ML17305B468

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Insp Repts 50-528/90-54,50-529/90-54 & 50-530/90-54 on 901202-910105.Violations Noted.Major Areas Inspected:Plant Activities,Monthly Surveillance Testing,Monthly Plant Maint & Inadvertent Dilution of RCS Boron Concentration
ML17305B468
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 02/15/1991
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17305B466 List:
References
50-528-90-54, 50-529-90-54, 50-530-90-54, NUDOCS 9104220083
Download: ML17305B468 (40)


See also: IR 05000528/1990054

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Re ort Nos.

Docket Nos.

License

Nos.

Licensee:

~Fi1it

II

50-528/90-54,

50-529/90-54

and 50-530/90-54

50-528,

50-529,

50-530

NPF-41,

NPF-51,

NPF-74

Arizona Public Service

Company

P.

0.

Box 53999, Station

9012

Phoenix,

AZ 85072-3999

Palo Verde Nuclear Generating Station

Units 1, 2&3

>is 0/

Approved By:

a

e

sgne

Ins ection

Summar

Ins ection

on December

2

1990 throu

h Januar

5

1991

(Re ort

um ers

-

-

-

-

an

Ins ection Conducted:

December

2,

1990 through January

5, 1991

Inspectors:

D.

Coe,

Senior Resident

Inspector

F. Ringwald,

Resident

Inspector

J.

Sloan,

Resident

Inspector

ong,

ie

Reactor Projects

Branch,Section II

Areas

Ins ected:

Routine, onsite,

regular

and backshift inspection

by

e

ree resl ent inspectors.

Areas inspected

included: previously

identified items; review of plant activities; monthly surveillance

testing; monthly plant maintenance;

inadvertent dilution of reactor

coolant system boron concentration - Unit 1; diesel

generator operability

- Unit 1; turbine driven auxiliary feedwater

(AFM) pump oil levels-

Units 1 and

3,; closure of one of four main steam isolation valves

(MSIV)

while at 100 percent

power - Unit 2; use of improper fuses in

safety-related

applications - Units 1, 2, and 3; and review of licensee

event reports - Units 1, 2,

and 3.

During this inspection the following Inspection

Procedures

were utilized:

61726,

62703,

71707,

92700,

92701,

92702,

and 93702.

Results:

Of the 10 areas

inspected,

1 violation was identified in

Unit 1.

The violation pertained to a licensee-identified

inadequate

procedure to place

a

new letdown ion exchanger

resin

bed into service.

91042"OOS.:

51021g

F'DR

ADOCK 00005:28

n

PDR

General

Conclusions

and

S ecific Findin

s

Si nificant Safet

Matters:

Summar

of Violations:

Summar

of Deviations:

0 en Items

Summar

None

1 Violation (Unit 1) regarding

an inadequate

procedure

None

14 items closed,

1 item left open,

and

3 new items opened.

DETAILS

1.

Persons

Contacted:

The below listed technical

and supervisory personnel

were among

those contacted:

Arizona Nuclear

Power Pro'ect

(ANPP)

"R. Adney,

"J. Bailey,

"T. Bradish,

"E. Dotson,

".R. Flood,

"R. Fullmer,

"D. Gouge,

"S. Guthrie,

~K. Hall,

"R. Henry,

P.

Hughes,

"M. Ide,

F. Larkin,

"J. Levine,

"J. Minnicks,

"G. Overbeck,

~R. Rogalski,

"J. Scott,

"S. Terrigino,

Plant Manager,

Unit 3-

Yice President,

Nuclear Safety

8 Licensing

Compliance,

Manager

Engineeri,ng

8 Construction,

Site Director

Plant Manager,

Unit 2

gA and Monitoring, Manager

Plant Support,

Manager

(Ch. Plant Review Bd.)

~

~

~

~

~

A, Dep. Director '

Paso Electric Co., Site Representative

Salt River Project, Site Representative

Site

Rad.

Protection,

General

Manager.

Plant Manager,

Unit 1

Security,

Manager

Yice President,

Nuclear

Power Production

Maintenance

Manager,

Unit 3

Technical

Support, Director

gA, Supervisor

Operations

Manager,

Unit 1

Management

Services,

Supervisor

The inspectors

also talked with other licensee

and contractor

personnel

during the course of the inspection.

"Attended the Exit meeting held with NRC Resident

Inspectors

on

January

8, 1991.

2. ~P'

Id

iit

d it

Il it

1

2

d 1 292701

d 927027

a.

Unit 1:

1.

(Closed)

Enforcement

Item (528/89-56-02):

"Motor 0 crated

702)

This violation consisted of two examples in which the

MOY

database

document,

13J-ZZI-004,

was found to be inappropriate.

The first example

concerned

a technician

who selected -incorrect

switch settings

from 13J-ZZI-004, apparehtly

due to confusion"

resulting from 34 Drawing Change Notices

(DCNs) which had not

been incorporated.

The licensee

has since determined that the

values selected

were actually correct

and that none of the

outstanding

DCNs were applicable to the valve in question.

However, the licensee

recognized that confusion could result in

errors

and has

developed unit-specific database

documents

and

0

2.

has

implemented administrative controls to keep them more

current.

The inspector

reviewed these

documents

(1J-ZZI-004, 2J-ZZI-004,

and 3J-ZZI-004) and found them to be updated in accordance

with

the administrative controls.

, The administrative controls

require future

DCNs related to implemented

changes

to be

incorporated

such that none is over six months old and

no more

than five of these

implemented

change

DCNs exists at a time.

These actions

appear

adequate.

The second

example

concerned

the lack of review and approval

documentation to support the calculations for the setpoints

in

13J-ZZI-004.

The licensee

stated that the calculations

and

appropriate

review. and approval

documentation

does exist.

The

inspector

reviewed the documentation

supporting the 13J-ZZI-004

setpoints for the following ten safety-related

valves:

1J-AFC-HV0033

1J-SIA-HV0698

1J-SIA-HV0666

1J-SIB-HV0676

1J-SIA-HV0684

1J-SPA-HV0049B

1J- EWA-UV0145

1J-AFA-HV0054

.

3J-SIB-HY0689

2J-CHB-HV0530

While the information was not readily available or well

organized,

the licensee

was able to produce the required

documentation,

including review and approvals,

for the opening

and closing thrust minimum and

maximum values for all these

valves,

as appropriate

(some valves

open

and close

based

on

limit switch position and

do not have thrust values in the

database).

.Procedure

73PR-9ZZ04,

"Valve Motor Operator

Monitoring and Test Program," specifies

the defau]t settings

'nd methodology for determining limit switch settings.

The

limit switch settings

appeared

consistent. with this procedure.

The licensee is taking steps to better organize the

calculations

which preceded

the Generic Letter 89-10 program.

The inspector

also noted that several of the calculations

have

been

superseded

by new calculations resulting from the partial

implementation of the Generic Letter 89-10 program.

These

.

'ctions

appear

adequate.

This item is closed.

(Closed)

Enforcement

Item (528/89-56-10):

"Inade uate

orrec

>ve

c ions

or

ar

o

1 ica ion on

hami or ue

o or

nsu

a ion an

ec naca

anua

e scienc

"

nl

This violation was presented

in two examples of 'inadequate

corrective actions,

the first dealing with a 10 CFR Part 21

I

Notification and the second dealing with the response

to

Information Notice 85-22.

The licensee

disagreed that the first example represented

a

violation because

the facts presented,

while accurate,

do not

constitute

a violation of regulatory requirements.

The

violation concerned failure of the licensee to address

both

Type

SMB and Type

SB Limitorque operators

in its evaluation,

even though the

10 CFR Part 21 notification had only specified

Type

SMB operators

as having the potential

problem.

The

inspector

reviewed Engineering Action Requests

(EARs) 89-0448

and 89-0449,

and Engineering Evaluation Request

{EER)

88-XE-015,

and conf)rmed that, consistent with the licensee's

response,

EER 88-XE-015 addressed

the 10 CFR Part 21

Notification applicability to both Type

SMB and Type

SB

Limitorque operators.

The inspector

concluded that the

licensee's

r'esponse

to the violation was accurate

and that this

example

does not constitute

a violation.

The second

example resulted

from a technical

manual

not being

updated following the licensee's

response

to Information Not>ce

85-22.

The licensee

determined that technical

manual

J605-162

was the only manual

not updated.

This manual

has subsequently

been

updated

and issued.

Additionally, the licensee's

Vendor

'Technical

Manual project,

expected to be complete

by

December

31, 1993, appears to include in its scope

the types of.

deficiencies identified in this and other findings related to

technical

manuals.

These corrective actions

appear

to be

adequate.

This item is closed.

(Closed)

Followu

Item (528/90-03-02):

"Load Shed Potential

rans

ormer

al ure

-

ns

This item involved a load shed of a 13.8KV bus,

NAN-S02, due to

a failure of the potential transformer across

the "8" to "C"

phase of the bus.

A similar failure occurred

on the

NAN-S01

bus "A" to "B" potential transformer shortly before this event.

The licensee

conducted

a root cause of failure via Engineering

Evaluation Request

{EER) 90-NA-002.

The cause of failure was

determined

by Genera'l Electric to be internal turn-to-turn

=-

shorting of unknown origin.

An APS Nuclear Engineering fai'lure

rate analysis

concluded that the mean failure rate for this

type device is 6. 14E-7 which is close to the industry failure

rates

represented

by the

IEEE Reliability Data.

The inspector

concluded that these

results- appear

appropriate.=-

This item is

closed.

'0

en) Foll owu

Item (528/90-03-03):

"Fuel Buildin

Rollu

Door

ama

e

en

s

a ion

am er

um er

ns

a

a son

-

ns

This event involved damage to the Fuel Building rollup door as

a result of improper control of the insta11ation of pneumatic

jumpers.

Engineering Evaluation

Request

(EER) 90-ZF-009 was

initiated as

a result of this event.

EER 90-ZF-009 is still

open.

This item will remain

open until

EER 90-ZF-009 is closed

and reviewed by the inspector.

Closed)

Followu

Item

528/90-23-02

"Review of Historicall

al ve

revents ve

as n enance

as

s

-

n)

This item involved a review of the licensee

commitment to

ensure that there are

no

PM tasks which had been waived which

could affect safe plant operation.

A significant number of PN

review forms- were found to contain inadequate

documentation for

the conclusion

reached.

The licensee

committed to repeating

the review, identifying those which were inadequately

documented,

and providing adequate

documentation

where needed.

In addition, the licensee

committed to notifying the inspector

of any additional

concerns

or

PM requirements

identified during

this re-review.

No additional

concerns

were identified by the

licensee.

The licensee

completed the re-review as committed.

The inspector

reviewed about

lOX of the approximately

2000

PM

task review sheets

and

had

no concerns with the additional

documentation.

This item is closed.

(Closed)

Enforcement

Item (528/90-23-03):

"Im ro er

erat>on

o

an

tmos

er>c

um

a ve

>n

anual"-

n>t

This item involved the failure to correctly follow a procedure

which resulted in the manual mis-operation of ADV SGB-HV-178,

while under the supervision of a more experienced

Auxiliary

Operator

(AO) and

a licensed'Senior

Reactor Operator

(SRO).

The licensee's

System Engineer evaluated

the mis-operation

and

concluded that

no damage

had occurred.

The licensee

sampled

the knowledge

and abi 1>ty of several

AOs at all three units and

determined that the

AOs knew how to properly operate

the

ADYs

manually and this issue

was not a training concern.

A Human

Performance

Evaluation System report was completed which

concluded that:

(1) inadequate

work practices

caused

the

event,

(2) the newly qualified

AO was under stress

due to the

presence

of the

NRC Inspector,

(3) having two actions

combined

into one step

was

a contributing factor to the mis-operation of

the

ADV, and (4) a thumbscrew would eliminate the

need for the

AO to use

a tool which could be dropped - not a contributing

factor, but identified during the investigation.

The licensee

counseled

and reexamined

the

AO who mis-operated

the

ADV and

verified that this task could be properly performed.

In

addition, Instruction Change

Request

(ICR) 11033

was written to

have the tightening of the setscrew

made

a separate

step in

procedure

4XOP-XOPOl, "Manual Operation of Air Operated

Valves," and

a plant change

request

was issued to replace the

setscrews

with thumbscrews.

This item is closed.

5

7.

(Closed)

Followu

Item (528/90-23-04):

"0 eratin

Procedures

evsew

or

n

e en

en

eri

sca

son

e usrements

-

nit

This item was associated

with Enforcement

Item 528/89-16-03,

which was closed in Inspection Report'28/90-23.

The

enforcement

item was closed

by evaluating the licensee's

commitment to review operating procedures "...for human factors

considerations,

locked valve and breaker

requirements,

and the

new independent verification requirements."

The inspector

noted that this procedure

review initiative went well beyond

the scope of the violation.

However, the January

2, 1996,

scheduled

completion date

seemed

not to be timely, particularly

with respect to independent verification requirements.

In

addition,

Enforcement

Item 530/89-56-01

noted further

independent verification weaknesses

and is reviewed in

Paragraph

2. C. l. of this report.

This Notice of Violation

included

a commitment to revise "...applicable Operations

. procedures

to include sign off steps to document

independent

verification" by September

2, 1991.

This action will be more

timely and will also address

the independent verification

questions

associated

with this Followup Item.

This item is

closed.

8.

9.

I

(Closed)

Followu

Item (528/90-39-02):

"Technical

Su

ort

701)

en er

a ter)es

o

ar

e

ro er

-

nl

The inspector

noted specific gravity problems with the

TSC

diesel

generator batteries that were noted but not addressed

in

Employee

Concerns File 89-104-12.

Based

on the inspector's

questions,

the licensee

then supplemented

the existing file to

address

these

comments.

The supplement reflected

an expanded

look at

TSC battery preventive

maintenance

(PM) tasks.

This

expanded

look resulted in guality Deficiency Report ((DR)

(Closed)

Followu

Item (528/90-28-02):

"Dama ed Reactor

r>

rea er

-

nl

This item involved the unexpected

operating characteristics

and

subsequent

damage to a reactor trip breaker while racking it in

and out.

The Root Cause of Failure Engineering Evaluation

Request

(EER) 90-SB-046

was completed

on December

21, 1990.

This

EER concluded that

a slightly bent or misaligned closing

spring discharge

linkage was the most likely root cause of

failure.

Secondary

damage

during removal

hampered

a complete

understanding

of the root cause of failure.

Corrective action

included replacing the breaker,

routing this

EER to Training

for all Operations

Department personnel,

and the issuance

of

Instruction Change

Request

25254 to eliminate unnecessary

breaker racking operations.

The training on

EER 90-SB-046 will

.be for people

who rack breakers

to be alert for any abnormal,

off-normal or unusual

condition and to determine

the cause'f

the anomalous

condition before proceeding.

This item is

closed.

90-0440 which documented

a negative trend in the performance of

PM tasks

on these batteries,

which are non-safety related.

Problems

noted included personnel

not identifying, documenting,

or reporting problems,

and makin~ administrative

and

calculation errors while performing

PH tasks

on TSC batteries.

In addition,

examples

were noted in which Work Group

Supervisors

signed

PH task work orders

as satisfactory

when the

acceptance

criteria had not been met, failed to note the

administrative

and calculation errors noted above, failed to

initiate appropriate corrective action documentation,

and

signed

a

PH work order as complete

and satisfactory

two days

prior to the dates of the actual

work.

In addition, this

supplement identified problems in which the Central Haintenance

Electrical

Work Control Planner/Coordinator

misunderstood

information on the Station Information Management

System

(SIMS)

terminal display and

made errors

due to inattention to detail.

The inspector

reviewed

(DR 90-0440

and the associated

corrective actions.

The Central

Maintenance Electrical

Supervisor is conducting mandatory briefings for all Central

Maintenance electric

shop personnel

includ>ng Electricians,

Foremen

and Work Group Supervisors,

and Central

Maintenance

Electrical

Work Control Planner/Coordinators

addressing

the

concerns

noted above.

The inspector

concluded that this

corrective action appears

appropriate.

This item is closed.

Unit 2

(Closed)

Followu

Item (529/90-23-01):

"Inadvertent Tri

of the

eac

o

oo an

um

rea er

-

ns

This item involved the tripping of a second

Reactor Coolant

Pump

(RCP) breaker in a three month period due to jarring of an

adjacent

breaker cubicle while manually rolling the adjacent

breaker into its cubicle.

Engineering Evaluation

Request

(EER)

90-NA-009, which was issued

as

a result of the first event,

was

closed without additional corrective action recommendations.

The Site Maintenance

Manager

and Maintenance

Standards

Manager

discussed their intent to devise

a tool to use to move these

breakers

into their cubicles with the inspector.

During the

Unit 1 Surveillance Testing Outage

due to. begin

on January .12,

1990, Central

Haintenance

plans to remove

a breaker to

take'easurements,

then devise

and fit up and finalize the design of

the tool.

No permanent

changes will be made to plant

equipment.

The inspector

concluded that this represents

a.

positive step toward providing improved control of these

breakers.

This item is closed.

(Closed)

Followu

Item (529/90-28-01:

"Inade uate Detail

s n

urves

ance

roce ure

-

ns t

This item addresses

the "Main Steam

PSV Set Pressure

Verification" procedure,

73ST-9ZZ18, which contained

no steps

detailing the proper connection of test equipment or

performance of the test,

using the Trevitest method.

The

0

C.

2.

inspector

reviewed Revision 4, Procedure

Change Notice

2 of

procedure

73ST-9ZZ18, which was effective

on November

6, 1990.

Sufficient detail

was

added to the procedure to ensure

the test

device

was properly installed

and the test properly performed..

Based

on this review, this item is closed.

Unit 3

(Closed

Enforcement

Item

530/89-56-01):

"Failure to Follow

urves

ance

roce ure

-

n)

This item involved the failure to close valve SIA-UV-603 at

step 8.2. 12 while performing surveillance test procedure

43ST-3SI06,

"Iodine Removal

System - S.C.A.P.

Discharge

Flow

and Pressure

Test."

-The licensee

restored

the valve lineup,

counselled

the operator involved and issued

a night order

addressing

the issue to all operators.

The procedure

was

revised to include

an independent verification signoff;

The

licensee further committed to reviewing all Operations

procedures

to include signoff steps to document

independent-

verification by September

2, 1991.

The licensee

has also

conducted training for all operators

on the

new independent

verification requirements.

This item is closed.

(Closed)

Enforcement

Item

530/89-56-05):

"Im ro er Atmos heric

um

a ve

ac in

-

nest

This item involved the improper packing of valve

3J-SGB-HF-0178.

The licensee

reviewed this event in Human

Performance

Evaluation System

Report 89-038 which concluded

that there

was inadequate

self-checking

on the part of the

mechanics

and

an inadequate

program to control valve packing.

The

HPES report noted the development of a new valve packing

program and concluded that it should prevent recurrence

of the

use of valve packing which did,not meet the valve

manufacturer's

specifications.

The inspector

reviewed this program and noted that it is

described in program procedure

73PR-9ZZ05,

"PVNGS Valve Packing

Program,"

and implemented in procedure

31DP-9MP02,

"Valve Stem

Packing

and Gland Adjustment,'n the

new valve packing

specification

13-PN-220,

and the valve packing drawings

OX-P-ZZG-019 and OX-J-ZZI-005 where

X is the unit number.

According to the licensee,

specification

13-PN-220

was based.

heavily on EPRI Report NP-5697,

"Valve Stem Packing

, Improvements,"

which recommended flexible graphite packing,

and

Equipment

Change Evaluation

ECE-ZZ-A158, which justified the

use of graphite valve packing material at Palo Verde Nuclear

Generating Station.

The inspector noted two weaknesses

in the program.

The first

weakness,

in procedure

73PR-9ZZ05,

"PVNGS Valve Packing

Program," is that in the list of responsibilities

of Component

and Specialty Engineering

(C8SE), the program

does not require

P

3.

C8SE to review the Valve Survey and Data Sheets

(VSDS) for

technical

appropriateness

prior to forwarding them to Nuclear

Engineering for incorporation into the valve packing drawings.

The Manager,

C&SE, committed to having procedure

73PR-9ZZ05

revised to state this technical

review as

a responsibility of

C8SE.

The second

weakness

was that the Unit 1 valve packing

drawings were not issued

and

no schedule existed for the

issuance

of these

drawings.

The Manager,

CESE,

committed to

having these

drawings issued during the three

month period

following the end of the present Unit 1 surveillance test

outage.

The inspector

noted that the valve packing procedures

have only been issued for Unit 3 and are scheduled

to be issued

for Unit 2 February 28,

1991.

The inspector

concluded that the

corrective actions taken

as

a result of this violation appear

adequate

and that the

new valve packing program represents

an

improvement.

This item is closed.

(Closed)

Enforcement

Item (530/89-56-06):

"Failure to Identif

e

orrec

ann enance

om onen

-

ns

This item involved the installation of parts

from containment

purge exhaust valve 3J-CPA-UV-02B on containment

purge supply

valve 3J-CPB-UV-03A with a Quality Control

(QC) holdpoint

verification signoff.

The licensee

responded

by counselling

the individuals involved, performing

a Human Performance

Evaluation

System

(HPES) evaluation,

and c'onducting training on

"Effective Work Practices" for all site maintenance

personnel.

According to the Manager of Quality Control,

QC Inspectors

were

not requ>red to attend "Effective Work Practices" training,

however

a number of them did attend.

QC revised their Plant

Inspection

Report document to require

QC verification of

component identification and

QC personnel

were briefed on the

new form and on this event.

The

HPES report concluded that

inadequate

verbal

communication

and inadequate written

communication contributed to the event.

Corrective action

included reviewing the

HPES report with all affected work

groups,

conducting the "Effective Work Practices" training,

and

issuing Instruction

Change

Request

(ICR) 18899 to evaluate

the

use of accurate

descriptions

in work orders.

This item is

closed.

3.

Review of Plant Activities (71707 and 93702

a.

Umt 1

Unit 1 remained at essentially

100 percent

power throughout

this reporting period,

except for a downpower to 75 percent

on

December 17, 1990,

due to a Core Operating Limits Supervisory"

System

(COLSS) failure.

The unit was restored to full power

the

same

day.

b.

Unit 2

Unit 2 remained at essentially

100 percent

power throughout

this reporting period except for an HSIV closure event

on

December

21,

1990', which resulted in a forced power reduction

to approximately

65 percent for several

hours

(see paragraph

9).

c.

Unit 3

Unit 3 operated at approximately

100 percent

power throughout

this report period with the exception of a downpower to

40 percent

from December 25, to December 27,

1990, to locate

and repair a condenser

tube leak.

d.

Plant Tours

The following plant areas

at Units 1,

2 and

3 were toured by

the inspector during the inspection:

Auxi'liary Building

Control

Complex Building

Diesel Generator Building

Radwaste Building

Technical

Support Center

Turbine Bui1ding

Yard Area and Perimeter

The following areas

were observed

during the tours:

1.

0 eratin

Lo s and Records - Records

were reviewed against

ec nica

peci ica sons

and administrative control

procedure

requirements.

2.

Monitorin

instrumentation - Process

instruments

were

o serve

or corre

a ion

etween

channels

and for

conformance with Technical Specifications

requirements.

3.

Shift Staffin - Control

room and shift staffing were

o serve

or conformance with 10 CFR'art 50.54.(k),

Technical Specifications,

and administrative procedur'es.

5.

E ui ment Lineu

s - Various valves

and electrical breakers

were veri ie

o be in the position or condition required

by Technical Specifications

and administrative procedures

for the applicable plant mode.

E ui ment Ta

in - Selected

equipment, for which tagging

requests

a

een initiated,

was observed to verify that

tags

were in place

and the equipment

was in the condition

specified.

6.

General

Plant

E ui ment Conditions - Plant equipment

was

o serve

or in ica ions

o

sys

em leakage,

improper

~

'

10

lubrication, or other conditions that would prevent the

systems

from fulfillingtheir functional requirements.

The inspector

noted that

a bolt was missing from the

casing

on the Unit 1 Essential

Cooling Water "B" pump

coupling.

The licensee -.initiated Haterial

Non-Conformance

Report

(MNCR) 90-EW-Oll to address

the deficiency and the

bolt was replaced.

Fire Protection - Fire fighting equipment

and controls

g

dgg

dd

Specifications

and administrative procedures.

Plant Chemistr

- Chemical analysis results

were reviewed

or con ormance with Technical Specifications

and

administrative control procedures.

Securi t

- Activities observed for conformance with

regu

a ory requirements,

implementation of the site

security plan,

and administrative

procedures

included

vehicle and personnel

access,

and protected

and vital area

integrity.

Plant Housekee

in

- Plant conditions

and

mater>a

equipment storage

were observed to determine

the

general

state of cleanliness

and housekeeping.

Radiation Protection Controls - Areas observed

included

con ro

porn

opera Ion, records of licensee's

surveys

within the Radiological Controlled Areas

(RCA), posting of

radiation

and high radiation areas,

compliance with

Radiation Exposure

Permits

(REP), personnel

monitoring

devices

being properly worn, and personnel

frisking

practices.

material

Control - Warehouse

and material receipt,

g,

g

d

dddd

d

d.

The inspector discussed

the recent

implementation of--

Level I certified gC inspectors for material receiving

inspections with several

warehouse

personnel,

including

supervision

and Level I and II certified inspectors.

The

inspector

noted that although four warehousemen

were given

Level II training in October 1990, the licensee

implemented

a change to their receipt process

which only

required these

personnel

to be qualified to the lesser

Level I standard

(ANSI N45.2d 6).

Based

on discussions

with two of the four recently certified Level I

inspectors,

and

a review of training and certification

records,

the inspector determined that the change to the

licensee's

receipt inspection process

was being controlled

by procedure,

that the procedure

provided for specific

attributes for Level I receipt inspection, that this level

of inspection

was consistent with the level of

certification given to the Level I inspectors,

and that

previously all receipt inspections

for quality related

material

were performed completely by Level II certified

inspectors

even though non-certified warehousemen

also

routinely performed

some of the checks which would be

normally done by Level I inspectors.

Licensee

personnel

stated that receipt inspections

were

now more efficient in

taking credit for the Level I inspector's

checks,

freeing

the Level II inspector

to inspect higher level attributes.

Based

on these discussions,

the inspector

concluded that.

NSI N45.2.6 requirements

relative to receipt inspector

qualification and activities were being governed

by

approved

licensee

procedures.

No violations of NRC requirements

or deviations

were identified.

4.

Monthl

Surveillance Testin

- Units 1

2 and

3 {61726)

a.

Selected

surveillance tests

required to be performed by the

Technical Specifications

(TS) were reviewed

on a sampling basis

to verify that:

1) the surveillance tests

were correctly

included

on the facility schedule;

2)

a technically adequate

procedure

existed for perfoi mance of the surveillance tests;

3)

the surveillance tests

had been performed at the frequency

specified in the TS;

and 4) test results satisfied

acceptance

criteria or were properly dispositioned.

b.

Specifically, portions of the following surveillances

were

observed

by the inspector during this inspection period:

Unit 1

~voce

ure

Descri tion

o 31ST-9DG01

o 32ST-9PE01

o 32ST-9ZZ03

Unit 2

Hone

Diesel

Engine

18 Month Inspection

18 Month Surveillance Test of Diesel Generator

Surveillance Test Procedures

for the Class

4160

Bus,Under Voltage Protective

Relays

Unit 3

~roce

ure

Descri tion

o 43ST-3ZZ16

Routine Surveillance Daily Midnight Logs

No violations of NRC requirements

or deviations

were identified.

5.

Monthl

Plant Maintenance ; Units 1

2 and

3

62703

'a.

During the inspection period, the inspector

observed

and

reviewed selected

documentation

associated

with maintenance

and

problem investigation activities listed below to verify

compliance with regulatory requirements,

compliance with

0

12

administrative

and maintenance

procedures,

required Quality

Assurance/Quality

Control involvement, proper use of safety

tags,

proper equipment alignment and

use of jumpers,

personnel

qualifications,

and proper retesting.

The inspector verified

that reportability for these activities was correct.

b.

Specifically, the inspector witnessed portions of the following

maintenance activities:

Unit 1

Descri tion

o

Inspection of Emergency Diesel Generator

Piping and Oil

Sample

Unit 2

Descri tion

o

Repair of "B" Emergency Diesel Generator Silencer

Unit 3

~D

o

"B" Emergency .Diesel Generator High'ibration Trip

Troubleshooting

No violations of NRC requirements

or deviations

were identified,

6.

Inadvertent Dilution of Reactor Coolant

S stem Boron Concentration

n>t

an

The details of this event are described in LER 50-528/90-11

and the

licensee's

Incident Investigation

Report (IIR) 2-1-90-004.

In

summary,

on December

6, 1990, with Unit 1 at lOOX power, the reactor

coolant system boron concentration was'iluted

by approximately

3 ppm

when

a new ion exchanger

was placed into service without adequate

boron saturation.

There were several

weaknesses

which were evident

during the event

and missed opportunities which could have prevented

or mitigated the dilution event:

a.

There

was inadequate

technical

basis for the 20 minutes

specified in the procedure for the flush of the ion exchanger

and

an informal process

was

used to communicate the criteria in

the development of the procedure.

b.

Operations'nitial

concern with the adequacy of the time

specified in the procedure for boron saturation of the ion,

exchanger prior to being placed in service

was not pursued to

conclusion.

Operations

discussion with chemistry personnel

were not adequate

to resolve the concern.

0

13

c,

The decision to concurrently perform high rate

blowdowns of the

steam generators

also raised reactor

power in addition to the

dilution and caused

the Core Operating Limits Supervisory

System master

alarm to annunciate.

The operators

expected

the

alarm due to the high rate

blowdowns

and therefore

the alarm

did not alert the operators

to the dilution event.

d.

Computer technicians failed to coamunicate to the operators

the

inability of the control element

assemblies

to move in

sequential

control

mode which further complicated operator

response

to the dilution event.

The dilution occurred

from approximately I:53 a.m. to 2:49 a.m.

on

December

G. 'uring this time the steam generators

were being given

a series of two minute high rate blowdowns.

In combination with the

dilution effect, this caused

actual

reactor

power to exceed

100 percent for between

one to two hours

and exceed

101 percent for

between

14 to 26 minutes.

Although licensee calculations

show that

"best estimate"

thermal

power did not exceed

the safety analysis

upper limit of 102 percent,

the licensee

acknowledges

in the IIR and

LER that engineering calculations

which account for a11 worst case

uncertainties

can

be shown to result in peak power of nearly

104 percent.

The licensee

submitted the

10 CFR 50.73 report based

on having exceeded

licensed

thermal

power.

When the operators

attempted to drive CEAs into the core to limit the increased

reactor

power and

RCS temperature,

the

CEAs would not respond

in the manual

sequentia)

mode

due to the unrecognized

impact of a p')ant computer

system malfunction.

Operators

were able to control

CEAs in the

manual

group mode

and mitigate the transient.

The inspector reviewed the licensee's

IIR, LER, supporting

documents,

and noted the following:

The licensee

determined that

a dilution event in Mode I is bounded

by the faster

CEA withdrawal event which results in a reactor trip

on

VOPT or low Departure

From Nucleate Boiling Ratio

(DNBR), and no

fuel damage,

even

assuming

no operator action.

Maintenance of.

reactor

power below 102 percent

on

a steady state

basis

assures

consistency with safety analysis

assumptions.

Furthermore,

licensee

policy guidance to operators

allows for variations

above the

100 percent licensed

power, but held within the

102 percent limit,

based

on 1980

NRC guidance which suggests

100-102 percent

power is

"briefly" permissible "for as long as

15 minutes'," provided the

shiftly average of reactor

power remains at or below the licensed

(1GO percent) limit.

This guidance for shiftly average

power

appears

to have

been met in this case.

The licensee

review

acknowledges

the need to maintain tighter control over

RCS

parameters

during such evolutions

and management

counseled

the shift

supervisor

in this regard.

The inspector considered this action

appropriate.

The licensee's

review determined that computer technicians

were

aware of a computer malfunction which caused

de-energization

of

circuit cards in the plant computer

two days prior to this event.

The IIR did not acknowledge that these technicians

should

have been

able to provide operators

with enough information to alert them to

14

7.

the impact on

CEA Control:

This was demonstrated

by the

. technician

s ability to provide information to operators

in the

context of the plant indication and control which would be lost

whi,le restoring power to the cards.

In subsequent

discussions

with'he

inspector,

licensee

management

agreed to emphasize

to operators

and computer technicians

the need for thorough analysis of current

plant impact due to malfunctioning equipment.

Finally, the licensee

issued equality Deficiency Report

((OR)90-485

to correct the procedure

guidance for placinq

a

new resin

bed in

service

and for preventing recurrence of similar procedural

inadequacies.

The inspector

noted that the IIR did not delve into

the reasons

why the procedure

was deficient, relying instead

on the

(OR program to sufficiently resolve this issue.

The inspector

determined that the under lying cause

was that technical

information

regarding the length of time needed to.borate

a new resin

bed to

RCS

'oncentration

was communicated verbally from Chemistry Standards

to

the Operations

Standards

group writing a procedure

revision in May

1990.

Apparent misunderstanding

and lack of critical review of the

basis for this information contributed to its being approved in the

revision.

The response

to the (DR was to incorporate

the licensee's

existing Engineering Evaluation Request

(EER) program

as

a means of

documenting the transmittal

of technical

information between

Standards

groups.

Although this appears

to provide more formality,

the inspector

emphasized

to licensee

management

that such

documentation

must still.=be critically reviewed

and challenged

when

necessary

prior to its use in approved procedures.

A 'previous

example of a procedure deficiency due to misunderstood

engineering

input was recently discussed

in NRC Inspection

Report 528/90-46

(paragraph

9), but resulted in more conservative

requirements

than

were necessary.

The inspector

concluded that the failure to provide

a required procedure with appropriate criteria for determining the

satisfactory

accomplishment of this important activity is a

violation of 10 CFR Part 50, Appendix B, Criterion V

(50-528/90-54-03).

Diesel Generator

0 erabilit - Unit 1

61726

and 92700

Mhile observing performance of Surveillance Test 31ST-9OG01,

"18.

Month Diesel Generator Inspection,"

on the "B" Emergency Diesel-

'enerator

(EOG) on December

18, 1990, the inspector, noticed that the

opposite Train

EDG (Train "A") had

a "Diesel Inoperable/Malfunction"

local annunciator lighted.

The local annunciator for low lube oil

pressure

was also"lighted.

If these

alarms

were valid, the

EOG

.

would be inoperable.

The inspector determined that the

EOG "A" inoperable indication had

been first identified on December

15, 1990,

and that the Shift

Supervisor

(SS)

had evaluated

the problem and determined that it was

an annunciator

problem only and that the

EDG was operable.

This was

based

on the licensee's

verifications that none of the parameters

identified in the alarm response

procedure

were in a condition to

provide

a valid alarm, that

no control

room

EOG trouble alarm or

Safety Equipment Status

System

(SESS)

alarm was present,

and that

a

0!

~,

15

valid local annunciator

would result in the appropriate

control

room

alarms.

Additionally, the Assistant Shift Supervisor

telephoned

the

duty Instrumentation

and Controls (I8C) Technician

and explained the

observations.

The I8C Technician concurred with the conclusion that

EDG "A" was operable.

However,

no log entries

document the checks

which were

made to verify EDG

operability.'n

Monday,

December

17, 1990,

High Pressure

Safety Injection (HPSI)

Train "B'as taken out of service for planned

maintenance.

Later

that day, the Operations

Manager

became

aware of,the

EDG "A"

"Inoperable/Malfunction" annunciator

and directed that I8C confirm

that the condition was simply an annunciator circuit problem.

This

effort consisted of checking continuity across

the contacts

which

cause

the ahnunciator to be on.

The contacts

were determined to be

closed,

which should not cause

the alarm.

I8C concluded that the

annunciator circuit card was faulty.

However, the condition was not

corrected at that time.

Additionally, the

I&C Technician

used

an

uncontrolled diagram instead of controlled drawings while performing

this troubleshooting confirmation.

Licensee

management. stated that

their expectation

was that controlled drawings should

have

been

Used.

The Operations

Manager authorized the

SS to take the opposite Train

"B" EDG out of service

and declare it inoperable for 18 month

surveillance testing, providing the

SS

had

no operability questions

about the "A" EDG after the

I8C troubleshooting.

The "B 'DG was

thus

removed from service

on December

18, 1990.

The annunciator

circuit card on the "A" EDG was subsequently

replaced.

After detailed discussions

with the licensee's

engineering staff and

examination of the related logic prints, the inspector

agreed that

the

EDG "A" annunciator'problem

did not impact operability.

However,

up to this point, engineering

had not been involved in the

resolution of the problem,

and

no other attempt to confirm the scope

of the problem via the logic diagrams'had

been

made.

Procedure

40AC-90P02,

"Conduct of Shift Operations,"

states that

"when key decisions

are made,

the thought process for that decision

should

be logged, for reconstruction at

a later time."

The

determination that

EDG "A" was operable in spite of the

"inoperable/malfunction" annunciator, particularly prior to making

opposite train equipment inoperable for planned maintenance,

appears

to be

a "key" decision.

The inspector

concluded that adequate

information was

used

by the

SS

to verify EDG "A" operability, but that documentation

of this

verification was poor.

The licensee

concurred that this should. have

been

documented.

No violations of NRC requirements

or deviations

were identified.

16

Turbine Driven Auxiliar

Feedwater

(AFW) Pum

Oil Levels - Units 1

an

On December

28, 1990,

a Unit 1 Auxiliary Operator

(AO) reported that

the oil level in the turbine driven

AFW pump,

1AFA-P01, was 1/8 inch

higher than the upper limit mark on the s'ightglass.

A locally

mounted placard declares that oil level must be maintained

between

the marks

on the sightglass.

As a result of this finding, the

pump

was successfully

operated to ensure that the high oil level would

not prevent operation.

Subsequently,

the oil was changed

and level

restored to the normal

band.

A sample of the old oil was obtained,

analyzed,

and found to be normal.

On January 1, 1991, the oil level in lAFA-P01 was again observed to

be about 1/8 inch above the upper mark.

This oil was

sampled for

lab analysis

and about

12 ounces of oil were drained out to restore

the level.

The licensee initiated Engineering Evaluation Request

(EER) 91-AF-01 to determine

why the level

was too high.

On January 4, 1991, the inspector

checked the Units 2 and

3 turbine

driven

AFW pumps,

and found that the Unit 3 pump,

3AFA-P01,

had

an

oil level about 1/8 inch above the mark at the inboard bearing.

Level was about 1/4 inch above the mark at the outboard bearing

sightglass.

The Unit 3 shift supervisor

noted that the oil had been

changed

and

a routine oil sample

had been taken

a few days

previously.

He requested

maintenance

to drain the oil as necessary

to restore

the level.

The inspector

noted that the

AO logs

have

a different acceptance

criteria for oil level than what is provided by the placard.

The

logs

have

no limit on the maximum allowed level,

and the minimum

level allowed is "no visible level."

The normal level given is

50 percent,

though the sightglass

has

no numerical scale or

mid-point mark.

The licensee

submitted Instruction

Change

Request

(ICR) 15434 to correct this discrepancy.

The significance of marginally high oil levels

has not been

determined.

This item will remain

open until the inspector reviews

the results of the licensee's

evaluation of the cause

and

significance of high oil levels (Followup Item 528/90-54-01).

No violations of NRC requirements

or deviations

were identified.

Closure of One of Four Main Steam Isolation Valves

(MSIV

While at

ercen

ower -

n>

At approximately 5:45 AM, (MST) on December

21, 1990,

MSIV 170

unexpectedly

closed while the plant was operating at 100 percent

power.

This malfunction affected only one of two MSIVs associated

with the

No.

1 steam generator.

Operators

reduced plant power to

approximately

65 percent

and stabilized plant parameters.

Plant

response

to this event

was subsequently

determined

by the licensee

to be as expected,

with no significant abnormalities

noted.

Operator action was briefly required to operate

the

No.

1 steam

17

generator

feedwater control system in manual,

and an approximately

seven

degree difference in cold leg temperatures

between

steam

generators

created

a sufficient core azimuthal flux tilt (1.03) to

require changing the Core Protection Calculator

(CPC) AZTILT

parameter

in accordance

with the provisions of Technical

Specifications.

Additionally, the unaffected

steam line on the

No.

1 steam generator initially passed

excessive

steam flow and

over-ranged

the steam flow instrument

used to correct the steam

header

pressure

instrument which inputs to the Core Operating Limits

Supervisory

System

(COLSS) secondary calorimetric power calculation.

The steam flow instrument

came into range at power levels less than

70 percent

as expected.

The licensee

determined that the cause of MSIV closure

was

a failed

solenoid operated air valve (Skinner/Honeywell

Model V5-61090)

associated

with the Anchor/Darling MSIV.

Once plant conditions were

stabilized,

the air valve was replaced,

and the MSIY was opened

and

surveillance tested satisfactorily.

The licensee initiated a

root-cause-of-failure

analysis

on the failed valve (Engineering

Evaluation Request

90-SG-221).

The overall licensee

response

to this event appeared well

coordinated.

The

NSSS vendor was promptly consulted,

Nuclear Fuels

Management

department quickly provided

a simulation of plant

response

which helped confirm that the actual

response

was

as

'expected,

Reactor

Engineering coordinated on-site engineering

evaluation

and assessment,

and maintenance

and material

support were

efficient and effective in restoring the MSIV to service.

The

licensee

restored

the plant to normal operations

late that afternoon

and restored full power operation later that evening.

The licensee

also initiated an Incident Investigation to assess

the transient in

more detail.

The inspector

noted two areas

of apparent

weakness

in the licensee's

performance in response

to this event.

First, the licensee

based

the determination of satisfactory plant response

on the simu'1ation

which showed

a maximum seven

degree delta T-cold, operator

statements

that delta T-cold was not seen to be larger than seven

degrees,

engineering

judgement which extrapolated

a four degree

delta T-cold at 83 percent

power to a seven

degree delta T-cold at

100 percent" power,

a review of CPC functional requirements

of which

protection from this specific transient

was included,

a physical

check of CPC auxiliary trip setpoints

of fifteen degrees

delta

.

T-cold, and

NSSS vendor concurrence

with the above.

The inspector

noted that after the plant had been restored to normal operation but

prior to restoring full power operation,

available precise plant

parameter transient

response

(TDAS) data

was not accessed

and

reviewed.

Although the inspector considered

the licensee

had

sufficient basis to assure

the plant remained within its design

envelope

throughout the transient,

the

TDAS plots represented

the

most precise

data available to confirm actual plant response.

Licensee

management

agreed that this data could have further

contributed to confirmation of plant response.

18

Second,

the inspector questioned unit operations

management

during

the transient

on how the over-ranged

steam flow instrument affected

the calculations

performed

by COLSS.

Operations

management

at that

time could not confirm that

COLSS was impacted

by this over-ranged

instrument.

The operations staff or shift. had .not been

informed of

any impact and were not considering the possibility of any adverse

effect.

On further questioning,

the operators

and

a computer

technician

confirmed the use of this instrument

as

an input to

COLSS.

Subsequently

the licensee

informed the inspector that the

impact on

COLSS did not affect the validity of COLSS calculations.

The inspector stressed

the need for operators

to task supporting

groups

such

as engineering to provide such assessments.

Licensee

management

acknowledged

these

comments

and noted that consideration

was being given to creating additional reference

documents

to assist

operators

in assessing

the impact of various sensor or instrument

failures.

Additionally, development of an operations

procedure

was

initiated to provide specific guidance to operators for this event.

No violations of NRC requirements

or deviations

were identified.

Use Of Im ro er Fuses

In Safet -Related

A

lications - Units 1

2

an

The inspector

reviewed

an issue previously identified by the

licensee

related to the possible

use of incorrect fuses in Beta

Products

equipment.

The inspector

reviewed Reportability Evaluation Report

(RER) 89-03,

which determined that these

problems did not warrant

a 10 CFR Part 21 report.

The corrective action section did, however, indicate the

need for an evaluation of other Beta supplied fused equipment to

determine if this problem existed in other equipment.

This

evaluation

was to be documented

in Engineering Action Request

(EAR)

89-0831.

The inspector concluded that the

RER appeared

appropriate.

The inspector

reviewed

EAR 89-0831

and found that it was still open.

The

EAR was initiated on May 10,

1989 with the Nuclear Engineering

Department responsible for this

EAR.

Unit 3 inspections

were

completed

by August 1989,

however,

due to personnel

changes,

the

Nuclear Engineering

Department

was

unaware of this status

until;"=

January

1991.

The status of the inspections

and individual

responsibility for the

EAR had not been

communicated until

questioned

by the

NRC inspectors

in December

1990.

The

NED

supervisor responsible for the completion of this

EAR indicated=that

it had routine priority and that it would be completed after.

completing higher priority work.

The inspector

concluded that in

this case,

the

EAR prioritization process

was weak, in that after

..

one year there

was

no planned completion date.

The inspector-

further concluded that in this case

communications

were ineffective

in transmitting requested

data from the field to NED.

The inspector reviewed Work Orders

393611,

393528,

400054,

and

429555,

which covered all the units.

These work orders

were issued

to perform these

fuse inspections

in various safety

and non-safety

19

cabinets.

The inspector

noted that the form used to collect the

data in Unit 2 had

a pen and ink column added to document

independent verification of the reinstallation of the fuses.

In the

work orders for Unit 3, the data form had pre-printed

columns which.

duplicated the independent verification pen-and-ink

columns

used at

Unit 2.

Unit 1 used

a determ/reterm

sheet:

The inspector

noted

that Procedure

30DP-OAPOl, "Maintenance Instruction Writer's Guide",

states

in Section 3.2.4

on page ll of 44 that "The removal

and

reinstallation of the

same

component shall

be documented

on

a

component removal/reinstallation

form ... or controlled by the work

instruction."

While the

use of a column on a form or a

determ/reterm

sheet is not explicitly in accordance

with the

requirements

of 30DP-OAP01, its use provided the

same

independent

verification of that required

by the component

removal

form.

The

inspector

concluded that this was

a minor difference.

In addition, the inspector

noted that the work order entry for Work

guality Related

("WK gR") was listed

as

no ("N") on the cover page

of the work orders for each unit, yet the work orders

received the

technical

and quality reviews normally associated

with guality Class

work orders.

The reason for this is that

some of the fuses being

inspected

were g-Class

and

some were not,

and this had been marked

"N" in error.

The work order received

a technical

and quality

review despite the incorrect flag in the

"WK gR" field.

The

inspector concluded that except

as

noted above,

the work orders

appeared

appropriate for the planned task with adequate

detail

and

references.

Work order 393611 for Unit 1 had not been completed.

According to

notes in the work order and discussion with personnel

from Work

Control

including the Planner

Coordinator, this work stopped

when

a

g-Class

fuse for the annunciator circuit for a Class

1E circuit was

broken in May 1990.

These discussions

also indicated that this fuse

only had

a Beta Products part number which they could not cross

reference

to any other fuse.

In addition, other higher priority

work delayed the procurement of the replacement

fuse.

By June

14,

1990 the Planner

Coordinator initiated a request to Materials for a

replacement

fuse.

Purchase

Request

9535389

was written on August 2,

1990.

The Station Information Management

System indicates that the

lead time for procuring this fuse after a purchase

order is issued

is 37 weeks.

According to the Planner Coordinator,

as of January

7,

1991

a Purchase

Order had not been issued.

This broken fuse

had

no

impact on the affected equipment

because it was in a redundant

power

supply.

The inspector discussed availability of g-Class

fuses with

an

18C Foreman,

the

18C System Engineer for these

systems,

the

NED

I8C Engineer for these

systems,

and with a Procurement

Engineering

representative.

None of these

discussions

identified any unusual

difficulties in obtaining g-Class

fuses.

The'inspector

also

discussed this with the Planner Coordinator who said that there

had

been difficulty obtaining fuses in some situations

and that in this

case there

was

a class

and item number but no stock for the fuse in

the warehouse.

The inspector

concluded that low priority resulted

in the lengthy delay in obtaining the replacement

fuse.

'

20

The inspector

concluded that inadequate

ownership of this issue

appears

to have delayed the completion of corrective action.

The

licensee initiated Problem Resolution Sheet

1613 to evaluate

the

significance of the concerns

raised regarding this

EAR and any

possible

broader implications.

The inspector will review the

results of this investigation

when the

PRS is closed (Followup Item

528/90-54-02).

ll.

Review of Licensee

Event

Re orts - Units 1

2 and

3 (90712

an

The following LER was reviewed by the Resident

Inspectors.

Unit 1

528/90-ll-LO (Closed

"Reactor Thermal

Power License Limit

xcee

e

.

-

n)

This event is described

and reviewed in paraqraph

7 of this

inspection report.

Based

on this review, thss

LER is closed.

12.

~Eit N

The inspector met with licensee

management

representatives

periodically during the inspection

and held an exit meeting

on

January

8, 1991.

0

i