ML17305B031

From kanterella
Jump to navigation Jump to search
Ack Receipt of 900620 Response to Violations Noted in Insp Repts 50-528/90-12,50-529/90-12 & 50-530/90-12
ML17305B031
Person / Time
Site: Palo Verde  
Issue date: 08/29/1990
From: Richards S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Conway W
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
References
NUDOCS 9009120186
Download: ML17305B031 (19)


See also: IR 05000528/1990012

Text

'0

>'- 2 9

1990

Docket Nos.

50-528,

50-529,

50-530

Arizona Public Service

Company

P.

0.

Box 53999,

Sta.

9012

Phoenix,

Arizona

85072-3999

Attn:

Mr. Milliam F.

Conway

Executive Vice President,

Nuclear

Gentlemen:

Thank you-for your letter of June

20,

1990 in response

to our Notice of

Violation and Inspection

Report Nos.

50-528/90-12,

50-529/90-12,

and

50-530/90-12,

dated

May 21,

1990, informing us of the steps

you have taken to

correct the items which we brought to your attention.

Your corrective actions

will be verified during

a future inspection.

Your cooperation with us is appreciated.

Sincerely,

/ ) jj +f (

S.

A. Richards,

Chief

Reactor Projects

Branch

CC:

J.

Levine,

APS

J

~

N. Bailey,

APS

T. Bradish,

APS

bcc w/copy of ltr. dated 6/20/90:

Docket File

Resident

Inspector

Project Inspector

G.

Cook

B. Faulkenberry

J. Martin

A. Johnson

J. Zollicoffer

State of Arizona

bcc w/o copy of letter dated 6/20/90:

H. Smith

REGION V ~)

D. Coe/jg ~

HMong

v'/M/90

P />f90

SRichards

e,/g/90

e

9009i20i8/i

Q

PDR

AQQgg 90<.)ip y

0 400528

F'DC

S /

NO

]

C

ES / .NO

]

S /

NO

YES /

NO

]

6 jg',

WILLIAMF. CONWAY

EXECUTIVEVICE PRESIDENT

NUCLEAR

Arizona Public Service Company

P.O. BOX 53999

~

PHOENIX. AIIIZONA85072-3999

102-01738-MFC/TRB/JJN

June

20,

1990

v

U. S. Nuclear Regulatory Commission

Document Control Desk

Washington,

DC

20555

Reference:

Letter from S. A. Richards,

Chief Reactor Projects

Branch,

to W. F.

Conway,

Executive Vice President

Nuclear,

Arizona Public Service

dated

May 21,

1990

Dear Sirs:

Subj ect.:

Palo Verde Nuclear Generating Station

(PVNGS)

Unit 1,

2,

and

3

Docket No.

STN 50-528

(License

No. NPF-41)

Docket No.

STN 50-529

(License

No. NPF-51)

Docket No.

STN 50-530 (License

No. NPF-74)

Reply to Notice of Violations 50-528/90-12-01, 50-530/90-12-01,

and

50-530/90-12-02

File

90-070-026

This letter is provided in response

to the inspection conducted

by Messrs,

D.

Coe, J. Ringwald, J. Sloan,

C. Myers, and P. Quells from March 4 th

h A

'1

ased

upon the results of the inspection,

three apparent violations

of NRC requirements

were identified.

The violations are discussed

in Appendix

A of the, referenced letter.

A restatement of the violations and PVNGS's response

are provided in Appendix A and Attachment 1, respectively,

to this letter.

Should you have any questions

regarding this response,

please

contact

me.

Very truly yours,

WFC/TRB/JJN/tlg

Attachments

~ CC

J.

B.

D. H.

T

L.

A. H.

A. C.

Martin

Coe

Chan

Gutterman

Gehr

Document Control Desk

Page

1 of 2

102-01738-WFC-TRB/J JN

June

20,

1990

APPENDIX A

NOTICE OF VIOLATION

Arizona Nuclear

Power Project

Palo Verde Unit 1 and

3

Docket Number 50-528

and 50-530

License

Numbers

NPF-41 and NPF-74

During an

NRC inspection conducted

on March 4 through April 14,

1990,

three

violations of NRC requirements

were identified.

In accordance

with the

"General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix

C (1989),

the violations are listed below:

A.

Unit 1 Technical Specifications, Section 3.3.1, requires in part that

a

minimum of two Excore Neutron Flux Logarithmic Power Level - High

instrument will be operable in Mode 5,

and allows for operation with

only one channel provided certain Action Statement

requirements

are met.

Contrary to the above,

from March 21,

1990, until March 24,

1990, all

four channels

of Excore Neutron Flux Logarithmic Power Level

instrumentation

were deenergized

by licensee

personnel

to perform

cabinet

and drawer repairs while Unit 1 was in Mode 5.

This is

a Severity Level IV violation applicable to Unit 1 (Supplement

I) ~

B.

10 CFR Part 50, Appendix B, Criterion V, states

in part that

instructions,

procedures,

or drawing shall include appropriate

quantitative or qualitative acceptance

criteria for determining that

important activities have been satisfactorily accomplished.

Contrary to the above, Material Non-Compliance [sic] Report,

90-RC-

0009, Conditional Request

Release,

did not include an appropriate

quantitative

acceptance

criteria in that it did not specify the maximum

allowable torque for us> on valve 3PRC-B-V-207.

The conditional release

appeared

to allow a maximum torque of 75 ft-lbs, whereas

the proper

maximum allowable

was

30 ft-lbs.

This is a Severity Level IV Violation applicable to Unit 3 (Supplement

I).

C.

Unit 3 Technical Specifications, Section 6.8.1, states

in part:

..."Written Procedures

shall

be established,

implemented,

and maintained

.covering the activities referenced

below:

'

Document Control Desk

Page

2 of 2

102-01738-WFC-TRB/JJN

June

20,

1990

This program is implemented,

in part,

by licensee

Procedure

14AC-OFP03,

"Control of Combustible/Flammable

Materials

and Liquids" which states

in

part in paragraph

3.2.10, that "combustible material shall not be stored

next to outdoor safety-related

water storage

tanks."

Contrary to the above,

on March 5, 1990,

two apparently untreated

wood

packing crates,

an apparently full 55 gallon drum with a National Fire

Protection Association tag labeled

3 for flammability (extreme hazard),

and a number of other

55 gallon drums similarly marked were stacked

immediately adjacent to the Unit 3 Condensate'torage

Tank (a safety-

related tank required for safe shutdown).

This is a Severity Level IV Violation applicable

to Unit 3 (Supplement

I).

Document Control Desk

Page

1 of 8

102-01738-I"FC/TRB/JJN

June

20,

1990

ATTACIIMENT 1

Re

1

to Notice of Violation 50-

28 90-12-01

I.

REASON FOR THE VIOIATION

The event

was

a result of a misinterpretation of the Technical

Specifications.

Unit 1 Management

reviewed Technical Specifications 3.3.1,

3.3.1

ACTION 4 (which describes

the action to be taken with only

one channel

operable but does not address

having no operable

channels),

and 3.0.3

(which describes

actions to be taken if a limiting condition

of operation is not met).

Based

on the fact that Technical

Speci.fication 3.0.3 is not applicable in Mode 5,

and that the action

statement for the condition with only one operable

charm'el

was being

met, unit management

concluded that removal from service of all the log

channels

would be consistent with the intent of the Technical

Specifications.

However, unit management

did not recognize that it

would not be acceptable

to voluntarily enter into a condition that is

not defined by the Technical Specifications.

CORRECTIVE STEPS

THAT HhVF. BEFN TAKEN AND THE RESULTS hCIIYI:,VED

The wiring in the

PPS cabinet'nd

the cabinet drafters

were reworked in

.accordance

with approved

work <<uthorization'documents.

Document Control Desk

Page

2 of 8

102-01738-WFC/TRB/JJN

June

20,

1990

On March 23,

1990,

the Plant Review Board

(PRB) reviewed the event,

the

Updated Final Safety Analysis Report (sections

7.1, 7.2,

and 15.4.6),

Combustion Engineering

Standard

Safety Analysis Report (sections

7.1,

7.2, 15.4.6),

and

NUREG 0852,

0800,

and 0857.

The

PRB determined that

there was no safety significance in having all log power channels

inoperable

based largely on the plant conditions

and the operabilty of

the startup

channels

and the Boron Dilution Alarm System.

There

was no

impact on the health and safety of the public.

Log channel

D was declared

operable at approximately

0938

MST on March

26,

1990.

This placed the unit within the Technical Specifications 3.3.1 Action 4,

a condition defined by Technical Specifications.

On

March 26,

1990 at approximately

1554 MST, log channel

A was declared

operable.

This placed the unit in compliance with Technical

Specification

LCO 3.3.1.

Log channel

B was declared operable at

approximately

1955

MST on March 26,

1990.

At approximately

2132

MST

on'arch

26-,

1990,

Log channel

C was declared

operable.

A plant guideline applicable

to Units 1, 2,

and

3 has been promulgated

defining APS's position on voluntarily entering

a condition not defined

by the Technical Specifications.

The plant guideline clearly

communicates

hPS's position that it is not acceptable

to voluntarily

enter

a condition not defined by tho Technical Specifications.

If such

a condition is experienced

because

of equipment failure,

.:".:::.ed!ate

Document Control Desk

Page

3 of 8

102-01738-WFC/TRB/JJv,

June

20,

1990

action must be taken to return to a condition defined by the Technical

Specifications.

III.

CORRECTIVE"STEPS

THAT WILL BE TAKEN TO AVOID VIOLATIONS

APS believes

the actions

taken

as described

above

are adequate

to

prevent recurrence.

IV.

DATE WHEN FULL COMPLIANCE WAS ACHIEVED

Full compliance

was achieved

on March 26,

1990,

when the

Log channel

D

was declared

operable.

I

f

Document Control Desk

Page

4 of 8

102-01738-WFC/TRB/JJN

June

20,

1990

Re

1

to Notice of Violation 50-530 90-12-01

I.

REASON FOR THE VIOLATION

Material Nonconformance

Report

(MNCR) 90-RC-0009

was initiated to

document

the packing leakage

on the Reactor Coolant System

(RCS)

Pressurizer

instrument root valve

3PRCBV207.

The nut and eyebolt

on the

packing gland follower were galled which limited the ability to adjust

the valve packing to reduce

leakage.

Engineering analyzed

the

feasibility of installing a spacer

around the existing eyebolt/nut

and

threading

an oversized nut on the remaining eyebolt threads.

The

analysis

was performed to calculate

1) the compressive

forces

and

potential buckling of the spacer

and 2) tensile/shear

forces

and

potential stripping of the eyebolt and the

new nut which was

made of a

material different than the original nut.

To assure

that the

calculation was conservative,

Engineering applied

a factor of 2.5 to the

nominal

30 ft-lbs field specification and then analyzed for a torque of

75 ft-lbs.

The calculations

demonstrated

that the installation of the

spacer

and new nut was acceptable.

An analysis of the pins which connect

the eyebolts

to .the valve body was

not performed nor required because

the existing analysis of the pins::as

still valid.

The change

involved only new spacers

and nuts.

An

increased

torque

was not requested

for the conditional rel.',u:

. "Ie

l

I

Document Control Desk

Page

5 of 8

102-01738-WFC/TRB/JJN

June

20,

1990

assumption

was correctly made that the valve would be torqued using

"good mechanical

judgement" in accordance

with procedure

"Fastener

Tightening/Preload"

(30DP-9MP02)

step 3.1.8

and 3.1.9.

This procedure

provides detailed guidance

on torquing based

on material,

dimensions,

application, etc.

Therefore,

no torque specification

was required.

The original preparation of the work order did not include

a value for

the torque specification other than the use of "good mechanical

judgement".

Attached to the work order

was

a copy of the

flNCR

conditional release for the installation of the spacer

and oversized

nut.,

During the review process of the work order

(and therefore

the

MNCR conditional release),

the bounding analysis of 75 ft-lbs in the

disposition for the

MNCR conditional release

was misinterpreted

to mean

a limiting field specification.

The work order was subsequently

revised

to include the restriction of 75 ft-lbs.

The misinterpretation of the

MNCR disposition

was caused

by Engineering including bounding design

calculations within the conditional release

and not specifying that the

information was for analysis only.

II.

CORRECTIVE STEPS

Tl'fAT 1fAVE BFl'.N TAKEN AND THE RFSULTS AClfTFVFD

As a result of this event,

an investigation

was conducted.

A

description of the event

and

f.he lessons

learned

were distr buted to the

site technical support personnel.

These

lessons

learned

w;","

..:,"crated

Document Control Desk

Page

6 of 8

102-01738-WFC/TRB/JJN

June

20,

1990

in site technical support group communication meetings.

In summary,

the

lessons

learned which were discussed with Engineering included:

1)

Precisely stating the problem and scope

(which should be

appropriately

documented),

2)

Clearly stating the required

"as left" condition,

3)

Technically reviewing dispositions with a questioning attitude,

and

4)

Following up Engineering dispositions/analysis

work with formal

verbal communication

when appropriate

to ensure

understanding

of

the issues

and resolution.

III.

CORRECTIVE STFPS

THAT WILL BF. TAKEN TO AVOID VIOLATIONS

APS believes

the actions

taken as described

above are adequate

to

prevent recurrence.

IV.

DATF. WHEN FULL COMPLIANCE WAS ACHIFVFD

Full compliance

was achieved

o>> April 17,

1990,

when the Work Order was

revised to specify

30 ft-lbs.

c~

Document Control Desk

Page

7 of 8

102 - 01 7 38 - WFC/TR8/J J N

June

20,

1990

Re

1

to Notice of Violation 50-530 90-12-02

EASON FOR THE VIOLATION

The fifty-fivegallon drums of flammable material,

temporarily located

adjacent

to the Unit 3 Condensate

Storage

Tank, contained

tendon grease

which was staged for pickup and disposal.

The individuals responsible

for conducting the surveillance test were not aware of the requirement

to obtain a transient combustible/flammable

permit for interim staging

adjacent

to t."he condensate

storage

tank.

II.

CORRECTIVE STEPS

THAT HAVE BEEN TAKEN AND THE RESULTS ACHIEVED

The Director of Operations

and Maintenance

issued

a

memo to onsite

supervisors

and managers

identifying the safety related

tanks

and

reiterating the requirement

to not store combustible/flammable

material

within 50 feet of the tanks.

Daily fire prevention tours of the plant have been conducted

to monitor

the control of combustible/flammable

materials

and to initiate

corrective actions.

0

A label request

form has

been initiated to evaluate

posting warning

labels

on the condensate

storage

tanks,

the refueling water

>>)
s,

<<>>d

Document Control Desk

Page

8 of 8

102-01738-WFC/TRB/J JN

June

20,

1990

the reactor

makeup water tanks.

III.

CORRECTIVE STEPS

THAT WILL BE TAKEN-TO AVOID VIOLATIONS

The transient

combustible material program will be revised to clarify

the administrative controls for storage

and inspection of transient

combustible materials.

Engineering is conducting

a review and

verification of plant areas

where the storage of flammable material

should be controlled.

Maps will be added to the procedure

to identify

areas

where

a transient

combustible permit may be applicable.

Expected completion date:

July 31,

1990.

IV.

DATE WHEN FULL COMPLIANCE WAS ACHIEVED

Full compliance

was achieved

on March 5,

1990,

when the combustible

material

was removed.

.~