ML17292B225

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Insp Rept 50-397/97-18 on 971109-1220.Violations Noted:Major Areas Inspected:Operations,Maint,Engineering,& Plant Support
ML17292B225
Person / Time
Site: Columbia 
Issue date: 01/15/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17292B221 List:
References
50-397-97-18, NUDOCS 9801220170
Download: ML17292B225 (32)


See also: IR 05000397/1997018

Text

ENCLOSU

E

U.S. NUCLEAR REGULATORYCOMMISSION

REGION IV

Docket No.:

License No.:

Report No.:

Licensee:

Facility:

Location

Dates:

Inspectors

Approved By

50-397

NPF-21'

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- 50-397/97-18

'Washington Public Power Supply System

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Washington Nuclear Project-2

Richland, Washington

.: ,'ovember 9 through December 20, 1997

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'. A. Boynton*, Seriior Resident Inspector

G. W. Johnston, Senior Project Engineer

T. O. McKemon, Senior Operator License Examiner

G. M. Good, Senior Emergency Preparedness

Inspector

H. J. Wong, Chief, Reactor Projects Branch E

Attachment:

Supplemental Information

980i220i70 '980i i5

PDR

ADQCK 05000397

8

PDR

EXEC TIVE S

MMARY

Washington Nuclear Project-2

NRC Inspection Report 50-397/97-1 8

~Oer

ions

A number of inspectoridentified deficiencies in the control of transient equipment

indicated weak implementation of the licensee's program to prevent seismic interactions

between the equipment and safety-related components.

Three examples of a violation of

plant procedures were identified (Se'ction'G1;1):-

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The licensee's material condition inspection program was not fullyimplemented to

maintain and assess

those areas of the reactor building not routinely accessed

by plant

personnel.

As a'result, a lower standard was established for these areas and equipment

and housekeeping

deficiencies were allowed to persist (Section M2.1).

The methodology utilized by the licensee for testing the control room emergency

.

charcoal filters was identified as being from a different, more recent version of the

standard specified in Technical Specifications (TS). Based, in part, upon the staffs

acceptance of the version of the standard utilized by the licensee, and the more

conservative results produced by its methodology, the noncompliance was viewed as a

minor violation (Section M8.2).

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Identified performance issues in the leakage surveillance and prevention program

regarding plant staff knowledge, program implementation, and procedural

inconsistencies,

were indicative of weak management

involvement (Section E1.1).

The licensee's use of an uncontrolled database

during its power uprate implementation

resulted in an affected design calculation for the ultimate heat sink being missed in the

, review process.

The existing revision of the calculation bounded the parameters of the

power uprate (Section E8.2).

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Weaknesses

in the licensee's program for monitoring and control of combustibles in the

plant resulted in: (1) materials accumulating in limited access areas without being

properly evaluated or tracked, and (2) reducing the value of the licensee's combustible

loading calculation as a tool in supporting plant modifications due inconsistencies

in

calculation, coupled with a relatively large backlog of modifications to the current revision

of the calculation. A violation of transient combustible material control was identified

(Section F1.1).

'-2-

The licensee's failure to test the control room facsimile machine contributed to an

inoperable piece of emergency response equipment going undetected

until it was

required to be used during an actual event. A noncited violation was identified

(Section P2.1).

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The plant began the inspection period at 100 percent power. Power was reduced to 75 percent

on December 5 to allow for exchange of deep and shallow control rods and for recovery of a

single control rod whose associated scram accumulator had been replaced.

The plant was

returned to full power on December 6 and remained at full power for the balance of the

inspection period.

01

Conduct of Operations

01.1

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During routine plant tours over the months of November and December and during tours

of limited access areas (Section M2.1), a number of equipment storage concerns were

noted. The inspector reviewed the licensee's program for controlling transient equipment

in the plant.

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The licensee's program for controlling transient or portable equipment in the plant is

described in Plant Procedure Manual (PPM) 10.2.53, "Seismic Requirements For

Scaffolding, Ladders, Man-Lifts, Tool Gang Boxes, Hoists, and Metal Storage Cabinets,"

Revision 16. PPM 10.2.53 provides specific instructions for the proper storage of the

subject items to prevent them from damaging safety-related equipment in a seismic

event.

For equipment covered under PPM 10.2.53, the following storage concerns were noted:

~

Three ladders in the reactor water cleanup (RWCU) heat exchanger room were

found extended and staged for use.

Tw'o additional ladders in the RWCU pump

room mezzanine were found extended and staged for use.

Upon subsequent

entries by licensee personnel, the ladders were properly laid down on the floor.

Based upon the specific location of the ladders, the possibility of damage to

safety-related equipment was considered to be low. Section 7.2.1 of

PPM 10.2.53 requires ladders to be stored in an assigned storage location when

no longer needed for a job.

In addition, ifa ladder does not have an assigned

storage rack, PPM 10.2.53 provides that the ladder shall be laid down on the

floor. The as-found condition of the ladders in the RWCU equipment rooms did

not conform to the requirements of PPM 10.2.53 and is the first example of a

violation of TS 5.4.1 (VIO 50-397/97018-01) for the failure to follow procedures.

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Scaffold equipment carts were found unsecured

in the Division I emergency

diesel generator room and the diesel building corridor. Specifically, the carts',

brakes were not adequately engaged to prevent the carts from rolling and

potentially impacting safety-related equipment nearby.

From discussions with the

personnel using the carts, it was determined that attempts were made to engage

the brakes; however, the brakes were ineffective. Section 7.2.2.d of PPM 10.2.53

,requires these types of carts to have at least two wheels immobilized to prevent

them from rolling during a seismic event.

The failure to adequately-secure

the

scaffold carts is the second example of a violation.of TS 5.4.1'(VIO. 50-

397/9701 8-01).. >,

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.

A large (approximately 7-foot high) storage cabinet was found on the 501 foot

elevation of the reactor building, in close proximity to safety-related equipment.

The cabinet was unsecured and had the potential, ifoverturned, to impact and

damage several instrument lines associated with the reactor recirculation system

and leakage detection system.

The cabinet had been in place for several years.

Section 7.2.2.a of PPM 10.2.53 requires cabinets of this size to be secured or

stored greater than or equal to the cabinet's full height plus 12 inches from any

safety-related equipment.

The failure to properly secure or place the storage

cabinet was identified as the third example of a violation of TS 5.4.1

(VIO 50-397/97018-01).

Several additional examples were identified by the inspector in areas which were

covered by PPM 10.2.53, but which did.not contain safety-related equipment.

Specifically, a scaffold cart and a large portable electrical load bank were found

unsecured

in the corridor outside the vital electrical switchgear rooms on the 467 foot

elevation of the radwaste building. A large gang box was also found in the storage area

adjacent to the spent fuel pool that was in close proximity to spent fuel pool cooling flow

instrumentation sensing lines. Although these conditions did not conform to the

requirements of PPM 10.2.53 and were indicative of weak licensee performance in this

area, they were not considered violations of NRC requirements.

~on I~ion.>

A number of identified deficiencies in the control of transient equipment indicated weak

implementation of the licensee's program to prevent seismic interactions between the

equipment and safety-related components.

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The inspector observed the monthly Diesel Generator

1 operability test performed in

accordance with Procedure OCP-Elec-M701, "Diesel Generator

1 Monthly Operability

Test," Revision 2.

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During performance of the monthly operability test, the inspector observed good

coordination of the test between the control room operator and the equipment operator

station at the diesel generator local control station. The reactor operator maintained

communications with the in-plant operator, exercised good three-way communications,

practiced good self-checking practices, and utilized the control room supervisor as a peer

checker to verify correct hand switch manipulations.

The control room operator started,

paralleled, and loaded the diesel generator successfully and ran the diesel generator for

the prescribed

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> duration at full load. Other technicians took the required lube oil

samples and vibration reading. Afterthe

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> period, the diesel was unloaded and

power to the 4160V bus was transferred back to normal supply.

No test anomalies were

identified during the test.

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The monthly Diesel Generator

1 operability test was run successfully.

Control room

operators demonstrated

good communications and performed good self-checking and

peer checking.

02

Operational Status of Facilities and Equipment

02.1

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The inspectors walked down accessible portions of the following safety systems:

Reactor Core Isolation Cooling

Residual Heat Removal, Trains A and B

Containment Atmosphere Control, Trains A and B

The systems were found to be in the appropriate configuration for the current plant

conditions.

Material condition of the systems was generally good with two exceptions:

Valves RCIC-V-64 and RHR-V-42Awere found with active packing leakage that had not

been previously identified. These are discussed further in Section M2.1.

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08

Miscellaneous Operations Issues (92901)

08.1

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Viol

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-: failure to adhere to procedures related to log

entries and record retention.

The inspector verified that the licensee had taken the

applicable corrective actions committed to,in a letter to the NRC dated

November 1, 1996, and Notice of Violation response letter dated October 14, 1996.

R

08.2

osed

Viola i

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1 - 3: failure to adhere to procedures for reactor startup.

This violation involved the failure to followprocedures during an approach to criticality on

July 27, 1996,, when both a shift turnover and shift.brief were conducted during the

approach to criticality.

During this inspection, the inspector verified that the applicable corrective actions

committed to by the licensee in a letter to the NRC dated November 1, 1996, had been

completed.

083

Additionally, the inspector verified other commitments, which had not yet been fully.

completed, were being tracked and scheduled for completion.

For example, the licensee

was in the process of developing an analytical tool for estimating critical position based

upon subcritical multiplication. This action was scheduled for completion by

January 1,1998.

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6 -: failure to have an appropriate procedure for

adjustable speed drive testing to preclude a nonlicensed person from operating the

reactor controls. The inspector verified that corrective actions that the licensee

committed to in Notice of Violation response letter dated December 6, 1996, and in a

letter to the NRC dated November 1, 1996 (Items 5, 18, 22, 23, and 24), had been

completed.

08.4

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inadvertent main steam isolation valve (MSIV)closure

while in cold shutdown.

The licensee determined that the root cause of the closure of the

MSIVs involved deficiencies in the governing surveillance procedure that was testing the

MSIVisolation logic to the reactor protection system.

Poor communications between the

two operating crews involved with the testing and the lack of a questioning attitude when

faced with unexpected results were also considered to be contributing factors.

In response to the event, the licensee verified that the closure signal was an artifact of

the test procedure and not required by actual plant conditions. The procedure was

subsequently revised and the testing was completed satisfactorily.'he procedure

preparation process was also revised to require verification that a procedure adequately

addresses

each plant operating condition in which the procedure may be performed.

To

address the contributing factors, operators were counseled on the expectation for a

questioning attitude when faced with unexpected plant response and to involve other

crew members when dealing with unexpected alarms.

Recognizing that the first

-'5-

operating crew involved with the testing.was aware, of the procedural deficiencies,

expectations were also reemphasized for the need to promptly correct-procedural

weaknesses.

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M1.1

Conduct of Maintenance

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The inspectors observed and/or reviewed the followingwork activities:

Drywell Pressure

Instrument (CMS-PT-8) Replacement (Work Order ¹DXG3)

OSP-ELEC-M703, High Pressure Core Spray Diesel Generator Monthly

Operability Test

Repack of Valve MS-V-20 (Work Order ¹JKR8)

Repair of High Pressure Turbine Flange Leak (Work Order ¹JKZ6)

Good coordination was noted between the disciplines for each of the work activities.

Strong engineering and health physics involvement was noted in the repack of the main

steam valve and the repair of the high pressure turbine leak. Coordination of these

activities with the reactor downpower on December 5 provided for reduced area dose

rates and a dose savings.

Personnel qualifications were verified and the appropriate TS action statement was

entered for replacement of the drywell pressure transmitter and for the repacking of

Valve MS-V-20.

M2

Nlaintenance and Material Condition of Facilities and Equipment

M2.1

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Tours were conducted of specific areas of the reactor building and turbine building that

are infrequently accessed

during power operations.

The areas included normally locked

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high radiation and/or contamination areas.

Emphasis was placed upon examining

material condition of equipment and evaluating the impact of transient equipment and

material.

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Deficiencies were identified to varying'degrees

in each of the areas inspected.

Taken

individually, a majority of the deficiencies were considered minor with minimal or

negligible impact on equipment reliability. However, several of the deficiencies were

considered to be more than minor and, taken collectively, the number of deficiencies

indicated an overall weakness

in the licensee's maintenance-and

housekeeping of these

areas.

I

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The following material condition deficiencies were identified:

Active packing leakage was identified on Valve RCIC-V-64. Valve RCIC-V-64

originally provided for steam admission to the now defunct steam condensing

mode of the residual heat removal (RHR) system.

The valve is deactivated in the

closed position and performs the safety function of containment isolation. Further

discussion of this valve and the licensee's programs for evaluating its condition

are provided in Section E1.1

Minorflange leakage (one drop per minute) was identified on the'upstream

piping

of the RWCU nonregenerative

heat exchanger.

Packing leakage was also

identified on Valves RWCU-VR and RWCU-V-704. Valve RWCU-V-4 is the

outboard containment isolation valve to the RWCU system, while Valve RWCU-

V-704 is a pressure gage root valve downstream of Valve VC.

Operational

leakage from this system is undesirable due to the relatively high activity levels in

process fluid.

The inspector noted that packing leakage from Valve RWCU-V-704 contributed to

elevated reactor building effluent levels early in the current operating cycle. As a

result, the licensee made an entry into the RWCU pump rooms to tighten the

valve's packing in August 1997.

Valve RHR-V-24A (Suppression

Pool Cooling/Test Return), RHR-V-27B

(Suppression

Pool Spray), and RHR-V-42A (Low Pressure Coolant Injection

Isolation) each showed signs of packing leakage.

Active leakage (10 drops per

minute) was observed on Valve VQ2A, while standing water was observed

around the packing and bonnet wells of Valves V-24A and V-27B. Leakage from

these components is undesirable as each of the valves is within the boundary of

the postloss-of-coolant accident RHR recirculation loop.

A number of manual Borg-Warner valves were identified without their t-handle

operator installed, including Valves RHR-V-708A and C. Although no reference

0

was identified within the emergency operating procedures for manipulating these

valves, the lack of a'manual operator unnecessarily.complicates

system

alignment and alignment verification.

Lighting deficiencies, were identified in each'of the areas inspected, the'most

significant being the RHR Loops A and.C pipe chase on the reactor building

522 foot elevation where none of the permanently installed lighting was

functional. Occasional access to this area is required for emergency core cooling

system venting and RHR system leakage inspection.

The following housekeeping

deficiencies, were observed:

~

Five ladders were identified as being improperly stored in areas containing

safety-related equipment.

The improper storage of the ladders was a violation of

licensee procedures and is discussed

in Section 01.2.

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Parts from an abandoned

pipe support, constructed of heavy-gage steel plate

and 4-inch x 4-inch steel box beam, were discovered on a mezzanine in'the

southwest valve room on the 471 foot elevation of the reactor building. A review

of plant records found that the pipe support was abandoned

in 1986. The

improper storage of this material was considered significant in that, during a

seismic event, the potential existed for the material to fall from the mezzanine on

to some small-bore RHR piping below.

In the traversing incore probe mezzanine and the 492 foot RHR horizontal pipe

chase, quantities of transient combustibles were discovered in excess of the

allowable limits established by licensee procedures.

Transient combustibles

were also discovered in several other areas, including the RWCU heat exchanger

room and the RWCU pump room mezzanine.

However, a thorough inventory

was not completed to determine whether or not those quantities were within

limits. Further discussion of transient combustibles and the licensee's fire

protection program are provided in Section F1.1.

An empty beer can was found in the 492 foot RHR horizontal pipe chase and

cigarette butts were found in the southwest valve room on the 471'levation of

the reactor building. Information obtained from the bottom of the can showed that

the beer was produced in 1995. The age of the cigarette butts was unknown.

Although the specific circumstances surrounding these items cannot be

determined, their presence

is of concern in that they are prohibited to be

consumed inside the radiologically controlled area.

Furthermore, licensee

procedures prohibit alcoholic beverages

on the plant site.

Based upon the number of discrepancies

identified, the inspector reviewed the licensee's

program for evaluating plant material condition. This program is described in

PPM 1.3.19, "Plant Material Condition Inspection Program," Revision 21. The plant

general manager has overall responsibility for this program.

PPM 1.3.19 provides

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guidelines and examples for inspecting material condition, housekeeping,

radiological

conditions, and fire protection.

Department:managers

are informally assigned specific

areas of the plant by the plant manager and are expected to include out-of-the-way and

limited access areas as part of their assigned inspection. The program, however, does

not provide specific guidelines on the frequency in which inspections are to be performed

and no information was found to indicate that department managers had performed

recent inspections in the areas'walked down b'y the inspector.

Had inspections been

performed in these areas, the guidance in PPM 1.3.19 was found to be sufficient to

identify each'of the above discrepancies."

For high radiation ar'eas', PPIVI'-1.3.19 provides the radiation protection manager the

discretion in determining the'frequency of inspection..'owever,

from discussions with

the radiation. protection manager, it was found'that'he had not been familiarized with the

program or his'responsibilities.

Plant procedures would require specific radiation work

permits to be developed for'these inspections; however, none could be found for

calendar year 1997.

From disc'ussions with several plant staff, including health physics, engineering, and the

plant general manager, it appeared that conditions went unidentified or uncorrected due

to a perceived difference in expectations for compliance with housekeeping

procedures

for those areas not routinely accessed

due to radiation exposure concerns.

It was noted

that operations, maintenance,

and engineering personnel had made entries into several

of the areas for emergent maintenance during the current cycle; however, no material

condition or housekeeping

deficiencies were documented during those entries.

The lack

of management

inspection in these areas was considered to be a contributor to the

difference in standards.

The licensee's material condition program was not fullyimplemented to maintain and

assess

those areas of the reactor building not routinely accessed

by plant personnel.

As

a result, a de facto lower standard was established for these areas, and equipment and

housekeeping

deficiencies were allowed to persist.

Miscellaneous Maintenance Issues (92902)

I

V'

00 -: failure to preplan, document, brief, and authorize

troubleshooting.

This violation involved troubleshooting work outside the defined scope

of the plan. As a result of a human error during the work, the plant experienced a half-

scram actuation.

During this inspection, the inspector verified that licensee corrective actions committed to

in the licensee's response to the NRC in a letter dated May 1, 1996, had been

completed.

The incident had been reviewed with involved individuals, instrumentation

and control technicians had been counseled on self-checking practices, and applicable

procedures had been revised.

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50-39

00 -: the licensee's TS 4.6.5.3.b.2

directs testing of engineered safety feature (ESF) charcoal filters in accordance with

ANSI N509-1976; which requires, in part, the filter bed to be heated to 80'C. However,

the licensee's Final Safety Analysis Report (FSAR), Section 6.5, indicates that charcoal

filtertesting would be accomplished using ANSI N510-1980, which requires, in part, that

the filterbed be heated to 30'C.

As part ofthe licensee's conversion to Improved Technical Specifications (ITS),

implemented in'March 1997, the specific testing requirements for the ESF filters were

relocated to TS 5.5.7, "Ventilation Filter Testing Program." TS 5.5.7 now references

ANSI N510-1989 as the applicable version of the testing standard.

Th'e 1989 standard

did not change fhe te'sting methodology from th'e 1980 standard.

The staffs approval of

the Ventilation Filter Testing Program in ITS indicated that the testing methodology of the

later versions of the ANSI standa'rd would provide confidence that the filters would

perform their safety function. Additionally, it was found that testing of the charcoal beds

at lower temperatures

provided more conservative results in that, at lower temperatures,

the activated charcoal has a lower affinityfor iodine retention and, thus, a higher leakage

rate through the bed.

Based upon the staffs approval ofthe licensee's ITS and its use of ANSI N510-1989 and

the fact that the more recent versions of the standard, utilized by the licensee, provide a

methodology that produces more conservative results, the failure to test ESF charcoal

filters using the 1976 version of the ANSI standard was not considered to be safety

signiTicant. The licensee's actions to implement ITS effectively addressed

the

discrepancy between TS and the FSAR. This failure constitutes a'violation of minor

significance and is being treated as a noncited violation, consistent with Section IVof the

NRC Enforcement Policy (NCV 50-397/97018-02).

II. E

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Conduct of Engineering

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In response to packing leakage identified on Valve RCIC-V-64 (Section M2.1), the

inspector reviewed the licensee's program for controlling primary coolant leakage outside

containment.

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The requirement to evaluate and reduce leakage'from systems outside containment

stems from TMIAction Item III.D.1.1, as described in NUREG-0737. The licensee

addressed

this item in Appendix B of their FSAR and incorporated the requirements in

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the TS. TS 5.5.2, "Primary Coolant Sources Outside Containment," outlines the

requirements of the prograrri, including preventive maintenance,

visual inspections, and.

integrated leak tests.

PPM 1;5.6, "Leakage Surveillance and Prevention Program," Revision 8, implements'the

requirements of TS 5.5.2. 'Ih reviewing PPM 1.5.6, the inspector noted a,number of

discrepancies

between the procedure, TS, and the FSAR.

It was also noted that

Valve RCIC-V-64 (discussed

in Section-M2.1) was not covered by PPM 1.5.6. Some of

the specific discrepancies

identified include:

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PPM 1.5.6 directs visual inspections of the applicable systems during routine

plant operations, including surveillances.

Visual inspection requirements were

verified to be included in. system surveillance procedures,

but were not included

in system operating procedures.

The visual inspection requirements in

TS 5.5.2 and the FSAR were not as clearly defined and, thus, subject to some

interpretation.

Although PPM 1.5.6 indicates the need to inspect systems during

routine operations, the licensee contended that visual inspections were only

intended to be performed during surveillances.

That position does not conflict

with TS requirements or the language in the FSAR.

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Visual inspections of selected instrument racks are required by PPM 1.5.6 during

operator rounds.

However, the specific instrument racks required to be inspected

are not defined by the procedure, nor are they captured in operating instructions

for equipment operators.

During.routine plant tours, the inspector did not identify

any leakage from safety-related instrument racks.

The lack of specific guidance

on inspecting instrument racks was considered a program weakness

in

PPM 1.5.6.

TS 5.5.2 speciTically references the standby gas treatment system as one of the

systems covered under the leakage surveillance program. As such, periodic

maintenance,

visual inspections, and integrated leak tests are required.

PPM 1.5.6 also references the standby gas treatment system; however, no

requirements are included for performing visual inspections and integrated leak

tests.

At the end of the inspection, insufficient information was available to

reconcile this discrepancy and, therefore, an unresolved item was opened

(URI 50-397/97018-03).

TS 5.5.2 requires integrated leak tests to be performed on a 24-month interval.

The leakage surveillances are listed as biennial procedures in Attachment 6.1 to

PPM 1.5.6.

However, Section 3.2.1 and Note 2 of Attachment 6.1 both state that

the surveillances are performed on an 18-month cycle. From discussions with

the program manager, it was determined that PPM 1.5.6 was not adequately

updated upon the conversion to ITS.

A review of the most recent integrated leakage surveillances for the systems covered by

TS 5.5.2 showed that the systems were relatively leak-tight. That conclusion was

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supported by a low number of leakage-related work requests against those systems.

As

noted in Section M2.1; packing leakage was identified for several valves located in high

radiation/contamination areas.

Valves RCIC-V-64 and RHR-V-42A both had identifiable

.

packing leakage that had not been previously documented by the licensee.

Allof the integrated leakage surveillances were found to be current, with the exception of

the surveillance for reactor core isolation cooling'(RCIC). The latest RCIC surveillance

was in the review process, while the previous surveillance had been completed in June

1995.

Based upon the original 18-month frequency required by TS 6.8.4.a.2, the RCIC

surveillance was overdue in. January 1997.. The surveillance became overdue based

upon the licensee's surveillance scheduling program applying a 25 percent extension to

the surveillance interval (application of TS 4.0.2).

However, TS 6.8.4.a.2 provides no

basis for allowing the use of TS 4.0.2 in scheduling the surveillances.

The practice of

applying an extension period to these surveillances had apparently been in place since

initial facility licensing. Atthe end of the inspection period, the licensee was reviewing

other TS administrative programs to determine ifTS 4;0.2 had been inappropriately

applied in other situations.

Pending the licensee's further review of other TS programs,

this is an unresolved item (URI 50-397/97018-04).

The inspector noted that, through approval of the licensee's

ITS, implemented in March

1997, the staff authorized the extension of the surveillance interval to 24 months and

allowed the use of Surveillance Requirement 3.0.2 to extend the interval by 25 percent

for scheduling flexibility. Thus, the licensee has already taken action to 'explicitly

authorize the historical scheduling practice for the leakage surveillance and prevention

program.

In discussing the above issues with licensee personnel, including managers,

knowledge

gaps were identified with respect to the current status of the program and its

implementation.

Specifically, the program manager was unaware of the discrepancies

noted in the procedure and was not knowledgeable of the outstanding leakage-related

work requests for those systems covered under the program. The operations manager

was unfamiliar with his responsibility to ensure periodic visual inspections are performed

for the systems included in the program, while the system engineering manager,

responsible for overall program implementation, was unfamiliar with the requirements of

PPM 1.5.6.

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Performance issues regarding plant staff knowledge, program implementation, and

procedural inconsistencies were indicative of weak management involvement and poor

maintenance of the primary coolant system leakage surveillance and prevention

program.

ES

Miscellaneous Engineering Issues (92903)

-12-

E8.1

E8.2

Clo e

IFI

-3 7

00 -0: failure to'update the FSAR when the standby service

water, keep-full system was abandoned

in place.

This, issue was converted to an

unresolved item in NRC inspection Report 50-397/96-201 and willbe dispositioned

through that report item. This IFI is administratively closed.

s

.the licensee had not performed a review of.

Calculation ME-02-85-75, Revision 2, which analyzes the heat removal capacity of a

single service water pond during an accident, prior to implementing the reactor power

uprate during the spring 1995 refueling outage.

I'

The, licensee determined the cause of the failure to perform a review of the calculation

was the incorrect title entry in the database that was utilized to track reviews. The

abbreviation for the. service water system utilized by the Calculation Review was "SSW."

The database

used during the review for the power, uprate identified this acronym as

"Sacrificial Shield Wall." The incorrect title in the database

led the reviewers, relying on

the database,

to erroneously assume that the identified calculation was unaffected by the

power uprate.

The licensee conducted a further review of the database,

concluding that

there were no other cases where a system was erroneously identified. The database

used in this instance was a working file on a reviewer's computer and not part of one of

the licensee's sitewide databases.

Further, the database was not formally controlled by

the licensee.

The inspector noted that the reliance on this database

appears to be a

weakness

in the licensee's performance of the power uprate review.

The licensee noted in Problem Evaluation Request (PER) 296-0787, that the service

water pond calculation, ME-02-85-75, Revision 2, used a conservative heat generation

rate that bounded the power uprate conditions.

The licensee further indicated that ME-

02-85-75 will be revised to reflect the current conditions, which include the power uprate.

The licensee's corrective actions were considered appropriate.

The erroneous entry of

SSW in a database

appeared to have been an isolated occurrence.

The inspector

concluded the licensee's review of affected calculations was weak in that it relied upon

an uncontrolled database.

E8.3

sed

-397/

33-: the licensee's evaluation of the standby service

water (SSW) system leaks, the quantifying and evaluation of hydraulic transient (water

hammer) loads of the SSW system, and the control of SSW flow control valve opening

times were examined.

On November 29, 1995, an NRC inspector and a licensee equipment operator identified

a leak from the weld area of a 3/4-inch Sock-o-let fitting, near the high point of the

service water line Loop B. A stream of water was spraying from the leak onto an

adjacent motor control center.

The licensee initiated PER 295-1229 to resolve the issue.

The evaluation performed for the leak indicated that the leak occurred due to wet/dry

cyclic conditions in the crevice area of the socket weld. In addition, the local crevice

corrosion rate was affected by microbiological-induced corrosion. The causes of the leak

were attributed to inadequate corrosion monitoring and chemical treatment for corrosion

-'1 3-

and biological control. Further, a contributing cause was the crevice of the socket weld

design of the SSW small bore piping.', The licensee dispositioned the leak by initiating

=

rework and the affected Sock-o-let flittingwas replaced.

The licensee has subsequently

implemented an ongoing program to reduce microbiological-induced corrosion in the

affected SSW and high pressure core spray service water (SW) systems.

The licensee conducted a visual inspection of SSW Loop B following-the troubleshooting

associated with the SSW pinhole leak on November 29, 1995.

Personnel, including

equipment operators, the system engineer, the shift support supervisor, and an NRC

inspector, observed the restart of the'SW line Loop B., The observers heard a bang in

the system, which the inspector characterized to the licensee as an apparent hydraulic

transient or water hammer.

Following the startup, the licensee inspected the SSW

Loop B restraints and supports, finding no apparent damage.

In a continuing effort to evaluate the water hammer, a startup of Loop Awas conducted,

with similar results. The licensee noted a bang in Loop A, but of a lower magnitude than

that of Loop B. Further investigation by the licensee identified a difference in opening

times for the butterfly valves, which control service water flow at the initiation of SW

system startup.

The control circuitry of the butterfly valves limits their opening during the

initial seconds of system startup in order to limitthe initial flowof water and to soften its

impact on the partially voided SW system.

Subsequent testing indicated the valves were

operating within their specified operating times and met the inservice testing

requirements.

Further investigation revealed a temperature control valve to

Chiller CCH-CU-1 B may have been the cause of the water hammer events.

When room

temperature

in the chiller room was less than 70'F, Valve SW-TCV-15B would remain

closed. A change to the setpoint of the valve had occurred previous to the events from

55'F to 70 F. With a space heater in place in the chiller room raising temperature above

70'F, no observation of a water hammer noise was generated.

The licensee has

changed the setpoint of the temperature switch associated with Valve SW-TCV-15B to

63'F. This change was considered appropriate to assure that the valve does not

contribute to future water hammer events.

The inspector began a review of the licensee's analysis of SW Loop B piping. This was

documented in Calculation Modification Record (CMR) ME-02-96-25. The calculation

was to evaluate the SW Loop B piping hydraulic transients in response to

PER 295-1275.

The inspector noted that the results of the calculation did not indicate

there were any substantive stresses

imparted to the piping or supports.

The inspector at

the time of the inspection had not completed a review of the calculational methodology.

This issue willbe tracked as an IFI (IFI 50-397/97018-05).

lo

d

ER

0-397/9

01 -00: the licensee found that the test methodused to satisfy

a RCIC surveillance requirement was incomplete. The TS requirement to verify the

RCIC Division 2 automatic isolation seal-in relay contact function was not covered in the

applicable surveillance procedures.

The RCIC Division 2 functional testing procedures

-14-

were deficient in that none of them verified that the automatic isolation signal would seal

in to maintain the RCIC system inboard steam supply isolation valve closed in the event

of a steam line break.

The licensee immediately performed the appropriate testing upon discovery and revised

PPMs 7.4.3.2.1.80, "RCIC Isolation on RCIC Steam Supply Flow High DIV2-CFT/CC,"

and 8.3.303, "Isolation - Response Time Testing RCIC-RLY-K33, K54, K55, K66 (Valve

Group 8/9) (DIV,2),"to adequately meet the intent of the requirement.

The licensee also

completed a technical adequacy review of all logic system functional tests for seal-in

contacts to ensure that these tests were adequate.

The licensee found that most

surveillance tests used a,test-sequence

that leaves in place the channel trip until

restoration of the circuit logic, which masks the direct.seal-in function verification. All

affected surveillances were corrected.

The inspectors reviewed the corrective actions and found them to be acceptable.

This

nonrepetitive, licensee-identified and corrected violation is being treated as a noncited

violation consistent with Section VII.B.1 of the NRC Enforcement Policy

(NCV 50-397/97018-06).

V

a

F1

Conduct of Fire Protection Activities

F1.1

o

s'be

In response to the identification of uncontrolled transient combustibles in limited access

areas (Section M2.1), the inspector reviewed the licensee's program for controlling

transient combustibles in the plant. The inspector also reviewed the licensee's fire

hazards analysis (FHA) to ensure that the identified combustibles did not exceed that

assumed

in the FHA.

The licensee's fire protection evaluation is described in Appendix B to the FSAR.

Appendix B provides a general overview of the methodology utilized in the FHA and

references Calculation FP-02-85-03 for the specific assumptions utilized in each fire area

for determining combustible loading.

To ensure that transient combustibles in the plant do not exceed that assumed

in the

FHA, the licensee has implemented PPM 1.3.10C, "Control of Transient Combustibles,"

Revision 0. To accomplish this, PPM 1.3.10C provides guidelines for different areas of

the plant to help plant staff determine when transient combustibles need to be evaluated

and controlled through the transient combustible permit process.

Depending upon the

-1 5-

specific fire area, as defined by the FHA, the amount of transient combustibles can be

evaluated against specific guidelines to determine the need for'a permit.

Based upon insights from the FHA, the licensee has designated certain areas of the

plant as "combustible free zones,". and others as "zones of limited combustibles."

For

"combustible free zones," any use of combustibles must be continuously attended and

no storage of combustibles is allowed. For "zones of limited combustibles," stricter

controls are placed upon transient materials.

For most other areas of the power block,

Attachment 9.2 of PPM 1.3.10C defines the amount of material that requires a transient

combustible permit.

P

During tours of limited access areas, the inspector found transient combustibles in

varying amounts in two.areas (the traversing in-core probe room mezzanine and the

492 foot level horizontal pipe chase in the reactor building). In both areas, the amount of

combustibles exceeded the guidelines of PPM 1.3.10C for requiring a transient

combustible permit. However, permits had not been reviewed or issued for either of the

areas.

Based upon the infrequent access to the areas, it appeared that the combustibles

had been in the areas since at least June 1997, during the licensee's last refueling.

outage.

Preliminary indications were that the material was left in the areas based upon

the perception by plant staff that a lower'standard is acceptable

in these areas to support

ALARA(as low as reasonably achievable) considerations.

A review of the FHA showed

that the quantities of material identified in the various areas did not exceed the

assumptions of the FHA and, therefore, the safety significance was considered to be

relatively low. The failure to properly track and control transient combustibles in the two

limited access areas was identified as a violation of TS 5.4.1 (VIO 50-397/97018-07) for

the failure to followprocedures

In reviewing Calculation FP-02-85-03, the inspector identified several discrepancies

in

the assumptions

utilized in the analysis and noted that the calculation was last revised in

1993 with 35 CMRs against it. Although each CMR was evaluated to determine its

impact upon the combustible loading for the applicable fire area, without updating the

base calculation, multiple CMRs affecting a single fire area could lead to an undesirable

cumulative effect that would not be captured in the CMR review process.

At best, the

CMR process becomes cumbersome

in evaluating multiple changes and supporting

plant modifications.

The base calculation also contained several internal discrepancies

and discrepancies

with PPM 1.3.10C.

Specifically, the combustible loading analysis for the Division I 4160V

switchgear room assumes that the silicone-based coolant in the 4160V/480V

transformers is combustible, with a heat release of approximately 60 million Btu.

However, the combustible loading analysis for the Division II 4160V switchgear room

assumes that the same silicone-based fluid is noncombustible and does not contribute to

the heat release.

The analysis for the diesel fuel oil day tank rooms does not provide an

allowance for transient combustible materials bas'ed upon the practice that the rooms are

normally locked.

However, PPM 1.3.10C does not explicitly prohibit transient

combustibles in the day tank rooms and it was noted that the rooms are, in fact, not

-'16-

normally locked. The combustibles found in the day tank rooms, including adsorbents,

wooden dipsticks, and a 2-gallon container of diesel fuel oil, did not exceed the general

limits of PPM 1.3.10C for requiring a transient combustible permit.

In the 480V vital motor control centers, the combustible loading analysis assumed

a

transient combustible loading equivalent to 50 Ibs of paper.

However, PPM 1.3.10C

allows for up to an equivalent of 100 Ibs of paper in this area without requiring a transient

combustible permit.

The review of Appendix B to the FSAR noted'that the specific assumptions and results of

the combustible loading analysis for each fire area were removed from the FSAR in

conjunction with a change to the FHA methodology in,1994.

However, a safety

evaluation, in accordance with 10 CFR 50.59, had not been documented to show that the

change did not constitute an unreviewed safety question.

The licensee initiated a PER to

address the issue and was reviewing the impact of the FSAR changes at the end of the

inspection period. An unresolved item was opened to disposition this issue (URI 50-

397/97018-08).

The licensee's program for controlling transient combustibles in the plant has been

applied inconsistently in that materials have been allowed to accumulate in limited

access areas without being properly evaluated or tracked.

Inconsistencies

in the licensee's combustible loading calculation, coupled with a

relatively large backlog of modiTications to the current revision of the calculation, resulted

in reducing the value of the calculation as a tool in supporting plant modifications.

P2

Status of Emergency Preparedness

Facilities, Equipment, and Resources

P2.1

in

nanc

of

n

27

The inspectors reviewed the licensee's actions to address

PER 297-0242, dated

March 25, 1997,

involving an inoperable control room facsimile machine.

b.

rva ions and Findin

While attempting to make offsite agency notifications during a notification of unusual

event on March 20, 1997, the operator discovered that the control room facsimile

machine was inoperable.

Notifications were made via alternate methods, and the

inoperable facsimile machine was replaced about 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> later. The licensee's

investigation disclosed that the last documented preventive maintenance test on the

-17-

facsimile machine was September 1996.

However, PPM 13.14.4, "Emergency

Equipment," Revision 24, Attachment 5.5, requires a monthly check of the control room

facsimile machine.

Based on the investigation results, the licensee took the following corrective actions:

Alltelecommunications service instructions were revised and updated to include

detailed checklists for performing preventive maintenance activities with individual

sign-offs.

~

A 1-year program was being developed to require a telecommunications systems

team lead to observe one preventive maintenance task per month to ensure that

the task was properly performed.

~

A self-assessment

of the telecommunications service procedures and preventive

maintenance program was scheduled to be performed.

~

Procedural compliance training for telecommunications services personnel has

been completed.

~

Procedural compliance training for information services and facilities personnel

has been scheduled.

The failure to perform a monthly check of the control room facsimile machine is a

violation of TS 6.8.1, which requires the licensee to followprocedures that implement the

emergency plan. This nonrepetitive, licensee-identified and corrected violation is being

treated as a noncited violation, consistent with Section VII.B.1 of the NRC Enforcement

Policy (NCV 50-397/97018-09).

~Co

tugign

The licensee's failure to test the control room facsimile machine contributed to a piece of

emergency response equipment being inoperable until it was required to be used during

an actual event. A noncited violation was identified.

V

ana

e

en

Me

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management after the

conclusion of the inspection on December 31, 1997. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection should

be considered proprietary.

No proprietary information was identified.

0

AITkCtl

NT

Supplemental Information

PARTIALLIST OF PERSONS CONTACTED

D. Hillyer, Radiation Protection Manager

P. Inserra, Licensing Manager

D. Kobus, Fire Protection, Supervisor

M. Monopoli, Operations Manager

J. Peterson,

Fire Protection Engineer

G. Shindehite, Operations

G. Smith, Plant General Manager

J. Stacks, Engineering

S. Szendre, Raytheon Foreman

INSPECTION PROCEDURES USED

IP 37551:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 82701:

IP 92901:

IP. 92902:

IP 92903:

Onsite Engineering

Surveillance Observations

Maintenance Observations

Plant Operations

Plant Support

Operational Status of the. Emergency Preparedness

Program

Followup - Operations

Followup - Maintenance

Followup - Engineering

0 ene

ITEMS OPENED, CLOSED, AND DISCUSSED

50-397/97018-01

50-397/97018-02

50-397/97018-03

50-397/97018-04

50-397/97018-05

50-397/97018-06

50-397/97018-07

50-397/97018-08

50-397/97018-09

VIO

failure to properly secure transient or portable equipment

NCV

failure to test control room charcoal filters in accordance with TS

URI

adequacy of suweillance procedures for SGT to meet TS 5.5.2

URI

application of TS 4.0.2 to surveillances required by TS 6.8.4.a.2

IFI

review oftransient hydraulic loads on SSW loop piping

NCV

inadequate procedure for verifying RCIC isolation seal-in logic

VIO

failure to control transient combustibles

URI

lack of a written safety evaluation for changes made to the FHA

NCV

failure to perform required monthly tests of control room facsimile

Qmd

-2-

50-397/95009-01

LER

inadvertent MSIVisolation during testing

50-397/95011-00

LER

50-397/95033-01

IFI

50-397/9600'I-01

VIO

50-397/96003-05

.

IFI,

50-397/96006-04

IFI

inadequate procedure for verifying RCIC isolation seal-in logic

review of licensee actions in response to identified SSW system

leakage

failure to pre-plan, document, brief, and authorize

troubleshooting

conformance of.charcoal filtertesting with TS requirements

failure to update the FSAR when SSW keep-full system was

abandoned

50-397/96016-01

VIO

failure to adhere to procedures related to log entries and record

retention

50-397/96016-03

VIO

failure to adhere to procedures for reactor startup

50-397/96016-05

VIO

failure to have an appropriate procedure for adjustable speed drive

testing to preclude a nonlicensed person from operating the

reactor controls

50-397/96024-02

URI

failure to review ultimate heat sink capacity calculation prior to

implementation of reactor power uprate

50-397/9701 8-02

NCV

failure to test control room charcoal filters in accordance with TS

50-397/97018-06

NCV

inadequate procedure for verifying RCIC isolation seal-in logic

50-397/97018-09

NCV

failure to perform required monthly tests of control room facsimile

I

-3-

LIST OF ACRONYMS USED

CMR

ESF

FHA

FSAR

IFI

, ITS

LER

MSIV,

NCV

NRC

PER

PPM

'RCIC

RHR

RWCU

SSW

SW

TS

URI

VIO

WNP-2

calculation modification record

~engineered safety feature

fire hazards analysis

Final Safety Analysis Report

inspection followup item

Improved Technical Specifications

licensee event report

main steam isolation valve

noncited violation

U.S. Nuclear Regulatory Commission

problem evaluation request

Plant Procedure Manual

reactor core isolation cooling

residual heat removal

reactor water cleanup

standby service water

service water

Technical Specifications

unresolved item

violation

Washington Nuclear Project-2

~

~

4

5

~