ML17328A531

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Insp Repts 50-315/89-29 & 50-316/89-29 on 891004-1116. Violations Noted.Major Areas Inspected:Actions on Previously Identified Items,Plant Operations,Radiological Controls, Maint,Surveillance,Security,Bulletins & Generic Ltrs
ML17328A531
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 12/06/1989
From: Burgess B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17328A529 List:
References
REF-GTECI-093, REF-GTECI-NI, TASK-093, TASK-93, TASK-OR 50-315-89-29, 50-316-89-29, GL-88-03, GL-88-3, NUDOCS 9001100070
Download: ML17328A531 (34)


See also: IR 05000315/1989029

Text

e

U.S.

NUCLEAR REGULATORY COMMISSION

REGION III

Reports

No. 50-315/89029(DRP);

50-316/89029(DRP)

Docket Nos. 50-315;

50-316

Licensee:

Indiana Michigan Power

Company

I Riverside Plaza

Columbus,

OH

43216

Licenses

No. DPR-58;

DPR-74

Facility Name:

Donald C. Cook Nuclear Power Plant, Units I and

2

Inspection At:

Donald C.

Cook Site,

Bridgman, Michigan

Inspection Conducted:

October

4 through

November 16,

1989

Inspectors:

B. L. Jorgensen

E.

R. Schweibinz

R. A. Paul

D. G. Passehl

Approved By:

B. L. Burgess,

Chief

Projects Section

2A

a

e

Ins ection

Summar

Ins ection

on October

4 thru November

16

1989

(Re ort No. 50-315/89029(DRP);

0 ~

Areas

Ins ecte

Routine unannounced

inspection

by Regional

and resident

inspectors

o

actions

on previously identified items; plant operations;

radiological controls; maintenance; -surveillance; security; safety assessment/

quality verification; engineering

and technical

support; reportable

events;

Bulletins, Notices

and

Gener ic Letters; Allegations; and,

NRC Region III

requests.

In addition,

on November 16, 1989,

a Management

Meeting was

conducted

in NRC Region III, to discuss

operations

and management

issues

and

a second

meeting

was conducted

regarding

licensed operator training.

The

'following Safety Issues

Management

System

(SIHS) items were reviewed, with the

indicated results:

(Open) Generic Safety Issue

GSI 93 and Generic Letter

GL-88-03 concerning

steam binding of auxiliary feedwater

pumps.

Results:

Of the

13 areas

inspected,

no violations or deviations were identified

~sn

areas.

One violation was identified (Level iv - operation

in MODE

1 with

neither

ECCS subsystem

OPERABLE - Paragraph

10.g) in the remaining area.

The inspection disclosed

weaknesses

in the licensee's

control of work activities,

~

~

~

~

~

~

~

~

to ensure

such activities are confined to a single safety "Train."

This is

reflected in the Notice of Violation and was the focus of the November 16, 1989,

Management

Meeting.

900ll00070

891206

PDR

ADOCK 05000315

Q

PDC

DETAILS

1.

Persons

Contacted

a.

Ins ection:

October

4 - November

16

1989

"A. Blind, Plant Manager

"J.

Rutkowski, Assistant Plant Manager,

Technical

Support

L. Gibson, Assistant Plant Manager,

Projects

"K. Baker, Assistant Plant Manager,

Production

B. Svensson,

Executive Staff Assistant

J.

Sampson,

Operations

Superintendent

E. Horse,

gC/NDE General

Supervisor

T. Beilman, Maintenance

Superintendent

"J. Droste, Technical

Superintendent,

Engineering

T. Postlewait,

Design Changes,

Superintendent

L. Matthias, Administrative Superintendent

J. Wojci k, Technical

Superintendent,

Physical

Sciences

H. Horvath, equality Assurance

Supervisor

D.

Loope, Radiation Protection Supervisor

The inspector also contacted

a number of other licensee

and contract

employees

and informally interviewed operations,

maintenance,

and

technical

personnel.

"Denotes

some of the personnel

attending the Management

Interview on

November 17,

1989.

b.

Mana ement Meetin

- November

16

1989

Licensee

H.

P. Alexich, Vice President,

Nuclear Operations

A. A. Blind, Plant Manager

P.

A. Barrett, Director of equality Assurance

S. J.

Brewer, Nuclear Safety

and Licensing

K.

R. Baker, Assistant Plant Manager,

Production

NRC

H. J.

Clausen,

Deputy Director, Division of Reactor

Projects

W.

L. Axelson, Chief, Projects

Branch

2

B.

L. Burgess,

Chief, Projects

Section

2A

B.

L. Jorgensen,

Senior Resident

Inspector

E.

R. Schweibinz,

Project Engineer

2.

Actions on Previousl

Identified Items

92701)

As a result of a special

safety inspection

conducted

by an

NRC

Augmented Inspection

Team (AIT) documented

in NRC Inspection

Reports

No. 50-315/89025(DRSS);

No. 50-316/89025(DRSS),

and concerning

the

0

Qi

Unit 2 reactor trip of August 14, 1989, the licensee

responded

to the

four issues identified in Paragraph

9 of the inspection report by a

letter

(AEP:NRC: 1090J)

dated October 25,

1989.

Item 9.a:

The failure mode of the silicon controlled rectifier (SCR 209)

was confirmed as

random.

1

Item 9.b:

The loads supplied

by all CRIDs have or will have electrical

independence

such that

a failure of a single

CRID will not cause

a loss

of all channels

of some parameter

(such

as

steam generator

wide range

level indication) monitored in the control

room.

Item 9.c:

Engineering guidelines

are in place

and

a procedure will be

issued for testing

GRID Inverters prior to switching from the alter nate

to normal

power supplies.

The preventive

maintenance

procedure

in effect

for the

CRID Inverter will be expanded

to include the Static Transfer

Switch.

,

Item 9. d:

Finally, training was upgraded

on operation of the

AMSAC (ATWS

Mitigating system actuation circuitry) system.

The inspector

had

no further questions

on these matters.

They are

considered

closed.

No violations, deviations,

unresolved

or

open items were identified.

0 erational

Safet

Verification

71707

71710

42700)

Routine facility operating activities were observed

as conducted in the

plant and from the main control

rooms.

Plant startup,

steady

power

operation,

plant shutdown,

and system(s)

lineup and operation were

observed

as applicable.

The performance of licensed

Reactor Operators

and Senior Reactor Operators,

of Shift Technical Advisors,

and of auxiliary equipment operators

was

observed

and evaluated

including procedure

use

and adherence,

records'and

logs,

communications,

shift/duty turnover,

and the degree of

professionalism

of control

room activities.

The Plant Manager, Assistant

Plant Manager-Production,

and the Operations

Superintendent

were well-

informed on the overall status

of the plant,

made frequent visits to the

control

rooms,

.and regularly toured the plant.

Evaluation; corrective action,

and response

to off-normal conditions or

events, if any, were examined.

This included compliance with any

reporting requirements.

Observations

of the control

room monitors, indicators,

and recorders

were

made to verify the operability of emerge'ncy

systems,

radiation monitoring

systems

and nuclear reactor protection systems,

as applicable.

Reviews

of surveillance,

equipment condition,

and tagout logs were conducted.

Proper return to service of selected

components

was verified.

Both Unit 1 and Unit 2 were. in continuous routine power operation

throughout the inspection period.

Operation

was at full rated power

with a few brief exceptions of reduced

power operations

to permit

- inspection or maintenance

of the main feed pumps.

On October 12, 1989,

a non-licensed, auxiliary equipment operator

(AEO) assigned

to the Unit 1 turbine building tour was discovered to

have logged activities (area inspections)

which were not performed.

A pattern of increasing

nonperformance

over the preceding

week was

identified via cross-checks

between tour logsheets

and computerized

access

records.

The individual was discharged effective October 16,

1989.

An audit of required tour performance

by numerous other AEO's

identified occasional

discrepancies

but no chronic problems.

The

licensee

enhanced

monitoring of the area

and evaluated

programmatic

changes

to clarify how tours are to be performed

and logged.

Minimum shift crew requirements

were not violated.

However, the

inspector identified that the

AEO described

above failed to make

some checks

committed to in the licensee's

response

to Generic Letter 88-03 (e.g.,

see

Paragraph

11).

The licensee's

procedure

(OHI-4013, "Operators:

Authorities and

Responsibilities" ) for shift operations

and duties,

however,

was

violated.

Since adherence

to this procedure

is

a requirement of

Technical Specification 6.8. l.a, through reference

to Regulatory

Guide 1.33,

Appendix

A - 1972, failure to perform the specified

area tours is considered

a violation of the referenced

Technical

Specification.

This violation was identified and corrected

by the licensee.

It was

not highly safety significant, nor was it repetitive of previous

violations.

In accordance

with normal practice

as established

in

the

NRC Enforcement Policy (10 CFR2, Appendix C) no Notice of

Violation is being issued

on this matter.

Some additional

NRC

reviews to verify corrective actions

and associated

issues

is

anticipated.

On NovemberlO,

1989, the licensee

determined that

a previously

identified problem, which was undergoing

an engineering

and safety

evaluation,

represented

a condition outside the plant design basis

and was reportable.

Required notifications were made.

The problem is described further in Paragraph 6.f of this inspection

report and involved a licensee

Inservice Test (IST) of the Unit 2

Turbine Driven Auxiliary Feedpump.

Twelve hour operating shift schedule

has

been developed.

The Target

date to have this in effect is January

1, 1990.

The inspector

was

provided with a draft rotation schedule

encompassing

a 15-week cycle

of 8-hour training shifts and 12-hour operating shifts.

Overtime

backup

was considered

in the schedule.

The inspector discussed

the

need to consider

two issues

in implementing the revised rotation.

First, administrative control of overtime will need to be considered

and, if necessary,

changes

made in the methods for assuring

compliance to applicable limitations.

Second,

commitments

and

schedules

which currently specify three-times-per-day

activities

will need review and appropriate

adjustments.

The licensee

is developing

a computerized

"clearance

permit" database

system,

which the inspector

reviewed.

The ultimate goal is to

produce

an automatic

system,

providing the user with an extensive

detailed

summary of individual components

and systems.

The database

will supply the information necessary

to tag out entire systems,

subsystems,

or components.

It will have the capability to

cross-check for other clearances

written on equipment with a

pre-existing clearance.

A control

room team

has investigated all control switches in both

units'ontrol

rooms, verifying the switches against existing plant

data,

drawings,

and other information applicable to the particular

control.

Computer generated

"standards"

have

been sent to each shift crew for

a quality assurance

check.

Once this is completed the approved

Clearances will be officially accepted

as standards

in the computer

database.

12

OHP 4021.019.001

"Operation of the Essential

Service Mater

(ESW)

System."

The inspector

performed

a walkdown of a section of the

ESM

system

as described

in Data/Signoff Sheet 5.2,

"ESW,

Loop

1M Normal

Valve Lineup."

Prior to the walkdown, the change

sheets

associated

with the procedure

were reviewed to assure

proper inclusion into

selected

portions of the procedure.

Approximately 50 valves were.

inspected; all were found correctly positioned.

Some minor discrepancies

were noted between the valve number

as

stated

on the data sheet

and the valve number printed on the'ag

attached to the valve.

For example,

1-WPI-712-VllW on the data

sheet

corresponded

to 1-MPI-712-Vl on the valve's tag.

This and

other differences

were given to the appropriate

onsite group for

followup.

Other observations

unrelated to the

ESW system were identified

during the walkdown and also relayed to plant supervisory staff.

One involved damage to a 1/2 inch line connected

to 1-CPI-450-V1

(component cooling water to miscellaneous

pressure

indicator).

The line appeared

to have

been

stepped

on; it was bent

down and

flattened at a fitting joint.

Also,

on the platform grating below

the valve,

a lock and chain were lying unattached

to any piece of

equipment.

One final observation

relayed to the plant staff was

a loose,

ceiling-mount, adjustable

ring hanger for a length of pipe just

upsteam of the Turbine

Room Sump'verflow discharge line, located

in the screen

wash

pump room.

One violation (not cited)

and

no deviations,

unresolved or open items

were identified.

Radiolo ical Controls

71707)

During routine tours of radiologically controlled plant facilities or

areas,

the inspector

observed

occupational

radiation safety practices

by the radiation protection staff and other workers.

Effluent releases

were routinely checked,

including examination of on-line

recorder traces

and proper operation of automatic monitoring equipment.

Independent

surveys

were performed in various radiologically controlled

areas.

On November ll, 1989, the

an Emergency Notification

an at-power purge of Unit

discovered

which the duty

substantial

potential for

material.

On that basis,

licensee

reported,

then subsequently

withdrew,

System

(ENS) notification.

During setup for

2 containment,

a procedure deficiency was

Shift Supervisor decided might cause

loss of control of the release

of radioactive

the

ENS notification was

made.

The problem involved a "note" in data/alignment

Sheet

No.

3 of the purge

procedure,

which stated certain

subsequent

steps

were "not applicable" in

MODEs 1 through 4.

This was in error.

The referenced

steps

involved

verification of operability of radiation monitor Trains

A and B, and

placing the monitor output circuits in "Normal".

Failing these actions,

purge would not isolate

on containment

high radiation

as designed.

The licensee

had not purged in MODEs 1-4 in several

years.

An alternate

procedure for containment pressure relief, using different lines,

was

verified as correctly aligning the radiation monitoring system.

Upon

further evaluation of the subject procedures

the licensee

determined that

the identified discrepancy

alone

(as stated in 10 CFR 50.72 for

ENS

notification) would not have

caused

uncontrolled release

of radioactive

material.

Two other statements

in the

same procedure directly contradict

the erroneous

statement,

and the frequent operation"of the pressure

relief system

has

made operators familiar with the necessary

realignment

of the radiation monitoring system.

On these

bases,

the

ENS notification

was withdrawn later the

same

day.

The procedure errors,

which occur red during a March 1989 revision, were

corrected.

The inspector verified the correction

and that

no use

was

ever made of the procedure with the error present.

The inspector also

re'viewed the system

and the licensee's

evaluation

and agreed with the

licensee's

assessment.

This review included verification that,

even

had

the error been

implemented,

containment

purge isolation from safety

injection and from high containment

pressure

would both have

been

unaffected.

No violations, deviations,

unresolved

or open

items were identified.

5.

Maintenance

(62703

42700)

Maintenance activities in the plant were routinely inspected,

including

both corrective maintenance

(repairs)

and preventive maintenance.

Mechanical, electrical,

and instrument

and control group maintenance

activities were included as available.

The focus of the inspection

was to assure

the maintenance activities

reviewed were conducted

in accordance

with approved

procedures,

regulatory guides

and industry

codes

or standards

and in conformance with

Technical Specifications.

The following items were considered

during

this review:

the Limiting Conditions for Operation

were met while

components

or systems

were

removed from service;

approvals

were obtained

prior to initiating the work; activities were accomplished

using approved

procedures;

and post maintenance

testing

was performed

as applicable.

The following activities were inspected:

a ~

b.

Job Order No. A011391, "Disconnect annunciator

drop 69 on panel

122,

titled, Individual Hotwell or Miscellaneous

Drain Tank or Feed

Pump

Turbine Condenser

Conductivity High.'econnect

when notified by

Design

Change Coordinator."

The activity was performed

as part of

the ongoing effort to attain

a "black board" status

in the control

room.

The system is currently under

a design

change

(RFC - "Request

for Change" ) which has not yet been

closed out.

The annunciator

was disconnected

because

of recur ring problems with

the detector

and the cation bed, which would result in frequent

alarms

in the control room.

The associated

alarm response

procedure

lists

no automatic actions

and requires

the Chemical

Lab to

investigate.

The system initiated numerous false alarms which led

to its disconnect.

The annunciator will be disabled until it is

made to function properly.

Any increase

in secondary

conductivity

would be seen

in the steam generator

blowdown samples,

which are

monitored

on

a shiftly basis.

Gob Order No. A002121,

"Repack 1-IMO-204 with Chesterton

Packing;

weld leakoff line."

The work was performed

on the valve (spray

additive tank outlet) using procedure

    • 12 MHP-SP-130, "Installation

Procedure for A.,W. Chesterton

Nuclear Valve Sealing System."

The

inspector

saw no problems with the work being performed.

It was

noted,

however, that the procedure

was inconsist'ent

as regarded

dimensions;

sometimes

they were provided,

sometimes

not.

One

example pertained

to stuffing box data.

Stem outer diameter

and box

C.

d.

e.

g.

inner diameter were simply listed as 0.750

and 1.250 respectively,

without stipulating units (e. g. inches,

centimeters).

Job Order No. A012011, "Investigate

and repair valve 1-FRV-256

(Unit 1 turbine-driven auxiliary feedwater

pump test line isolation

valve); valve leaks

by when closed."

This activity utilized

Procedure

""12 MHP 5021. 001. 012,

"Hammel

Dahl V-500 Series

Globe and

Angle Valves."

The valve disc was ground to remove surface cutting

and was

lapped

and blued to its seat.

Job Order No.

B010940, "Fabricate

and erect security enclosure for

Unit 2 "N Train" battery

and associated

switch gear."

Job Order

No.

B001217,

"Repair control air line hanger/support

where

damaged

above tray 2A1C6."

Job Order No.

A011251, "Fabricate

and install security cage for

Unit 1 panel

and charger."

The work was being performed

as directed

by a Request

For Change

(RFC 12-3019) to upgrade

the

"N train"

batteries

and support equipment.

Two procedures

were being followed

for the job, one of which (""12 MHP 5021.001.006)

provided instructions

for the fabrication and erection of structural steel,

and the other

("~12

MHP 5021.001.003)

provided instructions for anchor bolt

installation.

Review of these

items identified one minor problem;

wall mounted anchors

had to be installed

one inch lower than

originally intended

due to a surveying error.

This discrepancy

was

properly documented

and approved in an attachment to the relevant

procedure

noted above.

Job Order

No.

B003162, "Inspect

and measure orifice No. 2-FFX-253

Unit 2 Turbine Driven Auxiliary Feedpump test line orifice."

The

subject

Job Order was written in response

to the condition discussed

in Paragraph 6.f of this report.

The bolts installed at the orifice flange (2-FFX-253) were found

smaller in diameter than stated

on the associated

isometric drawing

(3/4 inch versus

7/8 inch),

and the flexitallic gaskets

were sized

for 1500 lbs.

versus

900 lbs.

Both the bolts and gaskets

were

replaced with those of the correct size.

The other Auxiliary

Feedpump orifices were checked,

and another

case

involving.

undersized

studs

was found in the Unit 2 East Motor Driven Auxiliary

Feedpump

Room.

Those studs

were also immediately replaced with the

correct size.

Separate

corrective action documents

were initiated

on each discrepancy,

to ensure root cause

and significance

evaluations

are performed.

Depending

on the findings of those

evaluations,

further inspection followup may occur.

No violations, deviations,

unresolved

or

open items were identified.

6.

Survei

1 1 ance

61726

42700)

The inspector

reviewed Technical Specifications

required surveillance

testing

as described

below and verified that testing

was performed in

accordance

with adequate

procedures,

that test instrumentation

was

calibrated,

that Limiting Conditions for Operation

were met, that removal

and restoration of the affected

components

were properly accomplished,

that test results

conformed with Technical Specifications

and procedure

requirements

and were reviewed

by personnel

other than the individual

directing the test,

and that deficiencies identified during the testing

were properly reviewed

and resolved

by appropriate

management

personnel.

The following activities were inspected:

a.

~"1 IHP 4030

STP. 100.001,

"Response

Time Testing of the Reactor

Protection

System Sensors."

The inspector

observed

various portions

of this multifaceted test,

including the Reactor Coolant

RTDs and

selected

Foxboro pressure/flow transmitters.

The testing was

conducted

by a contractor using plant-approved

(but contractor-

developed)

procedures

and with all electrical

connections,

switching,

and disconnections

by assigned plant Instrument

and

Control staff.

b.

C.

d.

e.

""2 IHP 4030

STP. 122,

"Steam Generator

2 and 4 Mismatch Protection

Set II Surveillance Test (Monthly)."

The inspector

noted plant

equality Control

was present for this test to independently

assess

test performance

and results.

""2 IHP 4030

STP. 134, "Reactor Coolant

Pump

No.

3 Underfrequency,

Bus

2A Surveillance Test (Monthly)."

""12 THP 6010

RAD. 1602, "Liquid Process

Monitor Detector Calibration."

The inspector witnessed part of the calibration process

for the Unit 2

East essential

service water header

(instrument

R-20) and did not

observe

a problem.

~"12 THP 6030

IMP. 012, "Radiation Monitoring System Calibration-

Air/Liquid/Gas."

Discussions

with the technicians

performing this

test

on process

monitor R-19 in Unit 2 (Steam Generator

Blowdown

Sampler)

revealed

a defective circuit card

had earlier

been

identified and replaced.

The inspector questioned

the whereabouts

of the associated

repair Job Order, which was not present,

and was

referred to the

18C office.

A Job Order was verified to exist

(No. 000253)

documenting the repair and accounting for traceability

of the

new part.

""2 OHP 4030 STP.017T,

"Turbine Driven Auxiliary Feedwater Test."

The subject test was performed during an

NRC review (ref.

NRC

Inspection

Report

No. 50-315/89028(DRS);

No. 50-316/89028(DRS)

of

the licensee's

pump In-Service testing (IST) program.

During the

test,

the

NRC auditor noted that the process

flow instruments

(2-FFS-258

and 2-FFS-260)

read

550

gpm while the pressure

differential across

the 3-inch test line orifice (2-FFX-253) equated

to 700

gpm.

The flow instruments

associated

with both the process

orifice and test orifice were checked

and found to be in calibration

and the instrument lines were verified to be free of blockage.

The

test

was rerun and the discrepancy still existed.

At that point it

was determined that the dimensions listed for one of the orifices

could be incorrect.

The test line orifice was disconnected

and measured

and found to be

correct.

The process orifice could not be disconnected

because

of

location, but based

on calculations, it is believed this orifice is

larger than design.

The associat'ed

"flow retention" switches

were

therefore reset to a lower setpoint,

proportionate to the observed

flow mismatch,

The significance (root cause

and potential

consequences)

of this

problem remained

under investigation with NRC Region III at the

conclusion of this inspection,

but are expected to be discussed

in

the Inspection

Report referenced

above.

""1 OHP 4030

STP. 017T, "Turbine Driven Auxiliary Feedwater

Systems

Test."

This test

was conducted for the purpose of restoring the

system to service following maintenance

on the associated

test valve

1-FRV-256 (ref.

Paragraph

5.c above)

and

as

a routine monthly test.

During the test,

the inspector

observed test

gauge

TG-097, which is

used to measure test flow (measure differential pressure

across

an

orifice in the test line) was quite erratic

and

had

a small leak out

the low-pressure

vent.

This raised

a question

about instrument

accuracy which was relayed to the test engineering

group onsite.

They determined that the test should

be rerun (initial data

showed

unexpectedly

high pump delta-P) with the test

gauge

pulse-dampened

and the vent not leaking.

The test then produced satisfactory

results.

Problem Report

(PR)89-887,

"2 MRV-210 main steam

stop valve for

No.

1 Steam Generator,

Unit 2 failed initial valve cycle time."

The problem involved a slow stroke time (5.45-seconds

versus

the

Technical Specification 5.00-second limit) for the subject valve,

using its "Train B" dump valve.

The valve met the 5-second

stroke

time limit (2.52-seconds)

when tested with its "Train A" dump valve.

The event'was initially classified

as

a Condition Report, but was

.

later upgraded

when the licensee

was asked to review the event

against

NRC reportabi lity requirements.

An investigation against

10 CFR 50.73,

"Licensee

Event Report (LER)

system,"

and

NUREG-1022

and

NUREG-1022,

Supplement

1, both of which

elaborated

on the

LER rule,

was performed.

The investigation

found

the event to be nonreportable,

since

2-MRV-210 met the full

requirements

of the Technical Specification

ACTION statement

and

since there

was

no evidence to believe the valve was inoperable

prior to the surveillance test.

10

Condensation

accumulation

in the piping associated

with the "Train

B" dump valve is believed to be the cause of the problem.

Formation

of a "water slug" could impede

steam flow and.thus

the closure time

of 2-MRV-210.

The licensee

intends to inspect the valve's internals

during the next outage of sufficient duration to determine if the

drain tube configuration associated

with the valve is in any way

damaged

or clogged.

No violations, deviations,

unresolved

or open items were. identified.

7.

Securit

71707)

Routine facility security measures,

including control of access for

vehicles,

packages

and personnel,

were observed.

Performance

of

dedicated

physical security equipment

was verified during inspections

in

various plant areas.

The activities of the professional

security force

in maintaining facility security protection were occasionally

examined or

reviewed,

and interviews were occasionally

conducted with security force

members.

On November 1, 1989, the inspector

was notified that licensee

equality

Assurance

had found an onsite contractor

(who provided background

investigative services

for personnel

who are granted

unescorted

access

to the plant) could not demonstrate validity of all of the information

provided in some individual screening

reports.

The finding was referred

to

NRC Region III Security personnel

for follow up.

No violations, deviations,

unresolved or open items were identified.

8.

Safet

Assessment/ ualit

Verification

37701

38702

40704

92720)

The effectiveness

of management

controls, verification and oversight

activities, in the conduct of jobs observed

during this inspection,

was evaluated.

The inspector frequently attended

management

and supervisory meetings

involving plant status

and plans

and focusing

on proper co-ordination

among Departments.

The results of licensee auditing and corrective action programs

were

routinely monitored by attendance

at Problem Assessment

Group

(PAG)

meetings

and by review of Condition Reports,

Problem Reports,

Radiological Deficiency Reports,

and security incident reports.

As

applicable,

corrective action program documents

were forwarded to

NRC

Region III technical specialists

for information and possible

followup

evaluation.

a.

The inspector

reviewed safety valve testing using the Trevitest

method,

pursuant to a question

from NRC Region III.

The concern

related to the performance of an appropriate

review to determine

whether testing via this method would result in an "unreviewed

11

safety question"

as defined in 10 CFR 50.59.

Specifically, if

the testing should

be permitted or performed in plant

MODEs not

originally envisioned,

does there exist

a safety evaluation

under

10 CFR 50. 59 to substantiate

its acceptability?

Safety valve testing via the Trevitest method

as performed at

D.C.

Cook plant is limited to secondary

system valves.

This testing

is governed

by procedure

""12 MHP 4030 STP.008,

which permits testing

in MODEs 1,

2 and 3.

This procedure

was approved at Plant Nuclear

Safety

Review Committee

(PNSRC) meeting

No.

2273

on June

15, 1989,

at which time

PNSRC decided

a 50.59 unreviewed safety question

determination

was not required.

Further investigation

showed that

the current procedure

was decended

from an earlier version

numbered

"~12

MHP SP. 126.

The earlier procedure

was subjected to a

10 CFR 50.59 safety evaluation

dated

June 22, 1987, which the

inspector

reviewed.

The safety evaluation

was imprecise with respect to carefully

covering all aspects

of 10

CFR

.50.59.

For example,

the Trevitest

method

does not increase either the frequency of testing or the

probability a given valve will fail to reclose

during any specific

test,

but the safety evaluation

does not explicitly address

any

potential for changing the probability of occurrence of an analyzed

event.

On the other hand,

the potentials for changing the nature or

magnitude of analyzed

events

were more explicitly evaluated.

Further,

the adaptability of the method to other than "during

scheduled

outages"

(original

FSAR, Section 10.2.4)

was recognized,

was determined to be bounded

by the

MODE 3 case,

and the

FSAR was

updated to read "prior to or during plant outages."

The safety evaluation relied upon certain procedural

prerequisites

or limitations.

For instance,

no seismic evaluation

was

deemed

necessary

due to procedure restrictions limiting testing to one

valve at a time and requiring the consideration of the valve in test

was "inoperable."

Test equipment is prohibited from being powered

off a safety related

(Class 1E),bus.

The inspector

concluded that the licensee's

determination,

while not

as explicit as desired in all details,

was correct - performing the

test pursuant to the procedure

as approved

does not constitute

a

.10 CFR 50.59 unreviewed safety question.

The above information was conveyed to the Region III requester.

Some

good technical findings by the licensee's

equality Assurance

(gA) organization resulted in the issuance

of Problem Reports

(PR).

Three worth noting are

PR 89-1177,

PR 89-1222,

and

PR 89-1184.

Problem Report 89-1177

documents

a finding that

some flow

instruments

used for the Inservice Testing

Pump Program

have

a full

scale

range greater

than that specified

by ASME XI (3.65 vs. 3.0

times reference

or less).

C.

Problem Report 89-122 discusses

a finding where elements of a

Technical Specification defined "reactor trip response

time" were

not incorporated into the associated

response

time procedure.

Specifically, gripper c'oil voltage decay time had been deleted.

Lastly, Problem Report 89-1184 describes

a technically inaccurate

change to a Maintenance

Department procedure.

The change

added

instructions for replacing

a Shunt Trip Attachment

(STA) which were

identical to those for replacing

an Under Voltage Trip Attachment

(UVTA).

These pieces of equipment differ and require separate

sets

of instructions for replacement.

The licensee

announced

an onsite reorganization

plan, effective

November 1, 1989, which is intended to produce

an improved emphasis

on maintenance,

and on project management

and support.

Significant

elements of the reorganization

include assembly of a

new Projects

division, from various existing departments,

headed

by an Assistant

Plant Manager.

The Projects division will be responsible for design

changes,

scheduling of major or long lead-time projects

and outages,

and construction

and contractor

management.

The Administration

division will no longer

be headed

by an Assistant Plant Manager,

but

some of its elements will be reporting directly to the Plant Manager;

this includes the independent

Safety

and Assessment

Department.

The

Production

and Technical

Support divisions will remain, with some

lesser internal restructuring,

and will be headed

by Assistant Plant

Managers.

A number of personnel

reassignments

or rotations occurred

within thes'e

groups,

the most significant being promotion of the

former Operations

Department Superintendent

to Assistant Plant

Manager-Production.

The reorganization

was discussed

at the

Management

Meeting on November 16,

1989 (Paragraph

14).

A review of

select personnel

qualifications

was incomplete at the conclusion of

the inspection.

The results of this review will be included in a

future report.

No violations, deviations,

unresolved

or open items were identified.

9.

En ineerin

and Technical

Su

ort

37701

41701

93701

The inspector monitored engineering

and technical

support activities at

the site and,

on occasion,

as pr'ovided to the site from the corporate

office.

The purpose of this monitoring was to assess

the adequacy of

these functions in contributing properly to other functions

such

as

operations,

maintenance,

testing, training, fire protection

and

configuration management.

ao

Unit 2 emergency

diesel

generator

2CD failed to load during a test

run on September

18,

1989.

The test

was being performed,

in part,

to verify proper instal'lation of design

change

No.

RFC-DC-12-2864,

which will provide "slow speed" start capability to all four onsite

diesels.

As part of the design,

the field flash to the generator

exciter rotor is disabled

and excitation depends

on residual

magnetism in the rotor.

This proved inadequate

during the subject

test - a condition apparently

not forseen during original design

and

13

not detected

in previous testing.

Some previous testing did not

include observing generator

performance

as

opposed to diesel

engine

performance;

some testing apparently

occurred with the original

rotor starting position coincidently aligned

such that excitation

was adequate,

and the generator

loaded successfully.

The problem was documented

on Problem Report 89-1041,

the "slow

speed" circuits were all disabled,

and

a redesign is under

evaluation.

The diesel

emergency

functions were not adversely

affected

by this design oversight.

Problem Report 89-1194, written on October 26, 1989,

documented

discovery of the fact that Unit 2

MODE 4 and

5 shutdown boron curves

in the Technical

Data Book (Figure 4.5) lacked appropriate

safety

margin for postulated

boron dilution accidents

while on residual

heat removal.

As an immediate,

interim corrective action,

instructions

were issued to add 300

gpm to the concentration

determed

from the referenced

Figure,

should

MODE 4 or 5 operation

occur before

new curves could be generated.

No such

shutdown

was

actually necessary;

new, correct curves

have

been produced

and

distributed.

This problem

had apparently existed since

March 1989,

when the

'curves

were generated

by evaluation of vendor (Advanced Nuclear

Fuels) data through corporate

and site nuclear engineering.

The

Unit was subsequently

in MODEs 4 and

5 during a.scheduled

outage

June 10-24,

1989,

The significance of the error and its implications considering

the actual

June

1989 outage

were still under evaluation at the

conclusion of the inspection.

Further inspection will occur if

the matter proves important.

Plant Control

Room Simulator Evaluation

On October

10 through 12,

a special

evaluation

was conducted

utilizing the D.C.

Cook Unit 2 control

room simulator.

A team of

NRC personnel

- consisting of the Senior Resident Inspector

and

Resident

Inspectors

assigned

to both

D. C.

Cook and to Palisades

(the backup site)

and of the responsible

NRC Region III Section

Chief and the

NRR Licensing Project Manager - performed this

evaluation.

The following procedures

were exercised

on the simulator:

(1)

""2 OHP 4021.001.011,

"Determination of Critical Conditions

Donald

C.

Cook Nuclear Plant"

(2)

""2 OHP 4021.001.002,

"Reactor Start-UP"

(3)

""2 OHP 4021.001.006,

"Power Escalation"

(4)

""2 OHP 4022.053.001,

"Decreasing or Loss of Condenser

Vacuum"

(5)

""2 OHP 4022.013.006,

"Tripping of Protection

Set Bistables"

(6)

02

OHP 4023. E-O, "Reactor Trip or Safety Injection"

(7)

02

OHP 4023.ES-O. 1, "Reactor Trip Response"

(8)

02

OHP 4023.E-1,

"Loss of Secondary

or Reactor Coolant"

(9)

02

OHP 4023,ES-1. 1, "SI Termination"

(10) 02

OHP 4023.E-2,

"Faulted

Steam Generator Isolation"

(ll) 02

OHP 4023.ECA-3. 1,

"SGTR M/Loss of Reactor Coolant-

Subcooled

Recover Desired"

(12) 02

OHP 4023.FR-S. 1, "Response

to Nuclear Power Generation/ATWS"

(13)

02

OHP 4023.FR-H. 1, "Response

to Loss of Secondary

Heat Sink"

The team noted that procedure

E-0 had been recently revised to eliminate

a potential

problem with handling

a loss-of-coolant accident concurrent

with complete loss of auxiliary feedwater.

Reordering the "exit" step

on

failure of auxiliary feedwater, still within the owner's

group

emer gency

response

procedure guidelines,

now assures

all the critical verifications

contained only in E-0 will be performed before the procedure is exited.

This revision resolves

a concern

NRC had raised in an earlier inspection.

Two potential

weaknesses

were identified in existing procedures.

First,

procedure

FR-S. 1 on

ATWS did not contain

an early instruction to close

the main steam

stop valves

as

an aid to conserving

steam generator

inventory.

Consequently,

substantial

inventory was (perhaps

unnecessarily)

lost.

Second,

procedure

FR-H. 1 on loss of secondary

heat sink had

no

early instruction (concurrent with commencement

of pressurizer

"feed and

bleed" ) regarding installation of "jumpers"

on phase

A isolation functions.

Phase

A is an inevitable result of "feed and bleed"

and results in loss

of the "bleed" function via isolation of operating air to the pressurizer

power operated relief valve.

It seemed

the procedure

could and should

prevent this, rather than respond to it after it occurs.

The above potential procedure

weaknesses

were conveyed to the procedure

group responsible for emergency

operating procedures

for their

consideration

and appropriate corrective action.

During one scenario

involving complete failure/loss of the condensate

storage

tank (CST) the simulator instructors indicated auxiliary

feedwater alignment to its alternate

supply (essential

service water)

should not include opening the supply valves.

Since these

are not

automatic valves,

they would have to be opened

by operator action from

the control

room in case of some additional

emergency requiring auxiliary

15

feedwater.

The inspectors

questioned

the implicit position that closed

the valves;

non-automatic

valves

can

make for an

OPERABLE flowpath,

and

were concerned that plant operator training includes this implication.

Other instruction concerns

related to the use of non-EOP criteria as

a

basis for rendering

(unneeded)

emergency

equipment inoperable during an

emergency.

Examples

were:

shutdown of an unloaded

emergency diesel

rather than letting it idle unloaded for more than five minutes

(an

operating/surveillance

guideline)

and; placing

a recirculating

LPSI pump

in "pull-to-lock" so that pump/water temperatures

would not gradually

build up,

Neither action

seemed critical to equipment protection,

so

securing

and defeating automatic

emer gency response

functions

seemed

unnecessary,

perhaps

even ill-advised.

The above instruction concerns

were conveyed to and discussed

with

appropriate

licensee staff for their consideration

and, if appropriate,

corrective action.

Overall, the inspection

team found the procedures

effective.

They were

generally clear

and straightforward

enough to permit successful

implementation

by knowledgeable

(but not specifically Cook-trained)

individuals.

The symptom-based

Functional

Restoration

Guides were

similarly exercised

in part

(02-OHP 4023.F-O. 1 through F-0.6) with no

significant deficiencies

noted.

No violations, deviations,

unresolved

or open items were identified.

10.

Re ortable

Events

92700

92720)

The inspector

reviewed the following Licensee

Event Reports

(LERs)

by means of direct observation,

discussions

with licensee

personnel,

and review of records.

The review addressed

compliance to reporting

requirements

and,

as applicable, that immediate corrective action

and appropriate

action to prevent recurrence

had been accomplished.

Closed)

Licensee

Event

Re ort LER 315/87007:

missed event-initiated

surveys

1

ance

sump eff uent radio oglca

sampling)

due to

unrecognized

disabling of automatic

sampler.

An incomplete

instrument calibration activity disabled the turbine

sump automatic

sample compositer

(by simulating

a no-flow signal)

when the test

equipment

was left connected at the end of the work day.

Sump

discharges

were very intermittent,

so the lack of sample

accumulation in the compositer receiver

was not readily apparent.

Mhen the problem'was

recognized

the next day,

an approximate

16-hour

interval

had elapsed,

which exceeded

the eight hours specified for

alternate

manual

sampling

and analysis.

To prevent recurrence,

instr ument group super visors

and work planners

were informed of the affect of the activity, and the recorder being

calibrated

was labeled with a sign warning of its connection with the

compositer.

16

Radiation monitors

on lines upstream of the

sump were checked; all

were operable

and showed

no unusual radioactivity over the period in

question.

(Closed)

Licensee

Event

Re ort

LER 315/89003:

Unit 1 reactor trip on

March 18, 1989, while shutting

down.

The unit tripped from about

10 percent

power when the high flux trip signal

from intermediate

range nuclear

instrument

channel

N-35 auto-unblocked

before it

cleared

and reset.

The reset

should occur first, normally at around

12. 5 percent.

This is because

reset is nominally calibrated to an

electric current equal to half the trip setpoint current (at or

below 25 percent).

In this case,

the trip setpoint

was conservatively

set

due to rounding

down calculated current values,

then the reset

setpoint (half the trip setpoint)

was also

rounded

down to the next

whole number.

The combined conservatisms

resulted in the reset

setpoint being below 10 percent nuclear

power on one channel.

When

the block cleared at 10 percent,

the trip followed immediately.

To prevent recurrence,

procedures

were changed to ensure

the reset

setpoint, while still conservative, will be set

above the auto-

unblock= setpoint.

An inspection of like instrument channels

in

Unit 2 disclosed

one with the

same type overlap problem, which was

corrected.

The plant responded

normally upon trip actuation, with no system or

equipment

problems

noted.

(Closed

Licensee

Event

Re ort

LER 315/89004:

containment isolation

va ve Type

test resu ts disclosed

leakage

above 0.60L

.

The

original

LER was submitted with some testing

and followlp actions

still incomplete.

LER Supplement

1 dated August 31, 1989, included

complete information on test results.

Further,

as discussed

in

Inspection

Report

No. 50-315/89018(DRP);

No. 50-316/89018(DRP)

(Paragraph

the Supplement

includes

a discussion of the circumstances

surrounding

a repair to valves

ICM-250 and ICM-251 which were

performed without first obtaining "as-found" leak rates.

The repair

to valves

ICM-250 and -251 was to replace

stem packing.

The valve

internals

were not repaired.

Hased

on very low as-left seat

leakage

(which should closely approximate

as-found in the absence

of internal

maintenance)

these

valves would not have

added significantly to the

as-found total.

The final total leak rate

(maximum pathway method)

was 3.08L

,

primarily due to just three valves.

All three valves were e5ch in

line with other valves having very low leak rates.

All three were

repaired or replaced.

None had

a significant failure history among

six previous

cases

of Type

C test results totaling above 0.60L

for

Unit l.

Determining as-found

leakage to be above 0.60L

is not a violation

of regulatory requirements

in the subject case,

because

the

significant contributors

appeared

to result from random component

degradation.

Failure to determine

as-found

leakage prior to

performing maintenance,

however, is contrary to licensee

procedures

17

and,

by reference

through Regulatory Guide 1.33 Appendix A, is

contrary to Technical Specifications.

Further,

such actions

are

contrary to 10CFR50 Appendix J

as applied to this valve design.

The violation was identified, reported

and corrected

by the licensee.

It resulted

from personnel

error by maintenance

personnel,

who

failed to follow procedure

controls correctly.

The procedures

properly cautioned that leak testing must precede

maintenance

because

of a similar occurrence

some

2 1/2 years earlier,

when such

precautions

did not exist.

Given the amount of time elapsed

between

the events,

the 1989 problem is- not considered repetitive or

programmatic.

Further, it lacks safety significance

because

the

work was external

to the valve seats

and would not have affected the

leak rate materially.

(Closed

Licensee

Event

Re ort

LER 315/89005:

inoperable

containment

iso ation va ve for component

coo ing water

(CCW) system.

Valve

1-CCM-458

(CCW supply to reactor coolant

pump coolers) failed to

close during testing

on March 30,

1989.

The unit was in a refueling

shutdown at the time,

so there

was

no immediate significance to the

failure.

Internal

damage

was found in the valve operator

upon

disassembly.

An "interim" LER was submitted

when the root cause

and

safety evaluations

were not able to be completed within 30 days.

The

estimated

submission

date for the final

LER was June

9, 1989.

On

that date,

the licensee

submitted

a letter withdrawing the

LER,

because

the event

was determined

not to be subject to mandatory

reporting requirements,

and not to be

a safety hazard or an unreviewed

safety question.

(Closed)

Licensee

Event

Re ort

LER 315/89006:

ECCS flow balance

out-of-speci

icatson.

Routine mandatory f ow balance testing,

conducted

during the 1989 refueling outage

as per Technical Specification 4.5. 2, found-total safety injection flow from the

North SI pump to be slightly in excess

(644

gpm vs.

640 gpm) of the

allowable upper limit.

Adjustments

were

made to system flow control

valves to restore

the flow within the specified

range.

The

deviation apparently resulted

from small

normal

system fluctuations

combined with instrument uncertainties.

An evaluation of the

magnitude of the discrepancy

showed it was not safety significant.

In fact, the licensee

concluded the currently prescribed

acceptance

range for SI flow is much more restrictive than necessary

to meet

safety requirements

with comfortable margins.

A broadening of the

acceptance

range

has

been requested

and is under evaluation

by NRC.

(Closed

Licensee

Event

Re ort

LER 315/89008:

deficient monthly

calibration checks.

his condition app ie

to both D.C.

Cook

units.

'

generic Westinghouse letter dated

December

1,

1988 and

entitled "Calibratioh of AFD Instrumentation"

addressed

how various

aspects

of excore-indicated

axial flux difference

(AFD) should

be

compared

as part- of monthly surveillance.

One such aspect

involves

comparing the excore-indicated

value to the value input to the

F

(Delta I) penalty function generator.

A review of licensee

procedures

against the Westinghouse clarification found this particular

'omparison

involving the penalty function generator

was being

done

as part of routine quarterly testing rather than monthly.

The described

comparison

was transferred

to a monthly test

procedure.

The reason for the original choice of quarterly vs.

monthly could not be determined.

A review of historic data found

the input to the penalty generator

had been quite stable,

requiring

only infrequent (and minor) adjustment.

Omission of two thirds of

the comparisons

had therefore

not constituted

a significant safety

hazar d.

The licensee's

omission of the described testing was,

however,

a

violation of Technical Specification requirements

at 3.3. 1. 1 to

perform testing stipulated in Table 4.3-1.

The inspector took

specific note, in reviewing this matter, of the fact that five

"Previous Similar Events" are listed in this

LER.

A further review

determined

the "similarity" to involve the fact that instrument

surveillance

procedures,

to accomplish testing governed

by Technical

Specification Tables,

contained

discrepancies

such that complete

literal compliance with the Specification

was not achieved.

Three

of the five previous "similar" events,

in fact, occurred in

close chronology during 1986; special

licensee

reviews for this

purpose

were conducted to address

a generic

concern

about the

technical quality of instrument test procedures

to implement "Table"

requirements.

A variety of causes,

a variety of instruments,

and

a

variety of discrepancy

types

(scope,

frequency; technical

consistency)

were involved in these

events.

LER 315/89008 did not involve the

same instruments,

the

same root cause

or consequences,

or the

same

technical

nature

as these

previous events,

so it was determined

not

to demonstrate

a repetitive problem.

(Closed)

Licensee

Event

Re ort 315/89012:

ECCS components

s)multaneously

inopera

e sn

oth trains.

With the "A" Train

safety injection pump inoperable for ongoing maintenance,

a

surveillance test

was authorized

and performed

on "B" Train

rendering it (including the associated

safety injection pump)

simultaneously

inoperable.

The test authorization resulted

from

errors

on the part of the Shift and Unit Supervisors

(both Senior

Reactor Operator licensed)

who did=not recognize

the unacceptability

of the specific test in the existing circumstances.

The test

procedure

was deficient in not highlighting the need to assure all

opposite-train

equipment

was

OPERABLE.

Also, the maintenance

scheduling

process

did not specifically coordinate with the testing

schedule;

the test occurred

second,

but it was scheduled first.

Though not addressed

explicitly in the

LER, simultaneous

inoperability of equipment in both

ECCS trains placed the unit

in Technical Specification 3.0.3.

This Specification requires

initiation of action within one hour to place the unit in an

acceptable

condition.

Because

the dual inoperability was not

recognized,

no such action was initiated.

Instead,

one train was

routinely restored to OPERABLE status

upon test completion, which

occurred after 68 minutes.

Failure to comply with an "action" requirement of Technical Specification 3.0.3 is considered

a violation of the Specification

(Violati on 315/89029-01) .

A violation of a Technical Specification "action" requirement is a

potentially significant enforcement matter.

An NRC Enforcement

Board was convened

on October 25, 1989, to consider this event.

The

Board concluded that this specific example

lacked any substantial

safety significance,

and it was adjudged to be

a Level IV violation.

In consideration

of the causes

of the event,

however,

along with the

occurrence

of a somewhat similar event

a few weeks earlier (ref.

Inspection

Report 50-315/89026(DRP);

50-316/89026(DRP)

Paragraph

3.6)

the Board recommended

a Management

Meeting be scheduled

between

NRC and licensee

representatives

to discuss

these

and other timely

matters.

The Management

Meeting is addressed

further in Paragraph

14.

below.

(0 en

Licensee

Event

Re ort

LER 316/88003:

RPS instrument

to erances

repeate

y vso ate

.

e orsgsnal

LER has

been

supplemented

four times,

most recently

on September ll, 1989.

The licensee

has concluded

the observed

instrument "drift" has

remained within safe limits, although outside current Technical

Specification tolerances,

and that

no more stable devices

are

currently available

as replacements.

Thus,

a request to relax

the Technical Specification tolerances

was submitted

on November 29,

1988.

A technical

review of this

LER was conducted within NRC

Region III which derived several

questions

concerning matters

not

explicitly stated in the

LER.

The inspector relayed these

questions

to the licensee

and plans to review this matter further upon receipt

of the requested

additional

information.

Closed

Licensee

Event

Re ort LER 316/88009:

containment integrity

requirements

urging core

a teratsons

not met.

This report describes

conditions applicable to both D.C.

Cook units.

At D.C.

Cook,

lower containment

atmospheric

radiation is sampled (essentially

continuously) for iodine and particulate concentrations

by drawing

a sample out of containment

through particulate filters and iodine

cartridges.

The filters and cartridges

require regular change out.

While they are being changed,

an open pathway

can exist from the

containment

atmosphere

to the auxiliary building, unless

the sample

inlet line is isolated.

Such

an open pathway is not permissible

during reactor core alteration (i.e. fuel handling) yet the changeout

procedure

did not require isolating the pathway for a changeout

made

during such periods.

Such events

(open pathway while handling fuel)

have almost certainly occurred repeatedly,

each lasting

up to a few

minutes,

during the past history of the two units.

A requirement of

each unit's Technical Specifications,

to suspend

core alterations if

integrity is not maintained,

has thus very likely been repeatedly

violated.

Applicable procedures

were revised to prevent

a recurrence.

(Closed

Licensee

Event

Re ort

LER 316/88010:

containment

purge in

service with snopera

e contro

room radlatlon alarm annunciation.

The subject alarm annunciation is required

by Technical

20

Specifications

whenever the purge is in service.

In the subject

event,

the reactor

and containment

were both completely void of

nuclear fuel (during a prolonged outage to replace

the steam

generators)

and purge

was in service.

Due to a misunderstanding

of

language

in an administrative guideline,

the radiation monitoring

system control terminal

was then removed from service for a design

change.

The individual authorizing this action (licensed

SRO)

understood

the guideline to indicate the Specification could be

satisfied

by recording local readings,

which is incorrect.

The

error was recognized

and corrected

about

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> later,

and the

guideline

was clarified to prevent

a recurrence.

Radiation monitor

system safety functions (to isolate purge

on high radiation) were

always

OPERABLE.

(Closed

Licensee

Event

Re ort

LER 316/88011:

unexpected

actuation

of engineered

sa ety feature

Phase

B Iso ation) during testing.

A

new circuit time-response

test

was being conducted with the unit

shutdown

and defueled.

Part of the test utilized logic test

switches

on the

SSPS test panel to initiate main steam isolation

valve closure.

This was the only actuation

expected.

Mhen the

switch was used,

however,

containment isolation

Phase

B also

actuated.

A subsequent

review of the details of the test circuit

showed this should

have

been expected;

the circuit worked as

designed.

Post actuation

response

of all in-service

Phase

B equipment

was

correct.

To prevent recurrence,

the test procedure

was revised

to incorporate

the subject portion into another section which

intentionally verifies the

Phase

B time response,

and

an alternate

means

was developed for actuating

steam isolation valve circuits

only.

(Closed)

Licensee

Event

Re ort

LER 316/89003:

reactor vessel

level

>ndscatson

system

RVLIS

calsbrat>on

shrift due to air leakage into

capillary tubing during mid-cycle outages.

This problem was

discovered

during a refueling outage

when a routine required

calibration

was performed.

Evidence

suggested

the system

had

become

inaccurate

during some previous mid-cycle outage,

when the reactor

was depressurized

so that air could leak into the tubing.

The design

accuracy specification of plus/minus one-percent

was exceeded

by all

three transmitters

on both trains, with a worst case of "drift" in

excess

of 40 percent

on one "A" Train transmitter.

The precise

time

the problem developed

could not be identified.

The system

was

made leak-tight by seal-welding the steel

dust cap

over the high-point*fill valve stem and seal.

The transmitters

were

then recalibrated

and restored to OPERABLE for unit operation.

An evaluation of the significance of the operators

receiving

erroneous

level indication was conducted.

The only likely incorrect

action identified was to vent the reactor vessel

post-accident

to

~21

remove voids and increase

indicated vessel

level.

This would result

in decreased

indicated level,

however,

and the

RYLIS error would

become evident.

Since it is likely the

RYLIS was out-of-calibration during periods

of required

system operability, the effective Technical

Specification

was violated.

(Closed)

Licensee

Event

Re ort

LER 316/89012:

incomplete monthly

channe

checks.

When Unit

echnical Specifications

were revised

by Amendment

No.

95 to add channel

check requirements for

containment water level instruments,

the licensee's

implementing

procedures

were not likewise revised.

As a consequence,

the

specified channel

checks

were not performed for four months.

The Amendment occurred in late 1987, but did not become effective

until a post-refueling unit startup in March 1989.

In the meantime,

a combination of errors occurred which resulted in the procedures

remaining

unchanged.

First,

no departmental

action request

was

initiated due to an oversight.

Subsequently,

the duplicative

corporate action item tracking system item was overlooked, .perhaps

due in part to an over-reliance

on the departmental

tracking list.

Qhen the error was discovered

in June,

1989,

a channel

check found

all the instruments

operable.

The governing procedure

was revised

and the required channel

checks

have subsequently

been routinely

performed.

The

NRC Enforcement Policy (10 CFR'2 Appendix C) describes

condition for

which violations of requirements will not normally be subject to a Notice

of Violation.

These include .that the violation be identified, reported

(if required)

and corrected

by the licensee,

that it be a Severity

Level IV or V (lesser safety significance)

and that it be neither

repetitive nor otherwise indicative of licensee failure to correct

a

known problem.

Among the items discussed

above,

Items c, f, i, j, 1,

and

m concern licensee-identified violations which are

deemed to meet

these criteria and for which no Notice of Violation is being issued.

One violation was identified in this area which will be the subject of a

Notice.

Six potential violations (not cited)

and

no deviations,

open or

unresolved

items were noted in this area.

ll.

NRC

Com liance Bulletins

Notices

and Generic Letters

92703

The inspector

reviewed the

NRC communications listed below and verified

that:

the licensee

has received the correspondence;

the correspondence

was reviewed

by appropriate

management

representatives;

a written

response

was submitted if required;

and, pl'ant-specific actions

were

taken

as described

in the licensee's

response.

(Open) Generic Letter 88-03:

Resolution of Generic Safety Issue

93,

Steam Binding of Auxiliary Feedwater

Pumps.

The inspector

reviewed

-the licensees

response

to GL 88-03 dated

May 31,

1988 and the below

22

referenced

procedures.

The response

indicates that the Operations

Department is required

by Procedure

OHP 4030.001.001

"Routine Plant

Inspection Outside of Control

Room" to perform a shiftly (every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />)

check on the auxiliary feedwater

(AFM) lines to verify the

AFW line

temperature

is ambient.

Review of this procedure

by the inspector

identified that the above

checks

were not requirements

but were

guidelines.

The guidelines to perform the checks

are part of the

procedure

in Attachments

No.

1 and

No.

2.

The procedure

states

"Although

these

do not represent

specific requirements,

be aware that the operator

should develop

a habit or pattern to routinely check those

items

on the

guidelines."

When this was communicated to the licensee

they agreed

to modify the procedure to make the

AFW line temperature

checks'

requirement.

In addition,

Procedures

OHP 4021.056 '02 "Operation of the

Auxiliary Feed

Pumps During Plant Startup

and Shutdown",

and surveillance

test Procedures

OHP 4030.STP.017T

and

OHP 4030.STP.017R

for the turbine

driven and motor driven auxiliary feedwater

pumps require checking the

AFW line temperature

30 minutes

and

90 minutes after stopping

an

AFW

pump.

Procedure

OHP 4022.056.001

"Steam Binding in Auxiliary Feed

Pumps"

provides guidance for recognizing

steam binding and for restoring the

AFW

pump to operable

status if steam binding were to occur.

The Hay 31,

1988 response

also committed to reference

the Generic Letter

in the above procedures

in the next biennial

review to assure that

procedures will be maintained.

Review of how the licensee

implements

changes

to procedures

because

of commitments disclosed

some weaknesses

in

their system.

Procedures

1-OHP 4030.STP.017T

and

1-OHP 4030.STP.017R

were

revised for their biennial review on June

10,

1988 and June

30,

1988 and

neither included the reference

to GL 88-03.

These

were realatively close

to the

May 31,

1988 commitment date

and it can

be understood

how the

reference

would not be included.

However,

Procedure

1-OHP 4021.056.002

was issued

as Revision 9, incorporating biennial review,

on February

21,

1989, eight and one half months after the commitment date

and did not

include the reference

to GL 88-03.

It was found the the licensee

took

six months to place the change letter for each of the procedures

in the

file so it would be reviewed during the next biennial review.

This

change letter

was dated

November 30,

1988 and was put in the file after

the biennial

review for the above

Procedure

(1-0HP,4021.056.002)

was

started.

It appears

that once

a biennial

review is started

the change

file is not reviewed during the revision process

even if that process

takes three months.

The fact that the reference to Generic Letter 88-03 was not included

in the above procedures

in a timely manner

and that

AFW line temperature

checks

were guidelines

instead of requirements

may have contributed to

the licensee's

inability to recognize

the lack of tour performance

in

the Auxiliary Feed

Pump

Rooms

by the auxiliary equipment operator

(AEO)

(see

Paragraph

3.b).

Additionally, the

AEO did not check the

AFP

discharge

lines to see if they were at ambient

room temperature.

Thus,

the licensee

did not fully meet their commitment as defined in their

May 31,

1988 response

to Generic Letter 88-03.

This item will remain

open pending additional

NRC investigation of the auxiliary operators

performance with regard to fulfillingthe above

commitments.

23

'P

No violations, deviations,

unresolved

or open items were identified.

Alle ations

92705)

(Closed) Allegation

(AMS No. RIII-89-A-0075):

An anonymous allegation

was received in the

NRC resident office on May 28,

1989.

It alleged that

a current trend at the station is to assign junior Radiation Protection

Technicians

(RPTs) to job coverage

for work formerly done

by experienced

RPTs,

and that the junior RPTs

do not perform as well as senior

RPTs in

that they give no direction or recommendations

regarding minimization of

contamination

and radiation exposure.

The alleger referred to current

work on the reactor

head

and cited an instance

where

a junior technician

was in the wrong place

when two contaminations

and

a 150 mr exposure

occurred.

In review of the allegation,

the inspector contacted

the Radiation

Protection

Manager

(RPM),

a plant health physicist,

the contractor site

manager

and training coordinator,

four licensee

RPTs, three of whom were

previously contractor

RPTs during previous refueling outages,

and two

mechanical

maintainance

workers with combined experience of about

24 years at the station.

The inspector also reviewed radiation

protection training and personnel

qualification records,

and radiation

protection logs.

The inspector's

review focused

on work performed

by

junior technicians

currently and during the previous

outage.

Discussion:

The current station

(house

and contractor )

RPT staff consists

of about

60 senior

and

17 junior.technicians.

During the two outages

which

overlapped

in winter/spring 1989,~the total

number of RPTs consisted

of about

110 seniors

and

65 juniors compared to about

80 seniors

and

15 juniors used during the spring 1988 refueling outage.

According to

the licensee,

the increase

in the ratio of juniors to seniors

was

due

to contract senior

manpower shortages

in early 1989.

It is licensee

practice that junior RPTs perform all radiation protection functions

under the direction of a senior

RPT and/or

a Job Coverage

Coordinator

(JCC).

According to the

RPTs interviewed these functions included

performing direct and indirect pre-job and routine surveys,

counting air

samples

and smears,

personal

and material control at control access

points,

personnel

frisking, providing guidance in removal of protective

clothing,

and general

assistance

to a senior

RPT or JCC.

The licensee

allows direct job coverage of

RWP work to be performed by junior RPTs

only under controlled conditions.

Only one of the

RPTs interviewed

indicated performance of senior

RPT work while a junior RPT.

This was

stated to have

been performed

under controlled conditions during the

last outage.

All of the

RPTs inter viewed stated that as junior RPTs it

was not their function to make recommendations/suggestions

concerning

radiological controls unless

authorized.

They stated that during outage

activities the junior RPTs did control access

points to check personal

dosimetry,

perform frisks if necessary,

and provide guidance in

minimizing personal

exposure

and contamination.

However, questions

0

involving workers

SRD readings

or existing radiological conditions in

a work area

were normally directed to a senior

RPT or JCC.

Neither of

the maintanance

workers recalled

seeing

any instances

where junior RPTs

were performing senior jobs,

nor could they recall other workers

expressing

concern

about this matter.

With regard to the alleged event involving anonymous individuals with

personal

contamination,

and

an

SRD reading of 150

NR, occurring when

a

junior RPT was at a control point to provide assistance,

the inspector

was unable to identify any such occurrences.

The inspector

reviewed training lesson plans, training and test records

and personnel

qualification check sheets for the

RPTs interviewed.

The

record

showed that the junior RPTs received

formal training by the

licensee:

General

Employee Training (GET) and

RCT Training.

Contract

junior RCTs receive

GET and Procedure training,

and additional training

by the contractor.

Based

on this review and discussions

with the

contractor training coordinator it appears

the training is sufficient

and commensurate

with junior RPTs assigned

duties.

The allegation

was not substantiated.

Although it appeared

there were

more junior RPTs

used in 1989 compared to the previous year,

the

inspector could not find any evidence to indicate there

was

a trend to

assign junior

RPTs to jobs formerly assigned

to senior

RPTs,

nor could he

establish that junior RCTs did not have the qualifications to perform

their assigned

duties.

Also, the inspector could not determine if one of

the junior RPTs

was in the wrong place

when two contamination

events

and

a 150

mr reading occurred

on a worker's

SRD.

No violations, deviations,

unresolved

or open items were identified.

Re ion III Re uests

(92705)

Based

on a report from another licensee with a similar design to

D.C.

Cook plant, that the

FSAR was incorrect in stating

steam generator

blowdown would isolate

on initiation of auxiliary feedwater,

the

inspector

was requested

to determine

how steam generator

blowdown would

be handled in conjunction with auxiliary feedwater initiation at

D.C.

Cook.

By review of design documentation

and discussions

with plant personnel,

the inspector determined that manual initiation of auxiliary feedwater

does not affect steam generator

blowdown.

All automatic auxiliary

feedwater initiations,

on the other hand,

are

accompanied

by steam

generator

blowdown isolation.

This is because

the auto-start logic

processes

the start signals

(steam generator

lo-lo level, main feed

trip loss of load,

SIS) via the "feedwater conservation circuit."

This circuit has

a separate

output to isolate

blowdown.

-FSAR Figure 7.2-1 does

not detail the above logic, but neither

does it

incorrectly claim a blowdown isolation which does

not exist.

25

The above information was conveyed to the requesting party in NRC

Region III.

No violations, deviations,

unresolved or open items were identified.

Mana ement Meetin

(30702

A Management

Meeting (attended

as indicated in Paragraph

1.b above)

was

conducted

on November 16, 1989, for the purpose of discussing

recent

operating events

and plant management/staff

changes.

The licensee

provided information and assessments

regarding the concerns

raised

by

the

NRC staff and was responsive

to associated

questions.

The focus

of the meeting

was generally

on plant status

knowledge

and control of

plant activities and configuration.

Failures to exercise

adequate

control,

as exemplified by the violation identified in this report

(Paragraph

10.g) were specifically discussed.

Licensed

0 erator Trainin

Meetin

An NRC concern

was raised

due to a high failure rate during the conduct

of operator licensing simulator examinations at

D. C.

Cook.

A follow-up

NRC inspection

was also conducted to help clarify the root cause for the

high simulator failure rate in July.

The inspection results

indicated

that the training program exhibited

some possible

weaknesses

that

collectively contributed to the failures.

These

included weakness

in

the program evaluation

methods,

inconsistency with the

NRC exam method,

weakness

in the

SRO control board training and ineffective program

feedback

mechanisms.

16.

In response

to the

NRC concerns

and findings the licensee

agreed with the

basic issues

but took exception to the numbers

and types of malfunctions

and events

used in NRC simulator

exams

as being inappropriate

and

unrealistic or of low probability.

The region responded

to the licensee

concerns

by inviting facility

training representatives

to the region to discuss

exam strategy.

During

the meeting held on November 16, 1989,

members of the region staff and

the facility training staff exchanged

viewpoints

and methods for

, establishing

simulator event sequences.

At the conclusion the facility

representatives

and region staff had reached

a clearer understanding

of

each others expectations.

Mana ement Interview

30703

The inspectors

met with licensee

representatives

(denoted in Paragraph l.a)

on November 17, 1989, to discuss

the scope

and findings of the inspection

as described

in these Details.

In addition, the inspector also discussed

the likely informational content of the inspection report with regard to

documents

or processes

reviewed by the inspector during the inspection.

The licensee

did not identify any such documents/processes

as proprietary.

The following items were specifically discussed:

a.

the licensee-identified violation of auxiliary operator shift tour

procedures

(Paragraph

3.b);

b.

the potentially significant discovery of erroneous

setpoints for

Unit 2 turbine-driven auxiliary feedwater

flow retention actuation

(Paragraph 6.f);

C.

d.

various observations

involving emergency

procedures

and training

which arose

from utilization/evaluation of the control

room

simulator (Paragraph 9.c); and,

the licensee-identified violation involving concurrent inoperability

of elements

of both independent

safety trains

(Paragraph

10.g)

and

the associated

Management

Meeting (Paragraph

14).

27