ML17328A974

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Application for Amends to Licenses DPR-58 & DPR-74,deleting Tech Specs 3.5.4.1 & 3.5.4.2 Re Boron Injection Sys & Changing Table 3.3-5 Safety Injection Response Times to Be Consistent W/New Analyses Assumptions
ML17328A974
Person / Time
Site: Cook  
Issue date: 03/26/1991
From: Alexich M
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: Murley T
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML17328A975 List:
References
AEP:NRC:1140, NUDOCS 9104010360
Download: ML17328A974 (17)


Text

, -'CCELERATED DISTRIBUTION DEMONS TION SYSTEM I

D

SUBJECT:

Application for amends to Licenses DPR-58

& DPR-74,deleting Tech Specs 3.5.4.1

& 3.5.4.2 re boron injection sys changing Table 3.3-5 safety injection response times to be consistent w/new analyses assumptions.

S DISTRIBUTION CODE:

AOOID COPIES RECEIVED:LTR J ENCL {

SIZE:

/ 2 + (7 TITLE: OR Submittal:

General Distribution NOTES: Sgg g+pC~N A

REGULATORY -XNFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9104010360 DOC.DATE: 91/03/26 NOTARIZED:

NO DOCKET. 5 FACIL:50-315 Donald C.

Cook Nuclear Power Plant, Unit 1, Indiana 05000315

, 50-316 Donald C.

Cook Nuclear Power Plant, Unit 2, Xndiana 05000316 AUTH.NAME AUTHOR AFFILIATION ALEXICH,M.P.

Indiana Michigan Power Co.

(formerly Indiana

& Michigan Ele RECIP.NAME RECXPXENT AFFILIATION R

~

MURLEY,T. E.

Document Control Branch (Document Control Desk)

RECIPIENT ID CODE/NAME PD3-1 LA COLBURN,T.

INTERNAL: NRR/DET/ECMB 9H NRR/DOEA/OTS B1 1 NRR/DST/SELB 8D NRR/DST/SRXB 8E OC XLE 01 EXTERNAL: NRC PDR COPIES LTTR ENCL 1

1 2

2 1

1 1

1 1

1 1

1 1

0 1

1 1

1 RECIPIENT ID CODE/NAME PD3-1 PD NRR/DET/ESGB NRR/DST 8E2 NRR/DST/SICB 7E NUDOCS-ABSTRACT OGC/HDS2 RES/DSIR/EIB NSIC COPIES LTTR ENCL 1

1 D

D I

S D

NOTE TO ALL"RIDS" RECIPIENTS:

D PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISI'RIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 18 ENCL 16

Indiana Michigan Power Company P.O. Box 16631 Columbus, OH 43216 AEP:NRC:1140 Donald C.

Cook Nuclear Plant Units 1 and 2

Docket Nos.

50-315 and 50-316 License Nos.

DPR-58 and DPR-74 TECHNICAL SPECIFICATION CHANGE REQUEST BIT BORON CONCENTRATION REDUCTION U.S. Nuclear Regulatory Commission Attn:

Document Control Desk Washington, D,C.

20555 Attn:

T. E. Murley March 26, 1991

Dear Mr. Murley:

This letter and its attachments constitute an application for changes to the Technical Specifications (T/Ss) for Donald C.

Cook Nuclear Plant Units 1 and 2.

Specifically, we request that T/Ss 3.5.4.1 and 3 ',4,2, which state the requirements for the boron injection system (including the boron injection tank [BIT] and its associated heat tracing),

be deleted.

In addition, we are requesting a change to the "safety injection (ECCS)" response times specified in T/S Table 3.3-5 to be consistent with the new analyses assumptions.

Deletion of T/Ss 3,5.4,1 and 3,5.4.2 will allow removal of the BIT.

As discussed in NRC Generic Letter 85-16, there have been incidents at operating reactor plants in which boric acid has crystallized in the internals of vital safety-related pumps and piping, thereby rendering those systems inoperable.

The NRC Staff concluded in Generic Letter 85-16 that there are inherent safety risks in the present system of using high concentrations of boron and further indicated that, based on improved analysis

methods, the BIT could be
removed, Consequently, we are making this submittal to implement the changes in the T/Ss identified above.

This T/Ss change is being requested for implementation during the next regularly scheduled refueling outages, To support the

schedule, we request that the amendments be approved for both units during the first half of 1992.

We will keep NRC project management informed of any schedule changes through routine project review meetings.

9104010360 910326 PDR ADOCK 05000315 P

PDR

Attachment 1 to AEP:NRC:1140 10 CFR 50.92 Analysis for Changes to the Donald C. Cook Nuclear Plant Units 1 and 2 Technical Specifications

A~chment 1 to AEP:NRC:1140 Page 1

I.

Introduction As discussed in NRC Generic Letter 85-16, there have been incidents at operating plants in which boric acid has crystallized in the internals of vital safety-related pumps and piping, thereby rendering those systems inoperable.

Heat tracing is presently necessary to maintain the boron injection tank (BIT) and associated piping at a sufficiently high temperature to prevent precipitation of the 12% by weight boric acid solution.

Furthermore, the safety-related nature of the BIT requires that the heating systems be redundant.

The required solubility temperature imposes a continuous load on the

heaters, and the potential for low-temperature alarm actuation and heater burnout exists.

Violation of the T/S on concentration in the BIT poses availability problems in that recovery is required within a very short time. If the concentration is not restored within one hour, the plant must be taken to the hot standby condition and borated to the equivalent of 1 percent delta k/k at 200 degrees Fahrenheit.

Thus, this requirement has a potentially serious impact on plant availability.

In addition, the high boric acid concentration makes recovery from a spurious safety injection signal (which results in injection of the BIT fluid into the reactor coolant system) both time consuming and costly.

Analysis for calculating the consequences of a steam line break have provided results that demonstrate a reduced need for the highly concentrated boron (20,000 ppm to 22,500 ppm) injection.

Based on the inherent safety risks in the present system and the analysis

results, we are making this submittal requesting the necessary T/Ss changes to support deactivation of the BIT.

Similar license amendments have been approved by the NRC for the North Anna Power Station, H.

B. Robinson Steam Electric Plant, Indian Point Unit No. 2, Surry Power Station, V. C.

Summer Nuclear

Station, Sequoyah Nuclear Plant, and Diablo Canyon Units 1 and 2.

1I.

Descri tion of Ph sical Modifications to the Plant A.

Current S stem Desi n Basis The BIT holds 900 gallons of water with a boron concentration in excess of 20,000 ppm, approximately a

12 weight percent solution.

Tank heaters and pipe heat tracing are provided to maintain a minimum solution 0

temperature of greater than or equal to 135 F.

Recirculation from the boric acid storage tanks (BASTs) to the BIT is maintained continuously via boric acid transfer pumps to ensure that the BIT is full of concentrated boric acid at all times and to prevent boric acid stratification.

The BIT is isolated from the reactor coolant system (RCS) during normal plant operation.

J

, II

AMchment 1 to AEP:NRC:1140 Page 2

During a safety injection, the suction of the charging pumps is diverted from the normal suction at the volume control tank (VCT) to the refueling water storage tank (RWST) and discharged through the BIT to the RCS.

Concurrently, isolation valves in the recirculation line to the BAST close.

The operability of the boron injection system currently ensures that sufficient negative reactivity is injected into the core to offset the increase in positive reactivity caused by RCS cooldown due to a steam line break.

B.

Desi n Chan es to the Boron In'ection S stem The BIT will remain in place connected to the ECCS injection piping system, but filled with water containing only a nominal boron concentration instead of 12 percent boric acid by weight.

The BIT recirculation piping to/from the BAST and attendant equipment (piping, valves, instruments, heat tracing, etc.) will generally remain in

place, but will be disconnected at appropriate locations.

All controls that are deactivated will be removed to lessen distractions and make additional panel space available.

An alternate solution considered was the entire removal of the tanks, piping, heat tracing, etc.

Due to the obvious cost savings in labor and radiation exposure between removing and disposing of these contaminated components versus abandoning in place, the practical course was determined to be disconnecting the BITs and their ancillary components from interfacing systems.

Furthermore, abandoning in place allows for easy restitution if a future need arises to return the BITs to service.

The following system design changes will'e made to the boron injection system:

Piping Modifications The BZT/BAST recirculation piping and the BIT flushing lines will be cut and capped to isolate the 12% boric acid system from the BIT.

AtTachment 1 to AEP:NRC:1140 Page 3

2.

Valve Impacts (a)

BZT/BAST recirculation valves will remain in place with their air supplies disconnected (these are fail-closed valves).

The control switches for these valves will be removed from the main control room panels.

(b)

Manual valves in the BIT recirculation path will remain in place, in the closed position.

3.

Instrumentation Impacts (a)

Flow instruments 1-and 2-IFA-250 will remain in place with their alarm wiring disconnected.

The main control room annunciator windows, which warn the operator of low BIT recirculation flow, will be "blanked" and made available as spares.

(b)

The wiring for BIT temperature alarms will be disconnected and their annunciator windows, warning the operator of low BIT temperature, will be "blanked" and made available as spares.

4.

Heat Tracing (a)

Heat tracing circuits applicable to the BZT recirculation piping will be de-energized and abandoned in place.

The thermostats/alarmstats will be disconnected and removed.

Annunciators applicable to these heat trace circuits will be "blanked" and made available as spares."

(b)

The BIT strip heaters will be de-energized and abandoned in place.

The temperature controllers will be de-terminated and removed.

IZI. Descri tion of Pro osed Technical S ecification Chan es A.

T S Index a e VZI Section 3/4.5.4 is being deleted and the index therefore indicates that pages 3/4 5-9 and 3/4 5-10 are intentionally left blank.

%4

  • 3;

At%hchment 1 to AEP:NRC:1140 Page 4

B.

T S Index a e XIII Delete section 3/4.5.4 (Boron Injection System) from the bases.

C.

Table 3.3-2 Table 3.3-2 is being changed to reflect the overpower delta T reactor trip response time supported by the analysis of steam line break mass and energy release outside containment.

In addition, for Unit 1, the orientation of the second page of the table is being changed to make the pages in the table consistent.

D ~

Table 3.3-5, En ineered Safet Features Res onse Times Additional notes were added to Table 3.3-5 to address the response time for charging pump suction switchover from the VCT to the RWST.

The note reference for function 3g was changed from an "*" to a "++" to be consistent with the note changes described.

However, it should be noted that the response of essential service water is not in any way associated with the alignment of the ECCS system for safety in)ection.

The time responses for the essential service water included in Table 3.3-5 reflect the response time with and without offsite power available.

Table 3.3-5 engineered safety feature (ESF) actuation system response times were increased to reflect the safety analyses supporting the elimination of the BIT.

The reactor trip on SI response time for all ESF trips has been increased from 2.0 to 3.0 seconds.

This increase is supported by the safety analyses.

Zn addition, we also wrote out "less than or equal to" where the symbol was previously used.

E.

T S

3 4 5.4, Boron In'ection S stem Technical Specifications 3.5.4.1 and 3.5.4.2 covering the BIT and its associated heat tracing will be deleted.

These pages will be left intentionally blank.

AMchment 1 to AEP:NRC:1140 Page 5

F.

Unit 1 T S 5.5, Desi n Features ECCS This T/S states that the ECCS shall be maintained in accordance with the original design provisions contained in Section 6.2 of the FSAR.

An exception statement will have to be added to note the reduction in the boron concentration of the BIT.

G.

Bases Section 2.2.1 The discussion in this section pertaining to overpower delta T is being revised to reflect the new analysis.

H.

Bases Sections 3 4.3.1 and 3 4.3.2, Protective and En ineered Safet Features ESF Instrumentation A paragraph is being added to this section that discusses the changes being made to Table 3.3-5.

The addition of this paragraph is resulting in a large amount of text being shifted on the pages that follow in Bases Section 3/4.3.

Consequently, we are submitting those pages as well.

I.

Bases Section 3 4.5.4, Boron In'ection S stem This section describes the basis for T/S 3/4.5.4 noted above and therefore will also be deleted.

J.

Bases Section 3 4.5.5, Refuelin Water Stora e Tank This section of the bases is being revised to reflect the new analysis.

IV.

Justification for Chan e

The only accident analyses that are significantly affected by boron reduction and deactivation of the BIT are the steam line break transients.

These transients are affected with respect to both core integrity and mass and energy releases inside and outside of containment.

The analyses for most of these transients have previously been submitted to the NRC and are summarized below.

It should be noted that the assumption of 0 ppm boron concentration is conservative.

In reality, the BIT will be filled with water that has a nominal boron concentration.

A.

Steam Line Break Core Res onse The reanalysis of this event with a BIT boron concentration of 0 ppm for Unit 1 is documented in WCAP-11902, Section 3.3.4.13, which was previously submitted in our letter AEP:NRC:1067 dated October 14,

AWchment 1 to AEP:NRC:1140 Page 6

1988.

The NRC Safety Evaluation Report dated June 9, 1989, for Amendment No.

126 to Facility Operating License No.

DPR-58 (Unit 1) from Mr. J.

F. Stang to Mr. M. P. Alexich provided NRC approval of this analysis.

This analysis has been, incorporated into Chapter 14 of the Updated Final Safety Analysis Report (UFSAR).

The reanalysis of this event for Unit 2 with a BIT boron concentration of 0 ppm is documented in Attachment 4, Appendix B of our letter AEP:NRC:1071E dated February 6,

1990.

The NRC Safety Evaluation Report dated August 27, 1990, for Amendment Nos.

148 and 134 to Facility Operating License Nos.

DPR-58 and DPR-74 (Units 1 and 2, respectively) from Mr. T. G. Colburn to Mr. M.

O'. Alexich provided the NRC approval of this analysis.

B.

Steam Line Break Mass and Ener Inside Containment The reanalysis of this event with a BIT boron concentration of 0 ppm for both Units 1 and 2 is documented in WCAP-11902, Supplement 1, Section S-3.3.4.1 (Attachment 4 to this letter).

This analysis provides a

series of mass and energy release rates which are evaluated for containment integrity in Item D.

This section of WCAP-11902, Supplement 1 was previously submitted in Attachment 5 to our letter AEP:NRC:1071E dated February 6,

1990.

The NRC Safety Evaluation Report

.dated August 27, 1990, for Amendment Nos.

148 and 134 to Facility Operating License Nos.

DPR-58 and DPR-74 (Units 1

and 2, respectively) from T.

G. Colburn to Mr. M. P.

Alexich provided the NRC approval of this analysis.

Attachment 4 to this letter contains a complete copy of WCAP-11902, Supplement 1 entitled "Rerated Power and Revised Temperature and Pressure Operation for Donald C.

Cook Nuclear Plant Units 1 and 2 Licensing Report" for your review.

C.

Steam Line Break Mass and Ener Outside Containment The reanalysis of this event with a BIT boron concentration of 0 ppm for both Units 1 and 2 is documented in WCAP-11902, Supplement 1, Section S-3.3.4 (Attachment 4 to this letter).

As discussed in WCAP-,11902, Supplement 1, Westinghouse regenerated the outside containment mass and energy releases for 68 separate cases considering different break sizes,

units, initial power levels, and auxiliary feedwater flow rates.

The evaluation of the affect of these mass and energy release rates on equipment outside of containment is summarized in Item E.

AWchment 1 to AEP:NRC:1140 Page 7

D.

Steam Line Break Containment Inte rit The reanalysis of this event with a BIT boron concentration of 0 ppm for both Units 1 and 2 is documented in WCAP-11902, Supplement 1, "Section 3.4.2.1 (see Attachment 3 to this letter).

This section of WCAP-11902, Supplement 1 was previously submitted in Attachment 5 to our letter AEP:NRC:1071E dated February 6,

1990.

The NRC Safety Evaluation Report dated August 27, 1990, for Amendment Nos.

148 and 134 to Facility Operating License Nos.

DPR-58 and DPR-74 (Units 1 and 2, respectively) from Mr. T. G. Colburn to Mr. M. P. Alexich provided the NRC approval of this analysis.

E.

Steam Line Break Outside of Containment The reanalysis of this event supporting a BIT boron concentration of 0 ppm and associated response timing changes for both Units 1 and 2 is documented in.

This analysis utilizes the spectrum of mass and energy releases summarized in Item C to develop the temperature response of the main steam enclosures as well as important equipment within those enclosures.

The limiting case was determined to be a Unit 2 break of 1.2 square feet from 70% initial power.

For this case, as discussed in Attachment 5, the instrument surface temperatures were determined,to remain below the qualification temperatures.

Therefore, reducing the BIT concentration to 0 ppm is acceptable.

V.

No Si nificant Hazards Anal sis We believe that operating with the BIT boron concentration requirement eliminated will not adversely impact public health and safety.

10 CFR 50.92 Criteria Per 10 CFR 50.92, the proposed amendment will not involve a significant hazards consideration if the proposed amendment does not:

1) involve a significant increase in the probability or consequences of an accident previously analyzed, 2) create the possibility'of a new or different kind of accident from an accident previously analyzed or evaluated, or 3) involve a significant reduction in a margin of safety.

Our evaluation of the proposed changes with respect to these criteria is provided below.

Attachment 1 to AEP:NRC:1140 Page 8

Criterion 1

The deactivation of the BIT affects the steam line break transients with respect to core integrity, mass and energy release to containment, and mass and energy release outside containment for instrument qualification.

With the assumption that the BIT remains installed without heat tracing and with boric acid concentration reduced to 0 ppm, analyses show that the departure from nucleate boiling design basis is met and no consequential fuel failures are anticipated.

Additionally, temperatures and pressures reached in containment would be below the containment design limits. All instrument surface temperatures remain below the qualification temperatures.

Therefore, the equipment inside and outside containment necessary to mitigate the consequences of an accident would function as intended.

Therefore, no significant increase in the probability or consequences of a previously analyzed accident would occur.

Criterion 2

The BIT is a component of the safety in)ection system whose sole function is to provide concentrated boric acid to the reactor coolant to mitigate the consequences of a postulated steam line

,break.

The deactivation of the BIT will therefore affect the steam line break transients, but will not create the possibility of a new or different type of accident.

Criterion 3 The analyses performed for the deactivation of the BIT indicate that the departure from nucleate boiling design basis continues to be met.

Additionally, the temperatures and pressures reached in containment would fall below the containment design limits.

Finally, in Attachment 5 we have shown that the impact on instrumentation of mass and energy release outside containment meets acceptance criteria.

Since the design bases contain the required margins of safety, no significant reductions in margins of safety will occur.

Lastly, we note that the Commission has provided guidance concerning the determination of significant hazards by providing certain examples (48 FR 14780) of amendments considered not likely to involve significant hazards considerations.

The sixth of these

'xamples refers to changes that either may result in some increase to the probability or consequences'f a previously analyzed accident or may reduce in some way a safety margin, but where the results of the change are clearly within limits established as acceptable.

AMchment 1 to AEP:NRC:1140 Page 9

The analyses that are referenced in this submittal have been demonstrated to comply with the licensing basis of the plant.

In fact, all but the mass and energy release outside containment analysis and its impact on instrumentation have already received NRC approval in SERs previously issued to Cook Nuclear Plant.

Thus, we believe the example cited is applicable and that the changes should not involve significant hazards consideration.

Dr. T. E. Murley AEP'NRC:1140 The requested T/Ss changes are supported by the attachments to this letter.

Attachment 1 contains a description of the changes and our evaluation concerning significant hazards considerations.

The proposed revised T/Ss pages are included in Attachment 2.

Attachment 3 consists of the existing T/Ss pages marked-up to reflect the changes proposed in this amendment request.

Attachment 4 is a copy of WCAP-11902, Supplement 1, "Rerated Power and Revised Temperature and Pressure Operation for Donald C.

Cook Nuclear Plant Units 1 and 2 Licensing Report."

Attachment 5

contains an analysis entitled "Main Steam Line Break Outside Containment Analysis Summary."

We believe that the proposed changes will not result in (1) a significant change in the types of effluents or a significant increase in the amounts of any effluent that may be released offsite, or (2) a significant increase in individual or cumulative occupational radiation exposure.

The proposed changes have been reviewed by the Plant Nuclear Safety Review Committee and by the Nuclear Safety and Design Review Committee.

In compliance with the requirements of 10 CFR 50.91 (b)(l), copies of this letter and its attachments have been transmitted to Mr. J.

R. Padgett of the Michigan Public Service Commission and to the Michigan Department of Public Health, This document has been prepared following Corporate procedures that incorporates a reasonable set of controls to ensure its accuracy and completeness prior to signature of the undersigned.

Sincerely, MD P. Alexich Vice President ldp Attachments cc:

D. H. Williams, Jr.

A. A. Blind - Bridgman J.

R. Padgett G. Charnoff A. B, Davis - Region III NRC Resident Inspector

- Bridgman NFEM Section Chief

A' e