ML17332A922

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Insp Repts 50-315/95-09 & 50-316/95-09 on 950620-0817. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support
ML17332A922
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 09/08/1995
From: Kropp W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17332A919 List:
References
50-315-95-09, 50-315-95-9, 50-316-95-09, 50-316-95-9, NUDOCS 9509190067
Download: ML17332A922 (25)


See also: IR 05000315/1995009

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION III

REPORT

NO. "-50-316 95009'0-316

95009

, FACILITY

Donald

C.

Cook Nuclear Generating

Plant

V+

LICENSEE

Indiana Michigan Power

Company

Donald

C.

Cook Nuclear Generating

Plant

1 Riverside Plaza

Columbus,

OH 43216

DATES

June

20 through August 17,

1995

INSPECTORS

J.

A. Isom, Senior Resident

Inspector

D. J. Hartland,

Resident

Inspector

C.

N. Orsini, Resident

Inspector

D. S. Butler, Reactor Inspector

R. A. Paul,

Reactor

Inspector

APPROVED

BY

W. J.

Kropp, Chief

Reactor Projects

Branch

2A

AREAS

INSPECTED

D te

A routine,

unannounced

inspection of operations,

engineering,

maintenance,

and

plant support

was performed.

Safety

assessment

and quality v'erification

activities were routinely evaluated.

Follow-up inspection

was performed for

non-routine events

and certain previously identified items.

95091900b7

9509i.2

PDR

ADQCK 050003i5

8

PDR

RESULTS

Assessment

of Performance

Performance within the area of OPERATIONS was poor during this inspection

period

see Section 1.0.

Concerns with regard to procedural

adherence

and

awareness

of plant conditions were evident

as described

in Section

1.0.

Some

of these

events

were either identified by the inspectors,

identified by the

licensee,

or were self-revealing.

Each event

by itself was not significant,

but in the aggregate

represented

a marked decline in operator

performance

over

the last two months.

Recent

NRC administered initial operator licensing

examinations

(Inspection

Report 50-315/OL-95-01(DRS)) identified

a weakness

where

a lack of self-checking

caused

operator candidates

to miss steps

during

procedure

performance

and others to miss irregularities in system responses.

The inspectors

were concerned

that this weakness

was observed

in actual plant

'perations.

A violation for operator failure to follow procedural

requirements,

including

response

to

a decrease 'in condenser

vacuum that resulted in a reactor trip,

was identified.

In addition, the inspectors

noted weaknesses

in operator

awareness

of plant conditions,

including failure to recognize

the over-

energization of the main transformer in a timely manner during

a generator

"

paralleling evolution.

The inspectors

also identified

a violation for failure

to comply with 10 CFR Part 72 reportabilty requirements.

The examples

given

for the events that were not reported all pertained to operator errors. and

represent

a programmatic

weakness

in reportability.

Overall performance

in the area of MAINTENANCE was considered

adequate - see

Section 2.0.

However, there were three instances

where procedures

were not

followed during maintenance

and testing activities.

One pertained to the

testing of an

Emergency Diesel Generator,

and one to the exercising of the

main steam safety valves

(MSSV), both of which were identified by the

inspectors.

The other pertained to repair of a manual

voltage regulator

potentiometer that was self-revealing.

A concern

was also identified

regarding failure to perform adequate

post-maintenance

testing

(PHT) resulting

in a violation.

The three

examples

in the violation were either identified by

the inspectors

or self-revealing,

with the other example the subject of

'inadequate

PHT during

a previous inspection.

The inspectors

were also

concerned that actions

taken

by the licensee

to address

a previous event

failed to prevent the miswiring of the voltage regulator.

Performance within the area of ENGINEERING was adequate - see Section 3.0.

The licensee's initiative to attempt to resolve the

MSSV bonding issue

was

considered

a strength.

However, the licensee

did not address

the issue

regarding the Technical Specification

(TS)-required as-left lift setpoint of

the

MSSVs until prompted

by the inspectors.

The inspectors

were concerned

with the non-conservative

approach

by engineering of not assessing

data

obtained during the exercising of the valves for TS compliance.

Performance within the area of PLANT SUPPORT

was good

see Section 4.0.

One

weakness

was identified concerning

an investigation

by the radiation

protection department.

Summar

of 0 en

Items

Violations: identified in Sections

1. 1, 1.2, 1.3, 2.3,

and 2.5

Unresolved

Items: not identified in this report

Ins ector Follow-u

Items: not identified in this report

Non-cited Violations: not identified in this report

INSPECTION DETAILS

1. 0

OPERATIONS

NRC Inspection

Procedure

71707

was

used in the performance of an inspection of

ongoing plant operations.

Operator

performance with regard to procedural

adherence

and awareness

of plant conditions

was poor as evident

by several

events

described

in the following paragraphs.

Some of these

events

were

either identified by the inspectors,

identified by the licensee,

or were self-

revealing.

Each event

by itself was not significant, but in the aggregate

represented

a marked decline in operator

performance

over the last two months.

A recent

NRC administered initial operator licensing examination

(Inspection

Report 50-315/OL-95-01(DRS)) identified

a weakness

where

a lack of self-

checking

caused

operator candidates

to miss steps

during procedure

performance

and others to miss irregularities in system response.

The inspectors

were

concerned that this weakness

was observed

in actual plant operations.

1. 1

Performance of 0 erations at Power

1. l. 1 Unit

1 Technical

S ecification

TS 3.0.3 Entr

On July 4,

1995, while performing

01-OHP 4030.STP.053B,

"ECCS Valve

Operability Test-Train 'B," the reactor operator

missed

step 1.8. l.e., which

required that

RHR discharge crosstie

valves

1-IMO-314 and 1-IMO-324 be opened.

This step

was required to maintain four loop safety injection capability while

the "S" SI

pump discharge crosstie valve, l-IM0-275, was being cycled.

Upon

identifying the discrepancy,

the licensee initially determined that

TS 3.0.3

had

been entered

during the short time that

IMO-275 was closed.

However,

upon

further review as part of the investigation into the event,

the licensee

concluded that

TS 3.0.3

was not actually entered

and that the event

was not

reportable.

The inspectors'eview

of the reportability determination is

discussed

in paragraph

1.3.

1. 1.2 Unit

1 Main Condenser

Low Vacuum Tri

On July 14,

1995, the Unit

1 reactor tripped due to loss of condenser

vacuum.

The licensee

determined that the cause of the loss of vacuum was the fatigue

failure of a 1" main steam

dump valve condensate

drain line.

All safety

systems

functioned

as required.

The operators

became

aware of decreasing

vacuum approximately

10 minutes

before the turbine trip when

a condenser

"A" high hotwell level alarm, closely

followed by a low hotwell level alarm,

was received in the control

room.

About three minutes later, the operators

received

a "main condenser

vacuum

low" alarm which was

common to all three condensers.

Since the operators

were

not immediately able to determine

the cause for the decreasing

vacuum,

an

attempt

was

made to place the start-up air ejectors

("hoggers") in service to

try to regain

some

vacuum.

However, the operators

encountered

a delay in

placing the hoggers

in service

due to the need to locally close

a valve which

was

open to drain condensate

build-up in the steam

header to the hoggers.

The

condensate

build-up was due to leakby past the steam supply valve,

SM0-400.

4

The unit tripped about

8 minutes after the low condenser

vacuum alarm was

received,

before the operators

were able to place the hoggers

in service.

The inspectors

identified some concerns

regarding operator action taken prior

to the trip.

The inspectors

noted that step 3. 1 of the annunciator

response

procedure,

Ol-OHP 4024. 118 (drop 71), stated to "reduce turbine load as

rapidly as possible".

A note in the procedure

stated that step

1 and step

2

(investigate

the cause for the decreasing

vacuum)

could

be done concurrently.

The operators

decided

not to reduce

load due to the rate at which vacuum was

decreasing

based

on the belief that there would be limited benefit from

reducing load

and operator resources

should

be used to investigate

the

problem.

Licensee's

management

position was that concurrent did not mean at

the

same time but rather the operator

has

a choice of what step to perform.

Licensee

management

stated that the operators

met management's

expectations

in

the response

to the loss of vacuum.

However, the inspectors

concluded that

the operators

decision not to reduce

power was non-conservative

because

a

reduction would have

increased

the margin of safety if complications

had

occurred following the reactor trip.

The operators'ailure

to follow the

annunciator

procedure to decrease

load rapidly is considered

an example of a

violation of TS 6.8. 1.(50-315/95009-01a(DRP)).

In addition, the inspectors

also concluded that, with vacuum decreasing

at

an

excessive

rate,

the operators

should

have manually tripped the reactor to

avoid challenging the automatic trip function.

The inspectors

noted that

an

error existed in procedure

Ol-OHP 4021.050.001

because

the procedure

required the reactor

be manually tripped only if vacuum could not be

maintained

above 21.6", which was below the automatic trip setpoint of 21.8".

1.2

Performance of 0 erations

While Shut

Down

1.2. 1 Hain Generator

Parallel

0 eration

While the unit was in Node 3, the licensee

repaired the drain line and

performed several

other. corrective maintenance activities, including repair of

the main generator

manual

voltage regulator.

On July 16,

1995, while

attempting to parallel

the main generator

during unit restart,

the operators

. inadvertently applied excessive

voltage to the Unit

1 main generator

and the

Unit

1 main output transformer.

The inspectors

determined that the operators failed to perform step 4.3. 15 of

procedure

Ol-OHP 4021.050.001,

"Turbine Generator

Normal Startup

and

Operation," which required that the generator

core monitor be placed into

service per attachment

1 before closing the exciter breaker

(step 4.4.4).

Shortly after closing the exciter field control breaker the operators

received

some unexpected

annunciators,

including

a

generator internals overheated"

alarm.

Because

the operators

had not yet completed

step 4.3. 15 (placing the

generator

core monitor in service),

the operators

did not respond to the valid

"generator internals overheated"

alarm.

The operators'ailure

to follow

procedure

01-OHP 4021.050.001

to place the main generator

core monitor in

service is considered

another

example of a violation of TS 6.8. 1.

(50-315/95009-01b(DRP)).

About

a minute or two later, the operators

received

a "main transformer

gas

relay operated

or hydrogen concentration

high" alarm,

which was symptomatic of

overheating/breakdown

of the transformer cooling oil.

At that point, the

operators

identified that the generator

output voltage

was excessively

high at

approximately

146 volts, well above the expected

value of 106 volts with the

manual voltage regulator adjusted to the minimum position.

After

unsuccessfully

attempting to lower the voltage with the regulator,

the

operators

opened

the exciter breaker.

The operators

then confirmed the high

hydrogen concentration

at

a local panel.

The overvoltage condition for the

Unit

1 main generator

and the main transformer

existed for approximately

5

minutes.

The licensee

determined that the cause of the over-energization

of

the transformer

was incorrectly landed leads

associated

with the manual

voltage regulator that was worked during the forced outage.

This issue is

discussed

further in paragraph

2.0.

Based

on the following, the inspectors

concluded that the operator

performance'uring

the generator parallel operation

was poor because

the over-excitation

of the main generator

was not recognized

in a timely manner:

Paragraph

4.4.5 of 01-OHP 4021.050.001

required that the operators

verify that all three

phases

were energized

on the generator

voltage

meter following closure of the exciter output breaker.

Although no

acceptance

criteria was given for output voltage in the procedural

step,

the operators

had the opportunity at that point to recognize that the

value was outside the normal operating

range.

The operators

did not ensure that the main generator

core monitor was

placed in service prior to closing the exciter field breake'r.

The inspectors

had previously identified concerns

regarding operator

performance

during generator parallel operations

in inspection report

50-315/94022;

50-316/94022.

In response

to this event,

the licensee

updated

Ol-OHP 4021.050.001

to include

acceptance criteria for the generator

output voltage

upon closure of the

exciter output breaker.

In addition, the licensee clarified the procedure to

ensure that the core monitor would be operational prior to closing the

breaker.

The licensee

performed

an internal inspection of the accessible

portions of

the main transformer

and generator

and did not discover

any damage.

However,

on July 27, the licensee

re-energized

the transformer

and

a high hydrogen

concentration

developed

in the transformer cooling oil due to apparent

damage

'in a portion of the transformer that was not accessible

during the inspection.

Due to the extended

outage required for replacement

of the transformer,

the

licensee

elected to enter the refueling outage approximately six weeks prior

to the scheduled

date.

The licensee

had the unit in Mode

5 at the end of the

inspection period.

~

~

1.2.2 Auto Start of Turbine Driven Auxiliar

Feedwater

TDAFW

Pum

On July 28,

1995, the licensee

removed the reserve

feed transformer

from

service for maintenance

to correct

a "hot spot" identified during thermography

inspections.

In order to perform this evolution with Unit

1 shutdown,

the

licensee

revised

Procedure

    • 01-OHP 4021.082.001,

"4KV Buses

Power Source

Transfer

and De-energizing

a Safeguards

Bus." This revision described

the

method to parallel

an emergency diesel

generator

(EDG) to a safety bus,

load

the

EDG,

and

open the tie-breakers

between

the related reactor coolant

pump

(RCP)

buses

and the safety bus.

During the initial planning of this evolution, the licensee

discussed

that the

turbine-driven auxiliary feedwater

(TDAFW) pump would receive

an autostart

signal

when two of the four RCP buses

were de-energized,

and that the

possibility existed for the under-frequency

relays to cause

the remaining two

RCPs to trip.

Neither of these

issues

was incorporated into the procedure,

and the pre-job briefing in the control

room did not include

a discussion

regarding the

TDAFW pump auto start.

The

TDAFW pump autostarted

at 3:38 p.m.

when breaker

T1181

was opened,

de-

energizing the second

RCP bus.

The operators realizing why the

pump started,

manually tripped the

pump

and declared it inoperable.

The

TDAFW pump was

reset

and declared

operable at 11: 18 p.m., after the reserve

transformer

maintenance

was

completed.'he

inspectors

had the following concerns with the performance of this

evolution:

The inspectors

determined that the autostart of the

TDAFW pump was

an

ESF actuation that was not indicated

by a procedural

step nor were the

control

room personnel

aware of the specific signal

before its

occurrence.

This concerned

the inspectors

because

the operators

did not

evaluate

the ramifications of deenergizing two'f the

RCP busses

and the

subsequent

initiation of the

ESF signal.

The inspectors

al,so

had

some concerns

regarding the licensee's

justification that the

ESF actuation

was not reportable.

This issue is

discussed

in paragraph

1.3.

~

At approximately

2100, the shift technical

advisor identified that

conditions

1

and

2 were

no longer satisfied for TS 3.0.5 for the West

MDAFW pump because its normal

power source

(reserve

feed)

was not

available

and its redundant

component

(the

TDAFW pump)

was inoperable.

This would have given the licensee

8 hrs.

from 3:38 p.m. to have the

plant in Mode 4.. The shift did not take action to cooldown the plant

because

the reserve

feed

was expected to be returned to service prior to

the 8 hrs expiring.

However, this

LCO entry was not logged in the

control

room log book after being identified.

The licensee

has

'nitiated

condition report No.

1107 to determine

why the planning

process

did not identify this

LCO.

The inspectors'ere

also concerned that since the

TDAFW pump autostart

and the possibili.ty of the under-frequency

relays actuating

were not

documented

in the procedure,

the evolution could be performed in the

future without these

issues

being considered.

1.2.3 Erroneous

0 eration of Containment Ventilation

On July 29,

1995, with Unit

1 in Mode 3,

a licensee

reactor operator performed

the wrong attachment of Ol-OHP 4021.028.005,

"Operation of the Containment

Purge System."

The pro'cedure

required that the system

be operated

in the

"clean-up"

mode when containment integrity was required

(Modes 1-4 per

TS 3.6. 1. 1). However, the operator erroneously

operated

the system in the

"ventilation" mode of service for approximately

5 minutes.

The significance

appeared

to be that the vent stack radiation monitor was not source

checked

and

a release

permit was not forwarded to Radiation Protection.

The licensee

initiated

a condition report for this event.

1.2.4 Unit

1 Cooldown

On July 30,

1995, while cooling down Unit

1 in Mode 4,

a licensee unit

supervisor did not follow the required

sequence

of steps

in procedure

Ol-OHP

4021.001.004,

"Plant Cooldown

From Hot Standby to Cold Shutdown," for

establishing

Low Temperature

and Operating

Pressure

(LTOP) protection

and

prematurely racked out

a

CCP pump.

The consequence

was that the licensee

made

an unidentified entry into TS 3. 1.2.4,

which required

two operable

CCPs in

Mode 4, for over

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> before being discovered

by shift management.

The

licensee initiated

a condition report for this event.

1.2.5 Inadvertent Drainin

of Reactor Coolant

S stem

On August 4,

1995, after isolating

a seal injection filter for maintenance

and

attempting to drain the header,

an auxiliary equipment operator

(AEO) observed

excessive

water coming 'from an open vent valve due to the apparent

leakby of a

clearance

isolation valve.

In response,

the

AEO closed the vent valve and

went to the control

room to report the problem.

However, the

AEO left another

valve that was also

used to drain the system in the open position.

Approximately

15 minutes after the drain valve had

been left opened,

control

room operators

noticed that pressurizer

level

had decreased

from about

12

percent to 5 percent,

or about

1500 gallons.

The water had drained to

a

sump

tank.

The operators

immediately initiated

RCS make-up

and the drain valve was

closed.

The licensee initiated

a condition report for this event.

1.3

Followu

on Previousl

Identified Items

A review of a previously opened

unresolved

item was performed

per

NRC

Inspection

Procedure

92901.

This item was closed

based

on

a violation being

identified regarding the failure of the licensee to report events

as required

by 10 CFR Part 72.

Closed

Unresolved

Item 50-316 94024-01:

The inspectors initiated this item

in response

to

a concern regarding the licensee's justification for

classifying events

as not reportable.

During the inspection period,

the

inspectors

identified the following events that should

have also

been reported

to the

NRC:

An example identified as part of the unresolved

item involved an

unintended

entry into TS 3.0.3

on April 2,

1994,

due to the inoperabilty

of both trains of Unit 2 engineered

safety feature

exhaust

(AES) fans.

The function of the

AES fans

was to provide cooling for ECCS equipment

and to ensure that radioactive material leaking from equipment following

a

LOCA is filtered prior to reaching the environment.

The licensee

had

placed the control switch for the 2-HV-AES-2 fan in the "stop" position

after starting the 2-HV-AES-1 fan for post-maintenance

testing

(PNT),

thus making both fans inoperable.

The licensee

had taken the AES-1 fan

out-of-service for replacement

of a

HEPA filter.

The licensee

concluded

that since the

PHT on AES-1 fan was successfully

completed,

the event

was not reportable

because

the AES-1 fan was capable of performing its

intended function at the time AES-2 was stopped.

The inspectors

concluded that the licensee's justification, which was

based

on

retroactively applying the successful

completion of testing,

was in

error.

Therefore,

the inspectors

concluded that the event

was

reportable

per

10 CFR 50.72,

paragraph (b)(1)(ii)(B), as

a condition

outside the design basis of the plant.

On October

10,

1994, during performance of STP 205,

"ESF Time Response

Testing-Train A," the licensee

received

an unexpected

phase

"A"

isolation of the containment

purge system.

As part of the preparatory

steps of the surveillance testing,

the operators

had removed the 'purge

system

and closed the containment isolation valves to prevent automatic

isolation during the testing.

However,

due to poor communication,

an

operator placed the purge system

back in service before the test

was

initiated.

As

a result,

the operators

experienced

the phase

"A"

isolation signal,

which resulted

in the isolation of the containment

purge isolation valves.

The phase

"A" containment isolation signal

was

listed in paragraph

3.a of Table 3.3-3 of TS as part of the

ESF

actuation

system instrumentation,

and

was not an expected result of the

procedure.

Therefore,

the inspectors

concluded that the event

was

reportable

per

10 CFR 50.72 paragraph (b)(2)(ii)(A).

As discussed

in paragraph

1. 1 of this report, the licensee initially

determined that

TS 3.0.3

was entered

on July 4,

1995,

due to loss of

four loop safety injection capability.

The licensee

determined that

a

one hour phone call per

10 CFR 50.72

was not required

because

manual

four loop injection was available.

In addition,

upon further review of

the event,

as documented

in condition report

(CR) 95-1107,

the licensee

performed

an analysis that demonstrated

that the plant was not in an

unanalyzed

condition that significantly compromised plant safety.

This

conclusion

was

based

on the unit being at

a reduced

power level at the

time (57 percent);

therefore,

UFSAR acceptance

criteria for the

accidents

impacted would continue to be me't.

The inspectors

reviewed the licensee's justification.

The inspectors

noted that the licensee

could not take credit for operator action for

establishing

four loop injection.

In addition,

since the currently

docketed

design

bases

and accident

analyses

approved

by the

NRC does not

recognize

two loop injection for both the

RHR and SI,

an unanalyzed

condition did exist

and entry into TS 3.0.3

was appropriate.

An

analysis after the event

was not justification for not submitting

an

LER, but rather

an analysis to ascertain

the safety significance of the

event.

Therefore,

the inspectors

determined that the event

was

reportable

as

a condition outside the design

basis of the plant

as

required

by 10 CFR 50.72(b)(1)(ii)(B).

~

As discussed

in paragraph

1.2.2

above,

on July 28,

1995, the licensee

experienced

an automatic start of the Unit

1

TDAFW pump while performing

a power source transfer.

The

pump autostart

was

due to reactor coolant

pump bus undervoltage.

This feature

was listed in paragraph

7.b of TS

Table 3.3-3

" Engineered

Safety Feature Actuation System

Instrumentation"

as part of the

ESF actuation

system instrumentation.

The licensee initially concluded that the event

was not reportable

as

an

ESF actuation

because

some individuals discussed this feature during the

initial planning

phase of the evolution.

However, the inspectors

noted

that the actuation

was not addressed

in the procedure

and

was not

expected

by the operators.

The licensee's

procedure that defines the

reportability process,

PHP 7030.001.001,

"Prompt

NRC Notification",

states that

a trip actuation

should not be

a surprise to the operator to

be not reportable.

Therefore the inspectors

concluded that the event

was reportable

per

10 CFR 50.72 paragraph

(b)(2)(ii)(A) because

the

TDAFW pump is an

ESF

as defined in TS and the auto start

was not

preplanned

(documented

in a procedure

or logged prior to actuation).

The licensee's

failure to report the above four events is considered

a

violation of 10 CFR 50.72.(50-315/95009-02(DRP)).

2. 0

MAINTENANCE

NRC Inspection

Procedures

62703

and 61726,

and 92902 were used to perform an

inspection of maintenance

and testing activities.

Overall performance in'his

area

was considered

adequate.

However, there were three instances

where

procedures

were not followed during maintenance

and testing activities.

One

pertained to the testing of an

Emergency Diesel Generator,

one to the

exercising of the main steam safety valves,

both of which were identified by

the inspectors,

and the other pertained to repair of a manual voltage

regulator potentiometer that was self-revealing.

A concern

was also

identified regarding failure to perform adequate

post-maintenance

testing

(PHT) resulting in a violation.

Of the three

examples

in the violation, one

was identified by the inspectors,

one

was self-revealing,

and the other was

an

example of inadequate

PHT during

a previous inspection.

The inspectors

were

also concerned that actions

taken

by the licensee to address

a previous event

failed to prevent the miswiring of the voltage regulator.

10

Maintenance

and Surveillance Testin

Activities

The inspectors, observed

routine preventive

and corrective maintenance

and

surveillance activities to ascertain

that they were conducted

in accordance

with approved

procedures,

regulatory guides,

industry codes or standards,

and

in conformance with Technical Specifications.

The following activities were

observed

and/or reviewed:

~

JO¹ C0030956,

"Repair Water Leak on 12-ZRV-404-RV"

~

JO¹ C0031204,

"Adjust 12-ZRV-404-RV For 165 Psig"

~

JO¹ C0031146,

"2-(T-502-AB, Replace

Turbo Rotating Assembly"

~

JO¹ C0025062,

"Adjust Limit Switches

on Hain Generator

Voltage

Regulator"

~

12 THP 6040

PER. 106,

"Emergency Diesel

Generator

Control

Panel

Tests"

~

JO¹ C24371, Unit 2

CD EDG, "Replace

Woodward Governor"

~

Ol

EHP 4030 STP.217A,

"CD

EDG Load Shedding

& Performance

Test"

~

02

OHP 4030

STP. 103,'Hain Turbine Stop

& Control Valve Testing"

~

01

OHP 4030

STP. 19F,

"Steam Generator

Stop Valve Operability Test"

~

12 EHP.6040.PER. 141,

"Main Steam Safety Valve Exercising Using AVK

ULTRASTAR Equipment,"

~

12 EHP4030STP.256,

"Hain Steam Safety Valve Setpoint Verification,"

2.2

Miswired Volta e'Re ulator

The licensee

established

a team to investigate

the root causes

of the main

generator over-excitation

event discussed

in paragraph

1.2.

Although the

investigation

has not been completed,

the licensee

has determined that the

cause for the event

was improperly landed leads

on the manual

voltage

regulator potentiometer that was replaced

during the forced outage.

The

miswiring caused

the regulator to be at maximum voltage regardless

of the

potentiometer setting.

In addition to the wiring error, licensee

personnel

failed to perform adequate

post-maintenance

testing

(PHT) following the maintenance activity.

The

original scope of the work on the regulator

was to adjust the limit switches

for the maximum and minimum voltage light circuits.

While performing the

activity, the

I&C technicians

damaged

the potentiometer,

expanding the scope

of the job.

Due to poor communication,

lack of understanding

of system

operation,

and perceived

urgency to complete the work, the original

PHT, which

consisted of verifying proper operation of the light circuits,

was not updated

to ensure

the regulator would work properly following the potentiometer

replacement.

The inspectors'oncern

regarding the inadequate

PMT is discussed

in paragraph

~2.5 below.

The inspectors

had several

concerns

regarding this event.

The licensee

had

experienced

a similar event in March 1993,

when

an

EDG load conservation

relay

was improperly wired following a calibration activity during

a refueling

outage,

which would have rendered

the function inoperable.

Fortuitously, the

licensee identified the miswiring during blackout testing,

which was not

specifically performed

as

a

PMT after the work on the'DG load conservation

relay,

but before the

EDG was declared

operable.

As action to prevent recurrence

of that event,

the licensee

reinforced the

use'f

self-checking

and verification methods

appropriate

to the consequences

of

improperly performing the activity.

The licensee

also committed to compare

restored wiring configurations with approved

drawings to ensure final

configuration agreed with design.

This comparison

was not performed following

the potentiometer

replacement.

The inspectors

also noted that the form used

to document the verification of leads lifted and landed for the regulator work

activity did not include the potentiometer

leads.

Therefore,

the technicians

had to use

a hand-drawn

sketch,

and there were

no signoffs for verification of

lifting and landing these

leads.

2.3

Exercisin

of Main Steam Safet

Valves

MSSVs

While exercising the

MSSVs per procedure

12 EHP.6040.PER. 141,

"Main Steam

Safety Valve Exercising Using AVK ULTRASTAR Equipment,"

MSSV 1-SV-3-2, which

had

a setpoint of 1085 psig, the equivalent of 1180 psig was applied without

the valve lifting.

The test

was stopped to confer with the valve vendor to

determine if more force could be applied without damaging the valve.

Procedure

12 EHP.6040.PER. 141, step

5. 17 stated that in the event that

a valve

cannot

be exercised,

stop testing immediately and notify the shift supervisor

(SS).

The

SS

and control

room operators

were not informed that testing

had

stopped

because

1-SV-3-2 would not lift.

The inspectors felt that,

although

1-SV-3-2 was already considered

inoperable,

operations

personnel

should

have

been

informed of the status of 1-SV-3-2 and the plans to apply more force on

the valve.

The failure to notify the

SS is considered

an example of a

violation of Technical Specification 6.8. 1 (50-315/95009-Olc(DRP)).

This

activity is discussed

in further detail in paragraph

3.2 of this report.

2.4

Missed Procedural

Ste

s

On June

22,

1995, during performance of an engineering test,

12 THP 6040

PER. 106,

"Emergency Diesel

Generator

Control

Panel Tests,"

the inspectors

observed that the operators

inadvertently skipped

some procedural

step's.

The

objective of the procedure

was to provide

a record of adjustments

made to the

voltage

and speed

potentiometers

following replacement

of the. Unit 2 "CD"

emergency diesel

generator

(EDG) governor.

Redundant

potentiometers

were

located in the control

room and at the

EDG local control panel.

12

Following adjustment of the control

room potentiometers

per paragraph

6.2 of

procedure

12 THP 6040

PER. 106, the operators

shut

down the

EDG to perform the

steps

required for making the local panel

adjustments.

However, the control

room operators

restarted

the

EDG before the remote-local

switch located at the

EDG sub-panel

was placed in the local position,

as required

by paragraph

6.3. 1

of 12

THP 6040

PER. 106.

Paragraph

6.3. 1 was required to be performed in order

to demonstrate

the capability of starting the

EDG locally, which was

an

acceptance

criterion in the procedure.

The cause for the missed

step

was due

to apparent

miscommunication

between

the operators

and the test engineer

coordinating the evolution.

Upon realizing the step

had

been missed,

the engineer

decided to continue with

the procedure

and evaluate

the

need to perform the missed

step afterwards.

However,

because

of the problems

found with the potentiometer

at the local

EDG

control panel,

the operators

shutdown the Unit I "CD"

EDG and the engineers

were not able to complete the test.

After making minor adjustments

to the

potentiometer,

the licensee

then satisfactorily performed the

"Emergency

Diesel

Generator

Control

Panel

Tests" during

a subsequent

EDG maintenance

run.

The inspectors

discussed

the event with the engineer,

who initially indicated

that the missed

step

was not

a procedural

adherence

issue.

The engineer

based

this determination

on paragraph

3.3 of the procedure,

which stated that test

steps

could

be completed

out. of order if the

EDG was already running.

However, the inspectors

concluded that the statement

did not apply to the

situation,

as the

EDG was not running at the time.

In response

to the

inspectors'oncerns,

the licensee initiated

CR No. 95-0965 to document the

missed step.

The inspectors will review the licensee's

investigation into the

event

and continue to monitor licensee

performance

in this area.

2.5

Follow-u

on Previousl

0 ened

Items

A review of a previously opened

unresolved

item was performed per Inspection

Procedure

92902.

Closed

Unresolved

Item 50-315 94014-06

DRP

The inspectors

had previously

documented

an issue regarding

PHT for non-routine corrective maintenance.

The

inspectors

were concerned that work planners

did not always

have

an adequate

background in system operation to ensure that appropriate

PHT would be

performed.

In response

to the inspectors

concern

and other related

events,

the licensee

issued

procedure

PHSO. 154,

"Planning of Post Maintenance Testing

Activities," which outlined the circumstances

when planners

should request

engineering

review of job orders for PNT.

The inspectors initiated the

unresolved

item to monitor the effectiveness

of the

PHSO.

The inspectors

noted three

examples of inadequate

PNT during the inspection

period..

~

The inspectors

noted that despite the apparent unfamiliarity of system

operation

by the planner involved with the voltage regulator maintenance

13

0

discussed

in paragraph'.

1 above,

no engineering

review of the job order

was requested

after the scope of the work was expanded

to replace

the

potentiometer.

On July 18,

1995, the licensee

performed

an activity to repair

a leak on

the controller associated

with valve 12-ZRV-404,

"West" Diesel

Driven

Fire

Pump back pressure

regulating valve.

The valve was located

on

a

recirculation line back to the fire water storage

tanks

and functioned

to maintain

165 psi header

pressure

under load.

The

PHT specified

by

the planner in JO C0030956

was to verify no leaks at normal

system

pressure.

However,

when Operations

operated

the

pump per

12-OHP 4030.STP. 121FD,

"Diesel Fire

Pump Operability Test," during the

PHT, it was observed

that the

pump only developed

120 psi discharge

pressure.

Although the

procedure

and the work order did not contain

any acceptance criteria

for'he

discharge

pressure,

the operators

questioned

the operability of the

pump.

The operators

contacted

the system engineer,

who initially

determined that the condition

was not

an operabil.ity issue.

On the

following day, the engineer

reconsidered

his position.

The licensee

subsequently

determined that the regulator

was

damaged

during the work

activity and initiated action to replace it.

The unresolved

item had

been initiated when the inspectors

identified

a

similar concern regarding

PHT of the pressure

regulating valve

associated

with the motor-driven fire pump,

12-ZRV-402.

At that time,

the inspectors

were concerned that,

although the setpoint of the valve

was adjusted to 165 psi, the

PHT did not demonstrate

the backpressure

regulating function of the valve to maintain header

pressure.

On August 2,

1995, after the licensee

completed

maintenance

on the

"AB"

emergency diesel

generator

turbocharger,

the resident

inspectors

raised

a concern regarding the adequacy. of the

PHT performed.

The licensee

performed the maintenance

in response

to a recent failure

of a similarly designed

turbocharger

at another plant.

The failure was

attributed to

a design

change.to

an insert that provided starting air to

the turbocharger

during initial roll-up to assist

in getting it up to

operating

speed.

The

new insert caused

the compressor

impeller blades

to reach

resonance

frequency at normal turbocharger

operating

speed,

resulting in excessive vibration and fatigue failure of the blades.

During the maintenance activity, the licensee

replaced

the insert with

the design previously used

and inspected

the impeller blades for damage.

The licensee's

PHT consisted

of a slow start

and full load run.

The

inspectors

determined that the test

was inadequate

because

starting air

was not provided to the insert during

a slow start; therefore,

the

licensee did not verify that the turbocharger

would perform its intended

function under

an accident condition.

The inspectors

noted that during

a slow start,

the

EDGs would not typically roll up to normal

speed until

30 seconds after the

EDG was started.

On an auto start signal,

the

EDGs

would be required to get

up to full speed within 10 seconds

and begin

accepting

sequenced

loading.

In response

to the inspectors'oncern,

the licensee

successfully

completed

a fast start

and run.

The above instances

are considered

examples of a failure to perform adequate

PMT and considered

a violation of 10 CFR Part 50, Criterion XI (50-315/95009-

'3(DRP)).

This unresolved

item is closed

based

on the issuance

of this

violation.

3. 0

ENGINEERING

NRC Inspection

Procedure

37551

was

used to perform an onsite inspection of the

engineering function.

Items closed

as

a result of this inspection

met the

criteria established

in the Inspection

Procedures.

Although the initiative to

attempt to resolve the

MSSV bonding issue described

in paragraph

2.4 was

considered

a strength,

the engineering

personnel

did not address

the Technical

Specification

(TS)-required as-left lift setpoint

issue until prompted

by the

'nspectors.

The inspectors

were concerned with the non-conservative

approach

by engineering of not assessing

data obtained during the exercising of the

valves for TS compliance.

3. 1

Follow-u

on Non-Routine

Events

NRC Inspection

Procedure

92700

was

used to perform

a review of the following

written report

on

a non-ro'utine event:

Closed

LER 50-315

94001

and

LER 50-316 94006:

The

LERs were written

concerning

MSSVs lifting outside the required tolerances.

The

LERs are closed

and resolution of this issue will be tracked

under Inspection

followup Item 50-315/94002-05;

50-316/94002-05(DRP)

as discussed

below.

3.2

Follow-u

on Previousl

.0 ened

Items

A review of the follow'ing previously opened

unresolved

and inspection followup

items

was performed per Inspection

Procedure

92902.

0 en

Ins ection Foll owu

Item

50-315 94002-05

50-316 94002-05

DRP

As discussed

in previous

NRC Inspection

Report

Nos. 50-315/94002;

50-

316/94002(DRP),

50-315/93019;

50-316/93019(DRP),and

50-315/92009;

50-

316/92009(DRP),

the licensee

has

had historical

problems with main steam

safety valves

(MSSVs) lifting at pressures

above the setpoint.

The licensee

believes that bonding between the valve disc

and nozzle

may be causing the

setpoint drift.

This theory was supported

by the fact that generally the

MSSVs which lift above the setpoint

on the initial test will lift at lower

pressures

on subsequent

tests without adjustment.

In response

to this issue the licensee

developed

procedure

12

EHP.6040.PER. 141,

"Main Steam Safety Valve Exercising Using AVK ULTRASTAR

Equipment," to exercise

the

MSSVs during power operation.

The purpose of this

evolution was to determine if bonding

was time dependent

(Unit

1 was

12 months

15

into a cycle,

and

MSSV testing is normally performed at the

end of an

18 month

cycle)

and if so, to determine

the proper interval for future exercising to

prevent bonding.

The licensee's

initiative to attempt to resolve this industry wide issue

was

considered

a strength.

However the inspectors

had

some concerns with the

licensee's

implementation.

On June

19,

1995, with the unit at approximately

55 percent

power, the

licensee

began exercising

the Unit

1 MSSVs.

The inspectors

identified the

following concerns:

~

While testing

MSSV 1-SV-3-2, which had

a setpoint of 1085 psig, the

equivalent of 1180 psig was applied without the valve lifting.

The test

was stopped to confer with the valve vendor to determine if more force

could

be applied without damaging the valve.

Procedure

12

EHP.6040.PER.141,

step 5. 17 states

that in the event that

a valve cannot

be exercised,

stop testing

immediately

and notify .the Shift Supervisor

(SS).

The

SS

and control

room operators

were not informed that testing

had stopped

because

1-SV-3-2 would not lift.

The inspectors felt that,

although

1-SV-3-2 was already considered

inoperable,

operations

personnel

should

have

been

informed of the status of 1-SV-3-2 and the

plans to apply more force on the valve.

On the subsequent lift attempt,

the valve lifted at approximately

1179 psig,

and

was returned to

service.

TS 3.7. 1. 1 requir'es that

a safety valve shall

be reset to the nominal

value a

1 percent

whenever

found outside the a

1 percent tolerance.

After 10 of the

20

MSSVs were exercised,

the inspectors

questioned

why

valves found outside the a

1 percent tolerance

were not being reset.

Initially the licensee

responded

that actual lift pressures

were not

required to be recorded

by procedure

12

EHP 6040.PER. 141

and therefore

TS 3.7. 1. 1 did not apply.

However,

although lift pressures

were not

being recorded,

the pressures

were displayed

and saved

by the testing

equipment.

Also, knowing the pressure

at which the valve lifted was

essential

to the purpose of this evolution.

Without knowing the actual

lift pressure,

the licensee

would not be able to determine if bonding

forces were present during the initial lift, nor ensure that the bonding

forces were relieved during subsequent lifts.

After further discussion,

the licensee

determined that

TS 3.7. 1. 1

applied whether or not the data

was required to be recorded.

The

licensee

then tested all Unit

1

MSSVs according to procedure

12

EHP4030STP.256,

",Main Steam Safety Valve Setpoint Verification," which

required all valves to be left within a

1 percent of the nominal

setpoint.

This approach

to testing

MSSVs did not demonstrate

a

conservative

approach

to TS surveillance

requirements.

This inspection followup item will remain

open pending the final determination

by the licensee of the. cause

and actions

necessary

to prevent the

MSSVs from

lifting above the setpoint.

I

16

Closed

Unresolved

Item

315 316 92003-04 DRS:

The Electrical Distribution

System Functional

Inspection

(EDSFI) team

was concerned

that the safety-

related electrical

buses

could decrease

to 79 percent of rated voltage

and set

at this value for 2 minutes until initiation of the degraded

voltage logic.

In response,

the licensee

provided the inspectors

the "D.C.Cook Voltage

Performance

Study,

1991-1995 Operating Period" system voltage analysis.

The

analysis indicated that the low and medium voltage safety-related

buses

would

not decrease

below 90 percent of rated voltage during the worst case

transmission

system contingency.

Safety-related

motors were designed

to start

at 80 percent of rated voltage

and were capable of operating within a voltage

range of a 10 percent.

The

2 minute time delay was selected

to provide

sufficient time to start

a reactor coolant

pump.

This time delay was accepted

by the

NRC in the June

1,

1981, safety evaluation,

"Adequacy of Station

Electric Distribution System Voltages," that was issued to D.C.Cook.

The

inspectors

concluded

the licensee

was operating electrical

equipment within

the design basis.

This item is considered

closed.

Closed

Unresolved

Item

315 316 92003-06

DRS

The

EDSFI team identified

that

250 Vac rated fuses

were

used in

DC applications.

The team was concerned

that the licensee's

evaluation,

"Analysis of D.C.Cook 250 Vdc System

Compared

to UL198L Test Results," did not substantiate

that

AC rated fuses

could be

used in

DC circuits.

In response,

the licensee

re-evaluated

the analysis

and issued calculation

No.

PS-FUSE-001,

"AC Rated

Fuses

in

DC Applications."

The calculation

showed that

the stored

energy dissipated

in TR-R fuses during

DC fault current

interruptions

were

bounded

by the fuse manufacturer's

stored energy test

values.

The inspectors

concluded that 30A and

100A TR-R current-limiting

fuses

would interrupt

a

DC circuit fault and limit the let-thru current to

a

value that would not damage

equipment.

This item is considered

closed.

0 en

Ins ection Followu

Item

315 94002-13 DRP:

In late September

1993,

Unit

1 operators

received

a low oil level alarm to the No.

14 reactor coolant

pump

(RCP) motor lower radial bearing.

The low oil condition eventually led

to damage to the lower radial bearing.

Based

on this event,

the inspectors

had additional

questions

on the causes

for the low oil condition.

On July 21,

1995, Unit 2 operators

received

a similar low oil level alarm on

the

No.

23

RCP.

The lower radial bearing temperature

appeared

stable during

the remainder of the inspection period.

The lower radial bearing temperature

indicated

about

132 degrees

Fahrenheit

and was in the observed

temperature

range for the other three

RCPs with normal oil levels.

The operators

continued to monitor the

No.

23

RCP bearing temperature.

Based

on the fai'lure observed with the Unit

1 No.

14

RCP, the system engineer

estimated that the No.

23

RCP could experience

a lower radial bearing failure

as early as October or November of 1995.

At the

end of the inspection,

licensee

management

was reviewing actions required to address

the low oil

level condition with the No.

23

RCP.

Inspectors will monitor conditions of

the No.

23

RCP and licensee

followup actions.

17

4.0

PLANT SUPPORT

NRC Inspection

Procedures

71750,

83750,

and 92904 were used to perform'an

inspection of plant support activities.

Two non-cited violations were

identified in the area of radiological controls.

Overall performance

in the

area of plant support

was considered

good.

4. 1

Radiolo ical Controls

The health physics staff has

remained stable.

Although

a corporate health

physicist left the company,

the radiation protection department

remains

technically sound.

The station also

has

a large

number of employees

who are

National Registry Radiation Protection Technician qualified.

The inspectors

reviewed several

quality assurance

(gA) audit

and surveillance

reports covering work activities that occurred over the previous

18 months.

Audit activities appeared

to be probing

and critical of the subject

area

being

reviewed.

Results

were effectively communicated

to the appropriate

department

and,

when appropriate,

a condition report was generated

for identified

deficiencies.

The inspectors

concluded that the licensee's

gA program,

specifically with regard to radiation protection,

was effective in identifying

opportunities for improving overall performance,

as well as procedural

deviations,

and

was considered

a licensee

strength.

4. 1. 1 Follow-u

on Non-Routine

Events

NRC Inspection

Procedure

92700

was

used to perform

a review of the following

written reports of non-routine events:

Closed

LER 50-315

94011

and

LER 50-315 94012:

The

LERs were written

concerning analysis

problems in the liquid and gaseous

sampling program.

The

LERs are closed

based

on inspector review of the procedural

changes that were

made to strengthen

the program

and to prevent recurrence.

4. 1.2 Radiolo ical Occurrences

IP 83750

The inspectors

reviewed the licensee's

investigation of a radiological

event

which involved 'two operators

who entered

Unit

1 upper containment during in-

core detector

movement operations.

Upper containment

was posted

as

a

radiation area instead of an extreme high radiation area

(EHRA) as

appropriate,

because

a Radiation Protection Technician

(RPT) failed to post

and control the area

as

an

EHRA when the moveable detector

system

(IHDS)

clearance

was not in effect.

Although the dose rates

in upper

and lower

containment

ranged

from about

26 mR/hr to 6 mR/hr, respectively,

during this

evolution, containment entry procedures

required that both entry areas

be

posted

and controlled

as

an

EHRA during any incore detector

movement.

When

the containment is properly posted

and controlled, the operators

are allowed

entry and provided constant

Radiation Protection

(RP) coverage.

Thes'e

controls are required to prevent

access

into the instrument

room where

extremely high dose rates

could exist when moving in core-detectors.

The

licensee identified this event

when another

RPT who knew the clearance

was not

in effect, discovered

operators

coming out of the upper containment.

The

18

operators

wore electronic dosimeters

(EDs), were exposed

to low dose rates

and

received less

than

5

mRem each,

and

made

no attempt to enter lower containment

from upper containment:

Any attempt to enter lower containment

(where the

instrument

room is located)

from upper containment"would

have required

an

intentional violation of the hatch entry access

controls leading into lower

containment.

During the investigation of this matter,

the licensee

also found that the

entrance

into Unit I lower containment

was not posted

and controlled

as

an

EHRA.

The instrument

room is located

immediately inside the entry hatch

and

although

none of the detectors

from the reactor vessel

were sent to the seal

table in the instrument

room during this specific evolution, the entrance

should

have

been

posted

and controlled

as

EHRA. If the operators

had entered

from the Unit I lower containment

entrance

during in-core detector

movement,

the controls in place to prevent possible

overexposure

consisted of personal

use of alarming

EDs,

area radiation monitors

(ARMs) located inside the

containment

near the instrument

room which had remote annunciator

alarms,

a

requirement to notify the control

room before entry,

and the issuance

of the

lower containment

entrance

lock key by

RP staff.

The investigation of this

event included discussions

with all participants,

and radiation verification

surveys

in both upper

and lower containment during flux mapping operations.

As

a result of the investigation,

the licensee

concluded that there

was not

a

substantial

potential for a whole body overexposure.

The root cause

assessment

indicated there

was

an

RPT personnel

error, procedural

and key

control weaknesses,

and

no verification to ensure

the

IMDS clearance

was not

in effect.

Although the inspector's

review of the licensee's

investigation indicated that

the assessment

of the root causes

and corrective actions to prevent recurrence

was good, the inspectors identified some weaknesses

in the lower containment

alert/control

warning system that were not identified by the licensee

during

followup of this event.

For instance,

after the inspectors

entered

into the

Unit 2 lower containment

near the seal. table during unit operation,

the

inspectors

found that the

ED alarm and warning light worked, but the alarm was

barely audible

because

of the noise level from operating

equipment.

The

inspectors

also noted that in Unit 2 there

was

an operable

seal table area

. radiation monitor

(ARM) with a local warning light and alarm function with the

alarm setpoint at

20 mR/hr.

However, the Unit I seal table area

ARM did not

'have local alarm

and

a warning light, but instead

had annunciator

alarms in

the control

room and in a designated

RP office in the turbine building; the

alert alarm set point was

20 mR/hr and the high alarm was set at

100 R/hr.

Because

these

weaknesses

in the Unit I alarm /control warning

system

(no local

alarm

and warning light,

a high

ARM set point and possible

inaudible

EDs in

noisy areas)

were not identified in the condition report for the subject

radiological event,

no corrective actions would have

been taken to strengthen

the alert/control

warning system.

The inspectors

discussed

this matter with

the licensee

who indicated that these

weaknesses

were corrected

by installing

an interim local

ARM with both audible

and visible functions

and

an alarm set

point of 20 mR/hr in Unit I;

a permanent

system revision will.be

made in the

near future.

Although .there were

19

weaknesses

in the overall control of this evolution

and in the alert/control

system, it did not appear likely that there

was

a substantial

potential for a

whole body exposure

in excess of regulatory limits.

5.0

PERSONS

CONTACTED AND MANAGEMENT MEETINGS

The inspectors

contacted

various licensee

operations,

maintenance,

engineering,

and plant support personnel

throughout the inspection period.

Senior personnel

are listed below.

At the conclusion of the inspection

on August 17,

1995, the inspectors

met

with licensee

representatives

(denoted

by *) and summarized

the scope

and

findings of the inspection activities.

The licensee

did not identify any of

the documents

or processes

reviewed

by the inspectors

as proprietary.

  • A. A. Blind, Site Vice President/Plant

Manager

  • K. R. Baker, Assistant

Plant Manager-Operations

  • J.

R.

Sampson,

Assistant Plant Manager-Support

  • D. L. Noble, Radiation Protection Superintendent
  • T. K. Postlewait,

Site Engineering

Support

Manager

  • J. S.

Wiebe, Superintendent,

Plant Performance

Assurance

L. H. Vanginhoven,

Superintendent,

Material

Management

  • W. M. Hodge,

Plant Protection Superintendent

  • W. A. Nichols, Acting Operations

Superintendent

  • G. A. Weber, Superintendent,

Plant Engineering

  • M. E. Barfelz, Superintendent,

Nuclear Safety

8 Analysis

"A. A. Lotfi, Superintendent,

Site Design

  • J.

D. Allard, Maintenance

Superintendent

  • D. 0. Morey, Chemistry Superintendent
  • D. M. Fitzgerald,

Superintendent,

Environmental,

Safety

and Health

  • T. P. Beilman, Superintendent,

Integrated

Scheduling

  • T. E. guaka,

Superintendent,

Project

Management

and Installation Services

  • P.

G. Schoepf, Staff Assistant

20