ML17304B438

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Insp Repts 50-528/89-30,50-529/89-30 & 50-530/89-30 on 890612-0806.Violations Noted.Major Areas Inspected:Plant Activities,Esf Sys Walkdowns,Monthly Surveillance Testing, Licensee Contractor Qualifications & Unit 2 Reactor Trip
ML17304B438
Person / Time
Site: Palo Verde  
Issue date: 08/24/1989
From: Richards S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17304B434 List:
References
50-528-89-30, 50-529-89-30, 50-530-89-30, NUDOCS 8909130134
Download: ML17304B438 (37)


See also: IR 05000528/1989030

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION

V

Re ort Nos.

Docket Nos.

License

Nos.

50-528/89-30,

50-529/89-30

and 50-530/89-30

50-528$

50-529,

50-530

NPF-41,

NPF-51,

NPF-74

=

Licensee:

. Arizona Nuclear

Power Project

P. 0.

Box 52034

Phoenix,

AZ. 85072-2034

E

P1

Y

d

l

i

i

i

1,

53

Ins ection Conducted:

June

12 through August 6,

1989

Inspectors:

Approved By:

T. Polich, Senior Resident

Inspector

D. Coe, Resident

Inspector

C. Myers, Resident Inspector,

Rancho

Seco

P. squalls,

Resident

Inspector,

Rancho

Seco

ic ar s,

ie

Reactor Projects

Section II

e-29-89

a

e

igne

Ins ection

Summar

Ins ection

on June

12 throu

h Au ust

6

1989.

Re ort Nos. 50-528/89-30,

5-

an

-5

-3

Areas

Ins ected:

Routine, onsite,

regular

and backshift inspection

by

t e two resi ent inspectors,

and two Regional

inspectors.

Areas

inspected

included: previously identified items; review of plant

activities; engineered

safety feature

system walkdowns; monthly

surveillance testing; monthly plant maintenance;

review of licensee

contractor qualifications - Units 1, 2, and 3; restart - Unit 2; missed

procedure

step while flashing generator field - Unit 2; forced outage

due

to pipe break - Unit 2; reactor trip and safety injection - Unit 2; main

feedwater suction piping overpressurization

- Unit 2; load rejection from

100% power - Unit 2; improper maintenance

on atmospheric

dump valve

nitrogen supply reducing regulator valves

(ADV regulator valves)-

Unit 2; integrated

safeguards

surveillance testing - Unit 3; review of

licensee

event reports - Units 1,

2 and 3;

and review of periodic

and

special

reports - Units 1,

2 and 3.

During this inspection the following Inspection

Procedures

were utilized:

40500,

61701,

61726,

62703,

64704,

71707,

71710,

92700 and 93702.

8g09i30184

8~r082g

PDR

ADOCK 0 '000528

9

PDC

Safet

Issues

Mana ement

S stem

SINS) Items:

None

Results:

Of the nine areas

inspected,

two violations were identified.

One violation pertained to failure to control work on safety-related

equipment with an approved work order.

The second violation pertains to

fire 'protection in that flammable liquid lockers

had expired storage

permits.

General

Conclusions

and

S ecific Findin s

Si nificant Safet

Matters:

None

Summar

of'iolations:

Two

Summar'f Deviations:

None

0 en Items

Summar

Two items closed,

and five new

items were opened.

DETAILS

Persons

Contacted:

The below listed technical

and supervisory

personnel

were

among

those contacted:

Arizona Nuclear

Power Pro 'ect

ANPP

  • R. Adney,

J. Allen,

  • R. Badsgard,

J. Bailey,

  • B. Ballard,
  • C. Belford;
  • H. Bieling,

P. Brandjes,

C. Churchman,

  • W. Conway,
  • J. Haynes,
  • D. Heinicke,

P.

Hughes,

  • W. Ide,
  • D. Karner,

J. Kirby,

J. LoCicero,

  • W. Marsh,

A. McCabe,

D. Phillips,

J. Reilly,

  • A. Rogers,

C. Russo,

  • T. Shriver,

G. Sowers,

R. Younger,

  • W. guinn,

Plant Manager,

Unit 3

Relief Plant Manager

Supervisor Nuclear Engineering

Department

Assistant Plant Manager, Unit 3

guality Assurance

Director

Supervisor Fire Protection

Emergency Planning/Fire

Department

Manager

Central

Maintenance

Manager

Work Control Manager, Unit 3

Executive Vice President - Nuclear

Vice President,

Nuclear Production/Site Director

Plant Manager, Unit 2

Radiation Protection

5 Chemistry Manager

Plant Manager, Unit I

Vice President - Nuclear

Director, Nuclear Production Support

Independent

Safety Engineering

Manager

Plant Director

Maintenance

Manager, Unit 1

Outage

Management

Manager

Standards

and Technical

Support

Director'icensing

Manager

Assistant

equality Assurance

Director

Compliance

Manager

Engineering Evaluations

Manager

Plant Standards

and Control Manager

Nuclear Safety

and Licensing Director

The inspectors

also talked with other licensee

and contractor

personnel

during the course of the inspection.

  • Attended the Exit meeting held with NRC Resident

Inspectors

on August 10, 1989.

Previousl

Identified Items - Units

1

2

and

3

92702,

92701

a. 'losed

Fol 1 owu

Item

529/88-31-01:

"Maintenance

Work Order

Ste

s Not Si ned

f - Unst

The inspector

reviewed the training records

documenting

retraining of maintenance

personnel

in the proper stepwise

signoff technique to be used in performing work under

a

maintenance

work order.

!

C

f

I

(

II

I

l

l

The inspector questioned

several

crafts personnel

and found

them to be aware of the proper signoff techniques.

The inspector

found the licensee's

actions to be adequate.

This item is closed.

b.

Closed

Followu

Item

529/88-42-02

"Dama ed'Batter

Cell"-

nit

This item involved damage to

a battery cell case in the class

1E, "B" battery,

channel

"D," which the licensee

discovered

during surveillance testing.

Upon discovery

on January

16,

1989 the licensee

had initiated a controlled shutdown in

compliance with technical specifications.

A temporary

modification to jumper out the affected cell was installed,

and

the licensee

restored

the battery to service after completing

the surveillance test to demonstrate

the battery operable in

the modified condition.

The inspector

reviewed the licensee's

event investigation

report, Special

Plant Event Evaluation Report

(SPEER)

89-02-002,

dated

February 7, 1989, which identified that the

damage

most probably occurred during dismantling of scaffolding

in the battery

room on January

12,

1989.

The inspector

found the licensee's

evaluation to be thorough in

identifying the cause of the

damage

and establishing corrective

actions to preclude reoccurrence.

This item is closed.

No violations of NRC requirements

or deviations

were identified.

3.

Review of Plant Activities

71707,

71710;

93702)

a

~

Unit 1

b.

Unit

1 remained in a refueling outage status with fuel off"

loaded during the entire reporting period.

Unit 2

Unit 2 began

the inspection period in mode 3.

On June

23,

1989

the licensee

requested

NRC concurrence

to restart Unit 2 after

completing repairs to Steam

Bypass Control Valve 1008.

The

licensee

determined

the Steam

Bypass Control Valve 1008

had

been incorrectly modified in April 1988.

The licensee

subsequently

submitted

a second letter requesting

NRC

concurrence for restart of Unit 2 after modification of valve

1008

and three other Steam

Bypass

Control valves.

The unit was restarted

on June

29,

1989 and paralleled

onto the

grid on June

30,

1989.

On July 4,

1989 at 12:33

am,

MST,

a

power reduction

was initiated due to an unisolable

feedwater

leak from a Main Feed

Pump

(MFP) suction drain, line (see

paragraph

10).

The reactor

was taken to mode

2 at 3:31

am,

,

MST.

The plant entered

Node

1 on July 6, 1989.

The unit

operated

at

100%%d power until July 12,

1989 when

a reactor trip

and safety injection occurred

(see

paragraph

11).

The reactor

was restarted

on July 20,

1989.

The plant operated until

August 4, 1989,

when

a turbine trip occurred.

The plant was

synchronized

to the grid on August 6,

1989 (see

paragraph

12).

c.

Unit 3

Unit 3 remained in a refueling outage status.

The core was

refueled beginning

on July 24, 1989,

when

Mode

6 was

reestablished.

The fuel reload

was completed'on July 31,

1989.

The unit remained in mode

6 until the end of the inspection

period.

d.

Plant Tours

The following plant areas

at Units 1,

2 and

3 were toured

by

the inspectors

during the inspection:

Auxiliary Building

Containment Building

Control

Complex Building

Diesel

Generator Building

Radwaste

Building

Technical

Support Center

Turbine Building

Yard Area and Perimeter

The following areas

were observed

during the tours:

1.

0 eratin

Lo s and Records

Records

were reviewed against

Tec nica

peci ication and administrative control

.procedure

requirements.

2.

Monitorin

Instrumentation

Process

instruments

were

o serve

or corre ation

etween

channels

and for

conformance with Technical Specification requirements.

'3

~

~Ehif

M

i

C

1"

"d lift

i

g

observed for conformance with 10 CFR 50.54.(k), Technical

Specifications,

and administrative

procedures.

The inspectors

observed

licensee

operators

to be attentive

and alert during backshift

and weekend tours.

4.

E ui ment Lineu s

Various valves

and electrical

breakers

were veri ie

to be in the position or condition required

by Technical Specifications

and administrative

procedures

for the applicable plant mode.

This verification included

routine control board indication reviews

and the conduct

of partial

system lineups.

E ui ment Ta

in

Selected

equipment, for which tagging

requests

a

een initiated, were observed

to verify that

tags

were in place

and the equipment

was in the condition

specified.

General

Plant

E ui ment Conditions

Plant equipment

was

o serve

or in scations

o

system leakage,

improper

lubrication, or other conditions that would prevent the

systems

from fulfillingtheir functional requirements.

Fire Protection

Fire fighting equipment

and controls were

f

i hi hi

1SP if'

d

administrative

procedures.

On August 1, 1989, the inspector identified three

flammable storage

lockers with expired flammable storage

permits in Unit l.

One was

on the Auxiliary Building roof

and expired

on March 2, 1989.

,The other two were

on the

120'levation of the Radwaste

Building and the permits

expired

on July 15,

1989.

The storage of combustible/-

flammable materials with expired permits

was identified as

a potential violation of a license condition

(528/89-30-01).

Plant Chemistr

Chemical analysis results

were reviewed

or con ormance with Technical Specifications

and admin-

istrative control procedures.

Securit

Activities observed for conformance with

regu atory requirements,

implementation of the site

security plan,

and administrative

procedures

included

vehicle

and personnel

access,

and protected

and vital area

integrity.

The licensee

reported

two instances

of security guard

inattentiveness

during this inspection period.

The events

will be followed as part of the next routine security

inspection.

Plant Housekee

in

Plant conditions

and

mater>a

equipment storage

were observed to determine the

general

state of cleanliness

and housekeeping.

Housekeeping

in the radiologically controlled areas

was

evaluated with respe'ct to controlling the spread of

surface

and airborne contamination.

Radiation Protection Controls

Areas observed

included

contro

point operation,

records of licensee's

surveys

within the radiological controlled areas,

posting of

radiation

and high radiation areas,

compliance with

Radiation

Exposure

Permits,

personnel

monitoring devices

being properly worn, and personnel frisking practices.

~

~

~

~

The licensee

discovered

several

radioactive

isotopes

[Cobalt-60 (Co-60), Cesium-137

(Cs-137),

Manganese-54

(Mn-54) and Antimony-125 (Sb125)j in the Unit 1 and

3

cooling tower sludge

on July 14,

1989.

This sludge

had

been

dumped on-site in the Water Reclamation Facility

landfill in May 1989.

The licensee's

guality Audits and

Monitoring personnel

identified the problem during

a

routine audit.

Regional

health physics

inspectors will

followup on the licensee's

monitoring and disposal of the

sludge.

One violation of an

NRC license condition was identified.

4.

En ineered Safet

Feature

S stem Walkdowns - Units 1,

2 and

3

Selected

engineered

safety feature

systems

(and systems

important to

safety)

were walked

down by the inspector to confirm that the

systems

were aligned in accordance

with plant procedures.

During

the walkdown'of the systems,

items

such

as hangers,

supports,

electrical

cabinets

and cables,

were inspected

to determine that

they were operable,'and

in a condition to perform their required

functions.

Accessible portions of the following systems

were walked

down during this inspection period.

Unit 1

o

Class

lE Batteries

o

Remote

Shutdown

Panel

o

"B" Emergency

Diesel

Generator

Unit 2

o

Class

1E Batteries

o

Remote

Shutdown

Panel

o

Auxiliary Feedwater

System

o

"A" and

"B", Emergency Diesel

Generator

Unit 3

o

Class

1E Batteries

o

"B" Emergency Diesel Generator

During the inspection period, the inspector walked

down the Unit 3

Class

1E batteries.

The inspector

observed that the inter-cell

bus

ties for the "C" battery

had been

removed from 42 of the 60 cells in

the battery.

The inspector inquired into the work in progress

and

found that the "C" battery

had been out of service for approximately

3 weeks

pending resoluti'on of a problem involving proper torque for

the bolted connector for the inter-cell

bus ties to the cell posts.

Licensee representatives

from electrical

maintenance

stated that the

problem was found to exist only on the "C" battery

and not the other

batteries

which were in service.

The inspector found the ongoing

resolution of the problem to be adequate.

No violations of NRC requirements

or deviations

were identified.

5.

Monthl

Surveillance Testin

- Units 1,

2 and

3

61726)

a

~

b.

Selected

surveillance tests

required to be performed

by the

Technical Specifications

(TS) were reviewed

on

a sampling basis

to verify that:

1) the surveillance tests

were correctly

included

on the facility schedule;

2)

a technically adequate

procedure

existed for performance of the surveillance tests;

3)

the surveillance tests

had

been

performed at the frequency

specified in the TS; and 4) test results satisfied

acceptance

criteria or were properly dispositioned.

Specifically, portions of the following surveillances

were

observed

by the inspector

during this inspection period:

Unit 1

P

d

~D

o 36MT-9Sg01

Radiation Monitoring Monthly Functional

Test

o 36MT-9ZZ02

Remote

Shutdown

Panel

System Instrumentation

Calibration

Unit 2

d

o 42ST-2ZZ16

Routine Surveillance Daily Midnight Logs

o 42ST-2AF02

Auxiliary Feedwater

Pump AFA-POl Operability

Test

Unit 3

Procedure

Descri tion

o

73ST-3DG01

Class

1E Diesel

Generator

and Integrated

Safeguards

Surveillance'Test

Train "A".

No violations of NRC requirements

or deviations

were identified.

6.

Monthl

Plant Maintenance

- Units 1,

2 and

3

62703

a

~

During the inspection period, the inspector

observed

and

reviewed selected

documentation

associated

with maintenance

and

problem investigation activities listed below to verify

compliance with regulatory requirements,

compliance with

administrative

and maintenance

procedures,

required

gA/gC

involvement, proper

use of safety tags,

proper equipment

alignment

and use of jumpers,

personnel

qualifications,

and

proper retesting.

The inspector verified that reportability

for these activities

was correct.

fl

l

I

II

b.

Specifically, the inspector witnessed

portions of the following

maintenance activities:

Unit 1

Descri tion

o

Plant Protective

System

Power Supply Replacement.

o

Emergency Diesel

Generator

"A" Piston/Cylinder

Replacement.

Unit 2

o

Steam

Bypass

Control Valve Tear

Down of 1008.

o

Steam

Bypass

Control Valve Modifications,

o

Atmospheric

Dump Valve Nitrogen Regulator Rebuild.

o

Main Feed

Pump Drain Line Die Penetrant

Test.

o

Replacement

of the Linear Calibrate Switch on Nuclear

Instrument

Channel

"B".

Unit 3

Descri tion

o

Repacking of Shutdown Cooling System Suction Line

Isolation Valve SI-654.

o

Calibration of High Pressure

Safety Injection

Pump

S04E

Agastat

Time Delay Relay.

No violations of NRC requirements

or deviations

were identified.

7.

Review of Licensee Contractor (}ualifications - Uriits

1

2,

and

3

The inspector

reviewed

the qualifications

and background verifi-

cations of two licensee contract

employees

from two different

contractor organizations.

The inspector

assessed

each individual's

reported training and experience

against their a'ssigned

duties.

In

addition, the inspector

assessed

the adequacy of the contractor

documented

background verification check.

Finally, the inspector

spot checked

the validity of the background

checks

by independently

verifying one of each

employee's

most recent

employment positions

which supported

the required qualification level per ANSI/ANS

3.1-1978Property "ANSI code" (as page type) with input value "ANSI/ANS</br></br>3.1-1978" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process..

8.

The 'inspector

concluded that the training and experience of each

employee

was accurately

represented

on the employee's

resume, that

the stated qualifications were sufficient for the duties assigned

and that the contractor organization

background verification check

was sufficiently detailed to provide assurance

that the

qualifications were acc'urate.

The inspector

had

no further

questions.

No violations of NRC requirements

or deviations -were identified.

Restart - Unit 2

92700

Palo Verde Unit 2 was voluntarily shutdown

on March 15,

1989 after

problems

were identified with the, Unit 1 Atmospheric

Dump Valves

(ADVs).

The

NRC subsequently

issued

a Confirmatory Action Letter

(CAL) on March 28, 1989, which confirmed the course of action the

licensee

would take prior to requesting

NRC concurrence

to restart

any of the Palo Verde units.

The licensee

compiled

a list of all

NRC concerns,

as well as all

concerns identified by their own investigation.

The

NRC review of

licensee

actions

taken in response

to these

concerns

was

documented

in inspection report 50-529/89-21.

On June

23,

1989, the licensee

responded

in writing to the

CAL dated

March 28,

1989.

The licensee

confirmed that the agreed

upon actions,

to restart

Palo Verde Unit 2 were complete with the exception of

work on Steam

Bypass

Control Valve (SBCV) 1008.

The licensee

also

agreed

to provide due dates for the completion of Unit 2 Post

Restart

items within 30 days of Unit 2 restart.

Additionally, the

licensee

indicated that

a Category

3 Investigation regarding

the

vendor interface with maintenance

during the setting of ADV nitrogen

'regulators

was expected

to be complete

by July 10,

1989.

On June 28,

1989, the licensee

sent another letter to the

NRC

explaining the discovery that

SBCV 1008 internals

were not in the

configuration required

by the design.

Specifically, three

wave

springs

were found in the valve rather than the one required.

The

licensee

also indicated that

a formal investigation

was initiated to

determine

the root cause of the extra wave springs.

Additionally,

the letter stated that

SBCV 1008 was restored to its design

configuration

and tested satisfactorily.

The licensee certified

that the Steam

Bypass

Control System

was fully functional.

The

NRC responded

to the licensee

on June

28, 1989, indicating the

licensee

had

NRC concurrence

to restart

Palo Verde Unit 2.

The Palo Verde Unit 2 reactor

was taken critial on June

29,

1989 at

0401

MST.

No violations of NRC requirements

or deviations

were identified.

Missed Procedure

Ste

While Flashin

Generator

Field - Unit 2

On June

29,

1989, at 1800

MST, with'eactor

power at approximately

12K, the Unit 2 Main Turbine tripped.

The secondary

oper'ator

(licensed reactor operator)

was attempting to flash the main

generator field when

he observed

the field ammeter

increase

to

approximately

4000

amps vice the normal

2100 amps, just prior to the

turbine trip.

The licensee's initial review determined that the operator

apparently failed to perform

a portion of the step prior to

attempting to flash the generator field.

The operators

performed

the immediate actions for a turbine trip and

no further attempts

were

made to flash the generator field.

The Plant Manager,

who was

in the Control

Room at the time, requested

that the System Engineer

return to the site to trouble shoot the problem and verify that the

higher than normal current observed

did not damage

the control

circuit.

The licensee's

subsequent

investigation indicated the operator

had

missed

a procedure

step

by not minimizing AC and

DC voltage

regulator settings

and observing the proper indicating lights prior

to flashing'he

generator field.

The licensee is continuing the

investigation

and

has

removed the operator

from control

room duties.

The generator

was successfully

placed in service

on June

30,

1989.

The licensee

changed

the investigation to a

Human Performance

Evaluation,

HPES-89-018,

which was not complete at the

end of the

report period.

The inspector will followup on this

HPES

and the

licensee's

HPES backlog in a future inspection

(529/89-30-01).

No violations of NRC requirements

or deviations

were identified.

Forced

Outa

e

Due To Pi

e Break - Unit 2

93702

On July 4, 1989, at 0033

MST, the licensee

began

a power reduction

from 100$ power'ue to

a leak on

a Main Feed

Pump suction pipe drain

line.

The initial leak

was from a one inch line upsteam of valve

FWN-V110, however,

a one inch line upstream of valve CDN-V628 also

started

leaking

and eventually failed.

The unit was taken off the

grid at 0324

MST and the reactor entered

Mode

2 at 0331

MST.

The licensee initiated an incident investigation to determine

the

cause of the piping failures.

The incident investigation

was not

complete at the

end of the inspection period,

however

the licensee

suspects

that the drain valves failed due to high cyclic fatigue

caused

by a feedwater recirculation valve not being fully closed.

Additionally, the licensee initiated Engineering Evaluation Request

EER-89-FW-013,

which was not complete at the

end of the inspection

period.

This item will be followed in a future inspection

(529/89-30-02).

10

The licensee

completed repairs to the piping and dye penetrant

testing of the other valves

on the Main Feed

Pump suction.

The

licensee

increased

power and paralleled

onto the grid on July 20,

1989.

No violations of NRC requirements

or deviations

were identified.

Reactor Tri

and Safet

In ection - Unit 2

93702

and

92700

On July 12,

1989 at 2212

MST, the Unit 2 reactor tripped from 100%

power on low DNBR due to the loss of power to 13.8

KV bus

NAN-S02,

which supplys

the

1B and

2B Reactor

Coolant

Pumps

RCPs).

The

resulting transient

caused

Reactor

Coolant System

RCS) pressure

to

decrease

below the

1837 psig setpoint for the Safety Injection and

Containment Isolation Actuation Signals

(SIAS) and (CIAS).

The

licensee

declared

an Unusual

Event

(UE) at 2223

MST due to low RCS

pressure,

which decreased

to 1823 psig.

The licensee

terminated

the

UE at 2322

MST after the plant was stabilized in mode

3 with two

RCPs running.

The licensee

did not activate the autodialer at the Shift

Supervisor's

discretion

and the wrong number

was dialed to activate

the county wide beeper

system, resulting in a failure to notify

emergency

response

personnel

as required.

Although these

notification methods failed an adequate

number of 'licensee

personnel

and management

responsed

to the event.

The inspector

responded

to the event

and personally

observed that

the unit had

been stabilized in mode 3.

The inspector closely

followed the licensee's

review of the event,

and in particular, the

licensee

engineering organization's efforts to determine

why RCS

pressure

decreased

to the point at which a SIAS occurred.

The

licensee

concluded that the excessive

RCS depressurization

was

caused

by

a combination of an improper Steam

Bypass

Control

System

(SBCS)

response

and excessive

leakage

past the pressurizer

spray

valves.

Through discussions

with licensee

personnel,

the inspector

determined that the spray valves

had

a 2-3 year history of problems

with the calibration of the valve operators.

Repeated

attempts

had

been previously made to correct the problem, apparently without

success.

In discussions

with licensee

managers, it appeared

that

the spray valve issue

had only recently

been brought to the

attention of a management

level high enough to ensure that

a more

comprehensive 'review of the problem would be undertaken.

The

inspector questioned

why this issue

had taken

such

a long period of

time to be addressed

by management

and suggested

that the licensee

thoroughly review the issue to assess

how it had been previously

handled.

The licensee

agreed that such

a review would be useful.

Pending further inspector

review of the adequacy of the licensee's

previous corrective actions for the spray valve, this was identified

as unresolved

Item 89-30-05.

Regarding

the

SBCS, the licensee

determined that the "Ouick Open"

controllers

had

been calibrated with data that had been superseded.

This resulted in the bypass

valves being open longer than

anticipated,

thereby resulting in an excessive

cooldown of the

RCS.

The loss of power to bus

NAN-S02 was

caused

by a failed potential

transformer fuse.

The licensee

was unable to determine

why the fuse

opened,

and returned

the fuse to the manufacturer for evaluation.

The inspector

reviewed the actions

taken

by the licensee to

determine whether the fuse

had

opened

due to

a valid circuit fault

and considered

the licensee's

actions appropriate.

As discussed

in

Licensee

Event Report

(LER) 50-529/89-009,

the licensee's

review of

the event is continuing.

The

LER will be supplemented

with the

results of this review.

The licensee

restarted

the unit on July 21, 1989, after the

immediate restart

concerns

were addressed.

No violations of NRC requirements

or deviations

were identified.

12.

Main Feedwater

Pum

Suction

Pi in

Over ressurization

- Unit 2

On July 21,

1989, during restart of Unit 2 following a reactor trip

on July 12, the licensee

discovered all six of the main feedwater

pump

(MFP) suction pressure

switches

deformed

due to

overpressurization.

The licensee

evaluated

the cause

and

consequences

of the overpressurization

and determined that it'did

not offset continuation of power escalation.

The licensee

determined that the piping was overpressurized

when

a

MFP

recirculation valve was opened, .thereby connecting

the

pump suction

and discharge

piping.

This allowed the

MFP suction piping to be

pressurized

by the

AFM system

due to a leaking check valve.

The inspector

reviewed the event

and the licensee's

resolution of

the problem as part of the lice'nsee's

post trip review.

Based

on

interviews with licensee

personnel

involved in the event,

the

inspector

determined

the following to be

an approximate

time line

for the event.

1989:

7/12

2200 Reactor Trip due to potential transformer

fuse

failure.

7/13

0100 Operations

started

the non-safety related auxiliary

feedwater

pump (AFN-POl).

0800 Post trip walkdown by systems

engineers

and

operations identified unexpected

cooldown of 7A

feedwater

heater outlet from 350 degrees

F to 140

de'grees

F.

Also cooldown

was noted affecting leakage

flow through the economizer control valve to the

No.

1 steam generator.

1000 Operations initiated Long Path Recirculation

(LPR) of

main feedwater inorder to cooldown the feedwater

heaters,

12

7/14

7/19

Operator noted difficulty'in opening

HFP bypass

valve V-13 due to high differential pressure.

(Apparently,

due to pressurization

of the down-

stream piping caused

by the leaking check valve

V-431).

1530

A MFP low pressure trip alarm.

(Apparently due to

failure of the pressure

sensor

due to over

pressurization

of the

HFP suction piping).

1930

B MFP low pressure trip alarm.

Operations

opened

V-46 to initiate LPR in support of

testing to determine

leakage

past

V-431

MFP alarms

were noted

by Operations

and Systems

Engineers

but no work order was written to

investigate

the problem.

V-431 seat

leakage

was repaired.

h'ork Order to investigate

MFP pressure

switch problem

was.written

when alarms

were again, noted during

startup preparations.

7/20

Reactor startup

commenced.

7/21 0030 Reactor Critical.

Six MFP pressure

switches

were replaced

when found to

be unable to calibrate in place.

0700 Pressure

switch was disassembled

in

18C shop

and

found deformed

due to,overpressure.

EER-89-CD-029 initiated.

0840 Hain generator

was synchronized to grid.

0900 Management

informed of concern for

overpressurization.

(Rx power

13K).

o

Calculation to evaluate

consequences

were

initiated.

1200

INC destructively evaluated

a new pressure

switch to

confirm failure mode

due to overpressure

at 1200 psi.

(Rx power 18K)

1330 Onsite engineering

concluded piping stresses

were

acceptable.

1400 Management decision

made to continue

power

escalation.

13

1700 Corporate

engineering

concurred with acceptable

stress

analysis results

EER-89-CD-029 dispositioned.

Based

on

a review of this time line, the inspector

observed

several

weaknesses

in the licensee's

approach

to resolution of this problem.

The licensee's

post trip review did not identify the abnormally

pressurized

feedwater piping due to the recognized

check valve

leakage.

Neither did it identify the overpressure

condition

resulting from initiation of LPR.

The post trip review did

address

the leakage

past

V-431 to ensure that it was repaired

prior to startup.

However, the inspector

found that the review

did not formally evaluate

the potential for pressurization

of

the feedwater piping as

a consequence

of the leakage.

As

a

result, the abnormally pressurized

condition of the feedwater

piping was not recognized

or evaluated prior to initiating LPR

to cooldown the feedwater heaters.

Although the operator

noted

unusual difficulty in opening

V-13 to initiate

LPR indicating

an unexpected

high differential pressure

across

the valve, the

potential for,overpressurizing

the

NFP suction piping was not

recognized.

2.

Due to inadequate

communications

between Operations

and Systems

Engineers,

a work order to investigate

and repair the

unexpected

NFP low pressure

alarms

was not initiated in a

timely fashion

when the condition was noted

on July 13, 1989.

The inspector

found that the delay in initiating corrective

actions until July 19,

1989,

appeared

to contribute to the

hurried review and disposition which resulted during startup.

3.

The management

decision to continue

power escalation

appeared

to have

been

based

on an informal resolution of the

consequences

of the overpressurization.

The initial bounding

calculations

and reviews appeared

to have. been

performed in a

hurried and informal manner with questionable

conservatism.

The review was not documented

and checked,

but rather

consensus

was obtained

from various engineering

organizations

over the

phone.

Walkdowns of the affected portions of the systems

were

done without procedures

or written guidance.

In resolving this problem involving non-safety related

equipment,

the inspector

found that the licensee

exhibited

a considerable

relaxation

from the rigor and formality exercised

in the control of

safety related

systems

and equipment.

Although the post trip review

addressed

all identified problems resulting from the trip, the

inspector

found the licensee's

resolution to be less

thorough in

dealing with non-safety related

problems.

The inspector considered

that this lack of a consistent

methodology

appeared

to be

a weakness

in the conduct of the licensee's

post trip review.

With the assistance

of technical

personnel

from the

NRC Office of

Nuclear Reactor Regulation

(NRR), the inspectors .reviewed in some

detail

the. licensee's

engineering

analysis of the effect of the

overpressure

condition

on the

MFW pipe.

The associated

pipe has

a

design

pressure

of 500 psia.

The licensee

analyzed

the pipe for an

overpressure

condition of approximately

1580 psia.

Initially the

licensee

assumed

that the weakest

component of the system

was the

large bore pipe.

The licensee

therefore

analyzed

the pipe, 'assuming

that if the pipe were found acceptable, it would bound all other

components.

The inspector

strongly questioned this assumption,

and

based

on prompting from the

NRC, the licensee

reviewed other

components.

The licensee

then determined that several

30 inch

flanges

were actually the limiting components,

and that these

flanges

may have exceeded

the minimum yield strength.

The licensee

concluded that the flanges

were acceptable for continued

use

based

in part

on hardness

testing,

magnetic particle testing,

and visual

inspections, all of which indicated that the flanges

were not

damaged

by the event.

The inspector discussed

the various

above observations

with licensee

management

who acknowledged

the inspector's

concerns.

The licensee

indicated that they were continuing their investigation into the

incident and would be revising their Incident Investigation

Report

IIR-2-2-89-001 to include

a more thorough review of the

overpressurization

incident.

This report was not complete at the

end of the inspection period.

Pending further inspector

review of licensee corrective actions,

this was identified as

a second corrective action item for

unresolved

item 89-30-05.

No violations of NRC requirements

or deviations

were identified.

Load

Re 'ection

From 100K Power - Unit 2

93702,

92700

On August 4,

1989, at 0822,

MST, Unit 2 experienced

a load rejection

due to a turbine trip from 100% power .

The operators

stabilized the

plant at 40K reactor

power on the Steam

Bypass Control System after

the turbine trip and subsequently

reduced

power to

10% while the

cause of the trip was being investigated.

The licensee initiated

a Catagory

3 investigation

immediately.

The

licensee

found that the turbine trip was initiated from Control

Element Drive Mechanism

(CEDM), Control System

Power

Bus Under

Voltage

(UV) coils that deenergized

with power still present.

The

drop out voltage

as

found to be abnormally high for UV coils

1 and

3, and within acceptable

limits for coils

2 and 4.

Additionally,

the

CEDM Motor Generator

(MG) output voltage

was found to be set at

233 volts rather than the required

240 plus-or-minus

3 volts.

Coils

1, 2, and

3 were replaced

and the output of the

MG sets

was

increased.

No violations of NRC requirements

or deviations

were identified.

II

4

1

Il

f

t

1

l

15

14.

Im ro er Maintenance

on Atmos heric

Dum

Valves Nitro en

Su

1

Re ucin

Re

u ator

a ves

V.

e

u ator

a ves

-

n>t

62 03

The inspector

reviewed- several

completed

work packages

and

interviewed craftsmen,

supervisors,

engineers

and

a vendor

representative,

all associated

with the Unit 2 ADV regulator valves

(2JSGAPCV0310,

2JSGAPCV0317,

2JSGBPCV0303,

and

2JSGBPCV0323)

due to

ongoing difficulties with the operability and reliability of the

ADV

regulators.

Work order No. 00354032 for ADV regulator valve

2JSGAPCV0317

required the valve to be disassembled,

cleaned

and inspected,

and

re-assembled

per technical

manual

No. J091-32 using sections

applicable to MDL No. 7Gg-'010.

This work order was performed from

April 14 to April 16,

1989.

The 'instructions for re-assembly

and

setting the regulator valve contained in the technical

manual

were

not used;

instead

the regulator valve was re-assembled

and set

based

on verbal information obtained

from a vendor representative.

This

assembly

and setting of the regulator valve caused

a continued

lack

of reliability and operability until the valve was reworked in mid

June

1989.

Upon subsequent

rework of the regulator valve, with the aid of a

different vendor representative, it was determined, that the

regulator valves

were incorrectly set

and that proper reassembly

and

setting could be achieved

by following the instructions in the

technical

manual.

Craftsmen,

supervisors,

and quality control personnel

were aware

that the information provided by 'the first vendor representative

deviated

from the technical

manual;

however,

no actions

were taken

to resolve the issue.

Working per verbal information and failing to follow approved

work

orders

and the vendor technical

manual,

which resulted

in lack of

reliability of the

ADV regulator valves, is considered

a violation

of regulatory requirements

(529/89-30-03).

Arizona Public Service

Company

memorandum

No. 260-00112-WCM, dated

June

21,

1989, briefly

describes

the improper maintenance

and

immediate corrective actions.

Work orders

365985,

365995,

365996,

and 365997 for ADV regulator

valves

2JSGBPCV0303,

2JSGAPCV0310,

2JSGAPCV0317,

and

2JSGBPCV0323,

respectively,

were all performed during June 17-20,

1989,

and

required work to be performed

per vendor technical

manual

No. J691-32.

This technical

manual,

dated

November, 5, 1980,

was

superseded

when the vendor issued

a new technical

manual

dated

December

28,

1983.

The

new technical

manual,

No. J691-83,

was

reviewed

by engineering,

plant standards,

engineering evaluation,

and the material control group,

and subsequently

approved

on

April 19,

1989.

The

new manual,

J691-83

was not used or referenced

in the above work orders,

except in an amendment to work order 365997,

where technical

manual

No. J691-83

was required for several

steps

but technical

manual

No. J691-33

was required for a later

step.

It was not clear as to what technical

manual

should

have

been

16

used

on all four of the work orders

and it was not clear that there

were adequate

measures

to ensure that vendor technical

manuals

were

properly controlled to provide the most recent,

approved versions

for maintenance.,

This item is open pending further review

(529/89-30-04).

Inte rated Safe uards Surveillance Testin

- Unit 3

61701

The inspector

reviewed procedure

73ST-3DG01,

Revision 1, "Class

1E

Diesel

Generator

and Train "A" Integrated

Safeguards

Surveillance

Test",

and observed

selected

portions of this test.

During the review of the procedure

the inspector

noted that there

was

no mention of pretest briefings

and that the pre-requisites

for

the procedure

were complex and confusing 'in that not all

pre-requisites

are required for each test section

and not all test

sections

indicated the applicable pre-requisites.

The procedure

did

require that the shift supervisor

and test engineer establish

the

pre-requisites

as required.

The inspector

observed

the pre-test briefing for section 8.3 of the

procedure.

The test director briefed the operators

on the

objectives of the test

and the actions

expected of each operator

during the test.

Ouestions

about the test were properly resolved at

this time.

During the test the inspector

observed that the operators

maintained

control of plant conditions

and the test sequence.

When

a

procedural

problem arose,

the inspector

observed that the test

director and shift supervisor

took proper actions to ensure that

plant administrative

procedures

were properly followed.

Problems

identified by the test appeared

to be properly documented

by plant

personnel

to be resolved

by following the proper

Palo Verde Nuclear

Generating Station procedure.

During this test the inspector also observed

operations of the "A"

Train emergency

diesel

generator.

The operator s properly adhered

to

the plant written procedures.

The equipment functioned

as designed.

No violations or deviations of NRC requirements

were identified.

Oualit

Hotline Review

71707)'he

inspector

reviewed the licensee's

Ouality Hotline status

and

selected

several

current

and closed investigations for review.

The

files 'that were reviewed appeared

to address

the concerns,

and

contained

conclusions

and supporting documentation.

The inspector

will continue

t'o followup on selected

Ouality Hotline concerns

in

future inspections.

No violations or deviations of NRC requirements

were identified.

17

17.

Office of Nuclear Reactor

Re ulation

NRR

Reviews

18.

Several

issues

associated

with restart of Unit 2 were referred to

NRR for review.

The issues

were as follows:

Multiple Control Element Assembly

(CEA) slippage

Position indication problems with CEA ¹9

Steam generator

tube plug integrity

Low pressure

safety injection header drain valve weld performed

by an unqualified welder.

NRR interfaced directly with the licensee

on these

issues

and

concluded that the licensee's

actions

were acceptable

for restart of

Unit 2.

Review of Periodic

and

S ecial

Re orts - Units

1

2 and

3

90713

Periodic

and special

reports

submitted

by the licensee

pursuant to

Technical Specifications 6.9.1

and 6.9.2 were reviewed

by the

inspector.

This review included the following considerations:

the report

contained

the information required to be reported

by

NRC

requirements;

test results

and/or supporting information were

consistent with design predictions

and performance specifications;

and the validity of the reported information.

Within the scope of

the above,

the following reports

were reviewed

by the inspector.

Unit

1

o

Monthly Operating

Report for June,

1989.

Unit 2

o

Monthly Operating

Report for June,

1989.

Unit 3

19.

20.

o

Monthly Operating

Report for June,

1989.

No violations of NRC requirements

or deviations

were identified.

Unresolved

items are matters

about which more information is

required to determine

whether

they are acceptable

or may involve

violations or deviations.

One

new unresolved

item identified during

the inspection is discussed

in paragraphs ll and

12.

Exit h1eetin

The inspector

met with licensee

management

representatives

periodically during the inspection

and held an exit meeting

on

August 10, 1989.

The licensee

acknowledged

the inspectors

comments

and concerns.

'