ML17313A560

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Forwards Insp Repts 50-528/98-14,50-529/98-14 & 50-530/98-14 on 980526-0721.Apparent Violations Being Considered for Escalated Enforcement Action
ML17313A560
Person / Time
Site: Palo Verde  
Issue date: 08/28/1998
From: Howell A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: James M. Levine
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
Shared Package
ML17313A561 List:
References
50-528-98-14, 50-529-98-14, 50-530-98-14, NUDOCS 9809090298
Download: ML17313A560 (77)


See also: IR 05000528/1998014

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

~

REGION IV

6) ) RYAN PLAZADRIVE SUITE >00

ARLINGTON TEXAS 760)) 6064

August 28,

1998

EA 98-382

James

M. Levine, Senior Vice

President, Nuclear

Arizona Public Service Company

P.O. Box 53999

Phoenix, Arizona 85072-3999

SUBJECT: NRC INSPECTION REPORT 50-528/98-14; 50-529/98-14; 50-530/98-14

Dear Mr. Levine:

From May 26 through July 21, 1998, a special inspection was conducted at your Palo Verde

Nuclear Generating Station, Units 1, 2, and 3, reactor facilities in response to your identification

of degraded performance capabilities of the high-pressure safety injection system.

Additional

in-.office review was conducted following the onsite portion of the inspection and an exit meeting

was conducted on July 21, 1998. The enclosed report presents the scope and results of that

inspection.

Based on the results of the inspection, four apparent violations were identified and are being

considered for escalated enforcement action in accordance with the "General Statement of

Policy and Procedure for NRC Enforcement Actions" (Enforcement Policy), NUREG-1600,

Revision 1. These apparent violations involve: 1) one apparent violation with two examples of

Technical Specification 3.5.2 for operating Units 1 and 2 with an'inoperable high-pressure

safety injection system flowpath for greater than the allowed outage, time; 2) one apparent

violation with three examples of Technical Specification 3.0.3 for having both trains of the

high-pressure safety injection system (Units 1 and 2) inoperable without initiating actions to shut

down the plant; 3) one apparent violation with five examples of 10 CFR Part 50, Appendix B,

Criterion XVI,"Corrective Action," for not promptly identifying and not promptly

correcting'roblems

with the high-pressure safety injection pump discharge check valves; and 4) one

apparent violation with two examples of Technical Specification 6.8.1 for not making required

control room log entries.

Accordingly, no Notice of Violation is presently being issued for these

inspection findings. In addition, please be advised that the number and characterization of

apparent violations described in the enclosed report may change as a result of further NRC

review.

An open predecisional enforcement conference to discuss these apparent violations has been

scheduled for September

14, 1998, at 9 a.m. (CDT) in the Region IV office. The decision to

hold a predecisional enforcement conference does not mean that the NRC has determined that

violations have occurred or that enforcement action will be taken.

This conference is being held

PDR

ADQCK 05000528

1

J'.

PDR

Arizona Public Service Company

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to obtain additional information to enable the NRC to make an enforcement decision, such as a

common understanding of the facts, root causes,

missed opportunities to identify the apparent

violations sooner, corrective actions, significance of the issues, and the need for lasting and

effective corrective action.

The predecisional enforcement conference willprovide an opportunity for you to point out any

errors in our inspection report and for you to provide any information concerning your

perspectives on 1) the severity of the violations, 2) the application of the factors that the NRC

considers when it determines the amount of a civil penalty that may be assessed

in accordance

with Section VI.B.2 of the Enforcement Policy, and 3) any other application of the Enforcement

Policy to this case, including the exercise of discretion in accordance with Section Vll.

In addition, during the predecisional enforcement conference, we would like you to address:

1) the adequac'y of your operating experience assessment

program to identify the applicability

of operating experience and to properly assess

industry or in-house information on the

operation of your facilities; 2) the adequacy of your inservice testing program to determine

check valve operability; 3) efforts to improve operator logkeeping practices; 4) the evaluation of

the as-found degraded condition of the high-pressure safety injection system with respect to

conformance to the emergency core cooling system acceptance

criteria of 10 CFR 50.46; and

5) the justification that a failure of an emergency diesel generator to continue running at some

point during its mission time should not be considered the most limiting single failure

consideration.

With respect to item 4), to the extent that this evaluation used assumptions and

inputs that were different from those that were in effect prior to the discovery of the condition,

we request that you specifically identify these differences and discuss the bases for them.

You willbe advised by separate correspondence

of the results of our deliberations on this

matter.

No response

regarding these apparent violations is required at this time.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure willbe placed in the NRC Public Document Room (PDR).

Should you have any questions concerning this inspection, we willbe pleased to discuss them

with you.

Since rel,

Arthur T. Ho

II III Director

Division of Reactor Safety

Docket Nos.:

50-528; 50-529; 50-530

License Nos.: NPF-41; NPF-51; NPF-74

Arizona Public Service Company

~3-

Enclosure:

NRC Inspection Report

50-528/98-'I4; 50-529/98-14; 50-530/98-14

cc w/enclosure:

Mr. Steve Olea

Arizona Corporation Commission

1200 W. Washington Street

Phoenix, Arizona 85007

Douglas K. Porter, Senior Counsel

Southern California Edison Company

Law Department, Generation Resources

P.O. Box 800

Rosemead,

California 91770

Chairman

Maricopa County Board of Supervisors

301 W. Jefferson, 10th Floor

Phoenix, Arizona 85003

Aubrey V. Godwin, Director

Arizona Radiation Regulatory Agency

4814 South 40 Street

Phoenix, Arizona 85040

Angela K. Krainik, Manager

Nuclear Licensing

Arizona Public Service Company

P.O. Box 52034

Phoenix, Arizona 85072-2034

John C. Horne, Vice President

Power Supply

El Paso Electric Company

2025 N. Third Street, Suite 220

Phoenix, Arizona 85004

Terry Bassham,

Esq.

General Counsel

EI Paso Electric Company

123 W. Mills

El Paso, Texas

79901

Arizona Public Service Company

Mr. Robert Burt

Los Angeles Department of Water & Power

Southern California Public Power Authority

111 North Hope Street, Room 1255-B

Los Angeles, California 90051

Mr. David Summers

Public Service Company of New Mexico

414 Silver SW, ¹1206

Albuquerque, New Mexico 87102

Mr. Brian Katz

Southern California Edison Company

14300 Mesa Road, Drop D41-SONGS

San Clemente, California 92672

Mr. Robert Henry

Salt River Project

6504 East Thomas Road

Scottsdale, Arizona 85251

Arizona Public Service Company

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E-Mail report to T. Frye (TJF)

E-Mail report to D. Lange (DJL)

E-Mail report to NRR Event Tracking System (IPAS)

E-Mail report to Document Control Desk (DOCDESK)

bcc to DCD (IE01)

bcc distrib. by RIV:

Regional Administrator

DRP Director

Branch Chief (DRP/D)

Senior Project Inspector (DRP/D)

Branch Chief (DRP/TSS)

W.L. Brown, RC

OE:EA File, MS: 7-H5

Resident Inspector

DRS-PSB

MIS System

RIV File

G.F. Sanborn, EO

J. Lieberman, OE, MS: 7-H5

DOCUMENT NAME: r:QpApv814rp.rib

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Arizona Public Service Company

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E-Mail report to T. Frye (TJF)

E-Mail report to D. Lange (DJL)

E-Mail report to NRR Event Tracking System (IPAS)

E-Mail report to Document Control Desk (DOCDESK)

bcc to DCD (IE01)

bcc distrib. by RIV:

Regional Administrator

DRP Director

Branch Chief (DRP/D)

Senior Project Inspector (DRP/D)

Branch Chief (DRP/TSS)

W.L. Brown, RC

OE:EA File; MS: 7-H5

Resident Inspector

DRS-PSB

MIS System

RIV File

G.F. Sanborn, EO

J. Lieberman, OE, MS: 7-H5

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DOCUMENT NAME: rA pv'tpv814rp.rib

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OFFICIAL RECORD, COPY

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ENCLOSURE

U.S. NUCLEAR REGULATORYCOMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-528; 50-529; 50-530

NPF-41; NPF-51; NPF-74

I

50-528/98-14; 50-529/98-14; 50-530/98-14

Arizona Public Service Company

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

5951 S. Wintersburg Road

Tonopah, Arizona

May 26 through July 21, 1998

R. Bywater, Reactor Inspector, Engineering Branch

N. Saigado, Resident Inspector

Thomas F. Stetka, Acting Chief, Engineering Branch

Division of Reactor Safety

ATIACHMENTS:

Attachment 1:

Supplemental Information

Attachment 2:

Simplified HPSI Flow Diagram

Attachment 3:

Degraded HPSI Flow Profile

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EXECUTIVE SUMMARY

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

NRC Inspection Report 50-528/98-14; 50-529/98-14; 50-530/98-14

This special inspection was conducted to review the safety and regulatory implications of

excessive high-pressure safety injection pump discharge check valve reverse leakage for

Units 1 and 2. The licensee identified and reported these conditions to the NRC in accordance

with 10 CFR Part 50.72 on May 14 and 15, 1998. The onsite portion of the inspection was

conducted during the weeks of May 25 and June 8, 1998. Additional in-office inspection was

conducted through July 21, 1998. The inspection also assessed

the licensee's evaluation of

the degraded conditions.

~oerations

Two examples of an apparent violation of Technical Specification 3.5.2 were identified

for inoperability of the Unit 1 Train "B" high-pressure safety injection flow path for

approximately 6 years and the Unit 2 Train "A"high-pressure safety injection flowpath

for approximately 5 years (Sections E1.1.b.2 and E1.1.b.4).

Two examples of an app'arent violation of Technical Specification 6.8.1 were identified

for inadequate logkeeping practices.

Abnormal conditions were not recorded in the Unit

2 control room logs when an unexpected safety injection tank level decrease

occurred

on October 10 and 28, 1997 (Section E1.1.b.1).

Two examples of an apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI,

were identified for not identifying and correcting excessive reverse flowthrough

Valve 2PSIB-V405 following two Unit 2 safety injection tank level decrease

events on

October 10 and 28, 1997 (Section E1.1.b.1).

Units'

and 2 log entries on May 13 and 14, respectively, did not address operability

of the opposite-train high-pressure safety injection flow path when operability of

Valves 1PSIA-V404 and 2PSIB-V405 was in question (Section 01.1).

One example of an apparent violation of Technical Specification 3.0.3 was identified for

not initiating actions within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, to place Unit 1 in a mode in which Technical Specification 3.5.2 did not apply when the Train "A"high-pressure safety injection

system was declared inoperable because of a problem with Valve 1PSIA-V404

(Section 01.1).

A second and third example of an apparent violation of Technical Specification 3.0.3

were identified for performing online maintenance

on the Unit 1 Train "A"and Unit 2

Train "B" high-pressure safety injection systems without isolation from the opposite train,

in excess of 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />, while the associated

high-pressure safety injection pump

discharge check valves were inoperable (Section E1.2).

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~

The licensee's investigation report was objective and provided a candid self-assessment

of its performance; however, it did not evaluate inspector-identified issues in the areas

of operations or online maintenance (Section E8.1).

Maintenance

A third example of an apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI,

was identified. On April 9, 1998, the licensee missed an opportunity to correct the

inoperable condition of Valve 1PSIA-V404 when a personnel error was made during

maintenance,

resulting in the valve being reassembled

incorrectly and the excessive

reverse leakage not being corrected (Section E1.1.b.2).

~En ineerin

~

A fourth and fifth example of an apparent violation of 10 CFR Part 50, Appendix B,

Criterion XVI,were identified for inadequate corrective actions in the development of

maintenance and testing procedures following operating experience assessments

of

NRC Information Notices 88-70 and 89-62 (Section E1.4).

Re ort Details

Event S no sis

This event involved excessive reverse flow through high-pressure safety injection (HPSI) pump

discharge check valves in Units 1 and 2 caused by the incorrect assembly of the check valves.

The incorrect assembly of the check valves prevented the valves from properly seating during

reverse flowtest conditions. Therefore, the reverse leakage caused by an improperly seating

valve, could have caused reduced HPSI injection flowduring an accident

A simplified diagram of the HPSI system is depicted in Attachment 2. The HPSI system for

each unit is comprised of two trains, "A"and "B," and each train has a pump, which takes

suction from either the refueling water tank (RWT) or the containment recirculation sump. The

discharge of each pump passes through a check valve, designated xPSIA-V404 for the

Train "A"valve (where 'x's the unit designator) and xPSIB-V405 for the Train "B"valve. The

discharge from each pump is then separated

into four cold-leg injection lines, one for each of

the cold legs of the reactor coolant system (RCS), and a hot-leg injection line. Each cold-leg

injection line contains a motor-operated valve and the flowpath is combined with the opposite

HPSI train to form a single flowpath. Upon a safety injection actuation signal, the HPSI trains

are cross connected via the cold-leg injection lines.

If a HPSI pump is not operating and the

motor-operated valves for both trains are open, the HPSI pump discharge check valve for the

idle pump provides isolation from the operating train. This prevents diversion of HPSI flowfrom

the RCS to ensure that an adequate amount of flow is provided for emergency core cooling

~

during a loss-of-coolant accident (LOCA).

A check valve that was improperly assembled

could affect the leakage through the valve during

reverse flow conditions.

For example, referring to the simplified flowdiagram in Attachment 2, if

the "B" HPSI pump discharge check valve SIB-V405 were to fail to close completely under

reverse flow conditions, and the "B" HPSI pump was not running with the injection valves open,

part of the injection flowfrom the "A"HPSI pump would be directed back through HPSI Valves

SIA-UV617, -627, -637, -647 and SIB-UV616, -626, -636, -646. The flowwould then be

directed through the "B" HPSI pump mini-flowline Valves SIB-UV667 and SIB-659, and back to

the RWT. As stated previously, upon a safety injection actuation signal, the cold-leg injection

valves would open and remain open.

The HPSI pump discharge check valves are 4-inch, 1500-pound, bonnet-hung, pressure-seal

swing check valves manufactured by Borg-Warner.

On April 9, 1998, during a Unit 1 refueling

outage surveillance test, Valve 1PSIA-V404, the Unit 1, Train "A"HPSI pump discharge check

valve, failed to meet its acceptance

criterion for reverse flowduring a flow test. The cause of

the condition was determined to have been vertical misalignment of the valve disc within the

valve body, which caused the disc to become cocked and not seat properly. On May 7, 1998,

the licensee concluded that the amount of leakage resulted in a condition outside the design

basis of the facility.

Valve 1PSIA-V404 was repaired during the Unit 1 refueling outage and its post-maintenance

test was completed satisfactorily.

However, on May 13, 1998, with Unit 1 operating, the check

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valve system engineer determined that the valve had been repaired incorrectly. Additional

testing confirmed that the valve was inoperable because of excessive reverse leakage.

The

licensee repaired the valve and returned the Unit 1 HPSI system to an operable condition on

May 15, 1998.

During its review of the applicability of the vertical misalignment issue to other HPSI pump

discharge check valves, the licensee performed non-intrusive measurements

of valve

dimensions and reviewed previous surveillance test data.

On May 14, 1998, the licensee

suspected that Valve 2PSIB-V405, the Unit 2, Train "B" HPSI pump discharge check valve was

also misaligned and testing confirmed that the valve had excessive reverse flow. The licensee

reworked the valve and returned the Unit 2 HPSI system to an operable condition on May 16,

1998. On June 5, 1998, they reported the condition to the NRC in Licensee Event Report

(LER) 50-528/-529/-530/98-006.

The reverse leakage conditions were masked prior to April 9, 1998, due to an inadequate

surveillance test.

Specifically, the surveillance test in use only measured the injection flow rate

to the reactor vessel under limited conditions and did not quantify the reverse flow leakage

through the check valves..

The NRC initiated this inspection to review the event, determine if the licensee had returned the

HPSI systems to an operable condition, and assess

the licensee's performance.

I 0 erations

01

Conduct Of Operations

01.1

Unit 1 and Unit 2- Technical S ecification TS 3.0.3 Late Ent

The inspectors reviewed events and circumstances associated with the initial logging of

a late entry into TS 3.0.3 for Unit 1 and Unit 2 when HPSI pump discharge check valves

were inoperable because of excessive reverse flow leakage.

Observations and Findin s

Unit 1

The Limiting Condition for Operation (LCO) for TS 3.5.2 requires that two emergency

core cooling system (ECCS) subsystems

shall be operable for each unit with each

subsystem comprised of an operable HPSI pump, an operable low-pressure safety

injection (LPSI) pump, and an independent operable flowpath.

If a HPSI pump

discharge check valve allows excessive reverse flow, then the opposite-train ECCS

subsystem does not contain an independent operable flowpath. When the HPSI

systems are interconnected via the cold-leg injection valves, the check valve is the

flowpath boundary.

An action requirement associated

with TS 3.5.2 allows one ECCS

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subsystem to be inoperable for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> prior to requiring the initiation of a plant

shutdown.

Technical Specification 3.0.3 requires if an LCO is not met, except as allowed by the

associated

aqtion requirement, that the licensee shall initiate action within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to

place the unit in a mode in which the LCO is not applicable.

As documented

in the Unit 1 log for May 13, 1998, at 3 a.m. the licensee began a

planned Train "A"equipment maintenance outage and declared Train "A"equipment,

including the Train "A" HPSI system inoperable.

On May 13, 1998, at 1 p.m., the licensee conducted a meeting to discuss operability of

Valve 1PSIA-V404, the Unit 1 Train "A"HPSI pump discharge check valve. The

licensee had questioned whether the valve had been assembled correctly following

maintenance during the April 1998 refueling outage.

(For additional details, see Section

E1.1.b.3).

The licensee's reportability determination, dated May 21, 1998, documented

that at this meeting, operations personnel concluded that sufficient evidence existed to

suggest that the valve might not perform its intended function, and that the valve was

declared inoperable, pending testing.

J

Following the

1 p.m. meeting, the Unit 1 operators made an entry in the Unit 1 log at

2:32 p.m. that HPSI Train "A"was inoperable due to the potential that the internals for

Valve 1PSIA-V404 were misaligned (HPSI Train "A"was already inoperable.

This entry

explicitly identified a new cause for the inoperable condition.) The entry also stated that

operations would establish conditions necessary to test the valve for reverse flowand

was proceeding with isolating the Train "A"HPSI system from the Train "B" HPSI

system.

The inspectors noted that the log entry did not address operability of the HPSI

Train "B" flowpath.

The operators completed the isolation of the HPSI trains at 3:45 p.m.,

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 13

minutes after the 2:32 p.m. Iog entry. The licensee informed the inspectors that the

isolation of the HPSI trains, by closing and removing power from the Train "A"HPSI loop

injection valves, was performed to provide equipment isolation in preparation for testing

and maintenance on Valve 1PSIA-V404. The licensee further stated that the isolation

was not initiated to separate

the HPSI trains to prevent flow diversion from the Train "B"

HPSI system through the Train "A"HPSI pump discharge check valve during an

accident.

Since, as discussed

in Section E1.2 of this report, the reverse flow leakage

through the check valve reduced the HPSI flow required to mitigate an accident

condition, the inspectors considered that Train "B"did not have an independent operable

flowpath. The Train "A"HPSI system was already inoperable for maintenance.

Consequently, this condition exceeded the LCO for TS 3.5.2, and therefore, if operators

had known that the check valve would not perform its intended function, an entry into

TS 3.0.3 was required.

Control room operators did not record the TS 3.0.3 entry in the Unit 1 log. The LER for

this event, dated June 5, 1998, stated that TS 3.0.3 was unknowingly entered when

Valve 1PSIA-V404 was declared inoperable.

During later discussions,

the licensee

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informed the inspectors that operators recognized the flowdiversion potential and

impact on system operability, but considered the condition to be a degraded condition

until testing confirmed otherwise.

The inspectors believed that this contradicted the

documentation of the conclusions reached at the May 13 meeting as documented in the

reportability determination.

The inspectors concluded that TS 3.0.3 should have been

entered at 2:32 p.m. on May 13, when HPSI Train "A"was declared inoperable due to

Valve 1PSIA-V404.

TS 3.0.3 required that within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, action shall be initiated to place the unit in a mode

in which TS 3.5.2 did not apply. The basis for T.S. 3.0.3 stated that the purpose of the

1

hour was to allow for the preparation for an orderly shutdown before initiating a change

in plant operation and that this time permits the operator to coordinate the reduction in

electrical generation with the load dispatcher to ensure the stability and availability of the

electrical grid. Even though the control room operators recognized that the inoperable

check valve had an impact on system operability, they did not initiate action to place the

unit in a mode in which the HPSI system was not required.

When the inspectors

discussed this issue with department management

representatives,

the inspectors

determined that these managers were unfamiliar with the 1-hour requirements of

TS 3.0.3. The managers informed the inspectors that they considered the

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

specified in TS 3.0.3 as an additional hour that was available to correct the inoperable

condition instead of the time allowed to prepare for an orderly plant shutdown.

At 3:45 p.m. on May 13, 1998, operators completed the isolation of all four Train "A"

HPSI RCS injection valves (Valves SIA-HV-617, 627, 637, 647). Therefore, Train "B"of

the HPSI system was made operable at that time. On May 16, 1998, operators

concluded that both trains of the HPSI system were inoperable on May 13, 1998, and

documented a late entry into TS 3.0.3. The operators initiated CRDR 180317 to have

,the TS 3.0.3 issue evaluated.

The inspectors verified that a late entry was made into

the Unit 1 log. The inspectors considered that TS 3.0.3 was declared from 2:32 p.m. on

May 13, 1998, when Valve 1PSIA-V404 was inoperable, until the Train "B" HPSI system

flowpath was made operable at 3:45 p.m. by isolating the two HPSI trains. Subsequent

to the onsite portion of the inspection, the licensee changed its position with respect to

the late entry into TS 3.0.3 and revised the logs accordingly.

The licensee's failure to comply with the requirements of TS 3.0.3 was determined to be

an example of an apparent violation (50-528/-529/-530/9814-01).

Unit 2

On May 14, 1998, at 9:55 p.m., operations declared the Train "B" HPSI pump inoperable

after receiving a memorandum from engineering (see Section E1.1.b.4) recommending

that Valve 2PSIB-V405, the Train "B" HPSI pump discharge check valve, be declared

inoperable.

The memorandum did not differentiate between the operability of the safety

function of the valve to close versus the safety function of the valve to open. The

inspectors'eview of the log entries indicated that operators did not recognize that when

the Train "B" HPSI pump discharge check valve was inoperable, it affected HPSI system

operability of both trains, and required entry into TS 3.5.2 for an inoperable Train "A"

flowpath and possibly an entry into TS 3.0.3 if there was a concern about the operability

of the safety function of the valve to open.

Operators did not declare the Train "A"HPSI

flowpath inoperable.

In a similar manner to the Unit 1 actions, operators isolated the

HPSI trains in anticipation of performing testing and maintenance on Valve 2PSIB-V405.

For this case, however, isolation of the Train "B" HPSI injection valves was completed

within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, at 10:35 p.m. On May 16, 1998, the Unit 2 log had a late entry

documenting that at 9:55 p.m. on May 14, 1998, an entry into TS 3.0.3 was required due

to the Train "A"HPSI system being inoperable due to Valve 2PSIB-V405 being

suspected of having excessive back leakage.

Another late entry on May 16

documented that at 10:35 p.m. on May 14, TS 3.0.3 was exited when the Train "B" HPSI

injection valves were isolated.

Subsequent

to the onsite portion of the inspection, the

licensee changed its position with respect to the late entry into TS 3.0.3 and revised the

logs accordingly.

Conclusions

03

Operations personnel did not demonstrate

an understanding of TS requirements nor an

understanding of the impact of the misaligned HPSI check valve on system operability.

A'n example of an apparent violation was identified for failure to implement the

requirements of TS 3.0.3 for Unit 1

~

Operations Procedures and Documentation

03.1

Res

onse to Inade

uate HPSI Flow

Ins ection Sco

e

The inspectors reviewed existing procedures that the licensee would have used during

LOCA scenarios involving inadequate

HPSI flow. The inspectors also interviewed

reactor operators and observed two crews in the simulators respond to a LOCA with

degraded HPSI flow.

Observations and Findin s

A senior reactor operator walked the inspectors through existing procedures that control

room operators would be expected to use during a LOCA with inadequate safety

injection flow. Emergency Procedures 40EP-9EO03, "Loss of Coolant Accident,"

Revision 5, and 40EP-9EO09, "Functional Recovery," Revision 6, addressed

the

degraded HPSI flow condition and the required actions to recover the inventory control

safety function. The inspectors verified that the instrumentation available to the

operators in the control room would allow for the diagnosis of a degraded HPSI flow

condition.

If HPSI flowwas unacceptable

and unrestorable, the emergency procedures

provided a method of alternate response to recovery.

The inspectors also observed two

crews successfully respond to a LOCA with degraded HPSI flow scenario on the plant

simulators.

The circumstances

of this simulator scenario, "LOCAwith Degraded HPSI

Flow," July 14, 1998, were a LOCA and a failure of the Train "B" HPSI pump with its

associated

discharge check valve stuck at 15 perceht open.

Operator performance was

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considered acceptable

if the crew took action to depressurize

the RCS to initiate LPSI

injection flow prior to the reactor vessel outlet plenum level decreasing to less than 23

percent.

The performance of both crews was good.

Conclusions

The inspectors concluded that existing procedures were adequate and available for

responding to a degraded HPSI flowcondition.

II Maintenance

M1

Conduct of Maintenance

M1.1

Valve Maintenance

The inspectors reviewed the maintenance history of the HPSI pump discharge check

valves, interviewed maintenance and engineering personnel, reviewed maintenance

procedures, and examined a spare valve in the maintenance shop.

b.

Observations and Findin s

Evolution of Maintenance Procedure

The subject HPSI pump discharge check valves were 4-inch, 1500-pound, bonnet-hung,

pressure-seal

swing check valves manufactured by Borg-Warner. The licensee's

maintenance procedures for these valves had evolved since plant construction.

The

original maintenance procedure applicable to the subject valves, 08 M Manual 1024,

Revision A, did not identify specific instructions regarding how far the bonnet retaining

ring should be threaded into the body of the valve. The licensee informed the inspectors

that during plant construction, valves were disassembled

prior to being welded in place.

During reassembly,

the bonnet retaining ring was threaded into the valve body until it

bottomed after the internals were installed.

As described to the industry in NRC Information Notice (IN) 89-62, "Malfunction of

. Borg-Warner Pressure

Seal Bonnet Check Valves Caused By Vertical Misalignment of

Disc," dated August 31, 1989, the assembly instructions for the subject valves were

missing an essential assembly step, which, if not implemented, would result in the disc

assembly being suspended

too low inside the body of the, valve.

If the disc assembly

was suspended

too low, the valve may initiallyseat acceptably but still become jammed

after forward flow exercised the valve, thus preventing proper valve seating and

subsequently allowing reverse flow leakage.

The original factory assembly process

included a step that unthreaded the bonnet retaining ring after it bottomed in the valve

~ body until the correct disc height, as viewed through the end of the uninstalled valve,

was obtained.

Backing out the retaining ring to achieve the correct vertical dimension

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was not included as a required step in the licensee's original procedure

(i.e. vendor

instruction manual).

The licensee issued Procedure 31 MT-9ZZ17, "Disassembly and Reassembly of

Borg-Warne~ Check Valves," Revision 0, on November.30, 1992, after receiving.vendor:

information developed in response to IN 89-62. As discussed

in Section E1.4, the

licensee had initiallydetermined that no actions were necessary

in response to the IN.

This contributed to the 3-year delay from the time that IN 89-62 was issued to the time

that Procedure 31MT-9ZZ17 was issued.

As recommended by the vendor, the

procedure included a step of measuring the distance from the top of the valve body to

the top of the bonnet retaining ring (called the "A"dimension) before valve disassembly

and after reassembly.

However, this step did not ensure that the valve disc-to-body

vertical alignment was correct.

If the valve had been previously disassembled,

measuring the "A"dimension prior to maintenance and returning the valve to that "A"

dimension during reassembly would have merely returned the valve to its previous

configuration, which may have been incorrect.

The licensee issued Revision

1 of Procedure 31MT-9ZZ17 on November 17, 1994.

This revision included measurement

of the "B"dimension, the distance from the top of

the valve bonnet to the top of the valve body. The procedure contained instructions to

determine the correct vertical disc-to-body configuration, as determined by the

disc-to-body measurements,

and place the valve in the correct alignment.

However,

performing these steps was only required if inspection of the valve identified improper

seating.

An enhancement

to the dimensional measurement

process was implemented

in Procedure 31MT-9ZZ17, Revision 4, on January 24, 1997, to simplifythe

measurement

process.

The licensee did not adjust valve alignment when this procedure

revision was made.

The 1994 revision of Procedure 31MT-9ZZ17 appeared adequate

to ensure that the correct valve alignment was established.

Maintenance Histo

With respect to Valve 1PSIA-V404, the Unit 1, Train "A"HPSI pump discharge check

valve, when maintenance was performed on April 10, 1998, Procedure 31MT-9ZZ17

.

was not followed because of personnel error while taking measurements

to establish the

correct "A"and "B"dimensions.

This resulted in the erroneous conclusion that the

valve disc had been approximately 0.5 inches too high inside the body of the valve.

To correct this condition, a 0.5-inch spacer ring was installed.

Later, as discuhsed in

Section E1.1.b.3, the licensee recognized this error and corrected the condition by

removing the spacer on May 15, 1998.

Th'e previous time that Valve 1PSIA-V404 was

disassembled

was May 1, 1992. The steps to measure the "A"or "B" dimensions and

verify that the disc-to-body alignment was correct were not included in the maintenance

procedure at that time. Therefore, the valve disc was susceptible to cocking open since

May 1, 1992.

On May 15, 1998, the licensee discovered that the disc in Valve 2PSIB-V405, the

Unit 2, Train "B" HPSI pump discharge check valve was vertically misaligned.

Valve 2PSIB-V405 was previously disassembled

on April 14, 1993. The Unit 2 valve

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was last reassembled

prior to the revision of Procedure 31MT-9ZZ17 that would have

established the correct vertical alignment. Therefore, the valve disc was susceptible to

cocking open since April 14, 1993.

'For the remaining HPSI pump. discharge check valves on all three units, the licensee,'.-,

'valuated

the maintenance and testing history, performed as-found external

measurements

of the "A"and "B"dimensions, and performed reverse flowtests.

Each

of the remaining four valves had as-tound reverse flowtest results of 0 gpm.

Conclusions

The licensee's maintenance procedure for Borg-Warner bonnet-hung, pressure-seal

check valves did not include adequate instructions for ensuring correct vertical disc

alignment until November 1994. The inspectors concluded that the licensee missed an

opportunity to identify and correct the vertical alignment issue at that time. Once the

problem was recognized in 1998, the licensee developed and implemented an

acceptable plan to identify and correct the adverse condition on all of the HPSI pump

discharge check valves.

Valve Testin

The inspectors reviewed the inservice testing (IST) history of the HPSI discharge check

valves, interviewed maintenance and engineering personnel, and reviewed testing

'rocedures.

Observations and Findin s

The licensee identified in its OEA review of NRC IN 88-70, "Check Valve Inservice

Testing Program Deficiencies," that its IST program did not require reverse-flow testing

of the HPSI pump discharge check valves.

As discussed

in Section E1.4, the licensee

originally concluded that because they had an NRC-approved IST program, any

changes to the program were considered enhancements.

Therefore, the need for

procedure revisions was not considered a priority. The licensee added reverse-flow

testing requirements for these valves to its IST program on July 26, 1992. The test

methodology involved operating one HPSI pump and verifying adequate flowwas

delivered to the RCS when both trains of the HPSI system were cross-connected.

This

method was intended to demonstrate that the HPSI pump discharge check valve in the

idle train had closed as evidenced by maintaining sufficient flow to the RCS with

inconsequential flow diversion through the check valve. No explicit acceptance

criterion

was specified for reverse flow through the check valve. The test was performed for

each valve during refueling outages to satisfy the IST program surveillance

requirements of TS 4.0.5.

Due to the absence

of reverse flow measurements

through

these check valves, these surveillance tests did not identify that Valves 1PSIA-V404 and

2PSIB-V405 were inoperable since 1992 and 1993, respectively.

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This forward-flow testing methodology continued until the 1998 Unit 1 refueling outage.

As discussed

in Section E1.1, Procedure 73ST-9XI33, "HPSI Pump and Check Valve

Full Flow Test," Revision 9, was issued on March 12, 1998, to perform a forward-flow

type test and included an allowable 20 gpm variance in the measured flow in the

acceptance

criterion. The development of an explicit acceptance

criterion for check,

valve reverse flowwas a corrective action from Condition Report/Disposition Request

(CRDR) 2-7-0420 that was written following the October 28, 1997, Unit 2, safety

injection tank (SIT) level decrease

event described in Section E1.1.b.1. After

Valve 1PSIA-V404 failed this test on April 9, 1998, and was repaired, plant conditions

had changed and precluded the forward-flow type test from being performed.

Therefore, the licensee issued Revision 10 of Procedure 73ST-9XI33 on April 11, 1998,

which included a new testing methodology consisting of pressurizing the downstream

side of the check valve and monitoring reverse flowthrough the valve. The new

methodology was subsequently described in a new procedure (Procedure 73ST-9XI35)

issued on May 13, 1998.

After the test failure of Valve 1PSIA-V404 during the Unit 1 refueling outage,

engineering personnel continued investigation of the performance requirements for

HPSI discharge check valve reverse flow. Based on engineering analysis of ECCS

performance requirements and actual HPSI system performance (Section E1.2), the

licensee determined that a reverse flowacceptance

criterion of 10 gpm at a test

differential pressure of 50 - 125 psid would be valid for all six valves in the three units.'-

. Procedure 73ST-9XI35, "HPSI Pump Discharge Check Valve Closed Exercise Test,"

was revised to include the 10 gpm acceptance

criterion in Revision 6 on May 26, 1998.

Technical Specification 4.0.5 states, in part, that, "... Inservice testing of ASME Code

Class 1, 2, and 3 pumps and valves shall be performed in accordance with Section XI of

the ASME Boiler and Pressure Vessel Code and applicable Addenda...."

Prior to January 15, 1998, the applicable Edition of the ASME Code was the 1980

Edition through Winter 1981 Addenda.

Subsection IWV, "Inservice Testing of Valves in

Nuclear Power Plants," of Section XI of the ASME Code, Article IWV-2000, defines

Category A valves as those for which seat leakage is limited to a specific maximum

amount in the closed position for fulfillmentof their function and defines Category C

valves as those which are self-actuating in response to some system characteristic,

such as check valves. Article IWV-2000 also states that valves within the scope of this

section shall be placed in one or more categories and that when more than one

distinguishing category characteristic is applicable, all requirements of each of the

individual categories are applicable.

Effective January 15, 1998, the applicable Edition of the ASME Code was the 1989

Edition. Subsection IWV, "Inservice Testing of Valves in Nuclear Power Plants,"

required that valve testing be performed in accordance with the requirements stated in

ASME/ANSI Inservice Testing of Valves in Light-Water Reactor Power Plants OM-10,

OMa-1988 Addenda to the OM-1987 Edition. The definitions and requirements

identified above for the 1980 ASME Code Edition are equivalent to the 1989 ASME

Code Edition.

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The HPSI pump discharge check valves have a safety-related function to close to

prevent diversion of flow between trains of a system.

As identified in NUREG-1482,

"Guidelin'es for Inservice Testing at Nuclear Power Plants," the ASME Code does not

specifically require that these valves be Category A; although, there may be a leakage

limitbased qn the total system requirements.

The licensee conducts their IST program

in accordance

with Procedure 73DP-9XI01, "Pump and Valve Inservice Testing Program

- Component Tables," Revision 5. Procedure 73DP-9XI01 identified that the HPSI pump

discharge check valves were classified as Category C valves. This classification was

acceptable; however, NUREG-1482 also identified that for valves of this type that the

licensee should evaluate the consequences

of reverse flow. This evaluation should

consider: 1) the loss of water from the system and connecting systems; 2) the effect that

the leakage might have on components and piping downstream of the valve; and 3) any

increase in radiological exposure resulting from the leakage.

The licensee had not

performed evaluations of this type until the current problems with the HPSI pump

discharge check valves were identified. These evaluations are discussed

in Sections

E1

~ 1 and E1.2. At the conclusion of the onsite portion of the inspection, the licensee

was evaluating whether the HPSI pump discharge check valves should be re-classified

as Category A in the IST program.

Conclusions

The IST program was ineffective at demonstrating operability of the HPSI pump

discharge check valves.

Conduct of Engineering

HPSI S stem De raded Condition Review

Ins ection Sco

e

To review the HPSI system degraded condition, the inspectors toured relevant areas

of the facilityincluding the auxiliary building, control room, and maintenance shop.

The inspectors also conducted interviews with licensee personnel, reviewed

selected procedures, calculations, maintenance packages,

OEAs, and corrective

action documents, and reviewed the licensee's investigation report and

LER 50-528/-529/-530/98-006.

Observations and Findin s

1997 Unit 2 Outa

es

On October 28, 1997, during Unit 2 restoration prior to startup from a forced outage,

operators were performing Procedure 40OP-9SI02, "Recovery from Shutdown Cooling

to Normal Operating Lineup," Revision 14, Section 7.0, "Boration Of Cold Leg Injection

Lines," using the Train "A" HPSI pump.

During the evolution, pressure and water level

in SIT 1A decreased

unexpectedly when Valve SIB-UV638, the SIT 1A check valve

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leakage line isolation valve, was opened to establish a recirculation path for the 1A

injection line. The reactor operator closed Valve SIB-UV638, which terminated the loss

of inventory, and restored the SIT pressure.

The onshift crew contacted engineering

personnel, who determined the cause of the loss of inventory in SIT 1A was leakage

past Valve 2PSIB-V405, the Train "B" HPSI pump discharge check valve, to the.RWT;

.

The engineering personnel reviewed the results of the previously performed reverse

exercise test of Valve 2PSIB-V405, conducted during the previous refueling outage in

accordance with Procedure 73ST-9XI33, and identified that the check valve was found

to have a leakrate of approximately 30 gpm. This test had been performed to satisfy the

IST program requirements.

As stated previously in Section M1,2, the refueling outage

test was accepted because adequate forward flow to the RCS was obtained when the

HPSI trains were cross connected but there was no explicit acceptance

criterion for

reverse flowthrough the check valve. Therefore, the operators concluded that this

amount of reverse flow did not prevent the HPSI system from performing its design

function and plant startup continued.

The onshift crew initiated CRDR 2-7-0420 to

evaluate a procedure change to alert operators of the potential to affect SIT level when

performing the cold-leg boration evolution.

The check valve leakage caused a depressurization

of the loop injection piping during

the cold-leg boration to approximately 600 psig and the SIT began to discharge as

designed.

The licensee documented in the CRDR that the condition could have been

identified before ifoperations had questioned why safety injection header pressure did

not respond as expected during the cold-leg recirculation line-up prior to opening

SIB-UV638. The safety injection header pressure should have not decreased

below SIT

pressure and the SIT should not have discharged.

The CRDR also documented that,

"Operations noted the response to Pl-339 [safety injection header pressure] was not

normal, however, they were unable to explain the condition so the procedure was

continued."

The CRDR also contained a reference to a similar event, which occurred on October 10,

1997, during plant restoration prior to startup from the previous refueling outage.

Again,

SIT level decreased

during the performance of Procedure 40OP-9SI02, Section 7.0 with

the Train "A"HPSI pump.

In that particular instance, the decrease

in level was

terminated by the reactor operator closing the Train "B" injection valve and isolating the

trains. This similar example was highlighted in the CRDR because the same crew was

on duty when each SIT transient occurred during the cold-leg boration evolution. The

crew did not request engineering assistance

to evaluate the SIT level transient and the

crew did not conclude that Valve 2PSIB-V405 was leaking. Reactor startup activities

continued and the reactor was made critical later that day. With respect to the October

10, 1997, event, operations personnel had concluded that the unexpected loss of SIT

inventory was caused by an "eductor effect," which caused a localized low pressure

condition at the SIT outlet during HPSI cold-leg recirculation, and that the condition

should have been expected.

The inspectors did not consider this to be a plausible

explanation because of the high localized pressure drop that would be required to

decrease

pressure below SIT pressure.

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The inspectors reviewed control room and unit logs for October 10 and 28, 1997, and

identified that no log entries were made regarding the SIT level decreases.

The

licensee's Procedure 40DP-9OP22, "Operations Logkeeping," Revision 9, Step 3.3.5

stated, in part, "The information entered in the Control Room Log shall include...

abnormal occurrences,

unless previously logged and identified by an active corrective,. -.,

action document." The licensee did not agree with the inspectors'haracterization

that

the SIT level transients were abnormal occurrences.

The inspectors determined that the

licensee's procedures did not exempt the conditions experienced on October 10 and 28

from being logged in accordance with the logkeeping procedure.

Therefore, the

inspectors concluded that the failure to log the abnormal SIT level transients that

occurred on October 10 and 28, 1997, were two examples of an apparent violation of

TS 6.8.1, which required adherence to Procedure 40DP-9OP22

(50-528/-529/-530/9814-02).

While the licensee identified a check valve reverse leakage problem as documented

in

CRDR 2-7-0420 on October 28, 1997, they failed to take prompt corrective actions to

resolve the problem.

10 CFR Part 50, Appendix B, Criterion XVI,"Corrective Action,"

requires that measures

shall be established to assure that conditions adverse to quality

are promptly identified and corrected and in the case of significant conditions adverse to

quality that the measures shall assure that the cause of the condition is determined and

corrective action taken to preclude repetition. The inspectors considered the October 10

and 28, 1997, Unit 2 SIT drain events to have been occurrences where a significant

condition adverse to quality (excessive reverse flowthrough Valve 2PSIB-V405) was not

promptly identified and corrected.

These were considered the first two examples of an

apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI

(50-528/-529/-530/9814-03).

During the evaluation and resolution of CRDR 2-7-0420, the licensee concluded

that a 20 gpm check valve reverse leak rate acceptance

criterion should be sufficient

to prevent unacceptable

HPSI flow diversion. This conclusion was not based upon a

rigorous calculation of the impact of flow diversion; rather, it was based on a review

of leakage acceptance

criteria for some check valves in the LPSI system and the

methodology employed to select their leakage acceptance

criteria.

Procedure 73ST-9XI33 was changed in Revision 9 to include the explicit acceptance

criteria of either: 1) less than 20 gpm difference between the sum of hot and cold-leg

injection flow rates before and after the HPSI trains were cross connected; or 2) hot-leg

injection flow greater than or equal to 525 gpm, cold-leg injection flow greater than or

equal to 525 gpm, and total HPSI flow less than or equal to1200 gpm. The

forward-flow acceptance

criteria were consistent with the surveillance requirements in

TS 4.5.2.h.

Conclusions

The inspectors concluded that the licensee had an opportunity to detect the flow

diversion through Valve 2PSIB-V405 on October 10, 1997; however, the operators failed

to identify the cause of unexpected decrease

in SIT level. On October 28, the licensee

identified the condition but did not take effective corrective action because of an

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incorrect assessment

of the operability implications. Two examples of an apparent

violation were identified for the failure to make log entries for the SIT level decreases,

which occurred on two separate occasions while performing the cold-leg boration

process.

Two examples of an apparent violation were identified for inadequate

corrective aqtion to identify and correct a significant condition adverse to quality..

b.2

1998 Unit 1 Refuelin

Outa

e and Subse uent0

eration

On April 9, 1998, the licensee had indication of excessive reverse flowthrough

Valve 1PSIA-V404 during performance of Procedure 73ST-9XI33. The control room

received an unexpected equipment drain tank (EDT) high level alarm and the test was

suspended.

The licensee concluded that reverse-direction flowthrough the check valve

pressurized the Train "A"ECCS suction piping and the Train "A"containment spray (CS)

pump discharge piping to the 650 psig setpoint of Valve 1JSIA-PSV194, the Train "A"

shutdown cooling heat exchanger (SDCHX) outlet relief valve. The leak rate through

Valve 1PSIA-V404 was initiallyestimated to be 85 gpm. On April 10, 1998, the licensee

initiated CRDR 1-8-0238 to document the event and classified the CRDR as "significant"

with action requests to perform an equipment root cause of failure evaluation and

reportability determination.

During a subsequent

engineering evaluation, the licensee

estimated that the event resulted in relief valve blowdown to the EDT at a flow rate of-

approximately 120 gpm and a total leak rate through Valve 1PSIA-V404 of

approximately 214 gpm. The licensee also concluded that the valve body and disc had

been in a misaligned condition for the entire previous operating cycle and likely had

been misaligned since the last time maintenance was performed on the valve on May 1,

1992. At that time, the licensee had not yet incorporated additional guidance for

addressing vertical'misalignment concerns for Borg-Warner check valves in the

maintenance procedure.

The licensee's review and implementation of in-house and

industry operating experience is discussed

in Section E1.4 of this report.

The licensee performed Operability Determination (OD) 203 to evaluate the operability

impact of the inadvertent pressurization.

The OD evaluated the pressure rating and

ASME Code allowables for stresses

of piping and system components in the HPSI and

CS suction piping, CS discharge piping, and SDCHX. The OD concluded that the piping

and components remained operable on the basis of not exceeding ASME Code

allowable stresses for the suction piping, not exceeding the design pressure for the CS

discharge piping, and not exceeding the pressure rating of valves or flanges in the

suction piping. The licensee also performed a system walkdown with the HPSI and CS

pumps operating to examine performance of the pump seals and pipe flanges.

No leaks

were identified and no pipe supports exhibited signs of water hammer.

The inspectors

reviewed the OD a'nd concluded that the licensee's evaluation of system operability was

acceptable.

Maintenance technicians disassembled

and inspected Valve 1PSIA-V404 via Work

Order (WO) 836600 and Procedure 31MT-9ZZ17 on April 10, 1998. With engineering

support, the technicians determined that a vertical offset existed in the alignment of the '

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valve disc with respect to the valve body. The licensee concluded that the valve disc

had been located too high in the body of the valve and that the disc needed to be

lowered approximately 0.5 inch. Personnel reverified the calculation for the desired

vertical dimensions, but did not independently verify the measurement of the

dimensions., The technicians made a measurement

error that resulted in an. incorrect.

determination of the magnitude of the vertical offset. Maintenance and engineering

personnel concluded that a spacer ring would have to be installed to adjust the height of

the disc. Therefore, WO 836600 was amended to Deficiency Work Order

(DFWO) 836600 to install a carbon steel spacer ring between the silver plated pressure

seal ring and the threaded retaining ring to compensate for the vertical offset. Longer

bonnet studs were also required to accommodate the spacer.

Installation of the spacer

ring resulted in the valve disc being located too low within the body of the valve to seat

properly. The failure to correctly assemble the check valve to correct the reverse

leakage condition was considered to be the third example of an apparent violation of

10 CFR Part 50, Appendix B, Criterion XVI (50-528/-529/-530/9814-03).

A DFWO was the licensee's method for which degraded and nonconforming conditions

requiring engineering direction were dispositioned and corrected.

The licensee

considered the DFWO a design change and completed a 10 CFR 50.59 safety

evaluation to document that the change did not involve an unreviewed safety question.

The inspectors reviewed the DFWO and concluded that it included an adequate

'evaluation of the acceptability of these subcomponents

in the valve. The inspectors

asked if any as-built drawings were revised to reflect the implementation of the DFWO

and were informed that the design documents were not changed nor were they planned

to be changed.

The inspectors were concerned that installation of the spacer and

replacement of the bonnet studs without updating any design documentation was

representative of inadequate design control. The licensee informed the inspectors that

when a maintenance planner reviews the maintenance history of a component as part of

work package preparation, the maintenance history would reveal that subcomponents

had been installed or replaced such as the spacer and studs for Valve 1PSIA-V404.

The licensee, upon further evaluation, initiated CRDR 9-8-0893 to address this issue.

NRC review of CRDR 9-8-0893 is considered to be an unresolved item (URI)

(50-528/-529/-530/9814-04).

Procedure 73ST-9XI33 required full HPSI flowwith the reactor vessel head removed.

On April 11, 1998, after completion of the DFWO, the reactor vessel head had been

reinstalled.

Therefore, plant conditions did not allow the normal, forward flowtest to

be performed.

An alternate test method was developed in Revision 10 of

Procedure 73ST-9XI33 using demineralized water to pressurize the down stream side

of the check valve and opening a drain valve on the upstream side of the valve to

determine reverse flow. On completion of the test, Valve 1PSIA-V404 was declared

operable with a measured leak rate of 18 gpm at a test pressure of 96 psig. The leak

rate exceeded

an administrative limit of 10 gpm, which in accordance with the test

procedure, required the initiation of a work request.

The inspectors verified that Work Request 941341 was initiated to repair the valve during the next outage.

The licensee

informed the inspectors that it had accepted these test results as satisfactory because

they assumed that reverse-flow leakage would decrease

when HPSI pump discharge

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pressure from the opposite train improved the valve disc-to-body seat contact during

system operation.

On May 7, 1998, the licensee determined during its investigation of CRDR 1-8-0238 that

the as-foun4 condition of Valve 1PSIA-V404 on April9, 1998, represented a condition.:-

that would have prevented it from performing its intended function during an accident.

The licensee concluded that this event was reportable to the NRC per 10 CFR 50.73

and submitted LER 50-528/98-006 on June 5, 1998. The results and consequences

of

this assessment

are discussed

in Section E1.2.

Technical Specification 3.5.2 requires in Modes 1, 2, and 3, that two independent ECCS

subsystems

shall be operable with each subsystem comprised of one operable HPSI

pump, one operable LPSI pump, and an independent operable flowpath. Action

statement a. associated with TS 3.5.2 required that with one ECCS subsystem

inoperable, restore the inoperable subsystem to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in

at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in hot shutdown within the following

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

As discussed earlier, Valve 1PSIA-V404 was installed incorrectly and did not

have correct vertical disc alignment from May 1, 1992, until May 15, 1998. Therefore,

Train "B"of the Unit 1 ECCS did not have an independent operable flowpath from

May 1, 1992, until May 15, 1998, and the licensee did not comply with Action a. of

TS 3.5.2. This was considered to be the first example of an apparent violation of

TS 3.5.2 (50-528/-529/-530/9814-05).

c.2

Conclusions

The April 1998, Unit 1 refueling outage test results demonstrated that Valve

1PSIA-V404 was in a significantly degraded condition. The maintenance history for the

subject valve indicated that it had been in that condition since 1992. An example of an

apparent violation of 10 CFR Part 50, Appendix B, Criterion XVIwas identified for failure

to correct the problem with Valve 1PSIA-V404 during maintenance.

An incorrect

interpretation of the 18 gpm April 11, 1998, post-'maintenance

testing results,

contributed to continued operation with an inoperable valve. An example of an apparent

violation of TS 3.5.2 was identified for having an inoperable independent HPSI flowpath

for approximately 6 years.

b.3

Online Corrective Maintenance of Valve 1PSIA-V404

On May 13, 1998, as part of the CRDR 1-8-0238 review, the check valve engineer

reviewed measurements

of a spare Borg-Warner check valve and discussed the

maintenance

procedure and spacer installation with maintenance technicians.

The

engineer determined that a measurement

error may have occurred during the April 1998

maintenance on Valve 1PSIA-V404, resulting in a vertical disc-to-body misalignment.

The test methodology that was used in Procedure 73ST-9XI33, Revision 10, was

extracted and placed in Procedure 73ST-9XI35, Revision 0. Since the Unit 1 refueling

outage, engineering personnel had determined that a new acceptance

criterion of

30 gpm reverse flow through Valve 1PSIA-V404 would still maintain acceptable

HPSI

)I

I

-19-

forward flowfor system operability. This was based on an evaluation of the

operating performance of the HPSI pumps and system flowcharacteristics.

Procedure 73ST-9XI35, Revision 0 contained the 30 gpm acceptance

criterion. On

May 14, 1998, the licensee performed the test on Valve 1PSIA-V404 and it failed with an

as-found result of 33 gpm at a differential pressure of 95 psid. The licensee made a

- .

one-hour 10 CFR 50.72 notification to the NRC to report that this was a condition

outside the design basis of the facility.

After the failed test, the licensee disassembled

the valve, removed the spacer, ring in

accordance with WO 840712, and verified that the disc was misaligned in the valve

body. The maintenance technicians performed an inspection and exercised the valve

internals per WO 840826 and Procedure 73ST-9ZZ25. The technicians then attached a

stainless steel wire to the swing arm of the valve, installed the internals with the wire

extending outside the valve body (without the silver seal gasket installed), and set the

bonnet height to the desired vertical dimension.

When this was done, the technicians

stroked the valve by pulling on the wire until a metallic noise was heard, indicating that

the disc had contacted the backstop.

This provided an additional indication that the

valve was free to stroke. The technicians then removed the wire and reassembled

the

valve with the silver seal to the correct vertical dimensions.

The inspectors noted that WO 840712 was written to disassemble,

rework, and

reassemble

Valve 1PSIA-V404. There were no instructions included to remove the

spacer ring: The inspectors asked whether a special WO or WO amendment was

required prior to the removal of the spacer ring and whether removing the spacer ring

was a design change, as was the case previously for the installation of the spacer ring..

The licensee stated that they considered the removal of the spacer to be a rework

activity and not a design change.

Rework was defined as the process by which a.

degraded or nonconforming item is made to conform to a prior specified design

requirement by completion, machining, reassembly,

replacing, or other corrective

measures.

The inspectors noted that the materials list for Valve 1PSIA-V404 that

was attached to WO 840712 had not been updated to reflect the installation of the

new bonnet studs or spacer ring. This issue will be reviewed as part of

URI 50-528/-529/-530/9814-04 to determine whether the licensee implemented

adequate design control.

After reassembly of Valve 1PSIA-V404 without the spacer ring, operations performed

Procedure 73ST-9XI35, Revision

1 on May 15, 1998, and the valve passed its reverse

flow test with a result of 0 gpm at 142 psid.

c3.

Conclusions

The questioning attitude of the check valve engineer was instrumental to the

identification of the misalignment of Valve 1PSIA-V404. Corrective actions were taken

to restore the valve to an operable condition.

t~

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-20-

b.4

Ino erabili

of Valve 2PSIB-V405

After the April 1998 test failure of the Unit 1 Valve 1PSIA-V404, the licensee initiated

CRDR 2-8-0128 and OD No. 204 to evaluate the operability impact of this condition for

Units 2 and g.

- Included in this evaluation was a review of past HPSI fullflowtest results

conducted during the previous refueling outages and measurement of external valve

dimensions.

On May 14, 1998, as a result of this review and the results of the Unit 1

testing performed the previous day, engineering and maintenance personnel determined

that Valve 2PSIB-V405 was misaligned.

Engineering recommended to operations in

Memorandum 469-00170-BJR that the valve be declared inoperable, that reverse flow

testing be performed, and that corrective maintenance and post-maintenance

testing be

performed.

The inspectors noted that the memorandum only addressed

operability of

Valve 2PSIB-V405 and did not address operability of the entire HPSI system.

The operators declared the Unit 2 Train "B" HPSI pump inoperable based on the

recommendation of the memorandum from engineering.

The inspectors noted that this

was not consistent with the memorandum, which recommended that the Train "B"valve,

not the Train "B"pump, be declared inoperable.

The impact of reverse flowthrough

Valve 2PSIB-V405 on operability of the Train "A"HPSI system flowpath was not

addressed

in the Unit 2 log. The licensee informed the inspectors that the" Unit 2 log

entry only addressed

the inoperability of Train "B"because the operators were preparing

to perform testing and maintenance on the Train "B"valve, which required removing the

Train "B" HPSI system from service.

Based on the recommendation from Engineering

that the valve should be declared inoperable, this inoperable check valve required that

the opposite HPSI train flowpath be declared inoperable, ifthe trains were not isolated,

because of the safety function of the valve to close and prevent diversion of flowfrom

the RCS.

The licensee performed Procedure 73ST-9XI35 to measure the as-found condition of

Valve 2PSIB-V405 on May 15, 1998. The test results indicated a reverse flow rate

through the valve of 37.5 gpm at a differential pressure of 6 psid. As discussed

in

Section E1.2, this amount of reverse flowwould prevent the HPSI system from meeting

the minimum-required ECCS performance assumed

in the safety analysis during a

LOCA. The licensee issued WO 836005 to disassemble

the valve and verified that the

vertical alignment of the disc within the body of the valve was too low and had caused

the disc to hang in a cocked-open position. The valve alignment was corrected and the

valve was retested in a manner similar to that discussed above for Valve 1PSIA-V404.

The retest of Valve 2PSIB-V405 passed with a leakage rate of 0 gpm at 150 psid and

the system was declared operable on May 16, 1998. As discussed

earlier,

Valve 2PSIB-V405 was installed incorrectly and did not have correct vertical disc

alignment from April 14, 1993, until May 16, 1998. Therefore, Train "A"of the Unit 2

ECCS did not have an independent operable flow path from April 14, 1993, until May 16,

1998, and the licensee did not comply with Action a. of TS 3.5.2.

This was considered

to be a second example of an apparent violation of TS 3.5.2

(50-528/-529/-530/9814-05).

c.4

Conclusions

Cg

0

-21-

Licensee personnel successfully evaluated and confirmed that Valve 2PSIB-V405 was

misaligned and corrective actions were taken to restore the valve to an operable

condition. Testing results demonstrated that the valve was in a significantly degraded

condition and the maintenance history for the subject valve indicated that it had been in

that condition since 1993. The inspectors considered the communication between..;

.

engineering and operations a weakness,

as demonstrated

by the May 14, 1998,

memorandum from engineering, which did not provide a recommendation

regarding

HPSI system operability. An'example of an apparent violation of TS 3.5.2 was

identified.

b.5

Testin

and Vertical Dimension 0 timization of Remainin

Valves

The licensee performed reverse flowtests of the four remaining HPSI pump discharge

check valves. Allof the valves passed the 73ST-9XI35 test with 0 gpm reverse flow.

Based on external dimension measurements

and a review of previous forward-flow

surveillance tests performed during refueling outages, the licensee concluded that two

of the four valves, Valves 3PSIB-V405 and 1PSIB-V405, should be reworked for

"vertical dimension optimization."

Valve 3PSIB-V405 was disassembled,

inspected, reassembled

to a new desired

vertical dimension, and retested with 0 gpm reverse flowon May 18, 1998. When

Valve 1PSIB-V405 was inspected and reassembled

to the desired dimension on-

May 26, 1998, maintenance technicians discovered that the disc was not seating

properly. The technicians discovered that the seat angle of the valve was different than

expected.

Instead of an expected seat angle of 12 degrees, the licensee discovered

that this valve had a seat angle of 5 degrees.

The licensee contacted the vendor and

was informed that all 4-inch Borg-Warner hung-bonnet pressure-seal

valves were

supplied with a 12-degree seat angle. The inspectors questioned the licensee regarding

the procurement process and quality assurance

receipt inspection for the subject valve.

After further investigation, the licensee determined that the vendor implemented a

design change in 1980 that changed the seat angle from 5 to 12 degrees.

Valve 1PSIB-V405 was procured in 1979 and was the only HPSI pump discharge check

valve that was built prior to the vendor design change.

Therefore, its seat angle was

correct.

The licensee documented this condition in DFWO 842362.

The inspectors will

review the issue of updating design documents regarding this condition as part of the

URI regarding design control (50-528/-529/-530/9814-04).

The licensee calculated a

revised vertical dimension to account for the different seat angle, reassembled

the valve

and successfully retested the valve with no reverse flow on May 27, 1998.

c.5

Conclusions

Licensee personnel successfully confirmed that the remaining four HPSI pump

discharge check valves were operable by performing reverse-flow tests.

Testing

performed after maintenance confirmed that the valves remained operable.

The

licensee adequately demonstrated

that one of the valves (Valve 1PSIB-V405) that had

an unexpected seat angle, was acceptable for its application and was also operable.

-22-

Assessment of As-found Conditions

lns ection Sco

e

The inspectprs reviewed calculations and test results and interviewed engineering,.

~: *,

personnel to determine the safety and regulatory implications of the as-found degraded

condition of the Unit 1 and Unit 2 HPSI systems.

Observations and Findin s

Check Valve Leaka

e and De raded HPSI S stem Performance

The inspectors reviewed Calculation 13-MA-SI-982, "Evaluation of Allowable Leak Rate

Criteria for 1,2,3PSIA-V404 and 1,2,3PSIB-V405/Assessment

of As-Found Leakage for

2PSIB-V405/1PSIA-V404," Revision 0 and Calculation 13-MC-SI-215, "Revised Single

HPSI Pump Delivery Curve for Cold Leg Injection and Flow Rate Requirements for

Technical Specification 4.5.2.h," Revision 1. In Calculation 13-MA-SI-982, the licensee

performed a best-estimate

evaluation of the current as-built HPSI system delivery profile

for each HPSI pump based on historical system performance data and compared the

resultant delivery profiles to the minimum-required HPSI system delivery profile

identified in Calculation 13MC-Sl-215 that was used in the LOCA safety analyses.

The

margin between the as-built HPSI system delivery capability and the minimum-required

HPSI system delivery used in the LOCA analyses was used to estimate a maximum

allowable leakage profile'for the opposite-train HPSI pump, discharge check valve. The

results indicated that the most limitingsystem was Train "B"in Unit 3.. A maximum

leakage rate of 10.2 gpm at 40 psid was determined for Valve 3PSIA-V404, the

opposite-train HPSI pump discharge check valve, to ensure that the Train "B" HPSI

system would meet its minimum performance requirements.

The licensee also evaluated the April 9, 1998, as-found condition of Valve 1PSIA-V404

and the May 15, 1998, as-found condition of Valve 2PSIB-V405 in

Calculation 13-MA-SI-982. This evaluation concluded that the actual reverse flow rate

through Valve 1PSIA-V404 during the performance of the Procedure 73ST-9XI33,

forward-flow HPSI refueling outage test, was approximately 214 gpm. Because this test

had not been intended to obtain direct differential pressure measurements,

it did not

provide sufficient data to quantify a HPSI performance curve. However, the licensee

had enough information to conclude that the results were qualitatively similar to the

results obtained for the Unit 2 valve as described below.

Valve 2PSIB-V405 had an as-found reverse leakage test result of 37 gpm at 6 psid.

The licensee calculated an as-found loss coefficient for the subject valve and developed

a HPSI delivery curve that accounted for leakage through Valve 2PSIB-V405. The

as-found degraded HPSI delivery curve and the minimum-required ECCS delivery curve

are depicted in Attachment 3. As shown, the estimated as-found HPSI delivery

fi

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-23-

capability was significantly degraded compared to the minimum-required HPSI delivery

performance that was assumed

in the LOCA analyses.

For example, at an RCS

pressure of 1200 psig, the estimated HPSI flow rate was approximately 350 gpm less

than the flowrate assumed in the LOCA analyses..The

licensee concluded that the

results for Unit 1 were comparable.

Sin le Failure Consideration

The licensee identified in Calculation 13-MA-Sl-982 that the initial evaluation of the

April9, 1998, Unit 1 refueling outage event included assessments

of ECCS suction

piping overpressurization,

degraded HPSI performance, dose consequences,

and

impact on containment sump level following a LOCA. The licensee determined that

degraded HPSI performance (due to failure of a HPSI pump to start) was the most

limitingfactor with which to assess

the safety significance of the condition.

The inspectors questioned the basis for the licensee's conclusion. The inspectors

considered the failure of an emergency diesel generator (EDG) during a LOCA

coincident with a loss-of-offsite power to be the most limiting single failure for

consideration since none of the ECCS pumps in the affected train would be operating.

(The licensee documented

in the calculation that ifthe LPSI and CS pumps associated

with an idle HPSI pump were running, the ECCS suction piping would not be

overpressurized

as occurred on April 9, 1998, when the SDCHX relief valve lifted).

The licensee noted that failure of an EDG to start would not be a concern because the

RCS loop injection valves associated with the failed EDG would not open and cross

connect the HPSI trains,

However; the inspectors noted that under a condition where an

EDG failed to continue running after the RCS loop injection valves had opened due to a

safety injection actuation signal, a flow path would be established to pressurize the

ECCS suction piping and containment spray pump discharge piping to the SDCHX relief

valve setpoint as occurred during the April 9, 1998, Unit 1 test. The inspectors also

noted that this event created a release path via the vented RWT through the HPSI pump

minimum flow line and a loss of water inventory to the auxiliary building via the SDCHX

relief valve and should be evaluated. The licensee stated that it considered this possible

event scenario but determined that it was not necessary to consider the failure of a

component to continue running as an assumed single failure.

Section 6.3.1, "ECCS Design Bases," of the UFSAR states that, "Adequate physical

separation shall be maintained between the redundant piping paths and containment

penetrations of the SIS (safety injection system) such that the SIS willmeet its functional

requirements even with the failure of a single active component during the injection

mode, or with a single active failure or a limited leakage passive failure during the

recirculation mode."

The bases for TS 3/4.5.2 and 3/4.5.3, "ECCS Subsystems," states, "The operability of

two separate and independent ECCS subsystems

with the indicated RCS pressure

greater than or equal to 1837 psia, or with the indicated RCS cold-leg temperature

greater than or equal to 485

F ensures that sufficient emergency core cooling capability

j

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-24-

willbe available in the event of a LOCA assuming the loss of one s'ubsystem through

any single failure consideration."

The inspectors reviewed ANS-51.7/N658-1976, "Single Failure Criteria for PWR Fluid

Systems," ANSI/ANS-58.9-1981, "Single Failure Criteria for Light Water-Reactor -",.'.

-

Safety-Related

Fluid Systems," and NRC SECY 77-439, "Single Failure Criterion." The

inspectors concluded that guidance existed for application of the single failure criterion

that required the proposition that single failures can occur at any time. Therefore, the

inspectors concluded that the licensee should have demonstrated that its assessment

of

consequences

had assumed the most limiting single failure.

Online Maintenance

The inspectors asked the licensee if they had performed online maintenance of the

HPSI system involving system configurations consisting of an inoperable HPSI pump,

the associated discharge isolation valve open, and the associated

RCS injection valves

operable (i.e., would open on a safety-injection actuation signal). The inspectors also

asked if the licensee had considered this configuration as a system vulnerability in its-

event investigation. The licensee reviewed its maintenance

rule database

and provided

the inspectors a list dating back to 1994, that identified several occasions when online

HPSI maintenance was performed that matched this system configuration., The

inspectors were concerned that during these online maintenance periods, a single

failure was not necessary for degraded HPSI performance during a postulated accident.

The inspectors concluded that during these periods of maintenance on the Unit 1 Train

"A"HPSI system and Unit 2 Train "B" HPSI system (the trains with the reverse leakage

check valves) the licensee was in a condition prohibited by the TSs and that TS 3.0.3

required a unit shutdown.

The licensee informed the inspectors that it had not evaluated

this system configuration as a vulnerability in its event investigation.

The inspectors reviewed the out-of-service data provided by the licensee and noted that

the maintenance activities generally consisted of minor preventive maintenance

including oil changes, and valve and breaker maintenance.

With respect to

maintenance on the Unit 1 Train "A" HPSI system (associated with Valve 1PSIA-V404)

and Unit 2 Train "B" HPSI system (associated with Valve 2PSIB-V405) the length of time

for each occurrence ranged from as short as 0.92 hours0.00106 days <br />0.0256 hours <br />1.521164e-4 weeks <br />3.5006e-5 months <br /> to as long as 19.58 hours6.712963e-4 days <br />0.0161 hours <br />9.589947e-5 weeks <br />2.2069e-5 months <br />.

The out-of-service data indicated that the Unit 1 Train "A" HPSI pump was unavailable

when the unit was operating in Mode

1 on September 4, 1996, for 19.58 hours6.712963e-4 days <br />0.0161 hours <br />9.589947e-5 weeks <br />2.2069e-5 months <br /> arid that

no documentation was available to demonstrate that Train "A"wa's isolated from

Train "B." Therefore, the inspectors determined that Unit 1 did not have any

independent ECCS subsystem operable when Train "A"of the HPSI system was out of

service without isolation from Train "B" of the HPSI system, and Valve 1PSIA-V404 was

inoperable.

Action was not initiated to place the unit in hot standby within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> as

required by TS 3.0.3. This was considered to be the second example of an apparent

violation of TS 3.0.3 (50-528/-529/-530/9814-01).

~ lp

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-25-

The out-of-service data also indicated that the Unit 2 Train "B" HPSI pump was

unavailable when the unit was operating in Mode 1 on October 21, 1994, for 19.8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

In this case, a clearance order for WO 6773826 identified that a clearance had been in

effect during this period of time that closed the Train "B" HPSI pump discharge isolation

valve. The exact length of time that the isolation valve was closed was indeterminate;=

The inspectors were able to conclude that the isolation valve was closed from between

2.5 to 6.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />. When the clearance order was cleared, the Train "B" HPSI pump

- discharge isolation valve was opened and the Train "B" HPSI pump was still unavailable

due to other maintenance.

The inspectors determined that Train "B"of the HPSI system

was unavailable during the maintenance activity and was not isolated from Train "A"for

a period of 13.5 to 17.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. Therefore, Unit 2 did not have any independent ECCS

subsystem operable for a period in excess of 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> when Train "B"of the HPSI

system was out of service without isolation from Train "A"of the HPSI system, and

Valve 2PSIB-V405 was inoperable.

Action was not initiated to place the unit in Hot

Standby within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> as required by TS 3.0.3. This was considered to be the third

example of an apparent violation of TS 3.0.3 (50-528/-529/-530/9814-01).

Allother examples of online maintenance of the Unit 1 Train "A"HPSI system and the

Unit 2 Train."B" HPSI system were less than 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> in duration. Therefore, while the

completion of a unit mode change was not required, the licensee failed to recognize the

applicability of TS 3.0.3.

C.

Conclusions

The misalignment of the Unit 1 and Unit 2 HPSI pump discharge check valves placed

the units in a significantly degraded and vulnerable condition with respect to the

capability to mitigate the consequences

of a LOCA. Two examples of an apparent

violation of TS 3.0.3 were identified.

E1.3

Assessment

of Generic Im lications

Ins ection Sco

e

The inspectors reviewed licensee investigation reports, surveillance procedures, and

maintenance procedures to determine whether the licensee had adequately addressed

the issues of check valve misalignment and inadequate testing practices with respect to

other safety-related valves.

Observations and Findin s

The inspectors questioned whether the licensee had evaluated the generic aspects of

the misaligned HPSI pump discharge check valves relative to other safety-related

valves.

The licensee had performed a study of other check valves. There were

27 Borg-Warner pressure-seal,

bonnet-hung check valves installed in each of the three

units. None of the valves in this population except for the two HPSI pump discharge

check valves per unit had the welded-neck design that appeared most susceptible to the

disc-cocking phenomenon.

Valves with a forged-neck design did not have vertical

c

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-26-

alignment variability similar to welded-neck models. The licensee performed a review of

the closed-direction exercise tests for the remaining 25 valves per unit and concluded

that the testing performed on each valve adequately demonstrated operability. The

licensee also examined a 3-inch valve in the maintenance shop and was unable to

reproduce tfIe disc-cocking phenomenon, even with the bonnet retaining ring,threaded;:

fullyinto the valve body. During the inspection, the licensee also initiated a generic

review of check valve testing practices to evaluate the adequacy of testing.

The inspectors selected a sample of valves to verify that the surveillance tests were

adequate to demonstrate valve closure.

The valves chosen for this review were the

LPSI cold-leg injection valves (xSIE-V114, xSIE-V124, xSIE-V134, and xSIE-V144,

where 'x's the unit designator) and their associated

test, Procedure 73ST-9SI05, "Leak

Test of HPSI/LPSI Containment Isolation Check Valves," Revision 4. The test

methodology involved pressurizing the downstream side of the valves with a HPSI pump

or a hydro test pump and measuring the leak rate on the upstream side. The inspectors

determined that the surveillance test was adequate to verify check valve closure.

Conclusions

The licensee adequately addressed

the generic implications of the misalignment issue

to other pressure-seal,

bonnet-hung check valves to conclude that no additional

operability concer'ns existed.

In-house and Indust

OEAs

Ins ection Sco

e

The inspectors reviewed licensee in-house and industry OEAs pertinent to the HPSI

pump discharge check valves.

Observations and Findin s

NRC IN 88-70 "Check Valve Inservice Testin

Pro ram Deficiencies"

In its January 12, 1989, evaluation of NRC IN 88-70, the licensee identified that reverse

flow testing of several check valves, including HPSI pump discharge check Valves

1PSIA-V404 and 2PSIB-V405, was not performed.

However, the licensee concluded

that because they had an NRC-approved IST program, any changes the program were

considered enhancements.

The licensee did not give this item a high priority and a due

date to add these tests to the program was established for 1996. The licensee's quality

assurance

organization conducted an audit of the check valve programs in 1992,

concluded that this schedule for action was untimely, and identified this as a finding. As

corrective action, the licensee initiated action to revise the IST program to include

reverse flow testing of the subject valves.

Surveillance Procedure 73ST-xXI29, "Section

XI Check Valve Operability Verification - Mode 6 - Full Stroke Testing of Safety Injection

s t

-27-

Check Valves," was approved on July 26, 1992, to conduct the test. The test

methodology consisted of measuring forward HPSI flowto the RCS via the hot-leg

injection flow path. The HPSI pump discharge check valves were considered operable if

an acceptable forward flowwas measured to the RCS with one HPSI pump operating

while cross connected to the opposite train, but no e'xplicit acceptance

criterion was

.

included to determine check valve reverse flow.

10 CFR Part 50, Appendix B, Criterion XVI,"Corrective Action," required that measures

shall be established to assure that conditions adverse to quality are promptly identified

and corrected and in the case of significant conditions adverse to quality that the

measures shall assure that the cause of the condition is determined and corrective

action taken to preclude repetition. The test procedures developed in 1992, as a result

of the January 12, 1989, evaluation were not adequate to identify excessive reverse

flow, a significant condition adverse to quality (excessive reverse flowthrough HPSI

pump discharge check valves). This was considered to be the fourth example of an

apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI

{50-528/-529/-530/9814-03).

NRC IN 89-62 "Malfunction of Bor -Warner Pressure Seal Bonnet Check Valves

Caused B Vertical Misali nment of Disc"

The licensee performed a review of IN 89-62 and concluded that no action was required.

Engineering Action Request (EAR) 89-1931, completed January 26, 1990, concluded

that the vendor manuals were adequate and had the necessary steps to 'ensure original

factory-established seat/disc alignment. The licensee's initial screening, documented in

'an October 9, 1989, memorandum correctly identified that vertical disc/seat

misalignment due to incorrect retainer rin'g position resulted in the problem identified in

the IN and that the vendor manual did not include procedure steps for adjusting retainer

ring position to achieve the correct alignment.

The licensee identified that a review

would be performed of check valve maintenance procedures to determine whether a

similar problem existed.

The licensee documented'its evaluation conclusions in the

EAR and in a memorandum dated February 15, 1990. The licensee identified that their

procedures included instructions for match-marking the valve body and bonnet to

ensure alignment of the disc and seat.

Therefore, the licensee concluded that

procedures contained adequate instructions. This conclusion addressed

horizontal

alignment concerns but did not consider the vertical misalignment issue and the need to

ensure correct retainer ring position.

In 1992, the licensee re-evaluated applicability of IN 89-62 and documented

in

CRDR 9-2-0412 that its original conclusions were incorrect. The vendor had revised its

technical manual in October 1990, which included instructions for measurement

of the

vertical "A"dimension (top of retainer ring to top of valve body) before and after

maintenance.

Borg-Warner issued a clarification to its Technical Alert 8909-77-001

(which addressed

the vertical seat alignment issue) in a letter to the licensee dated July

8, 1992.

The letter stated that the vertical alignment problem was limited to

~

~

~

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-28-

welded-neck check valves (such as Valve 1PSIA-V404) and that the welding of the neck

to the body had caused the neck to shrink down, thus causing the bonnet disc assembly

to sit lower in the valve body and possibly not seat properly on the valve seat.

The

licensee issued Procedure 31MT-9ZZ17 on November 30, 1992, which included the

Borg-Warnel technical alert instructions regarding permanent match marks for,

horizontal orientation and measurement

of the "A"dimension.

The licensee's February

15, 1990, evaluation failed to correct an inadequate maintenance procedure for

establishing the correct vertical alignment of the valve disc within the valve body of

Borg-Warner check valves. The resultant excessive'reverse

flowthrough HPSI pump

discharge check valves was considered to be a significant condition adverse to quality.

This was considered to be the fifth example of an apparent violation of 10 CFR Part 50,

Appendix B, Criterion XVI (50-528/-529/-530/9814-03).

C.

Conclusion

The inspectors considered the licensee's OEAs and corrective actions regarding

Borg-Warner check valves to have been inadequate

in preventing or detecting, in a

timely manner, significant conditions adverse to quality relative to the HPSI system.

Two examples of an apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI,

were identified.

e

'I

ES

Miscellaneous Engineering Issues

E8.1

Review of Licensee's Followu

and Si nificant Investi ation Re ort

Ins ection Sco

e

The inspectors reviewed the licensee's activities to assess,

evaluate, and correct the

degraded HPSI system and any potential impact on other safety-related systems.

Included in the review was Significant Investigation Report CRDR 1-8-0238, "Excessive

Leakage Through HPSI Pump Discharge Check Valve 1PSIA-V404," Revision 0,

June 10, 1998. The licensee completed Revision

1 of the report on July 10, 1998, but

the inspectors did not perform a detailed review of the report because it was completed

following the onsite portion of the inspection.

b.

Observations and Findin s

CRDR 1-8-0238 was initiated to evaluate the April9, 1998, failure of Valve 1PSIA-V404

to satisfy its reverse-flow acceptance

criteria. On April 10, 1998, the CRDR review

committee classified the subject CRDR as significant. An investigation team was

assembled

to evaluate the event. The inspectors reviewed the licensee's significant

investigation report dated June 10, 1998. The licensee performed a thorough historical

review of past testing and maintenance

practices.

The report identified the root cause

of the failure of the check valve to be attributed to a common-cause

error in assembling

the valves stemming from inadequate maintenance instructions.

Periodic surveillance

testing was ineffective in identifying excessive reverse flow. The root cause of the

inadequate surveillance test was an ineffective testing configuration developed by

'I

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~

0

-29-

engineering.

Missed opportunities to identify and correct problems with the check

valves also existed in the form of in-house and industry operating experience reviews.

Revision 0 of the report identified the need for 20 corrective actions associated with this

.

event. As of,June 12, 1998, three of the corrective actions had been completed.

A

schedule for the remaining corrective actions had been developed with planned

completion dates ranging from June 21, 1998, through the Unit 3 1998, and Unit 2 1999,

refueling outages.

The inspectors noted that the investigation did not identify any problems regarding

operator performance with respect to the October 1997, Unit 2 outages or the May

1998, entries into TS 3.0.3. Also, the report did not evaluate the safety consequences

of performing routine online maintenance of the Unit 1 and Unit 2 HPSI systems when

the HPSI trains were not isolated from each other.

The licensee informed the inspectors that additional assessment

of the safety

significance of the degraded HPSI condition would be performed and the results of the

assessment

would be documented in the LER supplement.

C.

Conclusions

The licensee's investigation report was objective and provided a candid self-assessment

of its performance; however, it did not evaluate inspector-identified issues in the areas

of operations or online maintenance.

V Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors met with licensee representatives

on June 11, 1998, to conduct a

technical debrief prior to leaving the site.

Following additional in-office inspection, and

telephonic discussions of findings, the inspectors conducted an exit meeting with

licensee representatives

on July 21, 1998. These representatives

acknowledged the

findings presented,

but disagreed with the May 13, 1998, apparent violation of TS 3.0.3.

The licensee stated that operations recognized that Valve 1PSIA-V404 was in a

degraded condition but information existed to conclude that the valve was operable until

testing could determine otherwise.

With respect to Unit 2, the licensee stated that

operations also recognized that Valve 2PSIB-V405 was in a degraded condition but

information existed to conclude that the valve was operable until testing could determine

otherwise.

The inspectors asked the licensee representatives

whether any materials examined

during the inspection should be considered proprietary.

No proprietary information was

identified.

l

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ATlACHMENT1

SUPPLEMENTAL INFORMATION

PARTIALLIST OF PERSONS CONTACTED

Licensee

G. Andrews, Section Leader, STNOperations

B. Blackmore, Engineer

P. Borchert, Site Manager, Operations

J. Brown, Engineer

R. Buzzard, Senior Consultant, Regulatory Affairs

D. Garnes, Unit 1 Department Leader, Operations

D. Fan, Acting Department Leader, System Engineering

R. Fullmer, Director, Nuclear Assurance

R. Hazelwood, Senior Engineer, Nuclear Regulatory Affairs

W. Ide, Vice President, Nuclear Engineering

A. Krainik, Department Leader, Regulatory Affairs

J. Levine, Senior Vice President, Nuclear

D. Marks, Section Leader, Nuclear Regulatory Affairs

D. Mauldin, Director, Maintenance

D. Oakes, Section Leader, Specialty Engineering

K. Parrish, Section Leader, Transient Analysis

G. Shanker, Department Leader, Specialty Engineering

D. Smith, Director, Operations

N. Spooner, Engineer

P. Wiley, Unit 2 Department Leader, Operations

NRC

M. Fields, Project Manager, Office of Nuclear. Reactor Regulation

J. Shackelford, Senior Reactor Analyst, Region IV

INSPECTION PROCEDURES USED

93702 Prompt Onsite. Response

to Events at Operating Power Reactors

'r

11

-2-

ITEMS OPENED CLOSED and DISCUSSED

~Oened

50-528/-529/-530/$ 814-01

APV

Three examples of an apparent violation of TS3.0.3

involving: 1) failure to initiate actions within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to place

Unit 1 in a mode in which TS 3.5.2 did not apply on May

13, 1998 (Section 01.1); failure to initiate actions to place

the unit in hot standby within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> when Unit1 did not

have an independent ECCS subsystem operable on

September 4, 1996 (Section E1.2); and 3) failure to initiate

actions to place the unit in hot standby within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />

when Unit 2 did not have an independent ECCS

subsystem operable on October 21, 1994 (Section E1.2).

50-528/-529/-530/9814-02

APV

Two examples of an apparent violation of TS 6.8.1

involving: 1) failure to record in the Unit 2 log an

unexpected decrease

in SIT level on October 10, 1997

(Section E1.1.b.1); and 2) failure to record in the Unit 2 log

an unexpected decrease

in SIT level on October 28, 1997

(Section E1.1.b.1).

50-528/-529/-530/9814-03

APV

Five examples of an apparent violation of 10 CFR Part 50,

Appendix B, Criterion XVI involving: 1) failure to identify

and promptly correct excessive HPSI pump discharge

check valve excessive reverse flowleakage following an

unexpected decrease

in SIT level on October 10, 1997

(Section E1.1.b.1); 2) failure to identify and promptly

correct excessive HPSI pump discharge check valve

excessive reverse flow leakage following an unexpected

decrease

in SIT level on October 28, 1997 (Section

E1.1.b.1); 3) failure to correctly assemble the Unit 1 Train

"A"HPSI pump discharge check valve to correct a reverse

flow leakage condition on April 10, 1998 (Section

E1.1.b.2); 4) failure to develop adequate test procedures

to identify and correct HPSI pump discharge check valve

excessive reverse flowfollowing evaluation of IN 88-70

(Section E1.4); and 5) failure to correct inadequate

maintenance procedures for establishing the correct

assembly of Borg-Warner check valves following

evaluation of IN 89-62 (Section E1.4) ~

0

50-528/-529/-530/9814-04

URI

Check valve design control issues (Sections E1.1.b.2,

E1.1.b.3, and E1.1.b.5).

II

I

1

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-3-

50-528/-529/-530/9814-05

APV

Two examples of an apparent violation of TS 3.5.2

involving: 1) failure to have an independent operable flow

path for the Unit 1 Train "B" HPSI system from May 1,

1992 through May 15, 1998 (Section E1.1.b.2); and 2)

failure to have an independent operable flow path for the

Unit 2 Train "A"HPSI system from April 14, 1993 through

May 16, 1998 (Section E1.1.b.4).

Closed

None

LIST OF ACRONYMS USED

APV

'SME

CFR

CS

CRDR

EAR

ECCS

EDG

EDT

EOP

gpm

HPSI

IN

IST

LCO

LER

LOCA

LPSI

NRC

OEA

OD

psia

psld

pslg

RCS

RWT

SDCHX

SIS

SIT

TS

UFSAR

URI

apparent violation

American Society of Mechanical Engineers

Code of Federal Regulations

containment spray

Condition Report/Disposition Request

Engineering Action Request

emergency core cooling system

emergency diesel generator

equipment drain tank

emergency operating procedure

gallons per minute

high-pressure safety injection

Information Notice

lnservice Testing

Limiting Condition for Operation

licensee event report

loss-of-coolant accident

low-pressure safety injection

U.S. Nuclear Regulatory Commission

operating experience assessment

operability determination

pounds force per square inch absolute

pounds force per square inch differential

pounds force per square inch gage

reactor coolant system

refueling water tank

shutdown cooling heat exchanger

safety injection system

safety injection tank

Technical Specification

Updated Final Safety Analysis Report

Unresolved Item

l

0

-4-

LIST OF DOCUMENTS REVIEWED

Procedures

NUMBER

73DP-9XI01

73DP-9XI02

DESCRIPTION

Pump and Valve Inservice

Testing Program-

Component Tables

Pump and Valve Inservice

Testing Program-

Administrative Requirements

REVISION

Revision 5

Revision 5

73ST-9XI33

73ST-9XI33

73ST-9XI33

HPSI Pump and Check Valve

Revision 9

Full Flow Test

HPSI Pump and Check Valve

Revision 10

Full Flow Test

HPSI Pump and Check Valve

Revision 11

Full,Flow Test

e

73ST-9XI35

31MT-9ZZ17

31MT-9ZZ17

31 MT-9ZZ17

73 ST-9ZZ25

73ST-9SI01

40OP-9SI02

HPSI Pump Discharge

Check Valve Closed

Exercise Test

Disassembly and Assembly

of Borg-Warner Check

Valves

Disassembly and Assembly

of Borg-Warner Check

Valves

Disassembly and Assembly

of Borg-Warner Check

Valves

Check Valve Disassembly,

Inspection, and Manual

Exercise

ECCS Flow Balance Test

Recovery, from Shutdown

Cooling to Normal Operating

Lineup

Revision 6

Revision

1

Revision 4

Revision 5

Revision 2

Revision 7

Revision 14

ll

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t

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f

-5-

73ST-9SI05

73ST-9SI05

40EP-9EO03

40EP-9EO09

Leak Test of HPSI/LPSI

Containment Isolation Check

Valves

Leak Test of HPSI/LPSI

Containment Isolation Check

Valves

Loss of Coolant Accident

Functional Recovery

Revision 4

Revision 3

Revision 5

Revision 6

Calculations

NUMBER

13-MA-Sl-982

DESCRIPTION

REVISION

Evaluation of Allowable Leak

Revision 0

Rate Criteria for

1,2,3PSIA-V404 and

1,2,3PSIB-V405/Assessment

of As-Found Leakage for

2PSIB-V405/1 PSIA-V404

13-MC-SI-215

Revised Single HPSI Pump

Delivery Curve. for Cold Leg

Injection and Flow Rate

Requirements for Technical Specification 4.5.2.h

Revision

1

Drawincrs

NUMBER

01-M-SIP-001

01-M-SIP-002

79120

DESCRIPTION

Safety Injection and

Shutdown Cooling System

Safety Injection and

Shutdown Cooling System

Valve Assembly- 4 inch,

1500 LB, swing check valve

REVISION

Revision 22

Revision 21

Revision C

-6-

Condition Re ort/Dis osition Re uests

NUMBER

1-5-0131

'

DESCRIPTION

REVISION

Valve 1PSIEV113 failed seat

May 22, 1995

leakage test

9-2-0412

9-8-0893

2-7-0420

1-'8-0238

2-8-0128

Incorrect conclusion in

review of IN 89-62

Design configuration

documents not updated "

SIT level dropped during

cold-leg boration

Valve 1PSIA-V404 failed

reverse-flow leakage test

Evaluate excessive check

valve back leakage

July 6, 1992

June 5, 1998

October 28, 1997

April 10, 1998

April 16, 1998

0 erabilit

Determinations

NUMBER

203

204

DESCRIPTION

Evaluation of piping

operability after

pressurization

Evaluation of HPSI

operability

REVISION

April 12, 1998

May 22, 1998

Work Orders

Deficiency Work Order 836600 and Work Orders 840712 and 840826 associated

with the

assembly and disassembly of 1PSIA-V404.

Other Documents

NUMBER

DESCRIPTION

REVISION

.7

-7-

Significant Investigation

Report CRDR 1-8-0238

I

Significant Investigation

Report CRDR 1-8-0238.

Reportability Determination

316-42-WEW/EDF

109-374-RAK/6LI/TNW

167-460-ECS/RRR

Excessive Leakage Through

HPSI Pump Discharge

Check Valve 1PSIA-V404,

Revision 0

Excessive Leakage Through

HPSI Pump Discharge

Check Valve 1PSIA-V404,

Revision

1

HPSI Discharge Check

Valves

Memorandum Regarding IN 88-70 Evaluation

Memorandum Regarding IN 88-70 Evaluation

Memorandum Regarding IN 89-62 Evaluation

June 10, 1998

July 10, 1998

May 21, 1998

August 31, 1990

January 12, 1989

October 9, 1989

161-2874-ACR/RAB/DAF

Memorandum Regarding IN

.

February 15, 1990

89-62 Evaluation

162-8368-KCP/PMC

281-2103-MAR/JAB

Simulator Training Scenario

Clearance Order for

WO 6773826

Individual Plant Examination

Memorandum Regarding

HPSI Safety Assessment

Memorandum Regarding

Check Valve Leakage

Criteria

LOCAwith Degraded HPSI

Flow

- May 20, 1998

May 14, 1998

July 14, 1998

October 21, 1994

April 7, 1992

I

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ATTACHMENT2

SIMPLIFIEDHPSI FLOW DIAGRAM

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Higlt/LowPrcssure Safety Injection System

pc1. 0

4/7/92

5.2.1 Front-l.Inc Systems

5-166

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ATTACHMENT3

DEGRADED HPSI FLOW PROFILE

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1800

1600

1400

1200

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PERFORMANCE WITH LEAKAGE

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