ML17331B373

From kanterella
Jump to navigation Jump to search
Insp Repts 50-315/94-06 & 50-316/94-06 on 940328-0401. Violations Noted.Major Areas Inspected:Radiation Protection Program Including Audits & Appraisals,Internal Exposure, Outage ALARA & Contamination Control
ML17331B373
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 04/29/1994
From: Cox C, Grobe J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17331B371 List:
References
50-315-94-06, 50-315-94-6, 50-316-94-06, 50-316-94-6, NUDOCS 9405100035
Download: ML17331B373 (7)


See also: IR 05000315/1994006

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION III

Repor t Nos.

50-315/94006(DRSS);

50-316/94006(DRSS)

Docket Nos. 50-315;

50-316

Licensee:

Indiana Michigan Power

Company

1 Riverside

Plaza

Columbus,

OH

43216

.License

Nos. DPR-58;

DPR-74

Facility Name:

D.

C.

Cook Nuclear Plant, Units

1 and

2

Inspection At:

D.

C.

Cook Site,

Bridgman, Michigan

Inspection

Conducted:

March 28 through April 1,

1994

Inspector:

.R.

o

Approved By:

n

.

ro e,

cting

ie

eactor Support

Programs

Branch

'

e

I

Ins ection

Summar

Ins ection

on March 28 throu

h

A ril

1

1994

Re ort Nos.

50-315

94006

DRSS

and 50-316

94006

DRSS

Areas Ins ected:

Routine inspection of licensee's

radiation protection

program (IP 83750),

including audits

and appraisals,

internal

exposure,

outage

ALARA, and contamination control.

In addition, the inspector

reviewed

licensee follow up to a previous violation and to previously identified

inspection

items.

Results:

The licensee's

radiation protection program

was generally well',

conducted.

Low source

terms

were attributed to good shutdown chemistry

control

and decontamination

of hot spots.

Overall station cleanliness

was

excellent but problems in cleaning

up after jobs were noted in containment.

A strength

was noted in the quality of the radiation protection

and chemistry

guality Assurance

audit tea'm.

Some problems

were noted in ALARA planning

reflected

by exceeding

the

ALARA dose goals for the outage.

One violation of

NRC requirements

was identified as

a result of a resin spill and associated

personnel

contaminations.

9405l00035

940429

PDR

ADOCK 050003l5

'Q

PDR

DETAILS

Persons

Contacted

  • B. Auer, Site guality Assurance

Auditor

  • W. Burgess,

Superintendent

Scheduling

  • J. Fryer,

General

Supervisor Radioactive Material Control

  • L. Gibson, Assistant

Plant Manager

  • J. Lyon, Secretary,

Radiation Protection

  • D. Morey, Superintendent

Chemistry

  • D. Noble, Superintendent

Radiation Protection

  • H. Springer,

ALARA Supervisor

  • R. West,

Licensing Coordinator

  • J.

S. Wieble, Superintendent

guality Assurance

and Control

  • J.

Isom, Senior Resident

Inspector

The inspector

also interviewed other licensee

personnel

in various

departments

in 'the course of the inspection.

  • Present at the Exit Meeting on April 1,

1994

Licensee Action on Previous

Ins ection Findin

s

IP 92701

Closed

Ins ection

Fol 1owu

Item

IFI

315 92017-01

316 92017-01

Radiological liquid release

from condensed

airborne releases

via the

Unit

1 blowdown startup fl'ash tank which discharged

through the storm

sewer

system to Lake Michigan.

A plant modification .package

was

approved

and the modification has

been

scheduled for June

1994.

This

item is closed.

Closed

Notice of Violation

NOV

315 93010-01

316 93010-01

Exceeding

0.5 millirem per hour dose rate limits of Department of

Transportation

(DOT) requirements

during the shipment of an empty

package.

The vendor receiving the package

decontaminated

the package.

Procedure

Number

12

THP 6010

RPP.800

"Preparation of Radioactive

Shipments"

was revised to require

independent

surveys,

use of an optimal

instrument for the surveys,

and incorporated

a checklist to ensure

the

DOT limits for radiation

and contamination

would not be exceeded.

Training on the revised

procedure

was completed

in 1993.

The corrective

actions= appear

adequate.

This violation is closed.

Closed

Notice of Violation

NOV

315 93010-02

316 93010-02

Failure to ensure

surface

doses .rates limits of 0.5 millirem per hour

were not exceeded

on

an empty shipment to guadrex Recycling Center.

Procedure

Number

12

THP 6010

RPP.800

"Preparation of Radioactive

Shipments"

was revised to require

independent

surveys,

use of an optimal

instrument for the surveys,

and incorporated

a checklist to ensure

the

DOT limits for radiation

and contamination

would not be exceeded.

Training on the revised

procedure

was completed

in 1993.

The corrective

actions

appear

adequate.

This violation is closed.

I

Recent

S ent Resin

S ill Event

On Saturday,

March 19,

1994,

contaminated

spent resin

was spilled in the

587 Drumming room during the transfer of spent resin from the Chemical

and Volume Control

System

(CVCS) mixed bed demineralizer to the Spent

Resin Storage

Tank.

The spill was the result of some spent resin being

inadvertently diverted to and overfilling a High Integrity Container

(HIC) in the

Drumming room.

As the resin dried out on the floor of the

Drumming room, the ventilation in the

room spread

the contaminated

resin

into several

areas of the Auxiliary Building causing

20 personnel

to

receive foot contaminations.

Radiation Protection

(RP) personnel

were

alerted to the problem when the contaminated

personnel

alarmed the

personnel

contamination.,monitors

(PCHs)

upon trying to exit the

Radiologically Controlled Area

(RCA).

RP p'ersonnel

quickly responded

by

securing

access

to the Auxiliary Building, locating the source

and

extent of the contamination,

and decontaminating

the affected personnel

'nd affected

areas of the Auxiliary Building.

Full decontamination

of

the Drumming room was completed

several

days later.

Whole body counts

conducted

on the affected

personnel

on March

21 through March 22,

1994,"

indicated there

may have

been four uptakes of the contamination.

Those

four uptakes

indicated approximately 0.1 per cent of the annual limit

for intake (ALI) with the maximum committed effective dose equivalent

(CEDE) of 3 millirem.

While the radiological significance of the contaminations

appears

minor,

the events that lead to the inadvertent diversion of the spent resin to

the

HIC raised

some concerns.

On Friday,

March 18,

1994, the Radio-

active Waste Handling Supervisor

(RWHS) tried to conduct

a sluicing of a

new liquid radwaste

processing

system using

a procedure

(12

THP 6010

RPP.606

"Operation of the Radioactive

Waste Water Demineralization

System

(RWDS)") recently revised to conduct the evolution.

The valve

lineup in the procedure

proved to be inadequate

to conduct the evolution

and in the process

of troubleshooting

the valve lineup,

two valves were

left open which led to the diversion of the resin

on the following day.

An Auxiliary Operator

(AO) used

Procedure

02

OHP 4021.007.002

"Reactor

Coolant Demineralizer

Resin Sluicing and Replacement" for the resin

transfer

on March 19,

1994.

That procedure failed to direct the

AO to

verify the position of the two valves that were left open from the

previous

day which provided the alternative flow path.

Also during the

resin transfer evolution, the

AO did note flow noises

from a valve that

should

have

been closed

so

he shut that valve.

Both the

RWHS and the

AO

had indications that their procedures

were inadequate

due to no flow on

the first day

and flow through the valve on the next.

However, the

sluicing operation

attempt continued

as did the resin transfer.

Both

procedure

inadequacies

are considered

a violation of 10 Code of Federal

Regulations

(CFR) Part

50 Appendix

B Criterion

V (315-94006-01/316-

94006-01).

Audits and

A

raisals

IP 83750

The guality Assurance

(gA) department

was recently reorganized

to

strengthen

the licensee's

overall self-assessment

capabilities.

The

,3

reorganization

resulted

in a new Superintendent

of guality Assurance

and

Control.

No major effect from the reorganization

was noted

on

an

already strong chemistry

and radiation protection

gA audit team which

consisted of four auditors.

Team members

had health physics or

chemistry experience.

Several

chemistry

and radiation protection surveillances

were completed

during the outage.

One major finding in chemistry identified

a

continuing negative trend in the Chemistry Department

performance.

A

condition report

was written acknowledging that corrective actions to

previous

problems in procedural

compliance

and document control were

ineffective which resulted

in the negative trend.

A new chemistry

manager

was brought in to address

the negative trend.

Issues identified

in radiation protection during an ongoing work in progress

audit

included not meeting the

ALARA goals,

reviewing the personnel

contamination

incidents

(PCIs) to determine the effect of reduced

respirator

use,

and reviewing the effectiveness

of early boration during

the shutdown

and chemistry decontamination

of the regenerative

heat

exchanger

and the resistance

temperature

detector

(RTD) loops for source

term reduction.

The conclusions

from the work in progress

surveillance

report will be reviewed during the next inspection.

No violations or deviations

were identified.

Control of Radioactive Naterials

and Contamination

Surve

s

and

Honitorin

IP 83750

Tours of the plant

and selected

work areas

did not identify any problems

,in the implementation of the licensee's

contamination control program.

Overall, work areas

were well maintained

and the cleanliness

of the

station

was noteworthy.

An exception to the overall high standard of

cleanliness

at the facility was in containment..

Tie wraps

and other

debris left over from completed jobs were noted accumulating in

containment.

The licensee

planned to clean

up any debris left over from

completed

work towards the end of the outage.

While no foreign material

exclusion

problems

were noted,

the accumulation of the debris

increased

the potential for such

problems to arise.

Also, potentially higher

doses

could

be received

from cleaning

up at the end of the outage rather

than having workers clean

up their work site

on

an ongoing basis.

Through March 29,

1994, there were

205 PCIs,

most of which were

identified during the refueling outage.

While that number

was high,

higher numbers

were expected

due to the reduced respirator

use.

Of the

205 PCIs,

60 were attributed to the

new

10 CFR Part 20 evaluated

conditions,

75 due to personnel

error,

and

107 to facial contaminations.

The high number of facial contaminations

is similar to what other

facilities have

been experiencing with r educed respirator

use.

The

licensee

was re-evaluating

the method

used to determine reportable

contaminations.

Using

a threshold value of total effective dose

equivalent

(TEDE) appeared

to be the approach

they were planning to use.

Any PCI not resulting in a dose

exceeding

the threshold

TEDE would still

be evaluated

and recorded to trend the data,

but would it would not be

considered

reportable.

The methodology

and procedures

implementing the

new system will be reviewed in a future inspection.

No violations or deviations

were identified.

I

aintainin

Occu ational

Ex osures

ALARA

IP 83750

There

have

been

no major changes

in the overall station

ALARA management

program since the previous inspection.

The inspector

reviewed

ALARA

program performance

and initiatives implemented during the on-going

refueling outage.

Six weeks into the outage

had resulted

in 195 person-

rem verses

an

ALARA goal of 135 person-rem,

approximately

140 per cent

off the goal for the sixth'eek of the outage.

A major contributor to

the high dose

appeared

to be the hydro-lazing work causing all four

steam generators

to be drained at the

same time and for a longer period

than the

ALARA planners

expected.

Having all four steam generators

drained at the

same time caused

higher than planned

doses for all the

other activities in the general vicinity of the steam generators.

The'LARA

group estimated that the final outage total exposure

would be 210,

person-rem.

That would place the total outage

exposure

approximately

116 percent

over the total goal of 180 person-rem.

Overall station

dose

rates indicate that the license

has low source

terms.

Therefore,

the

planning problems

encountered

during the outage did not cause

the

ALARA

g'oal to be exceeded

by

a significant margin.

However, the licensee

acknowledged that significant lessons

could

be learned

from the outage

and

be used to better plan the

1994 Unit 2 outage.

Source

term reduction at the facility appears effective as evident

by

the low dose rates

encountered

during the outage.

Efforts included

chemical

cleanup of the reactor coolant

system

performed at shutdown

using acidification of. the coolant

by lithium removal

and boration

followed by addition of hydrogen peroxide

and control of reactor coolant

temperature

to increase

solubilization of crud

and removal

by

demineralizers.

The chemical

cleanup

accounted for the removal of 1279

curies of cobalt-58

and

17 curies of cobalt-60 from the primary system.

A chemical

decontamination

was also performed

on the Regenerative

Heat

Exchanger

and the Resistance

Temperature

Detector

(RTD) loops.

The

decontamination

appeared

very effective for the heat

exchanger

but had

mixed results with the

RTD loops.

The licensee initiated *a more

rigorous dose rate measurement

of the effectiveness

of the

decontamination

by bringing in a vendor to conduct the measurements.

The new data was'eing

analyzed to provide

a baseline for future

decontaminations.

No violations or deviations

were identified.

Trainin

and

uglification of Personnel

Contractor Radiation Protection'Technician

qualifications were reviewed

by the inspector.

The screening

process for the technicians

involved

the contractorsite representative

reviewing resumes

and sending the

licensee

a list of potential

candidates

with their qualifications.

Likely candidates

would have their references

checked.

As an additional

screening tool,

an examination

developed

by another utility would be

administered

by the facility., Test scores

would be tracked

by the

utility who developed

the examination

and technicians

would be required

to retake the

exam every two years.

The contractor,

the licensee,

and

other licensees

were participating in the program.

No violations or deviations

were identified.

8.

Exit Interview

The scope

and findings of the inspection

were reviewed with licensee

representatives

(Section

1) at the conclusion of the inspection

on

April 1,

1994.

The licensee

did not identify any documents

as

proprietary.

The following specific items were discussed

with the

licensee

during the exit meeting:

o

The resin spill and the resulting violation.

The exceeded

ALARA goal

and the lessons

learned.

The overall station cleanliness

compared to the problems

noted in

containment.

The quality of the guality Assurance

surveillances for Radiation

Protection

and Chemistry.