ML17312B021

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Insp Repts 50-528/96-13,50-529/96-13 & 50-530/96-13 on 960825-1005.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support
ML17312B021
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 10/25/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17312B019 List:
References
50-528-96-13, 50-529-96-13, 50-530-96-13, NUDOCS 9611010230
Download: ML17312B021 (46)


See also: IR 05000528/1996013

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-528

50-529

50-530

NPF-41

NPF-51

NPF-74

50-528/96-1 3

50-529/96-1 3

50-530/96-1 3

Arizona Public Service Company

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

5951 S. Wintersburg Road

Tonopah, Arizona

August 25 through October 5, 1996

'. Johnston,

Senior Resident Inspector

J. Kramer, Resident Inspector

D. Garcia, Resident Inspector

D. Carter, Resident Inspector

V. Gaddy, Resident Inspector, Fort Calhoun

Dennis F. Kirsch, Chief, Reactor Projects Branch F

ATTACHMENTS:

Attachment 1:

Partial List of Persons Contacted

List of Inspection Procedures

Used

List of Items Opened,

Closed, and Discussed

List of Acronyms

96iiOi0230 96i025

PDR

ADCICK 05000528

8

PDR

>J

h

-2-

EXECUTfVE SUMMARY

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

NRC inspection Report 50-528/96-13; 50-529/96-13; 50-530/96-13

~Oerarinne

Although operator performance, shift supervision command and control, and overall

communications

were not effective in preventing an SG overfill event, the licensee's

initial corrective actions were prompt, cautious, and thorough,

and the subsequent

investigation was self-critical and demonstrated

the licensee's commitment to

operations

excellence

(Section 01.1).

~

Operators displayed

a high degree of professionalism

and demonstrated

the

implementation of effective corrective actions when performing the high rate steam

generator blowdowns (Section 01.2).

~

An example of weak attention to detail was identified by the inspectors regarding

the degraded

Class

1E Motor Control Center panel doors (Section 02.2).

~

The licensee did not implement fully effective corrective actions following a May,

1996, event involving the control of ventilation boundary doors, when they

recognized weaknesses

in worker understanding

of door control procedures

and in

the labeling of doors.

Three similar events subsequently

occurred which could have

been prevented

had corrective actions been implemented.

Following the third

event, the licensee implemented more comprehensive

interim corrective actions and

planned longer term corrective actions to prevent recurrence

(Section 02.3).

Maintenance

~

The licensee responded

effectively to problems experienced

while lifting the Unit

1

upper guide structure (UGS) by stopping the evolution, involving plant management,

and developing

an appropriate

plan (Section M1.3).

~

Management's

expectations

and procedural requirements for performing procedure

steps out-of-sequence

were not clearly understood

by certain maintenance

personnel

performing a surveillance (Section M4.1).

~En ineerin

~

Civil and system engineering organizations demonstrated

poor communications

on

the status of unsealed ventilation boundary penetrations.

Additionally, although

civil engineering

had made progress

in the resolution of penetration design

deficiencies, they had not ensured that the interim condition had been adequately

reviewed for system impact (Section E2.1).

li

h

-3-

Engineering's

recently established testing of the auxiliary building essential

ventilation design basis requirement to develop

a measurable

negative pressure

in

emergency mode was seen as improvement to the testing program, although the

acceptance

criteria and the initial conditions for the test had not been welf

established

to assure that the test results were both accurate and could provide

meaningful trend information (Section E3.1).

Radiological protection (RP) personnel demonstrated

weak health physics practices

when entering infrequently accessed

areas that have not recently been surveyed

and in the fabrication of an inadequate

drip catch.

However, RP management

responded

appropriately to the inspectors'oncerns

(Section R1.1).

In an effort to improve on material condition and housekeeping

issues, the licensee

initiated a housekeeping

improvement and area ownership program.

However, the

inspectors continued to identify material condition and housekeeping

issues which

had not been previously identified by the licensee (Section R2.1).

1

I

i

Re ort Details

Summar

of Plant Status

Unit

1 began this inspection period at essentially 100 percent power.

On September

3, the

unit began an end-of-core life power coastdown.

On September 21, the unit began

Refueling Outage

1R6 and at the end of the inspection period was defueled.

Units 2 and 3 operated at essentially 100 percent power for the duration of the inspection

period.

I. 0 erations

01

Conduct of Operations

01.1

Feedwater

S ill While Fillin

Steam Generator

Unit

1

a.

Ins ection Sco

e 71707

On September

22, while in Mode 5, operators overfilled a Unit 1 steam generator

and spilled approximately 4000 gallons of uncontaminated

condensate

water

through an open atmospheric dump valve to the main steam support structure.

They had been in the process of implementing

a procedure to cool the steam

generator metal mass to facilitate outage work. The inspectors reviewed the

licensee's

response

to the event.

b.

Observations

and Findin s

The licensee investigated the cause of the spill and identified several weaknesses

in

engineering performance.

The temporary level instrument used to measure the

SG level was not connected

at a location which supported

the intended use.

The

level instrument was connected to the top of the SG, which was not vented, so the

instrument provided an incorrect level reading once the line to the vented

atmospheric dump valve was covered with water.

In addition, the licensee

considered that the temporary installation did not receive an adequate

independent

design review and could have been improved by an additional diverse level

monitoring method.

The licensee also identified several weaknesses

with operations performance.

Crew

supervision did not maintain command and control of the evolution.

The shift

supervisor and control room supervisor allowed mechanical engineering

to lead the

evolution and did not direct or concur with all manipulations.

Verbal

communications

were weak, in that the reactor operator failed to notify supervision

of difficulty in raising the SG level.

The licensee performed the following actions as a result of the spill:

~

Place the evolution on hold.

Contacted

appropriate levels of management

and the inspectors.

!

)

)

jl

-2-

Initiated investigations to review the impact of the spill on main steam piping

and supports

and, subsequently,

determined that no impact had occurred.

~

Initiated investigations to determine the cause of the event from both

instrumentation

and human performance perspectives.

Before restarting the evolution, the licensee improved the level instrumentation to

include a tygon tube tor an alternate level indication, revised the procedure to

provide additional guidance for the operators,

and conducted

a detailed prejob

briefing.

The revised procedure was implemented without further incident

approximately

1 day after the spill.

c.

Conclusions

Although operator performance, shift supervision command and control, and overall

communications were not effective in preventing the SG overfill event, the

licensee's

initial corrective actions were prompt, cautious, and thorough, and the

subsequent

investigation was self-critical and demonstrated

the licensee's

commitment to operations excellence.

01.2

0 cretin

the Steam Generator Blowdown S stem

Unit 3

a.

Ins ection Sco

e 71707

The inspectors observed the control room staff perform high rate steam generator

blowdowns to the main condenser

using Procedure 40OP-9SG03,

"Operating the

Steam Generator Blowdown System."

b.

Observations

and Findin s

On October 2, the inspectors observed the control room staff perform high rate

steam generator blowdowns.

In the past year, operators

have made errors while

performing this routine evolution that have resulted in unplanned

increases

in

reactor power.

The inspectors observed that in this instance the shift supervisor

(SS) ensured that there were no distractions to the operators and he strictly

controlled control room access.

The reactor operator followed the procedure when

performing the board manipulations

and the control room supervisor displayed

positive command and control of the activity. Operator communication included

verbatim repeatbacks,

and procedural performance

included independent

verification.

e

-3-

02

Operational Status of Facilities and Equipment

02.1

De raded Batter

Powered Emer enc

Li htin

Unit 3

a.

Ins ection Sco

e 71707

The inspectors performed

a routine tour of the Train A emergency diesel generator

and verified valve lineups, material condition, and housekeeping.

b.

Observation

and Findin

s

On August 29, the inspectors noted the electrolyte levels in some of the cells of

Emergency Light 3E-ZGL-DSO-05-100-04 were below the minimum level.

The

inspectors informed the Unit 3 SS, who contacted the system engineer.

The

system engineer verified the levels and requested

electrical maintenance

to adjust

the levels.

The inspectors reviewed the design requirements of the emergency

lights in the

Updated Final Safety Analysis Report (UFSAR).

Section 9.5.3.2.2.3 stated that the

emergency lights should be capable of providing a minimum of 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />

illumination. The lights in question were nonquality related and were designed to

provide emergency lighting to support personnel

egress upon the loss of power.

The inspectors discussed

whether the emergency lights would have met design

requirements with the system engineer.

The system engineer indicated that the

emergency lights were equipped with cells which had an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> illumination rating

and concluded that the lights would have met the design requirements

even with

the low electrolight level observed.

The licensee inspected other emergency lights in all three units and identified

another light that had low electrolyte levels.

The system engineer subsequently

determined that the preventive maintenance

task frequency for this type battery

would be increased from once every six months to once every quarter.

c.

Conclusions

Operations

and engineering

personnel

responded

appropriately to the inspectors

identified battery electrolyte level discrepancy.

02.2

Motor Control Center

MCC Doors Found 0 en

Unit

1

a.

Ins ection Sco

e 71707

The inspectors toured the Unit 1 electrical penetration rooms and held discussions

with operations personnel.

-4-

b.

Observations

and Findin s

On September

14, the inspectors identified two Panel Doors, PHA-M3325 and

PHA-M3514, on the Class

1E 480 volt MCCs that were open and other panel doors

that were improperly secured.

The MCCs were located on the 120 foot elevation

west electrical penetration room and the 100 foot elevation east electrical

penetration room.

The inspectors notified the control room and an auxiliary operator (AO) responded

to the area.

The AO identified that the door handle to PHA-M3514 was broken, the

door latch to PHA-M3325 was bowed preventing the door from closing.

The AO

initiated Work Request 915103 to have the doors repaired.

The inspectors discussed

the discrepancies

with the site shift manager

(SSM).

The

SSM indicated that a previous work request was generated

to correct discrepancies

with MCC PHM34.

The inspectors informed the SSM that the doors identified on

September

14, were from MCCs PHM35, PHM33, and PHM37.

The SSM

determined that a walkdown of all safety-related

MCCs for each unit would be

performed.

The inspectors questioned

the SSM about the safety impact of having the doors

open and the requirements for the doors to be shut.

The SSM discussed

the

discrepancies

with equipment qualification, fire protection, and system engineering

personnel,

and determined that the opened doors did not have

a safety impact, nor

were there any requirements for the doors to be shut.

The SSM indicated that

management's

expectations

were that licensee personnel

ensure that the doors

remain properly secured.

The inspectors

inquired whether

a Condition Report/Disposition

Request

(CRDR) had

been initiated for the identified door discrepancies.

The SSM indicated that a CRDR

had not been written and subsequently

generated

a CRDR for followup

documentation.

c.

Conclusions

The MCC panel door discrepancies

demonstrated

a weak attention to detail by both

operations

and maintenance

personnel.

02.3

Closed

Licensee Event Re ort

LER 50-528 96003

a.

Ins ection Sco

e

92901

Between May and August 1996, both the licensee and NRC identified instances

where barriers doors to essential ventilation system boundaries

were open.

These

instances

impacted the ability of ventilation systems to perform during a design

basis event.

One of the events was the subject of LER 50-528/96003.

The

J

-5-

inspectors reviewed these events, the licensee's safety and cause analyses,

and

their proposed corrective actions.

b.

Observations

and Findin

s

S stem Descri tion

The auxiliary building essential ventilation system (licensee system designation

EHA)

was designed to maintain the area containing the essential safety features pumps at

a measurable

negative pressure following a loss of coolant accident to prevent the

unfiltered release of possible airborne radioactivity to the surroundings.

The EHA

envelope includes the volume of the auxiliary building below the plant

100'levation

(essentially ground level).

The EHA boundary includes the auxiliary

feedwater (AFW) vaults, since they are connected

through ventilation ducting.

Additionally, the lower level shares boundaries with the fuel handling building and

the outside yard.

During a safety injection actuation signal (SIAS), the EHA is isolated from the

normal auxiliary building ventilation supply and exhaust.

The lower levels are then

aligned to the fuel handling building essential ventilation exhaust filter train.

The

design basis for EHA is discussed

in UFSAR Section 9.4.2.2.

Technical Specification (TS) 3.7.8 requires that two independent

trains of EHA be

operable.

Although the TS did not require testing for a negative pressure,

a

measurement

of system flow was required.

The licensee had established

a test for

negative pressure

in this lineup in 1995 and had completed testing in all units in

August 1996.

On October 4, 1996, the licensee submitted improved TS, which

included testing for a measurable

negative pressure.

Control of Barriers

As discussed

in Inspection Report 50-528, 529, 530/96-07, on May 7, 1996, the

inspector, observing

a leak rate test of a containment purge isolation valve in

Unit 3, noted that technicians had propped open two doors to run a service air

hose.

The inspector determined that the technicians involved in the leak rate test

had not contacted either the control room or the fire department

as required by

instructions printed on the doors and described

in Procedure 40AC-9OP17, "Control

of Security, Fire, and Heating, Ventilation, and Air Conditioning Barrier Doors."

The

inspector identified this as a noncited violation with minor significance.

The licensee determined,

during their evaluation, that the labeling on the doors had

contributed to the technician's confusion.

Dooi number labels were at the top of

doors and room number labels were at the center of the doors.

Both door and room

numbers were typically a letter and three digits with the letter and first digit

referencing the building and elevation of the door.

As a result, the first portion of

most room and door numbers were identical.

Procedure 40AC-9OP17 used the

4

I

-6-

door number as its reference.

Procedure 40AC-9OP17 was subsequently

revised

and renumbered

as Procedure 40DP-9ZZ17 on June 4.

Subsequent

to this event, the licensee identified the following similar events:

~

On June 6, the Unit 3 SS discovered

a door between the auxiliary building

and the fuel handling building had been propped open by carpenters

erecting

scaffolding.

The carpenters

had called the fire department

as a sign on the

door required, but had not called the control room as required by Procedure

40DP-9ZZ17.

As corrective action, the carpenters

were provided with

training on the door procedure

and the signs on the doors were modified.

The licensee concluded that the fuel handling building essential ventilation

system had been inoperable for the 45 minutes the door was opened.

However, since there were no operations underway involving the spent fuel

pool, the licensee met TS limiting conditions for operations

~

On June 26, a painter in the access stairwell to the Unit

1 AFW vaults noted

that both water tight doors to the area were open.

The doors had been

opened by a valve service technician who was working on a valve in the

Train B AFW pump room.

The licensee determined that the technician had

not followed Procedure 40DP-9ZZ17.

However, they determined that the

open doors would not have prevented

establishing

a negative pressure

in the

EHA following a SIAS.

As corrective action, the licensee put labels on the AFW vault doors stating

the requirement to keep the doors closed.

~

On August 2, contract maintenance

technicians propped open an EHA

boundary door after they had used the room number, instead of the door

number, when asking the control room for authorization.

The door was open

for approximately 75 minutes when discovered

and questioned

by an AO.

Subsequently,

engineers

calculated that it would not have been possible to

maintain the EHA at a measurable

negative pressure.

The licensee

concluded that both trains of EHA were inoperable for the 75 minutes the

door was open.

On September 4, the licensee submitted

LER 50-528/96003, reporting this as a condition which could have prevented

the fulfillment of a safety function.

These three events resulted from a combination of workers not familiar with the

door control procedure

and workers confusing the room number labels for the door

number.

The events on June 6, June 26, and August 2 were three examples of

failure to follow procedures

{Violation 528; 530/9613-01).

Although each of the events was identified by the licensee, the inspectors

determined that they could have been prevented

had the licensee implemented

interim corrective actions in a timely manner.

Instead, the immediate corrective

-7-

actions for the May 7 event and the subsequent

events in June were limited to the

crews and doors involved and long term corrective actions, although more

comprehensive,

had not been implemented.

While the causes of the August 2

event were very similar to the causes of the previous three events, the event was

significant in that it resulted in both trains of a safety system being inoperable.

The

licensee did implement more comprehensive

interim corrective actions after the

August 2 event by taking actions to increase worker awareness

of the door control

procedure requirements

and by improving door labeling.

The inspectors noted that

the interim actions, while more comprehensive,

were simple in approach

and

execution and considered that there was sufficient basis to have expected these

actions to have been taken prior to the August 2 event.

C.

Conclusion

The licensee did not implement fully effective corrective actions following a May,

1996, event involving the control of ventilation boundary doors, when they

recognized weaknesses

in worker understanding

of door control procedures

and in

the labeling of doors.

Three similar events subsequently

occurred which could have

been prevented

had corrective actions been implemented.

Following the third

event, the licensee implemented more comprehensive

interim corrective actions and

planned longer term corrective actions to prevent recurrence.

II. Maintenance

M1

Conduct of Maintenance

M1.1

General Comments on Maintenance Activities

a.

Ins ection Sco

e 62707

The inspectors observed

all or portions of the following work activities:

32MT-9ZZ56 Motor Operated Valve Testing on Low Pressure

Safety

Injection Heat Exchanger

Bypass Valve SIA-HV-306 (Unit 1)

33MT-9ZZ02 Freeze Seal Installation for Low Pressure

Safety Injection

Minimum Flow Recirculation Valve SIA-UV-669 Work (Unit 1)

b.

Observations

and Findin

s

The inspectors found these work activities were performed acceptably

and in

accordance

with procedures.

-8-

M1.2

General Comments on Surveillance Activities

a.

Ins ection Sco

e 61726

The inspectors observed

all or portions of the following surveillance activities:

~

73ST-9XI16

Economizer Feedwater Isolation Valves - Inservice Test (Unit 3)

~

73ST-9ZZ18 Main Steam Safety Valve Online Set Pressure

Verification

(Unit 1)

b.

Observations

and Findin s

The inspectors found these surveillances were performed acceptably

and as

specified by applicable procedures.

In addition, see the specific discussion of

surveillance observed

in Section M4.1.

M1.3

Removal of the UGS Unit

1

a.

Ins ection Sco

e

627~07

On September

26, 1996, while in the process of lifting the Unit

1 UGS prior to

defueling operation, one of two guide bushings

became stuck on its guide pin and

the arm holding the guide bushing was damaged.

The inspectors attended

a

management

review and prejob brief and observed the subsequent

liftoperation.

b.

Observations

and Findin s

About midnight on September

26, as maintenance

personnel were in the process of

conducting the UGS lift operation, they heard

a loud noise.

Upon further inspection,

they determined that one of the guide bushings

had become stuck and, as the UGS

was lifted, the arm that holds the bushing was deformed.

Maintenance

personnel

lowered the UGS back into place and informed outage management.

The licensee convened

a management

review team at 6 a.m. to review the

condition of the UGS and discuss plans for its subsequent

removal.

The inspectors

noted that the management

review was thorough, covering several possible

scenarios.

Ultimately, they concluded that a second lift attempt be made, provided

that maintenance

personnel

add precautions to their work instructions and cameras

to monitor the UGS removal.

The inspectors observed the prejob briefing and found that the appropriate

personnel were in attendance

and the work scope was adequately

covered.

The

inspectors subsequently

observed the liftoperation from the refueling bridge.

The

licensee proceeded

with caution and the lift attempt was successful.

-9-

At the end of the inspection period, the licensee had not yet determined what had

caused the guide bushing to become stuck on the guide pin.

The licensee has

experienced difficulty in the past with the guide bushings and, in an earlier Unit 2

outage, the guide bushing had detached

from the UGS.

The licensee did identify

that within 3 feet of the final position, there was little clearance between the guide

bushing and the guide pin which appeared

to contribute to interference.

The

licensee initiated a CRDR to evaluate this recurring problem and to develop repairs

to the Unit

1 UGS.

c.

Conclusions

The licensee responded

effectively to problems experienced

while lifting the Unit

1

UGS by stopping the evolution, involving plant management,

and developing

an

appropriate

plan.

The root cause of the problem is being evaluated

according to the

CRDR process.

Ni4

IVIaintenance Staff Knowledge and Performance

M4.1

Class

1E Station Batter

Channel A Dischar

e Test

Unit

1

a.

Ins ection Sco

e 61726

The inspectors observed the performance of Procedure 32ST-9PK03, "18 Month

Surveillance Test of Station Batteries," Revision 10.

b.

Observations

and Findin s

On September

23, the inspectors observed

electrical maintenance

technicians

perform a surveillance test on the Class

1E Station Battery Channel A. During this

observation,

the technicians,

in the process of performing Step 8.3.2.2, lifted the

leads on the spare battery bank, prior to performing preceding Step 8.3.2.1 to open

the output circuit breaker on the battery charger.

The inspectors questioned

the test director about performing the step out of

sequence.

The test director indicated that the procedure allowed performance of

steps out of sequence.

The inspectors reviewed the procedure

and did not find any

such allowances.

This discrepancy was discussed

with the test director, who noted

that the conduct of maintenance

procedure

allowed the performance of steps out of

sequence.

The test director subsequently

stopped work, prior to the technicians performing

Step 8.3.2.2, and contacted

an electrical maintenance

supervisor to resolve the

issue of performing the procedure out of sequence.

The electrical maintenance

supervisor directed the test director to perform the procedure

as written.

t

-10-

The inspectors subsequently

determined that Procedure 01DP-OAP01, "Procedure

Process," Section 7.8, "performance of activities out of sequence,"

provided

applicable requirements.

The procedure allows the performance of steps out of

sequence,

if plant safety is not compromised,

the performance does not cause an

intent change to the procedure,

the change

is properly documented,

the work leader

has authorized it, and the SS is notified.

The inspectors noted that while the test director did not clearly understand

the

requirements

for performing the procedure out of sequence,

he took appropriate

actions by stopping work, notifying supervision,

and obtaining clarification.

The inspectors discussed

the issue with the electrical maintenance

department

leader.

The department

leader indicated that it was management's

expectation to

perform the procedures

as written. However, he was unclear as to the specific

requirement for performing steps out of sequence

and where they were located.

The department

leader noted that, in this instance, performing the steps out of

sequence

would not have affected the intent of the surveillance test.

The department

leader concluded that the requirements for performing steps out of

sequence

were not well understood

by maintenance

department

personnel

and

planned to provide training on the procedural requirements.

C.

Conclusion

Management's

expectations

and procedural requirements for performing procedure

steps out of sequence

were not clearly understood

by certain maintenance

personnel performing the surveillance.

III. En ineerin

E2

Engineering Support of Facilities and Equipment

E2.1

0 en

Ins ection Followu

Item 50-528 96012-01

Ins ection Sco

e

This item involved the control of EHA boundary penetrations.

On July 7, the

inspectors found an unsealed

penetration through the 100'HA boundary.

The

penetration

had been opened to allow cable routing for an ongoing radio

communications

modification.

The licensee initiated an investigation and

determined that they had not established

appropriate controls of the EHA boundary

penetrations.

The inspectors reviewed the licensee's

response

to this issue and

performed EHA boundary walkdowns.

\\'

-11-

b.

Observations

and Findin s

The licensee initiated CRDR 9-6-0691 to address

this issue.

As immediate action,

on July 8, system and maintenance

engineers

performed walkdowns of the auxiliary

buildings in all three units and identified a number of penetration deficiencies.

Engineers performed analyses of the as-found condition in all units and determined

that the additional area would not have had a significant impact on the ability of the

EHA to maintain a negative pressure following a SIAS. An EHA system description

is provided in Section 02.3 of this report.

The inspectors performed

a subsequent

walkdown and found eight additional

unsealed

penetrations

in Units

1 and 2. These penetrations

were for piping running

from the south yard to the essential pipe tunnel area,

a tunnel within the boundary

of the EHA which is under the yard and runs between the refueling water tank and

the auxiliary building.

These penetrations

appeared

to be of more significance since

they were located relatively near the tunnel which connects the EHA to the fuel

handling building essential ventilation trains.

The inspectors determined that these unsealed

penetrations

had not been identified

during the July walkdowns and the maintenance

and system engineers

were not

aware of this condition.

However, civil engineering

had work requests,

initiated in

1995, to repair these and 22 other EHA boundary penetrations.

The inspectors

reviewed the history of these penetrations

with the licensee and was informed of

the following:

In 1991, the licensee established

a penetration

seal project to identify all

building penetrations,

establish the functions of each, and identify

deficiencies.

Eight thousand

discrepancies

were identitied in fire function barriers.

These

barriers were given first priority for repair and were all dispositioned

by late

1 994.

Approximately 2000 discrepancies

were identified in barriers with flood, high

energy line break (HELB), and ventilation functions.

The licensee had

established

that all these penetrations

be classified as "not quality related."

As a result, they did not place a high priority on the resolution of these

deficiencies.

An evaluation, documented

in Calculation 13-NS-A73, determined that there

was no safety significance to the unsealed

barriers with flood and HELB

functions.

The licensee was not able to identify where they had performed

similar reviews for the barriers with ventilation functions.

II;

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By 1995, civil engineering

had dispositioned

all but 170 of these

penetrations

as "use-as-is."

Work requests

were initiated for the remaining

170 penetrations.

~

At the time of the inspection, the licensee was in the process of evaluating

600 penetrations

which served as radiation accident mitigation.

They had

not repaired any of the 170 penetrations

with open work requests.

In response

to the inspectors'uestions,

the licensee determined that the additional

unsealed

penetrations

to the EHA boundary did not impact the operability of the

EHA. They based this determination on the successful tests which had been

performed in each unit during the past year (See Section E3.1).

The inspectors determined that, for both the penetrations

identified in July 1996,

and the penetrations

identified during the September

1996 walkdown, the

penetrations

were not in conformance with design drawings.

In each case, the

licensee had established

work requests to bring these penetrations

into

conformance with the design drawings.

However, in both cases

the licensee had

not performed an evaluation of the impact on the EHA until questioned

by the

inspectors.

Additionally, the deficiencies identified during the September

1996,

walkdown had been known to the licensee since 1992.

The licensee had established

that all the penetrations with flood, HELB, and

ventilation boundary functions were not quality-related.

This determination

appeared to be inconsistent with the licensing basis and the quality assurance

program documented

in UFSAR Section 17.2.

The licensee has established that

design basis flood and HELB mitigation are safety-related functions.

Additionally,

EHA has been identified as a safety-related

system with the primary function of

preventing unfiltered release paths.

At the end of the inspection, the licensee

stated that they would review the classification of these penetrations.

This item

remains open pending the conclusion of this review and the licensee's development

of a resolution for the penetrations.

c.

Conclusions

Civil and system engineering organizations

demonstrated

poor communications

on

the status of unsealed ventilation boundary penetrations.

Additionally, although

civil engineering

had made progress

in the resolution of penetration design

deficiencies, they had not ensured that the interim condition had been adequately

reviewed for system impact.

E2.2

Feedwater

S ill While Fillin

a SG

Unit

1

92903

The inspector reviewed the licensee's investigation in response

to overfilling the SG.

The engineering activities preceding the SG cooldown were not effective in

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designing

an accurate

SG level monitoring system.

Further aspects of this event are

discussed

in Section 01.1.

E3

Engineering Procedures

and Documentation

E3.1

EHA Surveillance Testin

a.

lns ection Sco

e 37551

The inspectors reviewed Surveillance Procedure

33ST-9HF01 for the testing of each

train of EHA in the SIAS mode and discussed

the results of the test with the

maintenance

and system engineer.

b.

Observations

and Findin

s

Procedure

33ST-9HF01

had been revised in 1995 to add testing to verify that a

measurable

negative pressure

between the EHA and outside atmosphere

was

established

consistent with UFSAR requirements.

Prior to this revision, the licensee

had not performed

a similar test since system startup testing.

Testing had been

completed in all units and had determined that each train could maintain a

measurable

negative pressure.

A brief description of the system's design basis is

provided in Section 02.3.

The inspectors reviewed the test results and noted considerable

variations in the

differential pressures

achieved from train to train and from test to test.

For

example:

~

The differential pressure

achieved on August 14, 1996, for Unit 1 Train A

was -0.045" water gage {w.g.). The following week, the differential

pressure

for Train B was -0.134" w.g.

~

For Unit 2 Train A, testing in June 1995, established

a differential pressure

of -0.410 w.g. Testing of the same train in August 1996, established

a

differential pressure

of -0.070" w.g.

Maintenance

and system engineers

could not explain why there was such

a

variation in the test results.

The inspectors reviewed the test procedure

and found

that it did not establish sufficient prerequisites to control of the EHA envelope

during the test, thus establishing uniform conditions to assure test repeatability, by

ensuring that doors remained closed.

Additionally, the test did not establish control

of the ventilation configuration in other buildings.

The inspectors noted that either

of these factors could contribute to the variation of test results.

Licensee

engineering

stated that they planned to address

these issues

in future procedure

revisions.

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Additionally, the surveillance established

the test acceptance

criteria to be

measurab(e

negative pressure,

but did not provide a numerical limit. The inspectors

subsequently

found that a numerical acceptance

criteria for a measurable

negative

pressure of -0.01 inch w.g. had been established

in a 1987 UFSAR change

evaluation.

However, this minimum criteria had not been translated into either the

surveillance test or other design basis documents.

The inspectors did note that all

of the current tests met the acceptance

criteria.

The inspectors noted that the test acceptance

criteria was based on the capabilities

of the instrumentation

and did not address

other physical characteristics

such as:

~

air expansion

caused by post loss-of-coolant accident room heating,

potential wind effects on the outside building reference leg of the differential

pressure instrumentation,

and

~

whether the measurement

location was at a point in the building, which

would be expected to be the least negative.

Engineering stated that they would assess

these attributes and determine whether

they had established

the appropriate criteria.

The inspectors noted that while a test

for negative pressure

was not required by the current TS, it was a requirement

in

the proposed

improved TS, submitted by the licensee for NRC review on October 4,

1 996.

c.

Conclusions

Engineering's

recently established

testing of the EHA design basis requirement to

develop

a measurable

negative pressure was seen as improvement to the testing

program, although the acceptance

criteria and the initial conditions for the test had

not been well established

to assure that the test results were both accurate and

could provide meaningful trend information.

ES

Miscellaneous Engineering Issues

E8.1

Closed

LER 50-529 96005:

inadequate

procedure controls allow equipment

qualification boundary to be breached.

On June 12, a hatch through the

100'levation

of the Unit 2 main steam support structure, which leads to the Train B

AFW pump room, was open for approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

The licensee subsequently

determined that the hatch served

as a barrier to protect the AFW pump room vaults

from the environmental

and flooding impacts of a postulated

HELB. Additionally,

they determined that the hatch served

as an EHA boundary since the AFW vaults

communicate with the auxiliary building through ventilation ducts.

However, these

functions of the hatch were not captured

in the licensee's door control

Procedure 40DP-9ZZ17.

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The licensee determined that the personnel involved in opening the hatch had

properly reviewed and followed the door control procedure.

Additionally, the

appropriate operations

and ventilation maintenance

engineering personnel had been

involved in the initial assessment

for opening the door.

The licensee found that an

error had been made in a recent revision of the door control procedure.

The failure

to have a procedure

adequate

for the circumstances

is a violation.

The inspectors

reviewed CRDR 2-6-0123, and found the licensee's investigation, safety analysis,

and corrective actions to be appropriate.

This issue is being treated as a noncited

violation consistent with Section Vll of the NRC Enforcement Polic

(50-529/961 3-02).

IV. Plant Su

ort

R1

Radiological Protection and Chemistry Controls

R1.1

RP Controls

a.

Ins ection Sco

e 71750

During the inspection period, the inspectors performed several tours in the

radiological controlled areas including high radiation and locked high radiation areas.

Specifically, the equipment drain tank (EDT) rooms, 88 foot elevation pipe chases,

and mechanical piping penetration rooms were examined.

b.

Observations

and Findin s

On August 29, the inspectors identified that Valve SIBV-832 (High Pressure Safety

Injection Header Drain and Test Valve), located in the Unit 2 east mechanical piping

penetration

room, had a yellow shoe cover wrapped around

a leaking pipe cap in

place of a drip catch.

Tape labeled as "Internal Contamination" was used as the

posting information.

In addition, the inspectors observed that a piece of the tape

used to label the covering had fallen off and was stuck to the floor. The inspectors

showed

an RP department

leader the drip catch, and the leader concluded that the

drip catch was unacceptable

and did not meet his expectations.

RP subsequently

replaced the containment with a proper drip catch.

The inspectors determined

these actions were acceptable.

On September

18, the inspectors

and a RP technician toured the Unit 1 EDT room.

Although the EDT room was a locked high radiation area, it was not posted

as a

contaminated

area.

Additionally, the room had last been surveyed approximately 'l4

months prior to the inspectors'ntry

and licensee entries into this room were

infrequent.

The inspectors observed

a valve in the mezzanine

area above the EDT

was labeled "Contaminated Area - bottom of valve and inside packing gland" and

had no containment or enclosure device.

In addition, the inspectors observed

a

vertical pipe with boron leaking from a flange coupling.

After leaving the EDT room,

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the inspectors performed

a personal frisk and identified contamination of

approximately 2000 DPM/100 cm~ on a shoe.

The licensee decontaminated

the

shoe and prepared

a personnel contamination report.

Radiation protection surveyed the EDT room and identified contamination on the

pipe flange and pipe, the posted valve, on the tank below the valve, and on the

floor of the room.

The licensee subsequently

posted the EDT room as a

contaminated

area.

The RP operations manager indicated that it would have been

prudent to survey or to have required protective clothing prior to entering this

infrequently surveyed room.

The licensee issued

a RP night order establishing precautionary contamination

controls when entering any area that has not been accessed

within the fast 90

days.

The licensee also initiated a CRDR to evaluate the event and provide

corrective actions.

The inspectors determined these actions were appropriate.

c.

Conclusions

Radiological protection personnel demonstrated

weak health physics practices when

entering infrequently accessed

areas that have not recently been surveyed

and in

the fabrication of an inadequate

drip catch.

However, RP management

responded

appropriately to inspectors concerns.

R2

Status of RP and Chemistry Facilities and Equipment

R2.1

Material Condition and Housekee

in

a.

Ins ection Sco

e 71707

71750

The inspectors performed routine walkdowns and inspections of the facility and

assessed

plant material condition and housekeeping.

b.

Observations

and Findin

s

On August 29, the inspectors identified an inadequate

containment

on

Valve CHB-HV530 (Refueling Water Tank to Safety Injection Train B Valve).

The

containment

had openings that could allow contamination to leak out.

The drip

hose connection leaked liquid onto the floor below the valve.

The floor drain,

containing the drip hose, had boron build-up above the drain cover, which had

smearable

contamination of 1500 DPM/100 cm'.

The licensee repaired the

containment

and decontaminated

and modified the drain cover.

The inspectors

determined these actions to be acceptable.

On September

17, the inspectors identified a 12 foot length of unattached

grounding cable in the Unit 2, 88-foot pipe chase.

The licensee issued

a work

request to attach the grounding cable.

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On September

18, the inspectors identified the following housekeeping

deficiencies

in the Unit 1, 88-foot pipe chase:

an unusual radiation protection stantion,

a

12 x 12 foot plastic sheet covered with debris, and a bag of old light bulbs.

The

licensee removed all materials from the area.

The inspectors determined this action

to be appropriate.

As noted in Inspection Report 50-528, 529, 530/96-12, the licensee had recently

initiated a housekeeping

improvement program which had established

housekeeping

standards

for 111 plant areas.

Throughout this inspection period, the licensee was

in the process of inspecting these areas and addressing

weaknesses.

At the end of

the inspection period, they had concluded that only 9 areas of the 111 had met

their standards.

Conclusions

The inspectors continued to identify material condition and housekeeping

issues

which have not been previously identified by the licensee.

The licensee was

continuing to implement their housekeeping

improvement program.

V. IVlana ament IVleetin s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management

at the

conclusion of the inspection on October 2, 1996.

The licensee acknowledged

the findings

presented.

The inspectors

asked the licensee whether any material examined during the inspection

should be considered

proprietary.

No proprietary information was identified.

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ATTACHMENT 1

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Flood, Department Leader, System Engineering

C. Foster, Engineer,

Design Engineering

R. Fullmer, Director, Nuclear Assurance

J. Gaffney, Department Leader, Radiation Protection

J. Glover, Engineer, System Engineering

R. Hazelwood, Engineer, Nuclear Regulatory Affairs

W. Ide, Vice President,

Engineering

K. Jones,

Section Leader, Design Engineering

A. Krainik, Department Leader, Nuclear Regulatory Affairs

R. Lucero, Department Leader, Electrical Maintenance

D. Mauldin, Director, Maintenance

G. Overbeck, Vice President,

Nuclear Operations

M. Powell, Department Leader, Nuclear Engineering

F. Riedel, Acting Director, Operations

C. Seaman,

Director, Emergency Services

M. Shea, Director, Radiation Protection

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INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 9290'I: Followup - Operations

IP 92903:

Followup - Engineering

IP 92904:

Followup - Plant Support

IP 93702:

Prompt Onsite Response

to Events

ITEMS OPENED

CLOSED AND DISCUSSED

~Oened

50-528; 530/9601 3-01

50-529/9601 3-02

NOV

failure to follow procedures

for ventilation boundary

door control

NCV

inadequate

procedure controls allow equipment

qualification boundary to be breached

Closed

50-528/96003

50-529/96005

50-529/9601 3-02

LER

open auxiliary building door causes

fuel building

essential filtration inoperability

LER

inadequate

procedure controls allow equipment

qualification boundary to be breached

NCV

inadequate

procedure

controls allow equipment

qualification boundary to be breached

Discussed

50-528/9601 2-01

50-530/96007-04

IFI

control of ventilation boundary penetrations

NCV

failure to follow procedure for blocking open

controlled doors

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LIST OF ACRONYMS USED

AFW

AO

CRDR

EDT

EHA

HELB

LER

MCC

RP

SIAS

SS

SSM

TS

UFSAR

UGS

W.g.

auxiliary feedwater

Auxiliary Operator

condition report/disposition request

equipment drain tank

auxiliary building essential ventilation system

high energy line break

Licensee Event Report

Motor Control Center

Radiological Protection

safety injection actuation signal

Shift Supervisor

Site Shift Manager

Technical Specifications

Updated Final Safety Analysis Report

upper guide structure

water gage

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