ML17305A431

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SALP Repts 50-528/89-48,50-529/89-48 & 50-530/89-48 for Nov 1988 to Oct 1989.Category 2 Assigned in Areas of Plant Operations,Radiological Controls,Emergency Preparedness & Security
ML17305A431
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 11/22/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17305A430 List:
References
50-528-89-48, 50-529-89-48, 50-530-89-48, NUDOCS 8912110100
Download: ML17305A431 (76)


See also: IR 05000528/1989048

Text

SALP BOARD REPORT

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

SYSTEMATIC ASSESSMENT

OF LICENSEE

PERFORMANCE

50-528/89-48,

50-529/89-48,

50-530/89-48

ARIZONA NUCLEAR POWER

PROJECT

PALO VERDE NUCLEAR GENERATING STATION

NOVEMBER 1, 1988

THROUGH OCTOBER 31,

1989

TABLE OF

CONTENTS

I.

Introduction

II.

Summary of Results

A.

Effectiveness of Licensee

Management

B.

Results of Board Assessment

C.

Changes

in SALP Ratings

III. Criteria

~Pa

e

IV.

Performance

Analysis

A.

B.

C.

D.

E.

F.

G.

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency

Preparedness

Security

Engineering/Technical

Support

Safety Assessment/equality

Verification

5

8ll

13

15

17

19

V.

Supporting

Data and Summaries

A.

Licensee Activities

B.

Direct Inspection

and Review Activities

C.

Enforcement Activity

D.

Confirmation of Action Letters

E.

, AEOD Events Analysis

TABLES

22.

22

23

24

24

24

Table 1 - Inspection Activities and Enforcement

Summary

Table

2 - Enforcement

Items

Table

3 - Synopsis of Licensee

Event Reports

Attachment

1 - The Office for Analysis and Evaluation of Operational

Data

'AEOD) Input to SALP Review

INTRODUCTION

The Systematic

Assessment

of Licensee

Performance

(SALP) is an integrated

NRC staff effort to collect available observations

and data'n

a periodic

basis

and to evaluate

a licensee's

performance

based

on this information.

The program is supplemental

to normal regulatory processes

used to ensure

compliance with NRC rules and regulations.

It is intended to be

sufficiently diagnostic to provide

a rational basis for allocating

NRC

resources

and to provide meaningful

feedback to the licensee's

management

r'egarding the NRC's assessment

of their facility's performance in each

functional area.

An NRC.SALP Board,

composed of the members listed below, met in the

Region

V office on November 13,- 1989, to review observations

and data

on

the licensee's

performance

in accordance

with NRC Manual Chapter 0516,

"Systematic

Assessment

of Licensee

Performance,"

dated August 16, 1989.

The guidance, and evaluation criteria are

summarized in Section III of

this report.

The Board's findings and recommendations

were forwarded to

the

NRC Regional Administrator for approval

and issuance.

This report is the NRC's assessment

of the licensee's

safety performance

at Palo Verde for the period November 1, 1988, through October 31, 1989.

The

SALP Board for Palo Verde was composed of:

~"A. Chaffee , Deputy Director , Division of Reactor Safety

and Projects ,

Region

V (RV) - Board Chairman

  • "G.

Knighton , Director , Project Director ate

V,

NRR

  • "D.

Kirsch , Chi ef , Reactor Safety Branch ,

RV

.

"*G. Yuhas , Chief , Emergency

Prepar edness

and Radiological Protecti on

Branch ,

RV

  • R. Pate , Chief , Nuclear Material s Safety

and Safeguards

Branch ,

RV

"*S. Richards , Chief , Reactor Projects

Section II,

RV

  • L. Miller, Chief , Operations

Section ,

RV

"R.

Huey , Chief , Engineering Secti on ,

RV

"R. Fish , Chief ,

Emergency

Preparedness

Secti on,

RV

""T. Chan , Project Manager,

PD 5 ,

NRR

""H. Davis , Project Manager ,

PD 5 ,

NRR

""T. Pol ich , Seni or Resident Inspector ,

RV

    • M. Ang , Project Inspector ,

RV

H. Cillis , Seni or Radi ati on Speci al ist ,

RV

  • L. Norderhaug , Safeguards

Inspector ,

RV

"Denotes voting member in functional area of cognizance.

  • "Denotes voting member in al l functional areas.

II.

Summar

of Results

A.

Effectiveness of Licensee

Mana ement

The momentum of previously existing weaknesses

resulted

i'h a general

continuance

of past weak performance of the site during the first

half of the

SALP period.

In recognition of the magnitude of the

problems at the site,

APS instituted

numerous

changes

in Palo Verde

management.

A new Executive Vice President,

Nuclear,

was appointed

to head

Palo Verde and

assumed

those duties in May, 1989.

Other

changes

in the Palo Verde management

team included replacement of-

the Vice President,

Nuclear Production;

replacement of the gA

Director; addition of a Vice President,

Nuclear Safety

and

Licensing; addition of a Plant Director; replacement

of the Director

of Standards

and Technical

Support;

replacement

of the Nuclear

Training Manager;

replacement

of two of the Unit Plant Managers;

and

addition of a Relief Plant Manager.

Most changes

appeared

to be

positive in nature despite

the resultant perturbations

caused

by the

interruption of management

continuity.

The

new management

team continued to implement existing improvement

programs

and instituted additional

needed

improvements to attempt to

identify and correct weaknesses.

These

programs

included;

Revamping the nonconformance

identification and corrective

action programs

Performance'f

a Preventive

Maintenance

Program self-assessment

Performance

of a Design Configuration Assessment

Formation of unit restart task forces to improve plant restart

performance

Formation of three training program project .management

task

forces to improve the management

and performance of training

activities

Formation of a Management

Review Committee to provide

management

oversight of the restart of Units 1 and

3

Contracted for and received

an independent

assessment

of- safety

oversight groups

'Contracted for and received

a self-initiated

SALP

Contracted for and received

a self-initiated Maintenance

Team

Inspection

Requested

performance of an

INPO design engineering

assessment

The

new Palo Verde management

team was receptive to NRC initiatives

and exhibited

an eagerness

to improve identified weaknesses.

Although improvements

have

been noted during the last six months of

the assessment

period,

the above noted management efforts had not

been fully completed

as of the end of the period, therefore the full

impact of these actions

remains to be seen.

A need for increased direct observation of plant activities by Palo

Verde management

continued to exist.

Strong management

support

and

insistence

in full implementation of all new programs is

recommended.

The licensee

also

needs

to conduct periodic

assessments

of the effectiveness

of their performance

.improvement

initiatives to provide for timely mid-course corrections,

as

needed.

B.

Results of Board Assessment

Overall, the

SALP Board found the performance of NRC licensed

activities by the licensee

to be acceptable

and directed toward safe

operation of Palo Verde.

The

SALP Boar d has

made specific

recommendations

in most functional areas for licensee,

management

consideration.

The results of the Board's

assessment

of the

licensee's

performance in each functional area,

including the

previous

assessments,

are

as follows:

Functional= Area

Rating

Rating

Last

This

Period

Period

Trend*-

A.

B.

C.

D.

E.

F.

G.

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency

Preparedness

Security

Engineering/Technical

Support

Safety Assessment/equality

Verification

improving

1mprov1 llg

The trend indicates

the

SALP Board's appraisal

of the

licensee's

direction of performance in a functional area

near

the close of the assessment

period such that continuation of

this trend may result in a change in performance

level.

Determination of the performance

trend is made selectively

and

is reserved for those instances

when it is necessary

to focus

-.NRC and licensee attention

on an area with a declining

performance trend,

or to acknowledge

an improving. trend in

licensee

performance.

It is not necessarily

a comparison of

performance

during the current period with the previous

period.'.

Chan

es in SALP Ratin

s

Licensee

performance in the Radiological Controls area

improved from

a category

3 to a low category 2.

The increased

rating resulted

from licensee

improvements of its Radiological Controls procedures,

organization, training and day-to-day performance.

Licensee

performance

in the area of Plant Operations marginally

improved to a category

2 rating due to a reduction of significant

events directly attributable to the operations

department. 'owever,

the Board recommendations

also emphasize

several

improvements that

are considered

necessary

to maintain the category

2 rating.

Licensee

performance in the Safety Assessment/guality

Verification

area

remained

a category 3.

This was attributed to a lack of

management utilization of gA and the oversight groups to identify

weak areas of performance,

and the failure in many cases

to

implement meaningful corrective actions,

although

improvement was

noted toward the end of the period.

Licensee

performance in the Maintenance/Surveillance

area declined

from a category

2 to a category

3.

This was attributed to existing

past weaknesses

that remained uncorrected

and were finally

manifested significantly during this period.

Host noteworthy of

these

weaknesses

were maintenance

practices that resulted in

multiple equipment malfunctions during the March 3, 1989 Unit 3

Unusual

Event.

Licensee

performance in the Engineering/Technical

Support area

declined from a category

2 to a category

3.

Much of the decline was

attributed to long standing

weaknesses

in the management

of the

System Engineering organization,

which the licensee

has

been unable

to effectively address.

The lack of a sense of ownership and

acknowledgement

of responsibility by both corporate

and .system

engineers

appeared

to contribute to plant performance

problems.

III. CRITERIA

Licensee

performance is assessed

in selected

functional areas,

depending

on whether the facility is in a construction or operational

phase.

. Functional

areas

normally represent

areas significant to nuclear safety

and the environment.

Some functional areas

may not be assessed

because

of little or no licensee activities or lack of meaningful observations.

Special

areas

may be added to highlight significant observations.

. The following evaluation criteria were used,

as applicable to assess

each

functional area:

1.

Assurance of quality, including management

involvement and control;

2.

Approach to the resolution of technical

issues

from a safety

standpoint;

3.

Responsiveness

to

NRC initiatives;

4.

Enforcement history;

5.

Operational'and

construction

events (including response to, analyses

of, reporting of, and corrective actions for);

6.

Staffing (including management);

and

7.

Effectiveness

of the training and qualification program.

However, the

NRC is not limited to these criteria and others

may have

been

used where appropriate.

On the basis of the

NRC assessment,

each functional area evaluated is

rated according to three performance

categories.

The definitions of

these

performance

categories

are as follows:

1.

Cate or

1.

Licensee

management

attention and involvement are

rea

s y evident

and place

emphasis

on superior performance of

nuclear safety or safeguards activities, with the resulting

performance substantially exceeding regulatory requirements.

Licensee

resources

are ample

and effectively used

so that a high

level of plant and personnel

performance is being achieved.

Reduced

NRC attention

may be appropriate.

2.

Cate or

2.

Licensee

management

attention to and involvement in the

per ormance of. nuclear safety or safeguards

activities is good.

The .

licensee

has attained

a level of performance

above that needed to

meet regulatory requirements.

Licensee

resources

are adequate

and

reasonably

allocated

so that good plant and personnel

performance is

being achieved.

NRC attention

may be maintained at. normal levels.

3.

Cate or 3.. Licensee

management

attention to and involvement .in the

per ormance of nuclear safety or safeguards

activities. are not

sufficient.

The licensee

s performance

does not significantly

exceed that needed to meet minimal regulatory requirements.

Licensee

resources

appear

to be strained or not effectively used.

NRC attention should be increased

above normal levels.

IV.

PERFORMANCE ANALYSIS

The following is. the Board's

assessment

of the licensee's

performance in

each of the functional areas,

plus the Board's conclusions for each

area.

and its recommendations

with respect to licensee

actions

and management

emphasis.

II.

~PI

t II

tt

1.

~Anal sis

During the assessment

period, the licensee's

plant operations

activities were observed routinely by both the residents

and

the regional staff.

A total of 2627 hours0.0304 days <br />0.73 hours <br />0.00434 weeks <br />9.995735e-4 months <br /> of inspection effort

were devoted to this functional area.

During this

SALP period

significant site operations

management

changes

have occurred,

including:

new or different Plant Managers at each unit; a new

Vice President,

Nuclear Production;

the addition of three

Assistant Plant Managers,

a Relief Plant Manager

and a Plant

Director.

Experienced

personnel

were hired for the positions

of Executive Vice President;

Vice President,

Nuclear Safety and

Licensing; Site Services, Director; guality Assurance, Director;

Radiation Protection

and Chemistry Manager,

and Training

Manager.

Most of the

new managers

were hired during the last

half of the assessment

period, with the majority reporting in

t

the last quarter.

Increasing

management

experience

and

staffing are considered positive accomplishments,

however the

ability of the

new management

team to improve plant operations

has not yet been fully demonstrated.

The licensee's

performance

was rated

as Category

3 improving

during the previous

SALP rating period.

The rating had

declined primarily due to events at Unit 1 and the lack of

prompt and decisive efforts by senior corporate

management

to

establish

a working atmosphere

which encourages

critical

assessment

during the conduct of operations.

During this

SALP

period, several

events

occurred in which the licensee

continued

to exhibit non-conservative

attitudes

toward operations

and an

inability to learn from previous problems,

however actions

taken for several

operational

type problems at the end of the

assessment

period were considered

conservative

and appropriate.

With the exception of .increasing

management

staffing including

a completely different operations

management staff at Unit 1,

the previous

SALP Board recommendations

concerning striving to

ensure that plant operations

are conducted in a conservative

formal manner

and that problems

be promptly addressed

continue

to be appropriate.

The licensee

accepts

NRC initiatives in a positive spirit;

however, the resolution of these matters often requires

continued

NRC scrutiny to ensure corrective actions

are taken.

Some

examples

are slow progress

in improving simulator

fidelity, licensee

management's

lack of direct observation of

plant activities and'everal

examples of failure to control

equipment

and system status.

Several

events

which reflect negatively

on the plant operations

functional area included:

an auxiliary operator failing to

completely close

a Hain Feedwater

Pump

(HFP) bypass

valve

resulting in the fatigue failure of a drain line and

a forced

outage at Unit 2;

a licensed operator failing to perform a

procedure

step while flashing the main generator field

resulting in a turbine trip at Unit 2; and

an operations

support technician repeatedly

operating the condensate

demineralizer

system after abnormal

indications were observed

at Unit 2.

Escalated

enforcement

was taken in this functional area for

inadequate training and incor rect operation of the Atmospheric

Dump Valves during the Unit 3 Unusual

Event of March 3, 1989.

In addition, several

other violations were identified in this

functional area.

These violations all dealt with failure to

follow procedures

which resulted in:

unnecessarily

increasing

the Reactor Coolant System

(RCS) cooldown at Unit 2; rendering

inoperable

the only operable

ADV at Unit 1; expired flammable

storage

permits posted

on flammable storage

containers

at Unit

1; lowering the Spent

Fuel

Pool level to less than the

Technical Specification

minimum a't Unit 1; spil.laqe of RCS

water into the refueling cavity at Unit 3; not switching the

ji

nuclear instrumentation

High Voltage meter from Startup to

Control

as required during a reactor startup at Unit 2; and not

making a required licensed operator report on time.

During this

SALP period the regional licensing examiners

conduct'ed

two replacement

examinations

and are in the process

of completing

a licensed operator requalification program

evaluation.

The operator

replacement

examination results

indicate that the traininq provided to initial and upgrade

'icense

candidates

is satisfactory.

The pass/fail ratio during

this

SALP period has increased

from 18/3 to 33/1.

Even though

the upgrade

and the initial licensed operator training progi ams

appear

to be satisfactory,

there is a need for greater

ownership

and involvement in the training program from the

units'perations

departments.

For the past several

SALP periods the'issue

of training

provided by the facility's plant specific simulator has

been

a

continuing concern.

The concern

was reconfirmed

by the

operator's inability to operate

the Atmospheric

Dump Valves,

(ADVs) from the control

room using the methods taught in the

simulator, during the Unit 3 Unusual

Event.

I

The licensee

has recently contracted with a simulator

manufacturer to. upgrade

and make repairs to the site specific

simulator.

This action was taken after years of in-house

efforts that failed to produce

a reliable simulator,

and to

meet the

NRC requirements

that each facility have

a certified

simulator by May of 1991 in order for NRC operator

licensing

examinations to be administered.

Non-licensed operator training was also questioned

during the

Unit 3 Unusual

Event due to Auxiliary Operators

(AO) being

called

upon to perform valve operation at the remote

shutdown

panel without any previous training on the equipment.

In

addition-, during the

same event,

one

ADY was

damaged

when an

AO

improperly operated

the valve.

This was attributed in part to

inadequate

training of the

AO.

A review of the licensee's

Emergency Operating

Procedures

(EOPs) conducted during this

SALP period indicated that the

EOPs were usable but were overly complex and contain

numerous

problems

and inconsistencies.

Two previous inspections

identified similar problems.

This indicates

an inability of

the management

to correct this

known deficiency.

Two

examinations

in this period also identified a reluctance

by

some operators

to use or refer to normal operating procedures.

This resulted in significant valve 'lineup errors during the

examinations.

The licensee's fire protection personnel

responded

to one major

fire during this assessment

period involving a capacitor

bank

fire in the

525

KV switchyard.

Although this fire was brought

under control, it burned for over an hour before sufficient

Aqueous Film Forming

Foam was available to extinguish the fire.

In addition, -a recent violation and ongoing un'reso]ved matters

concerning qualifications of the Fire Protection Supervisor

and

maintenance'ersonnel,

coordination of offsite fire department

assistance,

and engineering

evaluations

on fire doors indicate

a decline in fire protection. program performance

since the last

SALP period.

Overall, operations

personnel

are knowledgeable of plant

systems

performance.

However, during several significant and

complicated operational transients,

weak operations

personnel

performance

was attributable to inadequate training.

Plant

shift crews generally conduct thorough shift turnovers

and

briefings which include discussions

with other unit departments

such

as chemistry, radiation protection and work control.

However,

improper valve status

and system lineups during both

complex and routine plant operations

continue to be a problem.

The ability of the

new site and corporate

management

team to

effect a long term change in plant operational

performance is

still unproven.

2.

Performance

Ratin

Performance

Assessment - Category

2

3.

Board Recommendations

The licensee

should strive to ensure that all operations,

especially valve and system manipulations,

are conducted in a

formal, conservative

manner at all units.

Licensee

management

should continue actions initiated to assure that there is both

sufficient management

staffing and appropriate

management

involvement in problem evaluations

and resolution.

Training,

specifically, requires

improvement

and greater

management

attention.

Priority attention should be given to conducting

thorough evaluations of problems

and establishing

a working

atmosphere

which encourages

thoughtful, cr'itical assessments

of

all phases

of plant operations.

B.

Radiolo ical Controls

1.

~Anal sis

Nine routine

and two special

inspections

related to

'radiological controls were performed by the NRC's regional

office and resident staff during this assessment

penod.

Over

869 hours0.0101 days <br />0.241 hours <br />0.00144 weeks <br />3.306545e-4 months <br /> of inspection time were expended in this functional

area.

During the previous

SALP period

a total of two Severity Level

III vtolations,

seven Severity Level IV violations and two

Severity Level

V violations were identified.

= The Severity

.Level III violations resulted in an escalated

enforcement

\\

action with the imposition of civil penalties.

For the last

assessment

period the license

was assigned

a Category

3 rating.

The licensee

has

been responsive to the previous

SALP report

and other

NRC initiatives in this functional area.

Policies

for assurance

of quality and management's

commitment to the

implementation of a strong radiation protection program were

emphasized

and conveyed to the staff'during this

SALP period.

This is reflected

by the licensee's

overal] performance in .

radiological controls, which showed

improvement during extended

periods of continuous multiple reactor

outages.

Many of the

licensee's

radiological control procedures

were strengthened.

Other

improvements

included:

organizational

changes

intended

to strengthen

the Chemistry and Radiation Protection group;

filling of a key management position vacated during the

November'987 reorganization;

increases

in the chemistry and

radiation protection technician staffing levels;

ALARA planning

and preparation for radiological work during outages;

General

Employee Training and Advanced Radiation Workers Training

programs;

and the evaluation of events.

The licensee's

selection criteria and training program for contractor

radiation protection personnel

were also strengthened.

The

licensee's

laboratory measurements

of radioactivity in

effluents were determined to be satisfactory.

Transportation

of radioactive materials,

waste

management

and environmental

monitoring were performed without incident during this

SALP

peri Od.

Although management

has

been very responsive

in addressing

NRC-

concerns,

corrective actions

are sometimes

delayed

and

may not

be effective in correcting the root cause of the problem,

as

indicated

by occasional

repetition of events.

In addition,

several

examples

were identified indicating a need for more

pro-active

management

involvement.

For example:

(1)

The licensee audit findings involving the Americium check

sources

were not resolved in a timely manner.

(2)

Instances

of chloride, sulphate

and sodium intrusion into

the condensate

from polishing demineralizer

systems

continue to occur, particularly at .Unit 1..

The condition

of in-line instrumentation

used to monitor water quality

in steam generators

had declined.

(3)

There

have not been major improvements in the reduction .of

personnel

skin and clothing contamination events.

II

(4)

Numerous deficiencies in the implementation of basic

radiation protection measures

by the refueling contractor

went unreported to APS management until it was brought to

.

their attention by the

NRC.

(5)

An individual exceeded

his administrative whole body

exposure limit becau'se

of poor surveys,

and

due to a

10

failure to properly review survey records

and the

individual's prio~ exposure

records.

This problem was

similar to the events

leading

up to the over exposure

event during the last

SALP period.

(6)

. ALARA exposure

estimates

established

for performing eddy

current inspection

and repair of Unit 1 Steam Generators

were exceeded

in part due to the erroneous

plugging of one

tube.

(7)

Weaknesses

in the training of Radiation Protection

Instrumentation

Technicians

were

known to exist for at

least two years before

an acceptable

training program was

developed

and approved in Hay of 1989;

however, the

new

training had not been

implemented

as of September

1, 1989.

The licensee's

efforts to improve the reliability of the

Radiation Honitoring Systems

(RHS) does not appear to have

been

fully effective.

This is reflected

by the numbers of LERs and

Special

Reports that have

been identified in this area during

this and the previous

SALP period.

During this

SALP period,

approximately

90K of the fifteen LERs and ten Special

Reports

related to radiological controls were associated

with the

RHS.

The total occupational

doses in Units 1,

2 and

3 through

October 19, 1989, were 332 rem,

36 rem and 232 rem,

respectively.

The annual

ALARA goals established

for these

Units for 1989,

were 340 rem,

50 rem and 215 rem, respectively.

The reason for exceeding

the

ALARA goals in Unit 3 was

attributed to the extended refueling outage

and it appears that

Unit 1's

dose could have

been

lower if it had not been for the

licensee's

performance in the inspection/repair of the Unit 1

Steam Generators.

The licensee's

enforcement history during this

SALP period

showed considerable

improvement over the previous

SALP period.

There were five Severity Level IV violations.

The violations

involved improper posting of a high radiation area,

improp'er

posting of a contaminated

area,

improper labeling and control

of non-exempt quantities of Americium-241 sources,

a radiation

monitor which did not have any sampling media installed

and an

environmental

monitor's flow meter which was not properly

adjusted.

In addition,

two Non-cited Violations were

identified during this

SALP period.

They included

one Severity

Level IV violation involving the failure to perform a leak test

of one check source

and one Severity Level

V violation

- involving an unauthorized entry into a high radiation area

by a

worker.

2.

Performance

Ratin

Performance

Assessment

- Category

2

3.

Recommendations

11

The Board emphasizes

the need for continued

improvement in this

area

and specifically recommends that the licensee

be-

aggressive

in maintaining radiation monitoring equipment,

instrumentation,

and practices for chemistry control -and

. analysis.

Management

should take

a more pro-ac'tive ro'te in

assuring that basic occupational

radiation protection measures

are accomplished

Haintenance/Surveillance

l.

~Anal sis

The licensee's

performance

was rated

as Category

2 during the

last

SALP period.

Strengths

included

a good chemistry

surveillance

and control program, only two violations and

no

plant shutdowns attributable to maintenance.

Weaknesses

last

SALP period included

a large maintenance

backlog,

poor or

inadequate

work planning and little improvement in the conduct

of maintenance.

During this assessment

period the corrective

maintenance

backlog continued to increase

and several

events'ere

directly attributable to poor maintenance.

In general,

work planning

and the conduct of maintenance

has continued to

be weak inspite of management's

efforts to correct these

areas,

and in several

respects

the significance of long standing

weaknesses

was more clearly focused during this assessment-

period by several

operational

events.

This functional area

was observed routinely during the

assessment

period by both the resident

and regional inspection

staff.

The Augmented Inspection

Team which investigated

the

March 3, 1989'Unusual

Event at Unit 3 had significant findings

in this functional area.

A Maintenance

Team Inspection

was

conducted during this assessment

period.

Approximately 1556

hours of inspection effort were devoted to this functional

area.

Strengths

included the rigorous maintenance

performed

by

the Operational

Computer System personnel

and

a dedicated

snubber testing facility and staff.

Additionally, the licensee

has recently established

a 12-week rolling schedule to

coordinate preventive

maintenance

and reduce safety system

unavailability due to maintenance.

Several

deficiencies in the Maintenance/Surveillance

area were

noted in the Augmented Inspection

Team (AIT) report and were

the subject of escalated

enforcement:

failure to properly

maintain

and test

emergency lighting in the area of the

Atmospheric

Dump Valves (ADVs); failure to implement an

adequate

Preventive

Maintenance

(PH) program to ensure

'perability

of the ADYs; and failure to correct the Steam

Bypass Control System

(SBCS) permissive timer problem

identified in a July 1988 Unit 3 Post Trip Review Report.

The Maintenance

Team Inspection

(MTI) noted three major

concerns:

inadequate

attention to detail in work

12

implementation;

inadequate

work planning;

and inadequate

pr oblem resolution.

An example of inattention to detail in work implementation

was

noted by the MTI during an emergency diesel

generator

surveillance test.

The voltage to be adjusted

was between

3694

and 3794.

The fixed volt meter

used to measure

the voltage

had

100 volt divisions, which appeared

to be outside the accuracy

. limits needed.

Furthermore,

the technician

recorded

an

out-of-specification reading of 3795 and signed off the task as

complete without noting the discrepancy.

Licensee

management

developed

and implemented short term

maintenance

actions

as

a result of the Unit 3 Unusual

Event

prior to restarting Unit 2.

However, significant programmatic

improvements

and changes

were not evident late in the

SALP

period.

For example,

the NTI noted deficiencies in the

development of maintenance

work plans, in the implementation of

maintenance

work instructions,

and in the root cause

analyses

which should

have resulted in the development of comprehensive

corrective action plans.

The licensee exhibited

an inability to resolve long standing

weaknesses

in the control of equipment status

(maintenance

backlog), including both the adequacy of governing procedures

and work instructions,

and adherence

to procedures

and

instructions

by the plant staff.

Such deficiencies resulted in

notices of violation for failure to follow procedures

which

resulted in an Emergency Diesel Generator

(EDG) fuel line

disconnecting

from the cylinder while the

EDG was running at

Unit 1, and

an

ADV nitrogen supply regulator being assembled

at

Unit 2 on verbal instructions,

which deviated

from the approved

work order and technical

manual.

The licensee

often did not get to the root cause of problems,

and in several

cases,

known problems persisted

because

they

were not thoroughly addressed.

For example,

galvanic corrosion

which occurred

on Emergency Diesel Generator

(EDG) intercooler

drain plugs at Unit 3,

and then at Unit 2 during the last

SALP

period recurred in April 1989 on a Unit 2

EDG intercooler elbow

fitting before all susceptible

steel fittings were replaced.

Late in the

SALP period, the licensee

stated their intentions

to establish

a basis for.all maintenance

tasks.

This

initiative appears

to be good.

However,

program implementation

remains to occur.

Overall, maintenance craft are knowledgeable

and capable of

performing quality maintenance.

The craft still need to

develop

a more inquisitive attitude regarding the performance

of work.

In several

instances

maintenance

personnel

were

hindered

by inadequate

work planning, lack of supervisory

guidance,

lack of engineering direction and management's

13

failure to respond to maintenance

program deficiencies in the

past.

2.

Perfor mance Ratin

3.

Performance

Assessment

- Category

3

Board Recommendations

Licensee

management

should strive to ensure

work 'control

instructions

are clear and complete.

The licensee

maintenance

craft should ensure

they follow procedures,

and request

management

and engineering

assistance

when problems

are

encountered.

Additionally,. planner coordinators

should

be more

aggressive

in enlistinq the system engineers'upport

in the

correction of non-routine equipment problems.

Maintenance

management

should increase efforts to observe

ongoing work and

provide corrective feedback into the maintenance

program.

0.

Emer enc

Pre aredness

1.

~Anal sis

During this

SALP period, approximately

116 hours0.00134 days <br />0.0322 hours <br />1.917989e-4 weeks <br />4.4138e-5 months <br /> of inspection

effort were utilized to assess

the licensee's

Emergency

Preparedness

(EP) Program.

This included the observation of

one exercise

and two routine inspections.

The previous

SALP

board

recommended

an emphasis

on timely resolution of

identified deficiencies

and encouraged

the licensee to evaluate

the interface

between the emergency planning and site

operations

departments.

Management

involvement affecting the

EP Program

has increased

since the last appraisal.

This was evidenced

by management

directives prior to and during the 1989 exercise in support of

emergency

preparedness

and by management participation during

the exercise.

Management

presence

during

NRC exit interviews

was also noted to have increased.

Policies regarding the

conduct of the dress

rehearsal

and the exercise

were well

stated

and understood.

The licensee's

gA program continued to meet

NRC requirements

and to provide for an independent

audit of the

EP Program

including evaluation of the interface with state

and local

governments.

The licensee's

efforts to resolve technical

issues

from .a

safety standpoint

were generally

sound,

but resolutions

were

not always timely.

For instance,

the licensee

had identified

numerous

areas

on. site where the plant public address

system or

sirens

may be inaudible.

This problem was

known to the

licensee for a number of years;

however,

the resolution of the

problem was scheduled for 1991.

It appears

the licensee

had

focused

on a more comprehensive

resolution than was actually

14

needed to address

the concern.

The licensee'as

added

numerous

facilities and personnel

to the emergency notifications lists;

added

more security

sweeps;

and provided pocket pagers

to key

personnel

to insure personnel

are notified of emergency

events

and instructions.

Licensee

management

has demonstrated its responsiveness

to

NRC

initiatives.

Items identified by-the

NRC have been evaluated

by

management

and- acted

upon.

Three areas

addressed. in NRC

inspection reports

were checked

and all were noted to have

been

improved.

The three areas dealt with General

Employee Training

(GET) for the Mater Reclamation Facility personnel;

further use

of the simulator for emergency

preparedness

traininq; and

activation times for the emergency

response facilit)es.

There were

no violations of NRC requirements

observed in the

area of emergency

preparedness

during this

SALP period.

1

Two operational

events

were examined this

SALP period.

One

involved a loss of communications capability for Unit 1.

The

event

was promptly and conservatively classified

as

an Unusual

Event and appropriate notifications and reports

were completed

in a timely manner.

The Augmented Inspection

Team noted

communications

problems that occurred during the March 3, 1989

Unit 3 Unusual

Event.

Staffing of the

EP Program appears

adequate.

Key positions

are

identified and responsibilities

are well defined.

Expertise is

usually available within the licensee's staff,

and consultants

have

been appropriately

used to address

problems affecting

emergency

preparedness.

Vacancies within the

EP Program

have

usually been'illed in a timely manner;

however, there

have

been three vacancies

open during the last year and only one

has

been filled.

The vacancies

when filled should further provide

resources

to expand the

EP drill program and to provide more

reactor operations

experience

to the

EP Program.

The licensee

appears

to have

a good emergency

preparedness

training and qualifications program.

Records of training and

inter views with control

room personnel

demonstrated

a good

understanding

of the principles of emergency

preparedness

and

also indicated

improvements to the

EP training program.

Improvements in the training program for dose

assessment

were

also noted.

Some areas

were identified where training in

emergency

response

capabilities

would be beneficial,

such

as

for the Mater Reclamation Facility.

The licensee

had initiated

plans to provide training for certain additional facilities, or

groups

on or near the site,

who do not receive routine general

employee training.

Performance

Ratin

Performance

Assessment

- Category

2.

Licensee

performance

was

determined to be improving during this assessment

period.

IJ

15

3.

Board Recommendation

The licensee

needs to continue

management

support of the

EP

Program to assure

the program continues to improve.

-The board

recommended

active involvement by the

new members of'he

new

management

team.

In addition, the board

recommends

licensee

management

attention to accomplishment of corrective actions in

,

a timely manner.

E.

~Securit

1.

~Anal sis

Ourinq the assessment

period,

RV conducted four physical

security inspections.

Over 147 hours0.0017 days <br />0.0408 hours <br />2.430556e-4 weeks <br />5.59335e-5 months <br /> of direct inspection

effort was expended

by regional inspectors.

In addition, the

resident

in'spectors

provided continuing observations

in this

area.

One material control

and accounting inspection

was'

conducted during this assessment

period.

With regard to management

s involvement in assuring quality,

corporate

and plant management

continued to review the

operation of the overall security program.

In April of 1988,

staffing limitations were imposed

on the security organization.

Routine staffing levels were limited to that needed to provide

for normal security operations.

Additional security officers,

needed for the extra work related to refueling, etc.,

were to

be hired and trained coincident with planned plant outages.

At

that time the

NRC noted the problems of unplanned

equipment

failures

and the lead time necessary

to recruit and train the.

additional security "outage" cadre.

Of particular concern,

as

expressed

at the time,

was the fatigue factor associated

with

holding security officers over their normal

12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shift and

the difficulty of providing adequate relief of officers when

operating with several

compensatory

posts.

The current unplanned station-wide outage,

which began in March

l989,

has

imposed

demands

on'the security organization for

which'additional staffing could,not

be expeditiously provided.

This resulted in substantial

overtime work by the security

officers and was,identified in the last physical security

inspection

as

a contributing cause of compensatory officers

falling asleep

on post.

In response

to that inspection,

the

licensee

stated their intent to expand the training for

contract security personnel

normally used outside the protected

area.

This will provide

a larger reservoir of trained guards

to supplement

the permanent plant security force during periods

of peak security workload.

equality assurance

and quality control programs

and policies are

generally adequately

stated

and understood

although the lack of

acceptance

criteria for CCTV image quality resulted in the

inappropriate

acceptance

of substandard

images

from aged

CCTY

cameras

used for protected

area barrier alarm assessment.

The

review and upgrade of the security maintenance

program

and

procedures

is proqressinq,

albeit slowly.

Of the 43 procedural

review tasks originally sdentified,

21 remained to be reviewed

's

of August; 1989.

Concerns

were also identified with the

adequacy of past corrective actions for a licensee-identified

problem related to the Security Access Control computer,

which

resulted in enforcement action during the current evaluation

period.

-The previous

SALP report encouraged

licensee

management to

complete the construction of an a]ternate

vehicle

access

control point, to expeditiously address

the

engineering

.issues

associated

with the evaluation of roll-up

doors serving

as vital area barriers,

and to upgrade

the

perimeter barrier to eliminate potential vulnerabilities

'dentified by the Regulatory Effectiveness

Review (RER) team.

During this

SALP period, construction of an inner protected

area

fence

and

a new vehicle access

portal were completed.

The

upgrading of the roll-up doors

has

been completed for two of

the three units.

Identification and resolution of technical

issues,

while slow,

has

been generally

sound

and thorough.

However,

two issues,

the

image quality of CCTY cameras

and the licensee's-initial

assessment

of the vulnerabilities of the personnel

access

hatches

to.conta'inment

were identified as being inadequate.

Durinq the assessment

period,

two information notices

and one

gener>c letter related to security were issued.

The

licensee's

actions

were found to be adequate.

The enforcement history for the period November

1,

1988,

through October 31,

1989, includes three violations and one

devi'ation, related,

respectively,

to inadequate

assessment,

aids; lack of positive computerized

access

control; inattentive

compensatory security officers; and failure to complete

as

committed (or to report delays in the comp'Ietion of) an

investigation into the causes

of a security event.

During this

SALP period, the licensee

reported six safeguards

eve'nts.

Five of these

events

resulted

from personnel

error:

failed security compensatory

measures

(three); lack of

positive access

control (one);

and an uncontrolled pathway to

a vital area (one).

The remaining event resulted

from a

design deficiency of a vital area barrier vulnerability.

Mith respect to staffing,

key positions were identified, and,

although limited by staffing considerations,

position

responsibilities

were generally well defined.

The security

training staff is continuing their special

advanced training

program.

This program exceeds

regulatory requirements,

and

augments

current offsite security resources

to meet the

special

security

demands

caused

by the plant's isolated

location.

17

2.

3.

Performance

Ratin

Performance

assessment

- Category

2.

Recommendations

Licensee

management

is encouraged

to expeditiously complete

their review of CCTV camera

coverage

and illumination necessary

for adequate

protected

area barrier alarm assessment

and to

limit overtime effects

on guard alertness,

to include

expediting, the expanded

implementation of their planned

security tr'aining program.

F.

En ineerin /Technical

Su

ort

~Anal sis

This functional area

was reviewed routinely by both the

regional

and resident staff of the Region

V office, and by the

staff of NRR.

Over

260 inspection

hours were expended.

These

reviews focused primarily on the degree to which the system

and

corporate

engineers

are involved in plant operations

in a well

focused

manner,

and the quality of the work they contribute.

The System Engineer program

has continued to lack management

direction during this assessment

period and the results of this

group's efforts have generally

been disappointi'ng,

in spite of

an initiative by the licensee to achieve

improved performance.

The inspectors

have found the System Engineers to'e typically

capable,

however,

the broad scope of their responsibilities

and

an apparent

lack of clear prioritization of activities

has left

many of the System Engineers frustrated

and unfocused

on more

important tasks.

Although the licensee

took action to increase

both the number of System Engineers

and the number of

supervisors,

this positive action was

somewhat cancelled

out by

a lack of continuity at the senior management

level.

During

the

SALP period, three individuals have occupied the Director,

Standards

and Technical

Support position.

At the close of the

SALP period, the position was being temporarily filled while

the licensee

continues to search for a permanent Director.

The System Engineer's

lack of focus

has

been highlighted by

their failure to identify and promptly resolve technical

issues

prior to the issues

becoming self-revealing via a plant event.

The Augmented Inspection

Team (AIT) review of the Harch 3, 1989

Unit 3 reactor trip/loss of offsite power event identified that

long-standing engineering

issues

regarding the operation of the

atmospheric

dump valves

had not been promptly addressed.

Additionally, the AIT found that the emergency lighting system

testing

was not adequate

to verify that the lighting system

could meet its design requirements;

a previously identified

problem with a Steam

Bypass

Control System

(SBCS) permissive

timer card

had not been

addressed

and contributed to the event;

the nitrogen backup

system for the

ADV had not been properly

18

tested;

and engineering

issues

regarding the compressed

gas

system

had not been fully addressed.

In summary,

the AIT,found

that if previously identified problems

had been thoroughly

addressed

by engineering in a timely way, the siqnificance of

the parch

3 event would probably have

been greatly lessened.

The event re'suited in a prolonged

shutdown of all three units

and

a $250,000 civil penalty.

Other examples of long-standing

known engineering'issues

not being promptly addressed

included:

excessive

leakage

past the pressurizer

spray valves;

deficiencies in the

EE580 Cable

Raceway Tracking 'System;

questions

regarding the proper storage of safety related

materials;

recurring problems with the radiation monitoring

system;

an issue regarding the operation of emergency diesel

generator

excess

flow check valves associated

with the air

starting system;

and

a long delay in implementing

a spent pool

level switch modification at Unit 1, which contributed to a

loss of level event.

The performance of the System

Engineers

in responding

reactively to events

which occurred durinq the assessment

period was also considered

weak in severaT

cases.

Troubleshooting of a part length control element

assembly

(PLCEA) drop at Unit 1 was considered to be incomplete,

and

allowed a second

PLCEA to drop the following day.

Hore

illustrative

was the inadvertent overpressurization

of main

feedwater piping at Unit 2 following a unit trip.

The

engineering

review of this significant occurrence

was

considered

to be hastily performed, initially poorly

documented,

and based

on assumptions

which later proved to be

incorrect.

In contrast to those failures

and weaknesses

listed above,

which occurred earlier in this period, several

examples of good

technical

work were observed late in the period which

demonstrated

the licensee's

capability to react correctly and

thoroughly when properly guided by management.

Examples

observed

included the response

to a diesel

rocker arm failure

at Unit 3; the engineering

response

to questions

concerning

main steam safety valve ring settings;

the identification and

resolution of. issues

regarding high pressure

safety injection

flow to the reactor coolant system hot legs;

and the

engineering

response

to address

the identification of

counterfeit switches in the 125

VDC system.

These

examples

provide a hopeful indication of positive changes

in the

licensee

s approach to engineering activities.

Another indicator of difficulties with the technical

support

area is the backlog of issues

which needed to be addressed.

Significant backlogs or overdue

items have existed for

Engineering Evaluation Requests,

Post-Trip Review actions,

Special

Event Evaluation Report actions,

and Incident

Investigation

Report actions.

Late in the

SALP period, the

licensee

displayed

a good recognition of the problems with

backlogs

and stated their intention to reduce the total backlog

j

ll

f

>C

f

'Ji

I

t

l

1l

t

19

to a more manageable

size.

Some reduction

was noted toward the

end of the per>od.

With regard to corporate engineering,

the licensee

continues

to'mplement

their Engineering Excellence

program,

which includes

'econstitution of the plant design

bases

and increased

technical training of engineers.

A section of the corporate

engineering staff has

been relocated to the site,

and

'lessons

learned"

reviews of design

change

packages

have

been started.

In conjunction with the site System Eng>neers,

the corporate

engineers

have

commenced

scheduled

walkdowns of their systems.

'lthough the corporate engineering staff appears

to be headed

towards increased

involvement in site activities, their

effectiveness

remains to be assessed.

2.

Performance

Ratin

Performance

Assessment

- Category

3

3.

Board

Recommendations'he

licensee

appears

to have defined the problems with the

System Engineer'rogram

as, primarily a lack of focus

on

important issues.

The licensee

should permanently fill the

Director, Standards

and Technical

Support position,

and should

provide the System Engineers with clearly defined

and

prioritized tasks

focused

on ensuring the reliable operation of

their systems.

The System Engineers

should then

be held

accountable for the performance of their systems.

Corporate

engineerinq

should continue to increase their involvement in

site activsties

and problem resolutions.

The licensee

should

continue the emphasis

being placed recently

on reacting

conservatively,

deliberately

and comprehensively to plant

engineering problems..

G.

Safet

Assessment/ ualit

Verification

1.

~Anal sis

This functional area

was observed routinely during the

assessment

period by both the resident

and regional inspection

staff.

Approximately 1663 hours0.0192 days <br />0.462 hours <br />0.00275 weeks <br />6.327715e-4 months <br /> of inspection effort were

devoted to this functional area.

Strengths identified in this

functional area

were manifested in the licensee's

willingness

to correct past weaknesses

in both the gA/gC organization

and

program, and,in the licensee's

responsiveness

to NRC

initiatives.

However, weaknesses

observed

appeared

to be

a

continuation of past weaknesses

that had yet to be corrected.

These

weaknesses

included (1) root cause

analyses

that were

limited in scope,

(2) lack of effectiveness

of the gA and

oversight organizations,

and (3)

a lack of sufficient

technically experienced staffing of the

gA organization.

2D

Significant management

changes

in the gA department

had been

made by the =licensee during this period.

The gA Director was

replaced;

the

gC Manager

was appointed temporarily as the

new

gA Deputy Director;

a new gC Manager

was temporarily appointed;

and

new managers

were selected for guality Engineering

and

equality Systems.

These

changes

appeared

to be positive

corrective action for past weaknesses

of the gA/gC

organization.

However, the need to permanently. select

a Deputy

gA Director and

a gC Manager

was viewed as

a weakness

in that

both selections affect the efficient functioning'.of the

gC

organization

and the

gC inspectors.

The other notable weakness

of the

gA organization

was the relative lack of technically

experienced

and operations

experienced

personnel

to allow

detailed technical evaluations

and to provide insightful and

subjective observations

to manaqement

regarding conduct of work

by organizations

such

as operations

and maintenance.

During this evaluation period,

improvement of the licensee's

root cause analysis

process

had been noted.

Examples of

'mproved root cause

analyses

were:

(1) the Emergency Diesel

Generator

(EDG) rocker arm failure analysis,

and (2) the fire

suppresion

system test records investigation.

However, through

the evaluation period,

lapses

in the depth of root cause

reviews were still noted.

Significant examples of these

were:

(1) the

AOV and compressed

gas reports for the Unit 3, March 3,

1989,

Unusual

Event were limited in scope in that the hardware

problems

appeared

to have

been evaluated

but the root cause of

how the hardware

problems persisted

did not appear to have been

addressed;

(2) a Unit 2 post-trip review failed to recognize.

signs of a leaking check valve which eventually resulted in the

overpressurization

of the

MFM piping.

The equality Assurance

and oversight organizations

have not been

a visible force in the operation of Palo Verde, particularly

during the first half of the assessment

period.

Senior

Management

has not demanded that these

groups

be sufficiently

crit>cal and aggressive

in their reviews,

such that major

problem areas

could be identified prior to manifesting

themselves

and affecting safe plant operations.

The

-effectiveness

of the licensee's

gA and oversight organizations

was predominantly marginal although

improvements

were noted

toward the

end of the evaluation period.

The Nuclear Safety

Group

(NSG) was ineffective .in identifying and initiating

changes

to existing weak programs.

The Plant Review Board (PRB)

'as

predominantly occupied

by review of procedure

changes.

The

PRB often missed opportunities to provide recommendations

to

the

NSG that were meaningful.

The gA and Independent

Safety

Evaluation Group participation in the Unit 3 mid-loop

operations

were ineffective in recognizing

needed

changes to

operating procedures,

orqanizational

interfaces

and operating

policy.

gC verified satisfactory installation of a Unit 1

EDG

fuel line that was installed in accordance

with procedure

but

not in accordance

with vendor instructions.

The fuel line

connection failed during subsequent

testing.

Similarly, prior

It

~

II'

to Unit 2 restart,

gA/gC failed to identify that the procedure

utilized for adjusting

AOY nitrogen. pressure

regulators

was

based

on verbal information rather than documented

vendor

manual instructions.

Toward the end of the rating'peiiod,

licensee

management

utilization of the gA organ)zation'and

the increasing

involvement of the department

became visible in the Unit 2 Main

Steam Relief Valve and Pressurizer

Safety Valve blowdown ring

setting problems.

Independent

gA evaluations of the

Engineering Evaluations

Department analysis

was performed

and

significant gC coverage of the subsequent

testing

was observed.

Also, in June

1989,

a Project Self Ass'essment

Group

(PSAG) was

formed to coordinate oversight functions.

This appeared

to be

a

needed

change but actual results

were not yet evident at the

end of this

SALP period.

In the area of licensing activities, evaluations

related to

licensee

amendments

and

10 CFR 50.59 evaluations

were generally

adequate

.

However,

two license

amendment

requests

were found

to lack adequate

bases

to support the requested

changes,

and

one facility change applied under

10 CFR 50.59 regarding fire

protection

was found to have

been inappropriately

implemented..

Responses

to generic communications

were generally timely and

appropriately detailed.

Two exceptions

were noted:

,submission

of followup information to

NRC Bulletin 88-04, "Potential

Safety Related

Pump Loss" regarding Ingersoll-Rand

pumps

was

repeatedly

delayed;

and the licensee's

response

to Generic Letter 88-14 "Instrument Air Supply System

Problems Affecting

Safety-Related

Equipment"

was limited in scope.

The licensee

is very responsive to

NRC special

requests

that

require quick responses

and is prompt in addressing

NRC

concerns

regarding written communications

and licensing

evaluation.

It appears

that the licensing organization

needs to maintain

an

increased

awareness

in plant operations

and status,

and that

this is being limited by poor communications

and participation

between

the corporate

licensing organizations

and the site

operations

organization.

2.

Performance

Ratin

Performance

Assessment

- Category

3 - Improving Trend

3.

Board Recommendations

r

Licensee

management

should continue to demand aggressive

and

technically competent

reviews by the gA and oversight

organizations.

The licensee

is encouraged

to continue to

include technically competent

personnel

in the oversight

organizations staff.

Strong management

support

and insistance

il

t

22

in the thorough implementation of changes

to the gA program

such

as the

new nonconforming condition reportinq

and

corrective action procedures

and the

new correct)ve action

request

procedure is encouraged

to assure effective

continuation of corrective actions that have

commenced.

Further strengthening

of the root cause analysis

program should

be performed to 'prov)de greater

depth

and scope

and

sn turn-

result in more meaningful corrective'ctions.

V.

SUPPORTING

DATA AND SUMMARIES

A.

Licensee Activities

In general, all three units operated satisfactorily during the

assessment

period.

Units- 1 and

3 operated relatively free of

problems until both units experienced

reactor trips in March.

Both

units have been in refueling outages

since that time.

Unit 2 has

been hindered

by generic problems,

and voluntarily shutdown three

times to address

)ssues identified on the other units.

Specific

operational

events

were as follows:

Unit 1

Unit 1 entered

the assessment

period at lOOX power.

After'perating

at essentially full power for 170 consecutive

days,

on February 17,

the unit .substantially

reduced

power to investigate

and repair

feedwater heater

and condenser

tube leaks.

The unit returned

to'00X

power -on February

22.

The reactor tripped

on March 5 due to a

failure of a processor

board

on Control Element Assembly Computer

(CEAC) No. 2. 'his outage continued .to allow testing of Atmospheric

Dump Valves

(ADVs), which had failed to operate

remotely on Unit 3.

The unit remained

shutdown for the duration of the assessment

period

to modify its ADV's and conduct its second refueling outage.

I

Unit 2

Unit 2 operated at 100K power 'from the beginning of the assessment

period until November 16, when

a shutdown

was initiated due to

excessive

unidentified

RCS leakage.

The reactor tripped on low

steam generator

level

due to problems experienced with the

MFW

control

system during

MFW swapover.

The unit returned to service

on

November 23,

and operated at essentially

100X power until

December

23, when the turbine tripped due. to an inadvertent

isolation of a moisture separator

drain valve.

The turbine was

returned to service the following day.

On February 16, the reactor

tripped

on low steam generator

level

due to a feedwater

control

system malfunction and the unit again returned to service

on

February 28.

The plant was voluntarily shutdown

on March 15, to

test

and repair atmospheric

dump valves.

A Confirmatory Action

Letter was issued to confirm licensee

commitments to correct in Unit

2 'significant discrepancies

identified in Unit 3 during .the March 3,

1989 event.

The confirmatory action letter was lifted for Unit 2 on

June

28.

The unit was returned to service

on June

29.

The plant

down powered to Mode 2 for two days

on July 4 to repair

an

'I

1

23

unisolable feedwater

bypass drain line break.

The plant operated at

100K power until July 12,

when a fuse failure for a potential

transformer

caused

the loss of electrical

bus

NAN-S02 and resulted

in a reactor trip.

The unit was returned to service

on July 21.

The turbine tripped and

a reactor power cutback was experienced

on

August 4 due to

CEDH control, system problems.

The turbine was

restarted

on August 6.

On September

6, the plant was voluntarily

shutdown to inspect main steam safety relief valves,

and was

returned to service

on September

22.

On October

14

the plant was

again voluntarily shutdown to replace

two potential)y 'counterfeit

electrical

breakers

in the 125

V DC distribution system.

An attempt

to restart the reactor

on October 14'was

abor'ted

due to Control

Element Drive Mechanism

(CEDH) coil grounds.

The reactor

was

restarted

on October 30, but tripped from 66K power on October

31

due to various plant protection system

element failures."

The unit

ended the assessment

period in Mode 3.

Unit 3

Unit 3 entered the assessment

period at lOOX power.

A shutdown

was

performed

on January

6 due to a diesel

generator failure ending 141

continuous

days of power operation.

The unit was returned to

service

on January

21 and operated

near

100X power until March 3.

On that date

a grid disturbance

resulted in a reactor trip on low

steam generator level.

The unit entered its first refueling outage

and was shutdown for the remainder of the assessment

period.

Plant status at end of SALP

eriod

Palo Verde ended the evaluation period with Unit 2 operating in Mode

3 and i Confirmatory Action Letter in effect that acknowledges

licensee

committments for corrective actions prior to restart of

Units 1 and 3.

The licensee

was preparing Units 1 and

3 for restart

at the end of the period.

B.

Direct Ins ection

and Review Activities

An average of approximately three resident inspectors

were assigned

to Palo Verde during the

SALP assesment

period.

Forty inspections,

five team inspections,

and five management

meetings

were conducted

during this period. Significant team inspections

included

. Augmented Inspection

Team in response

to the March 3,

1989

Unusual

Event

.

Emergency Operating

Procedures

inspection

team

. Health Physics

team inspection

. Maintenance

team inspection

.

Emergency

Preparedness

exercise

A total of 7198 hours0.0833 days <br />1.999 hours <br />0.0119 weeks <br />0.00274 months <br /> of direct inspection were performed during

this

SALP period.

Table

1 provides

a summary of those inspection

activities.

C.

Enforcement Activit

A summary of inspection activities is provided. in Table 1 along with

a summary of enforcement

items resulting from those inspections.

A

description of the enforcement

items is provided in Tab]e 2. During

the

SAl.P period

a three part escalated

enforcement action ($250,000)

was identified concerning the March 3,

1989 Unit 3 Unusual

Event.

D.

Confirmation of Action Letters

A Confirmatory Action Letter

(CAL) was issued

on March 3, 1989,

resulting from the Unit 3 Unusual

Event, to assure that multiple

equipment failures experienced

during the event were thoroughly-

investigated

and to assure that

NRC was informed of the. results of

those investigations

and the corrective actions taken prior to

restart of Unst 3.

The

CAL was expanded

on March 7, 1989 and March

28,

1989 to assur e that lessons

learned

from the Unit 3 event

and

a subsequent

Unit 1 event would be applied

by the licensee in all

three

Palo Verde units.

On June 23,

1989 and June 28, 1989, 'the licensee certified that

restart corrective actions for Unit 2 had been completed.

A CAL was

again

issued

on June

28,

1989 to allow Unit 2 restart

and to

reconfirm the necessary

licensee

actions for restart of Units 1

and 3.. Licensee actions for this last

CAL had not been completed at

the

end of this

SALP period.

E.

AEOD Event Anal sis

The Office for Analysis and Evaluation of Operational

Data

(AEOD)

reviewed the licensee's

events

and prepared

a report which is

-. included

as Attachment l.

AEOD reviewed the LER's and significant

operating

events for quality of reporting and effectiveness

of

identified corrective actions.

1

I

Table

1

INSPECTION ACTIVITIES AND ENFORCEMENT SUMMARY ll/Ol/88 - 10/31/89)

Palo Verde Unit 1 ***

Functional

Area

Ins ections

Conducted

nspec

son

ercen

Hours*

of Effort

Enforcement

Items

Severit

Level*"

I

~ Q

A.

Plant Operations

B.

Radi ologi cal

Controls

C.

Maintenance/

Surveillance

D.

Emergency

Prep.

E.

Security

F.

Engineering/

Technical

Support

G.

Safety Assessment

equality Verif.

Total s

702

331

75

93

637

29

14

21

27

Allocations of inspection

hours to each functional area are

approximations

based

upon

NRC form 766 data.

These

numbers

do not include

inspection

hours

by NRC contract personnel.

Severity levels are in accordance

with NRC Enforcement Policy (10 CFR Part 2, Appendix C).

"** Does not include inspection report 89-45.

Table 1

Page

1

Table

1

'INSPECTION ACTIVITIES AND ENFORCEMENT SUMMARY (11/Ol/88 - 10/31/89

Palo Verde Unit 2 "**

~

Functional

Area

Ins ections

Conducted

Enforcement

Items

nspec

ion

ercen

Severit

Level""

Hours*

of Effort

D

A.

Plant Operations

B.

Radiol ogical

Controls

C.

Maintenance/

Surveillance

1095

252

501

"

18

3

1

2

D.

Emergency

Prep.

47

E.

Security

36

F.

Engineering/

78

.Technical

Support

G.

Safety Assessment

705

equality Verif.

Total s

-

-

2762

26

Allocations of inspection

hours to each functional area are

approximations

based

upon

NRC form 766 data., These

numbers

do not include

inspection

hours

by

NRC contract personnel.

"*

Severity levels are in accordance

with NRC Enforcement Policy (10,CFR Part

2, Appendix C).

No deviations

were identified during this'SALP period..;:

  • "" Does not include inspection report 89-45.

Table 1

Page

2

Table 1

=INSPECTION ACTIVITIES AND ENFORCEMENT

SUMMARY (11/01/88. - 10/31/89

i

Palo Verde Unit 3 **""

Functional

Area

A.

Plant Operations

830

39

Ins ections

Conducted

nspec

ion

ercen

Hours**

of Effort

Enforcement

Items

Sever it

L'eve 1*"."

D

1*

3

B.

Radiological

Controls

C.

Maintenance/

Surveillance

D.

Emergency

Prep.

E.

Security

F.

Engineering/

Technical

Support

G.

Safety Assessment

equality Verif.

Totals

286

541

25

36

83

321

14

26

15

1*

2

1*

2

A'250,000 Civil Penalty

was issued for the three Severity Level III

violations associated

with multiple equipment failures during the March 3,

1989 Unit 3 Event.

Allocations of inspection

hours to each functional area

are

approximations

based

upon

NRC form 766 data.. These

numbers

do not include

inspection

hours

by NRC contract personnel.

- *"* Severity levels are in accordance

with NRC Enforcement Policy (10 CFR Part 2, Appendix C).

    • "*Does not include inspection report 89-45.

Table

1

Page

3

Re ort

Ttuum>er

UNIT 1

Table

2

p'aaaee rd e

Enforcemen

ems

~Sub 'ect

Severity

Fun'ctional

Level

Area

88-40

Environmental Monitoring flowmeter

was

improperly adjusted.

89-10

An operator

who tested positive was not

placed in follow-up test program.

'9-10

Failure to compensate

for unusable

CCTV

camera.

89-10

Failure to provide positive access

control.

4

~

89-16

LLRT conducted with unapproved criteria.

ADV N2 isolation valve closed not iaw

procedure

rendering

ADV inop.

EDG fuel line

installed not iaw procedure

and disconnects

while engine

was running.

89-24'ome

non-exempt Americium-241 sources

were

not tracked,

inventoried, or labeled

correctly.

89-25

89"28

A high radiation area

was not posted

as

such.

Inadequate

corrective action to preclude

repetitive

EDG Cooling system plug and elbow

failures.

B

89-30

Three flammable liquids lockers with

expired permits were found in the aux

building and radwaste building.

C

89-32

89-34

Inattentive compensatory security officer.

4

Post-trip review corrective actions

were

not completed in a timely manner.

Table

2

Page

1

Table

2

paeee

erde

E~t

Re ort

S

ue er

~Sub 'ect

89-36

Spent fuel pool level was unintentionally

lowered below technical specification limits

due to valve not being shut and not being

verified shut.

everity

Functional

Level

Area

't

4

A

89-36

EDG excess

flow isolation valves were not

shut despite

design calculations requiring

them to be shut

due to procedural error.

89-43

Five T/S violations did not receive

a written

4

PRB evaluation

as required by T/S.

UNIT 2

A

88-31

Diesel Generator

maintenance

was done

without documentation of previously

.

completed steps.

88-39

Environmental monitoring flowmeter was

improperly adjusted.

89-03

Radioactive effluent monitors did not have

sample media; therefore,

they were

inoperable.

89-06

A contaminated

area was-not posted

as such.

89-06

Failure to place the steam generator

economize<

flow control in automatic

and

insure

FMCV was shut after a reactor trip.

89-16

LLRT conducted with unapproved criteria.

89-28

Inadequate

corrective action to preclude

repetitive

EDG Cooling-system plug and

elbow faHures.

89-30

Work was

done

on an Atmospheric

Dump Valve

nitrogen regulator valve not in accordance

with the approved work order or technical

manual.

Table

2

Page

2

C

Il

Re ort

um er

89-34

Table

2

Pa~o~er

e

Enforrcem~n

Reme

~Sob'ect

Corrective actions to change operating

procedur'es

were not accomplished

four

months after the required date.

Severity

Functional

Level

Area

89-36

89-43

89-43

89-43

EDG excess

flow isolation valves were not

4

shut despite

design calculations requiring

them to be shut

due to procedural

error.

,Five T/S violations did not receive

a written 4

PRB evaluation

as required

by T/S.

Contrary to procedure

a

CR operator did not

5

switch the

HV meter from start

up to control

and an assistant shift supervisor

signed off

accomplishment of the step.

In addition,

a

mechanic

used

a gauge other than the one

required by the work order for HS code

safety valve blowdown ring adjustment.

Operator

licensing report not submitted

on

4

time.

UNIT 3

88-38

89-06

89-13

Environmental

flowmeter was improperly

adjusted.

equality related work activities did not

receive

a quality review.

Inadequate

emergency lighting design,

maintenance

and testing.

4

D

89-13

89-13

89-16

Inadequate training and incorrect operation

3.

of Atmospheric

Dump Valves.

Lack of appropriate corrective action

3

concerning Atmospheric

Dump Valves,

Steam

Bypass Control Valves,

and compressed air

lines.

LLRT conducted with unapproved criteria.

Table

2

Page

3

1

I

Table

2

paeeo

erde

E~t

Re ort

um er

~Sub 'ect

h

Sever ity

Functi onal

, Level

Area

89-16

RCS drain operation procedure

had incorrect

4

.

F

correction curve for RCS level durinq

midloop ops.

Procedure

had ineffective

provisions to prevent vortexing causing air

entrainment.

89-28

Inadequate

corrective action to preclude

repetitive

EDG Cooling sytem plug and

elbow failures.

'4

89-28

Core Protection calculator work order steps

4

were completed without performance of

required sign-offs.

89-32

Failure to meet 'commitment in LER.

89-36

89-36

89-36

89-43

EDG excess

flow isolation valves were

not shut despite

design calculations

requiring them to be shut due to

procedural error.

Corrective action for an Engineering

4

Evaluation Report requirement to shut

EDG

Cooling system

excess

flow isolation valve

was not complied with.

Containment

Spray system valve lineup

procedure

was not followed resulting in

loss of control of RCS inventory.

Five T/S violations did not receive

a

written

PRB evaluation

as required

by T/S.

Table

2

Page

4

It

(t

TABI E 3

- SUMMARY OF

PALO VERDE 1 LICENSEE EVENT REPORTS

LERs

Functional

Area

A.

Plant Operations

B.

,Radiological'ontrols

C.

Maintenance/

Surveillance

D.,

Emergency

Prep.

E.

Security

F.

Engineering/

Technical

Support

G.

Safety Assessment/

equality Verif.

Totals.

SALP Cause

Code"

A

B

C

D

E

X

2

1

2

1

Totals

3

The above data are based

on

LERs 88-09, 88-20, 88-23

, 88-25 through 89-14,

89-16,

88-S08,

89-S03, and 89-S08.

" Cause

Code

- A - Personnel

Error

B - Design, Manufacturing or Installation Error

C - External

Cause

D - Defective Procedures

E - Component Failure

X = Other

Table

3

Page

1

Ij

TABLE 3

SUMMARY OF

PALO VERDE 2 LICENSEE EVENT REPORTS

LERs)

Functional

Area

A.

Plant Operations

SALP Cause

Code*

A

B

C

D

2

1

1

E

X

1

Totals

B.

Radi ol ogi cal

Controls

C.

Maintenance/

Surveillance

D.

Emergency

Prep.

E.

Security

F.

Engineering/

Technical

Support

G.

Safety Assessment/

equality Verif.

Totals

1

1

1

The above data are

based

on

LERs 88-14 through 89-06, 89-08, 89-09,

89-S01 and

89-S02.

  • Cause

Code

A - Personnel

Error

B - Design, Manufacturing or Installation Error

C - External

Cause

D - Defective Procedures-

E - Component Failure

X - Other

Table

3

Page

2

TABLE 3

SUMMARY OF

PALO VERDE 3 LICENSEE EVENT REPORTS

LERs

SALP Cause

Code*

Functional

Area

A.

Plant Operations

B.

Radiological

Contr ol s

C.

Maintenance/

Surveillance

D.

Emergency

Prep.

E.

Security

F.

Engineering/

Technical

Support

G.

Safety Assessment/

equality Verif.

Totals

A

B

C

D

3

2

1

2

Totals

3,

The above data are based

on

LERs 88-07 through 89-09,

and 89-SOl.

  • Cause

Code

A - Personnel

Error

B - Design, Manufacturing or Installation Error

C - External

C'ause

0 - Defective Procedures

E - Component Failure

X - Other

Table

3

Page

3

I

hi

J

Attachment

1

AEOD In ut to SALP Review For Palo Verde

Arizona Nuclear Power Project submitted

37 Licensee

Event Reports

(LERs) for

the three units at Palo Verde, not including updates,

in the assessment

period

from November 1, 1988 to October

31,

1989.

Our review included the following

LER numbers:

UNIT1,,

UNIT 2

UNIT 3

88-020

8( 025-

89-001 to- 89-014

88-014 to 88-017

89-001 to 89-009

88-008

89-001 to 89-009

~ Four

LERs in the assessment

period were considered significant by the

AEOD LER

screening

process.

These

LERs were:

Unit 1

.

LER

89-005

Unit 2

LER

89-001

Unit 3

LER

89-001

The manufacturer

determined

excessive

internal valve

.

leakage

could result in the inability to remotely or

manually operate

the Atmospheric

Dump Valves (ADV's).

The

event was considered significant because

credit is taken

for the ADV's to remove decay heat from the steam.

generators

in the event that the main condenser

is una-

vailable for service for any reason

including a loss of AC

power.

Contamination

from mineral deposits

from misting of the

cooling towers led to rain saturation of the

ESF

transformer

bushings

and

a complete loss of offsite power

(LOP).

The diesel

generators

started

and assumed all

safety-related

loads

and the plant remained stable at

approximately

100K power.

ROAB considers all

LOP events to

be safety significant.

'n

electrical grid disturbance

caused

the units main

generator

output breakers to open.

The steam

bypass

control system malfunctioned

and the reactor tripped from

low steam generator

(S/G) pressure.

After a main steam

isolation system activation, control

room personnel

attempted to remove decay heat

and control

S/G pressure

with the Atmospheric

Dump Valves (ADVs).

Control

room

personnel

could not remotely operate

the ADV's from the

control

room or from the remote

shutdown panel.

Heat

removal

was subsequently

established

by manually opening

the ADV's after one main steam safety valve had cycled to

reduce

S/G pressure.

li

Unit 3

LER

89-007

During post installation testing of Potter and Brumfield

relays,

approximately

25X of the

new relays malfunctioned.

The relays are used in the engineered

safety features

actuation

systems

and cause safety-related

components

to

. actuate

when de-energized.

The cause of relay malfunction

was inadequate

design.

A breakdown of the root causes attributed to the

LERs submitted in the assess-

ment period were:

Root Cause

Unit 1

Unit.2

Unit 3

Total

Personnel

Error

Procedural

Problems

Equipment Failures

Design/Installation

Not Determined Yet

Other

5

2

3

3

3

0

3

3

11

1

0

3

-4

3

10

1

1

5

0

'

6

2

0

2

The distribution of root causes

seem typical and do not reveal

any programatic

weakness.

Many LERs were promised to be updated. in the assessment

period.

These

LERs

were either

updated

by the promised submittal date,

or revised with a

supplemental

report with a new promised submittal date.

The

LERs were clear, specific, complete

and informative.

They satisfied all

"

reporting requirements.

The only suggestion is to include root cause classi-

fications, similar to those

used in the root cause table above,

in addition to

existing narrative

cause description.

There were 14 Preliminary Notifications of event or Unusual

Occurrence

(PNs)

. issued for the three units at Palo Verde in the assessment

period.

Our review

of the

PNs indicate that the licensee

reported all events with an

LER that were

reportable.

Me reviewed

55 reports received pursuant to 10CFR 50.72 in the assessment

period.

Many of these reports were duplicates for each unit.

All events

reported

by these calls were addressed

by an

LER, were too recent for an

LER to

be received or were not reportable

under

10CFR 50.73.

The only exception

may

be

EN 15281,

EVT 026548,

which reported

on 4/10/89 that the ADV's at Unit 1

were incapable of remote operation

due to isolation of all pneumatic valve

operator

sources.

However,

LER 89-005,

dated 4/12/89 reported the

inoperability of all

ADV s due to excessive

internal valve leakage.