ML17299B087
| ML17299B087 | |
| Person / Time | |
|---|---|
| Site: | Palo Verde |
| Issue date: | 02/21/1986 |
| From: | Miller L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
| To: | |
| Shared Package | |
| ML17299B086 | List: |
| References | |
| 50-529-86-02, 50-529-86-2, NUDOCS 8603130011 | |
| Download: ML17299B087 (2) | |
Text
5 8603130011 860221 PDR ADOCK 05000528 9
PDR APPENDIX A NOTICE OF VIOLATION Arizona Nuclear Power Project Post Office Box 21666 Phoenix, Arizona 85036 Docket.No. 50-529 License No. NPF-46 As a result of the inspection conducted on December 27, 1985 - February 2,
- 1986, and in accordance with NRC Enforcement Policy, 10 CFR Part 2, Appendix C, the following violation was identified:
10 CFR 50, Appendix B, Criterion XVI, Corrective Action states in part "Measures shall be established to assure that conditions adverse to quality.... are promptly identified and corrected.
In the case of significant conditions adverse to quality, the measures shall assure that the cause of the condition is determined and corrective action taken to preclude repetition.
Technical Specification 6.8.1 requires in part, that written procedures be established, implemented and maintained covering the activities referenced in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.
Paragraph 9.(e) of this guide includes general procedures for the conduct of operations in the list of typical safety related activities that should be covered by written procedures.
PVNGS procedure 36ST-9SQOl Revision 2, dated April 27, 1985, contains an instruction in paragraph 8.2.1.2 which requires the monitor under test to be bypassed prior to testing.
Contrary to the above on January 24, 1986, the containment purge radiation detection monitor RU-37 was tested while the channel was in an unbypassed mode resulting in an inadvertent actuation of the Containment Purge Isolation System and a cross trip of the Control Room Emergency Ventilation System.
The test actually called for the fuel building radiation detector monitor RU-31 to be tested.
Effective corrective actions to preclude repetition of such errors was not implemented as this represents a similar incident as those documented in NRC inspection report 529/85-44.
This is a Severity Level IV Violation (Supplement I)
Pursuant to the provisions of 10 CFR 2.201, Arizona Public Service Company is hereby required to submit to this office within thirty days of the date of this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) corrective steps which will be taken to avoid further items of noncompliance; and (3) the date when full compliance will achieved.
Consideration may be given to extending your response time for o
cause FEB 2i f986 Dated F. Miller,J.,
ief eactor Proj ec ion No.
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