ML17311A245

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Insp Repts 50-528/94-22,50-529/94-22 & 50-530/94-22 on 940612-0723.Violation Noted.Major Areas Inspected:Plant Status,Onsite Response to Events,Operational Safety Verification & Maint & Surveillance Observations
ML17311A245
Person / Time
Site: Palo Verde  
Issue date: 08/30/1994
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17311A243 List:
References
50-528-94-22, 50-529-94-22, 50-530-94-22, NUDOCS 9409120063
Download: ML17311A245 (44)


See also: IR 05000528/1994022

Text

PPENDIX B

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-528/94-22

50-529/94-22

50-530/94-22

Licenses:

NPF-41

NPF-51

NPF-74

Licensee:

Arizona Public Service

Company

P.O.

Box 53999

Phoenix,

Arizona

Facility Name:

Palo Verde Nuclear Generating Station,

Units 1, 2,

and

3

Inspection At:

Maricopa County, Arizona

Inspection

Conducted:

June

12 through July 23,

1994

Approved:

Inspectors:

K. Johnston,

Senior Resident

Inspector

H. Freeman,

Resident

Inspector

J. Kramer, Resident

Inspector

A. MacDougall, Resident

Inspector

D. Acker, Project Inspector

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ns ection

S mmar

td:

t ti,

di

p tt

dpi

t tt,

it

response

to events,

operational

safety verification,

and maintenance

and

surveillance observations.

esu ts

Units

1

2

and

3

~

Plant

0 erations

In June,

Unit

1 operators identified that

a routine channel calibration check

of core protection calculator channel

"D" could not be performed

because

a

reactor coolant system temperature

input was fluctuating greater

than the

channel calibration check acceptance criteria.

However, the magnitude of

channel fluctuations

had changed little since early

1993

and

had not been

properly addressed

by operations

(Section 2.1).

t

The

NRC inspectors

noted unauthorized

and inconsistent

operators

aids in the

control

rooms

(Section 3. 1).

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The

NRC inspectors

noted unauthorized

and inconsistent

operator

aids in the

control

rooms (Section

3. 1).

An alert

and questioning auxiliary operator identified

a leak in the Unit

1

spray

pond piping during

a routine tour (Section 4. 1).

~

Maintenance

The planning

and performance of an emergent repair to a leak in the spray

pond

piping was thorough

and well implemented.

Engineering evaluation of the

failure was thorough

(Section

4. 1).

En ineerin

While engineering's

evaluation of the cause

and safety

impact of fluctuations

in hot leg temperature

was thorough,

they missed

an

>pportunity to identify

that the daily channel calibration check of the

CPC could not be performed

(Section 2.1).

Engineering

appears

to have

made progress

in improving the performance

and

reliability of,the feedwater

and steam

bypass control

systems.

Additionally,

they appear to be pursuing further modifications to further improve

performance

(Section 6).

Engineering

has completed

a review of a cable installation data

base

which had

previously not been well controlled

and

was not reliable.

The. licensee

has

updated

the data

base

and

has

improved controls to assure

future data

base

reliability (Section 7).

Plant

Su

ort

Two portable chemistry monitoring instruments

were found by the inspector to

have

been installed for extended

periods.

The licensee

responded

quickly to

remove the monitors

and evaluate their procedures

for the use of temporary

monitoring equipment

(Section

5. 1)...

The licensee

has

used

temporary shielding in areas of high radiation for

extended

periods without aggressively

pursuing

permanent

solutions

(Section 5.2).

Material condition appeared

to have deteriorated

in some areas.

In Unit 3,

an

excessive

amount of debris

from maintenance

and cleaning activities was noted.

Additionally,

a program to monitor and minimize boric acid leaks in valve

packings

appeared

not to have

been fully implemented

(Section 3.4).

Also in

Unit 3,

an auxiliary feedwater

pump junction box was not fully secured

(Section 3.3).

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Mana ement Overview

During the inspection,

several

findings were identified that highlighted

an

apparent

lack of plant management

in the field.

For example,

a month after

a

refueling outage

the inspector

noted material condition weaknesses

in Unit 3

which could

be attributed to outage work.

It was also noted that, during this

period, licensee

management

focused

a substantial

amount of time on the

reorganization

selection

process.

Summar

of Ins ection Findin s:

~

One violation of NRC requirements

was identified (Section

2. 1).

Attachment:

Persons

Contacted

and Exit Meeting

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I

DETAILS

1

PLANT STATUS

.

1.1

Unit

1

Unit

1 operated

at 86 percent

power from June

12-30 when the licensee

raised

reactor

power to 98 percent

in response

to high electric

demand

on the

southwestern

grid.

Reactor

power was limited to 98 percent for the rest of

the inspection

period due to two inoperable

main steam safety valves.

On July

6, the licensee

implemented

a Technical Specification

(TS) change

which

allowed operation at

a 10'F lower

RCS temperature.

1.2

Unit

2

Unit 2 began

the inspection period in Mode

1 at 86 percent

power.

On

June

30,

1994,

the unit increased

power to 100 percent

due to high electric

demand

on the southwestern

grid.

On July 8, the licensee

decreased

power to

88 percent,

after the electric

demand

had decreased,

and remained there

through the

end of the inspection period.

Power was returned to 88 percent

vice 86 percent

based

on

a revised calculation of steam generator

tube dryout.

Also on July 8,

a management

meeting

was held in the Region

IV office in

Arlington, Texas,

to discuss

the

May 28,

1994, reactor trip.

1.3

Unit 3

Unit 3 began

the inspection period in Mode 5, completing the fourth refueling

outage.

The unit commenced

a normal reactor startup

and entered

Mode

2

operations

on June

18.

On June

24, the unit completed testing

and raised

power to

100 percent.

The unit remained

at essentially

100 percent

through

the

end of the inspection period.

2

ONSITE

RESPONSE

TO

EVENTS (93702)

2. 1

Unit

1

RCS Hot Le

Tem erature

Fluctuations

On June

19,

1994.

a reactor operator

noted that the digital readout of

calculated

thermal

power on

CPC Channel

D was oscillating by more than

6 percent

power.

The shift supervisor

concluded that the

TS surveillance

requirement

to calibrate the calculated

thermal

power to within a 2 percent of

the secondary calorimetric power could not be performed

because

the magnitude

of the oscillations

was greater

than z 2 percent

(4 percent absolute).

As

a

result,

the shift supervisor declared

CPC Channel

D inoperable

and placed the

affected reactor protection functions in bypass.

The licensee

determined

that the large fluctuation in c lculated thermal

power

was caused

by

a known fluctuation in the

CPC Channel

D Loop

2 hot leg

temperature

(T,.) instrument

used to calculate

thermal

power.

The fluctuation

appears

to be actual

loop temperature

fluctuations

and not an instrument

e

l

issue.

The licensee

developed

a temporary modification

(THOD) to upgrade

a

nonsafety-related

T.. resistance

temperature

detector

(RTD) that displayed

less fluctuations

and to use it as the input to the

CPC.

On July 2, the

licensee

installed the

TMOD and returned

CPC Channel

D to service.

The inspector

reviewed the

10

CFR 50.59 evaluation for installation of the

THOD, the

TS limiting conditions for operation

(LCO) and surveillance test

requirements,

the engineering

evaluation of the cause of the Channel

D hot leg

temperature

fluctuations,

and the plant review board's

response

to an

engineering

presentation

of the hot leg temperature

fluctuations.

The

inspector

conducted

a field verification of the

THOD installation.

The

inspector

concluded that:

Engineering

had identified oscillations of up to 5'F in the Unit

1

Channel

0 hot leg temperature

input to the

CPC

on February

18,

1993.

They identified that the temperature

fluctuations were due to hot leg

temperature stratification.

~

Engineering

subsequently

concluded that the fluctuations did not create

a situation adverse

to safety,

and the

CPC was able to perform its

design fgnction.

Their evaluation of the cause

and safety impact of the

fluctuations in hot leg temperature

was thorough.

Operators

were performing routine channel calibration checks of CPC

Channel

0 and did not conclude that the check

was out of calibration due

to the magnitude of the temperature

fluctuations until June

1994,

even

though the magnitude of the fluctuations

had

changed little since early

1993.

As

a result,

the

TS requirement to perform

a channel calibration

was not performed.

~

Licensee

management

missed opportunities to identify the impact of the

temperature

fluctuations

on the channel calibration check.

~

The development

and implementation of the

THOD was appropriate.

2, 1. 1

Engineering

Evaluation

On February

18,

1993,

the nuclear fuel engineering

analysis

group first

identified that the Unit

1

Loop

2 hot leg Channel

0 temperature

instrument

exhibited oscillations of up to 5'F.

Engineering

noted that the magnitude of

the oscillations

were substantially larger than

any similar instrument

on

site.

The licensee initiated

an engineering

evaluation

(EER 93-RC-017)

to'etermine

the cause of the fluctuation.

Engineering

gathered

data

from the instrument

and the

RTD.

The data

was

analyzed for any sharp

jumps or discontinuities,

which could indicate

component failure, but none were found.

The plotted data

appeared

to have

an

exponential

shape,

which was the expected

shape for an

RTD responding to an

actual

temperature

fluctuation.

Next, the licensee

analyzed

the data using

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fast Fourier transform analysis

to determine if there were any periodic

events,

such

as electrical

noise,

which could be the source of the

fluctuations.

The analysis

revealed that the fluctuations

appeared

to be

random

and were not the result of a periodic driving event.

Engineering

concluded

in the evaluation that the observed fluctuations in temperature

appeared

to be the result of the

RTD responding

to actual

changes

in the

RCS

temperatures

The

licensee

had previously replaced

another

RTD that

had

exhibited similar fluctuations.

The

new

RTD continued to exhibit the

same

fluctuations.

0

In January

1994,

the licensee

completed

a study

and concluded that the

RTD

fluctuations were due to

RCS hot leg stratification effects.

The study

included

a review of the impact of the temperature

variation

on the

CPC.

The

licensee

concluded that the only effect of the fluctuation on the safety-

related functions for the

CPC calculated

thermal

power was for protection

against

a 12-finger control element

assembly

(CEA) drop event.

The licensee

concluded that for a 12-finger

CEA dropped in the center of the core,

the

neutron detectors

may not detect

a flux tilt or power shift; however,

because

a 26 percent penalty factor would be automatically inserted for any 12-finger

CEA drop,

the reactor

would trip and the core would be protected.

The

inspector

reviewed the study

and agreed with the conclusions.

Engineering

noted to the inspector that the vendor,

Combustion

Engineering

(CE),

had conducted

a study of temperature stratification effects

on

CE reactors

which included data from Unit 1.

In a letter to the licensee

dated

February

22,

1991,

CE explained that the temperature stratification in

CE reactors

usually appears

to have

a static component,

the upper half of the

hot leg pipe is hotter than the lower half; phase rotation, the hottest

and

coldest point in the pipe is not necessarily

at the top and bottom of the

pipe,

but rotated

by an angle;

and

a dynamic component,

where

a semi-stable

vortex shifts from one portion of the pipe to another semi-stable

position.

CE had identified these conditions in other

CE plants.

At the time,

however,

Unit

1 did not exhibit the dynamic component.

Finally,

CE explained that the

characteristics

of the stratification depended

on numerous factors including

fuel loading,

rod position,

and core

age

and that the. characteristics

would

change

over time.

The inspector

concluded that the licensee

conducted

a thorough review of the

cause

and effects of the hot leg temperature stratification issue.

The

inspector

agreed with the licensee's

conclusion that the

CPC had

enough

margin

to account for the fluctuations

and that the core

was not in an unreviewed

condition.

The inspector

noted that this review had

been concluded

in early

1994.

As discussed

below, the inspector

was concerned that the effects of the

temperature

fluctuations

on the routine performance of CPC channel calibration

check were not fully evaluated.

2. 1.2

TS Verification

Facility TS require that

a channel calibration check

be performed every

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to verify that the linear power level, the

CPC thermal

power,

and the

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CPC nuclear

power signals

are within M percent of the calorimetric power.

This verification is conducted

as part of the "Routine Surveillance Daily

Hidnight Logs," Procedure

40ST-92Z16.

The procedure directs the operators

to

record

CPC total thermal

power,

CPC nuclear

power,

and secondary calorimetric

power.

The procedure

required that the

CPC channel

be calibrated if either

thermal

power or nuclear

power was more than

2 percent

above or below the

actual

(secondary

calorimetric) reading.

On June

19,

1994, operators

noted during the channel calibration check that

CPC Channel

D thermal

power was fluctuating by more than

6 percent.

Reactor

engineering

was contacted

when

CPC Channel

D was declared

inoperable

and

determined

that

known fluctuations in the Channel

D T., instrument

were

causing

the Fluctuations

in

CPC thermal

power.

The inspector determined

in

a review of engineering

data

and operator

interviews that there

had not been significant change

in the fluctuations of

CPC Channel

D from February

1993 to June

1994.

Since

1 degree of change of

temperature

across

the reactor

core represents

a change of about 1.5 percent

power,

the fluctuations of 4 to 5 degrees,

measured

in February

1993,

would

have

caused

the calculated

thermal

power to consistently deviate greater

than

the H percent,TS limit.

The inspector concluded that,

since February

1993,

the licensee

could not have acceptably

performed the required

channel

calibration.

This is

a violation of TS 4.3. 1. 1 (Notice of Violation 528/9422-

Ol).

The inspector recognized that the fluctuations in thermal

power did not create

a situation

adverse

to safety

(See Section

2. 1. 1)

and that

CPC Channel

D was

able to perform its design function.

However, this violation

was being cited

because

operators

had not recognized for over

a year that the calibration

check could not be adequately

performed.

Additionally, plant management

missed opportunities to identify the effects of the temperature

fluctuations

on the channel

calibration checks

(Section

2. 1.3).

The inspector

questioned

why operators

had not recognized earlier that the

channel calibration check could not be adequately

performed

on

CPC Channel

D.

The inspector

found from discussions

with operators

that they'ypically'ook

an informal

mean value of the fluctuating instrument reading.

The inspector

found that the licensee

did not have formal guidance for operators

to evaluate

oscillating or fluctuating i'nstrument readings.

The inspector

questioned

whether there

were other routine measurements

or readings

taken from

fluctuating instruments

which required further evaluation.

The inspector

discussed

these

concerns

with licensee

management

who indicated that the

reading of fluctuating instruments will be evaluated.

The inspector will

review this issue further in conjunction with the licensee's

response

to the

violation.

2.1.3

Plant

Review Board

(PRB) Review

The inspector

noted that in April 1994 representatives

from plant engineering

made

a presentation

to the

PRB concerning

the Unit

1 T fluctuations.

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inspector

reviewed the

PRB minutes

and noted that engineering

had questioned

how the

TS verification was performed.

In the presentation,

engineering

stated that "the temperature

reading variability has

added

some difficulty for

the

CPC thermal

power calibration in that it was difficult to decide

what

temperature

value

(an average,

the lowest,

the highest?)

to select for use in

the thermal

power calculation."

Engineering

also stated that "there

was not

any definite operations

guidance

on how to select the appropriate

reading."

Based

on the engineering

presentation,

the

PRB board concluded that there

was

not an unreviewed safety question or safety concern with the T., fluctuations.

However,

the licensee

did not conduct

any followup to investigate the

questions

posed

by engineering

concerning

the thermal

power calibration.

The

inspector

concluded that licensee

management

had missed

an opportunity to

identify the problem in April 1994.

Additionally, the inspector

concluded

that the licensee

had missed

a similar opportunity to identify the effects of

the temperature

fluctuations

when they were first identified in February

1993.

2. 1.4

THOD Development

and Implementation

The licensee

developed

a

THOD to swap

an installed nonsafety-related

T RTD,

used for input:to the core operating limit supervisory

system, for the safety-

related

RTD used

as

an input to

CPC Channel

D.

The inspector reviewed the

10

CFR 50.59 evaluation for the

THOD and agreed with the licensee's

conclusion

that the

THDD did not create

an unreviewed safety question

and was acceptable

for a short period.

The inspector

conducted

a walkdown of the affected electrical penetrations

and

cable

raceways.

The inspector

noted that

one of the covers

had

a missing

and

stripped fastener.

The inspector

was concerned

that the electrical

penetration

cover was not water tight due to the missing fastener.

The

licensee initiated

a work request to correctly install the fastener.

The

inspector

concluded that the licensee's

corrective actions

wet e appropriate.

2. 1.5

Licensee Actions

Based

on the inspector's

concerns,

the licensee

formed

a team to evaluate

the

effect of the T, fluctuations

on performance of the

CPC calibrations.

The

licensee

also

was issuing

a licensee

event report describing the problem with

CPC Channel

0 and concluded that

CPC Channel

D was inoperable for the last

2

operating cycles.

The licensee

event report will be reviewed in

a future

inspection.

3

OPERATIONAL SAFETY VERIFICATION

(71707)

3.1

Units 1.

2.

and 3.

Use of 0 erator Aids and Control

Room Labelin

On June

28,

1994,

the inspector

observed

red grease

)en marks

on the control

room

(CR) operating

switches for CR heating, ventilation

and air

conditioning

(HVAC) in Unit 2.

The inspector

was informed that the marks were

placed

on the switches to aid the operators

in the identification of valves

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required to be open during power operations.

Further inspection

revealed

the

same

marks present

in Unit 1.

The inspector

noted that the marks were not

controlled under the licensee's

operator

aid program

and notified operations

management

of the unauthorized

markings

on the

CR boards.

The licensee

removed the markings.

The inspector

checked

the consistency of the

CR labels,

placards,

and operator

aids.

The inspector

noted several

minor discrepancies

and brought them to the

attention of operations

management.

These

aids included

a plexiglass

cover

over

a Unit 2 reactor coolant

pump hand switch, apparently

used to prevent

operators

from inadvertently turning the

pump off, which was not used in

either Units

1 or 3.

Additionally, small placards

in Unit 3 cautioned that

synchronization

key switches

should not be inserted into more than

one

selector

switch at

a time.

Similar placards

were not used in Units

1 and 2.

The inspector

noted that the licensee

had

a detailed

procedure

governing the

use of operator aids.

The procedure

had

been developed

in response

to

weaknesses

identified in 1989.

The inspector

expressed

concern that the

program

was not being fully implemented.

In response

to the inspector's

concerns,

the licensee

assigned

the Unit

1 operations

department

leader to

review the use,of operator

aids

and the process

of labeling control

room

equipment.

On July 25, the inspector

observed that the

CR HVAC switch markings were once

again present

on the switches

in Unit 1.

The inspector notified operations

management

of the unauthorized

markings

on the

CR boards,

and once again the

licensee

removed the markings.

The licensee initiated

a night order to inform

operators

of management's

expectations

for marking

and labeling plant

equipment.

At the exit meeting,

the inspector

expressed

concern that

management

had not fully communicated

the expectation that the markings not be

used after the first incident,

nor had they identified the markings

themselves.

3.2

Unit

1 - Walkdown of En ineered

Safet

Features

ESF

E ui ment

Room

Ventilation

S stem

The inspector

reviewed the Updated Final Safety Analysis Report,

conducted

a

field walkdown,

and reviewed the design

heat loading calculation for the

ESF

equipment

room ventilation system.

The

ESF equipment

room ventilation system provides

room cooling for four

safety-related

125-Vdc and

120-Vac distribution systems.

Each system is

located

in

a separate

room that is cooled

by the normal control building

ventilation system.

The

ESF equipment

room ventilation system provides

cooling to the equipment

rooms

on

a loss of normal ventilation and

on

a loss

of offsite power or safety actuation signal.

The inspector

concluded that the

ESF equipment

room ventilation system would

provide sufficient cooling flow to ensure that the safety-related

120-Vac

and

125-Vdc electrical distribution systems

remained

operable.

The inspector

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noted

a minor material deficiency involving a missing nut on

a ventilation

damper support plate that

was promptly corrected.

The inspector

noted that the alarm response

procedure for a high temperature

alarm in the

ESF equipment

room did not indicate at what point TS

LCOs should

be entered.

The licensee

stated that the surveillance test procedure for

inoperable essential

chilled water

and ventilation systems

directed the

ESF

equipment

room to be declared

inoperable if both the normal

and essential

ventilation systems

were inoperable.

This would put the plant in a 72-hour

TS

shutdown

LCO.

The licensee

agreed that the alarm response

procedure

should

reference

the surveillance test procedure

and initiated an update to the alarm

response

procedure.

The inspector

concluded that the licensee

actions

were

appropriate.

3.3

Auxiliar

Feedwater

Pum

Junction

Box Unit 3

On July 5,

1994,

the inspector

noted that the cover to

a junction box on the

Unit 3, turbine-driven auxiliary feedwater

pump was not fully secured.

The

inspector contacted

the shift supervisor

and raised

concerns

about the

potential

impact of a high steam

environment

on the internal

components.

When informed by the inspector of the junction box cover,

the supervisor

immediately sent

an electrician to open

and inspect the components

in the

junction box.

The electrician

inspected

the junction box and did not find any

degraded

components.

Following the inspection,

the electrician fully secured

the junction box cover.

The licensee initiated

an operability determination

on the effect that the

condition had

on the pump's operability.

The junction box, which housed

power

and control cables to the turbine's trip and throttle valve motor operator

(AFA-HV-54), was approximately

14"x16"x6" and contained

a hinged cover.

The

junction box had four mechanisms

to secure

the cover but only one

had

been

engaged.

The licensee

conducted

a seismic review and concluded that one

mechanism

was adequate

to keep the cover in position during

a seismic event.

Additionally, the licensee

concluded that the junction box was not in a harsh

environment

and that the humidity during

pump operation

would not have

caused

electrical

problems to the trip and throttle valve motor operator.

The

inspector

agreed with the licensee's

conclusions.

Finally, the licensee

initiated

an investigation

on

how the junction box cover

became

not fully

secured.

The inspector

concluded that the licensee

took prompt corrective actions

and

that the impact of the condition did not affect the operability of the

auxiliary feedwater

pump.

3.4

Material Conditions - Unit 3

On July 14,

1994. during

a routine tour of the

77 foot level of the east

piping penetration

room in Unit 3, the inspector

noted that the material

conditions

had degraded

over the past

few months.

For example,

the inspector

1

I

-ll-

found several

valves which had boric acid accumulation

in the yoke area.

The

inspector

noted

a safety injection vent valve with a continuous

stream

discharging

into

a drain through

a tygon tube

and contacted

the operations

crew to secure

the leak.

The inspector also noted

a shutdown cooling system

valve that

had

a large

amount of dried boric acid crystals

on the valve body

and

on the floor.

Finally, the inspector

noted debris

(a cut mechanical

lock,

a bag of parts,

a roll of electrical

tape,

and other residual

trash)

from the

recent refueling outage that

had not been

removed

from the area.

The

inspector

concluded that the material condition

and housekeeping

in the space

did not represent

safety hazards,

but were indicative of an overall declining

trend.

The inspector

reviewed the licensee's

program for maintaining valve material

conditions

and minimizing valve packing leaks.

The inspector

noted that the

licensee

has

a zone inspection

program where

each operations

crew was

responsible

for

a specific area.

Each crew was expected

to perform an area

inspection

once

each

work cycle (every

6 weeks)

and

was to submit work

requests

when needed.

The inspector

reviewed the previous inspection for the

area

and noted that it had

been

completed

on July

13 but had not identified

the leaking vent valve or the boric acid

on the shutdown cooling system valve.

The inspector

also noted that the program

was more effectively used

by some

crews than others.

For example,

one previous inspection of three

zones

conducted

on February

8 (several

hundred valves) did not identify any

discrepancies

where other area

inspections typically identified 20 to

30 discrepancies.

The inspector discussed

the zone inspection

program

and general

plant

conditions with the licensee.

The inspector noted that the program was not

formally controlled

and

was not consistently

implemented.

Licensee

management

concurred that the program

has not been fully effective.

They anticipated

that the system responsibilities

assigned

to maintenance

crews in the

re-engineering

process

would promote material condition improvements.

The inspector

found in discussion

with Unit 3 management

that managers

had not

toured the area recently.

This was,of concern

since Unit 3 had recently

restarted

from a refueling outage.

Additionally, the- inspector noted that the

licensee's

response

to the previous Systematic

Assessment

of Licensee

Performance

committed to having management

in the field on

a frequent basis to

identify problems.

The inspector

concluded that the licensee's

program for

material

control

and housekeeping

required

more management

attention.

3.5

Unit 2 Crane

Breaker Closed

and Caution

Ta

ed "0 en"

On July 1,

1994,

the inspector

noted the breaker for an auxiliary building

crane

was closed with a caution tag

on the breaker stating "contact safety

department

before operating crane/energizing

breaker.",

The inspector

contacted

the safety department

and determined that the crane

was not being

used

and that the breaker

should

have

been in the o'en position.

Operations

was informed,

and the breaker

was opened.

I

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The licensee

had placed

the caution tag

on the crane breaker

as

an interim

corrective action until the crane's

pendant

could

be modified to comply with

Occupational

Safety

and Health Administration

(OSHA) standards

to have

an

emergency

stop

push button or equivalent.

As

a result of the inspector's

finding, the licensee

placed

an additional caution tag

on the control pendant

on all similar type cranes

in the plant

(11 total) to alert personnel

of the

potential

hazard

in operating this type of crane

and replaced

the caution tag

on the breaker with a danger tag.

The licensee

planned to evaluate

the

11 similar cranes

to determine

which were used frequently

and warranted

the

pendant modification.

They planned to remove

power from cranes that were not

frequently used.

The inspector

noted the quick and thorough response

of the licensee after the

inspector identified and informed the licensee of the problem.

The inspector

concluded that the licensee

actions

were adequate.

4

MAINTENANCE OBSERVATIONS

(62703)

During the inspection period,

the inspector

observed

and reviewed the selected

maintenance

activities listed below to verify compliance with regulatory

requirements

and licensee

procedures,

required quality control department

involvement,

proper

use of safety tags,

proper equipment

alignment

and use of

jumpers,

personnel

qualifications,

appropriate radiation worker practices,

calibrated test instruments,

and proper postmaintenance

testing.

Specifically, the inspector witnessed

portions of the following maintenance

activities:

4. 1

Unit

1

S ra

Pond

Pi in

Leak Due to Coatin

De radation

On July 10,

1994,

an auxiliary operator

(AO) noted water under

a portion of

the Train A spray

pond piping during

a routine tour.

The

AO inspected

the

piping and identified

a small pin hole leak in the piping.

The Train A spray

pond system

was declared

inoperable.

The spray

pond system is the ultimate

heat. sink for the essential

cooling water system which provides cooling water

to the essential

chilled water system,

the shutdown heat exchangers,

and the

emergency diesel

generators.

As

a result,

several

72-hour

TS

LCO action

statements

were entered.

The inspector

reviewed the work order to repair the leak,

observed

the

hydrostatic test of the repair,

and discussed

the leak with the licensee's

engineering

staFf.

The inspector

concluded that the licensee's initial

actions to solve the problem were good.

Specifically, the

AO was alert to a

deficient condition,

the planning

and conduct of the maintenance

was good,

and

the initial engineering

evaluation

was thorough.

The inspector

also noted

that the licensee

was evaluating

the scope of the overall underground

piping

inspection

program

based

on this failure.

I

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.

4. 1. 1

Corrective Actions

-13-

The licensee

drained

the system,

removed

and installed

a spool

piece in the

piping,

and performed

an inside/outside

weld repair of the defect.

On

July 11, the licensee

reassembled

the pipe

and satisfactorily performed

a

hydrostatic test of the affected portions of the spray

pond system.

The

licensee

determined

that the piping failure was initiated by a defect in the

piping coatings

The licensee

conducted

a visual inspection of the coating

on

the inside of the accessible

portions of the disassembled

spray

pond piping

and did not identify any other defects.

The licensee

subsequently

declared

the spray

pond

system operable

and exited the

TS

LCO action statements.

The inspector

noted that the licensee

had conducted

visual inspections of

selected

portions of the spray

pond piping during the previous refueling

outages

in each unit.

About 450 linear feet of the underground

portions of

the spray

pond supply

and return lines

and

a small portion of piping to the

emergency diesel

generators

were inspected.

The inspector noted that the area

of the defect

was not included in the inspection

because

the piping was not

underground.

Representatives

from the Electric Power Research

Institute

performed the inspections

and concluded that, in general,

the piping was in

good condition .and that

no immediate corrective actions

were needed.

The

inspector

reviewed the reports

and noted there

was

one area in each unit where

there

appeared

to be

an actual

break in the coating that could lead to

accelerated

corrosion.

The inspector

learned that the licensee

had previously evaluated

the defects

and determined that,

based

on the

known corrosion rates

and the limited number

of defects,

the repairs

could

be deferred to the next refueling outage.

The

licensee

planned to perform additional visual inspections

during the upcoming

refueling outages

to determine

the change in the affected

areas

and to conduct

any required repairs.

The inspector

concluded that the licensee's

basis to

defer the repairs

was reasonable

and that the existing spray

pond piping

inspection

program

was adequate.

4.2

Unit 2

CEA Sli

Durin

Testin

On June

18,

1994, during the performance of CEA Operability Checks

(Surveillance

Procedure

42ST-2SFOI),

CEA 60 slipped

about

2 inches

each time

it was given

a withdrawal

command

and then would withdraw as designed.

Operations

personnel

consulted with engineering

and the operations

manager

and

then placed

CEA 60 at the upper electrical limit (UEL) upon completion of the

surveillance to provid additional positive indication that the

CEA was fully

withdrawn and

had not slipped.

The other

CEAs remained at the program level

of UEL-2 (two steps

below the UEL).

The licensee initiated

a condition

report/disposition

request

to evaluate

the problem.

The inspector questioned

reactor engineering

about the placement of CEA 60.

Reactor engineering

stated

that the

CEA was within the

TS limit for deviation

from other

CEAs

and that the

CEA position did not violate the core data

book.

i

-14-

In addition, reactor engineering

stated that having one

CEA 1.5 inch (two

steps)

further withdrawn at the top of the core would not adversely affect

core

power distribution or guide tube wear.

The inspector

agreed with the

licensee

conclusions.

The inspector

noted in

a conversation

with the Unit 2 reactor engineer that

he

was

unaware that

CEA 60 had

been positioned at the

UEL.

While there

was

'ittle

safety significance,

the inspector

was concerned

that

a week after the

CEA had

been repositioned,

the responsible

engineer

was not cognizant of the

condition.

The licensee

acknowledged

the inspector's

comments

and indicated

that the issue

would be further reviewed.

On July 16, the licensee

repaired

CEA 60.

Two defective

equipment

cards

were

replaced.

The licensee

returned

CEA 60 to program position.'he

licensee

planned to repair the defective cards

in their rework shop.

The inspector

reviewed the licensee's

troubleshooting

proces:; for the defective

cards

and

noted

no discrepancies.

4.3

Other Haintenance

Observations

The inspector

qbserved

portions of the following maintenance activities

and

determined

that they were performed acceptably:

~

Unit

1 Feedwater

Pump Governor

Power Supply Repairs

~

Unit 2 Control

Room Essential Air Handling Unit Cooling Coil and Bellows

Inspection Preventative

Haintenance

~

Honthly Preventative

Haintenance

on the Security Diesel

5

PLANT SUPPORT

(71750)

The inspector

performed routine tours of the units to verify that

radiological,

physical security,

and fire protection

programs

were implemented

in accordance

with facility policies

and regulatory requirements.

Included in

these tours were verifications of the accessibility to locked high radiation

areas,

posting of radiation areas,

physical security control,

and general

material conditions.

5. 1

Continuous

In-Line Chemistr

Honitors

During routine plant tours.

the inspector identified

a condition in Unit 3

where

a portable

oxygen detector

was installed to

a condensate

storage

tank

test connection to obtain

a continuous on-line reading.

The inspector

also

noted

a similar condition in Unit 2 where

a portable conductivity meter

was

installed to

a sample point on the auxiliary steam

condensate

receiver tank

outlet valve to provide

a continuous on-line reading.

The inspector

noted

that these installations

were not controlled

as temporary modifications

and

questioned

the licensee

concerning plant configuration control.

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The licensee initiated

a condition report/disposition

request

to review the

control of these particular installations.

The licensee

determined that these

installations

were controlled

by approved

chemistry sampling procedures.

However, the inspector

was concerned that the intent of the procedures

was

primarily for short duration or "grab" type samples

and not for a condition

that

may require

a long-term continuous monitor.

The licensee

acknowledged

the inspector's

concern

and agreed to review the secondary

sampling

instruction procedure

to verify if the procedural

controls for continuous

sampling

were adequate.

The inspector

concluded that the licensee

had valid reasons for installing the

monitors, that they were being periodically reviewed

by chemistry

management,

and that they did not impact equipment operability.

The inspector

also noted

that the licensee

removed the monitors until the review of the procedure

was

completed.

The inspector

concluded that the licensee's

corrective actions

were prompt

and thorough.

5.2

Locked Hi

h Radiation Areas

Unit 3

On July 14,

1994, during

a routine tour of the Unit 3 auxiliary building, the

inspector

noted, that

some of the temporary shielding installed

around high

radiation

sources

had

been installed for extended

periods

up to 5 years.

For example,

the inspector

noted that the licensee

had installed temporary

shielding

and

a sign

on

a section of piping which stated that the radiation

levels

under the shielding met the conditions of a locked high radiation area.

Because

the shielding

was covered

by plastic sheeting,

the inspector

was

unable to view the installation.

The inspector

noted that the installation

had

been in place since

Narch

14,

1994.

The inspector discussed

the use of

temporary shielding with the licensee

and

was informed that temporary

shieldinp

was usually held in place

by plastic tie wraps or some other

nonpermanent

means.

Although the inspector noted that most temporary

shielding

was

removed after

2 weeks,

the inspector also noted

13 installations

which had

been

converted

to long-term use,

including four that were over

a

year old.

The inspector discussed

with radiation protection

management

the NRC's

guidance

on the use of temporary shielding

on areas that meet the requirements

of a locked high radiation area

as discussed

in NUREG/CR 5569,

"Health Physics

Positions

Data Base."

The

NUREG states

"other techniques

to reduce

source

term should

be

used (e.g.,

chemical

decontamination,

permanent shielding);

however,

as long

as reasonable

progress

is made toward the long-term fix (and

an effective system to preclude

unauthorized

removal of temporary shielding

exists),

the judicious

use of temporary shielding could

be justified on

an

interim basis."

The inspector

noted that the licensee

did not appear to be

aggressively

pursuing

the long-term fix.

The licensee

stated that they would

review the

use of temporary installations,

including shielding

and

modifications,

and attempt to limit their use.

The inspector

noted that the

licensee

had conducted

an audit

a few weeks earlier

and

had similar concerns

-16-

regarding

the

use of temporary shielding.

The inspector will follow up on the

licensee's

resolution of temporary installations

as part of a future routine

inspection.

6

FEEDWATER CONTROL SYSTEM (FWCS)/STEAM BYPASS

CONTROL SYSTEM (SBCS)

(71500)

The inspector

reviewed the design

and operation of the

FWCS and the

SBCS

and

discussed

recent

maintenance

problems concerning

these

systems with operators

and the system engineers.

The purpose of the inspection

was to determine

the

scope

and effectiveness

of the licensee's

long-term

FWCS and

SBCS improvement

program.

The inspector

noted that the licensee

has

made significant progress

in

correcting

a majority of problems with the

FWCS and

SBCS.

In 1991, the

licensee

performed major control

system modifications that significantly

reduced

the number of postreactor trip control

system complications.

For

example,

during

a 3-year period from 1989 to 1991 the site

had

19 reactor

trips which resulted

in

19 postreactor trip control

system complications

and

nine postreactor trip safety

system actuations.

After the modifications in

1991,

the site

has

had

a total of 13 reactor trips which resulted in

10 postreactor,trip

control

system complications

and

4 postreactor trip safety

system actuations.

The inspector determined that several

minor control

system problems still need

to be corrected with both the

FWCS and

SBCS.

These

problems include current

to pneumatic (I/P) transducer

and positioner zero drift, low power steam

generator

level oscillations,

and internal binding of the steam

bypass

control

valves

(SBCVs).

The licensee

has identified corrective actions for these

problems

and

has

scheduled

completion of the actions during the

1995 refueling

outages.

The inspector

also observed

a high level of management

involvement

to assure

that these corrective actions

are completed

as scheduled.

6. 1

SBCS Review

The inspector

reviewed the licensee's

corrective actions for SBCV problems

'identified during the Unit 2 load rejection

on May 14,

1994;

and the Unit 2

reactor trip on May 28.

SBCVs

1001

and

1004 were reported

as "jerky" during

the load rejection.

In addition,

valve

1004 did not fully close during the

reactor trip.

The licensee

performed diagnostic testing of SBCVs

1001

and

1004 following the

load rejection

and determined that Valve 1001 operated

properly and Valve 1004

had

a positioner zero drift which prevented

the valve from fully closing.

A

work order was written to calibrate the positioner of Valve 1004.

The work

was scheduled

for May 20 but was delayed

due to

a conflict with scheduled

work

in Unit 1.

As

a result,

the positioner

was not recalibrated until after the

reactor trip on May 28.

The licensee attributed

the jerky response

of Valve 1004 to internal clearance

problems that

had

been previously identified.

In Unit 2, the licensee

has

I i

-17-

completed

internal

clearance

modifications

on two of the eight

SBCVs

(1001

and

1003) to improve the smoothness

of the valves stroke with steam.

These

modifications

have

been

completed

on all eight control valves in Units

1

and 3.

The modifications of the remaining six control valves in Unit 2 were

scheduled

during the

1995 refueling outage.

6.2

FWCS Review

During the Unit 2 load rejection

and reactor trip in May 1994, operators

had

to close the

Steam Generator

1 economizer isolation valve due to excessive

feedwater flow, resulting in excessive

primary temperature

cooldown.

After

these

events,

the licensee calibrated

the economizer flow control valve and

determined

that the I/P had drifted

4 percent high.

As

a result,

when the

valve received

a signal

to close, it remained

approximately

4 percent

open.

The licensee

recalibrated

the I/P and the valve fully closed

when required.

The I/P drift was

a

common industry problem

and

was typically less

than

5 percent.

The licensee

was developing

a design modification to insert

a

negative

bias in the control circuit to ensure

the valve shuts after

a reactor

trip and during low power operations.

This modification was scheduled for

completion in September

1995.

The inspector

concluded that this improvement

should prevent;operator

intervention after

a reactor trip to prevent

overfeeding of the steam generator

and subsequent

overcooling of the primary

t

plant.

6.3

Meetin

With the Licensee

Re ardin

Feedwater

and

SBCS Problems

On July 8,

1994,

the licensee

met with the

NRC at the Region

IV office in

Arlington, Texas,

to discuss

the

May 28 reactor trip.

During this meeting,

the licensee

discussed

the history of problems with the

steam generator

flow

control

system

and the

steam

bypas

control

system

and their plans for system

improvements

discussed

above.

7

DESIGN CHANGES AND MODIFICATIONS

(37551)

The licensee

used

a computer

based. system called, the

EE580 system,

to maintain

a data

base for cable installations.

As documented

in Inspection

Report 50-

528/89-12;

50-529/89-12;

50-530/89-12,

previous

problems with the

EE580 system

had

been

found.

The cover letter of Inspection

Report 50-528/89-12;

50-

529/89-12;

50-530/89-12

requested

that the licensee

provide

an action plan

and

commitments

to review and correct deficiencies with the

EE580 system.

Under the

EE580 process.

installation cards

were issued for design

changes

and

the

EE580 data

base

was marked with a "C" to alert personnel

that

a change

had

been

issued for the installation covered

by the card.

When the installation

was complete,

the field verified card

was returned,

verified to match the

design,

and the

"C" removed

from the

EE580 data

base.

However, in 1989 the

licensee

determined

that

many more cards

had

been

issued

than

had

been

returned with field verification so that over 100,000

items in the

EE580 data

base

were marked with a "C." making the design

change

process difficult and

potentially affecting the accuracy of the data

base.

,

-18-

The. licensee

provided their corrective actions for the

EE580 system in letters

to the

NRC dated

October

20,

1989,

and

December

21,

1990,

and committed that

restoration

and documented

confirmation of the

EE580 data

base

would be

completed

by August

15,

1991.

The letters

noted that

6000 of the original

100,000

open

items still remained to be resolved.

NRC Inspection

Report 50-528/91-05,

50-529/91-05,

50-530/91-05 identified that

an internal licensee letter dated January

31,

1991, determined that there were

approximately

2200 open

items remaining to be corrected.

The licensee

documented

that they were unable to retrieve

741 lost

EE580

installation cards

in an internal letter dated August 6,

1991.

The licensee

stated that this action

was acceptable

based

on satisfactory unit operations,

notation in the data

base that these installations

had outstanding

cards,

and

the fact that the loss of the cards

was not technically significant, since the

circuits would be reverified by their current design

process prior to any

changes.

7. 1

Discussion

The inspector

reviewed the

EE580 system to ascertain if recent modifications

had

been correctly entered

into the system

and to ascertain if the existing

data

base

had

been

updated

as committed to correct the previously noted

problems.

The inspector determined that licensee

Procedures

81AC-OCC07, Revision 3,

"Cable

and

Raceway Control

& Tracking System,"

81PR-OD02,

Revision 4, "Plant

Design

Change

Program,"

81DP-ODC03,

Revision 5, "Final Engineering,"

and 81DP-

OCC25,

PCN 01,

"Cable

and

Raceway Control

8 Tracking System Activities,"

adequately

controlled changes

to the

EE580 data

base.

In addition, the

inspector

noted that the licensee's

guality Audits and Monitoring Department

Audit Report 92-011,

"Software guality Assurance," verified that the

EE580

program

had

a validation

and verification method that was initiated when

changes

to the

EE580

system

were made.

The inspector

selected

six cable trays,

including two with cables installed in

1993,

and veriFied that the number,

types,

and sizes of cables

in these trays

matched

the

EE580 data

base.

The inspector determined that the installations

matched

the

EE580 data

base,

except for one cable type which had

a slight

difference in the cable diameter;

the installed cables

were approximately

1. 1 inches

in diameter,

whereas

the

EE580 data

base

showed

them to be 1.4

inches in diameter.

The licensee

corrected

the

EE580 data

base.

The inspector

reviewed discrepancy

records

from

determined that guality Deficiency Reports

(and

issued

to request

engineering

resolution of any

EE580 data

base

and field installations.

Based

the inspector

considered

that the problems

were

problem with maintaining the

EE580 data

base.

1990 through

1994

and

other report types)

were being

differences

found between

the

on review of these

records,

not indicative of a systematic

P

'%

e

-19-

The inspector

determined that guality Control verified most aspects

of safety-

related

EE580 data

base related installations.

As noted in NRC Inspection

Report 50-528/89-12;

50-529/89-12;

50-530/89-12,

quality control also verified

initial EE580 installations'uring

the inspection,

the licensee

stated that

the

number of missing cards

had

been

reduced to 612, of which 179 involved

safety-related

equipment.

The inspector

noted that the licensee

had

based

acceptability of the missing data partly on unit operation.

The licensee

stated

that the

714 missing cards

from 1991

had

been

reduced to 612

as the

missing information was reverified by new changes

or missing cards

were found.

The inspector

noted that

10 CFR Part 50, Appendix R, safe

shutdown criteria

depended

on exact

knowledge of cable routing within and between fire areas.

The inspector

questioned

how unit operation

would show that the

EE580 data

base

was correct with respect

to cable routing.

The licensee

reviewed the

equipment

covered

by the 612 missing cards

and determined that

10 involved

cables,

5 of which were

10 CFR Part 50, Appendix R, cables.

The licensee

determined that the missing cards for three of the Appendix

R cables did not

involve any changes

to cable routing,

and that

no design

changes

were issued

which made

changes

to the other two cables

during the time that the missing

cards

were originally issued.

The licensee

concluded that no

10 CFR Part 50, Appendix R, cable routings were involved in the

612 missing cards.

The

licensee

also reviewed the other five cables,

determined that only two were

active,

and sighted the routing of these

cables

where they were accessible.

The licensee

determined that the

EE580 system

matched

the installations.

The licensee

determined that only 179 of the missing cards

were safety-

related.

The licensee

stated that they intended to sight equipment

as

'ecessary

to verify that the missing cards did not affect any installations.

The inspector determined that Procedure

70DP-ODC02,

Revision 4,

"System

Turnover," required engineering

signature verification that the

EE580 system

had

been

updated

using field verified installation cards for all design

changes.

The inspector

reviewed completed

EE580 cards

and did not identify any

problems.

The inspector

reviewed

a recent modification for station blackout

and verified

that selected

information from this modification had

been correctly entered

in

the

EE580 data

base.

7.2

Conclusion

The inspector

concluded that licensee

procedures

were acceptable

to properly

enter

new changes

in the

EE580 data

base

and resolve

any differences

between

field conditions

and the

EE580 data

base prior to making any design

modifications.

r

~ >

,I

t

-20-

The inspector

concluded that the licensee's

decision to suspend

actions to

locate the

714 missing

EE580 installation cards did not constitute

a failure

of the licensee

to perform the committed actions

associated

with the

EE580

data

base.

The inspector

concluded that the licensee's

review of cable installations

was

adequate

to ensure

that safety-related

cable routing information was correct

and that the licensee's

stated

action to sight installations involving the

missing

179 safety-related

EE580 cards

was adequate.

PI

1

Persons

Contacted

ATTACHMENT

1. 1

Arizona Public Service

Com an

R. Adney, Plant Manager,

Unit 3

  • J. Bailey, Vice President,

Nuclear Engineering

& Projects

L. Clyde, Operations

Manager,

Unit 3

  • P. Crawley, Director, Nuclear Fuels

Management

E. Dutton, Supervisor,

guality Control, Unit 2

A. Fakhar,

Manager,

Site Mechanical

Engineering

  • R. Flood, Plant Manager,

Unit

2

  • D. Garchow, Director, Site Technical

Support

  • B. Grabo,

Section

Leader Compliance,

Nuclear Regulatory Affairs

  • T. Gray, Supervisor,

Radiation Engineering

  • W. Ide, Plant Manager,

Unit

1

H. Kerwin, Maintenance

Manager,

Unit 3

  • A. Krainik, Manager,

Nuclear Regulatory Affairs

  • D. Larkin, Senior Engineer,

Nuclear Regulatory Affairs

  • J. Levine, Vice President,

Nucle'ar Production

  • 0, Hauldin, Director, Site Maintenance

and Modifications

  • G. Overbeck,

Assistant to Vice President,

Nuclear Projects

F. Riedel, Operations

Manager,

Unit

1

  • C, Russo,

Department

Leader,

Nuclear Assurance,

Maintenance

  • J. Scott, Assistant

Plant Manager,

Unit 3

C.

Seaman,

Director, Nuclear Assurance

G. Shanker,

Department

Leader,

Nuclear Assurance,

Engineering

  • W. Simko, Department

Leader,

Nuclear Assurance,

Strategic Analysis

E. Simpson,

Vice President,

Nuclear

Support

J, Velotta, Director, Training

P. Wiley, Operations

Manager,

Unit 2

1.2

NRC Personnel

  • K. Johnston,

Senior Resident

Inspector

  • H. Freeman,

Resident

Inspector

  • J. Kramer,

Resident

Inspector

  • A. HacDougall,

Resident

Inspector

1.3

Others

.

  • F. Gowers,

Site Representative,

El

Paso Electric

  • Denotes

personnel

in attendance

at the exit meeting held with the

NRC

resident

inspectors

on July 27,

1994.

2

EXIT MEETING

An exit meeting

was conducted

on July 27,

1994.

During this meeting,

the

inspectors

summarized

the

scope

and findings of the report.

The licensee

)

I t

f

'I>

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or reviewed by,

the inspectors.

'I

I

~ '

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I

,fi'l