ML17305B359

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SALP Repts 50-528/90-53,50-529/90-53 & 50-530/90-53 for Nov 1989 - Nov 1990.Overall Performance Satifactory
ML17305B359
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 01/31/1991
From: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17305B358 List:
References
50-528-90-53, 50-529-90-53, 50-530-90-53, NUDOCS 9102180052
Download: ML17305B359 (48)


See also: IR 05000528/1990053

Text

INITIAL SALP

REPORT

.U.

S.

NUCI EAR REGULATORY COMMISSION

REGION V

SYSTEMATIC ASSESSMENT

OF

LICENSEE

PERFORMANCE

INSPECTION

REPORT

NOS.

50-528/90-53,

50-529/90-53,

50-530/90-53

ARIZONA PUBLIC SERVICE

COMPANY

PALO VERDE NUCLEAR GENERATING STATION

NOVEMBER 1,

1989

THROUGH NOVEMBER 30,

1990

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4

TABLE OF

CONTENTS

I.

Introducti on

~Pa

e

II.

Summary of Results

A.

Overview

B.

Results of Board Assessment

C.

Changes

in SALP Ratings

III. Performance

Analysis

A.

B.

C.

D.

E.

F.

G.

Plant Operations

Radiological Controls

Naintenance/Surveillance

Emergency

Preparedness

'Security

Engineering/Technical

Support

Safety Assessment/equality

Verification

4

7

9

12

13

15.

18

IV.

Supporting

Data and Summaries

21

A.

B.

C.

D.

Licensee Activities

Direct Inspection

and Review Activities

Enforcement Activity

AEOD Events Analysis

21

.23

24

24

I

I

f

II. Summar

of Results

A.

Overview

Licensee

performance

during the assessment

period improved in most

. functional areas

due in large part to management initiatives to

upgrade

weak areas

and to address

Board recommendations

from the

previous

SALP.

The improved performance

was best demonstrated

by

the relatively event free operation of all three units.

Dedication

to improved performance

was exemplified by the increased

degree of

management

involvement in day-to-day plant activities

and several

management

and organizational

changes

that strengthened

various

departments

in most functional are'as.

Management

involvement and support in the Emergency

Preparedness

area

was superior

and resulted in an improved rating (Category 1)

from the last

SALP period.

The change

was the result of continued

improvement in the program throughout the

SALP period brought about

by continued attention

from licensee

management.

The equality Audits and Monitoring and the equality

Systems

groups

were considered

strengths

in the Safety Assessment/equality

Verification (SA/gV) functi'onal area.

Effective quality monitoring,

programmatic evaluation,

and coordination of quality data

by these

groups

were noted.

.However, continued

management

involvement was

considered

to be the most needed

in this functional area

(Category

2

after considerable

Board deliberation),'as

reflected

by the

SALP

Board recommendations.

Insistence

on consistent self-evaluation is

still needed.

The civil penalties

regarding

inadequate

correc.ion

of emergency lighting discrepancies

and licensed operator medical

records discrepancies

appeared

to stem from a lack of management

insistence for aggressive

self-evaluation.

The lack of equality

Assurance

in the emergency lighting and licensed operator medical

records

area

was

a notable contributory cause of the problems.

The

licensee

conducted

an electrical

system self-assessment;

however, it

failed to identify deficiencies

formed by the NRC's

EDSFI related to

design basis calculations.

This indicates

a need to be more

self-critical and to conduct

a more in-depth review.

Additional

attention in the SA'/gV functional area is also considered

necessary

to improve performance of line organization verifications and

gC

inspections.

Effort will also

be necessary

to assure

continued

improvement of performance of safety assessment

groups

(NSG,

PRB,

ISEG,

PSAG,

and

OSRC).

A recognition of improved safety performance resulting from

initiatives in the Maintenance/Surveillance

functional area resulted

in a Category

2 rating.

However, there were extended

Board

deliberations

in this functional area

due to continuing weaknesses.

Continued attention is needed to establish clear and complete work

instructions

and to improve procedural

adherence.

Continued

emphasis

is warranted for timely and effective corrective actions to

maintenance

problems.

The Maintenance

organization

should actively

involve the Engineering organization in maintenance

problems

when

appropriate.

lt

I(

3'ngineering/Technical

Support performance

(Category 2) improved due

to implementation of plans to. address

past weaknesses

in this area.

Continued implementation of those plans is recommended.

Increased

involvement in site activities and in resolution of plant problems

should

be continued.

The roles

and interfaces of the site and

corporate

nuclear engineering organizations

need to be clear and

consistently

implemented.

Continued

emphasis

on conservative

and

comprehensive

response

to plant engineering

problems is warranted.

Relatively event free operations

of the three Units and

an improving

safety performance

trend were noted in the Operations

functional

area

(Category 2, improving).

However, further improvement is

still needed

in the conservatism

of management

decisions,

in the

Operations staff's attention to detail

and in ensuring that

appropriate

technical

support

groups are included in Operations

decision making.

Continued attention to improvement of identified

weaknesses

in the Operations

functional area,

such

as the lack of

control over licensed operator medical

examinations,

is recommended.

Licensee

management

involvement in the Radiological Controls

(Category 2) and Security (Category 2, improving) functional areas

was apparent.

Continued

focus in pursuing effective results

from

improvements initiated in these

areas

is encouraged.

Results of Board Assessment

Overall, the

SALP Board found the performance of NRC licensed

activities by the licensee

to be directed toward safe operation of

Palo Verde.

The

SALP Board has

made specific recommendations

in

most functional areas

for licensee

management

consideration.

The

results of the Board's

assessment

of the licensee's

performance

in

each functional area,

including the previous

assessments,

are

as

follows:

Functional

Area

Rating

Rating

Last,

This

Period

Period

Trend*

A.

Plant Operations

B.

Radiological Controls

C.

Maintenance/Surveillance

D.

Emergency

Preparedness

E.

Security

F,

, Engineering/Technical

Support

G.

Safety Assessment/equality

Verification

2

improving

2

2

1

2

improving

2

2

Th'e

SALP report

may include

an appraisal

of the performance

trend in a functional area for use

as

a predictive indicator.

Licensee

performance

during the assessment

period was examined

by the Board to determine whether

a trend exists.

Normally,

a

performance

trend will be indicated only if (1) a definite

~

0

The Systematic

Assessment

of Licensee

Performance

(SALP) program is an

integrated

NRC staff effort to collect available observations

and data

on

a periodic basis

and to evaluate

licensee

performance

on the basis of

this information.

The program is supplemental

to normal regulatory

processes

used to ensure

compliance with NRC rules

and regulations.

It

is intended to be sufficiently diagnostic to provide- a rational basis for

allocating

NRC resources

and to provide meaningful

feedback to the

licensee's

management

regarding the NRC's assessment

of their facility's

performance

in each functional area.

An NRC SALP Board,

composed of the'staff

members listed below, met on

January

10,

1991, to review observations

and data

on performance,

and to

assess

licensee

performance

in accordance

with NRC Manual Chapter 0516,

"Systematic

Assessment

of Licensee

Performance,"

dated

September

28,

1990.

This report is the NRC's assessment

of the licensee's

safety performance

at Palo Verde Nuclear Generating Station for the period November 1,

1989

through November 30, 1990.

The

SALP Board for Palo Verde was

composed of:

R.

Zimmerman, Director, Division of Reactor Safety

and Projects,

Region

V (Board Chairperson)

J.

Dyer, Director, Project Directorate 5,

NRR

K. Perkins,

Deputy Director, Division of Reactor Safety

and

Projects,

Region

V

F. Wenslawski,

Deputy Director, Division of Radiation Safety

and

Safeguards,

Region

V

D. Kirsch, Chief, Reactor Safety Branch,

Region

V

S.

Richards,

Chief, Reactor Projects

Branch,

Region

V

G.

Yuhas, Chief, Reactor Radiological Protection

Branch,

Region

V

J.

Reese,

Chief, Safeguards,

Emergency

Preparedness,

and

Non-power Reactor Branch,

Region

V

H. Wong, Chief, Reactor Projects

Section II, Region

V

R.

Huey, Chief, Engineering Section,

Region

V

C. Trammell, Project Manager,

PD 5,

NRR

C. Holden,

SALP Program Manager,

NRR

D.

Coe, Senior. Resi'dent Inspector,

Region

V

W, Ang, Project Inspector,

Region

V

M. Cillis, Senior Radiation Specialist,

Region

V

P. Quails,

Reactor Inspector,

Region

V

K. Prendergast,

Emergency

Preparedness

Analyst, Region

V

L. Norderhaug,

Safeguards

Inspector,

Region

V

J.

Sloan,

Resident

In'spector.,

Region

V

  • Denotes voting members in all functional areas.

Other persons

advised

the Board in their areas of cognizance.

<!

l

>4

>t

trend is discernible

and (2) continuation of the trend could

.result in a change

in performance

rating.

The performance

trend is intended to predict licensee

performance

during the

next assessment

period and should

be helpful in allocating

NRC

resources.

Chan

es in SALP Ratin

s

The licensee's

performance rating in the Emergency

Preparedness

functional area

improved to Category

1 from Category

2 for the

previous

SALP period.

The improved rating in the Emergency

Preparedness

area resulted

from continued

improvement in management

attention to, and licensee self-initiative in, the implementation of

the Emergency

Preparedness

Program throughout the

SALP period.

The

licensee

s ratings in the Maintenance/Surveillance,

Engineering/

Technical Support

and Safety Assessment/equality

Verification

functional areas

improved to Category

2 from Category

3.

The

improved ratings,

in general,

resulted

from improved performance

brought about by management initiatives and organizational

changes.

III. PERFORMANCE ANALYSIS

The following is the Board's

assessment

of the licensee',s

performance

in

each of the functional areas,

plus the Board's .conclusions for each area

and its recommendations

with respect to licensee

actions

and management

emphasis.

A.

Plant

0 erations

1.

~Anal sis

During the assessment

period, the licensee's

plant operations

were

observed routinely by both the resident

and the regional staff.

A

total of 2699 hours0.0312 days <br />0.75 hours <br />0.00446 weeks <br />0.00103 months <br /> of inspection effort were devoted to this

functional area,

approximately

36 percent of the total inspection

effor t.

The licensee's

performance

was rated

as Category

2 during the

previous

SALP rating period.

The previous

SALP report emphasized

the need for continued attention to formal and conservative

operations,

particularly valve and system manipulations;

more

thorough evaluation of problems;

and encouragement. of a working

atmosphere

conducive to thoughtful

and critical assessments

of all

phases

of plant operations.

During the current

SALP period, the

licensee

conducted

a comprehensive

assortment of plant operations,

including completion of extended

maintenance

outages,

mid-loop

operations.,

one complete refueling outage,

and full power operation

of all three units for several

months.

These evolutions were

conducted safely and generally indicated that the licensee's

performance

in the area

was good and had improved from the previous

SALP assessment.

However, several

events

occurred during this

period which indicate

a need to continue to emphasize

conservatism

in decisions

and attention to detail

on the par t of the Operations

staff.

There were approximately the

same

number of operations

related

NRC enforcement actions

and licensee

submitted

LERs for each

unit, which supports

the

NRC observation that there is relatively

little difference in performance

between units.

The number of

violations, excluding those associated

with operator medical

records,

and

LERs was approximately the

same

as the previous

SALP

period 'and collectively does not indicate

a program breakdown.

Licensee

management

is routinely involved in this area

and

has

on several

occasions

demonstrated

conservatism

in operations

judgement.

These

have included dealing with defective 0-ri'ngs in

main steam

and feedwater isolation valves,

shutdowns of Unit 1 to

repair

a steam generator

tube leak,

and prompt inoperability

determinations

of seismically deficient emergency diesel

generators.

In addition, the licensee

improved the conduct of mid-loop

operations

since the previous

SALP period.

Finally, licensee

management

was effective in overseeing

and coordinating the actions

required

by the

NRC to resolve

a Confirmatory Action Letter for

Units 1 and 3, issued

as the result of a March 1989 Unit 3 event.

However, several

events reflected the

need to continue to emphasize

conservatism

in decisions

and better involvement of supporting

groups

such

as engineering,

licensing,

and radiation protection,

Those were:

deenergizing all logarithmic power neutron flux

instruments

in Mode 5, venting reactor

coolant system

gaseous

activity into containment

during outage

maintenance activities, loss

of reactor coolant while repacking

a shutdown cooling valve in an

operating

loop,

and restart of a unit following a reactor trip

without first determining whether the event was bounded

by existing

analysis.

These

events

were not of major safety significance.

The licensee

is generally prompt in dealing with safety concerns,

but still occasionally requires

NRC involvement to ensure that

timely corrective actions

are taken.

For example,

slow licensee

-followup regarding the proper control of required licensed operator

medical

records resulted in a subsequent

NRC finding of a,

significant programmatic deficiency in this area

and resulted in

escalated

enforcement action.

The licensee

has

made sustained

progress

toward =improving plant

simulator performance,

a longstanding

NRC concern,

and is making a

major financial commitment to purchase

a second full scale simulator

to support required licensed operator training needs.

The

licensee's

program to certify the existing simulator has

been

reported to be on schedule,

although

an extension

may be required

should

any delays

be encountered.

The Emergency Operating

Procedures

rewrite program

has

been delayed

by another year

due to

delays

by contractors

providing the writer s guide.

This is the

=

second significant delay to this program.

Operations

personnel

are generally knowledgeable:and

professional,

and their response

to the relatively few events

which occurred

during the assessment

period was 'good.

However,

some deficiencies

were noted which indicate that continued

emphasis

on operator

attention to detail is appropriate.

These include: refueling-

operations

resulting in a stuck fuel assembly

and

a mispositioned

fuel assembly,

missed boron samples

following charging

pump lineup

changes,

over-dilution of the

RCS during power ascension

testing,

exceeding

the limit for

RCS heatup rate,

and spills of RCS and

refueling water tank water due to valve misalignments.

It is noted

that a dilution event occurred just after the end of this

SALP

period and reemphasizes

the continued

need for operator attention to

detail.

None of these-events

were considered to have resulted in a

significant safety problem nor did they indicate

a major deficiency

in this area.

They do however indicate

an area for additional

attention.

Although there

were

no

NRC administered

licensed operator

examinations

conducted

during this period, the licensee training

program for licensed

and non-licensed

operators

was found to

implement

an effective Systems

Approach to Training and was

generally

supported

by facility personnel.

However, facility

procedures

governing the licensee

administered

annual

operating

tests

allowed an operator

who failed the test to return to shift

work prior to passing

a second test,

which is contrary to

NRC

requirements.

This weakness

and the lack of control over licensed

operator medical

examinations

noted above indicated

a general

weakness

in meeting

10 'CFR Part

55 administrative control

requirements

which is further addressed

in the Safety

Assessment/equality

Verification section.

The licensee's fire protection program

was viewed to be adequate,

except'in the areas

of emergency lighting and

gA program coverage,

which is addressed

in the Safety Assessment/equality

Verification

section.

Overall, the Board concluded that the licensee's

performance

in this

area

had improved over the previous

SALP period as evidenced

by the

relative absence

of significant operations

related events.

2.

Performance

Ratin

Performance

Assessment

- Category

2 improving

3.

Board Recommendations

In order to more thoroughly and critically evaluate

operations

problems

and improve operations

decision making processes,

the

licensee

should continue to work to better involve supporting

organizations

as appropriate.

Continued

emphasis

toward

conservatism in Operations

decisions,

toward attention to detai

1

during daily operations activities

and to a critically questioning

approach to problems is also warranted..

Program controls over 10 CFR Part 55 requirements

need increased

scrutiny and continued

emphasis

is warranted

toward accomplishing simulator certification

as required

by 10 CFR Part 55.

Radi ol o ical Controls

l.

~Anal sis

The licensee's

radiation protection program

was observed

during

routine operations

and outage periods

by both the regional

and

resident inspectors.

Approximately 605 hours0.007 days <br />0.168 hours <br />0.001 weeks <br />2.302025e-4 months <br /> of inspection effort,

approximately

8 X of the total inspection effort, were devoted to

this functional area.

The licensee's

performance

in the radiological controls area

has

improved during this assessment

period.

The previous

SALP Board

recommended

that the licensee

be more aggressive

in maintaining

plant equipment

and that management

assure that occupational

radiation protection measures

are accomplished

and that questions

concerning the reliability of the radiation monitoring system

(RMS)

are resolved.

The licensee

has demonstrated

management

strengths

by continuing the

reorganization of the radiation protection

and chemistry groups,

including the staffing of key positions with highly qua'lified

individuals.

Assurance of quality and management's

effectiveness

were demonstrated

in the reduction of personnel

exposures,

the

surveillance

programs for the Post-Accident

Sampling

System

and

RMS,

the General

Employee Training (GET) program,

and in control of

contamination in plant areas.'ollective

personnel

exposure

had

declined

from an average

of 223 person-rem/Unit during 1989 to an

anticipated

169 person-rem/Unit in 1990.

These reductions

were

exemplified by a reduction of exposure

during the 1990 Unit 2

refueling outage

compared to the prior outage.

The licensee

was

also successful

in reducing personnel

contamination incidents.

Control of secondary

water anions

and condensate

oxygen

had

improved and

a new reactor

coolant

pH regime was initiated to

reduce

system

dose rates.

The licensee

formed

a separate

group to

oversee effluents

and the

RMS.

RMS reliability has

improved, the

number of associated

Licensee

Event Reports

(LERs) have decreased,

and the cause of numerous

special

reports related to surveillances

is being addressed.

The licensee

continued to maintain effective

programs involving -transportation of radioactive materials,

solid

radwaste

processing

and environmental

monitoring during this

assessment

period.

The licensee

s timely implementation of corrective actions

was weak,

as evidenced

by the failure to control locked high radiation areas.

Attempts to improve in-line monitors for secondary

chemistry

had

mixed success,

as

new sodium monitors were unreliable.

Examples of

untimely corrective action in response

to internal audit findings

included:

failure to implement procedures

to evaluate

abnormal

releases,

failure to complete

an evaluation of possible radioiodine

plateout in

RMS sample lines, failure to resolve

RMS alarm setpoint

determinations,

failure to resolve the isokinetic sample

design for

the high range effluent

RMS,. and failure to resolve vendor audit

findings involving radioactive waste processing

from 1985'and

1987.

PP

l

On two occasions,

decision-making

was conducted at

a management

level that did not result in adequate

reviews of activities prior to

implementation.

This was exemplified by the decision to release

approximately

26 curies of fission product gases

to containment

while personnel

were present

and the use of junior radiation

protection technicians for senior radiation protection technician

tasks

during

a labor action.

The licensee's

approach to the resolution of significant technical

issues

was typically thorough.

One exception involved management

of

water processing

using the boric acid concentrator

system.

The

evaluation

was not thorough nor completed in a timely manner.

Four Severity Level IV violations and six non-cited violations were

identified during the course of the assessment

period.

Host of the

violations resulted

from failure to follow procedures,

poorly stated

procedures

and failure to implement timely corrective actions.

One

Enforcement

Conference

associated

with the failure to properly

control high radiation areas

was held during this assessment

period.

While the violations and weaknesses

are important, collectively they

did not indicate

any programmatic

breakdown.

Ther e wer e weaknesses

in the licensee's

training program for junior

contractor health physics

(HP) technicians

as evidenced

by their

poor performance

during the

HP technician labor action.

This was

highlighted by

NRC enforcement

actions

concerning radiologically

controlled area

ingress

and egress.

Problems with issuance

of

proper dosimetry

and control of alarming-dosimeter

alarm setpoints

were clearly associated

with inadequate training.

HP technician staffing was adequate

and the professional

health

physics staffing was improving.

Authorities and responsibilities

were defined by management

and understood

by the staff.

Key

positions

were filled on

a priority basis.

During this period there

were several

occasions

involving poor communications

related to

workers bringing safety concerns

to

NRC attention.

Although no

violations were identified, the licensee

demonstrated

responsiveness

to the problem by restating their position and reviewing their

performance.

2.

Performance

Ratin

Performance

Assessment

- Category

2

3.

Board Recommendations

The licensee

should take

a more aggressive

role in ensuring

corrective actions

are promptly and effectively accomplished,

and

that procedures

are clearly stated,

understood,

and implemented.

Efforts should continue to focus

on completion of the organizational

changes

and conservative

decision making.

li

0

Maintenance/Survei

1 1 ance

1.

~Anal sis

This functional area

was observed routinely during the assessment

period by both the resident

and regional inspection staff.

In

addition,

a Diagnostic Evaluation

Team

(DET) evaluated

maintenance

and surveillance

as part of their broad-based

evaluation effort.

Approximately 701 hours0.00811 days <br />0.195 hours <br />0.00116 weeks <br />2.667305e-4 months <br /> of inspection effort were devoted to this

functional area,

about

9 percent of the total inspection effort.

A

noted strength

was the licensee's

willingness to confront hardware

problems directly, although problem resolution

was not always

seen

to be completely effective.

Improvements

were noted in the

establishme'nt

of a Site Maintenance

Manager, initiatives to improve

preventive maintenance

and repetitive work order consistency,

the

incorporation of 12 week work planning schedules,

formal Work

Planner/Coordinator

training,

and improved maintenance

mockup

facilities.

Several

examples

were noted where major maintenance

activities were conducted with thorough planning, control,

and

execution.

Noteworthy examples

included work to repair the Unit 1

steam generator

tube plug leaks,

the Unit 2 molded case

DC circuit

breaker

replacements,

and the Unit 3 main feedwater isolation valve

4-way valve replacements.

Three broad areas

of weakness

were identified during the previous

SALP period:

inadequate

work planning;

inadequate

attention to

detail in work implementation;

and inadequate

problem resolution.

During the current

SALP period, work implementation varied

considerably.

Major work activities which benefitted

from close

management

attention,

as noted above;were

executed

very well.

Other examples

noted below reflect some weaknesses

in routine

maintenance activities.

These

weaknesses

are categorized

into the

same three

areas

previously identified to .be weak, although

some

improvement

has

been

noted.

Continued attention to these

areas

is

warranted.

In the area of work planning,

as noted above,

the licensee

has taken

steps

to train personnel

and improve their work planning system.

Some

improvement

was noted,

however instances

of poor work planning

were observed

and resulted in incomplete

or inaccurate

work order

instructions contributing to problems

such as:

.inter-system

leakage

due to inadequate

retest

requirements for motor operated butterfly

valves,

inadvertent dilution of the

RCS during steam generator

hydrolazing,

and

damage to the fuel building ventilation boundary

during ventilation system maintenance.

Inspector identified

problems included lack of jobsite checks

by work planners

as

required

by procedure,

freeze

seal instructions which lacked

contingency

measures

for a loss of seal

and work orders which

required field workers to use

a motor operated

valve

(MOV) database

having 34 change notices.

Additionally, weaknesses

in work

scheduling practices

resulted in scheduling valve repacking work on

an operating

shutdown cooling loop, thereby causing

a significant

RCS leak; inadvertently rendering

an emergency diesel

generator

inoperable

due to steam cleaning work; and

a loss of valuable

t

10

as-found information during troubleshooting

on an

MOV due to other

work. being performed

on the valve.

Although few significant operational

events

were attributed to

maintenance

or surveillance activities, several

lesser

events

indicate

a need to increase

attention to detail in work

implementation.

Examples

include

a loss of all s'hutdown cooling due

to I8C work, an

RCS leak from a newly installed vessel

level

indication system

due .to poor work boundary control,

a balance of

plant engineered

safety feature actuation

due to a missed procedure

step,

a spray

pond pressure

transmitter left isolated following

calibration,

and several

examples of failure to document work steps

as the steps

were performed.

Corrective actions for problems in this area were generally

initiated, but were not fully effective in some cases.

For example,

instances

were noted in which as-found conditions were not preserved

for root-cause-of-failure

determination.

One example of inadequate

corrective action was

a failed relay in an auxiliary feedwater

pump

control circuit which rendered

the

pump inoperable.

The previous

month the

same relay had failed in a different unit and

no root

cause of failure analysis

had been

conducted,

which was contrary to

licensee

procedures.

The Material Nonconformance

Report

(MNCR) pr'ogram was initiated near

the beginning of the evaluation period

and improved as the

assessment

period progressed.

Several

problems with its

implementation

were identified by inspectors,

including failure to

initiate an

MNCR when appropriate.

In some cases,

program problems

were corrected

by changing the program

and associated

procedures.

In other cases, it appeared

that workers were reluctant to follow or

did not understand

the program requirements.

Work Control personnel

now review Work Requests

for MNCR conditions

and have initiated

MNCRs where required.

While this is not the ultimate expectation of

the program, it appears

to be adequate

corrective action at this

point.

Additionally, workers still occasionally lack an

inquisitive, probing approach to plant problems.

In one example,

a

technician inadvertently

caused

a hydrogen monitor to alarm while

making

a routine adjustment

and did not evaluate its significance.

In another

case,

a worker noticed

a valve handwheel

detached

from

its valve and took no corrective action until prompted

by an

NRC

inspector.

Although relatively few plant events

were attributed to weaknesses

in the preventative'aintenance

program,

several

instances

were

noted which indicate that the licensee's initiative to improve this

program should continue.

The Electrical Distribution System

Functional

Inspection

(EDSFI) team found a number of safety-related

relays,

breakers

and electrical distribution panels

which lacked any

scheduled

preventive

maintenance

or testing.

Similarly, the

EDSFI

identified that safety-related

motors lacked

a program for routine

monitoring of motor insulation resistance.

Inadequate

preventative

and corrective maintenance

for the emergency lighting system

was

part af a larger

issue which was subject to escalated

enforcement.

While the number of violations and

LERs in this functional area

was

somewhat higher than in the previous

SALP period, these

did

not reflect the

same

degree of safety significance

as in the

past

and did not indicate

a program breakdown.

The

DET identified

numerous motor'operated

valve maintenance

problems including:the

absence

of a program to address

progressive

degradation,

and

a lack

of aggressive

followup on industry )nitiated check valve advisory

documents.

In addition, the

DET noted that vendor technical

manuals

were not always kept current.

Maintenance material

support

was variable.

Improper storage of

reactor coolant

pump oil resulted in moisture contaminated oil being

used in the Unit 1 reactor coolant

pumps.

Corrective action for

material

support problems

included assigning

a procurement contact

person for each unit to attend morning meetings

and provide

coordination,

which appears

to have improved the situation.

The basic surveillance

program

was considered

to be sound,

however

some problems

were noted at this three unit site.

In one case, test

performers

signed off steps

as complete

when it was not possible to

perform the steps

as written.

In one case,

problems getting the

expected results

prompted invalidation of the test rather than

documentation

of the problem.

In another

case,

workers were

reluctant to seek assistance.

Licensee

event reports identify a few

surveillance

tests

which were missed, 'although during the last

months of the evaluation period

no further similar events

have

been

reported.

Some surveillance test procedures

had deficiencies

including inadequate

acceptance

criteria,

inadequate

verification of

test equipment operation,

unclear directions which permitted

inconsistency

between units,

inadequate

detail to assure

consistent

test data,

and errors in supporting operating procedures.

However,-

the licensee

has

strengthened

the supporting

program by completing

cross

reference

documents

which ensure all surveillance

requirements

are

implemented

by procedure.

While some problems

were noted, the

surveillance testing program is viewed as stronger overall than the

maintenance

program.

Overall, maintenance

personnel

have

shown the capability to perform

quality maintenance.,

Some instances

of inadequate

inquisitiveness

were still apparent.

Program effectiveness

has improved, but is

still hindered

by weaknesses

in work planning, scheduling,

and

corrective action for identified problems in the maintenance

area.

2.

Performance

Ratin

Performance

Assessment

- Category

2

3.

Board Recommendations

The Board conducted

extended deliberations in this- area.

The

Board's previous

assessment

of Category

3 performance

was partly a

reflection of the maintenance

weaknesses

highlighted by the

operational

events

during that period.

During the current

evaluation period there

have

been

no maintenance

issues

similar to

those of the previous period and the Board has recognized

the

12

licensee's

current initiatives in the maintenance

area.

The

licensee

should clearly recognize

the need to continue the

initiatives that have

been started.

The Board recommendations

are

identical to those of the previous cycle.

The licensee

should continue to work to establish clear and complete work

,instructions.

Emphasi's

continues to be needed

toward procedural

adherence.

Maintenance

personnel

should actively involve

engineering when'ppropriate

and engineering

should strive to be

aware of ongoing maintenance

issues.

Maintenance

managers

should

continue efforts to observe routine ongoing work and to carefully

manage safety equipment

outage

schedules.

Continued attention to

establishing timely and effective corrective action is warranted.,

with respect

to concerns

in the maintenance

area.

Emer enc

Pre aredness

l.

~Anal sis

During thi s

SALP per iod, approximately

168 inspecti on hours,

approximately

2X of the total inspection effort, were utilized to

assess

the licensee's

Em'ergency

Preparedness

(EP) Program.

This

included the observation

of one exercise

and three routine

inspections.

The previous

SALP board

recommended

an emphasis

on

management

attention to timely implementation of corrective actions

and continued

management

'involvement in the program.

Management

involvement

has

been effective in improving the

EP

'program.

This was evidenced

by the improvement

and upgrading of

Emergency

Response facilities and equipment (i.e.,

new emergency

response

vehicles

and efforts to upgrade the offsite assembly

and

backup

EOF capabilities),

and being proactive in improving the

Emergency

Plan Implementing Procedures

(EPIP's)

and the Emergency

Plan to conform to

NUREG 0654.

Management

support

and participation

was also evidenced

by the >conduct of two accountability drills and

superior performance

during the annual

exercise.

The licensee's

gA program provides for an in-depth independent

audit

of the

EP Program.

The licensee

used

a Senior

EP supervisor

from

San Onofre to participate in the audit, contributing a level of

expertise

not usually obtained- in annual

EP audits.

Audit fin'dings

and recommendations

were well documented,

entered,

tracked,

and were

corrected in a timely manner.

The licensee's

efforts to resolve technical

issues

from a safety

standpoint

appeared

to be effective..

The effort to revise the

Emergency

Plan

and EPIP's to be consistent, with NRC guidance

documents

was being performed largely on the,licensee's

initiative

after the

NRC s identification of inconsistencies.

The performance

of two effective accountability drills, one

on a weekend

and one

during work hours,

also demonstrated

management's

wH lingness to

improve plant performance.

There

was

one violation of an

NRC requirement during the evaluation

period.

The violation involved a failure to declare

an Unusual

0

13

Event for a fire within the power block lasting more than ten

minutes.

The licensee's

corrective action for the violation was

prompt and effective to prevent recurrence.

However, it is noted

that this event was the only Unusual

Event (reportable)

which

occurred i n this rating period and appeared

to result from a lack of

conservatism

in management

decisions.

Subsequent

events

were

cor'rectly classified,

although

none were significant enough to be-

class'ified

as

an Unusual

Event or higher.

Staffing of the

EP Program appears

adequate.

Positions

are

identified and authorities

and responsibilities

are well defined.

Vacant

key positions

are filled on

a priority basi s.

Needed

expertise is available within the staff.

Consultants

are

used

as

appropriate

to supplement

the staff for major occurrences

such

as

the annual

exercise. 'he licensee

appeared

to have

an effective

program to ensure that adequate

emergency

response

personnel

are

onsite

and are current in all of the required training for their

specified positi.ons.

The licensee

appears

to have

a good emergency

preparedness

training

and qualifications program.

The program appears

to be effective in

ensuring that personnel

in key positions

are fully qualified and

have all required training.

Interviews with a number of Shift

Supervisor personnel

disclosed

a good understanding

of the Emergency

Plan

and event classification.

No weaknesses

were observed

during

those interviews.

2.

Performance

Ratin

Performance

Assessment

- Category

1

3.

Board Recommendation

The licensee

should continue support of the

EP program.

Management

emphasis

is appropriate

to ensure

aggressive

problem solving, to

validate the effectiveness

of recently implemented corrective

actions,

and to ensure that plant events

are pr'operly classified.

~Sec unit

1.

~Anal sis

During the assessment

period,

Region

V conducted four physical

security inspections.

Over 336 inspection

hours,

approximately

5X

of the total inspection effort, were expended

by regional

inspectors.

In addition,

a team inspection

and the resident

inspectors

provided continuing 'observations

in this area.

a

With regard to involvement in assuring quality, corporate

and plant

management

continued to review the operation of the overall security

program.

Significant weaknesses

had

been

noted early in the

assessment

period in the areas

of security event analysis

and alarm

trending to identify root causes.

The large

number

and age of

t

0

14

uncompleted

maintenance

requests

for security-related

equipment

was

also identified as

an area

needing attention.

Additionally,

communication

between levels of security management

and between

security

and other disciplines

was found to be weak.

There

was

significant improvement during the assessment

period in response

to

NRC concerns.

Licensee organizational

changes

appear to have

remedied

these

weaknesses.

The licensee

has established

a "Site

Services Division Action Plan" aimed at improving tactical training,

site exercises,

strategic planning

and target analysis,

to assure

that the contingency plan implementing procedures

provide proper

response

to the design basis threat.

Improvements

were

made to

facility hardware to reduce the need for compensatory

security

measures.

equality assurance

and quality control programs

and policies are

generally adequately

stated

and understood.

However,

Region

Y noted

that further dialogue

appeared

warranted

between reactor operations

and security personnel

so that armed

response

strategy

and tactics

could be initially focused

on protecting the most critical safety

systems

and components first.

The previous

SALP report encouraged

licensee

management

to complete

their review of closed circuit television

(CCTV) camera

coverage

and

illumination necessary

for adequate

protected

area barrier alarm

assessment

and to limit overtime effects

on guard alertness,

including expediting the implementation of their planned

expanded

security training program;

The licensee's

study to relocate

cameras

and illumination to improve coverage,

completed during the latter

part of the assessment

period,

appears

quite satisfactory.

However,

the current

CCTV cameras

require

a very high level of maintenance

to

remain operational

due to the severe

environmental

conditions

under

which they must function.

Evaluation of alternate

camera suppliers

is continuing.

To limit overtime effects,

the licensee

has,

during

the latter part of the assessment

period, completed their expanded

training program and improved access

control system reliability to

reduce

the number of compensatory

posts.

The licensee

has also

abandoned

the 12-hour work shifts for security officers,

implementing

a standard

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> per day,

5 days per week duty

schedule.

Identification and resolution of technical

issues,

while slow in

some cases,

has

been generally

sound

and thorough..

Early in the

assessment

period, lack of thorough analysis of root cause

and

systematic

implications of equipment failures were identified.

Improvements

in trending

and analysis of equipment/human

failures

has

been

noted in later inspections.

During the assessment

period, licensee

action relative to three

information notices dealing, respectively, with radio

communications,

review and analysis of safeguards

event logs,

and

potential

weakness

with certain types of security equipment

were

reviewed.

Mith the exception of the review of event logs, the

licensee's

actions,

as reviewed to date,

were found to be

appropriate.

15

The enforcement history for the period November

1,

1989, through

November 30,

1990,

includes

3 violations identified early in the

assessment

period,

which were related to a licensee identified (but

repeated)

failure to provide

a vital area barrier as described

in

their approved security plan, failure to provide proper

escorted

access

to vital areas,

and failure to properly package

safeguards

information for mailing.

Additionally, the enforcement history

includes

a non-cited violation regarding

implementation of an

unapproved training program of simulated night firing.

During this

SALP period, the licensee

reported four safeguards

events.

Three of these

events

resulted

from personnel

error:

failed security compensatory

measures

(two) and an uncontrolled

pathway to a vital area

(one).

The remaining event resulted

from a

design deficiency related to a vital area barrier vulnerability.

Mith respect to staffing,

key positions

were identified and,

although limited by staffing considerations,

position

responsibilities

were generally well defined.

The security training

staff is continuing their special

advanced training program

on .their

own initiative and augments

cur rent offsite security resources

to

meet the special

security

demands

of the plant's isolated location.

2.

Performance

Ratin

Performance

assessment

- Category

2 improving

3.

Board Recommendations

The licensee is encouraged

to complete their review of CCTV camera

designs

to improve the performance characteristics

of the alarm

assessment

system.

The licensee

should continue the

use of

management

action plans to critically review their security program,

i'dentify problem areas

and promptly resolve problems

when they are

identified.

En ineerin /Technical

Su

ort

l.

~Anal sis

This functional area

was reviewed routinely by both the regional

and

resident staff of the Region

V office, and by the staff of NRR.

Over 411 inspection

hours were expended

in this functional area,

approximately

5 percent of the overall inspection effort.

These

reviews focused primarily on the effectiveness

of the engineering

organizations

and in the quality of their work.

The licensee

has restructured

the engineering organizations

and

filled most remaining

key management

positions during this

assessment

period.

In February 1990, the

new position of Vice

President

= Engineering

and Construction,

was created

and filled.

In April, the permanent Site Technical Director position was filled.

The Engineering Evaluation Department,

which includes the System

Engineers,

was reorganized

under the Site Technical Director,

I

,I

I

t

I

e

16

creating four new departments.

These

changes

included formation of

a Component

and Specialty engineering

group which established

component

engineers

to address

motor operated

valves

and safety

relief valves,

check valves,

motors

and pumps,

and

a group to

'onitor component

performance

and maintenance

data.

This appears

to

have

improved the focus of the Site Technical

Support personnel,

although the interrelationship

and responsibilities of System

Engineers

a'hd Component

Engineers is not always clear.

In July

the

Director of Site Nuclear Engineering

and Construction position was

created

and filled, and the Site Nuclear Engineering

Department

(SNED) was formed, providing greater onsite design engineering

expertise

and .support.

In October,

these engineering functions,

including the corporate-based

Nuclear

Engineering

Department,

were

consolidated

under the Vice President - Engineering

and

Construction.

The Director -'Nuclear Engineering position was not

filled until after the end of -this assessment

period.

Additionally,

the licensee's

Business

Plan was developed

and is being implemented,

providing specific goals

intended to enhance

the effectiveness

of

the engineering

organization.

This Plan addresses

weaknesses

and

recommendations

from the Diagnostic Evaluation performed

by the

NRC

early in the assessment

period and incorporates

the licensee's

Engineering Excellence

Program.

In general,

engineering

work addressed

significant problems in a

typically timely and thorough manner.

Improvement

was specifically

noted in the responsiveness

of engineering to plant events.

Positive

examples

included involvement in resolution of embrittled

pins in safety-related. butterfly valves, retrieval of a broken

incore detector,

resolution of auxiliary feedwat'er

pump pressure

pulsations,

assessment

of improper backup rings in four-way valves

which control the feedwater isolation valves, control element

assembly

coi 1 testing to prevent slippage during surveillance

testing,

and retrieval of a heated junction thermocouple

sheath.

Additionally, Engineering

has proactively pursued

probl.em

identification, having identified several

deficiencies

during the

design basis reconstitution

process

and during fire barrier

walkdowns.

System engineers

appeared

to have improved their ability

to identify deficiencies in their systems.

Examples

include

inappropriate paint on the fuel metering ports;of an emergency

diesel

generator,

and

a deficient splice in the atmospheric

dump

'valve control system.

Although the licensee's

performance in this area

has clearly

improved as

a result of management

involvement and initiatives,

there were several

instances

which indicate that more than minor

weaknesses still remain to be addressed.

Most notable of these

examples

was the continuing problems with the emergency lighting

system.

Problems with the system

have persisted for years

and were

not dealt with in a thorough, integrated fashion, resulting in civil

penalties

in both 1989

and 1990.

In this instance, critical

self-assessment

of the issue

was clearly lacking and the -licensee's

approach to resolution of the associated

technical

problems

was

poor.

Other examples of weak engineering

work included inadequate

testing of motor operated butterfly valves, configuration

~

~

17

control problems with the Core Operating Limits Superv'isory

System

(COLSS), not clearly limiting the torque value for a Pressurizer

instrument valve gland nut in an associated

work document,

using

invalid assumptions

in determining

how to compensate

for temperature

changes for the

ADV nitrogen drop test,

inadequately justifying

waivers for some preventive

maintenance

tasks,

and failure to

recognize

the significance of the loss of preload

on

MOV spring packs..

Licensee engineeri ng and contract personnel

performed

a design

review of the electrical distribution system prior to the

NRC

Electric Distribution System 'Functional

Inspection

(EDSFI)..

While

the performance of these

types of reviews are considered

a strength,

the subsequent

NRC EDSFI identified an electrical

system

power

configuration which could have potentially caused

overloading of a

startup transformer.

The

EDSFI also identified load calculation

errors

and

a 1990 diesel

load calculation which used incorrect data

from a superseded

1989 calculation.

These

problems

were not noted

by the earlier

licensee

reviews

and were indicative of deficiencies

in the licensee's

design control

and verification process,

and of

the licensee's

overview review in this area.

In spite of the increased

focus

on the engineering

program, the

backlog of open Engineering Evaluation

Requests

has

decreased

only

about ten percent,

to approximately

2000, during this evaluation

period.

However, these

have

been prioritized by the licensee

based

on their significance.

Management of engineering

resources

to

address

these

items will require continued attention.

Training programs for Electrical Maintenance,

and for

Instrumentation

and Controls Maintenance

were found to be

acceptable.

The licensee's

efforts to implement the Systems

Approach to Training for the technical staff appeared

to be

effective and generally supported

by facility personnel.

Mith

,regard to enforcement in this area, with the exception 'of the

emergency lighting civil penalty, all other violations were

considered

minor and did not indicate

a programmatic

breakdown.

2.

Performance

Ratin

Performance

Assessment - Category

2

3:

Board Recommendations

Efforts to clearly define the role of System Engineers

should

continue.

Corporate

and Site Nuclear Engineering

should solidify

their organizations

and continue to increase their involvement in

site activities

and prob1em resolution,

however the roles

and

interfaces for all organizations

need careful definition due to the

organizational

changes

which have occurred.

The licensee

should

continue the emphasis

being placed

on responding conservatively,

deliberately,

and comprehensively to plant engineering

problems,

and

ensure

the involvement of all appropriate

supporting organizations.

H

tf

18

Safet

Assessment/

ualit

Verification

1.

~Anal aia

During this assessment

period, approximately

2457 inspection hours,

approximately

33 percent of the total inspection effort, were

.expended

by resident,

region-based,

and headquarters

inspectors.

Included in this functional area are the inspection

hours associated

with followup to the emergency lighting problems

and the restart of

Units 1 and

3 following the issuance

of Confirmatory Action Letters.

Inspections

were conducted in the areas of Quality Assurance

(QA)

and Quality Control

(QC), Independent

Safety Engineering

Group

(ISEG), Plant Review Board (PRB), Nuclear Safety Group (NSG),

Management

Review Committee

(MRC), Offsite Safety Review Committee

(OSRC), Plant Safety Assessment

Group (PSAG),

and the Licensing

organization.

Licensee

management

demonstrated

an increased

degree

of involvement in day-to-day activities which contributed to

improvement in this area.

Although improvements

were noted in all

safety assessment

groups required

by Technical Specifications

(TS),

and

some instances

of strong performance

were observed,

overall

some of the groups

are perceived

as not performing as effectively as

they could.

Licensee actions to correct past weaknesses

regarding

the problem identi,fication and corrective action programs,

root

cause

analysis

programs,

and the effectiveness

of QA and oversight

organizations,

are apparent.

Although programs

are in place

arid

have

improved, the resultant

improvement 'in safety performance still

remains to be fully demonstrated

by more committed implementation

and follow-through from all levels of the licensee's

organization.

A past weakness

regarding the lack of sufficient technically

experienced staffing of the

QA organization

was in the process

of

being corrected

by strengthening

of the Quality Department staff.

Weaknesses

of the

NSG in its effectiveness

in identifying and

recommending

changes

to weak programs

were noted to have improved

during this assessment

period.

NSG's assessments

and

recommendations

regarding the

PRB composition

and the 10 CFR 50.59

program implementation

appeared

to be contributing to nuclear

safety

improvement.

Based

on a

NSG recommendation,

the licensee

submitted,

obtained approval,

and implemented

a Technical Specification

change

to the composition of its PRB..

The inclusion of all Unit Plant

Managers

and the Director of Standards

and Technical

Support in the

PRB appeared

to initially have resulted in substajtiv'e

review of

plant problems

and recommendations

for resolution'f those'problems.

However, during the

same period, the PRB's review of -the October 20,

1990 Unit 3 simultaneous

opening of seven

Steam

Bypass Control

Valves and the associated

reactor trip appeared to have

been weak

and was not sufficiently probing to identi'fy that the condition had

a potential of subjecting the plants to a condition that was beyond

their design basis.

This demonstrates

a continuing, need to foster

a

probing and questioning attitude

by all oversight groups.

ISEG was

noted to also

have

made

some

improvements in its reviews

and the

presence

of ISEG's engineers

in the field was more visible.

However, the .effective utilization of ISEG, the consistency of ISEG

reports,

and the technical

accur'acy of ISEG investigations

continue

to warrant improvement.

19

The licensee utilized a non-TS required.MRC to provide senior level

oversight of restart activities associated

with the extended

shutdown of the units in 1989.

The

MRC oversight appeared

to have

contributed significantly to minimizing problems associated

with

completion of restart action items

and during the restart operations

activities.

Upon restart of all the units the

MRC was disbanded.

The advantages

and benefits brought about by the

MRC oversight were

recognized

by the licensee

and were subsequently

continued

on .to the

operations

phase

by the formation of the

OSRC.

.The non-TS required

PSAG appeared

to have .been contributing to plant safety in its

review and generic evaluation of the various oversight committee

reports

and identification of safety concerns that were not readily

apparent in the individual reports.

PSAG still had limited success

in effectively coordinating review activities of the various

oversight groups.

Although overall performance in this functional area is'onsidered

to have

improved and the licensee's

many initiatives are

recognized,

two escalated

enforcement actions during the period

create

doubt regarding whether the improvements in this area

can

be

sustained.

One civil penalty was related to long standing

deficiencies

in the emergency lighting area.

Of particular concern

was both management's

and QA's apparent

reluctance

to critically

assess

the technical

situation.and

then deal with it promptly and

thoroughly.

With regard to the civil penalty associated

with

operator medical

records,

the licensee

had substantial

prior notice

of problems in the area, yet the full extent of the problems

was

only realized following an

NRC inspection.

These

two events bring

into,question the depth of senior management's

commitment to

critically assessing

their organization,

and to reacting decisively

when significant issues

demand it.

There were

a number of other

lesser

enforcement

actions in this area,

however those

lesser

violations were not indicative of a major problem.

The licensee's

quality verification functions were accomplished

by

second party (non-Quality Department) verification, specified

QC

inspections,

QA monitoring and

QA audits.

The second party

verification process

and the

QC inspection process

generally met all

requirements.

The licensee

has

implemented its

MNCR and

QDR

corrective action programs

and they generally appeared

to be also

effective and appeared

to correct

many of the previous programmatic

weaknesses.

However, occasional

weakness

in the implementation of

the programs

have still been noted,

as discussed

in the maintenance

section of this report, in the apparent

occasional

hesitance

to

write MNCRs or QDRs in favor of work requests

or EERs.

Quality monitoring was viewed as

a strength of the licensee's

QA

program.

It was generally utilized effectively in areas

of concern

such

as control

room unit restart activities and provided primarily

performance-based

quality overviews of ongoing activities.

The

quality of QA audits

improved in scope

and performance

from previous

years

as demonstrated

by audits performed

on TS surveillances

and on

refueling operations.

The management

of both the Quality Audits and

Monitoring and the Quality Systems

group were considered

strengths

20

of the licensee's

equality Department.

Significant support of, and

involvement in the

gA program. by the Executive Vice President,

Nuclear,

was clearly demonstrated

by his detailed

comments

and

followup of both gA audits

and audits of the

gA program by

independent parties.

The staffing level

and qualifications of personnel

in safety

assessment

and quality verification organizations

generally appeared

to be adequate.

Key positions in the equality Department

and

on the

PRB,

whose functions were previously performed

on an acting bases,

were filled late in the assessment

period by the appointment of a

equality Department

Deputy Director and the appointment of a Manager

of Plant Support,

who serves

as the

PRB chairman.

The

gC inspection

staff assigned

to perform inspections

in the units appeared

to be

small

and usually required significant contractor

augmentation

during major outages.

.The small equality

Systems staff appeared

to be contributing

significantly by its involvement in quality improvement projects,

such

as its continuing oversight of the nonconforming condition

reporting program

improvements

and by its quality data evaluation,

trending,

and reporting.

The licensee self assessment

programs

included

an electrical

distribution system functional assessment,

a diesel

generator

safety

system functional inspection

and independent

audits/evaluations

of

the

gA audit functions.

However,

subsequent

NRC inspections

identified additional

problems to those identified by these self

assessments.

The licensee's

action demonstrated

a continuing desire

to improve performance

in this functional area,

although

more

critical assessments

are

needed.

The

NRC Office of Nuclear Reactor Regulation

(NRR) staff conducted

substantial

review activities in support of licensee

submittals

during the assessment

period.

The licensee's

submittals

were

generally acceptable

for the most part.

Occasional

lapses

were

noted.

In one notable

example,

the licensee's

original submittal to

extend the interval for steam generator

eddy current=examination

was

inadequate

because

the licensee

had submitted insufficient

information.

As a result,

the

NRC staff could not perform an

independent

analysis to support the proposed

amendment.

Subsequent

.

inquiries by NRR revealed further pertinent information that was not

included in the initial submittal.

Responses

to generic

communications

were generally timely and

appropriately detailed.

A cooperative attitude

was exhibited

throughout most discussions

regarding the licensee's

methodologies

and basis for analysis

as well as approach to resolution of issues.

The licensee's

responses

to

NRR staff questions

were generally

complete

and timely, thereby facilitating the staff's review.

2.

Performance

Ratin

Performance

Assessment

- Category

2

f

21

3.

Boar d Recommendations

The Board assessment

for this functional area recognizes

the

licensee initiatives to improve performance

in this area.

However,

the assessment

was the result of considerable

Board deliberation.

The Board strongly recommends

continued attention to performance in

this area.

The licensee

needs to continue to require that the

equality Assurance

(gA) organization

be more critical and aggressive

in their reviews,

such that major problem areas will be identified

prior to becoming self-revealing.

Management failures to recognize

problems,

and the lack of gA oversight in both the operator licensing

medical

records

area

and emergency lighting demonstrated

a-

.

continuing need for improvement.

The equality Department,

the

oversight groups,

and engineering

should develop

a more questioning

and probing attitude to ensure

in-depth root cause

review and

thorough,

prompt corrective actions.

Further strengthening

of the

gC organization,

gC inspections

and line organization verifications

is also

recommended for continued

good performance

in this

functional area.

Visible, strong support for the

gA program,

from

all levels of management,

should

be demonstrated.

The licensing organization

needs to increase

awareness

of plant

operations

and status,

and ensure that all licensing submittals

contain all information pertinent to the subject.

The communication

and participation

between the corporate

organizations

and the site

(operations

personnel)

also

needs

to be improved as discussed

in the

plant operations

functional area,

as

a joint effort.

IV.

SUPPORTING

DATA AND SUMMARIES

A.

Licensee Activities

C

During this assessment

period, Units 1 and

3 completed

extended

refueling outages

which began in March 1989.

Numerous corrective

actions'were

taken

by the licensee

in response

to an

NRC

Confirmatory Action Letter based

on the circumstances

surrounding

the unit shutdowns.

Following selected

NRC review of these actions,

the letters

were rescinded in December

1989 for Unit 3 and June

1990

for Unit 1,

Both units restarted

immediately following this

NRC,

action.

Unit 2 operated

during this assessment

period,

and also

completed

a five month refueling outage.

Specific operational

events

were

as follows:

Unit 1

Unit 1 was in Hode

6 in the midst of a refueling outage at, the onset

of this assessment

period.

Fuel loading was completed

and

Mode 5

entered

on January

9, 1990.

Mode 4 entry occurred

on April 17,

1990,

and

Mode

3 was entered

on April 18.

The Unit was cooled

down

to Mode

5 on Hay 4, 1990, to repair Steam Generator

tube leaks

and a

Reactor Coolant

Pump seal.

During mid-loop (reduced inventory)

operations,

a complete'oss

of Shutdown Cooling was experienced

on

May 9, 1990.

Repairs

were completed

and

Mode 4 was entered

on June

I

(

22

13, 1990, followed by Mode

3 entry on June

14.

The Confirmatory

Action Letter of December

24, 1989,

was lifted on June

24, 1990,

and

Mode 2 was entered that day.

On June 25, 1990,

a manual reactor trip test

was performed

and the reactor

was returned to Mode 2

=operation.

A slipped Control Element Assembly event occurred during

startup testing.

Mode 1 was entered

on June

30,

1990 and the Unit

was brought, to 100 percent

power.

A reactor trip occurred

on August 14, 1990, following a manual

turbine trip initiated because

of a loss of cooling to the main

transformer.

The reactor

was restarted

on August 18, 1990,

and

Mode

1 was entered

'on August 19.

A forced downpower and manual reactor trip occurred

on September

13, 1990,

due to leakage

past

a primary

Pressure

Safety Valve.

The Unit was subsequently

cooled

down to

Mode

5 for repairs.

Heatup to Mode

3 on September

19-20 revealed

leakage

from the pressurizer

vent system,

forcing a return to Mode 4

for repairs.

Heatup to Mode

3 was completed

on September

23, 1990,

and the reactor

was started

up on September

24.

A Hain Feedwater

Pump tripped,

causing

a Reactor

Power Cutback to about

50 percent

power to occur on October 2, 1990.

The Unit was restored

to, ful'l

power operation the

same

day.

Power

was reduced to about

64 percent

on November 24-25,

1990, to allow repair of secondary

equipment.

The Unit was operated at 100 percent

power for the remainder of the

assessment

period.

Unit 2

Unit 2 began this assessment

period in Mode

3 to. resolve

CEDH ground

indications, incorrect

HPSI flow orifices,

and brittle restraining

pins in containment

purge valves.

A reactor trip occurred

on

November 1,

1989

due to three independent

problems in the Plant

Protection

System.

A three

week shutdown resolved these

i.ssues

and

other maintenance

work was accomplished.

During the heatup in Mode

4,

RCS heatup rate limits in the Technical Specifications

were

exceeded

and the plant was returned to Mode 5 to assess

the impact

and

need for corrective measures.

After one week, the plant startup

was delayed after reaching

Mode 2 due to

CEA grounds,

but the unit

achieved

100 percent

power on December 5, 1989.

The reactor

was

shutdown

on February 23,

1990 to commence the second refueling

outage.

This outage

included defueling the reactor,

steam generator

inspection

and tube plugging, reactor coolant

pump .overhaul,

CEA

repair for grounds,

and diesel

generator

"B" overhaul.

The reactor

entered

Mode 2 on July 14,

1990 and following a series of unrelated

problems with high condenser

sodium levels,

loss of power to a

cooling tower,

a tripped condensate

pump,

and a

COLSS failure, the

unit achieved consistent

100 percent operation

on. August 17, 1990.

The unit operated at approximately this power for the remainder of

the assessment

period.

Unit 3

The unit began the

SALP period in Mode

5 in its first refueling

outage.

At the completion of outage

work the unit entered

Mode

3 on

November 30, 1989, then returned to Mode 4 for several

days 'due to

C

23

problems with steam-driven auxiliary feedwater

pump pressure

osci llations.

When these

problems

were resolved the unit returned

to Mode 3.

Additional auxiliary feedwater

pump work necessitated

a

second return to Node

4 on December

22,

1989 and the unit returned

to Mode

3 on December

24, 1989.

The

NRC lifted the Confirmatory

Action Letter dated

June

28,

1989 on December

24, 1990, permitting

entry into Mode 2.

On December

26,

1989 the unit entered

Mode 2 and

began

low power physics testing.

An internal fault on the "A" phase

masn transformer

occur'red shortly after the main generator

was

synchronized

to the grid and the reactor

was manually shutdown to

Mode 3.

Mode 2 was entered

on January

18,

1990 after replacement

of

the transformer

and the unit entered

Node

1 on January

19, 1990.

Power ascension

testing followed and the unit increased

power to 98

percent while the licensee

evaluated

the reason for output megawatts

being higher than expected.

Resolution of the output megawatts

issue permitted the unit to proceed to 100 percent until a reactor

trip occurred

as

a result of a dropped

rod on April 14,

1990 during

monthly

CEA testing.

The unit proceeded

from Hode.2-to

Mode 1 on

April 19,

1990 and increased

power to 90 percent

where it remained

for repairs of feedwater

heaters

5B and

6B.

Repair of these

heaters

required

a downpower to 50 percent

and the unit proceeded

to 100

percent

on April 29,

1990.

On May 29,

1990 a reactor

cutback

occurred

due to the tripping of the "A" main feedwater

pump during

preventive maintenance.

The unit returned to 100 percent

power on

May 30,

1990 where it remained except for minor testing until

a

slipped

CEA and unsuccessful

recovery required

an orderly shutdown

on August 5,

1990.

The unit returned to Node 2 later that

same

day

but returned to Node

3 because

of additional

CEA problems.

Repairs

were completed

and the unit proceeded

through

Mode 2 to Mode

1 on

August 7, 1990.

The unit reached

100 percent

power

on August 9,

1990

and remained there until a reactor cutback occurred

on

September

8, 1990 due to a trip of the "B" main feedwater

pump due

to a failed logic control circuit card.

The unit retur ned to 100

percent

power on September

9, 1990.

A reactor trip occurred

on

October 10,

1990 as

a result of a sudden

opening of all in-service

steam

bypass

control valves.'he

unit proceeded

to Mode

2 and Node

1 on October 21,

1990 and reached

100 percent

power on October 23,

1990.

On October 30,

1990 the "A" emergency diesel

generator

tripped

on a faulty .vibration switch.

The switch was repaired

and

the diesel

generator

was returned to operability within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The unit was forced to reduce

power on November 26, 1990 because

of

a'OLSS malfunction.

The unit returned to 100 percent

power later

that day and remained at 100 percent until the end of the

SALP

period.

Direct Ins ection and Review Activities

Three resident

inspectors

were assigned to Palo Verde during the

SALP assessment

period.

Forty-six routine arid special

inspections

were conducted

during this period. Significant team inspections

included

f

f

NRC Diagnostic Evaluation

Training Inspection

Electrical Distribution System Functional Inspection

A total of over 7378 hours0.0854 days <br />2.049 hours <br />0.0122 weeks <br />0.00281 months <br /> of direct inspection

were performed

during this SALP'period.

In addition, three

Enforcement

Conferences

and four Management

Meetings

were held with APS.

C.

Enforcement Activit

The 46 inspections

conducted

during this assessment

period

identified approximately

66 cited violations and approximately

26

non-cited violations.

Although counted individually, many of those

violations were

common to multiple units.

The significant

violations are discussed

in the individual performance

analysis

sections of this report.

Fifteen of the violations identified during this assessment

period

involved Emergency Lighting and 10 CFR Part 50, Appendix R, Fire

Protection

Program violations,

and licensed operator medical

records

violations.

Those violations resulted in the imposition of a

$125,000

and

a $75,000 civil penalty respectively.

D.

AEOD Event Anal sis

The Office for Analysis and Evaluation of Operational

Data

(AEOD)

reviewed the licensee's

events

and provided the following input.

Arizona Public Service

Company submitted

28 Licensee

Event Reports

(LERs) for the three unitsl at Palo Verde, not including updates,

in

the assessment

period from November 1,

1989 to November 30,

1990.

The

AEOD review included the following LER numbers:

UNIT 1

UNIT 2

UNIT 3

89-021 to 89-024

90-001 to 90-008

89-011

90-001 to 90-009

90-001 to 90-006

The review of these

LERs follows:

1.

Im ortant

0 eratin

Events

None of the

LERs submitted in the assessment

period were

identified as important operating

events

by the

AEOD screening

and review process.

However, the review did not inclu'de the

reactor trip at Unit 3 on October 20,

1990 that resulted in all

steam

bypass

valves opening or the identification that the

'jacket water return line supports for both emergency

diesel

generators

at Unit 2 did not meet seismic qualifications

on

November 10,

1990 because

the respective

LERs have not been

received at the time of this review.

25

2.

AEOD Technical

Stud

Re orts

No AEOD technical

studies

were initiated from the reports

submitted

by Arizona Public Service Company'for Palo Verde

Units 1, 2,

and

3 in the assessment

period.

3.

Abnormal Occurrences

There were

no events classified

as

AOs at Palo Verde during

this period.

In.addition,

no events

were reported

as Appendix

C items ("Other

Events of Interest" ) in the quarterly

AO

reports.

4.

~57472

2

4

The licensee

submitted

52 50.72 reports in the assessment

period.

Many of these reports

were duplicates for each unit.

These reports

were compared to the 50.73 submittals to

determine if the licensee is reporting all

LERs that they are

required to report.

All events

reported

by these calls were

addressed

by an

LER, were too recent for an

LER to be received

or were not reportable

under

10 CFR 50.73.

5.

LER

ualit

The

LERs reviewed were professional

quality technical

reports.

The information was well organized,, detailed,

informative and

submitted

on time.

Many reports were updated

as

more

information became available.

t

~'M

( ~

l

0