ML17329A028

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Insp Repts 50-315/91-10 & 50-316/91-10 on 910320-0430. Violations Noted.Major Areas Inspected:Plant Operations, Maint/Surveillance,Engineering & Technical Support & Radiological Controls
ML17329A028
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 05/16/1991
From: Jorgensen B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17329A027 List:
References
50-315-91-10, 50-316-91-10, NUDOCS 9105290156
Download: ML17329A028 (26)


See also: IR 05000315/1991010

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION III

Reports

No. 50-315/91010(DRP);

50-316/91010(DRP)

Dockets

No. 50-315;

50-316

.

Licensee:

Indiana Michigan Power

Company

1 Riverside Plaza

Columbus,

OH

43216

Licenses

No. DPR-58;

DPR-74

Facility Name:

Donald C.

Cook Nuclear

Power Plant, Units

1 and

2

Inspection At:

Donald C.

Cook Site,

Bridgman, Michigan

Inspection

Conducted:

March 20 through April 30,.1991

Inspectors:

J.

A. Isom

D.

G. Passehl

~

~

Approved By:

orge sen,

ie

Projects Section

2A

S

CPl

a

e

Ins ection

Summar

Ins ection from March 20 throu

h

A ril 30

1991

(Re orts

No. 50-315/91010(DRP);

o.

-

1

Areas Ins ecte

outine unannounced

inspection

by the resident

inspectors

o

plant operations;

maintenance/surveillance;

engineering

and technical

,support; radiological controls; actions

on previously identified items; safety

assessment

and quality verification; and,

NRC Region III requests.

Management

meetings

were held at the site between

NRC and licensee

representatives

on

April 2 and 17,

1991.

Results:

Of the

seven

areas

inspected,

no violations or deviations

were

~s enti7ied in six areas.

One violation was identified (inadequate

post-maintenance

testing - Paragraph

3.a) in the maintenance/surveillance

area.

The inspection identified

a weakness

in the post-maintenace

test in the

maintenance

area

and

a weakness

in the operator's

knowledge of the operation

of the liquid in-line rad monitor system

(RS-1000).

There were

no notable

weaknesses

identified in any of the other areas

reviewed.

~P1

0

During this reporting period, both Unit

1 and

2 operated essentially

at

100 percent

power with no major operational

problems.

On April 19,

1991,

Unit

1 entered

a short duration outage to repair the Unit 1 main transformer

and to perform other maintenance activities.

9105290156

910516

PDR

ADOCK 05000315

Q

PDR

Maintenance

and Surveillance:

I

The inspector

s review of the surveillance

and maintenance activities during

this reporting period found that most maintenance

and surveillance activities

were performed satisfactorily.

One problem was identified with improper

reassembly

and inadequate

post-maintenance

testing

on the charging

system

Appendix

R cross-tie isolation valve.

1.

Persons

Contacted

DETAILS

'a ~

Mana ement Meetin

- A ri 1

2

1991

American Electric Power/Indiana

Michi an Electric

E.

T.

P.

A.

J.

K.

B.

R.

J.

L.

J.

E. Fitzpatrick, Vice President,

Nuclear Operations,

AEPSC

0. Argenta, Assistant

Vice President,

Nuclear Engineering,

AEPSC

A. Barrett, Director, guality Assurance,

AEPSC

A. Blind, Plant Manager

E. Rutkowski, Assistant Plant Manager,

Technical

Support

R. Baker, Assistant Plant, Manager,

Production

A. Svensson,

Executive Staff Assistant

F. Kroeger, Division Manager, Electrical Systems,

AEPSC

A. Kobyra, Group Manager,

Nuclear Design,

AEPSC

H. Vanginhoven, Supervisor,

Site Design

B. Kingseed,

Senior Engineer,

Nuclear Safety

and Licensing,

AEPSC

R. A. Green,

Engineer,

Nuclear Safety

and Licensing,

AEPSC

NRC

Re ulator

Commission

(NRC)

A.

C;

H.

J.

M.

H.

J.

T.

E.

D.

W.

B.

J.

J.

A.

A.

B.

A.

G.

R.

G.

D.

Davis, Regiona'l Administrator, Region III

Paperiello,

Deputy Regional'dministrator,

Region III

Miller, Director, Division of Reactor Safety,

Region III

Zwolinski, Assistant Director for Region Reactors,

NRR

Ring, Chief, Engineering

Branch,

DRS, Region III

Clayton, Chief, Branch 2, Division of Reactor Projects,

RIII

Isom, Senior Resident

Inspector

Colburn, Licensing Project Manager,

NRR

Schweibinz,

Senior Project Engineer,

DRP, Region III

Passehl,

Resident

Inspector

Pegg, Intern,

NRR

b.

Mana ement Meetinq - A ril 17

1991

Ameri can

E 1 ectri c Power/Indi ana

Michi an Electr ic

D.

T.

S.

A.

L.

K.

J.

R.

H.

0.

J.

A.

S.

R.

E.

A.

Williams, Jr., Senior Executive Vice President,

AEPSC

Argenta, Assistant

Vice President,

Nuclear Engineering,

AEPSC

Brewer, Manager,

Nuclear Safety

and Licensing,

AEPSC

Blind, Plant YIanager

Gibson, Assistant Plant Manager-Projects

Baker, Assistant Plant Manager-Production

Rutkowski, Assistant Plant Manager-Technical

Support

Green,

Engineer,

Nuclear safety

and Licensing,

AEPSC

Nuc'lear

Re ulator

Commission

(NRC)

-K. M. Carr,

Chairman

A. L. Vietti-Cook, Chairman's

Technical Assistant

'.

J. Paperiello,

Deputy Regional Administrator, Region III

J.

A. Isom, Senior

Resident

Inspector

D. G. Passehl,

Resident

Inspector

E.

E. Hayden, Public Affairs staff

c.

Routine Ins ection

  • A. A. Blind, Plant Manager

J.

E. Rutkowski, Assistant Plant Manager - Technical

Support

  • L. S. Gibson, Assistant Plant Manager - Projects
  • K. R. Baker, Assistant Plant Manager - Production
  • B. A. Svensson,

Executive Staff Assistant

  • J. R.

Sampson,

Operations

Superintendent

P.

F. Carteaux,

Safety

and Assessment

Superintendent

T. P.

Bei lman, Maintenance

Superintendent

  • T. K. Postlewait,

Design

Changes

Superintendent

  • L. J. Matthias, Administrative Superintendent

J. T. Mojcik, Technical Superintendent

- Physical

Sciences

  • M. L. Horvath, guality Assurance

Supervisor

D. C. Loope, Radiation Protection Supervisor,

The inspector

also contacted

a number of other licensee

and contract

employees

and informally interviewed operations,

maintenance,

and technical

personnel.

  • Denotes

some of the personnel

attending

the Management

Interview on

May 3,

1991.

2.

0 erational Safet

Verification (71707

71710

42700)

Routine faci.lity operating activities were observed

as

conducted

ir, the

plant and from the main control rooms.

Plant startup,

steady

power

operation,

plant shutdown,

and system(s)

lineup and operation

were observed.

The performance of licensed

Reactor Operators

ard Senior Reactor Operators,

of Shift Technical Advisors,

and of Auxiliary Equipment Operators

was

observed

and evaluated

including procedure

use

and adherence,

records

and

logs, cohmunications,

and the degree

of professionalism of control

room

activities.

The Plant Manager, Assistant Plant Manager-Production,

and the

Operations

Superintendent

were we'l-informed on the overall status of the

plant,

made frequent visits to the control rooms,

and regularly toured the

plant.

Evaluation, corrective action,

and response

to off-normal conditions or

events,

were examined.

This included compliance with any reporting

requirements.

Observations

of the control

room monitors, indicators,

and

recorders

were

made to verify the operability of emergency 'systems,

radiation monitoring systems

and nuclear reactor protection

systems,

as

applicable.

Unit 1 began

the inspection period at 100 percent

power and operated

routinely until. April 19,

1991,

when

a planned

19 to 27 day outage

began to repair or replace, if necessary,

the main transformer

due

to elevated

levels of combustible

gas.

The outage

was also planned

to repair,a body-to-bonnet

leak on Chemical

and

Volume Control

System valve 1-CS-536.

The main transformer

was in the restoration

phase following repair at the

end of this inspection period.

Other

major activities that were accomplished

included replacement of'he

East Essential

Service

Water Pump,'aterial

condition upgrades

of

the Emergency Diesel Generator

CD, replacement

of the West

Centrifugal Charging

Pump Lubricating Oil Pump,

balance of the

No.

13 Reactor

Coolant

Pump,

and replacement

of the Emergency Boration

Flowpath to Charging

Header Suction valve 1-gMO-410.

The outage

appeared

to be well managed

and all of the scheduled activities were

completed

as intended.

The inspector

accompanied

licensee

personnel

on the containment

closeout tour and noted minor external boric acid

leakage

on

some valves.

The licensee

evaluated

and wrote job orders

to address

these.

The outage

was slightly ahead of schedule at

the close of the inspection period, with the unit in NODE-3 and with

startup testing

in progress.

b.

Unit 2 operated routinely at

100 percent

power throughout the

inspection period.

There were

no significant power reductions

throughout the period.

No violations, deviations,

unresolved or open items. were identified.

3.

Maintenance/Surveillance

(62703)

(42700)

(61726)

Maintenance activities in the plant were routinely inspected,

including

both corrective maintenance

(repairs)

and preventive maintenance.

Mechanical, electrical,

and instrument

and control group maintenance

activities were included

as available.

The focus of the inspection

was to assure

the maintenance activities

reviewed were conducted

in accordance

with approved

procedures,

regulatory

guides

and industry codes or standards

and in conformance with Technical

Specifications.

The following items were considered

during this review:

the Limiting Conditions for Operation

were met while components

or systems

were

removed from service;

approvals

were obtained prior to initiating the

work; activities were accomplished

using approved

procedures;

and post

maintenance

testing

wa's performed

as applicable.

The inspector also reviewed Technical Specification required surveillance

testing

as described

below and verified that testing

was performed in

accordance

with adequate

procedures,

that test instrumentation

was

calibrated,

that Limiting Conditions for Operation

were met, that removal

and restoration of the affected

components

were properly accomplished,

that test results

conformed with Technical Specifications

and procedure

requirements

and were reviewed

by personnel

other than the individual

directing the test,

and that deficiencies identified during the testing

were properly reviewed

and resolved

by appropriate

management

personnel.

The following activities were inspected:

a 0

The inspector's

review of a corrective maintenance activity documented

on Job Order A49131 for valve 1-CS-536 (Unit 1 Chemical

and

Volume

Control System

(CVCS) to Unit 2

CVCS discharge

header),

and his

discussion with the licensee's

maintenance staff on the adequacy

of

the subsequent

post-maintenance

test,

found that because

inadequate

post-maintenanc'e

testing

was performed

on I-CS-536, significant

body-to-bonnet

leakage

was not identified, which placed both units in

a 60 day Limiting Condition for Oper ation

(LCO).

The

LCO was

scheduled

to expire

on April 28,

1991.

Valve 1-CS-536 is a'four inch Conval

Clampseal

valve and is required

to be manually cycled during

a fire as postulated

in 10 CFR 50

Appendix

R, to support the shutdown functions of Unit 2.

During the

1990 Unit 1 refueling outage,

valve 1-'CS-536

was found to be leaking

past its seat.

Consequently,

the valve was disassembled

and the valve

disc and seat

were repaired.

The inspector's

discussion with the

licensee

maintenance staff indicated that during reassembly

of the

valve, the "timing .shim"

may have

been

cocked in such

a way as to

prevent

an adequate

body-to-bonnet'ealing

surface.

The inadequate

sealing of the body-to-bonnet

was not found during post-maintenance

testing of the valve in December of 1990,

because

the specified

post-maintenance

test for leak inspection

was

done with the valve in

the closed position.

Because of valve design

and the source of the

hydrostatic test

medium used,

the pressure

which would have identified

a leaking body-to-bonnet joint was isolated from this region of the

valve with the valve closed.

Although another test

was performed

which cycled the valve to verify its position indicator on the reach

rod,

when this test

was performed,

there were

no requirements

to have

the valve pressurized,

nor was it pressurized

because

of other

unrelated

circumstances.

As

a result,

no pressure

was applied to the

valve when it was cycled and therefore

leakage

from the valve

body-to-bonnet

area

was not detected.

However,

on February

27,

1991, during cycling of opposite Unit 2

crosstie

valve 2-CS-536 after

a packing adjustment,

a significant

body-to-bonnet

leak was identified on 1-CS-536

(see

NRC Inspection

Report 50-315/91004(DRP);

50-316/91004(DRP) ).

When 2-CS-536

was

cycled, full discharge

pressure

from the Unit 2 charging

header

was

applied to the body-to-bonnet

region of 1-CS-536,

which was not

adequately

sealed,

and subsequently

leaked.

Because

of this leak,

the licensee

conservatively

declared

valve 1-CS-536

INOPERABLE.

The

problem placed Unit 2 in a 60 day Limiting Condition For,Operation

(LCO), expiring on April 28,

1991.

Although the licensee initially intended to repair valve 1-CS-536 at

power and submitted

a Temporary Waiver of Compliance

Request to the

NRC to avoid

a shutdown of Unit 1, this request

was retracted.

The

licensee

chose to repair the valve during the planned Unit 1 outage

in which

r epairs to the main transformer

were planned.

The repair t'o

1-CS-536

was completed with the unit in

t~ODE 5, during the beginning

of the outage.

The inspector's

review of the job order and interviews with the

wor kers during the repair of I-CS-536 found that the work was

.performed satisfactorily.

The only problem experienced

by the

licensee

was that the replacement

valve's bonnet

and yoke assembly

had threads that'ould not properly engage

the threads

on the existing

body,

so the bonnet

and yoke assembly of the old valve were re-used.

The licensee

had anticipated this contingency.

The maintenance staff

did use the stem assembly

and packing cartridges

from the

new valve.

A small

amount of lapping

was also performed

on the seat

in the body

of the "old",valve due to slight scoring.

The reassembly

was

completed

and proper post-maintenance

testing

was satisfactorily

performed.

Valve 1-CS-536

was returned to OPERABLE status

on

April 21,

1991.

The inspector

noted that unlike the December

1990 test,

the

post-maintenance

test for the repair of 1-CS-536

completed

on

April 21,

1991 included

an

ASNE Code

YT-2 examination.

The VT-2 test

consisted of a visual inspection for external

leakage,

under normal

operating

pressure,

with the valve in the open position.

The

inspector

noted the results of the VT-2 examination indicated zero

external

leakage.

Also, the inspector

noted acceptable

post-maintenance

test results for internal leak by and valve cycling.

.

10 CFR 50, Appendix B, Criterion XI, as

implemented

by the

D. C.Cook

Updated Quality Assurance

Program Description, Section

1.17.11

(Test

Control), requires that post-maintenance

test prerequisites

be

specified in test procedures

and in the post-maintenance

tests that

are performed in accordance

with-established

programs to demonstrate

that structures,

systems,

and

components will perform satisfactori ly

in service.

The failure in December. of 1990, to establish

the

necessary

post-maintenance

test prerequisite

to pressurize

the

body-to-bonnet

region

and verify Code pressure

boundary integrity,

is an apparent violation of 10CFR50 Appendix B, Criterion XI,

(Violation 315/91010-01).

The inspector

reviewed

a licensee

work activity documented

on Job

Order A57382, associated

with the Unit, 1 Emergency Boration Flowpath

Valve 1-QNO-410.

The valve tripped

on thermal overload during

a

weekly surveillance test to check the emergency

boration flowpath

for blockage.

During the test,

the valve had failed to indicate the

full open position,

and Naintenance

Department

personnel

found upon

investigation that the valve disc

had

jammed into the seat.

The

cause of the problem was

a too high torque switch setting.

The

licensee

is still investigating whether the torque switch was

mispositioned

or had drifted from the proper setting.

Motor operated

globe valve I-QNO-410 controls the flow of fluid from

the boric acid transfer

pumps to the emergency

boration line.

The

valve is operated

to initiate emergency boration flow directly to

the suction of the charging

pumps.

J li

0

The inspector

reviewed the procedure

    • 12 NHP 5021.001.009,

"Disassembly,

Inspection,

Repair and Reassembly

of Velan Manual

and

Motor Operated

Gate Valves" (rev.3), which was used to work the

valve.

The procedure

was used for disassembly

and reassembly

of the

valve only, and was found to be proper ly documented.

However the

inspector

noted that the procedure

was written for work associated

with a gate valve,

and I-(NO-410 is a globe 'valve.

The inspector

questioned

whether

a more appropriate

procedure

to use would have

been **12 NHP 5021.001.052,

"Inspection

and Repair of Hand and Motor

Operated

Velan Globe Valves.."

The licensee replied that procedure

052 is used for work associated

with bonnetless

valves,

and that the

database

the plant uses to prepare

such jobs specified that procedure

.009 be used.

Procedure

.009

was

used only to disassemble

and

reassemble

the valve and

was adequate for those

purposes.

However,

it also appears

the licensee

does not have

an adequate

procedure

to

address

inspection

and repair of globe valves with bonnets

like

1-(NO-410.

The licensee replied that procedure

.009 would be

modified to address

Ye'1an globe valves.

The modifications would

apply only to the section of the procedure that addresses

the plug

and seats

of the valve.

Upon disassembly

the valve was determined to

be irrepairable,

and

a spare

valve was unavailable

from the licensee's

stock.

A search

was begun for a suitable

replacement

valve, which

was finally obtained, through Westinghouse.

A modification package

was prepared

as the licensee

was unable to procure

an exact

replacement.

The upstream

and downstream piping was modified to

allow the valve stem to sit vertically.

Some pipe supports

were

also re-configured.

A post-modification hydrostatic test and,valve

stroke for Inservice Testing were performed

and the results

were

satisfactory.

The post-maintenance

tests for leakage

and valve

position indication were performed with satisfactory results.

The

inspector

reviewed the Operations

Department surveillance

procedures

for the Boration Flowpaths,

which included

a functional test of

l-gN0-410.. The results of the surveillances

were satisfactory,

and

all acceptance

criteria were met.

The inspector

observed

corrective maintenance

on valve 2-lNO-220

(3-way selector

va1ve for No.

22 steam generator

main steam

stop

valve) and reviewed Job Order B21616, which was written to document

the activity.

The maintenance activity involved

a repack of the

valve because

of excessive

packing

leakage.

Valve 2-NNO-220 is used

for testing

the two pneumatically-operated

dump valves associated

with no.

22 steam generator

main steam stop valve

(NSSV).

The

review found that the corrective

maintenance

was performed

satisfactorily.

Post-maintenance

testing for leak inspection

and

valve stroke

was also performed satisfactorily

and all acceptance

criteria were met.

The

NSSV was returned to OPERABLE status within

the time frame allowed by the Technical Specification Limiting

Condition for Operation

(T/S LCO).

The licensee

decided to work the valve as part of the attempt to

reduce

the large backlog of'pen job orders,

roughly half of which

were written to address

leaking valves.

The Maintenance

Department is

in the process of forming a "valve improvement

team" to address

valve

problems.

The packing

'leak was not of a magnitude that would have

caused

inadvertant

closure of the NSSV, nor did it appear to have

any other noticeable

negative affects

on the

NSSV.

The licensee

made

a voluntary four hour T/S

LCO entry to repair the

valve, because

one of'he

MSSV dump valves

had to be isolated to do

the work.

The valve was repaired

and tested satisfactorily within a

period of about three hours.

The other

dump valve could have lifted

and closed the

NSSV upon receipt of the appropriate actuation

signal, but the valve was

assumed

not to function when required

because

of single-failure consideratsons.

The inspector

observed corrective maintenance

on components

associated

with the Unit

1 East Motor-Driven Auxiliary Feedwater

Pump

(EMDAFP).

Job Orders

(JOs)

A3507 and A53054 were written to

document the activity and were also reviewed.

The work involved a

repack of ENDAFP discharge

valve 1-FW-130

(JO A3507) and repair of

an oil leak on the

pump inboard bearing

(JO A53242).

The observations

and reviews found the work was performed satisfactorily within the

time constraints

allowed by the Technical Specification Limiting

Condition for Operation

(T/S LCO).

Post - maintenance

testing

was

also performed satisfactorily

and all acceptance

criteria were met.

The

pump was

INOPERABLE for 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />

29 minutes,

which was within the

72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> T/S

LCO Action Statement.

The packing leak on I-FR-130 was noted to be approximately 100'drops

per minute with the

pump running and was discovered

during

a run of

the

ENDAFP during emergency

diesel

generator

load sequence

testing

in October

1990.

The problem was not addressed

during the outage

because it was not identified until the work package

"window" on the

EMDAFP had been essentially

closed.

Thereafter

the problem was not

significant enough,

according

to the licensee,

to warrant removal of

the

pump during plant operation

unless

other jobs

needed

to be

performed.

The packing leak represented

an insignificant amount of

water inventory withheld from the steam generators.

The inspector

noted

no problems with the work and noted that the job order was

properly documented.

The post-maintenance

test consisted of a leak

inspection

and stroke

check of the valve,

and the results

were

satisfactory.

Additionally, no leaks were noted during the mohthly

surveillance

run that was performed after the work and prior to the

pump's

OPERABILITY declaration.

The magnitude of the 'oil leak on the inboard

pump bearing

was

slight, according to the licensee,

as evidenced

by the oi'l drops

found below the be'aring

on the

pump skid.

This problem was

discovered

by an operator while making tours of the plant in

January,

1991.

This work item 'also

was not significant enough to

warrant

removal of the

pump from service during plant operation,

and

was worked with the repack job described

above to minimize the

amount of time the

pump was

removed from service.

Operators

monitor

the oil level in the bearing via

a sight glass

on

a, shiftly basis.

No instances

of unacceptable

oil 'level were noted during tours

by the

plant operators.

A large oil leak would cause

problems if left

One

unchecked

and could stall the

pump.

The repair work involved slight

adjustment to a "slinger ring", which rides

on the

pump shaft with a

close tolerance

to the face of the bearing housing,

and serves

to

redirect

any escaping oil back into the bearing

housing

sump.

An oil

level adjustment

mechanism

was also set because

the oil level in the

bearing

sump was slightly high,

and

may have contributed to the leak

problem.

The post-maintenance

test consisted of a leak. check with

the

pump in operation,

and again

no problems

were noted.

The inspector

reviewed the surveillance test

documentation for the

Et1DAFP that was performed just after the maintenance

work described

above.

This scheduled

monthly test

was also performed to verify

OPERABILITY of the

EMDAFP in accordance

with the Technical

Specifications,

which included verification of the correct position

of all valves in the flowpath.

The inspector

found the surveillance

procedure,

    • I-OHP 4030.STP.OI7E,

Rev.5,

"East Motor Driven Auxiliary

Feedwater

System Test", to be complete

and noted

no problems.

The

procedure

instructions

were clear

and all data

was properly documented.

All acceptance

cr iteria were met.

violation, and

no deviations,

unresolved or open

items were identified.

4.

En ineerin

and Technical

Su

ort (37701

37828)

The inspector monitored engineering

and technical

support activities at

the site and,

on occasion,

as provided to the site from the corporate

office.

The purpose of this monitoring was to assess

the adequacy of

these functions in contributing properly to other functions

such

as

operations,

maintenance,

testing, training, fire protection

and

configuration management.

The inspector

reviewed the results of the licensee's

evaluation of

degradation

found with the incore flux thimble tubes during eddy

current examinations

performed during the

1990 refueling outages.

The results

confirmed the licensee's

suspicion of flow induced

vibration as root cause.

The flow induced vibration was believed to

have occurred at the lower core plate area

where the vibrations

would be most prominent.

The Unit

1 tube wear was not as

pronounced

as that found in the Unit 2 tubes,

which the licensee

believed

was

probably

due to the different flow characteristics

of the two units.

The licensee

plans to perform

some type of corrective action during

the

1992 refueling outages,

.in an attempt to reduce

the wear rate.

Several

technologies

are presently being investigated.

The licensee

is tending toward application of a wear resistant

coating to the

surface of the tubes,

to improve the lifetime of the tubes while

minimizing the risk of increasing

the vibrations.

The Unit 2 inspections

were performed in the

Summer

and Fall of 1990,

and resulted

in the replacement

of. 10 tubes

and the reposition

20

of 19 tubes.

The Unit 1 inspections

were performed in the Fall of

1990,

and resulted

in the reposition of 29 tubes.

The licensee

made

various submittals to

NRC at the time describing. the eddy current

examinations

and results.

The licensee,

accompanied

by

representatives

from Westinghouse,

made

a presentation

to

NRC at the

Headquarters

office on ApriI'l, 1991 to summarize

the results of

the root cause investigation.

To support the root cause

ihvestigation,

two of the degraded

Unit 2 flux tubes

were shipped to

a hot cell facility for examination.

Additionally, the inspector

noted that

on March 12,

1991, four

isolation valves

on the Unit 2 flux mapping

system were closed

as

a

proactive

means to reduce

the possible

damage to the flux mapping

system should those

tubes experience

a leak.

Three of the four

thimbles that were isolated

(C-7, A-9, and K-2) corresponded

to the

tubes that exhibited the most degradation.

The remaining thimble

(B-13) was isolated

due to its inaccessibility,

which was discovered

during containment

closeout activities during the last refueling

outage.

The isolation of the four tubes is not significant from

a'echnical

Specifications

(T/S) standpoint.

The T/S requires

75 percent of the tubes (or 44 total) be

OPERABLE; there are currently

54

OPERABLE tubes

remaining.

Following cleaning

and testing of the system,

the licensee

found

they were unable to run

a detector

through thimble B-13 to the top

of the core.

The licensee

believed the blockage

was related to the

leak in thimble C-7 that was identified on brune

18,

1990.

The steam

formed in C-7 at the time of the leak may have

caused

some slight

drainage of oil from the associated

ten path gear box, which may

have left an oil residue

in the B-13 tube that the cleaning

process

did not remove.

The licensee

stated that in the event that one of

the thimbles (except

B-13) be

n'ceded for a rod position determination,

the isolation valve could be re-opened for the

map and then isolated.

The thimbles were to remain isolated .at all other times.

The inspector

reviewed the program and the results of the licensee's

zebra

mussel control-strategy.

The program was reviewed

because

treatment

procedures

using the molluscicide "Clam-'trol" had begun

this inspection period for the control of the mussels

in the Service

Water

and Fire Protection

Systems.

The licensee

repo'rted

good

results with the Clam-trol treatments,

based

on mortality rates of

about

95 to 100 percent

in the nonessential

service water

(NESW) and

essential

service water

(ESW) systems

in both units.

Treatments

to

the Fire Protection

System were judged to be

100 percent effective.

The licensee

obtained

some suspect

data while treating

a part of the

Unit 1

NESW and the Unit 2

ESW system

because

of flow adjustment

problems

through the sample points,

and in these

cases

results

were.

conservatively

estimated

to be roughly 80 percent,

which was still

judged acceptable.

The acceptance

criteria for mussel mortalities

has

not been rigorously established,

and will become

more refined

as

the"

licensee

gains

more experience

in doing these

treatments.

11

The treatment

was timed for the present

period in order to assure

"clean" Service Water and Fire Protection

Systems,

in preparation

for a May 1991 chlorine treatment,

which will be performed for scale

and algae control as the lake water temperature

rises.

The chlorine

treatment also prevents

settlement of veligers (free swimming zebra

mussel

larvae), but it does not kill existing adult mussels.

The

licensee's

basic strategy for the zebra

mussel

control is'

two par t

program that includes

a plan to eradicate existing populations

within the plant's

raw water systems,

and

a control program to

.

either ki 11 or hinder settlement of veligers, juveniles,

and adult

mussels within the systems.

In order to monitor the

treatment'esults,

the licensee

connected

"bioboxes" to the treated

systems

at

various

sample points.

The bioboxes

were then

seeded with zebra

mussels for an acclimation period prior to the Clam-trol treatment,

and afterwards

monitored for extermination.

Because

the licensee

has

not yet detected

any significant numbers of zebra

mussels

in their

water systems,

the mussels for seeding

the bioboxes

had to be obtained

elsewhere,

in this case

Lake Erie. 'rogram upgrades

are still being

investigated

which would provide for more accurate

assessments

of

mussel

population density

and distribution.

,No violations, deviations,

unresolved

or open

items were identified.

5.

Radiolo ical Controls

(71707)

During routine tours of radiologically controlled plant facilities or

areas,

the inspector

observed

occupational

radiation safety practices

by

the radiation protection staff and other workers.

a ~

The inspector

reviewed

a March 8,

1991 event

when

a sampled but

unmonitored liquid release

occurred.

The problem involved

a release

of the contents of the No.

4 Monitor Tank, which is part of the l!aste

Disposal

System.

In accordance

with the licensee's

procedures,

the

tank was isolated

and properly sampled for release;

however,

the

in-line monitor (RRS-1000)

apparently

"locked-up" in a 'way that

valve 12-RRV-285 (Radioactive Liquid Waste Disposal to Discharge

Tunnels Shutoff) should

have received

a closure signal which would

have isolated

and terminated

the liquid discharge.

The event

apparently

resulted

in a violation of Technical Specification 3.3.3.9.

The inspector

noted that although the release

was well below the

10 CFR20 Maximum Permissible

Concentration

(MPC) limits, there

was

a

lack of operator

knowledge about the system.

Because

the system is

complex, the licensee

took appropriate

steps

to lessen

the burden

on

operators

to help avoid future mistakes.

The Technical Specification required,

in part, that with an

INOPERABLE in-line monitor, at least

two independent

samples

be

analyzed for radionuclide

makeup

and concentration prior to release.

The licensee

believed the monitor was

OPERABLE during the release,

and discovered just as the release

was terminated that the monitor

in fact was

INOPERABLE.

The licensee

reported

the event to the

NRC

in Licensee

Event Report

(LER) 315/91003;

12

The licensee's

analysis of the sample

showed that the Maximum

Permissible

Concentration

(MPC) value released

was about 3.70E-4,

which was below the

lOCFR20 limit of 1.00

MPC.

The primary cause of

the event

was attributed to

a crushed detector

cable associated

with

RRS-1000.

The licensee

was unable to determine

how or when the cable

was crushed.

A secondary

cause of the event

was operator failure to

recognize

the inoperability condition of the monitor.

The problem occurred

when Operations

personnel

began

the four hour

liquid waste discharge.

About one half hour into the discharge,

operator s received

an "external failure" status

alarm, which

automatically terminates

the release,

and is entered

when sample

flow is out of the normal range.

It is usually indicative of sample

flow adjustment

problems.

In accordance

with the procedure

    • 12-ONP 4021.006.004,

"Transferring Distillate From Monitor Tank",

the release

was re-started

and sample flow was re-adjusted.

About one

half hour later, the release

automatically terminated

again because

of

a flow adjustment

problem.

The RRS-1000 monitor then

made several

status

changes

between

"external failure" and "hi fai 1".

The hi fail

alarm should

have provided

a trip signal to the discharge

isolation

valve (RRV-285), and should not have allowed restart of the release.

An operator monitoring the release

erroneously

reasoned

the hi failure

alarm was invalid because

the detector

response

appeared

normal

and

below the high alarm setpoint.

The licensee later determined

the

hi fail alarm was valid, as evidenced

by the monitor values given on

the printout that were obtained at the conclusion of the discharge.-

To prevent recurrence,

the release

procedure

was upgraded

and would

require additional

channel

checks during the release

that would help

confirm abnormal conditions

and ensure

proper operation of the monitor.

A requirement

was also

added that operators

would terminate release

upon receipt of ~an

alarm, including

a trend alarm.

A preventive

maintenance

program was also developed for the monitor.

The crushed

detector

cable

was replaced

and the circuit boards

were removed,

inspected,

and reinstalled.

No problems

were noted that required

replacement

of the circuit boards.

This matter will be reviewed further during followup on the

referenced

Licensee

Event Report.

On April 2, 1991,

two maintenance

instructors

were exploring the

plant scrapyard for items that could be incorporated

into their

program

as training aids.

They discovered

a Reactor Coolant

Pump

Seal insert that appeared

to have

been installed at one time.

The

men took the insert into the Training Building where

a Radiation

Protection Instructor surveyed it and found

a small

amount of fixed

contamination.

The plant radiation protection staff was notified of

the incident and

an investigation

commenced.

The seal insert

was confiscated

and personnel

cordoned off the area

of the scrapyard

where the piece

was found.

An extensive

survey of

the Training Building was conducted

and

no radiation or contamination

levels greater

than background

were found.

Seven additional

items

with small

amounts of fixed contamination

were found in the

same

area

13

of the scrapyard

as the insert.

No removable

contamination

was

detected.

Numerous soil samples

were obtained

from the scrapyard

and

no activity greater

than background

was detected.

Well water sample

documentation

was researched

and

no activity above background

was

noted.

The contaminated

items

have

been

removed from the scrapyard

and were taken to the Auxiliary Building.

The affected area of the

scrapyard

was surveyed

and

no further contamination

was found.

The investigation determined that the. contaminated

items were removed

from the Auxiliary Building in the mid to late 1970's.

The plant's

release criteria for radioactive material

were not as conservative

then

as they. are

now.

The requirement

now is that

no material

can

be released if there is any detectable

radioactivity present.

According to the licensee,

this incident presented

no exposure

hazard

to plant employees

or the general public.

No removable

contamination.

was detected

and all soil and water sample

data indicated

no activity

above background.

A full description of the event

was given to

NRC

Region III Radiation Specialists for followup action.

No violations, deviations,

unresolved

or open items were identified.

6.

Actions on Previousl

Identified Items. (92701

92702)

The inspector

reviewed the following six inspection findings from the

NRC

Emergency

Operating

Procedure

(EOP) Inspection

Team.

The

EOP inspection

was conducted

from July 5-15,

1988.

The review of the licensee's

response

to these findings from the

EOP inspection

involved direct observation,

discussion with licensee

personnel

and review of records.

a ~

b.

(CLOSED)

EOP Inspection Finding 316/88017-01:

The

EOP inspection

team found through in-plant and control

room walkthroughs of the

emergency

and abnormal

procedures

listed in Appendix

A of the report

that instrumentation

and control labeling

on the control board

and

" the nomenclature

used in the procedures

were inconsistent.

The

discrepancies

determined

by the inspection

team to be significant

were identified in Appendix

C of the

EOP report.

The

EOP inspection

team

recommended

that the licensee

review and resolve not only those

discrepancies

identified in Appendix C, but also pe'rform

a

procedure/control'board

labeling review and evaluate all discrepancies.

The inspector's

discussion

with the Operations

department staff

found that all discrepancies

identified in Appendix

C of the report

were corrected.

Additionally, procedure/control

board labeling

review was completed

in Nay and June

1991 for Unit I and Unit 2

respectively,

and all significant labeling discrepancies

identified

from this review were corrected.

The inspector also performed

an

independent

check of roughly 20 percent of the deficiencies

identified in Appendix

C and noted that these deficiencies

had been

incorporated

into the licensee's

EOPs.

(CLOSED)

EOP inspection finding 316/88017-02:

The

EOP team

identified numerous

recommendations

to the licensee's

EOPs in

Appendix

B of the report.

The Appendix

B contained

some

20 pages of

14

P

I

~

technical

and writer's guide comments,

observations

and suggestions

for EOP improvements

made by the

EOP inspection

team.

Although the

majority of the

comments

were not regulatory requirements,

the

,

licensee

agreed

to evaluate

the

comments

and take appropriate

corrective action.

The inspector's

review of the licensee's

response

and discussion

with the operations staff found that

a majority of the technical

and

human factor discrepancies

outlined in Appendix

B of the

inspection report were corrected.

Those discrepancies

which were not

adopted for incorporation

as

recommended

by the

EOP inspection

were

documented

in Attachment

B of the

"NRC

EOP Audit Close Out Report."

The inspector's

review of Attachment

B of the licensee's

"NRC

EOP

Audit Close

Out Report" found that the licensee's justification for

not incorporating these

discrepancies

appeared

to be reasonable.

Additionally, the inspector

performed

an audit of approximately

10 percent of the procedures

identified in Appendix

B of the

EOP

report

and found that these

recommendations

had been

incorporated into

the licensee's

EOPs.

c ~

t

(CLOSED)

EOP inspection finding 316/88017-03:

The

EOP inspection

team identified two procedures

which were determined

to be inadequate.

"Reactor Shutdown from Hot Standby

Panel

due to Control

Room

Inaccessibility" procedure,

2-0HP-4023.001.011,

Rev. 2, contained

insufficient direction in that the majority of the procedure

appeared

to be an inventory of the instrumentation

and controls available'to

the operator at the hot standby panel.

Little guidance

was provided

on the control of the unit following a reactor trip when evacuation

of the control

room is,required.

Additionally, although discussions

with the licensee

indicated that this procedure

was to be implemented

in conjunction with existing plant procedures,

no reference

was

made

to the existing normal,

abnormal or emergency

procedures

within the

hot standby

procedure.

The second

inadequate

procedure,

"Loss of Control Air,"

2-0HP-4023.001.006,

Rev. I did not identify the instrumentation that

would be inoperative following a loss of control air.

The inspector

performed

a limited review of procedure

"Emergency

Remote Shutdown",

2-0HP-4023.001.011,

Rev. 3, Oct.

10.

1989.

The

procedure

appeared

to be adequate

and provided adequate

guidance

on

steps

required to place the Unit in a hot standby condition from the

hot standby

panel

in the event the evacuation of the control

room

became

necessary.

The inspector also performed

a limited review of procedure

"Loss of

Control Air," 2-0HP-4023.001.006,

Rev.

2, Apr. 17,

1989,

and found

that it listed the expected

responses

of various instruments/valves

to

a complete

loss of control air,

as well as the expected

response

of essential

valves in the plant due to

a complete

loss of control

air.

15

4

II

(CLOSED)

EOP inspection finding 316/88017-04:

The

EOP ins~ection

team

found out-of-date Attachments

"A" and,"B" used in ECA-O.O,

'Loss of All

-AC Power" and FR-Z.1,

"Response

to High, Containment Pressure."

The

Attachments

are

used to verify that the applicable valves'close

on

either

Phase

"A" or Phase

"B" containment isolation signals.

They

were apparently

not revised

when Attachments

"A" and "B" of E-O,

"Reactor Trip or Safety Injection", procedure

were revised to correct

several

errors

in the listing of valves.

Because

Attachments

"A" and

"B" to ECA-O.O and FR-Z.l were not revised at the time that procedure

E-0 was revised,

these

two attachments

contained

both missing

and

erroneous

information.

Additionally, Phase

"A" isolation valve

2-GCR-314

was not labeled

on the safety injection/accumulator

panel

as

a Phase

"A" isolation valve nor was it included

on Attachment "A",

Rev.

0 or 1.

The inspector

reviewed Attachments

"A" and "B" to ECA-O.O and FR-Z.I

and found that these

attachments

now contain the current listing of

the va1ves

under the proper 'attachments.

However, the inspector

noted

a minor discrepancy with the valve description of 2-ECR-32

which was identified as

"LMR CNTMT air SMPL to RMS/PASS" in

Attachment

B of procedure

E-O,

ECA-O.O and FR-Z. 1.

The valve

description

should read

"LWR CNTMT air SMPL to ERS-2300."

The

licensee.

'issued

a request to correct this deficiency.

Additionally, the inspector

noted through direct observation

in the

control

room that valve 2-GCR-314 is

now labeled

as

a Phase

"A"

isolation valve and it is included

as

a Phase

"A" isolation valve in

Attachment "A" to procedure

E-O,

ECA 0.0 and

FR-Z. I.

(CLOSED)

EOP inspection finding 316/88017-05:

The

EOP inspection

team was concerned with the controls for review and revision of

the

EOPs which existed at the time of the inspection.

The

EOP team

found that prior to final approval

and implementation of the

EOPs,

neither

gA nor other management

control groups

performed

an adequate

detailed technical

review.

Consequently,

the

EOP team

recommended

that the licensee:

(1)

Conduct wa1kthroughs of the procedure

in the control

room and

in the plant.

(2)

Conduct

a verification of technical specification requirements.

(3)

Conduct

a evaluation of the review and revision process

as it

applies to EOPs.

The inspector

was informed by the Operations

department staff that

100,percent

wa'Ikdown on the

EOPS

was completed

in about June of 1989

for both Units and all discrepancies

identified were corrected.

Also, the inspector

was informed that they

had conducted

verification of Technical Specifications

requirements utilizing two

different individuals for the purpose of performing

an independent

check to ensure

containment isolation valves

have

been

included in

the procedures.

Additionally, the licensee

has

issued

procedure

"Emergency Operating

Procedure

(EOP) Maintenance,"

Rev. 0,

16

'

March 31,

1989, which details the administrative requirements

with respect

to detailed verification/validation procedure,

processing

and prioritization comments.

f.

(OPEN)

EOP inspection finding 316/88017-06:

EOP inspection

team

identified a large

number of EOP procedure

comments

(well over

a

hundred

items of various kinds)

had been

accumulated for which the

final action

had not been taken.

The

EOP team viewed the failure to

make timely and thorough revisions to

EOPs concerning certain

known

deficiencies to be

a significant weakness.

, The inspector's

review found that currently there are about

40

EOP

comments

which require resolution.

These

comments

were found to be

prioritized into three categories:

"Priority Level

One

(1) - Immediate Action", "Priority Level Two (2) - Expedited Action",

and "Priority Level Three.(3) - Procedure

revision".

Comments

which

were classified

as requiring "Immediate Action" were incorporated within

one work week; those classified

as "Expedited Action" were corrected

within one month;

and those classified

as "Procedure revision" were

incorporated

during the next scheduled

revision.

The inspector

found

one priority 2 comment from May 1989 with no response

due date.

The

licensee

indicated the item would be re-evaluated

for a possible

higher priority, and that

a response

from the licensee's

corporate

office was requested.

Until the

comment is resolved this item wi 11

remain open.

No violations, deviations,'unresolved

or

open

items were identified.

7.

Safet

Assessment/gualit

Verification (37701

38702

40704

92720)

The ef'fectiveness

of management

controls, verification and oversight

activities, in the conduct of jobs observed

during this inspection,

was

evaluated.

The inspector frequently attended

management

and supervisory

meetings

involving plant status

and plans

and focusing

on proper co-ordination

among Departments.

The results of licensee

auditing

and corrective action programs

were

routinely monitored

by attendance

at Problem Assessment

Group

(PAG)

meetings

and by review of Condition Reports,

Problem Reports,

Radiological Deficiency Reports,

and security incident reports.

As

applicable,

corrective action program documents

were forwarded to

NRC

Region III technical specialists for information and possible followup

evaluation.

No violations, deviations,

unresolved or open

items were identified.

8.

Re ion III Re uests

(92705)

The inspector acted

upon

a March 8,

1991

memorandum

from

Nr. Hubert J. Hiller, Director, Division of Reactor Projects

(DRP), to

NRC

Region III Branch Chiefs regarding

hydrogen

recombiners.

The memorandum

17

requested

information on hydrogen

recombiners

installed in Region III

plants

because

of parts dedication

concerns that were identified at

another

U.S. utility.

Attached to the

memorandum

was

a questionnaire

which was completed

and -forwarded to the Region III Technical Support

Staff for compilation and evaluation.

The emphasis

was

on recombiners

stored remotely from the plant site, which would be connected

external to

the containment at need.

The D.

C.

Cook plant has its hydrogen

recombiners

permanently 'installed inside each

containment.

No violations, deviations,

unresolved or open items were identified.

9.

Mana ement Meetin

.(30702)

a ~

A management

meeting,

attended

as -indicated in paragraph l.a, was

conducted at the D.C.

Cook site

on April 2, 1991.

The purpose of the

meeting

was to discuss

various topics of interest,

and to tour the

plant.

The meeting

began with a discussion

related to the

10CFR50 Appendix

R

NRC inspection,

including pre-1984

candor issues,

as were described

in various submittals

by the licensee

to NRC.

The Regional

Administrator was satisfied with the resolution of the candor

issues

and that subject is considered

closed

(EA-82-139).

'b.

Among the other topics presented

by the licensee

staff,. were:

(1)

Engineering/Technical

Support organization

and function as

related to Corporate,

System Engineering,

and Site Design

Perspectives

(2)

Maintenance

Program status

A management

meeting; attended

as indicated in paragraph

1.b,

was

conducted at the D.C.

Cook site

on April 17,

1991.

The purpose. of

the meeting

was to discuss

licensee

performance

and initiatives,

and

to tour the plant.

Among the topics presented

by the licensee staff were:

(1)

Current Unit

1 and Unit 2 status.

(2)

Licensee

performance

indicators for years

1988,

1989,

1990,

and

the following subjects:

Equipment availability

Unplanned

auto

scrams

Fue 1

r e liab i 1 ity

(3)

Licensee Strengths:

People

Security

Emergency

Preparedness

18

(4)

Licensee

Challenges:

Eng/Tech Support

Maintenance

10.

Mana ement Interview (30702)

The inspectors

met with licensee

representatives

(denoted

in Paragraph

1)

on May 3,

1991 to discuss

the scope

and findings of the inspection.

In

addition, the inspector also discussed

the likely informational content

of the inspection report with regard to documents

or processes

reviewed

by the inspector during the inspection.

The licensee

did not identify

any such documents/processes

as proprietary.

19-