ML17333A100

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Augmentated Insp Team Insp Rept 50-458/89-20 on 890421-24. Major Areas inspected:890419 Freeze Seal Failure on 6-inch Svc Water Line,Review of Operator Response to Event & Licensee Plans for Recovery
ML17333A100
Person / Time
Site: River Bend 
Issue date: 05/16/1989
From: Callan L, Constable G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17333A101 List:
References
50-458-89-20, NUDOCS 8905220106
Download: ML17333A100 (22)


See also: IR 05000458/1989020

Text

APPENDIX

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

AUGMENTED INSPECTION TEAM

NRC Inspection Report:

50-458/89-20

Docket:

50-458

Licensee:

Gulf States Utilities (GSU)

P.O.

Box 220

St. Francisville, Louisiana

70775

Facility Name:

River Bend Station

(RBS)

Inspection At:

RBS, St. Francisville, Louisiana

Inspection Conducted:, April 21-24,

1989

Operating License:

NPF-47

Team Members:

H." F. Bundy, Reactor Inspector,

RIV

D.

R. Lasher, Electrical Engineer,

NRR

W. F. Smith, Senior Resident

Inspector,

RIV

C.

D. Sellers, Materials Engineer,

NRR

Assisting

Personnel:

E. Ford, Senior Resident

Inspector

W. Paulson,

Project Manager,

NRR

Team Leader:

onsta

e,

ie,

eactor

rogects

Section

C, Division of Reactor Projects

te

Approved:

L. J.

an, Director, Division o

Reactor

Pro ects

Da e

ppgSg2(>10/>

890516

PVP

ALeCK O.'=0004

8

9

PDC

'I

0

0

OETAILS

1.0

Persons

Contacted

2.0

J.

E. Booker, Manager,

River Bend Oversight

J.

L. Burton, Supervisor,

Independent

Safety Engineering

Group

J.

W. Cook,

Lead Environmental Analyst, Nuclear Licensing

T.

C. Grouse,

Manager, Quality Assurance

(QA)

R. T. Davey, Senior Enginee~,

Design Engineering

J.

C. Deddens,

Senior Vice President,

River Bend Nuclear Group

D.

R. Derbonne, Assistant Plant Manager,

Maintenance

L. A. England, Director, Nuclear Licensing

R.

G. Finkenaur, Electrical Engineer

A. 0. Fredieu, Supervisor,

Operations

P.

E. Freehill, Outage

Manager

J.

R. Hamilton, Director, Design Engineering

D. 0. Hartz,

Duty- Operations

Supervisor

G.

K. Henry, Director,

QA Operations

R. J. King, Supervisor,

Nuclear Licensing

, J.

D. Mullen, Mechanical

Maintenance

Foreman

T. F. Plunkett, Plant Manager

A. Soni, Supervisor,

Environmental Qualification and Specification

K. E. Suhrke,

Manager, Project

Management

R. J.

Vachon, Senior Compliance Analyst

J.

Venable, Assistant Operations

Supervisor

D. Zemel, Mechanical

Maintenance

Supervisor

The

NRC inspectors

also interviewed additional

licensee

personnel

during

the inspection.

General

2.1

Descri tion of Event

At about

11:45 p.m.

on April 19,

1989,

a freeze

seal failed on

a 6-inch

service water line.

The freeze

seal

had

been established

to allow

inspection

and repair work on manual isolation valves to

a safety-related

auxiliary building cooler.

The bonnet of the manually operated

valve was

off the valve and the service water system

was in operation at the time of,

the event.

The failure of the freeze

seal

resulted in flooding portions of

the auxiliary building. Approximately 15,000 ga'lions of service water was

discharged

through the disassembled

valve covering portions of the 141-foot

level of the auxiliary building with water.

A portion of the water flowed

through holes in the floor under safety-related

480 Yac motor control

centers

(MCCs) onto nonsafety-related

cabinets

on the 114-foot level

containing disconnect

links and

a 13.8 kY/480 Vac transformer.

The

cabinets

were not designed to shed the water leading to an electrical

fireball that damaged

the cabinet

and components.

A 13.8

kV supply breaker

opened

aeenergizing

that cabinet

and two others

causing the loss of the

0

operating residual

heat

removal

(RHR) system,

normal spent fuel cooling,

and normal lighting in the auxiliary building, control building, and the

reactorbuilding.

The operators

isolated the service water system in

15 minutes

and restarted

RHR in 17 minutes.

No increase. in reactor

temperature

was observed.

Backup spent fuel cooling (service water) was

available but was not immediately needed.

Temperature

in the spent fuel

pool rose to 123'F at which time normal cooling water was restored

and

temperature

was returned to normal.

The

NRC AIT arrived on site on April 21, 1989.

Prior to that time, the

NRC

senior resident inspector

(SRI) monitored the licensee's

preliminary

response

to the event.

The AIT was composed of a materials engineer,

an

electrical engineer,

an SRI,

a Region

IV inspector,

a team leader assisted

by the

NRR Project Manager,

and the

NRC resident inspectors

stationed at

River Bend.

The AIT reviewed the event,

inspected

the affected

equipment

and

interviewed various managers,

operators,

engineers,

and technicians

involved.

2.2

AIT Tasks

Region IV, in consultation with NRR, formed an AIT on April 20,

1989.

The

AIT tasks

were specified in a charter letter to ter.

G. L. Constable

from

Nr. L. J. Callan.

These tasks

were:

2.2.1

2.2.2

2.2.3

Perform

a thorough review of the sequence

of events

leading to and

recovery from the event.

Review the operator

response

to the event.

Review the licensee's

use

and control of freeze. seals

including

contingency

measures.

2.2.4

Pcview electrical

system vulnerability and response

to this event.

2.2.5

Review the licensee's

plans for recovery including restoration

from

switchgear water damage.

2.2.6

Review licensee's

management

control of outage activities with regard

to this event, including any potential tie with previous

outage-related

problems.

3Jl

~At 7 I

3.1

Se uence of Events

The following sequence

of events

was established

by the

NRC inspectors's

a

result of review of the control

room (CR) log and interviews with licensee

personnel.

Note;

All times are best estimate,

Central Daylight Time.

A ril 18,

1989

-12 midnight

~Ail 19,

1999

6 a.m.

9 a.m.

6 p.m.

11:48 p.m.

The maintenance

foreman briefed operations

personnel

on

installation of freeze seals to allow repair work on Standby

Service Water Isolation Valves

1SWP*525 and

1SWP*524 for

Auxiliary Building Unit Cooler HVR*UC11B.

Installation of freeze seals

was in progress.

Night shift

provided turnover to day shift.

Freeze

seals

were declared

established

and verified by

opening unit cooler vent and drain valves.

Work began

on

valve repairs.

Work was turned over to night shift.

The failure of the unit cooler inlet line freeze

seal

was

detected

by a maintenance

mechanic,

assigned

duty as the

freeze

seal

watch,

who heard

a loud noise

and observed

the

flow of service water from the open

body of the inlet

isolation valve.

11:50 p,m.

The control operating

foremen

(COF) in the control

room (CR)

received

a telephone call advising him that there

was

leakage

past

a freeze

seal in the auxiliary building (AB)

on the 141-foot elevation.

11:51

p.m.

11:52 p.m.

11:53 p.m.

11:54 p.m.

The

COF instructed the

AB senior nuclear equipment

operator

(SNEO) to assess

the severity of the leakage

and

report damage.

The

AB SNEO arrived at the 114-foot elevation of the east

side of the

AB and observed water on the floor.

He

irmediately went through the tunnel

on the 123-foot

elevation to the west side

and observed water falling from

the overhead.

He then proceeded

to the 141-foot elevation.

The

AB SNEO arrived at the

AB 141-foot elevation

and

observed water flowing across

the floor.

AA column of water

approximately

6 feet high was observed

flowing out of the

open bonnet of a valve near

AB Unit Cooler HVR*UC11A or B,

which are adjacent to each other.

(It turned out to be the

inlet isolation valve for Unit Cooler HVR"UCllB.)

He

assisted

maintenance

personnel,

who were trying to install

the bonnet

on the open valve body.

A nuclear control operator

(NCO) received

an emergency call

from a firewatch at the

AB 141-foot elevation regarding

the

lt

ll:55 p.m.

ll:56 p.m.

11:58 p.m.

ll:59 p.m.

A ril 20,

1989

12 midni ght

flooding and notified the

COF.

At the COF's direction, the

NCOs attempted to contact the

AB operator,

who did not

respond.

The

NCOs noted that all AB safety-related

sump

pumps were

operating in the crescent

area.

Also, an alarm

(H13P808)

was received indicating

a ground fault condition on

1 of

20 nonsafety-related

load distribution centers

(LDCs).

The

NCO initiated actions to identify the

LDC which was

grounded

and obtain additional

SNEOs to assist in the

AB

while the

COF briefed the shift supervisor

(SS)

on the

recent events.

The

COF informed the

SS that he thought the

leak was

on

a Division II standby service water

(SSW) line

to an

AB unit cooler, but that

he was not certain with

regard to the division.

Alarms and other indications received in the

CR indicated

the following:

A partial loss of CR AC lighting occurred.

Backup

DC

lighting was energized.

Reactor Protection

System

(RPS)

B normal motor

generator

(MG) set power was lost.

Division II containment isolation valves closed

as

a

result of the loss of power.

Residual

heat

removal

(RHR), which was operating in the

shutdown cooling. mode,

was lost as expected

when the

containment isolation valves closed.

Operators

entered

Abnormal Operating

Procedure

(AOP)-0010 to

respond to loss of RPS

B power by transferring this bus to

the alternate

source.

From

CR indications, the

NCOs

determined that the most probable

cause of the power-related

events

was

a trip of Breaker

NPSACB016, which at the time

was the sole feeder to LDCs 1A, 1B, IC, 1D, 1S,

and

1T.

An

NCO was dispatched

to the normal switchgear

(NSG) building

to check relay targets

on NPSACB016.

The

NCO at the

NSG building reported that all phases

on

Breaker

NPSACB016

showed instantaneous

over current.

The

AB SNEO called the

CR to report the power failure and was

asked to confirm that the leak was

on Division II SSW

piping.

The

AB SNEO reported that line tracing would be

required to confirm the division.

12:Ol a.m.

12:03 a.m.

12:04 a.m.

12:05 a.m.

The

COF received

a report from the scene that

smoke

was

emanating

from electrical

equipment in the

AB at the

114-foot level, elevation west.

The fire brigade leader

was

dispatched

to assess

the situation.

The

AB SNEO called back

to report that he thought the leak was from SSW Division II

piping, but that he could not be absolutely

sure without

tracing the line further.

The

COF dispatched

additional operators

to the

AB to confirm

the source of the leak.

The fire brigade leader called the

CR to report that Transformer

1NJS-LDC lA was not on fire,

but that cover plates

were buckled outward and

smoke was

still coming from the disconnect cubicle.

He reported that

the fire brigade would not be needed

because

the switchgear

was deenergized

and that he would proceed to the 141-foot

elevation to assist in controlling the water leak.

The

SS and

COF discussed

options for removing

SSW systems

from service

and other event information.

The

NCO verified

all isolations

occurred in accordance

with design

requirements

and restored

systems

to meet operational

requirements.

The

SS and

COF decided to isolate

and

remove Division II of

the

SSW system from service without positive confirmation of

the leak source.

12:06 a.m.

The

NCO isolated

the Division II SSW system in accordance

v ith the COF's directions.

12:08 a.m.

The

COF received reports from AB that th'e leakage

was

diminishing and that the bonnet

on the leaking

SSW valve was

nearly in place.

12:15 a.m.

The

RHR shutdown cooling was restored

by placing the

Division I

RHR System back in service.

1:50 a.m.

The water level in the

AB crescent

area

dropped to less than

floor level

as

a result of all four sump

pumps

running

continuously.

A ril 21,

1989

6:03 a.m.

Restored

power to component cooling water

(CCW)

pumps

and

reestablished

cooling water to spent fuel cooling heat

exchangers.

(Haximum temperature

in the spent fuel'ool was

123'F at this time.)

The delay in restoring

power to the

CCW pumps

was because all three

pumps received

power from

the

damaged

13.8

kV load center.

-7-

Review of 0 erator

Res

onse to the Event

On April 21 and 22, 1989, the team reviewed documentation

provided by the

licensee

and conducted

interviews with operations

personnel directly

involved with the loss of freeze

seal incident.

The interviews included,

among others,

the Senior Nuclear Equipment Operator

(SNEO); the Nuclear

Control Operator

(NCO), who was

a licensed

Reactor Operator;

the Control

Operating

Foreman

(COF), who was

a licensed

Senior Reactor Operator;

and

the Assistant

Operations

Supervisor.

The Shift Supervisor

(SS)

who had the

watch during the incident was unavailable for an interview (absent

due to

illness in family).

The team was able to obtain

a good insight as to the

operators'esponses

and the circumstances

to which they were subjected

while being called upon to act.

In the interest of brevity and clarity, the information provided in this

section of the report was expressed

as fact or observations

of the team

members;

however,

much of the information was based

on the viewpoint of

licensee

personnel

being interviewed and,

as such,

was not observed

directly by the team.

The first indication that

a problem existed

was at approximately

11:50 p.m.

on April 19, 1989.

The

NCO had received

several calls, from all of 'the

levels below the Auxiliary Building (AB) 141-foot elevation in the

Auxiliary Building (AB), reporting the presence

of water coming from the

overhead.

At the

same time, the

COF, who was in the back of the control

room, received

a call from the individual attending the freeze

seals

on

the 6-inch standby service water lines

on the

AB 141-foot elevation.

The

indivioual stated,

in a calm, matter-of-fact fashion, that

a freeze

seal

was leaking.

I(e did not identify the lines, nor did it appear that there

was

any need for emergency action.

Therefore, at the outset,

there

was

no

sense of urgency to the problem.

The

COF was in the back of the control

room because

he was also fulfilling

the du'ties of, the administrative

COF in his absence.

Normally, for the

refueling outage,

the licensee

assigned

four senior reactor operators

on

shift.

In addition to the shift supervisor

and the

COF,

a second

COF was

provided to perform administrative tasks,

such

as review of clearances.

A

duty operations

supervisor

was also provided to oversee

operations

department activity.

During this event, the administrative

COF was not

available

on shift.

At approximately

11:51 p.m., the

COF dispatched

an

SNEO to the

AB to

investigate.

It was not yet evident in the control

room what was

happening.

Upon arrival at the east

AB 114-foot elevation,

which is physically

separated

from the west side, the

SNEO found water on the floor.

He then

went back through the passageway

and proceeded

to the west

AB 114-foot

elevation where

he found water falling from the overhead,

particularly in

the vicinity of the 13.8 kV/480V load aistribution center

(LDC).

By

11:53 p.m., the

SNEO arrived at the leak site

on the

AB 141-foot elevation

and found the tlaintenance

Foreman

and

a mechanic struggling to install the

bonnet

on

a valve.

The floor was flooded with 2 to 3 inches of water and

a

6-foot high column of water was flowing from the valve body.

The

SNEO,

immediately climbed up the scaffo1d to assist without first informing the

control

room of his findings.

At approximately ll:54 p.m., the control

room received

a call

on the

emergency

channel of the plant paging system (Gaitronics) from a fire

watch on the

AB 141-foot elevation informing them that flooding existed.

Attempts to contact the

SNEO that had been dispatched

were unsuccessful.

He did not hear the calls.

For approximately the next

5 minutes,

a number of electrical

problems

occurred,

as evidenced

by telephone calls

and control

room annunciators

(among the multitude of those already lighted due to 'the refueling outage),

but none provided any good clues

as to where the flooding was coming from.

A ground fault alarm was received indicating

a problem on

1 of 20 possible

nonsafety-related

LDCs.

Lighting went out in the AB, reactor building,

and control building.

The reactor protection

system

(RPS)

B motor generator

output was lost,

a number of containment isolation motor operated

valves

closed,

and shutdown cooling was lost.

Reactor Plant

Component

Cooling

Pump

B lost power, which resulted in a loss of the heat sink for spent fuel

pool cooling.

At this point, discussions

continued

between

the

NCO,

COF, and

SS

to evaluate

the problem and

come

up with actions to recover from

the electrical

losses

and stop the flooding.

By process of elimination,

the

SSW system

was the only viable source of flooding.

Shutdown cooling

was

on Division I, and since it was not yet known which division of SSW was

leaking, they determined that Division II should

be secured first.

Abnormal Operating

Procedure

AOP-0010,

"Loss of One

RPS Bus," was entered

to recover from the loss of

RPS

8 power so that the isolations

could be

cleared

and shutdown cooling restored.

The operators

monitored reactor

temperature,

which did not change appreciably.

During the next

5 minutes, confirmation was received that there

was

no fire

at the

LDC, but it was visually damaged.

An operator at the

AB 141-foot

elevation reported that he thought the

SSW leak was from Division II but

could.not

be sure without tracing the line further.

Meanwhile, the control

room

w

NCO was restoring isolated

systems that .were needed for safety.

Spent

f

1

1 temperatures

were being monitored,

and

no rise was seen.

The

ue

poo

to the

t rs considered

the alternative of supplying

SSW directly

component cooling side of the fuel pool coolers,

but chose

not to until

necessary,

due to chemistry considerations.

At 12:06 a.m., the

NCO isolated the Division II SSW loop and secured

the

pumps

as instructed

by the

COF, although it had not been confirmed that

Division II was the source.

Preparations

were being

made to isolate

and

secure Division I if required,

but reports

came to the control

room from

the

AB that leakage

was diminishing.

It was

now possible to finish

installing the valve bonnet,

which had been unachievable until

SSW flow

through the valve body, was reduced.

Normal shutdown cooling was restored within 17 minutes following the loss

of the

RPS

B bus.

The team considered that to be excellent time for

restoration of shutdown cooling, under the circumstances.

Considering the

large volume of water in the reactor vessel

due to refueling activities,

the negligible temperature

rise,

and extended

shutdown time, the 17-minute

interruption

appeared

to be of minor safety significance.

Technical

Specifications

allow RHR to be stopped for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> in an 8-hour period

under the circumstances

that existed at the time of the event.

The team concluded that operator response

to the event

was adequate,

but

might have

been

more timely had the following weaknesses

not existed:

Operations

apparently

considered

freeze

seals to be comparable to a

closed valve and were insensitive to the potential for failure because

of human error,'nd to the possible

consequences.

As a result, there

was

no special visibility given to freeze

seal

status for control

room

operators

through logs or contingency plans that might be needed

in

the event of failure.

Nor did turnover, verbal or written,

seem to

address

the freeze

seals that were installed

on

SSW Division II.

NEOs and

SNEOs apparently

v ere not adequately trained to ensure

the

control

room was informed of the exact nature of a casualty before

becoming involved in the recovery.

At the time of the. event, the watch section

was short

one

COF than

had

been normally provided for this refueling outage.

This placed

additional

burdens

on the remaining

COF in dealing with the event.

CHP-9186,

Revision 4, "Freeze Seal,"

Precaution

7.3

NOTE states

that

the freeze

seal

should

be tagged

as

a system boundary

as if it were

'any other type of isolation.

This was not done for the

SSW freeze

seals.'f this note

had

been

complied with, the level of awareness

on

the part of the control

room might have

been greater.

3.3

Control

and use of Freeze

Seals

Freeze

seals or ice plugs are routinely used in nuclear reactor fluid and

t systems

to drain or isolate

components

which for various

reasons

cannot

be conveniently valved out.

Basically,

a freeze

seal is produce

y

d b

chilling the outside of the pipe, usually with liquid nitrogen supplied to

a jacket surrounding

the pipe.

Eventually, the water at the inner surface

of the chilled pipe freezes

and the ice/water interface

grows towards the

center of the pipe and also along its axis.

Obviously, the above

description is rather oversimplified and there. exists certain

problem areas

about which care must

be taken,

both for the establishment

of an effective

freeze

seal

and the assurance

that the freeze

seal will be adequately

maintained for the expected

duration of the repair.

It is essential,

-10-

therefore, that written procedures

be established

and that the procedures

be followed.

It also is obvious that adequate

training in the exercise of

the procedure

be provided.

At River Bend, freeze seals

are produced

by both outside contractor

personnel

and plant maintenance

personnel.

Each organization

has its own

freeze seal

procedure.

The River Bend procedure,

Corrective Maintenance

Procedure

CNP 9186, "Freeze Seal" Revision 4, dated

November 8, 1988,

permits

a freeze

seal contractor to use his own procedure.

Indeed,

much

of the in-house

knowledge

on freeze

seal

production

was gleaned

from

observation of the freeze

seal contractor during the first refueling

outage.

A memo from operations

gA to the gA manager

dated April 21, 1989,

"Review

of Freeze

Technology Inc.," states that freeze

seal contractor personnel

are all trained by the

company

owner on an on-the-job type of training.

There was

no formal training or qualified personnel list for River Bend

maintenance

personnel.

The procedures

have

some notable differences.

The freeze

seal contractor,

Freeze

Technology International Inc., "Freeze

Plug Procedures,"

dated

September

15,

1987, requires installation of a temperature

measuring

.device into a sleeve in the chamber.

The River Bend procedure is

ambiguous in that it states

a resistor temperature

sensor

probe

be taped

to the pipe,surface,

but shows

a sketch with a thermocouple

protruding

from the chamber.

The freeze

seal contractor requires

recording of

temperature

every

5 minutes during establishment

of the freeze plug and

every

15 minutes while the plug is being held.

The freeze

seal

contractor

utilizes

a manifolded boot and controls flow by having liquid nitrogen

dropping from a vent, whereas

the River Bend procedure

vents

gaseous

nitrogen.

In addition to temperature

measurement,

there are other

indications of freeze

seal conditions.

These are frosting of the pipe at

each

end of the boot and observation of water flow downstream

from the

freeze seal.

The freeze

seal contractor prohibits multiple seals

from a single nitrogen

bottle, but no such prohibition was stated in the River Bend procedure.

Other than

NDE of the pipe area in the vicinity of the freeze

seal prior to

placement of the freeze

seal

boot,

no other gC/gA involvement was required

by either procedure.

There

was

a gA review of the maintenance

work

package,

but no in-process

inspection

by gC was required.

In the incident of April 19, 1989, there were

no temperature

measuring

devices

used to monitor temperature.

Additionally, two freeze

seals

were

produced

from the

same nitrogen bottle.

Nitrogen flow was controlled by

observation of the plume at the vent,

and

some valve manipulation

was

required to produce

equal

plumes from both vents

and to maintain roughly

uniform plume size for the duration of the freeze.

Temperature

indication

was estimated

by the axial length of

rosting

on the pipe on either end of the

boot.

Because frost is more readily initiated or maintained

on empty pipe

-11-

than

one full of water, the more visible outlet ends of the freeze might

not have given any indication of loss of freeze.

This is speculative,

as the maintenance

individual on duty at the time the seal

was lost

stated that he did move around for observation of the frost from other

locations.

Following the loss of freeze

seal

event,

a revised maintenance

work

order

(NWO) package

was prepared to produce

seals in the

same lines but at

different locations.

The

new location chosen

was further away from the

valves (i.e., further upstream

on the inlet and further downstream

on the

outlet).

This was

done to permit a borescope

examination of the site of

the previous plugs.

Additionally, there were other changes.

These were:

1) the seals

would be produced

on a vertical run of pipe rather than

horizontal; 2) there would be

no flow in the line; and 3)

a freeze

seal

contractor,

Freeze

Technology International

Inc. (FTI), would produce the

, actual

seals.

FTI selected

the sites

and marked the area to be used.

The

paint was

removed from the marked area to permit a surface

examination of

the freeze

seal location.

The

gC inspector

performed

a magnetic particle

(dry) examination.

Six linear indications were found.

All were spirally

aligned at approximately

30 degrees

from the axis.

Two were

on the inlet

pipe and were tandem about

1 inch and 1/2 inch long with about 1/2 inch

between.

The other four were parallel

and

one was estimated

at 8 inches.

Because of the linear indications, the package

had to be modified to

require grinding out of the indications

and to require ultrasonic wall

thickness

measurements.

Light flapper wheel grinding failed to remove all

of the indications.

Ultrasonic wall thickness

measurements

were required

by the modified

NWO package to precede additional grinding so wall

thickness

measurements

were made.

Random spot measurement,

including the

ground areas,

showed

some locations with a wall thickness of less

than

.220 inch in several

locations.

Ninimum required wall thickness

was

.245 inch.

An engineering

analysis

and more maintenance

work package

modifications would be required prior to resumption of the work.

Observation-of the freeze

seal

work by the

NRC AIT member

was terminated at

this point.

3.4

Electrical

S stem Yulnerabilit

and

Res

onse

The team assignment

in this area

was to review the vulnerability of the

plant electrical

system to this type of event

and to review the manner in

which the electrical

system

responded

to this particular event.

During this inspection,

the team reviewed the available information on the

event

and its consequences

including the sequence

of events,

documents,

control

room logs, relevant procedures,

event description,

event location,

and drawings of affected

systems

ana equipment.

The team also inspected

the location of the event

and surrounding areas.

The team's specific work

activities included:

inspection of the damaged

13.8

kV load center;

-12-

verification of the path by which floodwater from the leak reached

the

damaged

load center;

reconstruction

and validation of the electrical portion of the event,

including the route by which the loss of the 13.8

kV bus caused

loss

of RPS

Bus

B and subsequent

closure of Division II Containment

Isolation Valves;

review for existence of potential

common cause

events

(see section 3.7

below); and

review to identify any ties between the current event

and any previous

events.

Inspection of the AB, in the vicinity of the leak,

showed extensive

flooding occurred

on the 141-foot level with subsequent

flow of water to

lower levels of the

AB through floor openings

and

down cable

and pipe

chases.

Also,

some electrical

equipment

on the 141-foot level

was wetted

by splashing

and spraying caused,

in part,

by operators

attempting to

replace

the valve bonnet to stop the leakage of water.

Electrical

equipment

on the next lower floor of the

AB -(114-foot level) was affected

mainly by water falling from openings in the floor above

and

down cable

and pipe chases.

Some electrical

equipment

on the 95-foot and 70-foot

levels were wetted slightly by water draining

down from the upper levels

and from water backing

up in floor drains

on these levels.

The immediate

effect of water flooding on electrical

equipment

was severe

damage to

LDC 1NJS-LDC 1A/B.

This was caused

by water from the 141-foot level

flowing through openings in the floor under

ViCCs 2J and 2L onto the top

of the load center

below causing

ground faults in the load center.

This, in turn, resulted in burning out the windings of step-down

Transformer

1NJS-X1A and

an electrical explosion in the adjacent

13.8

kV

manual

disconnect

switch bay.

Switchgear

1NPS-SWGIA Breaker

16 then opened

resulting in loss of power to Load Centers

1NJS-LDC 1C/D and 1S/T,

As a

result,

power to

RPS

Bus

B was lost giving a half scram

and closing the

Division II Containment Isolation Valves which resulted in loss of shutdown

cooling to the reactor core

and loss of cooling to the spent fuel pool.

Normal lighting to the reactor, control, and auxiliary buildings

was also

lost.

No safety-related

equipment

was

damaged

as

a result of this event.

The control

room operators,

upon observing the loss of power to the

RPS

Bus B, implemented

Abnormal Operating

Procedure

AOP-0010,

"Loss of One

RPS Bus," to restore

power to the bus, reset

the containment isolation,

arid

reopen the isolation valves to restore

shutdown cooling and spent fuel

pool cooling.

These actions

were taken in accordance

with preplanned

procedures

established

to handle the consequences

of this event.

The licensee

acted to restore lighting to the affected buildings by

establishing

temporary feeds

from an existing 480-volt construction

loop to

the

YiCCs which feed the lighting panels in the affected buildings.

This

-13-

action was assigned

a high priority because

having adequate

lighting in the

reactor, control, and auxiliary building was essential

for the recovery

and

restoration activities in these buildings.

The licensee

informed the team that an event with similar results,

not

involving a freeze seal,

had occurred in 1986.

The team reviewed

LER 86-005, Revision 1, together with the licensee's

Condition

Report 86-028 which showed that, although the event

was caused

by a

different source,

the

same transformer

was affected

and the result was

a

plant scram from startup

(3 percent power).

The analysis

concluded that,

had the openings

under the 2J and 2L NCCs on the 141-foot level

been

sealed,

the event would have

been terminated with less serious

consequences.

Initially, an

NWR was written to seal

these

openings

but it

was later determined that sealing the bottom edges of these

MCCs was

undesirable

because it would allow water that might enter the

HCCs to

accumulate

there

and consequently

sealing of these

openings

was not done.

The potential for damage to these

MCCs, caused

by heat

and combustion

products entering through these

openings

from a fire in the load center

located immediately below on the 114-foot level, was apparently not

considered

(see Section 3.7 below).

There was

no discernible effect on safety-related

equipment other than

minor moisture accumulation in some of the 480-volt NCCs,

and in some pull

boxes

and junction boxes for Rosemount transmitters that were located in

the splash

area of the 141.-foot level in the AB,

No loss of safety-related

equipment occurred.

The licensee's

failure to either plug the openings

under the 2J

and '2L NCCs

on the 141-foot level or arrange to divert water

draining through

them away from the

LDC NJS-LDC lA/B was

a major contributing

factor to the severity of the event.

These

openings constitute

a valid

path

by which heat

and combustion products

could enter the two safety-related

MCCs from a fire in the nonsafety-related

load center

immediately below.

This could cause their loss or damage'and

should

be considered

by the

licensee.

In discussions

with licensee

personnel, it appears

they are

considering fire sealing the openings

and providing

a drain duct under

each

MCC that would divert water collected under the

I'CC away from the

load center.

This appears

to be

a reasonable

solution since it would

drain away any water that collected under the

NCC, divert the drainage

away from the load center,

and prevent heat

and combustion products

from

gaining direct access

to the 2J

and

2L NCCs from a fire in the

INJS-LDC 1A/B

load center.

The AIT considers

the licensee's

actions to restore

shutdown cooling and

lighting to the reactor, control,

and auxiliary buildings appropriate.

From the

NRC inspectors

review of LER 86-005, Revision 1, and the

licensee's

Condition Report 86-028,

we concluded that action to either plug

the openings or to provide means for diverting water that could flow

through the openings

and fall onto the load center

below should

have

been

taken

as part of the recovery from the earlier event

and chat,

had such

action been taken,

the consequences

of the current event would have

been

-14-

3.5

much less

severe.

We conclude that the licensee's

proposed action to seal

the openings

on the 141-foot level or provide diversion of the

drainage'way

from the load center

on the 114-foot level should

be pursued.

Licensee

Plans for Recover

The AIT reviewed the licensee's

plans for recovering from the effects of

this event'including restoration of water damaged

switchgear.

The team

interviewed plant staff members that were involved in the recovery

and

restoration efforts.

Recovery from damage to electrical

equipment included

a walkdown of the affected areas to ascertain

the type and extent of damage

to electrical

equipment including wetting of electrical

equipment.

This

initial inspection

included the 141-, 114-, 95-, and 70-foot levels of the

AB and was conducted

by a team from the

RBS environmental qualification (Eg)

group which identified electrical

equipment that could have

been affected

and performed

a visual inspection for water intrusion into the equipment

components.

This initial inspection

was completed

and identified

a group

of electrical

equipment that

needed to be opened

up and partially

dismantled to inspect the internals for moisture ingress

and

damage.

This

latter activity was projected to be completed

by April 25,

1989.

Some

'reas

on the

AB 95-foot level were wetted

and

became

contaminated

zones

around

some of the electrical

equipment located there.

Inspection of this

equipment, for moisture intrusion and damage, will be done

by an

MWO when

clearance

to work in the contaminated

zone

can

be obtained.

Several

pieces

of equipment, particularly breakers

from MCCs in the splash

zone near the

break,

were found to have moisture inside.

These

were disassembled,

dried,

cleaned with solvent,

reassembled,

tested,

and returned to service.

The

damaged

13.8

kV Load Center

1NJS-LOC 1A/B will have the disconnect

switch

bay refurbished,

the.

transformer will be replaced,

the control

equipment will be cleaned

and tested,

and the individual breakers will be

dried, cleaned,

and terminals

and connections will be inspected for

corrosion.

Moving parts will be cleaned,

checked for corrosion

damage,

and

lubricated

as needed.

This work is being done under currently active

MWO RO-56269.

Lighting panels

supplying the reactor, control,

and

auxiliary buildings are currently being fed from the construction

loop

source

pending completion of recovery actions to the circuit breaker panels

of Load Center

1NJS-LDC lA/B.

The team believes

these actions to be

adequate.

3.6

Mana ement Control of Outa

e

The team reviewed this event to determine if there

was any tie to previous

events

during this outage.

Prior to the team's arrival, the licensee

had

evaluated

the event including root cause.

The licensee

performed

a

management

oversight risk tree

(MORT) analysis,

and

a

MORT chart was

prepared that indicated

inadequate

training as the principal root cause.

The

NRC review of this event led to the conclusion that

GSU underestimated

the hazards of using freeze seals.

As

a result controls were not

established

that would have required adequate

preplanning,

including

-15-

3.7

training,'rior to the use of freeze seals.

The problems associated

with

this event are sufficiently different from earlier outage

problems that no

strong connection to previous events

were noted.

Review of possible

Common Mode Failure in Auxiliar Buildin

Floodin

The team inspected

the various paths

taken

by water that leaked out of the

SSW system

and on to the

AB 141-foot elevation floor.

Consideration

was

given to the potential of flooding to become

a

common mode failure through

which redundant

systems

could be disabled.

The team noted possible

paths

on the east

and west ends of the 141- and ll4-foot elevations

where

safety-related

motor control centers

(MCCs) for redundant trains of

equipment, were installed.

Three possible

common cause

events that could result from water leakage,

such

as from the current event,

were examined.

One involved water flowing

down from the 141-foot level causing

a loss of safety-related

MCCs of

redundant divisions located

on the 114-, 95-,

and 70-foot levels of

the AB.

Another involved water flowing through openings

on the east side

of the 141-foot level of the

AB onto safety-related

NCCs and switchgear

located

on the 114-foot level at the

same time as'water flowing through

openings

under the 2J and

2L MCCs on the 141-foot level initiates

a fire in

the

1NJS-LDC lA/B load center.

Heat and combustion products

from this fire

can flow up through these floor openings into the safety-related

MCCs 2J

and

2L causing

loss of these

YiCCs.

The last postulated

event involves

flooding of safety-related

electrical

equipment located

on the 95- and

70-foot levels of the

AB caused

by water leaking

down from breaks or

fire fighting activities on higher levels coupled with water backing

up

from overloaded floor drains

on these

lower 'levels.

This last postulated

event is potentially more serious

because

the three

RHR pumps,

the reactor

core isolation cooling pump, the low pressure

core spray

pump and their

associated

MCC cabinets,

and the

HPCS

pump and its local control panel

are

located

on these

two levels, which are the lowest levels in the AB.

Mith regard to our postulation of common cause

events,

we believe the

probability of occurrence of the first postulated

event

(redundant

equipment lost due to flow paths of water) to be small given that the

MCCs

involved have the conduits entering from the top sealed with Duxseal, the

tops of the

NCCs are

one piece with a lip covering the side panels

which

acts to shed water,

and the lowest components

in the

MCCs are located at

least

6 inches

above the floor level.

The probability of occurrence of the

second postulated

event (loss of equipment in one train due to water with a

- loss in the other train due to an electrical fire in nonsafety

equipment)

is believed to be greater than that of the first but still to, be small

b

f th difficulty of getting enough of the splashing water inside

the par'tially sealed safety-related

YiCC to cause

shorts or gground faults.

The probability of occurrence of the last postulated

event (inadequate

capacity of drain system)

appears

to be large

enough to warrant

consideration.

Given that these levels are the lowest levels in the AB,

they will collect water from breaks

on higher levels because

of the

apparently quite limited capacity of the

AB floor drains to deal with

-16-

either water from large pipe breaks

or extended 'fire fighting activities.

Also, there is

a large

amount of safety-related

equipment

located

on those

levels.,

4.0

The use of freeze plugs, with the system operating

and with the loop not

securely isolated

(by valving it off), resulted in an opening in each line

lai ger than the design basis

opening

used to size the floor drains in the

area.

NUREG 0800, the Standard

Review Plan

(SRP), Section 3.6. 1,

Appendix

B (BTP ASB 3-1), -defines the design basis critical crack size

as

being "taken to be 1/2 the pipe diameter in length

and 1/2 the wall

thickness

in width."

Using this definition, the critical crack size

can

be

calculated

as (6x0.5) x (0.5x0.5)

= 0.75 sq. in. (assuming

pipe wall

thickness

as 1/2 inch) which is assumed

to be the design basis for sizing

the floor drain (assuming this 6-inch line was the largest in the area).

Each valve body opening (bonnet

removed)

could have

a nominal

area of

($ )~ Pi

= 28. 2 sq.

in. which appears

to far exceed

the design basis for

sizing the floor drains in the area.

SRP Section 9.3.3 states

that the

floor drain system

should

have the capacity to carry away the

maximum

potential flooding that could occur

from normal operation,

maintenance,

testing,

and postulated

accidents

(pipe break,

tank ruptures,

etc.)

as

required

by General

Design Criteria 4.

The River

Bend Station

Updated Safety Analysis Report,

Section 9.3.3.3,

states,

"The floor drainage

systems

servicing buildings which house

equipment

needed for safe

shutdown

and .accident prevention or mitigation

have sufficient capacity to minimize water buildups that could hamper those

activities."

The licensee

was requested

to review the floor drainage

system design to assure

that there is a sufficient basis to support the

statement.

The licensee

committed to review the adequacy

of the floor

drain system.

Conclusions

and Findin

s

4.2

4.3

GSU did not provide adequate

control over freeze

seal

work.

Specifically,

the licensee's

freeze

seal

procedure

did not clearly specify that

a

temperature

measuring

device.was

required to monitor the temperature

and

hence

the integrity of the freeze seal.

In addition,

two freeze seals

were

being fed liquid nitrogen from the

same nitrogen bottle which can lead to

seal failure; however, if the temperature

of the seal

had been monitored,

the degradation

in freeze

seal integrity should

have

been detected.

Technicians

monitoring the freeze

seal

received

no formal training.

Operations,

engineering,

and management

personnel

appeared

to be unaware of

the potential for a freeze

seal failure.

A freeze

seal failure was not

viewed as credible; therefore,

neither preplanning

nor an awareness

of

freeze

seal

status

was evident

among operations

personnel.

This lack of

awareness

delayed operator

response;

however,

the leak was isolated in

15 minutes.

The operators

responded

well under the circumstances

which

included flooding,,

a potential electrical fire,

and

a loss of lighting.

-17-

t

4.4

The electrical

system performed

as expected

under

the circumstances.

No

damage to safety-related

electrical

equipment

has

been identified.

4.5

The failure of the freeze

seal

on a 6-inch line resulted in flooding that

significantly exceeded

the design capacity of the floor drain system.

This event raised the potential for a

common

mode failure of certain

safety-related

equipment

due to the resulting collection of water in the

lowest levels of the AB.