 1.

Followup on Satellite Accumulation Area Re:

J.A. iUest MOS report 01/30/88 D

3.

Discussed with the "Hazardous Materials Coordinator" specifically O-ADM-015.3 paragraph 5.4 and 5.8.

B.

Professionalism, Summary of Shift, Comments 2.

3.

Shift briefings, days and peak shift, were very informative.

All'disciplines participated and had a good understanding of the current status of both units (Good practice).

Nuclear operator 'n charge conducting 4-OSP-075.6 "Auxiliary Feedwater Train Backup Nitrogen Test" conducted a briefing with other personnel involved in the test to ensure their understanding of the test (Good).

During performance of the test one step was performed out of sequence.

This is not in accordance with 0-ADM-201 paragraph 5.1.1 and 5.1.2 requiring verbatim compliance.

(Operator repeated in correct order).

02/01/88

0-ADM-019 anagement on Shift (MOSQ MOS DAILYREPORT Page Recommendations 2.

3.

Reference D A satellite accumulation drum is not required for used oil which itself is not

'a hazardous waste.

Revise O-ADM-015.3 to delete the requirement (paragraph 5.4.4) for a satellite accumulation drum.

Reference H

Test 4-OSP-075.6 was delayed 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> until IGC could process a PWO to install a test guage.

This may have been due to outage on Unit 3 or because test was moved up (Willfollowup on this item).

Nuclear Operations needs more leeway in performing steps out of sequence.

The one step performed out of sequence was due to a key being taken from the Control Room to unlock a root valve on a pressure guage.

Completed By:

dserver Date:

Reviewed By:

Management Review By:

perations Superintendent-Nuclear Date MANAGEMENTINITIALRESPONSE

  • Iloa.l OIIO7%5 02 01/88

0-ADM-019

~agement on Shift (MOS)~

MOS DAILYREPORT Page To:

Operations Superintendent - Nuclear Date:

8 From:

G rr A. Harris bseruer Shin;:

p Day Qx Night A.

Plant evolutions observed 4-OSP-075.1 Auxiliary,Feedwter Operability Test 4-OSP-075.6 Auxiliary Feedwater Nitrogen Backup Test Shift Turnover Meeting Normal Shift Operations B.

C.

D.

Immediated safety problems None observed Questionable work practices None observed Area(s) for improvement 2.

IVhile conducting procedure 4-OSP-075.7 Train 2

Back-up Nitrogen

Test, the Nuclear Operator was directed by the procedure to "measure and record oil level" (step 7.1.8) for the lube oil sump and governor oil sump.

The clause to measure and record requires that the shift indicators should be capable of being recorded in mm or inches or some other dimension, however only gross approximations are available.

If this is a requirement, then adequate measures should be taken to ensure that this action can be met.

During the execution of procedure 4-OSP-075.7 Train 2 Back-up Nitrogen Test, it was noted that the flow indicators on the Train 2 Auxiliary Feedwater Platform were labeled with pencil etchings to denote Auxiliary Feed Flow to steam generators (i.e. nC", nB", "A").

To ensure accuracy in reporting and eliminate possible confusion, permanent labels should be affixed.

B.

Professionalism, Summary of Shift, Comments l.

A strong sense of team work was evident at the shift turnover meeting.

All key players were present (i.e. Electrical, Maintenance, IGC Departments) and contributed significantly to the knowledge exchange between all groups.

2.

The PSN forseeing the possibility of the plant experiencing a lost of feedwater transient due to upcoming events reviewed emergency procedures with staff to ensure quick and timely response from all personnel.

a LltN.l I'Mha1 02/01-02/88

0-ADM-019 Qanagement on Shift (MOSQ MOS DAILYREPORT Page Recommendations Early in the peak shift, operators and Technical staff personnel attempted a

coordinated effort to simultaneously run three procedures 4-OSP-075.1 Auxiliary Feedwater Operability Verification, 4-OSP-075.6 Auxiliary Feedwater Backup Nitrogen Test and related Inservice Test OST) procedure.

In essence, a noticable lack of manpower and minor communications resulted in missing valve operability data and minor step displacement resulting in a procedure being repeated.

Although personnel involved were familar with the procedures, care should be taken that all parties are aware of procedural content and that the testing is adequately staffed.

Completed By:

Garr A. Harris M

bseroer Date: 02/02/88 Reviewed By:

Operations Superi ntendent-Nuclear Date: P ~

Management Review By:

P D~ae i >l>IR ate i~lrE Date MANAGEMENTINITIALRESPONSE 02/01-02/88

0-ADM-019 5nagement on Shift (MOS)

MOS DAILYREPORT Page To:

Operations Superintendent - Nuclear Date: o2 ol-o2 ss From:

William C. Miller M

bseruer Shift:

Q Day Qx Night Plant evolutions observed Shift turnover Shift meetings Normal shift operations Test Run "3Cn RCP B.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement PSN was quizzing two Nuclear Turbine Operators (NTO) regarding valve locations associated with feedwater supply from fossil Unit 2 and the opposite nuclear unit.

Neither NTO displayed strong knowledge of the location of the valves in question.

02/01-02/88

0-ADM-019 anagement on Shift (MOS MOS DAILYREPORT Page Professionalism, Summary of Shift, Comments 2.

3.

Good professional shift operations.

Operators did good quality shift turnovers and board walkdowns.

The shift briefing was well run.

Prior to the test run of the "3Cn RCP the Chief Electrician joined the NWH and RCO in the Control Room for a planning session.

Each person outlined what they were going to do and when they would do it.

When the pump run actually took place it was flawless.

The RCO's spent any extra time they had training the Group 11 candidates.

Informal quiz sessions and formal module checkouts were performed.

Challenging questions were asked and the candidates had to research any questions they could not answer.

Recommendations Training Department should evaluate the Nuclear Turbine Operators of unusual feedwater valve alignments.

As stated the weaknesses noted were in the identification of alternate flow paths to the steam generators from the opposite nuclear unit and Unit 2. Every NTO should be able to immediately locate the valves in question and align the system.

Completed By:

M dserver DI:~

Reviewed By:

Operations Superintendent-Nuclear Date:

Management Review By:

P Date V

Date V

I~~8'8 Date MANAGEMENTINITIALRESPONSE 4M(N;I OIIQ7%5 02/01-02/88

0-ADM-Q19 anagemenC on Shift(M(

MOS DAILYREPORT Page To:

Operations Superintendent

- Nuclear Date:

0 From:

John A. D er (M

bserver)

Shik:

Qx Day Night A.

Plant evolutions observed Morning meeting Shift briefings (Days and Peaks)

Review of procedures OP-041.8 nPilling and Venting The Reactor Coolant System".

- AP-0190.86 "Document Control" Plant tour with the Plant Supervisor Nuclear.

Filling Unit 3 Reactor Coolant System (Control Room).

Unit 4 Turbine oil temperature reduced to check effect on turbine vibration.

Westinghouse representative was in attendance.

B.

Immediate safety problems None Questionable work practices None Area(s) for improvement

'one Professionalism', Summary of Shift, Comments 2.

3.

4, Normal shift operations.

Unit 4 at 100',0 power.

Unit 3 Reactor Coolant System fillingin progress.

Si nificant Condition Adverse to ualit Instrumentation and Control Technicians caused a Control Room Isolation while working in the Process Radiation Monitoring System Racks (Actuation of Bngineered Safety Peature).

The Nuclear Regulatory Commission was notified in accordance with Administrative Procedure 0103.12.

Control Room Isolation caused by work in the Process Radiation Monitoring System Racks is a

recurring problem.

The Instrumentation and Control Department conducted a meeting to determine the root cause of the problem.

Allplant areas toured were clean - Good housekeeping practices.

Allpersonnel observed in hearing protection areas had ear protection.

02/02/88

0-ADM-019 management on Shift (MOS MOS DAILYREPORT Page Recommendation None Completed By:

bseroer Date:

Reviewed By:

Management Review By:

P perations Superintendent-Nuclear VP Date MANAGEMENTINITIALRESPONSE aMNL! oll07%4 02/02/88

0-ADM-019 5%agementon Shift(MOS)

MOS DAILYREPORT Page To:

Operations Superintendent

- Nuclear Date:

From:

bseruer Shift:

Q Day Qx Night Plant evolutions observed Filling and Venting the Reactor Coolant System 3-OP-041.8 Unit 3 Reactor Head/Control Rod Drive Mechanism (CRDM) Duct work reassembly.

Unit 3 Standby Steam Generator Feedpump Surveillance Test Unit 4 100% normal operation Shift meeting Shift turnover meeting B.

Immediate safety problems None observed

=C.

Questionable work practices None observed D.

Area(s) for improvement None observed B.

Professionalism, Summary of Shift, Comments None observed ALIELq.l I~lie'I 02/02-03/88

0-ADM-019

)Onagement on Shift (MOS)

MOS DAILYREPORT Page Recommendations The critical path events for completing Filling and Venting procedure 3-OP-041.8 were hampered due to testing being performed on valve 863A with MOVATS equipment.

A PWO (C309916) had earlier been written for this component when a Control Room hand switch failed to close the valve unless it was held in the closed position.

The test path chosen by the on-shift personnel required the closing of the RHR heat exchanger inlet and outlet valves 755A and 757A.

This operation was necessary since an interlock on the upsteam valves 863A/B would close these valves if RHR pump discharge pressure is greater than 210 psig.

The manual heat exchanger isolation valves are very time consuming to close.

In addition, with the isolation valves closed, the associated RHR loop becomes inoperable.

Mode 5 (cold shutdown) requirements (AP-0103.32 page 2 step 4.10.1) state the need for two operable coolant lo'ops one reactor coolant loop and one RHR loop or two RHR loops.

Thus extensive operations were conducted to meet this requirement upon isolation of the RHR loop.

Although the 863A RHR Alternate Discharge Isolation Valve was found operable late in the mid-shift, it is possible that critical path hours could have been saved by pre-planning and using on established method of testing the valve's operability.

According to OP-0209.1, page 28, Appendix B, sheet 7 of ll, the valve in question should have been tested using procedural 3/4 OP-050 step 7.2, Transferring to Alternate RHR Cooldown Lineup.

According to the procedure the alternate RHR discharge valves should be tested in this lineup instead of the lineup utilized.

Although utilizing this procedure would have required depressurizing the RCS to approximately 80 psig, the effort seems efficient and feasible.

The concern that extensive steps in the fill and vent procedure would have to be repeated is eliminated since pressurizer level would not decrease below 10%.

The effort to take an RHR loop out of service and establish an operable RCS loop would be eliminated.

It is recommended that future operability testing of Alternate RHR Discharge Isolation Valves 863 A/B be performed according to OP-0209.1 Appendix B.

Completed By:

A Harris I

bserver.

Date:

02/03/88 Reviewed By:

Operations uperintendent-Nuclear Date Management Review By:

P~M ate ate

  • Mtw:Iol/07'Ms 02/02-03/88

0-ADM-019 nagement on Shift (MOS)

MOS DAILYREPORT Page To:

Operations Superintendent

- Nuclear Date:

From:

(M 6seroer P

Plant evolutions observed Shift; p

Day px Night Shift turnover - RCOs and NWEs Shift briefing Steam Generator drain down System alignment for filland vent NTOs performing log readings Standby Steam Generator Feedpump Operability Test B.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement Nuclear Turbine Operators (NTO) had to share thermometers and hydrometers between batteries.

Surprisingly, this significantly added to the time required for him to monitor batteries.

Especially time cosuming was the wait for thermal equilibrium to be reached every time he moved the thermometer from one battery to the next.

I received new insight into how busy the NTO is during his shift.

If we can save him even a

few minutes (approximately 15-20 minutes could have been saved this evening),

that few minutes could be well spent elsewhere.

B.

Professionalism, Summary of Shift, Comments I followed an NTO through rounds and was very impressed by the work load he faced and by the careful manner in which he went about his business.

He was well,trained and very conscientious about doing a good job.

The secondary plant looked quite clean, and no serious problems were encountered during these rounds.

1MELkl I'@el ie7 02/02-03/88

~

0-ADM-019 j+nagement on Shift (MOS MOS DAILYREPORT Page Recommendations Purchase enough thermometers and hydrometers to ensure enough are available. for each battery plus spares.

Completed By:

W.C. Miller bserver D b:~i Reviewed By:

0 erations Superintendent-Nuclear Management Review By:

PM-VP D

VP Date MANAGEMENTINITIALRESPONSE 4 MORI oll07%I 02/02-03/88

0-ADM-019

'aanagement on Shift (MOSQ MOS DAILYREPORT Pago To:

Operations Superintendent-Nuclear Date:

02 03 88 From:

John A. D er (M

bseruer)

Shift:

Qx Day Q Night A.

Plent evolutions observed Morning meeting Shift briefings (Days and Peaks)

Planning meeting Plant tour of vital areas outside of the Radiation Control Area Procedure review GOP-503 "Cold Shutdown to Hot Standby"

- O-OSP-200.2 "Plant Startup Surveillancesn OSP-041.7 nRCS Heatup and Cooldown Temperature Verification Venting of the Reactor Coolant System in accordance with procedure 3-OP-041.8 B.

C.

Immediate safety problems None Questionable work practices None B.

Area(s) for improvement None Professionalism, Summary of Shift, Comments 1.

2.

Good housekeeping practices in all areas toured.

Good exchange of information at the shift briefings.

Plant 'upervisor Nuclear discussed how all plant personnel (Operations, Technical

Staff, Maintenance, etc.)

should work together as a team in the reduction of significant events.

He used the event discussed on 02/02/88 as an example.

This was well received and several constructive responses were noted.

STA indicated that a change to 0-ADM-701 "Plant Work Order Preparation" would probably be recommended to reduce maintenance related events.

RCO trainees were utilized as much as possible in the Reactor Coolant System Venting Evolution. The senior RCO asked the trainees pertinent questions as part of the operation training.

Subsequent to the shift briefing by the Plant Supervisor Nuclear (PSN) the senior RCO conducted a more detailed briefing with those specifically involved with the RCS venting, process (Good practice).

02/03/88

0-ADM-019 lnagement on Shift (MOS)~

MOS DAILYREPORT Page Recommendations None Completed By:

server Date:

Reviewed By:

Operations Superintendent-Nuclear Management Review By:

Dka vp Date MANAGEMENTINITIALRESPONSE a MORI oll07hN 02/03/88

0-ADM-019 agement on Shift (MOS)

MOS DAILYREPORT Page To:

Operations Superintendent

- Nuclear Date:

-04 88 From:

(MO bseruer Shift:

Q Day Qx Night Plant evolutions observed Unit 4 Diesel A Operability Test O-OSP-023.1 Unit 3 RHR pump A valve out operations Unit 4 Turbine eccentricity problem Unit 3 Pilling and Venting procedure 3-OP-041.8 Unit 4 Test procedure 398 Emergency Containment Cooler Periodic Test Shift turnover meeting Normal operations B.

Immediate safety problems None observed C.

Questionable work practices None observed D.

Area(s) for improvement Quality job performance demands operable quality tooling.

While conducting clearance operations on Unit 3 RHR pump A, the nuclear operators were required to close and lock shut several valves.

Pure manual manipulation of the valves is cumbersome and exhaustive since hundreds of turns are needed to close each valve.

Thus, the operators use an air-operated wrench to aid in the closure of the valves.

With the wrench, the operators managed to close the valves.

However, to facilitate its use one operator had to control air flow by crimping the supply

hose, while the other engaged the tool.

Obviously, quality and safety go hand in hand but the use of such tooling becomes a source of aggravation for the operators and could affect performance.

iMELRI IDelie7 02 03-04 88

0-ADM-019 5nagement on Shift (MOS) ~

MOS DAILYREPORT Page Professionalism, Summary of Shift, Comments 1.

Zeal, enthusiasm and attention to detail were all extremely evident during the Diesel Operability Test; The turbine operator was knowledgeable of the procedure and each intricate step displayed pride and quality-first attitude to the task at hand.

2.

Good communications resulted in a smooth transition from the fill and vent operations to the critical path RHR pump evolutions.

Recommendations 1.

Ensure operators (turbine/nuclear) are provided proper tools which are fully functional to preclude any questionable safety practices.

The review should extend beyond the example presented in section D.

Completed By:

bseruer Dt:~

Reviewed By:

Operations Superintendent-Nuclear Date:

Management Review By:

P

-N Date VP Date MANAGEMENTINITIALRESPONSE

  • Moa:I el/071ea 02/03.-04/88

0-ADM-019 anagement on Shift (MOS)

MOS DAILYREPORT Page To:

Operations Superintendent - Nuclear Date:

02 03-04 A8 From:

M bserver)

Plant evolutions observed Shift:

Q Day gx Night Shift turnover PSN Shift briefing Emergency Diesel Generator "A"Operability Run Toured Auxiliary Building and P.ad Vlaste Building Observed operators evaluating and attempting to correct the cause of high vibration on ¹9 bearing on Unit 4 turbine.

Normal plant operations B.

C.

Immediate safety problems None Questionable work practices None Area(s) for improvement l.

¹3 CCYP heat exchanger room - housekeeping needs improvement.

Area is cluttered and dirty.

Professionalism, Summary of Shift, Comments Relatively quiet shift with no significant operational issues.

During tour of Auxiliary Building I observed EIealth Physics personnel at their posts and assisting plant ivorkers.

They were courteous and attentive to their job.

They maintained a presence at the nevi vihole body friskers and briefed people exiting the RCA in their use.

Overall they exhibited very professional behavior.

Recommendations Have someone address the housekeeping of ¹3 CCVI heat exchanger room.

Completed By:

Revie'wed By:

Management Review By:

P

,uJ,

~

server te Operations Superintendent-Nuclear Date:

Date

  • MOS:I 01IU7/aa 02/03-04/88

0-ADM-019 anagement on Shift (M OS~'OS DAILYREFORT Page To:

Operations Superintendent-Nuclear Date:

From:

bseroer)

Shift:

Qx Day Q Night A.

Plant evolutions observed Morning meeting Practice Emergency Drill Shift briefings Plant tours-Radiation Controlled Area and balance of plant B.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement Non-Controlled Procedures

- refer to sections E and F procedure comments and recommendations.

02/04/88

0-ADM-019 144agement on Shift (MOS)

MOS DAILYREPORT Page Professionalism, Summary of Shift, Comments 2.'.

Practice Emer enc Drill a

In addition to the normal shift compliment, there were ten (10) players and/or controllers and three (3) NRC observers.

Thirteen (13) additional personnel in an already crowded Control Room.

In spite of the number of personnel the reactor control operator maintained control (Good work on the part of the operator).

b)

A fire drill was announced, but it was not correctly announced as part of the Emergency Drill.

There was some confusion as to who should respond to the fire drill; the normal shift fire team on the drill fire team.

The Nuclear Watch Engineer took immediate action to alert the shift fire team not to respond so they would be available to support plant evolutions (Good work on the part of the Watch Engineer).

c)

The Emergency Drill Coordinator had forgotten to provide for an Emergency DrillFire Team.

Uncontrolled o~on-Controlled procedures are verified against an "Upgrade Procedure Index" which is not a controlled document.

This is not in accordance with C?uality Assurance Manual Procedure QP 6.2 rev. 5 paragraph 5.4.

Shift briefings continue as a

highpoint.

Maintenance (mechanical) had some good feedback on how to aid in reaching the 200oF milestone.

The Plant Supervisor Nuclear complimented the htaintenance Foreman on his suggestions.

Good meeting.

Recommendations Reference section E.

1.

DrillCoordinator could make better utilization of:

a)

Experienced personnel and reduce the number of players/controllers in the Control Room.

b)

One (1) NRC observer should be sufficient during the drill; especially in the Control Room.

c)

Better preplanning and coordination with Operations prior to practice Emergency Drills.

2.

Procedures a)

Administrative Procedures 0-ADN-201 and AP-0190.86 require verification of Non-Controlled documents against the "Upgrade Procedure Index" on the nDocument Control Spare Copy File Index".

Neither of these indexes is a controlled document.

hiake the indexes controlled or revise the aforementioned procedures to require document verification against a controlled document.

  • blORl 1Ml/87 02 04 86

0-ADM-019 anagement on Shift (MOS)

MOS DAILYREPORT Page Recommendations (Continued) b)

Change Figure 1 Item D of AP-1090.86 to a stamp similar to:

FOR INFORMATIONONLY Before use verify with a controlled copy and verify if document is affected by an On The Spot Change (OTSC)

Date verified:

Intital c)

Provide operations with a stamp as recommended in item 2:

0-ADM-201 permits use of attachments on sections of procedures.

These portions of procedures should be stamped and verified prior to use in the field to ensure use of current procedures.

Completed By:

Date:

Reviewed By:

Operations Superintendent-Nuclear Date:

Management Review By:

ate ate I'INAI.PAGE

0-ADM-019 nagement on Shift (MOS)

MOS DAILYREPORT Page To:

I Operations Superintendent

- Nuclear Date:

From:

(MO 6server)

Shift:

p Day px Night Plant evolutions observed Vital power supply (Battery) periodic test - Units 3 and 4 O-OSP-059.1 Source Range Operability Test - Unit 3 MOVATTest for 749A RHR A CCW outlet valve - Unit 3 Plant tour Shift turnover meeting Start-up Transformer Periodic Test - Units 3 and 4 Turbine vibration problem - Unit 4 Unit 4 power operations at looa'o B.

Immediate safety problems None observed C.

Questionable work practices None observed D.

Area(s) for improvement 2.

Standby inverters A, B, C, and D are common alternates to supply vital buses.

As an example, Standby inverter A can supply 3P07 or 4P07; Standby inverter B can supply 3P08 or 4P08, etc.

Extensive efforts have been made to lessen operator error. by the use of the blue-Unit 4/brown-Unit 3 color designations.

Since common equipment exists that serves both units, the appropriate color coordination should be extended to the standby inverter units.

In the cable spreading room it was noticed that a

free-standing protective screen was placed at the rear of panel 3C11(G) (Gen. and Main Relay/Auxiliary Startup Transformer panel). It was communicated to the MOS observer that the screen was in place as precaution against inadvertent reactor trips caused by jarring of generator protection relays.

The 3C11(T) panel stands adjacent to the previously mentioned panel and is a mirror image of it in design and function.

However, no screens are present to prevent on inadvertent reactor trip.

Even though area is posted, travel through it is still possible and frequent.

iMELi:1 I ~le oz/o4-o5/ss

0-ADM-019

<<hnagement on Shift (MOS+

MOS DAILYREPORT Page ProfessIonalism, Summary of Shift, Comments A

strong sense of teamwork was evident during MOVATs testing of 1".OV-749A, Recommendations 2.

The color orange is used to designate common vital equipment between the units, thus the inverters should be affixed with orange emblems labeling them as such.

A similar free-standing screen should be placed at the, rear of the panel to shield the exposed protective relays.

Completed By:

bserver Date:

Reviewed By:

/

Operations Superintendent-Nuclear r

Date:

Management Review By:

P

/as-Date VP e

D VP Date MANAGEMENTINITIALRESPONSE IMos; I 0 lte7ttta 02/04-05/88

0-ADM-019 nagement on Shift (MOS)

MOS DAILYREPORT Page To:

Operations Superintendent-Nuclear Date:

From:

(M bserver)

Shift:

p Day Qx Night Plant evolutions observed Shift turnover - PSN and NWE Shift briefing Startup Transformers Periodic Test Site Evacuation Alarm Periodic Test System walkdowns in preparation for mode change Normal plant operations B.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement Operations again spent the night trying to control ¹9 turbine bearing vibration.

Lube oil temperatures, Hydrogen side and Air side seal oil temperatures "were all manipulated in an attempt to reduce vibration.

I do not see evidence of this problem having been evaluated by Engineering personnel (Plant or Engineering).

Instead the operators continue to try to deal with it on a daily basis, applying remedies that appear to be effective one time and are ineffective the next.

Professionalism, Summary of Shift, Comments Professional attitudes displayed by all personnel observed especially Turbine Operators who worked diligently the entire shift.

1MLLS:I IDelse1 02 04-05 88

0-ADM-019 50nagement on Shift (MOS)

MOS DAILYREPORT Page Recommendations I reconmend that the Technical Department investigate the turbine bearing vibration problem and give Operations some guidance on ho~v to solve the problem instead of merely living vfith it:

Completed By:

IV Date:

Reviewed By:

Operations Superintendent-Nuclear Management Review By:

PM-D Dvp Date VP Date MANAGEMENTINITIALRESPONSE

  • Noa."I olio7paa 02/04-05/88

0-ADM-019 anagement on Shift (MOS)

MOS DAILYREPORT Page To Operations Superintendent-Nuclear Date:

02/05/88 From:.

J A D (I seruer)

Shift:

Qx Day Q Night Plant evolutions observed Morning meeting Shift briefings Control Room Operations Plant tours Plant Operations Unit 3

Pressurizer heaters and "B" RCP operating.

Heating up to less than 2004F and drawing a bubble in pressurizer.

Unit 4 in Mode I at 100% power B.

C.

Immediate safety problems None Questionable work practices None D.

Area(s) for improvement l.

Adherence to Administrative Procedures 2.

Clarification on documentation of verification that documents/procedures are current (Refer to section F).

Professionalism, Summary of Shift, Comments 2.

3.

Turbine impeller oil pressure problem recurred again this morning.

Supervisor explained what might occur and what corrective actions should be taken.

He explained, that trainees were to stand aside, if an event did occur, and the reactor control operator would take corrective action.

Subsequently trainees would discuss the operation with the reactor control operator.

It was noted that operators were not conforming to paragraph 5.3.7 of 0-ADM-201 requiring sections 1, 2, 3, and 4 of the procedure in use to be attached to sections or attachments of the procedure being used.

This was brought to the attention of the Plant Supervisor Nuclear who immediately explained the requirement to the operators.

In addition, he made an entry in the "Shift Information Book" so that subsequent shifts would be reminded of this requirement.

Plant Supervisor Nuclear reminded all personnel that this was a

busy time in preparing to return Unit 3 to service.

He informed personnel that it was more important that work was to be performed correctly than it was for it to be performed quickly.

He stated that if they felt they were being asked to do too much, just to let him know.

02/05/88

0-ADM-019 Management on Shift (MOS)

MOB DAILYREPORT Pnge Recommendations (See D.2) 1.

Guidance is given to personnel in Administrative Procedure 0190.86 "Document Control" paragraphs 4.4, 5.2.9, 8.1.4, 8.2.4.2 and 9.9.4 on documentation of verification of "On the Spot Changes" to ensure they are current.

2.

Administrative Procedures 0190.8 and 0-AD14-201 require in paragraphs 4.1, 5.7.7, 8.1.11, 8.2.3 and 8.2.4.1 and 5.3.1 and 5.4.1.3 respectively that procedures/documents be verified to be current prior to use.

No guidance is given on how to document this verification.

This is necessary so personnel, especially Operations, can be consistent.

These procedures need to be revised and perhaps a stamp as recommended on my 02/04/88 report could be used.

The PSN suggest that verification could be made part of every procedure's prerequisites.

(See D.i) 3.

Stress administrative duties in the operator training and requalification programs.

4.

PSNs should frequently stress the importance of administrative duties at shift briefings.

This should reduce NRC violations due to administrative problems.

Completed By:

John A. D er bseruer gate; 02/05/88 Reviewed By:

Operations Superintendent-Nuclear PM N ate P

Dat VP ate MANAGEMENTINITIALRESPONSE

  • hid.l<<ldllw 02/05/88

0-ADM-019 anagement on Shift (MOS)

MOS DAILYREPORT Page To:

Operations Superintendent-Nuclear Date:

02/05-06/88 From:

Garr A. Harris (M

bseruer Shift:

Q Day Qx Night Plant evolutions observed GMI-028.4 CRDM and RPI cable installation Unit 4 Turbine evolutions Unit 3 in Mode 5 operations Unit 4 at 1009b power operations B.

Immediate safety problems None observed C.

Questionable work practices Trainees enthusiasm and attention to details is always highly visible and commendable during shift operations.

However, it has been observed several times during the peak and mid shifts that trainees are acknowledging alarms without direct verbal communications between himself and the RCO. "Although only routine annunciators seem to fall in this category, it was clearly noticed that several times an alarm was acknowledged.

A strong reminder is in order to ensure that RCO board responsibilities are not compromised.

D.

Area(s) for improvement l.

It was noted on an earlier report that operators were not conforming to paragraph 5.37 of 0-ADM-201 requiring sections 1, 2, 3, and 4 to be attached to sections or attachments of a procedure in use.

PSNs quickly remedied this situation by formal announcements during shift meetings and turnover meetings by the MOS observers.

However during observation of CRDM cable repair by IGC technicians, none of the sections were attached to the section of the procedure in use.

IGC technicians must be aware of the precautions and limitations in the above mentioned sections to ensure a quality job.

iMlLi.I I AUli'2/05-06/88

0-ADM-019 anagement on Shift (MOS)

MOS DAILYREPORT Page E.

Professionalism, Summary of Shift, Comments 2.

3.

4 The peak shift PSN should be commended for his initiative and creativity in problem solving and use of good sound engineering judgement during the review of impeller oil pressure induced transient.

Positive input from key management personnel showed strong justification of his ideas.

The mid. shift PSN and operators did an excellent job of implementing the agreed upon power manipulations to find the root cause of the impeller oil pressure problem.

The mid shift PSN and APSN ensured all personnel were well informed of the "game plan" and subsequent actions if the testing maneuver led to a trip.

Good communication and well thought out methodical steps led to an event free scenario.

The trainees performed the power reduction in near text book fashion.

Group cooperation and team pride were instrumental in the critical path RHR "A" pump repair being completed nearly seventeen hours ahead of schedule.

It was the concern of this MOS observe'r that with the critical path installation of RPI cabling nearly 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> behind schedule only two technicians were assigned to perform the procedural pre-installation testing and cabling hookup.

Both technicians worked diligently to facilitate the installation.

Recommendations Ensure all departments are aware of the MOS observation noted by J.

Dyer on his report of 02/04/88, section F.2 and are in compliance.

Note that section 8.2.2 of AP-0109.1 references 0-ADM-201 for procedural adherence policy.

Completed By:

I seruer u'>:.'eviewed By: ~..~.

~ t>.

<)~:.> r

'perations Superintendent-Nuclear D

/,.

Date: + f IP.

Management Review By:

  • M(LL.IelI01'bi<

s>.~I'.

ae ate P

02/05-06/88

0-ADM-019 anagement on Shift (MOS)

MOS DAILYREPORT Pilsl To:

Operations Superintendent

- Nuclear Date 02/05-06/88 From:

Daniel E. Meils (M

bser ver)

Shift:

Q Day Qx Night Plant evolutIons observed 0

Unit 3 - RCO rounds Unit 3 - Drain of "A"and "C" Steam Generators Liquid release (C-WMT LRP-88-044)

Unit 4 decrease in power to adjust impeller oil pressure Shift briefings Nuclear Operator (NO) "outside" rounds B.

C.

Immediate safety problems None Questionable work practIces l.

Entry into a highly contaminated area without proper protective clothing (PC s).

D.

Area(s) for improvement 2.

3, OP-5163.2 "Waste Disposed System - Controlled Liquid Release to the Circulating Water" step 8.2.2 requires the Nuclear Operator (NO) to have the RCO perform 3-OSP-67.1 "Process Radiation Monitoring Operability Test".

Step 8.2.2.1 of OP-5163.2 require a

source check of R-18, however the source check is not referenced in OSP-067.1.

As a result of this omission in OSP-067.1, the source check of R-18 was not performed prior to releasing the C-WMT, LRP-88-044.

While observing the Nuclear Operator perform "outside" rounds two areas for improvement were noted:

a)

Unit 4 SPP heat exchanger room is very noisy.

b)

Entry into a high contamination area in Unit 3 SPP heat exchanger

'room without the proper PCs.

Several employees were observed taking a short cut down the embankment south of Unit 4 containment between the Unit 4 SPP heat exchanger room and the Rad Waste Building.

02/05-06/88

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT, Professionalism, Summary of Shift, Comments 2.

3.

Shift turnover was well structured.

PSN, APSN and NV1E all participated in giving clear instructions for the shift.

The RCO's and NO's were congenial and discussed evolutions freely and openly.

The NO on shift went out of his way to check operability of all equipment.

F.

Recommendations 2.

3.

Evaluate the need to perform R-18 operability and source checks prior to every liquid release.

Change procedures OP-5163.2 and OSP-067.1 as necessary (See D.l).

Evaluate the need for additional marking of highly contaminated areas within contaminated areas.

Possible addition of more visual designation of high contaminated areas.

Also, evaluate the extent of this problem and upgrade knowledge/awareness as indicated (See D.2.f).

Evaluate hearing protection requirements for Unit 3

and 4

SFP heat exchanger rooms and post hearing protection requirements, as necessary (See D.2.a).

Completed By:

Reviewed By:

Daniel E. Meils I

bseruer

)

Operations Superintendent-Nuclear Date:

02/06/88 Management Review By:

)

D e

D t P

lip Date MANAGEMENTINITIALRESPONSE

  • Mlkklllli07>be 02/05-06/88

0-ADM-019 anagement on Shift (MOS)

MOS DAILYREPORT To:

Operations Superintendent - Nuclear Date:

02 06 88 From:

(M bseroer)

Shift:

Qx Day Q Night Plant evolutions observed Plant operations Tour of radiation control areas Morning meeting Planning meeting B.

C.

D.

Immediate safety problems None Questionable work practices None Area(s) for improvement E.

Administrative guidelines clarification (Refer to section F).

Procedure/System interactions (Refer to section F).

Professionalism, Summary of Shift, Comments l.

Again shift briefings continue as a highpoint.

A lot of information on plant status and shift goals is discussed.

This is a two way transfer of information between all concerned and everyone has an understanding of the evolutions schedule to occur on their shift.

2.

There is still some confusion/misunderstanding among shift personnel as to the use of the stamp depicted in Administrative Procedure 0190.86 figure/item.

Some personnel thought that the shift technician was responsible for fillingit out. There were occasions today where procedures were either in progress or completed and the stamp was not completed.

The supervisors on shift took immediate action when notified (Refer to section P).

3.

A dump flush of Unit 3 condensor was completed through paragraph 5.2.2.b of 3-OP-073 "Condensate System.

A problem was encountered in closing the recirculation valve to the canal 3-PDWR-010 when the dump was completed.

The supervisor decided to commence filling "3C" steam generator using 3-OP-079 Steam Generator Wet Layup System" while valve 3-FDWR-010 was being repaired.

After approximately one hour no level increase was evident in the "C" generator.

Shift investigation revealed the water was being pumped to the canal and filling of "C" generator was terminated (Refer to section F).

The supervisor was to contact the Procedures Upgrade Program Department to resolve this item.

02/06/88

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Puge Recommendations (Refer to E.2 and D.l) 1.

The recommendations made on the day shift MOS reports of 02/04/88 and.02/05/88 in regard to administrative areas still apply.

In addition perhaps the

PSN, APSN or the NlVE should check pro'cedures prior to use until these administrative duties are clarified.

(Refer to D.2 and E.3) 2.

Procedures 3-OP-073 and 3-OP-079 appear to be frequently used in conjunction with one another.

Caution notes should be added to alert personnel of problem areas or perhaps requisite section revised to preclude this problem.

Completed By:

John A. D er bseruer Date:

02/06/88 Reviewed By:

Management Review By:

Operations Superintendent-Nuclear PP-ae Pz D t

,/

Date/

D h

MANAGEMENTINITIALRESPONSE EM'.I Ol((17~

02/06/88

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT PGsL To:

Operations Superintendent-Nuclear Date:

02 06-07 88 From:

(M server Shift:

Q Day Qx Night Plant evolutions observed CV-3-1606 "3A" Steam Dump to Atmosphere body/bonnet repair Turbine crane hook inspection RPI and CRDM installation - Unit 3 "4S" Battery Charger inoperability - Unit 4 "3A" RHR Inservice Test - Unit 3 OSP-050.2 Turbine vibration problem - Unit 4 Unit 4 normal operations - 1009b Shift meeting Shift turnover meeting B.

C.

D.

Immediate safety problems None observed Questionable work practices None observed Area(s) for improvement 1.

During the Inservice Test of "3A" RHR pump it was noted that a support for interconnecting piping was left off and stored randomly on the floor.

Interconnecting piping for safety related equipment should be supported to ensure continued operability of the pump.

E.

Professionalism, Summary of Shift, Comments 2.

3.

Continued observations of Unit 4 turbine vibration problem show that careful methodical steps are being taken by peak and mid shift personnel to fine tune the correlation between lube and seal oil temperatures and the rise and fall of the recorded vibrations.

Unit 4 "4S" battery charger was declared inoperable which placed the unit in a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO.

Electrical Maintenance gave prompt attention to the matter.

An Inservice Test 3-OSP-50.2 was preferred on RHR pump "3A". Technical Staff personnel promptly summoned Mechanical Maintenance to the scene.

In the mean time, the nuclear operator continuously searched the pump for clues, and personnel monitored'local and Control Room indications (i.e. amperage, flow, tell tale seal

leakage, vibrations) for abnormal conditions.

All appeared normal.

bfechanical Maintenance personnel arrived on the scene and after a thorough inspection surmised the problem to be with and oscillating fiber ring. The test was continued and completed without any further problems.

Good group cooperation was responsible for immediate and prompt analysis of the problem.

However, a final resolution is still pending.

iMOli.lIDtllih7 02/06-07/88

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Page Recommendations 1.

install'missing support near the "3A" RHR pump immediately.

Completed By:

Garr A. Harris M

bseruer D:~i

,r Reviewed By:

j'.

Operations Superintendent-Nuclear

/

Date Management Review By:

PM

.n

/

ae VP Date MANAGEMENTINITIALRESPONSE le MOB.I IIII07'ea OZ/06-07/8A

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Psge To'perations Superintendent

- Nuclear Date:

02/06-07/88 From:

Deniel E. Wells M

bserver)

Shift:

p Day px Night A.

Plant evolutions observed Toured Auxiliary Building Toured Containment RCO shift turnover PSN shift turnover CRDM coil stack repair (G-5)

Turbine operator 1300 rounds B.

Immediate safety problems None C.

Questionable work practices D.

None Area(s) for improvement None Professionalism, Summary of Shift, Comments Continued good communications between and among shift players.

Tour of Auxiliary Building and Containment satisfactory.

RCO and PSN turnovers were structured and informative.

CRDM coil stack repair went very smoothly.

Due primarily to a new tool that Vern Miller has designed to pull the coil;stack.

It not only expedites IGC work, it also reduces Man Rem exposure.

1300 hour0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> turbine operator rounds were very well executed.

R'ecommendations None Completed By:

M bserver I

Reviewed By: W,.v '

//i. t i.:

Operations Superintendent-Nuclear Date:,-2

.)'e,s 5

Management Review By:

PC)

D e

( /~

ate VP ate

  • @os.i u<iini<<e 02/06-07/88

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT To:

Operations Superintendent-Nuclear Date:

02/07/88 From:

John A. D er (M

bseruer)

Shift:

Qx Day Night Plant evolutions observed Morning meeting Shift briefings Tour of Radiation Controlled areas including the Containment Building Down power of Unit 4 due to LCO (Interim T.S.)

being reached on "4" Spare Battery Charger.

Power down to 70<o 4-GOP-103 Power increase (Plant managers go ahead) 4-GOP-301 Unit 3

pressurizer level indicators back in service.

Bubble formation in progress.

"4" Spare Battery Charger back in service.

Shortly after "4" spare was put into service "3B" failed.

ERT looking into Battery Charger

problems, may be generic.

ERT determined Charger problem generic.

Unit 4 commenced power reduction at 1700.

Going to cold shutdown.

B.

C.

D.

Immediate safety problems None Questionable work practices None observed Area(s) for improvement 1.

Current Technical Specif ications 2;

Interim Technical Specifications 3.

Justif ication for Continued Operation (JCO's)

These are all one item Professionalism, Summary 'of Shift, Comments Shift turnovers and briefings continue to be detailed and thorough with feedback from attendees.

Supervisors always ask for comments from participants.

Supervisors on site approximately one hour ahead of schedule to get a good update on plant status.

Before downpower operation evolution was thoroughly explained and discussed.

RCO trainees on shift performed the power decrease.

Good interaction between the RCO trainees and the RCO.

The operators are working a lot of long hours but spirits remain. high.

The supervisors ensure that the operators with the longest hours on shift have the least stressful jobs.

Overall plant housekeeping is good.

02/07/88

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Page 2

Recommendations (Reference section D)

Much confusion exist with personnel having to make interpretations and judgements

. using current Technical Specifications, Interim Technical Specifications, and/or Justification for Continued Operations (JCO's).

This was very evident when the time ran out on the Limiting'Condition for Operation (LCO) on the "4" spare Battery Charger.

The Interim or Standard Technical Specifications need to be made part of the license as soon as possible to alleviate this confusion.

In the meantime when the plant gets into a grey area on LCO's, decisions should be made early on so the shift supervisor do not get into these stressful situations.

Completed By:

Revievred By:

Management Revievr By:

P ADer M

bseruer I

/

g I

I Operations Superintendent-Nuclear fii;y'

.i'~j i+8f ate ae Date:

02/07/88

/

/

Date:

Date MANAGEMENTINITIALRESPONSE

  • Nos,l allov'65 02/07/88

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Pug@

TQ:

Operations Superintendent-Nuclear Date:

02/08/88 From:

Garr A. Harris (M

bseruer)

Shift:

Q Day Qx Night Plant evolutions observed Unit 4 - Left stop valve closure on ramp down Unit 4 - RCS cooldown down and taking data per 4-OSP-041.7 Unit 3 - RCS Cold Shutdown to Hot Standby 3-OOP-503 Unit 3 - Rod Control Testing - OP-1604.9 Shift meeting Shift turnover Plant tour B.

Immediate safety problems None observed C.

Questionable work practices None observed D.

Area(s) for improvement None observed iMLLklIAUlilsl 02/07-08/88

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT f'use Professionalism, Summary of Shift, Comments While preceding to rampdown to hot standby conditions due to the inoperability of the "4A" battery charger, the left stop valve of the Unit 4 turbine suddenly went closed (Unknown to the operator at the time). In response the appropriate annunciatois and alarms were activated.

The trainees who were conducting the controlled shutdown were immediately replaced by senior personnel.

Immediate and concise communications between all operators and the PSN were initiated.

The PSN, in an attempt to structure the analysis, placed the RCO in charge.

The RCO promptly analyzed the problem to be due to the closure of the left stop valve.

Immediately decisions were made on the best method to preceed without worsening the problem.

Meanwhile, the remaining personnel fought rapidly sinking steam generator levels and turbine/reactor power mismatch.

With delta flux target driven low due to rods, boration and steam dump actuation it was feared that further manipulation of the left stop valve might induce a safety injection signal due to increased steam flow.

(The transient caused turbine load to drop from 480 MW to 70MW. Initially rods were in manual, thus dumps carried approximately 55% steam flow which is above their design valve.

A decision was made to open further the right stop valve.

The valve was opened and the turbine reloaded to 430 MW. The operators stabilized the plant at approximately 350 MW. Still implementing an earlier devised "game plant" the RCO ordered the ramp down to increase because of the steam/feed flow imbalance and possible worsening of the transient due to the left stop valve (Feared that valve may open and stick in position).

Turbine operators were dispatched to collect turbine control oil system data.

Minor equipment malfunctions occurred during the rapid shutdown, including the slipping of control rod J-I l.

A post shift meeting was held to summarize the transient and ensure no procedural steps and equipment malfunction were not accounted for.

The subsequent cooldown proved to be event free.

Plant is now in hot shutdown conditions.

The operators should be commended for the prompt analysis of the problem.

Strong communications and attention to detail was evident throughout the transient.

Creativity in problem solving was strong factor in mitigating the transient.

Team work and group cooperation between nuclear/turbine operators proved to be extremely beneficial.

PSN, APSN and RCO maintained firm leadership roles during the transient.

There was no doubt who was in charge.

Equipment operation was excellent during the transient.

A fine example of professionalism.

  • ILQklISO!IIP 02/078/88

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Page F.

Recommendat fons None Completed By:

server Date:

./..

ReviewedBy:', ~

/ '(

perations uperintendent-Nuclear Date: 2 /,

Management Review By:

tMOS:I mJ Ulte7%0 FINAI.PAGE ate 02/07-08/88

Jy

0-ADM-019 Management on Shift (MOS)

MOS DAILYREPORT Puss To:

Operations Superintendent

- Nuclear Date:

02/07-0S/68 From:

A.

Daniel E. Meils (M

bseruer)

Plant evolufions observed Shift:

Q Day Qx Night Unit 4 Controlled ramp down Unit 4 I.eft Turbine Stop Ualve closure Steam Generator level control Plant cooldown to below 350'F PSN turnover Shift briefing "3B" Battery Charger repair B.

Immediate safety problems None C.

Questionable work practice None Area(s) for improvement 1.

Unit 4 left turbine stop valve went shut unexpectedly.

2.

Steam Generator level control 0-15O'o power is extremely hard to maintain.

3.

¹6 (F) Gas Decay Tank is unavailable foi use during plant transients.

B.

Professionalism, Summary of Shift, Comments Communications continue, to be excellent.

The challenge of having a

turbine stop valve going shut during a controlled shutdown was handled by the on-shift operators with a great deal of professionalism and camaraderie.

Not only was the unit recovered from a greater than 400 megawatt swing, but when the unit was stablized after the event, an enthusiastic cheer of elation was shared by all the operators involved in "saving the Unit".. With the Unit stabilized a more subdued professional atmosphere was regained in order to complete the shutdown.

An excellent critique was held after the unit was off line to identify all problems encountered during this event.

iMUli:I I AUli'2/07/08/88

0-ADM-0>9 Management on Shift (MOS)

MOS DAILYREPORT Pege Recommendations 3.

Evaluate closure of Unit 4 left Turbine Stop Valve - determine and correct root cause (See D.l).

Evaluate, engineer, budget and install a

low power Steam Generator level control system (See D.2).

Restore 46 (P) Gas Decay Tank to "service available" status (See D.3).

Completed By:

Daniel E. Wells bseruer Date 02/08/88 r

Reviewed By: '.'-

Operations Superintendent-Nuclear r

Date:

Review By:

/')

/9.i" f

./,

PMN a

e

. Date MANAGEMENTINITIALRESPONSE iMOB.I Iii/07%is 02/07-08/88