ML17292B093

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Insp Rept 50-397/97-16 on 970817-0927.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML17292B093
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 10/21/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17292B091 List:
References
50-397-97-16, NUDOCS 9710240310
Download: ML17292B093 (24)


See also: IR 05000397/1997016

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

License No.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-397

NPF-21

50-397/97-1 6

Washington Public Power Supply System

Washington Nuclear Project-2

Richland, Washington

August 17 through September

27, 1997

S. A. Boynton, Senior Resident Inspector

G. D. Replogle, Resident Inspector

H. J. Wong, Chief, Reactor Projects Branch

E

Attachment:

Supplemental

Information

97i02403f.0 97i021

PDR'DOCK 05000397

8

PDR

EXECUTIVE SUMMARY

Washington Nuclear Project-2

NRC Inspection Report 50-397/97-16

.~Oerations

Operations

personnel

did not adequately

assess

available in'formation indicating

degraded

performance of the installed instrumentation for measuring reactor coolant

system

(RCS) identified leakage.

As a result, actions required to perform an

alternate method for s'atisfying the surveillance were delayed and the Technical

Specifications

(TS) required surveillance interval for evaluating

RCS operational

leakage was exceeded

(Section 01.2).

Operations

and engineering

personnel

did not demonstrate

a questioning attitude

following the identification of a broken lockwire on a safety-related

pressure control

valve associated

with the automatic depressurization

system (ADS). Verification of

the valve's pressure control setpoint was delayed

2 days.

The as-found setpoint

was determined to be below that to support long term operability of the associated

ADS valves (Section 08.1).

Maintenance

The implementation of the Foreign Material Control (FMC) Program was poor during

Refueling Outage R12.

Previous corrective actions to prevent recurrence

were

considered

weak (Section M8.1).

Encnineering

Problem Evaluation Requests

(PERs) were appropriately written in the majority of

instances when they were required.

However, one violation of procedures,

with

two exam'ples, was identified for the failure to write PERs for problems with

safety-related

equipment.

Some engineers

did not have an appropriate

understanding

of PER requirements

and were not using the applicable procedure

(Section E8.3).

Plant Su

ort

The failure of licensee personnel to recognize and address

potential radiological

concerns

associated

with several work activities resulted in unplanned

personnel

contaminations

and exposures.

A violation with three examples was identified.

In

an event involving the surveillance tests in the equipment drains radioactive

(EDR)

sump area, health physics (HP) and operations

personnel

did not properly address

the source of the contamination

and, as a result, a second equipment operator

(EO)

was contaminated

(Section R1.1).

0

0

Re ort Details

Summar

of Plant Status

The inspection period began with the reactor at 100 percent power.

On August 26, 1997,

power was temporarily reduced to 95 percent to compensate

for high main condenser

steam jet air ejector temperature that was a result of high ambient temperatures.

On

August 29, power was reduced to approximately 80 percent at the request of the

Bonneville Power Administration.

The plant was returned to full power on September

1.

On September

6 and 12, power was temporarily reduced to 90 percent to support gain

adjustments

to the digital feedwater control system.

During the weekends of

September

20-21 and September

27-28, power was again reduced at the request of

Bonneville Power Administration. At the end of the inspection period the plant was

operating at 80 percent power in economic dispatch.

I. 0 erations

01

Conduct of Operations

01.'I

Genera( Comments

71707

Using Inspection Procedure 71707, the inspectors conducted

frequent reviews of

ongoing plant operations.

The conduct of operations was generally professional

and

safety conscious.

01.2

Missed Surveillance for RCS Total Leaka

e

a.

Ins ection Sco

e 61726

During discussions with operations

personnel

on September

5, 1997,'the inspector

noted that TS Surveillance Requirement

(SR) for RCS total leakage had been

performed using an instrument which was not operating reliably. The inspector

conducted

followup to this observation.

b.

Observations

and Findin s

Background:

TS SR 3.4.5.1, in part, requires the licensee to monitor RCS total

leakage every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

The licensee would normally perform this surveillance

utilizing, in part, the identified leakage totalizer (FDR-FQ-38) in the control room.

On September

4, 1997, operators noted a step change

in the identified leakage rate

surveillance results.

While normal leakage was approximately 2.5 gpm, the

surveillance indicated that leakage was approximately 0.1 gpm.

Operations

questioned

the operability of the totalizer and initiated steps to measure identified

leakage using an alternate method ("bucket test," in accordance

with Plant

Procedure

Manual (PPM) 2.11.3, "Equipment Drain System" ).

-2-

An EO performed the first bucket test at approximately 6 a.m. on September

4.

However, operations

did not have confidence

in this initial test because

the EO had

observed

a flow surge during the surveillance.

Also, upon exiting the controlled

surface contamination

area, the EO was found to be contaminated.

At approximately'7 p.m. on September

4, following a flush of the EDR flow

instrument line, an EO completed

a second bucket test and found identified leakage

to be about 2.5 gpm.

Upon exiting the controlled surface contamination

area, the

EO was again found to be contaminated

(see Section R1.1 for a detailed discussion

of the contamination events).

Later in the shift, qualitative evaluations

by the

operating crew on the performance

of the leakage totalizer indicated that the

instrument was not measuring

an identified leakage flow consistent with the latest

bucket test or'historical instrument readings.

However, the operating crew did not

declare the flow totalizer inoperable,

and consequently

did not convey to HP

personnel the nee'd to be able to perfom another bucket test early in the day shift to

meet the TS SR.

At 7 a.m. on September

5, 1997, in consideration of the two contamination events,

the shift manager postponed

the next bucket test until additional HP controls could

be established

for the job.

Operators performed TS SR 3.4.5.1 utilizing FDR-FQ-38,

but operations recognized that the surveillance was not valid, based

on the

instrument's erroneous

indications.

At 8 a.m., FDR-FQ-38 was officially declared

inoperable.

HP established

improved contamination controls for the job, and at

approximately 3:30 p.m. the surveillance was successfully performed.

NRC Assessment:

Based upon the valid bucket test performed on the evening of

September 4 and taking into consideration

the 25 percent grace period allowed by

TS 3.0.2, the subsequent

surveillance for RCS total leakage was required to be

performed no later than 10 a.m., September

5. The failure to perform the

surveillance within the required interval was identified as a violation of

TS SR 3.4.5.1

(VIO 50-397/97016-01).

The inspectors

considered

the failure of Operations

personnel

to promptly inform HP

of the need to establish better HP controls for the bucket tests to be a key

contributor to the violation.

Operations

had clear indication that FDR-FQ-38 was

- inoperable on the evening of September 4, but did not inform HP of the need to

enhance

the HP controls for the test until the FDR-FQ-38 was officially declared

inoperable at 8 a.m. on September

5.

Conclusions

Operations personnel

did not adequately

assess

available information indicating

degraded

performance of the installed instrumentation for measuring

RCS identified

leakage.

As a result, radiological controls were 'not promptly established

to support

an alternate, manual method for measuring

leakage and, as a result, the 'I S required

surveillance interval for evaluating

RCS operational leakage was exceeded.

-3-

Operational Status of Facilities and Equipment

02.1

En ineered Safet

Feature

S stem Walkdowns

71707

The inspectors walked down accessible

portions of the following engineered

safety

feature systems:

Standby Service Water Loop A

Reactor Core Isolation Cooling

Emergency

Diesel Generators,

Divisions I, II, and III

Residual Heat Removal System, Trains A, B, and C

Low Pressure

Core Spray System

The systems were found to be properly aligned for the plant conditions with no

notable material condition deficiencies.

08

Miscellaneous Operations Issues (92901)

08.1

Closed

Licensee Event Re ort

LER 97-008-00:

inoperability of four ADS valves

due to improper setpoint of containment instrument air (CIA) pressure control valve.

On July 16, 1997, the licensee identified, through

a system engineer walkdown, a

broken lockwire on Valve CIA-PCV-2B. Subsequent

investigation on July 17 also

identified that the valve stem locknut was loose.

Valve CIA-PCV-2B provides a

supply of nitrogen to the four Subsystem

B ADS valves from the safety-related

backup nitrogen bottles.

The supply of nitrogen from these bottles is designed to

provide an actuating force to open the ADS valves in support of long-term alternate

core cooling.

Normal supply to the ADS valves is from the nonsafety-related

containment nitrogen system, which is not relied upon in the licensee's

loss-of-coolant accident analyses.

In addition, each ADS valve has

a safety-related

accumulator, which provides for at least one, and up to five, actuations of the ADS

valve for depressurizing

the reactor pressure

vessel.

Troubleshooting

performed on July 18 found that the setpoint of Valve CIA-PCV-2B

was 63 psig, well below the normal setpoint of 180 psig.

The licensee determined

that the set pressure

was insufficient in supporting long-term alternate core cooling

with the Subsystem

B ADS valves.

The valve was promptly readjusted to the

appropriate

180 psig setpoint, following the troubleshooting,

to restore operability.

Based upon the licensee's identification of the broken lockwire on July 16, and the

subsequent

setpoint restoration on July 18, the Subsystem

B ADS valves were

determined to have been inoperable for long-term cooling purposes for at least

52 hours6.018519e-4 days <br />0.0144 hours <br />8.597884e-5 weeks <br />1.9786e-5 months <br />.

TS 3.5.1.G requires the plant to be placed in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

when two or more ADS valves are inoperable.

Thus, the condition identified by the

licensee was a condition prohibited by TS and reportable under the requirements

of

10 CFR 50.73.

The inspector noted that the normal nitrogen supply and each individual ADS valve

accumulator were available for the duration of the time the valve was improperly

set.

Additionally, the licensee's

analyses

have shown that the operability of the

three Subsystem

A ADS valves would have been sufficient to provide the ADS

function of long-term alternate core cooling if the normal nitrogen supply was lost.

Therefore, the ADS depressurization

and long-term cooling safety functions were

maintained throughout this time period and the actual safety significance of the

event was considered

to be low.

Identification of the broken lockwire by the system'ngineer

demonstrated

a good

practice of inplant monitoring.

However, based upon the information available to

the licensee on July 16 and 17, and the 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> action time provided by

TS 3.5.1.G, the timeliness of troubleshooting

efforts to determine the valve's

setpoint was inconsistent with the potential impact on ADS operability.

The weak

follow-through on the identified discrepancy

by operations

and engineering resulted

in the four Subsystem

B ADS valves being inoperable for an extended

period of time

that could have been avoided.

A violation of 10 CFR Part 50, Appendix B,

Criterion XVI was identified (VIO 50-397/97-16-02).

As a result of the licensee's investigation of this event, the licensee was unable to

determine the specific cause of the misadjustment of Valve CIA-PCV-2B and there

was no clear evidence that would indicate tampering was involved.

II. Maintenance

M1

Conduct of IVlaintenance

M1.1

General Comments

a.

Ins ection Sco

e 62703

61726

The inspectors observed

the following work activities:

Work Order HFW3, Replacement

of SW-V-49, low pressure coolant spray

pump motor cooler throttle valve

~

PPM 2.11.3, Drywell Identified Leakage Bucket Surveillance

In general, work was appropriately performed.

However, problems associated

with

the drywell identified leakage bucket surveillances

are discussed

in Sections 01.2

and R1.1.

-5-

M8

Miscellaneous Maintenance Issues (92902)

M8.1

0 en

Ins ection Followu

Item 50-397/97009-02:

implementation of the FMC

Program.

The inspector identified that the craftsmen and supervisors

associated

with the Diesel Generator

2 cooling water heat exchanger work had an inadequate

level of knowledge to ensure proper implementation of the WNP-2 FMC

requirements.

Additionally, the work instructions associated

with the job did not

contain steps to ensure that required FMC inspections were performed.

This

inspection followup item was established

to track additional followup regarding the

overall implementation of the licensee's

FMC program.

The FMC controls for WNP-2 are specified in PPM 10.1.13, "FMC for Systems

and

Components,"

Revision 14.

The program requirements

apply to both safety- and

nonsafety-related

work. As a minimum, the procedure

requires

a documented

FMC

inspection by a craft supervisor prior to system/component

closure.

In response

to the inspector's

original finding, the licensee retrained all craft

supervisors

regarding the WNP-2 FMC requirements.

Craft supervisors

were

instructed to ensure that an appropriate

FMC inspection was documented

in the

"Work Performed" section of the work order.

This documentation

was required

even if the work document did not itself specify an FMC inspection.

WNP-2

management

stated that the individual work orders did not need to specify when

the inspections

were required,

as the craft supervisors

were already trained to

perform and document these inspections without such prompting.

As part of the followup to the inspector's

concern, the quality assurance

department

performed additional inspection of work packages to check compliance

with FMC requirements.

The quality assurance

inspectors reviewed 15 work

packages

in which the scope of work would have required an FMC inspection and

.found that an FMC inspection was not performed for eight of the jobs (all jobs were

from Refueling Outage R12).

Furthermore,

an FMC inspection was only performed

when the work package specifically required it. When craft supervisors

were

expected

to perform the inspections without being prompted by the work

document,

the supervisors

consistently failed to perform the inspections.

The

finding was documented

in PER 297-0683.

Since the sample of work orders reviewed was composed

primarily of

nonsafety-related

work, and all of the instances where FMC requirements

were not

met were associated

with nonsafety-related

work, no violations of NRC

requirements

were identified.

Nonetheless,

the inspectors considered

the overall

implementation of the licensee's

FMC program during Refueling Outage R12 to be

poor.

The inspectors

also noted that there were no indications of foreign materials

in systems following R12.

-6-

As corrective measures

for the issue, the licensee initiated plans to retrain all

maintenance

personnel

and planners regarding FMC requirements

prior to the next

outage.

The inspectors considered

the corrective measures

to be weak.

Specifically, training the maintenance

staff was performed on two previous

occasions

(once before the fast outage and once after the inspectors identified that

FMC program requirements

were not being met), but maintenance

personnel were

still not implementing the FMC Program requirements,

as demonstrated

by

PER 297-0683.

The inspector considered

the absence

of specific guidance

in the

work request (to specify and document the inspections)

as a significant contributor

to this problem.

The licensee's

corrective actions had not addressed

this

contributor.

In response

to the inspector's concern, the licensee planned to

strengthen the corrective actions.

This item will remain open pending further

review of the licensee's

FMC practices by the NRC.

M8.2

Reo

en

VIO 50-397 95020-02:

Inspection Report 50-397/97-12 erroneously

closed this item.

The item number closed should be VIO 50-397/95020-01, which

refers to the issue (qualitative/quantitative

acceptance

criteria) discussed

in the

report.

M8.3

Closed

VIO 50-397/95020-01:

See preceding paragraph.

III. En ineerin

E8

IVliscellaneous Engineering Issues (92903)

E8.1

Closed

Unresolved Item 50-397 97003-03:

inoperable reactor water cleanup

instruments.

On February 11, 1997, the licensee identified that reactor water

cleanup flow Switches LF-FS-15 and LD-FS-16 (Division I and II) were inoperable

since initial calibration in Spring 1995

~ The setpoints were found to be 276.5 gpm,

while TS permitted a maximum setting of 271.7 gpm.

The licensee reported the finding to the NRC in LER 97-001.

This issue will be

reviewed and tracked in conjunction with the LER. This unresolved

item is

administratively closed.

E8.2

Closed

Unresolved Item 50-397 96017-01:

This item pertained to the licensee's

deferral of one test associated

with the reactor recirculation control (RRC) and

reactor feedwater (RFW) systems.

The licensee planned to trip one RFW pump

from 100 percent reactor power to verify proper operation of RFW and RRC scram

avoidance capabilities.

The test was deferred until the end of the operating cycle.

On March 27, operators performed the subject test.

Due to the unexpected

operation of the plant, operators manually scrammed the reactor.

The NRC

subsequently

conducted

a special inspection of the event (NRC Inspection

Report 50-397/97-10).

This item is closed based

on that inspection effort.

0

-7-

E8.3

Closed

Unresolved Item 50-397/96024-03:

failure to write PERs.

The licensee

had identified repetitive instances

where plant personnel were not initiating PERs

when required.

PERs 296-0834, 295-1195 and 196-0357 each documented

multiple examples of the procedural noncompliance.

Background:

At WNP-2, the PER program is governed

by PPM 1.3.12, "Problem

Evaluation Reports."

The program applies to both nonsafety-related

and safety-

related system, structures,

and components.

PPM 1.3.12 requires

PERs to be

written, in part, for the following conditions:

Conditions adverse to quality, such as failures, malfunctions, deficiencies,

deviations, defective material and equipment,

and nonconformances

associated

with safety-related,

augmented

quality items, Maintenance

Rule

scoped systems,

and those used in emergency operation procedures.

Corrective work on an item because

it does not meet specified requirements,

unless the work is rework.

System, structures,

and components

malfunction, damage,

or degradation

considered

sudden or unexpected,

or outside the anticipated performance of

the item.

Although other processes

are redundant to the PER process with regard to

corrective actions (i.e. work requests),

PERs are still required in most cases to

ensure that plant problems are appropriately addressed

and trended, i.e.,

Maintenance

Rule.

Additionally, plant managers

review the new PERs each day.

Part of the information considered

at the PER meeting is previous, but similar, PERs.

Failure to write a PER could result in masking problems from plant management,

thus not allowing management

the opportunity to ensure that appropriate corrective

actions are taken.

Furthermore, management

may not get an accurate perception of

equipment performance

when past and current PERs are reviewed during the PER

meeting.

NRC Assessment:

The inspector audited

a 6-week sample of operator logs (July 5

to August 16, 1997) to determine if PERs were being written, when appropriate, for

equipment problems.

The inspector found that in most cases

PERs were written when required.

However, performance was not consistent.

For example, the inspector identified

the following conditions that met the PER criteria, but PERs were not written.

~

Hydraulic Control Unit 4619 experienced

low accumulator pressure

alarms

on six occasions

between July 10 and August 10.

In response

to each

alarm, the accumulator was secured

and recharged.

Although a PER was

required to be written to document tl e degraded

condition (leaking

-8-

accumulator),

no PER was written until the accumulator failed on August

11

when it could not be recharged.

A PER would have likely prompted

management

into taking more effective corrective actions to preclude failure

of the degraded

accumulator.

The failure to initiate a PER for the degraded

condition (prior to accumulator malfunction) is the first example of a violation

of 10 CFR Part 50, Appendix B, Criterion V which requires that procedures

be implemented

(VIO 50-397)97016-03).

~

On July 21, 1997 the containment hydrogen monitor (CMS-SR-14) failed and

was declared inoperable.

The hydrogen monitor is described

as

safety-related

in the Final Safety Analysis Report.

The failure to initiate a

PER for the inoperable hydrogen monitor is another example of a violation of

10 CFR Part 50, Appendix B, Criterion V (VIO 50-397/97016-03).

~

On July 23, during the RFW pump trip test, the reactor vessel level control

system unexpectedly tripped to single element control.

Adjustable Speed Drive 1B1, gate turn-off problems were noted on July 8,

10, and 15.

(The gate turn-offs are solid state devices that convert DC

current to an AC signal to drive the RRC pumps.)

On July 21, the low pressure

core spray keepfill pump bearing oil resevoir

was empty.

This was unexpected

because

the oil reservoirs

are verified to be

at least half full twice a day and the bearings do not normally use a

significant amount of oil. Additionally, keepfill pump bearings have suffered

repetitive problems at WNP-2. Most recently, on October 16, 1996, the

bearing associated

with the RHR-P-3 keepfill pump failed and rendered

residual heat removal Train C inoperable.

Off-gas explosive monitors were found to be inoperable

on July 21, 28, and

30.

On July 28, a coupling associated

with control rod drive Pump 1A was found

in a damaged

condition.

Compensatory

steps were established

to prevent

pump failure, but no PER was written.

For the above examples, the inspector discussed

the issues with the cognizant

engineers.

The inspector observed that in all cases the engineers

were generally

aware of the issues, but did not have a proper understanding

of PER requirements.

One engineer stated that he was only required to write a PER if the system failure

resulted in a plant power reduction.

Another stated that he did not believe that the

failure of the safety-related

containment hydrogen monitor warranted

a PER.

None

of the engineers

had used the PER procedure when deciding whether or not to write

a PER.

-9-

C.

Conclusions

PERs were appropriately written in the majority of instances when they were

required.

However, one violation of procedures,

with two examples, was identified

for the failure to write PERs for safety-related

component

problems.

Several other

examples were also identified where PERs were not generated

for nonsafety-related

equipment problems.

Some engineers

did not have an appropriate understanding

of

PER requirements

and were not using the applicable procedure.

IV. Plant Su

ort

R1

Radiological Protection and Chemistry Controls

R1.1

Inade

uate Job Plannin

for Establishin

Radiolo ical Controls

a.

Ins ection Sco

e 71750

The inspectors reviewed the circumstances

surrounding

several recent plant

activities that resulted in unplanned

contaminations

and exposures

to personnel.

The review included the planning aspects

of the activities and the actions taken in

response

to the events.

10 CFR 20.1501 requires that surveys be made to evaluate the extent of radiation

levels and the potential radiological hazards that could be present to ensure

compliance with the requirements of 10 CFR Part 20.

10 CFR 20.1902 requires the

posting as a high radiation area if areas accessible

to personnel for radiation areas

greater than 0.1 rem/hr at 30 cm.

10 CFR 20.21201

specifies limits for

occupational

exposures.

b.

Observations

and Findin s

Inadequate Area Posting:

On July 29, 1997, two contract workers were working in

the pit area of condensate

Filter/Demineralizer 1B, posted only as a radiation area.

During their work they received dose rate alarms on their electronic dosimetry

(indicating a dose rate ) 50 mr/hr) and exited the area.

Subsequent

surveys of the

pit area found general area radiation levels up to 150 mr/hr. As a result of the

workers'rompt action the dose they received was relatively low (9 mrem total).

Prior to the workers entering the pit area, the filter/demineralizer had been returned

to service following planned maintenance

performed several days before.

However,

neither the workers nor the HP technicians who granted them access to the area

recognized that there had been

a change

in plant conditions.

This resulted in the

workers performing work under an inappropriate radiation work permit (RWP).

Had

-10-

it been recognized that the area was, in fact, a high radiation area, additional

reviews of the activity would have been required to determine the appropriate

level

of radiological controls.

The root cause of this event appeared

to be poor communications

between

operations

and HP personnel with regards to changes

in plant conditions.

Additionally, HP personnel

did not demonstrate

the appropriate sensitivity towards

the need to verify that radiological conditions had not changed

prior to granting

access to the condensate

filter/demineralizer pit. The failure to survey the pit area

to evaluate the extent of radiation levels is the first example of a violation of

10 CFR 20.1501(a)(2)(iii) (VIO 50-397/97016-04).

Significant Personnel Contamination During Nonroutine Surveillance:

On

September 4, 1997, an EO was contaminated

while performing a manual

determination of identified RCS leakage into the drywell ~ A subsequent

whole body

count also showed an uptake of a small amount of Cobalt-60 (approximately

30 nCi).

Identified leakage into the drywell is collected by the equipment drain radioactive

system and directed to the EDR sump located on 422'evel of the reactor building.

Radioactive contamination

in the EDR system has resulted in the EDR sump area to

be posted

as a contaminated

high radiation area.

The EO was required to enter this

area to perform the manual leakage determination.

Although the activity was a nonroutine surveillance being performed in an area that

is not normally entered, the EO performed the work under a Group RWP for routine

equipment operation in high and high-high radiation areas.

The RWP did not provide

any specific information on the radiological hazards

around the EDR sump and so

required the HP prejob brief to include a review of the most recent surveys of the

area.

The most recent survey available for the EDR sump was performed in

May 1997 and indicated contamination levels between 20,000 and

150,000 dpm/100 cm~.

The RWP also required catch containers when breaching

contaminated

liquid systems unless the liquid is directed to an approved drain

system.

The RWP did not provide any requirements for the type of catch container

or drain system that would be acceptable.

The use of an open polyethylene bottle

to collect the EDR flow was an ineffective catch container and a key contributor in

the EO's contamination.

Contamination on the EO's hands can also be attributed to

the removal of his protective gloves to read his dosimetry while in the contaminated

area.

HP surveys performed following the contamination event showed

contamination

levels between 80,000 and 4,000,000 dpm/100 cm~ in the EDR

sump area. The EO's egress from the area also resulted in spread of contamination

outside of the posted area.

HP personnel decontaminated

the affected areas

reducing levels around the EDR sump to (80,000 dpm/100 cm'.

The inspector considered

the root cause of this event to be poor radiological work

planning and practices

in relation to the potential radiological risks.

Additionally, HP

0

-11-

personnel

were not sensitive to the need to verify the radiological conditions around

the EDR sump prior to entry into the area by the EO. The failure to perform surveys

to evaluate the potential radiological hazards prior to the EO performing the

surveillance

is the second example of a violation of 10 CFR 20.1501(a)(2)(iii)

(VIO 50-397/9701 6-04).

Second Personnel Contamination in EDR Sump Area:

During the evening of

September

4, 1997,

a second

EO entered the EDR'sump area to perform another

manual determination of drywell identified leakage.

HP personnel,

believing the

contamination of the first EO was due to poor work practices, accompanied

the

second

EO to the job site, but did not require any additional radiological controls.

In

fact, the EO utilized the same Group RWP used by the first operator earlier that day.

The HP technician accompanying

the EO did not identify any concerns with the

EO's radiological work practices.

However, upon exiting the area the second

EO

was also found to be contaminated.

A subsequent

whole body count also showed

an uptake of Cobalt-60 at a similar level to that of the first EO.

The root cause of the contamination appeared

to be from the significant

contamination

levels in the EDR system.

Based upon whole body counts performed

on each of the EOs, the licensee believed that the contamination

levels generated

airborne activity when the system was breached

and drained into the open bottle.

The erroneous

assumption

on the part of HP personnel that the initial contamination

was due only to poor radiological work practices prevented

them from appropriately

considering the radiological risks involved with breaching the system and taking

action to minimize that risk.

Following the second contamination event, HP personnel

again decontaminated

the

EDR sump area.

Additional engineered

and personnel

radiological controls were

established

under a specific RWP approved

by the radiation protection manager.

Subsequent

entries into the EDR sump area by EOs showed that the additional

controls were effective in minimizing the potential for personnel contamination.

Inadequate Surveys Resulted in Unplanned Personnel Contaminations:

On

September

11, 1997, four individuals were found to have low levels of

contamination (1000 - 8000 dpm/100 cm') after performing work on control rod

drive hydraulic Pump 1A. Subsequent

surveys by HP personnel found

contamination around the pump motor couplings and gear box.

These components

were not identified as potentially contaminated

prior to the job and no prejob

surveys had been performed.

From discussions

with the radiation protection manager it was iden.ified that the HP

supervisor was aware of the impending job, but directions to an HP technician to

evaluate the job site was not adequately

communicated.

Thus, no direct HP

coverage

was provided during the work. It was also identified that two of the

maintenance

personnel

involved with the job were qualified to perform

contamination surveys.

-1 2-

The root cause of this event was a lack of sensitivity on the part of both

maintenance

and HP personnel for the need to verify radiological conditions before

starting the work. The failure to survey the work area is the third example of a

violation of 10 CFR 20.1501(a)(2)(iii) (VIO 50-397/97016-04).

Conclusions

The failure to recognize and address

potential radiological concerns associated

with

several work activities resulted in unplanned

personnel contaminations

and

exposures.

In the event involving the surveillance tests in the EDR sump area, HP and

operations

personnel

did not properly address

the source of the contamination

and,

as a result, a second

EO was contaminated.

V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented, the inspection results to members of licensee management

after

the conclusion of the inspection on October 2, 1997.

The licensee acknowledged

the

findings presented.

The inspectors

asked the licensee whether any materials examined during the inspection

should be considered

proprietary.

No proprietary information was identified.

ATTACHMENT

Supplemental

Information

PARTIAL LIST OF PERSONS CONTACTED

Licensee

P. Bemis, Vice President for Nuclear Operations

D. Coleman, Acting Regulatory Affairs Manager

D. Hillyer, Radiation Protection Manager

J. Hunter, ALARASupervisor

P. Inserra, Licensing Manager

T. Messersmith,

Corporate Emergency Preparedness,

Safety and Health Officer

M. Monopoli, Operations Manager

G. Smith, Plant General Manager

J. Swailes, Engineering

Manager

R. Webring, Vice President Operations Support

INSPECTION PROCEDURES USED

IP 37551:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 92901:

IP 92902:

IP 92903:

Onsite Engineering

Surveillance Observations

Maintenance

Observations

Plant Operations

Plant Support

Followup - Operations

Followup - Maintenance

Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

~Oened

50-397/9701 6-01

VIO

failure to perform TS in a timely manner required surveillance

for identified leakage

50-397/9701 6-02

VIO

inadequate

corrective actions related to improperly adjusted

CIA valve for ADS valves

50-397/97016-03

VIO

failure to write PERs when required

50-397/97016-04

VIO

failure to perform radiological surveys

-2-

Closed

50-397/97008-00

LER

inoperability of four ADS valves due to CIA-PCV-28 pressure

setpoint discovered set less than required

50-397/97003-03

URI

inoperable reactor water cleanup isolation instruments

50-397/96017-01

URI

deferral of reactor feedwater pump trip test

50-397/96024-03

URI

failure to write PERs

50-397/95020-01

VIO

inappropriate qualitative/quantitative

acceptance

criter for

control rod drive housing support installation (closed as

50-397/95020-02

in IR 50-397/97-12}

Discussed

50-397/97009-02

IFI

50-397/95020-02

VIO

implementation of the FMC Program

(reopened

due to erroneous

closure in Inspection

Report 50-397/97-12}

LIST OF ACRONYMS USED

ADS

CIA

EDR

EO

FMC

HP

IFI

LER

NRC

PER

PPM

RFW

RRC

RWP

SR

TS

URI

VIO

WNP-2

automatic depressurization

system

containment instrument air

equipment drains radioactive

equipment operator

foreign material control

health physics

inspection followup item

licensee event report

U.S. Nuclear Regulatory Commission

problem evaluation request

Plant Procedures

Manual

reactor feedwater

reactor recirculation control

radiation work permit

surveillance requirements

Technical Specifications

unresolved item

violation

Washington Nuclear Project-2