ML17333A286

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Insp Rept 50-315/95-14 on 951220-960116.Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:I&C Technician Performance,Training & Quality of Procedures as Related to Calibr of Coil Relays
ML17333A286
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 01/22/1996
From: Kropp W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17333A285 List:
References
50-315-95-14, NUDOCS 9602060021
Download: ML17333A286 (15)


See also: IR 05000315/1995014

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION III

REPORT

NO.

50-315/95014

~FACI ITY

Donald C.

Cook Nuclear Generating

Plant

LICENSEE

Indiana Michigan Power

Company

Donald C.

Cook Nuclear Generating

Plant

1 Riverside Plaza

Columbus,

OH 43216

DATES

December

20,

1995 through January

16,

1996

INSPECTORS

B. L. Bartlett, Senior Resident

Inspector

D. J. Hartland,

Resident

Inspector

C. N. Orsini, Resident

Inspector

APPROVED

BY

4e

W. g; Kropp

Chief

Reactor

P ojects

Branch

3

Date

AREAS

INSPECTED

A special,

unannounced

inspection of the circumstances

surrounding the

inoperability of the Unit

1 Mest Centrifugal Charging

Pump

(CCP).

The areas

inspected primarily involved Instrumentation

and Control

(ISC) technician

performance,

training,

and the quality of procedures

as they related to the

calibration of safety-related

induction coil relays.

9b020b002i

9bOi25

.PDR

ADQCK 050003i5

8

PDR

xec tive Summ

A self-revealing

event occurred

where the licensee

subsequently

identified

that the Unit I Mest

CCP had been inoperable for 6 months.

It was identified

that

a lack of requalification training for the

I&C technicians,

a poor

procedure,

and

a poor review of as-found data contributed to this event.

In

addition, the licensee

had

an unnecessary

delay in determining the operability

and reportability of the as-found condition following the self-revealing

failure on September

12,

1995.

iI'

INSPECTION DETA

S

1.0

Summar

of

vent

On September

12,

1995, Unit I was in a refueling outage with all fuel removed

from the reactor vessel.

During the time the core was unloaded,

the licensee

performed full flow testing of the emergency

core cooling system

(ECCS).

During the full flow testing,

the West Centrifugal Charging

Pump

(CCP) tripped

on

a sensed

overcurrent after

7 minutes of full flow.

The licensee's

evaluation determined that the overcurrent relay was improperly set since the

last calibration

on March 15,

1995.

The licensee

has

two CCPs in each unit as required

by technical specification

(TS).

Each

CCP performs the dual role of CCP and of being the high-head

safety injection pump.

During normal operation,

the

CCPs

do not draw as

much

current

as when used for high-head safety injection.. During a loss-of-coolant

accident

(LOCA), reactor coolant system

(RCS) pressure

would drop, the

CCPs

discharge

flow rate would increase

and the motor amperage

drawn would

increase.

A timed overcurrent relay (I-51-TA8) was in the circuit in order to protect

the motor from harm during long term (seconds

to several

minutes) overcurrent

situations.

The relay was

a General Electric model

66 type

IAC (Induction

Disc Current sensing relay).

The greater the sensed

overcurrent,

the shorter

the time delay.

For overcurrents just slightly above the setpoint,

the relay

would normally take

a number of minutes to trip.

That the relay tripped

7

minutes into what would otherwise

be

a normal

run indicated that the setpoint

was close to the normal operating condition.

2.0

oot

C

ses

The licensee

and the inspectors

identified the following root causes for this

event:

The primary root cause

was the lack of requalification training which

lead to personnel

error on the part of the

IKC technicians.

The two

technicians

involved in the March 15,

1995, calibration

had been

properly trained in 1992.

However, the lead technician

had not

performed

any relay calibrations since this training.

The lead

technician

had calibrated the relay using

a wrong technique

as

a result

of his unfamiliarity.

The second technician

had

been qualified on this

type of relay on August 25,

1993,

and

had assisted

other lead

technicians

in the performance of this type calibration.

However,

he

did not question or closely observe

the lead technician in the

performance of this calibration.

Licensee

dent fied

The calibration procedure,

12IHP6030.IMP.014,

was written such that it

did not assist

the technicians

in the performance of their duties.

The

calibration procedure for this type of relay had remained essentially

unchanged

since it was written in the mid 1970s.

At that time,

technicians

specialized

in the calibration of relays

and

as such the

t

~r

amount of detail required in the procedure

was small.

Since then, the

licensee's

practice

was to have

any qualified I5C technician

capable of

calibrating relays.

This necessarily diluted the experience that any

one technician would gain, thus causing the procedure quality to become

inadequate.

Ins ector Identified

4

The as-found data taken

by the technicians

in the March 1995 calibration

was not identified as being erroneous.

The as-found data

showed that

the I times

(1X) overcurrent setpoint

was high, while the

3 times

(3X)

overcurrent setpoint

was low.

When the data

was reviewed following the

surveillance,

this should have

been identified as inconsistent with this

type of instrument.

Both setpoints

would either

be high or they would

both

be low, it would not be possible to have

one setpoint low and the

other setpoint high.

In addition, the

3X overcurrent

was by itself so low that it should

have

been identified as warranting further attention.

Using the calibration

curves of the relay, it was possible to identify during the event

assessment

that if the

3X overcurrent data

was correct, that the

pump

would have tripped

on sensed

overcurrent during normal operation.

ice see

dentif'ed

3.0

i e see

rr c 've

ct ons

~

Relay I-51-TAB was recalibrated

and returned to service..

~

The two IKC technicians

involved had their relay qualifications voided

and were to be requalified

on the calibration of IAC relays.

~

Periodic requalification for technicians

was added to the licensee's

training program.

The training program was to continue to assess

the

need for additional training.

~

The calibration procedure

was enhanced

by increasing

the level of detail

in the procedure.

~

All relays monitoring safety related motors that had not been tested

by

other surveillances

have

been

checked to verify their calibration.

The

licensee

stated that only one other relay was identified as being out of

calibration.

The Unit I West containment

spray

pump was identified as

being low, but was assessed

as still operable.

~

Until all technicians

were re-trained,

only those technicians that were

tested

using

bench devices

would be allowed to calibrate

IAC relays.

4.0

Ins ecto

se

s

e t o

icens

e Action

4.1

Review of As-found Data

One of the root causes

identified by the licensee

was that the review of

as-found data in Harch of 1995 should

have identified that calibration

~

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g

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4.2

technique

used to obtain the data

was incorrect.

However none of the

licensee's

corrective actions stated

in Licensee

Event Report 315/95-011

Revision 0,

addressed

this failure.

C

b ti

oce

ev

o

The calibration procedure

was revised

by the licensee

as stated in their

LER.

This revision was initially weak in that it failed to use the

same

terminology that was in the

18C technicians training program (for

example it did not use "just flicker").

Subsequently,

the licensee

revised the procedure to supply additional information.

This additional

information did supply the

IKC technicians with sufficient detail

and

also

added other enhancements.

As such,

the inspectors

concerns

were

resolved.

4.3

Time iness f

ve t Assessme t

4,4

The inspectors

determined that the licensee

promptly assessed

the trip

of the Unit

1 Mest

CCP following the failure to run on September

12,

1995.

The onsite efforts to identify the root cause

and its

implications were excellent.

Timeliness

o

0 er bilit

Re ortabilit

On September

22,

1995, site personnel

requested

the assistance

of

corporate

engineering

in assessing

the operability of the

CCP with the

relay set too low. It took corporate engineering until November 20,

1995, to respond.

It appeared

that corporate engineering failed to

place the appropriate priority on this response.

In addition,

once

corporate

engineering

made the determination of inoperability, corporate

licensing did not realize that

a high head safety 'injection pump being

inoperable for 6 months would be reportable to the

NRC.

These

two

factors combined,

added

up to an unnecessary

delay in reporting of about

2 months.

4.5

Perfo mance of the Technici

ns

During the performance of the surveillance

on March 15,

1995, the

technicians failed to question the as-found data which would have

shown

that his technique

was incorrect.

In addition, the second

I&C

technician,

who had

been trained

more recently than the lead technician,

did not observe

in detail or question the lead technician.

The

questioning

by the second technician did not occur even though

he

observed different lead technicians

performing the calibration using

different techniques.

5.0

Potential

Vio

tions

The following potential violations were identified:

Technical Specification 3.5.2 requires,

in part,

"Two independent

ECCS

subsystems

shall

be

OPERABLE with each

subsystem

comprised of:

a.

One

OPERABLE centrifugal charging pump,...."

The applicability of this

TS is Modes

1, 2,

and 3.

Action a. States,

"With one

ECCS subsystem

inoperable,

restore the

inoperable

subsystem

to OPERABLE within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in HOT SHUTDOWN

within the next

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />."

b.

Contrary to the above,

from 4:31 a.m.

on March 15,

1995, until

11: 17 a.m.

on July 30,

1995, the Unit

1 West (Train B) centrifugal

charging

pump was inoperable

due to

a mis-calibrated overcurrent

relay and the unit was not placed in hot shutdown.

Technical Specification 3.0.3 requires,

in part,

"When

a Limiting

Condition for Operation is not met, except

as provided in the associated

ACTION requirements,

within, one hour action shall

be initiated to place

the unit in a

MODE in which the Specification

does not apply by placing

it, as applicable,

in:

1.

At least

HOT STANDBY within the next

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,

2.

At least

HOT SHUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,

and

3.

At least

COLD SHUTDOWN within the subsequent

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />."

Contrary to the above,

both

CCPs were inoperable

which is

a condition

not covered

by TS 3.5.2

and the unit was not placed in hot shutdown:

~

On July 10,

1995,

from 1:00 a.m. until 2:50 a.m.

on July 12, the

Emergency Diesel Generator Train "A," the emergency

power source

for the East

CCP,

was out of service while in Mode l.

~

On July 19,

1995, for 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br />

and 35 minutes the East

CCP was

removed

from service while in Mode 3.

C.

10 CFR 50, Appendix 8, Criterion V, states

that activities affecting

quality shall

be prescribed

by documented

procedures

of a type

appropriate to the circumstances.

Contrary to the above, calibration procedure,

12IHP6030. IMP.014,

was not

appropriate for calibrating

a

GE model

66 type

IAC (Induction Disc

Current sensing)

relay.

This procedure

was originally written for

technicians

that specialized

in the calibration of relays

and had not

been

changed

since the mid-1970s.

The licensee's

practice for

calibrating relays

changed

to allow less specialized

18C technicians

to

calibrate relays.

However, the procedure

was not revised to contain

6.0

sufficient detail for this reduction in technician proficiency to ensure

proper calibration of the

GE model

66 type

IAC relay.

Sa et

Si

e

6.0

The inoperability of the Unit

1 West

CCP for 6 months

was considered

significant in that

an

ECCS component

was incapable of performing its

intended safety function assuming

a single failure.

In addition, there

was at least

one period in which no

CCP was capable of acting

as

a high

head safety injection pump.

Han

ement

eb

efin

7.0

The inspectors

met with licensee

representatives

(denoted in

Section 7.0) after the inspection

on January

16,

1996, to discuss

the

scope

and findings of the inspection.

During the exit meeting,

the

inspectors

discussed

the likely informational content of the inspection

report

and documents

or processes

reviewed

by the inspectors

during the

inspection.

Licensee representatives

did not identify any such

documents

or processes

as proprietary.

Pe

so

s

o t

censee

e sonnel

  • A. A. Blind, Site Vice President
  • J. R. Sampson,

Plant Manager

  • K. R. Baker, Assistant

Plant Manager-Production

  • H. E. Barfelz, Superintendent,

Nuclear Safety 5 Analysis

~J.

D. Allard, Maintenance

Superintendent

  • H. Depuydt,

Licensing Activity Coordinator

  • D. Walker, Haintenance

Procedures

'C.

Miles, Maintenance

Supervisor,

Instrumentation

8 Controls

+A. Lotfi, Supervisor,

Site Design

  • G. Gurnow, Plant Engineering,

Maintenance

ISC

  • E. Morris, Plant Performance

Assurance

Supervisor

  • D. Willeman, Training
  • J. Sankey,

Plant Engineering

  • B. Nichols, Acting Operations

Superintendent

  • T. Walsh,

General

Supervisor - Support

  • P. McCarty, Procedure

Supervisor - Maintenance

U.S. Nuclear

Re ulator

Commission

NRC

  • D. Hartland
  • C. Orsini
  • B. Bartlett
  • B. Fulle}
  • Denotes those present

during the exit meeting

on January

16,

1996.

January

25,

1996

EA 96-020

Mr. E.

E. Fitzpatrick

Senior Vice President

Nuclear Generation

Indiana Michigan Power

Company

1 Riverside Plaza

Columbus,

OH

43216

SUBJECT:

NRC SPECIAL INSPECTION

REPORT

NO. 50-315/95014(DRP)

Dear Mr. Fitzpatrick:

This refers to the special

safety inspection

conducted

by Messrs.

B. Bartlett,

D. Hartland,

and

C. Orsini of this office from December, 20,

1995,

through

January

16,

1996.

The inspection

included

a review of activities at your

Donald C.

Cook Nuclear Plant, Units

1 and 2.

At the conclusion of the

inspection,

the findings were discussed

with those

members of your staff

identified in the enclosed report.

Areas

examined during the inspection

are identified in the report.

The

inspectors

reviewed the circumstances

surrounding the inoperability of the

Unit

1 Mest Centrifugal Charging

Pump

(CCP).

Mithin these

areas,

the

inspection consisted of a selective

examination of procedures

and

representative

records,

observations,

and interviews with personnel.

Based

on the results of this inspection,

three apparent violations (Section

5.0) were identified and are being considered for escalated

enforcement action

in accordance

with the "General

Statement of Policy and Procedure for NRC

Enforcement Actions" (Enforcement Policy),

NUREG-1600.

The apparent

violations involved a personnel

error and procedural

weakness

that left one

CCP unable to meet its technical specification

(TS) requirement for

operability from March 15,

1995 to September

13,

1995.

The circumstances

surrounding

these

apparent violations, the significance of the issues,

and the

need for lasting

and effective corrective action were discussed

with members

of your staff at the inspection exit meeting

on January

16,

1995.

As

a

result, it may not be necessary

to conduct

a predecisional

enforcement

conference

in order to enable the

NRC to make

an enforcement decision.

However,

a Notice of Violation is not presently being issued for these

inspection findings.

Before the

NRC makes its enforcement decision,

we are

providing you an opportunity to either

(1) respond to the apparent violations

addressed

in this inspection report or (2) request

a predecisional

enforcement

conference.

If you choose to provide

a response,

your response

should

be submitted within

30 days of this letter

and

be clearly marked

as

a "Response

to Apparent

Violations in Inspection

Report

No. 50-315/95014(DRP)"

and should include for

each apparent violation:

(1) the reason for the apparent violation, or, if

E.

E. Fitzpatrick

contested,

the basis for disputing the apparent violation, (2) the corrective

steps that have

been t >ken and the results

achieved,

(3) the corrective steps

that will be taken to avoid further violations,

and (4) the date

when full

compliance will be achieved.

In addition,

we request your response

address:

(1) the potential of other maintenance activities being conducted

using

technicians

who have not maintained proficiency by requalification training or

on the job performance of specialized

procedures;

and (2) the factors

contributing to the delay in determining operability and reportability of the

Unit

1 West

CCP following the event.

Your response

should

be submitted

under

oath or affirmation and

may reference

or include previous docketed

correspondence, if the correspondence

adequately

addresses

the required

response.

If an adequate

response

is not received within the time specified

or an extension of time has not been granted

by the

NRC, the

NRC will proceed

with its enforcement decision or schedule

a predecisional,enforcement

conference.

If you choose

not to provide

a response

and would prefer participating in a

predecisional

enforcement

conference,

please

contact Hr. Wayne Kropp at (708)

829-9633 within 15 days of the date of this letter.

In addition,

please

be advised that the number

and characterization

of

apparent violations described

in the enclosed

inspection report

may change

as

a result of further

NRC review.

You will be advised

by separate

correspondence

of the results of our deliberations

on this matter.

In accordance

with 10 CFR 2.790 of the NRC's "Rules of Practice,"

a copy of

this letter, its enclosure(s),

and your response (if you choose to provide

one) will be placed in the

NRC Public Document

Room (PDR).

To the extent

possible,

your response

should not include

any personal

privacy, proprietary,

or safeguards

information so that it can

be placed in the

PDR without

redaction.

The responses

to the apparent violations described

in the enclosed

inspection

report are not subject to the clearance

procedures

of the Office of Management

and Budget

as required

by the Paperwork Reduction Act of 1980,

Pub.

L.

No.96-511.

Sincerely,

Docket No.

50-315

License

No.

DPR-58

/s/William L. Axelson

W. L. Axelson, Director

Division of Reactor Projects

Enclosure:

Inspection

Report

No. 50-315/95014(DRP)

See Attached Distribution

I

E.

E. Fitzpatrick

Distribution:

cc w/encl:

A. A. Blind, Site Vice President

John

Sampson,

Plant Hanager

James

R. Padgett,

Hichigan Public

Service

Commission

Hichigan Department of

Public Health

Distribution:

Docket File w/encl

PUBLIC IE-01 w/encl

OC/LFDCB w/encl

SRI D. C. Cook w/encl

RHB/FEES w/o encl

DRP w/encl

RIII'RR w/encl

D. C. Cook,

PH,

NRR w/encl

IPAS (E-Hail) w/encl

J.

Lieberman,

OE

J. Goldberg,

OGC

R. Zimmerman,

NRR

Document:

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