ML17300B270

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Insp Repts 50-528/96-07,50-529/96-07 & 50-530/96-07 on 960421-0601.Violations Noted.Major Areas Inspected: Engineering,Maint & Plant Support
ML17300B270
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 06/21/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17300B267 List:
References
50-528-96-07, 50-528-96-7, 50-529-96-07, 50-529-96-7, 50-530-96-07, 50-530-96-7, NUDOCS 9606280120
Download: ML17300B270 (65)


See also: IR 05000528/1996007

Text

ENCLOSURE

2

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-528

50-529

50-530

NPF-41

NPF-51

NPF-74

50-528/96-07

50-529/96-07

50-530/96-07

Arizona Public Service

Company

Palo Verde Nuclear Generating

Station,

Units 1,

2,

and

3

5951

S. Wintersburg

Road

Tonopah,

Arizona

April 21 through June

1,

1996

J.

Kramer, Resident

Inspector

D. Garcia,

Resident

Inspector

D. Carter,

Resident

Inspector

J. Russell,

Resident

Inspector,

San Onofre

D. Acker, Senior Project Inspector

A. Mcgueen,

Emergency

Procedures

Analyst

B. Olson, Project Inspector

P. Goldberg,

Reactor

Inspector

D. F. Kirsch, Chief, Reactor Projects

Branch

F

9bOb280120

9b0b2i

PDR

ADOCK 05000528

6

PDR

I

EXECUTIVE SUMMARY

Palo Verde Nuclear Generating Station,

Units 1, 2,

and

3

NRC Inspection

Report 50-528/96-07;

50-529/96-07;

50-530/96-07

This integrated

inspection

included aspects

of licensee

operations,

engineering,

maintenance

and plant support.

The report covers

a 6-week period

of resident

inspection.

~0eratioos

~

The conduct of operations

was generally professional

and safety

conscious

(Section 01.1).

~

Operators

exhibited

an overall strong performance

during the Unit

1

reduced

inventory condition.

The dedicated

midloop reactor operator

displayed

an excellent

example of board monitoring by noticing

unexpected

volume control. tank level loss

due to chemistry sampling

(Section 01.2).

I

Operators

performed the startup of the Unit

1 reactor

and main generator

in a careful

and professional

manner.

The control

room staff

appropriately

addressed

the failure of a control element

assembly

(CEA)

to initially move (Section 01.3).

The Unit 2 startup

communications

were generally concise

and utilized

repeatbacks.

The"control

room supervisor maintained positive control

over the evolution.

On two, occasions,

the operators

appropriately shut

down the reactor

when they encountered

reactivity discrepancies

(Section

01.4).

~

Operations

management

corrective actions for previously identified

p. oblems

appear to address

the observed

inconsistency

in operator

performance

(Section 01.5).

~

Crew briefings enhanced

communications within and between

crews (Section

01.6).

~

The inspectors

identified an example of a violation regarding

the

failure of operators

to follow procedure

and declare

both trains of low

pressure

safety injection (LPSI) inoperable.

In addition, the

operations

crew, site shift manager,

and

a compliance representative

decided the

LPSI trains were operable

by using

a justification that did

not contain

an adequate

technical

basis

(Section 04. 1).

An additional

example of a violation was identified regarding

the

failure of an auxiliary operator

to follow the

steam generator

blowdown

system realignment

procedure,

which resulted

in exceeding

the licensed

thermal

power limit by

a small

amount

(Section 04.2).

I

I

-3-

Maintenance

~

The inspectors

observed

a high level of interaction

between

the shift

supervisor,

maintenance

engineers,

and technicians

to ensure that

feedwater control

system troubleshooting

did not result in a feedwater

transient

(Section Ml.1).

~

The inspectors

observed

several

maintenance

activities during the report

period.

The activities were performed

as required

by instructions

and

in a professional

manner

(Sections

Ml. 1 and H1.2).

~

Troubleshooting efforts to determine

the root cause of the initial

overspeed trip of the auxiliary feedwater

(AFW) pump were extensive

and

detailed

(Section H1.3).

~

A noncited violation was identified regarding the failure to verify the

correct type of trisodium phosphate

required

by Technical Specification

(TS).

The licensee's

effort to identify the discrepancy

and to obtain

an emergency

TS change

was very good.

However,

the licensee

missed

an

opportunity to identify another

problem with a related surveillance

requirement

during review and submittal of the emergency

request

(Section M3.1).

~

The inspectors

identified

a noncited violation regarding

the failure of

a technician to follow procedures

when propping

open heating,

ventilation,

and air conditioning

(HVAC) doors.

Management's

response

to the inspectors-identified

problem was prompt (Section

M4. 1).

~

A noncited violation was identified regarding the Licensee

Event

Report

(LER) for failure to comply with the

TS surveillance

requirement

to test "at least

10 percent" of the circuit breakers

each

18 months

(Section

H8. 1).

~

A noncited violation was identified regarding the

LER reported

containment

spray

TS violation resulting from an unrecognized mini-flow

recirculation valve failure (Section H8.2).

~

A noncited violation was identified regarding the

LER reported failure

to comply with the

TS surveillance

requirement

to verify containment

penetration circuit breakers"were

open

(Section M8.3).

En ineerin

~

Engineering's effort to understand

the root cause of American Telephone

and Telegraph

(AT8T) round cell battery degradation,

to better predict

future cell performance,

and the technical

actions in response

to the

Unit 2 battery test results

were excellent

(Section

E2. 1).

l

1

I

Engineering's

original root cause

determination of a solenoid valve wire

degradation

was incorrect,

although it was reasonable

based

on

information available at the time.

Engineering's

planned corrective

actions to address

the long term environmental qualification of the

valves

were appropriate

(Section E2.2).

~

Engineering calculations

demonstrated

that

a full core offload of the

fuel assemblies

during refueling operations

was acceptable

(Section

E3.1) .

Plant

Su

ort

A noncited violation was identified regarding

the failure of a chemistry

technician to follow procedure.

During midloop operations

a technician

opened

a sample valve without notifying the control

room and left the

area.

The loss of inventory had

no safety

consequence

(Section Rl. 1).

The containment material condition

and housekeeping

improved,

as

compared to the previous Unit 3 containment

walkdown.

The safety

consequence

of the debris

found in containment

was negligible.

Additional walkdowns of containment,

as jobs were completed,

were

appropriate

(Section

R2. 1).

The inspectors identified

a violation with three

examples of improper

posting

and inadequate

contamination control.

Routine tours

by RP,

maintenance,

and operations

personnel

had not been effective in

identifying leaking components

which had inadequate

contamination

controls

(Section R2.2).

1

l

f

f

1

I

I

Re ort Details

Summar

of Plant Status

Unit

1 began this inspection

period in Mode 5.

The unit was in an outage to

replace

the shaft

on Reactor

Coolant

Pump

2B.

On May 3, the unit returned to

100 percent

power

and remained at essentially

100 percent

power for the

duration of the inspection period.

Unit 2 began this inspection period defueled.

On Hay 4, following completion

of Refueling Outage

2R6, the unit commenced

a reactor startup

and

power

ascension.

On May 8, the unit reduced

power to 40 percent to repair

a leak in

a circulating water system

manway.

On May 10 Unit 2 returned to 100 percent

power

and remained at essentially

100-percent

power for the duration of the

inspection period.

Unit 3 operated

at essentially

100 percent

power for the duration of the

inspection period.

I. 0 erations

Ol

Conduct of Operations

01. 1

General

Comments

71707

Using Inspection

Procedure

71707,

the inspectors

conducted

frequent

reviews of ongoing plant operations.

In general,

the conduct of

operations

was professional

and safety conscious.

Specific events

and

noteworthy observations

are detailed in the sections

below.

a.

Ins ection

Sco

e

71707

The inspectors

reviewed preparations

for and control of the reduced

inventory operations,

conducted

in accordance

with Procedure

400P-9Z216,

"Reactor Coolant System Drain Operations."

b.

Observations

and Findin

s

On April 21, the inspectors

observed

the operators

drain the reactor

coolant

system to

a midloop condition.

The inspectors

observed

good

communications

between the operators

and

a strong

command

presence

of

shift supervision.

The inspectors

observed

a nuclear

assurance

evaluator

ask probing procedural

and equipment questions.

On April 22, the dedicated

midloop reactor operator noted

an unexpected

response

in volume control tank level.

The reactor operator's

observation

subsequently

led to the identification of the uncontrolled

loss of inventory caused

by an open

and unattended

sample

valve

as

discussed

in Section

R1.1.

01.3

Plant Startu

Unit

1

a

~

Ins ectors

Sco

e

71707

The inspectors

observed

portions of reactor startup

performed in

accordance

with Procedure

400P-9ZZ03,

"Reactor Startup."

In addition,

the inspectors

observed

portions of main generation

and excitation

system startup

performed in accordance

with Procedure

410P-1MB01,

"Main

Generation

and Excitation."

b.

Observations

and Findin

s

01.4

The inspectors

observed

the operators

withdraw shutdown

Group

A control

element

assemblies

(CEAs)

and noted that the operators

performed the

operation in accordance

with the procedure.

When the operators

started

to withdraw shutdown

Group

B,

CEA 23 failed to move with the rest of the

shutdown

group

and

was out of sequence

with the other

CEAs in the group

by approximately

5 inches.

The operators

attempted

to move the'CEA in

manual with no success.

The licensee

performed troubleshooting

and

identified

a failed card associated

with this

CEA.

The licensee

replaced

the card

and successfully

withdrew shutdown

Group

B.

The

inspector

found that the licensee's

actions

were appropriate

in stopping

operations

to identify and correct the equipment

problem.

Reactor Startu

Unit 2

a.

Ins ection

Sco

e

71707

On May 1, the inspectors

observed

the initial attempt to perform the

Unit 2 reactor startup in accordance

with Procedure

400P-9ZZ03,

Reactor

Startup."

b.

Observations

and Findin

s

The control

room supervisor maintained positive control of the evolution

by providing appropriate direction to reactor operators,

reactor

engineers,

and other members of the operating staff.

The inspectors

noted during the startup that operators

on two occasions

appropriately

inserted

CEAs due to reaching licensee

established

administrative limits

for differences

between

the estimated critical position

and the critical

position plotted during the startup.

The engineering

aspects

of the

startup

are discussed

in Section

E1.3.

01.5

0 erations

Recent

Performance

a.

Ins ection

Sco

e

71707

The inspectors

had discussions

with the operations director,

an

operations

department

leader,

and nuclear

assurance

operations

concerning

recent operations

performance.

b.

Observation

and Findin

s

The licensee

had determined that improvements

in operation

performance

were not consistently

sustained.

Previous

NRC inspection reports

documented

negative findings concerning control board monitoring,

attention to detail,

and procedural

adherence.

The licensee

had taken several

actions

in response

to the

inconsistencies

identified in crew performance:

The Nuclear Assurance

organization

assigned

a staff of about

15

people dedicated

to the assessment'f

operations

performance.

This staff performs operations

audits

and assessments,

and

operations

department training.

The Operations

organization initiated several

actions to improve

crew performance.

Operations

management

clearly defined

a set of

operations

standards

for performance,

assured

that all operations

staff were trained

and knowledgeable of the standards,

and

=implemented

a practice of discussing

standards

and shortcomings

with individuals involved in events.

Several

self-assessments

of

operations

performance

were conducted,

and feedback

was provided

to the staff.

A continuous

assessment

program

was established

for

use

by individuals performing or monitoring activities to assess

various attributes of performance

in the areas of safety,

ownership

(watchstanding,

monitoring, verification practices,

logs, shift turnover,

documentation,

communications,

etc.),

professionalism,

and leadership.

In addition, expectations

have

been reinforced during requalification crew training.

The results of these, initiatives have

been manifested

by several

recent

evolutions which were performed well (Units

1 and

2 midloop operations,

Units

1 and

2 reactor startups

and shutdowns,

Unit 2 stuck fuel assembly

removal,

and Unit

1 reactor coolant

pump repair outage).

However,

as

noted in Section

04, additional attention is warranted to establish

consistent

good performance.

The licensee

plans to continue

implementation of activities to provide further improvement

and

consistency

to operations

organization

performance.

01.6

Shift Crew Briefin s

a ~

Ins ection

Sco

e

71707

b.

The inspectors

attended

several

operations

morning shift crew briefings

and held discussions

with the auxiliary operators.

Observations

and Findin

s

The inspectors

observed that auxiliary operators

played

an active role

in the crew briefings.

At the start of the brief, each auxiliary

operator

presented

the status of their areas

of responsibility.

The

inspectors

found that the auxiliary operators

were very familiar with

equipment status

and problems in their areas

of responsibility.

The licensee

had established

a reflection period

oF approximately

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, during the middle of the shift, where all nonessential

work is

stopped.

The operations

crew members

met in the control

room and

discussed

the morning activities

and plans for the remainder of the

shift.

In addition,

management utilized the time for lessons

learned

briefings,

as well as safety meetings.

At the end of the shift, operations

performed

a shift briefing similar

to the morning briefing.

The briefing'allowed the staff to focus

on the

information passed

on to the next crew.

01.7 'onclusions

on Conduct of 0 erations

Operators

exhibited

an overall strong performance

during the Unit

1

reduced

inventory condition.

The dedicated

midloop reactor operator

displayed excellent

board monitoring by noticing unexpected

volume

control tank response,

resulting in the early identification of reactor

coolant inventory loss.

The licensee

performed the startup of the Unit

1 reactor

and main

generator

in a careful

and professional

manner.

The licensee

appropriately

addressed

a failure of a

CEA to initially move.

The Unit 2 startup

communications

were generally concise

and utilized

repeatbacks.

The control

room supervisor maintained positive control

over the evolution.

The operators

performed appropriately to shut

down

the reactor

when they encountered

reactivity discrepancies.

Operations

management

corrective actions

appear

appropriate

to address

the observed

inconsistency

in operator

performance.

The crew briefings enhanced

communications within and between

crews.

04

04.1

Operator

Knowledge

and Performance

LPSI

0 erabilit

Unit 2

'a ~

Ins ection

Sco

e

71707

'b.

On May 2, during

a tour of the control

room, the inspectors

reviewed the

unit log and noted

an entry indicating that both trains of LPSI may have

been inoperable,

but not declared

inoperable.

Subsequently,

the

inspectors

reviewed the applicable

procedures

being utilized, 400P-

9SI02,

"Recovery from Shutdown Cooling to Normal Operating Lineup,"

and

40AL-9RK2B, "Panel

B02B Alarm Responses."

Observations

and Findin

s

The inspectors

reviewed the unit log and identified

a discrepancy

during

the performance of the boration of the cold leg injection lines.

The

unit log indicated that three of four pressure

indicators (safety

injection tank line pressure)

showed pressure

greater

than

1540 psig,

a

condition that could impact both

LPSI trains.

The log also indicated

that the shift technical

advisor, shift supervisor,

site shift manager,

and

a nuclear compliance representative,

discussed

the condition and

agreed that,

since the condition was .caused

by the performance of an

approved plant Procedure

(400P-9SI02)

and that actions

were taken to

promptly rectify the situation, operability of the

LPSI trains

was not

affected.

The licensee

had previously determined that if the pressure

exceeded

1540 psig downstream of the

LPSI injection valves,

the valves might not

"open with the large differential pressure

across

the valves

(pressure

locking).

Specifically, under worst case

design basis,

the valve

actuator

motor would be subject to stall torque conditions

and could not

open the injection valve.

The inspectors

requested

a pressure

history for the four transmitters

from the shift technical

advisor.

In review of the trends,

the

inspectors

noted that initially all four transmitters

indicated that

pressure

exceeded

1540 psig

and that pressure

on three of the four

remained

above

1540 psig for approximately

15 minutes.

In addition, the

maximum pressure

on one of the transmitters

reached

approximately

1700

psig.

Procedure

40AL-9RK2B, alarm window SI

CHK VLV LEAK PRESS

HI prescribed,

in part, that, if the indicated pressure

is greater

than

1540 psig, it

was necessary

to declare

the associated

LPSI train inoperable

and enter

the associated

TS.

The inspectors

considered

that the licensee's

stated

reason for not declaring the

LPSI trains inoperable

(because

the

operators

were performing

an approved plant procedure

to borate the cold

leg injection lines)

was without

a technical

basis

and was, therefore,

an inadequate justification for operability.

In addition,

when the

-10-

04.2

operators

decided

not to declare

the valves inoperable contrary to the

actions prescribed

by Procedure

(40AL-9RK2B), they did not take action

to revise the procedure.

The inspectors

concluded that operators failed

to declare

both trains of LPSI inoperable

as required

by 40AL-9RK2B.

This is an example of a violation of TS 6.8. 1 (50-529/96007-01).

On Hay 8, the inspectors

informed valve services

and system engineering

groups of the problem.

Both groups

were unaware of the event

and

indicated they would perform an operability evaluation

based

on actual

plant conditions to determine if the

LPSI trains were, in fact,

inoperable.

Subsequently,

engineering

determined that,

although the

pressure

in the alarm response

procedure

was exceeded,

revised

calculations with new degraded grid information provided

a technical

basis that the

LPSI valves were operable until the pressure

transmitters

exceed

1850 psig.

On Hay 17, the licensee

revised

Procedure

40AL-9RK2B to reflect the

new

pressure

value

and issued

a night order to the operating

crews to inform

them of the change.

Misali nment of Steam Generator

Blowdown

S stem

Unit 2

'a ~

Ins ection

Sco

e

71707

The inspectors

reviewed the licensee's

response

to the Hay ll,

misalignment of the steam generator

blowdown system,

which resulted

in

power operation

in excess

of the licensed

thermal limit.

b. Observations

and Findin

s

On Hay 11, Unit 2 operators

reduced reactor

power to 99 percent

and

performed high rate

steam generator

blowdowns to the main condenser.

Subsequently,

an auxiliary operator

was dispatched

to realign the steam

generator

blowdown system for normal

blowdown to the blowdown flash

tank.

The realignment

was completed,

and reactor

power

was returned to

100 percent.

On May 13,

a reactor operator questioned

a difference

between reactor

power calculated

from primary plant parameters

and reactor

power

calculated

from secondary

plant parameters.

At the

same time,

an

auxiliary operator questioned

the lineup of the blowdown system.

Investigation

found that the

blowdown system

from one of the steam

generators

to the

blowdown flash tank was isolated.

The isolation of

the system resulted

in actual

reactor

power being greater

than indicated

reactor

power.

The licensee

calculated that actual

reactor

power

exceeded

indicated

power by approximately 0.28 percent for a period of 66 hours7.638889e-4 days <br />0.0183 hours <br />1.09127e-4 weeks <br />2.5113e-5 months <br />.

The

highest rolling 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> average of actual

reactor

power was determined

to be 100.27 percent.

The inspectors

noted that this event

was

bounded

~ I

F,

-11-

04.3

by the assumptions

in the Updated final Safety Analysis Report

(UFSAR)

for thermal

power of 102 percent.

The inspectors

discussed

the event with Unit 2 operations

management.

The inspectors

learned that the auxiliary operator

had not carried

a

copy of nor followed Procedure

420P-2SG03,

"Operating the

Steam

Generator

Blowdown System,"

and

had relied

on memory while realigning

the blowdown system.

The failure of the auxiliary operator to follow

procedure is

a second

example of a violation of TS 6.8. 1

(50-529/96007-01).

The licensee initiated Condition Report/Disposition

Request

(CRDR) 2-6-0113 to evaluate

the event.

In addition to determining that

the auxiliary operator did not use

a procedure to perform the valve

realignment,

the licensee

determined that:

supervision

was not

adequately

ensuring

the operations

expectations

were being met with

regard to procedural

adherence;

and control

room operators

made wrong

assumptions

regarding the response

of indications

from the blowdown

flash tank after the realignment.

Conclusions

on 0 erator

Knowled

e and Performance

A violation was identified involving .two examples of failure to follow

procedures:

the failure to follow the 'alarm response

procedure

by not

declaring

both trains of LPSI inoperable,

and the failure to follow the

steam generator

blowdown procedure,

which resulted

in slightly exceeding

the licensed

thermal

power limit.

The decision that the

LPSI valves were operable

was

based

on inadequate

technical

information and did not include engineering's

evaluation.

An

engineering

evaluation of the situation

was not performed until the

inspectors

raised questions.

The licensee

performed additional

engineering

evaluations

and concluded that the

LPSI system

was operable

at the pressures

encountered

and revised the procedure to include the

new operability criteria.

The licensee

appropriately initiated

an investigation into the causes

of

the misalignment of the steam generator

blowdown system.

The results of

their preliminary investigation

appeared

to reflect the causes

of the

event.

08

08.1

MISCELLANEOUS OPERATIONS

ISSUES

(92901)

Closed

LER 50-529 94007:

momentary entry into TS 3.0.3

due to

personnel

error.

This

LER was

a minor issue for which the licensee's

actions

were appropriate.

This

LER was closed.

-12-

II. Maintenance

Hl

Conduct of Maintenance

Ml. 1

General

Comments

on Maintenance Activities

a

~

Ins ection

Sco

e

62703

The inspectors

observed all or portions of the following work

activities:

~

32MT-9SB03

Maintenance of Westinghouse

Type DS-416 Reactor Trip

Switchgear

(Unit 3)

~

31MT-9RC06

Reactor Coolant

Pump Disassembly

and Assembly (Unit 1)

WO 0756393

Troubleshoot

Feedwater

Control

System to Determine

Cause of Spurious Oscillations (Unit 2)

b.

Observations

and Findin

s

The inspectors

found these

work activities were performed in accordance

with procedures.

In particular,

the inspectors

observed

a high level of

interaction

between

the shift supervisor,

maintenance

engineers,

and

technicians

to ensure that the feedwater control

system troubleshooting

(WO 07566393)

did not result in

a feedwater transient.

In addition,

see

the specific discussions

of maintenance

observed

under Section Ml.3.

M1.2

General

Comments

on Surveillance Activities

a.

Ins ection

Sco

e

61726

The inspectors

observed all or portions of the following surveillance

activities:

~

32ST-9SB02

18 Month Surveillance Test for Westinghouse

Type 4DS-416 Reactor Trip Breakers

(Unit 3)

~

42ST-2SG03

Testing Atmospheric

Dump Valves in Mode

3 (Unit 2)

~

42ST-2ZZ24

Startup

Channel

High Neutron Flux Alarm

Inoperable

3. 1.2.7 (Unit 2)

b.

Observations

and Findin

s

The inspectors

found these surveillances

were performed

as specified

by

applicable

procedures.

-13-

Ml.3

AFW Pum

Tri

Unit 2

a

~

Ins ection

Sco

e

62703

On May 1, the inspectors

observed initial troubleshooting of the

overspeed trip of the turbine driven

AFW pump during the Unit 2 startup.

In addition,

the inspectors

reviewed the operability determination

and

discussed

the determination with maintenance,

engineering,

and

operations.

On May 17, the inspectors

observed

a performance test of

the

AFW pump.

b.

Observations

and Findin

s

C.

Approximately 10 minutes into

a postmaintenance

test run, the

AFW pump

speed

ramped

up over

a

15 second

period,

and the

pump tripped

on

overspeed.

The licensee initiated

an investigation

team to troubleshoot

and gather data.

The licensee

instrumented

and performed additional

test runs of the

pump.

Equipment evaluated

by troubleshooting

included:

the governor valve linkage, turbine governor controls

(both electric

and

hydraulic),

DC control

power,

and the steam drains.

After comprehensive

troubleshooting,

the licensee

concluded that

no abnormal

conditions

which would impact future turbine operation

could

be found.

The

licensee

wrote

an operability determination

which included the results

of the troubleshooting.

The licensee initiated

a weekly pump testing

program

on the

AFW pump to

monitor and detect

abnormal

pump performance.

On May 17, the inspectors

observed

one of the weekly tests

and noted

no discrepancies.

Conclusions

N3

The licensee

performed extensive troubleshooting efforts to determine

the root cause of the initial overspeed trip of the

AFW pump.

The

licensee

appropriately

performed additional tests of the

AFW pump.

Based

on the troubleshooting

and additional tests,

the inspector

concluded that the licensee's

operability determination

was reasonable.

Maintenance

Procedures

and Documentation

M3.1

Emer enc

TS Chan

e

a

~

Ins ection

Sco

e

61726

The inspectors

reviewed the licensee's

entry into TS 4.0.3

and their

emergency

request for a TS change

concerning trisodium phosphate

maintained

in containment.

I

-14-

Observations

and Findin

s

On Hay 14, the licensee

entered

TS 4,0.3 after determining that part of

TS Surveillance

Requirement 4.5.2.d.2,

to verify every

18 months that

a

minimum of 464 cubic feet of trisodium phosphate

was located in

containment,

had not been

performed in the three units.

During

a review

of the TS, the licensee

found that the form of trisodium phosphate

located in containment

was anhydrous rather than dodecahydrate,

as

specified

by the TS.

On Hay 15, the licensee

submitted

an emergency

request to change

the

TS to specify that anhydrous

trisodium phosphate

was to be verified in containment.

The emergency

request

was approved,

and the 'licensee

exited

TS 4.0.3.

The inspectors

discussed

this event with chemistry

and nuclear licensing

personnel

and reviewed original design calculations,

purchase

orders,

and the original

TS

~

The licensee

was designed for anhydrous

trisodium

phosphate

to condition water in the containment

sump following a loss of

coolant accident.

However, the original

TS was approved indicating that

the dodecahydrate

form of trisodium phosphate

would be used.

Surveillance

Requirement 4.5.2.d.3 tested

the ability of a specific

amount of trisodium phosphate

to condition water from the refueling

water storage

tank.

The inspectors

questioned

chemistry personnel

about

the requirement

and whether the amounts specified

by the test were based

on the anhydrous

or dodecahydrate

form of trisodium phosphate.

The

chemistry department

subsequently

determined that the amounts specified

were based

on the dodecahydrate

form of trisodium phosphate.

On Hay 20,

the licensee

performed

a determination

using

some of the original

trisodium phosphate

design calculations to confirm that operability was

maintained.

The inspectors

observed that Section

6. 1. 1.2 of the Palo Verde

UFSAR

indicated that trisodium phosphate

dodecahydrate

would be used in

containment.

Section

6. 1. 1.2 indicated that the chemical

would be

tested,

but the test parameter for water temperature

differed from the

water temperature listed in Surveillance

Requirement 4.5.2.d.3.

The licensee

developed

an action plan to address this issue.

The

inspectors

reviewed the plan

and found that the licensee

intended to

develop

a new test to verify the ability of anhydrous

trisodium

phosphate

to condition water from the refueling water tank.

The

licensee

intended to revise Surveillance

Requirement 4.5.2.d.3

based

on

the

new test.

The licensee

also intended to investigate

and correct the

inconsistencies

between

the surveillance

requirements

and the

UFSAR.

While the licensee

maintained the design basis,

the Surveillance

Requirement 4.5.2.d.2 to verify the type of trisodium phosphate

located

in containment

was not met.

This licensee-identified

and corrected

violation is being treated

as

a noncited violation, consistent

with

Section VII.B.I of the

NRC Enforcement Polic

(50-528;529;530/96007-02).

-15-

Resolution of the

UFSAR inconsistency will be reviewed in

a future

inspection (IFI 50-528;529;530/96007-03),

Conclusions

One noncited violation, regarding the failure to meet the

TS

Surveillance

Requirement 4.5.2.d.2,

was identified.

The licensee's

effort to find the discrepancy for the type of trisodium

phosphate

used

in containment

and to obtain

an emergency

TS change

was

very good.

However,

the licensee

missed

an opportunity identify another

problem with a related surveillance

requirement during review and

submittal of the emergency

request.

The licensee's

action plan to

resolve this entire issue

was appropriate.

Naintenance Staff Knowledge

and Performance

Containment Ventilation Pur

e Isolation Valve Leak Rate Test

Unit 3

Ins ection

Sco

e

61726

On Hay 7, the inspectors

observed

performance of Procedure

73ST-9CL10,

"Containment Ventilation Purge Isolation Valves (42")

Penetration

57."

Observations

and Findin

s

The inspectors

noted that the objective of the test

was to verify that

the leakage rate of the containment

purge isolation valves

was within

the limits specified in TS.

The test accomplished

the objective

by

pressurizing

the volume between

the two valves (inside

and outside of

containment

purge isolation valves)

by applying air to the drain/test

valve located

between

them.

The technician

was unable to properly pressurize

the volume between

the

valves.

The licensee

stopped

the surveillance test

and entered

the

appropriate

action statements.

The licensee

determined that the valve

outside containment

was not seated

properly.

Following maintenance

on

the valve, the technician

reperformed

the test satisfactorily.

The inspectors

noted several

discrepancies

during the performance of the

initial surveillance test.

The local leak rate test

(LLRT) technician

failed to perform the procedure

in sequential

order.

The technician

performed

Step 8.7 prior to performing Steps

8.5

and 8.6.

Step 8.7

opens the drain/test valve;

Steps

8.5 and 8.6 attach test fittings and

connect

an air supply, respectively.

Although the failure to perform

the procedure

in sequential

order did not have

an impact

on the outcome

of the test,

the action did not meet management's

expectation.

During the performance of the test,

the inspectors

observed

two propped

open

HVAC doors,

A347 and A348, through which

a rubber service air hose

-16-

protruded.

The doors were labeled with direction to contact fire

protection prior to propping open.

The technicians

indicated that they

had not contacted fire protection or any other organization prior to

propping

open the doors.

The doors

were listed

as

HVAC barrier doors in

Procedure

40AC-90P17,

"Control of Security,

Fire and

HVAC Barrier Doors,

Hatches

and Floor Plugs."

The procedure

indicated that fire protection

was to be contacted prior to propping

open doors to ensure that

appropriate

compensatory

measures

were implemented.

The inspectors

contacted fire protection,

and they determined that

no compensatory

measures

would have

been required for the propped

open doors.

The

failure to contact fire protection prior to propping

open the doors

constitutes

a violation of minor significance

and is being treated

as

a

noncited violation, consistent with Section

IV of the

NRC Enforcement

~Pol ic

(50-530/96007-04)

.

The inspectors

discussed

the performance of the test with the licensee.

The licensee initiated

a

CRDR to evaluate

the event.

Maintenance

supervision

discussed

the issues of concern with all the

LLRT

technicians

and reinforced management's

expectations.

Conclusions

The inspectors

identified that licensee

personnel

failed to follow

procedures

and instructions

when propping

open

two labeled

HVAC barrier

doors.

Management's

response

to the problem was prompt

and thorough.

Miscellaneous

Maintenance

Issues

(90712)

Closed

LER 50-528 94001-01:

Surveillance

Requirement 4.8.4. 1 not

fully met,

The licensee

determined that they did always

comply with the

TS surveillance

requirement to test "at least

10 percent" of the circuit

breakers

each

18 months.

Due to rounding,

the licensee

sometimes

tested

less

than

10 percent of the breakers;

however, their program would have

ensured

100 percent testing over

10 years.

As corrective action,

the licensee

tested

other circuit breakers

to

ensure that the "at least

10 percent"

requirement

was met.

The licensee

also

changed

preventive maintenance

tasks to ensure that the sample size

would meet the requirement,

The inspectors

reviewed

CRDR 9-3-0569 which included the licensee's

investigation of this event.

The inspectors

found the licensee's

investigation to be thorough

and their corrective actions to be

appropriate.

The inspectors

also reviewed

a sample of the preventive

maintenance

tasks

and found that the test

sample size met the

10 percent

requirement.

This failure constitutes

a licensee-identified

and

corrected violation of minor significance

and is being treated

as

a

roncited violation, consistent

with Section

IV of the

NRC Enforcement

~Polic

(50-526/96007-05).

I

-17-

M8.2

Closed

LER 50-528 95016:

TS violation due to unrecognized

containment

spray valve failure.

The Train

B mini-recirculation motor-operated

valve failed when

a motor set

screw

was tightened,

binding the motor.

The licensee

found that the motor's stator

had previously

been

replaced

and

had

been

machined to allow proper fit into the motor housing.

The

licensee

determined that enough material

had

been

removed to affect the

ability of the set

screw to hold the motor in place.

The licensee

determined that the valve had

been

inoperable for greater

than

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />,

in violation of TS 3.6.2,1.

H8.3

The licensee

corrected

the problem

by adding

a shim around the stator,

and the valve operator

was reoriented to improve performance.

The

licensee

also inspected

other similar valves

and verified those to be

operable.

The inspectors

reviewed

CRDR 1-5-0231,

which included the licensee's

investigation of this event.

The inspectors

found the licensee's

investigation to be thorough

and their corrective actions to be

appropriate.

This licensee-identified

and corrected violation is being

treated

as

a noncited violation, consistent

with Section VII.B.1 of the

NRC Enforcement Polic

(50-528/96007-06).

Closed

LER 50-529 95004:

TS violation due to missed surveillance

requirement.

On two occasions,

two inoperable

containment penetration

circuit breakers

were not verified to be open every

7 days

as required

by TS 3.8.4. 1, Action a.

The licensee

subsequently

identified that the

breakers

had remained

open

and were under clearance

control.

The

licensee's

corrective actions

included the use of a controlled procedure

for subsequent

verifications of breaker positions

and

a review of the

procedure after completion of the task.

The inspectors

reviewed

CRDR 2-5-0250,

which included the licensee's

investigation of this event.

The inspectors

found the licensee's

investigation to be thorough

and their corrective actions to be

appropriate.

This failure constitutes

a licensee-identified

and

corrected violation of minor significance

and is being treated

as

a

noncited violation, consistent with 'Section

IV of the

NRC Enforcement

~Polic

(50-529/95007-07).

III. En ineerin

El

Conduct of Engineering

El. 1

Reactor Startu

Unit 2

a

~

Ins ection

Sco

e

37551

On Hay 1, the inspectors

observed

the Unit 2 reactor startup in

accordance

with Procedure

400P-9ZZ03,

Reactor Startup,

and evaluated

engineering's

response

to identified reactivity anomalies.

4

0

-18-

Observations

and Findin

s

During the reactor startup,

the inspectors

observed

the reactor engineer

and shift technical

advisor correctly enter the information into the

computer to perform the I/m plot.

Two consecutive

anticipated critical

positions projected that the reactor would achieve criticality 500

pcm

below the estimated critical position.

In accordance

with licensee

administrative

procedures,

operators

inserted

the regulating

group

control element

assemblies,

and engineering

and management

evaluated

the

condition.

The licensee initiated

a

CRDR to evaluate

the problem.

Reactor

engineering

reviewed previous reactor startups

and noted similar

characteristics

during previous startups.

The licensee

determined that

the estimated critical position was accurate.

The licensee

determined

that it was appropriate

to perform another startup.

Operators

performed the second startup

and did not receive

two

successive

anticipated critical positions within 500

pcm below the

estimated critical position.

However,

as operators

performed the second

approach

to criticality, engineering

determined that with the next pull

of the

CEAs the reactor would become critical at

a 'point 500

pcm below

the estimated critical position.

The licensee

again performed

a reactor

shutdown.

The licensee

evaluated

the condition

and noted that this was the first

startup that included

an

11 parts

per million boron adjustment for the

use of guardian grid fuel.

Approximately two-thirds of the fuel

assemblies

in Unit 2 were manufactured

with the guardian grid.

The

licensee initially inserted

the ll parts per million adjustment to

increase

the accuracy of the low power physics test predictions

based

on

the results of the recent Unit 3 refueling startup.

The licensee

removed the guarding grid bias from their "simulate" model prediction,

which lowered the estimated critical position,

and successfully

performed the reactor startup.

The inspectors

noted that the 500

pcm limit was

a licensee

administrative requirement

based

on the

TS requirement that the overall

core reactivity balance

shall

be compared to the estimated

values

and

agree within 1000

pcm.

The licensee

planned to continue to evaluate

the

reactivity discrepancies.

Conclusions

Following the second

startup attempt,

engineering

research

into the

startup

anomalies

was thorough

and

had appropriate

management

review.

~.

t

j

-19-

E2

E2.1

The licensee

decisions

to shut

down when administrative limits were

approached

was conservative.

Engineering

Support of Facilities

and Equipment

Review of Class

IE Batter

Test Results

Unit 2

b.

Ins ection

Sco

e

92903

The inspectors

reviewed the test data from the Class

lE battery testing

performed during the recent

outage,

inspected

the batteries,

reviewed

licensee corrective actions,

reviewed licensee operability evaluations,

and discussed

preliminary root causes

for the degradation

of the

ATILT

round cell batteries with licensee

personnel.

Observations

and Findin s

During the recent

outage,

the licensee

performed battery performance

discharge

(capacity) testing of the Class

lE batteries.

The licensee

noted that the capacity of the batteries

was below expectations.

Surveillance

Requirement 4.8.2. l.e requires that

AT&T batteries

demonstrate

90 percent or greater capacity

when subject to

a performance

discharge test.

Surveillance

Requirement 4.8.2.1.f requires that

ATILT

batteries

be tested

annually if their capacity drops

below 95 percent

or

more than

5 percent

since the previous test.

Battery

A tested

at

107 percent,

a reduction of 7 percent

since the

previous test.

Battery

C tested

at 88 percent,

a reduction of

20 percent

since the previous test.

Test equipment failed during

testing of Battery

D.

The licensee

had previously picked the "best" individual cells from

several different lots of cells.

Therefore,

the batteries

contained

cells manufactured

at different times with different testing histories.

The licensee

determined that the recent Unit 2 battery degradation

was

lot related.

For example,

Battery

C contained cells from lots HG-l,

HG-14,

HG-16,

and

HG-18.

For battery

C, the capacitances

of the lots

were:

HG-1,

114 percent;

HG-14,

91 percent;

HG-16,

105 percent;

and

HG-18,

82 percent.

The lots experienced

similar results

in Battery A.

In order to comply with the

TS surveillance,

the licensee

reconfigured

the cells in all four batteries.

Battery

A currently contains

HG-1 cells,

Battery, B contains

new cells from the manufacturer,

Battery

C contains

HG-16 cells,

and Battery

D contains

new cells

received

from another utility.

The licensee's

preliminary root cause

investigation identified positive

plate destruction

on the

HG-18 cells.

In addition, the licensee

determined that the vendor

had increased

the

amount of platinum in the

l

!

-20-

negative plate of cells produced after mid 1994.

The vendor

added

additional

platinum to the negative plate to improve the float behavior

of the cells.

The platinum decreased

the charging efficiency of the

negative plates to more closely match the charging efficiency of the

positive plates.

Subsequent

testing of batteries

in all three units

showed corresponding

lower negative half-cell voltage readings

in the

Unit

2 batteries,

when compared

to the readings

from the Units

1

and

3

batteries,

which contained

the lower amount of platinum.

The licensee

planned to evaluate

the effect the increase

in platinum in

the negative plate

may have

on the long term capacity of the Unit 2

batteries.

In addition,

the licensee

planned to continue to monitor the

positive

and negative plate performance of the Unit 2 batteries

by

taking half-cell voltage readings.

The licensee

informed the

NRC of

potential generic

issues

concerning

AT&T round cell batteries

through

several

meetings

and conference calls.

Conclusion

The Unit 2 reconfigured

Class

1E batteries

were operable

and met the

TS

requirements.

The licensee's

effort to understand

the root cause of

AT&T round cell battery degradation,

in order to better predict future

cell performance,

and the technical

actions

in response

to the Unit 2

battery test results

were excellent.

Solenoid Valve 0 erator

De raded

Internal Wirin

Ins ection

Sco

e

92903

Inspection

Report 50-528;529;530/95025,

Section

7, discussed

resolution

of a problem with overheating of certain solenoid valves inside

containment.

Subsequent

to this report,

the licensee identified similar

problems with pressurizer

steam

space

sample line containment isolation

Valve SS-UV-205 in Unit 2 which indicated that the original root cause

was incorrect.

The inspectors

reviewed the problem with Valve SS-UV-205

and discussed

corrective actions with the licensee.

Observation

and Findin

s

The licensee

had determined that certain solenoid valves

had heat

damaged

wire insulation

and environmental

seals

because their electrical

circuits had failed and the solenoids

were continuously energized with

120

VAC, in lieu of the nominal

42

VAC.

The licensee

had replaced

the

heat

damaged

equipment

and repaired the electrical circuits.

Subsequently,

the licensee identified that solenoid Valve SS-UV-205 had

a heat

damaged

environmental

seal.

Electrical

checks

indicated that the

valve

had not been subjected

to

an over-voltage condition.

Based

on

this

new information and the temperature

measurements

on the external

surface of a similar valve, the licensee

determined that the

E

-21-

c

~

environmental qualification life of several

of the valve's internal

components

may

be nonconservative.

Because

the licensee

had recently

inspected

and repaired

Valve SS-UV-205 in Units

2 and 3, the licensee

concluded

these

valves

were operable.

The licensee

deenergized

and

tagged

Valve SS-UV-205 in Unit

1 in the required safety position.

The

inspectors verified that the Unit

1 valve was deenergized

and tagged.

This type of solenoid valve

and environmental

seal

were used in other

systems within containment,

but with lower process fluid temperatures.

The licensee

noted that inspection of these

valves indicated

no heating

problems.

The licensee

indicated that they have not experienced

failures of this type valve, only degradation

of environmental

seals

and

internal wiring.

The licensee

planned to perform laboratory testing of this type of valve

to determine

the expected

internal

temperatures

and adjust environmental

qualification life as required.

The licensee further planned to modify

the valves to lower the temperature

at the environmental

seal

area

and

remove the internal wiring with the lowest temperature

rating,

The

licensee

planned to complete these

actions

in Unit

1 to support the next

outage.

Conclusion

E2.3

The licensee's

operability determination

was acceptable,

pending the

testing results,

The licensee's

original root cause

determination

was

incorrect,

although it was reasonable

based

on information available at

the time.

The licensee's

planned corrective actions to address

the long

term environmental qualification of these

valves

appear

appropriate,

Review of Facilit

and

E ui ment Conformance to UFSAR Oescri tion

A recent discovery of a licensee

operating its facility in

a manner

contrary to the

UFSAR description highlighted the need for a special

focused

review that compares

plant practices,

procedures

and/or

parameters

to the

UFSAR description.

While performing the inspections

discussed

in this report,

the inspectors

reviewed the applicable

sections of the

UFSAR that related to the inspection

areas

inspected.

The following inconsistency

was noted

between

the wording of the

UFSAR

and the plant practices,

procedures

and/or parameters

observed

by the

inspectors.

As noted in Section

M3. 1, the inspectors

identified

a difference

was

identified between

the criteria for trisodium phosphate

contain in the

TSs

and

UFSAR section

6. 1. 1.2.

As noted in Section

E3. 1 the inspectors

identified several

differences

between

licensee

procedures,

the Combustion

Engineering

Standard

Safety

Analysis Report,

and

UFSAR Section

9. 1.3.3 concerning

the

SFP.

These

differences

were:

-22-

~

Cooling lineup prescribed

to cool

SFP,

when shutdown cooling is

not needed.

~

Description of water depth

above fuel assemblies.

~

Primary source of cooling water to the heat exchangers,

primary

heat sink,

and primary makeup source.

E3

Engineering

Procedures

and Documentation

E3. 1

S ent Fuel

Pool Current Licensin

Basis

a.

Ins ection

Sco

e

Representatives

of the NRC's Office of Nuclear Reactor Regulation

reviewed

UFSAR Section

9. 1.3,

"Spent

Fuel

Pool Cooling and Cleanup

System,"

and the licensee's

operation of the system in accordance

with

the

UFSAR descriptions.

b.

Observations

and Findin

s

UFSAR Section

9. 1.3.3. 1. 1 states

that one train each of the shutdown

cooling system

and the fuel pool cooling system will be in use in the

event of a full core offload.

Under these conditions,

(a core offload

90 days after startup

from previous refueling

and the pool containing

fuel from 12 previous refuelings)

the

maximum pool temperature will be

limited to less

than 125.2'F.

The inspectors

noted that

UFSAR

Table 9. 1-2 lists the maximum fuel pool temperature

as

145.5

F, with a

footnote stipulating that this was the design

heat load (one-third core

offload) with one fuel pool cooling train out of service.

The

information in this table did not show that

a calculation for a full

core offload with one train of spent fuel pool

(SFP) cooling had

been

performed

and will maintain

maximum fuel pool temperature

less

than

145.5'F.

The inspectors verified that the information in UFSAR

Section

9. 1.3.3. 1. 1 shows with a maximum heat load (full core offload),

and

a fuel pool cooling train augmented

by a shutdown cooling train, the

licensee

has

a calculation

on record indicating that pool temperature

remained

less

than 125.2'F.

The licensee

noted that the

SFP cooling pumps were not in the inservice

testing

program because

the

pumps

do not fall under the American Society

Of Mechanical

Engineering

(ASME) Section

XI applicability,

as described

in

a letter to the staff on December

12,

1984.

The letter explained

that there

was substantial

assurance

that these

pumps were ready to

operate

on demand

since they were normally running.

In a recent review

of the in-service testing

program,

the licensee identified the

need to

routinely monitor the performance of the fuel pool cooling system

and

issued

a

CRDR to evaluate

the concern.

-23-

Procedure

410P-1PC01,

"Fuel

Pool Cooling," provided lineups for the

SFP

cooling trains.

Section 3.0 of the procedure

states

that

a single

pump

and two heat

exchangers

should

be attempted

to maintain fuel pool

temperature

less

than 145'F prior to initiating shutdown cooling.

The

UFSAR states

that this lineup should

be used to maintain temperature

less

than 125'F,

and that two pump two heat

exchanger

operations

should

be employed

above

125'F.

The licensee

planned to address

the

discrepancy

between

the

UFSAR and procedures.

The inspectors verified

that Section 4.3.5 of the Procedure

410P-1PC01

directs the operator to

augment with shutdown cooling if temperature

exceeds

145'F.

The

inspectors

also verified that the

TS requirement

to not move fuel prior

to the reactor being shutdown

100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />

had

been satisfied for the last

three refueling outages.

The inspectors

noted that

UFSAR Section

9. 1.3.3. 1.3 states

that "a

minimum of 9 feet of water is maintained

over spent fuel assemblies."

However,

TS 3.9.11 requires

23 feet over the top of the fuel assemblies

seated

in the storage

racks.

The licensee

responded

that

UFSAR 9. 1.4.6

describes

the Combustion Engineering

Standard

Safety Analysis Report

interface requirement to maintain

9 feet of water above the active

portion of a fuel assembly during fuel handling,

and

UFSAR 9. 1.4.7

describes

the ability to meet that requirement.

Further,

Combustion

Engineering

Standard

Safety Analysis Report Section

9. 1.4.3.4,

which is

referenced

in UFSAR Section 9. 1.4.3.4,

describes

travel stops in both

the refueling

and spent fuel handling machines that restrict withdrawal

of the spent fuel assemblies

to maintain the minimum 9 feet of water

over fuel being moved.

The licensee

planned to review the need to

supplement

UFSAR Section 9. 1.3.3. 1.3 to clarify that the

9 feet

requirement

was for fuel being moved,

and that there

was

a

23 foot TS

requirement

above fuel assemblies

seated

in the storage

racks.

The inspectors

noted that

UFSAR Section

9. 1.3.3. 1. 1 lists essential

cooling water prior to nuclear cooling water

as the cooling source to

the

SFP heat

exchanges.

The inspectors

noted that nuclear cooling water

should

be listed first since it is the normal

method.

The inspectors

verified that the licensee

has

a procedure for manually initiating

essential

cooling water.

The inspectors

also noted that

UFSAR

Section

9. 1.3.3. 1. 1 stated that the spray

ponds

were the

SFP cooling

ultimate heat sink.

This would only be true if the licensee

had

switched the heat

exchanger

cooling to its backup (essential

cooling

water)

source.

The inspectors

questioned

certain control

room staff regarding

normal

makeup

paths to the

SFP.

The control

room staff indicated that the

normal

makeup

method

was the liquid radwaste

system monitor tank (in

order to minimize waste).

However,

UFSAR Section

9. 1.3.3. 1.3 states

that normal

pool

makeup is from the refueling water tank.

The backup

source

is from liquid radwaste

system monitor tank or condensate

storage

tank.

Plant procedures

address

makeup

from all of the

above sources.

~

'

-24-

C.

The licensee

indicated that they would review the noted

UFSAR

discrepancies

and clarify that

a full core offload was routinely

performed.

These

changes

were not completed prior to commencement

of

the Unit 2 refueling outage that started

March

16,

1996.

Additionally,

the licensee

planned to review the

UFSAR sections

pertaining to the

SFP

to further verify the consistency

between

actual plant operation

and

UFSAR descriptions.

Resolution of the

UFSAR inconsistency will be

reviewed in

a future inspection (IFI 50-528;529;530/96007-03)

Conclusion

E8

E8.1

Since the plant has

two independent

SFP trains

(each

capable of being

augmented

by

a shutdown cooling train),

and

has stored less

than half of

the maximum design

number of spent fuel assemblies,

the licensee

demonstrated

that

a full core offload of fuel assemblies

(the normal

practice)

was acceptable.

Miscellaneous

Engineering

Issues

(92903)

Closed

LER 50-529 94005-01:

high pressure

safety injection motor

operated

valve failed to open during

ASHE Section

XI testing.

The valve

failure resulted

in one subsystem of the emergency

core cooling system

being inoperable.

The failed valve

(2JSIAUV0627)

was

a

2 inch rotating

stem globe valve with a Limitorque SMC-04 actuator.

The licensee

determined that the root cause of the failure of the valve

to open

was

a combination of pressure

over the seat

and excessive

stem

to disc friction.

Downstream

check valve leakage

caused

the pressure

over the seat.

The licensee

did not determine

the specific cause of the

excessive

stem to disc friction.

However, the licensee

determined that

both the pressure

over the seat

and

a high stem to disc friction had to

occur simultaneously for the failure to be repeated.

The licensee

indicated that the Limitorque SMC-04 actuator

was obsolete

and not supported

by the original manufacturer.

The licensee

indicated

that

a previously approved

design

change

was

implemented to upgrade

the

Limitorque SMC-04 actuator to

a Limitorque SMB-00 actuator.

The

inspectors

reviewed draft equipment root cause failure analysis,

CRDR 9-4-0598,

and the report,

"Generic Evaluation of the Limitorque

SMC-04 Actuator and Borg Warner

2 Inch Angle Globe Valve in HPSI

Service," Revision 0.

The report indicated that

a conservative

determination of the

SMC-04 actuator torque required to operate

the

valve was approximately

75 ft-lbs, without considering

seating

torque.

The licensee

concluded that the

SMC-04 actuator

maximum output combined

with packing load adjustment

could not accommodate

the valve torque

requirements.

Therefore,

the licensee

installed the

SMB-00 actuator

with a 250 ft-lb rating.

The inspectors

reviewed

Work Order 681034

which replaced

the

SMC-04 actuator with the

SMB-00 and noted the work

was completed

October

19,

1994.

1

-25-

In addition,

the valve

had

a rotating stem which resulted

in operating

torque loads

on the actuator

which were not taken into account

when the

original application

was determined.

The licensee

indicated that

a

modification had

been

approved to change

the valve from a rotating

stem

to

a rising stem valve which would eliminate the stem to disc friction.

The licensee

issued

a purchase

order to the valve manufacturer

to design

a new valve.

The inspectors

concluded that the licensee

had taken appropriate

short

and long term corrective actions.

Closed

Violation 50-530 94012-03:

failure to take

immediate action

required

by TS.

This violation indicated that the feeder breaker for

the Train A LPSI

pump was racked into the test position rendering the

associated

shutdown cooling loop inoperable.

In addition,

immediate

action

was not initiated to restore

the shutdown cooling loop to service

or to establish

at least

23 feet of water above the reactor pressure

vessel

flange

as required

by TS.

The licensee

stated

they had not

considered

the

pump inoperable

because

they had taken credit for manual

operator action.

The licensee

stated that they had reasonable

assurance

that the breaker could have

been

racked

back in within the 3-hour time

period required to initiate shutdown cooling.

The licensee's

corrective actions

included surveying nuclear utilities

to determine

how other utilities view manual

operator actions for the

LPSI pump.

The licensee

concluded that the majority of the utilities

would have considered

the

pump inoperable.

The inspectors

reviewed

Procedure

40DP-90P26,

"Operability Determination," Revision 3,

Appendix

C.

The licensee

had revised this procedure to include guidance

for use of manual

actions to maintain operability.

Appendix

C of this

procedure listed the actions which had to be performed in order to take

credit for manual

operation.

It also included evaluations

of the

qualifications

and ability of the personnel

performing actions,

the

number of qualified personnel

needed,

the time needed

to accomplish

the

actions,

the communications

necessary,

and the criteria of 10 CFR 50.59.

The inspectors

reviewed

CRDR 3-4-0340,

dated July 15,

1994,

which was

prepared

to evaluate

the licensee's

position

on appropriate

manual

actions to support continued operability.

The licensee

developed

a

position paper

and distributed it to operators

in the three units.

The

position paper which contained

the minimum requirements

to credit manual

operator actions

in maintaining operability was

an expanded

version of

the Appendix

C operability determination

procedure.

The inspectors

concluded that the licensee's

corrective actions

were appropriate.

l'

IV.

Plant

Su

ort

Rl

R1.1

Radiological

Protection

and Chemistry Controls

Chemistr

Sam lin

Durin

Hidloo

Unit

1

a

~

Ins ection

Sco

e

71750

b.

On April 22, with Unit

1 in midloop operations,

the midloop reactor

operator

noted

an unexpected

level decrease

in the volume control tank.

Subsequently,

the licensee

determined that chemistry personnel

had

begun

a purging operation

associated

with reactor

coolant sampling without

required notification to the control

room.

The inspectors

reviewed the

licensee's

response

to the event, corrective actions,

and discussed

the

event with chemistry personnel.

Observations

and Findin

s

At approximately II a.m.,

on April 22, the senior chemistry technician

and

a chemistry technician discussed

performing the required shiftly

reactor coolant

system

sample in accordance

with Procedure

740P-9SS01,

"Primary Sampling Instruction."

The chemistry technician initiated the

purging process

by opening

a sample valve with an understanding

that the

senior chemistry technician

would actually draw the sample.

The

technician left the area.

The inspectors

noted that the purging process

takes

approximately

15 minutes at

a flow rate 0.5 to I gallon per

minute.

The senior chemistry technician believed the chemistry

technician

was doing the entire sample.

Neither technician notified the

control

room.

Procedure

740P-9SSOl,

Step 4.3.4 requires notification of

the control

room prior to sampling.

At approximately

12:30 p,m., the midloop reactor operator detected

a

slight loss in volume control tank level.

A control

room operator

contacted

chemistry

and discovered that the

sample

purge

had

been

initiated

and

was still in progress.

The reactor operator

estimated

that the volume control tank decreased

by approximately

1.5 percent or

approximately

60 gallons.

The licensee

discussed

the event in the control

room with operations,

chemistry personnel,

and the site shift manager.

Chemistry determined

that the flow rate

was approximately 0.75 gallons per minute

and that

the total loss of inventory from the volume control tank was

approximately

80 gallons.

The licensee initiated

a

CRDR and notified

chemistry management.

The site shift manager did not contact the

operations

department

leader or the operations director during the

shift.

The licensee notified the

NRC approximately

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after the

event.

The licensee

determined that the root cause of the event

was the failure

to follow procedure

by the chemistry technician in that the technician

-27-

C.

did not notify the control

room prior to sampling,

In addition,

communications

and notifications to licensee

management

and the

NRC did

not meet management's

expectations.

The inspectors

concluded that the licensee's

corrective actions

were

appropriate.

Additionally, the inspectors

noted that the event

was

identified by the licensee

and that there

were

no similar violations

identified by either the inspectors

or by the licensee

which could have

reasonably

prevented this occurrence.

This licensee-identified

and

corrected violation, failure to notify the control

room prior to

sampling,

is being treated

as

a noncited violation, consistent with

Section VII.B.I of the

NRC Enforcement Polic

(50-528/96007-08).

Conclusions

R2

R2,1

Chemistry personnel

did not follow procedures

for notifying the control

room prior to sampling, resulting in a noncited violation.

In addition,

chemistry personnel

failed to adequately

communicate,

resulting in an

unattended

open

sample valve

and subsequent

loss of inventory during

midloop operations.

The inventory lost was not significant.

The licensee's

investigation into the event

was thorough.

The

notifications to operations

management

were slow, in that the event

was

not discussed

until the following day.

Status of Radiological

Protection

b. Chemistry Facilities

and Equipment

Containment

Closure

Walkdown

Unit 2

a

~

Ins ection

Sco

e

71750

b.

On April 30, the inspectors,

accompanied

by a radiation protection

(RP)

technician

and the containment coordinator,

toured the containment to

assess

the state of housekeeping

and material condition prior to the

unit startup.

Observations

and Findin

s

The containment cleanliness

and material condition was generally good.

The inspectors

observed

minor debris,

such

as tie wraps,

in the reactor

coolant

pump areas.

The

RP technician

immediately retrieved the debris.

The containment coordinator indicated that the

pump bay areas

would be

recleaned

to ensure all small material

was removed.

There were minor

material discrepancies

with the few remaining jobs in containment.

The

containment coordinator indicated that additional

walkdowns would be

performed to verify containment cleanliness

as the work was completed.

I

I

~ g

~

4

-28-

R2.2

Material Condition of the

RCAs

Units

1

2

and

3

a.

Ins ection

Sco

e

71750

The inspectors

made tours of the radiologically controlled areas

(RCA's)

in each of the units.

Additionally, on Hay 9, the inspectors

and

a

NRC

manager

toured the RCA's for all three units.

b.

Observations

and Findin

s

On May 9, the inspectors

identified two Unit 2 leaks which were not

posted

as contaminated

areas.

For both leaks,

the previously

unidentified contamination levels were greater

than the licensee's

criteria for posted

contamination

areas

(greater

than

1000

disintegrations

per minute per

100 square

centimeters

(dpm/100cm').

~

Valve SIA-UV-655 had

a packing leak.

RP determined that the floor

under the valve had smearable

contamination of 15,000

dpm/100cm'.

RP subsequently

posted

the area

as

a "contaminated

area."

The

inspector determined that the packing for this valve had

been

worked during the refueling outage.

Maintenance

and

RP had

performed

walkdowns of the area

on May

1 and Hay 6, respectively,

and

had not identified leakage

or any contamination.

~

The pipe cap

down stream of valve SIB-V555 appeared

to be leaking,

with boron crystals

apparent

on both the pipe cap

and the floor;

RP subsequently

determined that smearable

contamination

was 30,000

dpm/100cm'n

the pipe cap

and 70,000 dpm/100cm'n

the floor.

RP

decontaminated

the valve and cleaned

up the area.

The inspector

determined that SIB-V555 had

been previously identified by the

utility maintenance

group

as having

a packing leak.

Maintenance

and

RP had performed

walkdowns of this area

on Hay

1

and

May 3,

respectively,

and

had not identified leakage or any contamination.

During the

May 9 tours,

the inspectors

also observed that Unit

1 valve

SIA-UV-655 had

a packing leak.

The bonnet

was posted

as

a "High

Contaminated

Area,"

and there

was

a drip catch installed underneath

the

valve bonnet

area to contain the leak.

The inspector

observed that

a

stalactite of boron crystals

had formed outside the drip catch.

On Hay 10, the

NRC manager

discussed

the general

conditions of the

RCAs

with licensee

management.

Licensee

management

subsequently

directed

RP

and utility maintenance

personnel

to perform walkdowns of the

RCA's in

all three units.

As

a result of the walkdowns,

the licensee identified

numerous

valves

and

pumps that needed repair and/or decontamination.

Licensee

management

classified

these material condition issues

as

a

RP

Management

Level

1 issue,

establishing

a high priority for resolution

and increased

management

awareness.

In addition,

the licensee initiated

CRDR 9-6-0557 to investigate

the discrepancies.

-29-

On May 14 and

15,

a

NAP inspector

performed radiological

walkdowns in

all three units

and documented

the results

in Evaluation Report 98-0303.

The

NAP inspector identified two contaminated

leaking valves in Unit

2

and one in Unit I which had not been properly posted.

The

NAP inspector

did not identify Unit

1 valve SIA-UV-655 as having improper posting.

On May 16, the inspectors

toured the Unit

1

RCA and observed that the

stalactite

formation outside the drip catch of valve SIA-UV-655 had

allowed liquid to drip onto the floor, forming

a puddle.

This area

had

not been

posted

as

a contaminated

area.

The inspector contacted

RP,

and

a technician

determined that the contamination

levels

on the floor were

up to 40,000

dpm/100cm'.

The utility maintenance

technicians

decontaminated

the area

and extended

the drip catch under the valve.

On May 21, the inspectors

discussed

the Unit

1 valve SIA-UV-655

observations

with the

NAP inspector.

On May 22, the

NAP inspector

observed

a puddle

on the floor under the valve in an area that was not

posted.

The

NAP inspector

found 150,000 dpm/100cm'mearable

contamination

on the floor, which met the criteria for a "high

contamination area."

The

NAP inspector notified RP,

who posted

the

floor as

a "high contamination

area."

The inspectors

held discussions

with RP management

and reviewed the

licensee's

program for identifying leaking components

and controlling

contaminated

areas.

The inspectors identified the following:

RP technicians

were required

by procedures

to perform monthly and

weekly surveys of the

RCA.

The surveys for the SIA-UV-655 valves

were performed monthly,

and the survey for the SIB-V555 was

performed weekly.

The most recent

surveys

had

been

performed

within a week of the

May 9

NRC walkdown.

The surveys did not

identify the valves or the areas

under the valves

as contaminated.

The

RP program included both shiftly tours

by

RP and area

ownership for technicians.

RP management

stated their

expectations

are that technicians

should

be performing both spot-

checks

and detailed tours of their area.

The licensee

had established

a Zone Inspection

Program

(ZIP) to

provide additional controls

and responsibilities for utility,

mechanical

maintenance,

and operation

departments

for identifying

and tracking leaking components,

The program

had established

a

monthly wal kdown of each unit.

However,

the program

was

disco'ntinued

in Unit 2 during the outage,

and

RP was given the

responsibility for contamination control.

The licensee

had previously recognized that the packing for the

SIA-UV-655 valves were unevenly loaded,

contributing to packing

leakage.

Although the packing

on the Unit 2 valve

had recently

-30-

been adjusted, it appeared

that the licensee

had

removed

an

installed drip catch without verifying the success

of the

adjustment.

Unit

1 valve SIA-UV-655 had

an open work request,

initiated in January

1994, to address

packing leakage.

~

In February

1996,

NAP documented

concerns

in Evaluation Report 96-

0089, that contaminated

areas/components

were not being identified

during

RP tours

and surveys.

NAP had concluded that

communications

between

RP, maintenance,

and operations

personnel

were inadequate.

In addition,

NAP found that documentation

and

resolution of problems varied

among

RP crews,

and that ZIP records

did not reflect the condition of leaking valves identified by

RP

and

NAP.

During walkdowns in March

and April 1996,

NAP noted

improvements

in contamination control.

The inspector determined that the licensee

had established

programs to

address

leakage

in the

RCA to prevent the spread of contamination.

Additionally, prior to this inspection,

the licensee

had recognized

weaknesses

in the implementation of these

programs

and

had

implemented

corrective actions.

However, the valves with leakage

were in accessible

areas

of the

RCA, there

was sufficient prior knowledge of deficiencies,

and the leakage

was significantly developed

to be clearly visible.

The

inspector

concluded it was reasonable

to expect that the licensee

identify the contaminated

areas prior to the

NRC tours.

Procedure

75RP-ORPOl required that areas

identified as having

contamination levels greater

than

1000 dpm/100cm'e

posted with

radiation warning sign(s)

bearing the words:

"Caution,

Contaminated

Area."

The inspector

concluded that the three

examples of unposted

contaminated

areas

represented

a violation (528,529/96007-09).

c.

Conclusions

One violation was identified for failure to follow procedure.

The

inspector

concluded that the three

examples of improper posting

and

inadequate

contamination control reflected

poor performance of the

licensee's

program for the control of contaminated

areas

in that routine

tours

by RP, maintenance,

and operations

personnel

had not been

effective in identifying leaking components

which had inadequate

contamination controls,

P8

Miscellaneous

Emergency

Preparedness

Issues

(92904)

PS. 1

Closed

Violation 529 94019-01:

failure to classify unusual

event.

On

May 3,

1994,

the licensee telephonically notified the

NRC Headquarters

Operations Officer that

an unusual

event

had occur'red at the site at

2:45 p.m.,

on March 12,

1994.

The licensee

indicated

an Unusual

Event

should

have

been declared at the time of the event

due to the manual

start of a third charging

pump to recover pressurizer

level while

I

~

s

~

h

-31-

drawing the bubble

(NRC Event 26773).

The event

was reviewed

by the

resident

inspectors

(NRC Inspection

Report 50-528;529;530/94009).

The licensee

indicated at

a May 25,

1994,

meeting with NRC inspectors

that three corrective actions

had

been identified and initiated.

~

The Director of Operations

prepared

a letter for all shift

supervisors

discussing

the failure to consider

and classify

an

event.

The letter reviewed the event

and emphasized

the failure

at the time of the event to "evaluate this incident with emergency

action levels in mind" and indicated that "a classification at the

Notification of Unusual

Event level would have

been appropriate."

~

Training in the nuclear

management

and resources

council

emergency

action level

scheme for the site

was prepared for immediate

training of emergency

response

personnel

and for immediate

implementation

upon approval

by the

NRC.

The licensee

nuclear

management

and resources

council

emergency

action levels were

subsequently

found acceptable

by the

NRC and the appropriate

training was conducted.

~

The Manager,

Operations

Training, indicated at the exit interview

that training "Lessons

Learned" regarding this and similar events

had

been

added to the Operations

Training program.

The inspectors

determined

during the Nay 1994 emergency

preparedness

inspection that appropriate corrective actions

had

been

implemented to

preclude

recurrence

of this type event.

Two subsequent

emergency

preparedness

inspections

at the site,

the

1995 annual

emergency

exercise

(Inspection

Report 50-528;529;530/95004)

and

a routine emergency

preparedness

inspection

(NRC Inspection

Report 50-528;529;530/95022)

observed

demonstrations

of assessment

of plant conditions

and

classification

of- emergency

events

by the licensee.

The classification

performance

in the annual

exercise

was characterized

as

good

and in the

control

room walkthrough scenarios,

during the routine inspection

as

generally good.

No failures to appropriately classify emergency

events

have occurred

in the two years

since this event.

V. Mana ement Meetin

s

Xl

Exit Neeting

Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on April 16,

1996.

The

licensee

acknowledged

the findings presented.

The inspectors

asked

the licensee

whether

any materials

examined during the

inspection

should

be considered

proprietary.

No proprietary information was

identified.

ll

PARTIAL LIST OF

PERSONS

CONTACTED

Licensee

W. Stewart,

Executive Vice President,

Nuclear

R. Flood,

Department

Leader,

System Engineering

J.

Hesser,

Director, Nuclear Engineering

W. Ide, Director, Operations

L. Johnson,

Department

Leader,

Chemistry

A. Krainik, Department

Leader,

Nuclear Regulatory Affairs

J.

Levine, Vice President,

Nuclear Production

D. Mauldin, Director, Maintenance

J.

NcDonald, Director,

Communications

G. Overbeck,

Vice President,

Nuclear Support

H. Shea,

Director, Radiation Protection

D. Smith, Director,

Outage

E. Sterling,

Department

Leader,

Nuclear Assurance-Operations

II

IP 37551'P

61726:

IP 62703:

IP 71707:

IP 71711:

IP 71750:

IP 92712:

IP 92901:

IP 92903:

IP 92904:

~0en ed

INSPECTION

PROCEDURES

USED

Onsite Engineering

Surveillance

Observations

Maintenance

Observations

Plant Operations

Restart

From Refueling

Plant Support Activities

In-office LER Review

Followup

Operations

Followup - Engineering

Followup

Plant Support

ITEMS OPENED

CLOSED

AND DISCUSSED

50-528/96007-05

50-528/96007-06

NCV

NCV

50-529/96007-07

NCV

50-528/96007-08

NCV

50-528;529/96007-09

VIO

Cl osed

50-529/96007-01

VIO

50-528;529;530/96007-02

NCV

50-528;529;530/96007-03

IFI

50-530/96007-04

NCV

failure to adhere to procedure

requirements

failure to meet surveillance

requirement

4.5.2.d.2

review of resolution of UFSAR inconsistencies

for SFP

and testing of trisodium phosphate

failure to follow procedure for blocking open

controlled doors

surveillance, requirement 4.8.4. 1 not fully met

containment

spray technical specification

violation due to unrecognized

valve failure

technical specification violation due to missed

surveillance

requirement

failure to follow chemistry procedure

failure to maintain required contamination

controls

50-529/94007

50-528/94001-01

50-529/95004

50-529/94005-01

50-530/9412-03

50-529/9419-01

50-528/95016

LER

LER

LER

LER

VIO

VIO

momentary entry into technical specification 3.0,3

surveillance

requirement 4.8.4. 1 not fully met

technical specification violation due to missed

surveillance

high pressure

safety injection motor operated

valve failed to open during

ASME section

XI

testing

failure to take action required

by technical

specification

failure to classify unusual

event

LER

containment

spray technical

specification

violation due to unrecognized

valve failure

ia

4

l

I

l

-3-

50-530/96007-04

50-528/96007-05

50-528/96007-06

50-529/96007-07

50-528/96007-08

NCV

NCV

NCV

NCV

NCV

50-528;529;530/96007-02

NCV

failure to meet surveillance

requirement

4.5.2.d.2

failure to follow procedure for blocking open

controlled doors

surveillance

requirement 4.8.4.

1 not fully met

containment

spray technical specification

violation due to unrecognized

valve failure

technical specification violation due to missed

surveillance

requirement

failure to follow chemistry procedure

C ~

0

J

~

w

~

~ 5

e

AFW

ASME

AT&T

CEA

CRDR

HVAC

LER

LLRT

LPSI

PCM

RCA

RP

SFP

TS

UFSAR

LIST OF ACRONYMS USED

Auxiliary Feedwater

American Society of Mechanical

Engineers

American Telephone

and Telegraph

Control

Element Assembly

Condition Report/Disposition

Request

Heating Ventilation and Air Conditioning

Licensee

Event Report

Local

Leak Rate Test

Low Pressure

Safety Injection

Percent Millirho

Radiological

Control Area

Radiation Protection

Spent

Fuel

Pool

Technical Specification

Updated

Final Safety Analysis Report

~ a

I