ML17292B041

From kanterella
Jump to navigation Jump to search
Insp Rept 50-397/97-10 on 970511-0730.No Violations Noted. Major Areas Inspected:Operations & Engineering
ML17292B041
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 09/02/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17292B039 List:
References
50-397-97-10, NUDOCS 9709050119
Download: ML17292B041 (60)


See also: IR 05000397/1997010

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

License No.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Team Leader:

Inspectors:

Accompanying

Personnel:

Approved By:

50-397

NPF-21

50-397/97-1 0

Washington Public Power Supply System

Washington Nuclear Project-2

3000 George Washington Way

Richland, Washington

May 11 through July 30, 1997

W. B. Jones,

Senior Reactor Analyst

P. Gage, Maintenance

Branch

C. Paulk, Maintenance

Branch

.J

~ March-Lueba, Senior Staff Analyst, Oak Ridge National Labs

J. Stewart, Nuclear Reactor Regulation, Senior Electrical Engineer

Dale Powers, Chief Maintenance

Branch

Division Reactor Safety

ATTACHMENTS:

1.

Supplemental

Information

2.

Letter, Licensee Response

to Supplemental

Questions dated June 25, 1997

(G02-97-1 31 )

9709050ii9 970902

PDR

ADQCK 050003'P7

6

PDR

TABLE OF CONTENTS

EXECUTIVE SUMMARY

Report Details

I. Operations

.

01

Conduct of Operations ~...................

01.1

Planned Reactor Feedwater

Pump Trip Test

04

Operator Knowledge and Performance.........................

5

04.1

Operator Performance

and Procedure

Implementation .....

~ ..

~

5

III. Engineering

E1

Conduct of Engineering

E1.1

Reactor Stability Perspective:

Entry Into Region A .........

E1.2

Review of Engineering Analysis in Support of Adjustable Speed

Drive Modification

E1.3

Integrated Plant Testing of Adjustable Speed

Drive and Digital

Feedwater

Level Control System......................

6

6

12

E7

Quality Assurance'in

Engineering

E7.1

Licensee Root-Cause

Investigation, Followup Activities, and

Corrective Actions...

~ ~.........

~

~ ~...

15

15

E8

Miscellaneous

Engineering

Issues

E8.1

Control Rod Position Indications

20

20

IV. Management

Meetings

22

X1

Public Meeting and Exit Meeting Summary....

~

~

~

~

~

~

~

~

~

~

~

~

22

EXECUTIVE SUMMARY

Washington Nuclear Project-2

NRC Inspection Report 50-397/97-10

This special team inspection reviewed the causes,

circumstances,

and corrective actions

associated

with the March 27, 1997, reactor recirculation system runback to minimum

speed

and the subsequent

digital feedwater system response

following the manual reactor

trip.

In addition, co .trol rod position indication concerns were reviewed.

~Qerarinna

r

The team identified a strength

in the overall operator preparations for the planned

reactor feedwater pump trip test, their response

to the unexpected

reactor

recirculation system flow runback to minimum speed

and apparent entry into the

power-to-flow instability region (Region A). The pretest briefing and subsequent

follow through of identified contingency actions were well implemented.

The plant response

to the planned feedwater trip was consistent with the as-built

differential temperature

cavitation interlock design.

Plant operation near Region A

did not result in power oscillations and core stability was maintained prior to and

following the manual reactor scram.

The digital feedwater response

to the reactor scram was consistent with previous

plant performance; however, the digital feedwater level control system design

changes

were not effective in preventing

a post-scram

Level 8 (high level)

feedwater pump trip without operator intervention.

~En ineerin

Safety and nonsafety-related

modifications resulted in an unexpected

plant transient

response

and operation at or near the area of power-to-flow instability region.

The

integrated effect of the digital feedwater level control system, adjustable

speed

drive, and power-up rate modifications were not considered

as they related to the

reactor recirculation cavitation interlock protection setpoint.

The resulting

recirculation system operating characteristics

and differential temperature

cavitation

interlock logic changes effectively reduced the margin to actuate the differential

temperature. cavitation interlock.

The engineering

analysis tools (REDY and RETRAN) were adequate

to predict the

integrated plant response

to the feedwater pump trip test; however, the licensee

failed to consider the recirculation differential temperature

cavitation interlock during

their analysis.

~

Two violations were identified involving failures to appropriately incorporate

recirculation system design information.

The first violation involved the failure to

incorporate the power-up rate modification analyzed recirculation differential

temperature

cavitation interlock temperature

setpoint into the plant.

The second

violation involved two examples where the recirculation system design basis was

not adequately

established

to support 10 CFR'50.59 unreviewed safety question

determinations.

~

The post-modification and power-ascension

testing performed prior to the March 27

loss of feedwater pump trip test provided appropriate

loop verification of adjustable

speed drive and digital feedwater level control system control functions and

sufficient overlap of the control systems.

~

The licensee's

approved procedure, for safety and nonsafety-related

software control

applications did not provide, or reference software quality controls for safety-related

software development

and management.

This procedure was determined not to

have been utilized for any safety-related

applications.

The initial event evaluation team and independent

evaluation team activities did not

provide the assurance

that the event and corrective actions were well understood

or

that the bases for the recommendations

were well supported

by analyses.

However, the subsequent

event evaluation team and independent

evaluation team

activities, reviewed by the NRC team, provided

a thorough understanding

of the

event and the conditions leading to it, as well as, establishing the root cause

and

the recommended

comprehensive

corrective actions.

The event evaluation team and independent

evaluation team plant restart issues

were appropriately identified and resolved prior to reactor criticality following the

refueling outage.

The integrated adjustable

speed drive and digital feedwater level

control system testing demonstrated

the plant operating setpoints

had been properly

implemented.

The additional analyses

provided the assurance

that the integrated

power-up rate, adjustable

speed drive and digital feedwater level control system

operational characteristics

(including tiansient response)

were well understood.

~

The licensee's

review of the'digital feedwater system performance

and control rod

indication problems were appropriately focused.

Re ort Details

Summar

of Plant Status

The reactor was manually scrammed

by the operators

on March 27, 1997, as a result of

unexpected

reactor recirculation pump runbacks to minimum speed

(15 hertz).

The reactor

had been operating at approximately 96 percent thermal power at the 96 percent control

rod line. A planned reactor feedwater pump trip test was initiated which resulted in a

recirculation pump runback to 27 hertz; however,

a second runback to 15 hertz occurred

when the recirculation system differential temperature

cavitation interlock actuated

on a

low differential temperature

sensed

between the recirculation loops and the steam dome.

The operators initiated a manual reactor scram because

of the apparent plant entry into the

instability region (Region A) on the power-to-flow map.'he digital feedwater system

subsequently

failed to control reactor vessel below Level 8 and a reactor feedwater pump

turbine trip occurred.

The unit was placed in cold shutdown for a maintenance

outage and

subsequently

entered Refueling Outage

12.

On July 23, with the unit at 99 percent thermal power, the reactor feedwater pump trip

test was performed successfully.

The recirculation system runback was as expected

and

the digital feedwater level control system maintained reactor water level above the low

water level scram setpoint.

I. 0 erations

01

Conduct of Operations

01.1

Pianned Reactor Feedwater

Pum

Tri Test

On March 27, 1997, at approximately 9 a.m. PST, the plant operators initiated a

planned feedwater pump trip with the reactor at 96 percent power.

During this

power ascension

test, an unexpected

reactor recirculation pump runback to 15 hertz

occurred.

The expected plant response

was for the reactor recirculation pumps to

runback to 27 hertz on the loss of a reactor feedwater pump coincident with reactor

vessel Level 4. However, a second runback to 15 hertz occurred when the reactor

recirculation differential temperature

cavitation interlock actuated.

The adjustable

speed drive system was designed to run the recirculation pumps

back to a slower speed on selected transients

and abnormal events.

These trips

and runbacks were to be equivalent to those provided by the replaced flow control

system and would maintain the same level of protection as the flow control system

for the scenarios

identified in the adjustable

speed drive safety evaluation report

(GI2-96-137), dated June 3, 1996, Table 1. This same level of protection was

provided through the adjustable

speed drive automatic actions.

Specifically, on a

sensed

condition of one feedwater pump tripped and reactor water level less than or

equal to +31.5 inches (Level 4) the adjustable

speed drive would run the pumps

back to 45 percent (27 Hertz), which was approximately 48 percent core flow.

A manual reactor scram was initiated when the operators conservatively concluded

that the reactor was operating in the instability Region A. Subsequently,

reactor

feedwater Pump A overfed the reactor vessel resulting in a Lev'el 8 feedwater

isolation.

The event chronology

is provided below.

8:30:00

Control room supervisor provide'd pre-job brief for reactor feedwater

pump trip (TC-6) in accordance

with Procedure 8.3.339, "Test

Instructions-Reactor

Recirculation Adjustable Speed

Drive and Reactor

Digital Feedwater

Control Ascension Test Program Power Ascension

Test," Revision 3.

9:04:53

r

The operators manually tripped reactor feedwater pump Turbine B in

accordance

with power ascension

Procedure 8.8.339.

9:05:03

Runback of reactor recirculation system to 27 hertz began

(Level 4

coincident with reactor feed pump trip) ~

9:05:29

Runback to 15 hertz began on actuation of reactor recirculation

system differential temperature

cavitation interlock (9.9'F as

measured

between the recirculation suction loops and the steam

dome pressure

converted to temperature

for a period equal to or

greater than 15 seconds)

~

9:07:28

Operators evaluated

apparent entry into Region A of the power-to-

flow map using abnormal operating Procedure 4.12.4.7,

"Unintentional Entry into Region of Potential Core Power Instabilities,"

Revision 14, for both the reactor recirculation pumps having ramped

down to 15 hertz.

Immediate operator action was taken for being in

Region A and a manual scram initiated (apparent entry into Region A).

9:07:29

Reactor vessel water level was at 44 inches narrow range and

indicated level decreasing

from void collapse (actual reactor vessel

water inventory was beginning to increase with increasing feedwater

flow).

9:07:32

Reactor feedwater Pump A governor valve opened consistent with

master level controller output.

A governor valve servo surge was

experienced

as the demand on the feedwater pump turbine hydraulic

control exceeded

the response

capability.

This resulted in a step

change

(close) in governor valve position and a momentary decrease

in the feedwater flow rate before the feedwater system recovered

and

continued to increase feedwater flow.

9:07:43

Reactor feedwater Pump A experienced

a second governor valve

servo surge resulting in a momentary decrease

in the feedwater flow.

Reactor vessel water inventory and indicated level were increasing.

9:08:35

Feedwater master level controller output zero; however, feedwater

9:08:40

9:08:41

9:36:00

pump turbine governor valve remained full open.

Reactor feedwater Turbine A governor valve started to close.

Reactor feedwater Turbine A tripped on reactor high level (Level 8)

4

Operators restarted reactor feedwater Pump A for reactor 'vessel level

control.

01.1.1

Plant Performance

Associated with the Event

a.

Ins ection Sco

e 93702

The team reviewed the expected

plant response

and the observed

plant response

to

the planned loss of feedwater pump trip test.

The plant initial conditions, feedwater

system performance,

and reactor recirculation system runbacks were considered.

b.

Observations

and Findin s

Significant modifications were made to the reactor recirculation and reactor

feedwater systems during the 1996 refueling outage.

The analog feedwater level

control system was replaced by a digital feedwater level control system and the

reactor recirculation loop flow control valves were replaced with reactor

recirculation pump motor adjustable

speed drives.

In 1994 the licensee had

implemented

a power-up rate to the plant which increased the megawatt

thermal (MWt) output of the reactor to 3486 MWt (a 163 MWt increase).

A power ascension

test program was developed to validate the adjustable speed

drive and digital feedwater level control system responses

and ensure the initial

power ascension

program acceptance

criteria would be met.

The power ascension

test report, dated December 31, 1996, concluded that the plant responses

were at

least equal to those obtained

in the original WNP-2 startup test and that the new

adjustable

speed drive and digital feedwater level control systems met all required

transient performance acceptance

criteria.

However, this did not include

performance of a reactor feedwater pump trip. The licensee had performed

a

review of adjustable

speed drive preoperational test results and ran the computer

code RETRAN to predict the plant response.

The analysis showed that the Level 3

low vessel water trip setpoint would not be reached.

On March 27, 1997, the licensee performed the reactor feedwater pump trip test to

verify the integrated effects of these modifications.

The test was intended to

demonstrate

the capability of the reactor recirculation and feedwater systems to

withstand a trip of one reactor feedwater pump from approximately 100 percent

power without a scram on a low reactor water level condition, as described

in Final

Safety Analysis Report Section H.2.3.3.2.2.

However, during the test, the

recirculation system differential temperature

cavitation interlock actuated,

resulting

in an unanticipated

runback of the adjustable

speed drive output to 15 hertz instead

of the expected

27 hertz.

The second runback of the recirculation pumps resulted

in reactor operation near Region A of the power-to-flow map.

The operators

determined that the reactor was operating

in Region A and initiated a manual reactor scram in accordance

with the Technical Specifications

and abnormal

operating Procedure 4.12.4.7.

This event was of concern because

this transient

resulted in apparent reactor operation in an area which could lead to reactor core

instability.

Subsequently,

the reactor feedwater Pump A tripped when the reactor

vessel Level 8 setpoint was reached.

The team reviewed the digital feedwater level control system response

following the

feedwater pump trip test conducted

during power ascension

testing.

The team

determined that the digital feedwater level control system response

was normal

prior to, and shortly, after ti>e manual scram was initiated by the plant operators to

prevent operation beyond the area of increased

awareness

on the power-to-flow

map.

The team noted that the reactor water level decreased

to a minimum value of

approximately 23 inches and had recovered to about 30 inches when the reactor

recirculation differential temperature

cavitation interlock initiated the second reactor

recirculation system runback.

This interlock was designed to provide jet pump

cavitation protection during transient plant conditions by ensuring

a minimum 9.9'F

differential temperature

was,maintained

between the recirculation loops and steam

dome temperature

(as measured

by steam dome pressure

and converted to

saturation temperature).

This condition had to exist for a minimum of 15 seconds

before the differential temperature

cavitation interlock would actuate.

Following the

differential temperature

cavitation interlock runback, reactor water level increased to

a maximum value of about 51 inches and was decreasing

when the manual scram

was initiated.

Immediately after the manual scram, the digital feedwater level control system

master controller output dropped sharply to zero, indicating the level controller

setpoint setdown to 18 inches narrow range had initiated.

The operating narrow

range level setpoint was 36 inches.

The team observed that the digital feedwater

level control system signals, reactor feedwater pump speed response,

and reactor

water level response

operated

as designed

until approximately

11 seconds

before a

Level 8 high reactor water level trip occurred.

The failure of the feedwater pump

turbine governor valve to begin closing when the master controller output signal

decreased

resulted in a significant amount of feedwater being supplied to the

reactor vessel following the scram.

The team determined that the reactor feedwater pump turbine governor valve

should have been closing based on the master controller output demanding

less

feedwater flow for the'corresponding

increasing reactor vessel level and associated

turbine feedwater pump speed.

The team noted that the governor valve position

started to close about 2 seconds

prior to the high level trip of the operating reactor

feedwater pump.

The licensee identified that there were no indications of any

communication interruptions between the FANUC (GE programmable

hardware

system) controller and the Lovejoy (digital feedwater level control system

manufacturer) controller during the event, and there was no time delay in the level

control system regarding governor valve response.

The licensee determined that

the probable cause for the governor valve staying open was sticking of the governor

servo pilot valve and the servo surges may have resulted in excessive travel of the

governor pilot valve.

The licensee subsequently

determined through analysis, including RETRAN

simulations, that the additional period the governor valve remained full open did not,

in itself, result in the Level 8 feedwater trip. The licensee's

analysis showed that

the digital feedwater level control system was not capable of preventing

a Level 8

high level trip following a reactor scram without operator intervention.

Based on a

review of the licensee's probabilistic risk assessment

and human recovery actions,

the team found that the operator action to recover feedwater following a scram was

risk important.

The team also reviewed the operational history for WNP-2 to determine whether any

instances

had occurred where the differential temperature

cavitation interlock had

initiated during feedwater transients.

No previous instances were identified where

the loss-of-single feedwater pump or other feedwater transient resulted in the

differential temperature

cavitation interlock being met.

c.

Conclusions

The observed plant response

to the planned feedwater pump trip was consistent

with the as-built plant.

The recirculation system differential temperature

cavitation

interlock actuated

in accordance

with the established

cavitation interlock setpoints.

The digital feedwater level control system responded

appropriately to the loss of a

single feedwater pump.

The failure of the digital feedwater level control system to

maintain reactor vessel water level below Level 8 following the reactor scram was

limited by the digital feedwater level control system response

characteristics

and

tuning and apparently not the result of the delayed governor pilot valve response.

04

Operator Knowledge and Performance

04.1

0 erator Performance

and Procedure

Im lementation

a.

Ins ection Sco

e

93701

The team reviewed:

(1) the test, operating,

and abnormal procedures

applicable to

the event; (2) operator preparations for the test, including simulator exercises

and

pretest briefings; and, (3) the operators'esponse

during the event.

b.

Observations

and Findin s

The licensee established

the planned feedwater pump trip test controls in

Procedure 8.3.339, "Test Instructions-Reactor

Recirculation Adjustable Speed Drive

and Reactor Digital Feedwater Control Power Ascension Program," Section 8.16,

"Reactor Feedwater

Pump Trip (TC-6)." The plant initial conditions were

established

consistent with the test instructions and ANNA (core monitoring) was

operable

in accordance

with Procedure 7.4.2.7.2, "Stability Monitoring System."

h

The operating crew that performed the test had participated

in simulator exercises

prior to performing the test involving the loss of a feedwater pump.

A detailed plant

recovery action was established

to maintain the reactor away from th

t b'I'

ins a iity

g'

is included specific control rod insertions and ad'ustabl

d d

'ani

ulations

o

jus a

e spec

rive

Region A. The lice

'p

to maintain the power-to-flow relationship awa

f

th

y rom

e instability

e icensee

had identified that during the initial transient, with the

recirculation pump runbacks to 27 hertz that the

I

t

ld b

p an

wou

e operating near

adequate

mar in to r

egion A; however, the recirculation pump runbacks to 2? he

o

ertz would provide

a equate margin to recover the plant.

The observed

simulator response.

did not

model that the recirculation s ystem differential temperature cavitation interlock

would actuate

and ca

cause

an additional recirculation pump runback to 15 hertz.

Prior to conductin

the

sheet (Ol-22

Rev

g

e test the licensee performed

a pre-evolution

b

f

h

k- ff

rie

c ec -o

, Revision B) for power ascension

test Procedure 8.3.339.

The

operators

again reviewed the established

plan for control rod mani ula io

ro

manipu ations and to

a ion

ow to prevent entry into the area of increased

awareness.

his prebriefing also included the contingency actions that would be taken if th

gi n

.

t was established

that the plant would be immediatel

e aenite

scrammed

on verifying Region A had been entered.

imme )ate y

During the performance of the test, the operators observed

a second,

unexpected

runback of the recirculation pumps.

Procedure 4.12.4.7

"U

ure...,

nintentional Entry into

egion o Potential Core Power Instabilities," was entered for both

had been entered

ba

g

pe

own to 15 hertz.

The operators determined th t R

'

a

egion

and the C cle 12

based

on main control board indications

core fl

f

ow re erences,

bein

in Re io

yc e 12 power-to-flow map.

Immediate operator

a t

c ion wasta

en

or

k

f

'

egion A and the reactor was manually scrammed.

Sub

taken to restore the reactor feedw

e

.

u sequent

action was

Level 8 high level trip.

e reactor

ee water Pump A to control vessel level following the

C.

Conclusions

The o erators w

pum

tri test a

p

tors were involved in extensive preparations

for the

I

d f

or

e p anne

eedwater

and Technical S

p

ip es

and had established

contingency actions consist

t

h

d

is en wit

proce

ural

re aratio

i a

pecification requirements.

A strength was not d 'h

s no e

in t e operators

egion

o the power-to-flow

p

p

'ons and response to the apparent entry into Re

'

f

III. En ineerin

E1

Conduct of Engineering

E1.1

Reactor Stabilit

Pers

ective:

Entr

Into Re ion A

a.

Ins ection Sco

e

93703

The

stabilit

he team reviewed the reactor physics, thermal-h

d

I

d

- y rau ics, an

reactor core

sta

i ity concerns with the apparent reactor operation in the instability region.

Observations

and Findin s

Region A was defined as an area on the WNP-2 core operating'imits report power-

to-flow map where the potential for unstable power oscillations cannot be ruled out

by analysis.

A manual reactor. scram was required by the Technical Specifications

and the licensee's

abnormal procedure

when entry into Region A occurs.

The licensee's

core operating limits report for Cycle 1.2 defined Region A as the area

bounded

by tl

100 percerit control rod line at 40 percent rated flow (59.1 percent

power) and the natural circulation line at 23.8 percent flow (35.3 percent power).

The team noted that the recirculation pump runback to 15 hertz resulted

in a total

core flow reduction to 37 percent flow. Based on the licensee's power-to-flow

map, the recirculation pumps running back to 15 hertz runback would result in a

flow less than 40 percent and entry in Region A with the plant operating from a

high rod line. The licensee subsequently

determined that Region A was not entered

when the recirculation pumps ranback to 15 hertz.

A review of the plant data by

the licensee and independently

by the team showed that the actual reactor power

level was 2 percent below the Region A boundary and slowly increasing prior to the

manual scram.

The team reviewed the licensee's

implementation of the "Stability Interim Corrective

Actions." The Boiling Water Reactor Owners Group interim corrective actions

define:

(1) Region A where a manual scram is required; (2) Regions

B and C, where

intentional entry is not allowed and

a prompt exit is required by control rod insertion

or flow maneuvering;

and (3) the area of increased

awareness,

where intentional

entry is only allowed if stability monitoring is functional.

The team concluded that

the interim corrective action implementation and operator training relating interim

corrective action procedures

were appropriately implemented.

The licensee identified that it had chosen "Stability Long Term Solution," Enhanced

Option 1-A (E1A), with plans to perform the initial testing of the flow control trip

reference cards in 1998 and full implementation

in 1999.

The team noted that the

E1A exclusion region would likely have resulted

in an automatic scram for.a similar

15 hertz runback at a high rod line.

The team reviewed three conditions which appeared

to have contributed to the

operators'etermination

that Region A had been entered.

These conditions were:

(1) the plant operation was near the 100 percent rod line prior to the feedwater

pump trip; (2) the core was at the end of life and the void reactivity coefficient was

estimated to be lower than average resulting in the actual flow-control rod line

having a steeper slope than the average

rod line used to define the stability regions;

and, (3) the reactor was scrammed

before full feedwater temperature

equilibrium

was reached

(i.e., the power was still increasing slowly) ~

The team reviewed the stability calculations performed using the licensed

frequency-domain

Code STAIF for the operating conditions reached just before the

scram.

These calculations indicated that the core decay ratio was 0.51, the out-of-

phase decay ratio ($ 1.038 subcritical mode) was 0.54, and the hot-channel

decay

ratio (a SVEA bundle with peaking factor of 1.558) was 0.22.

The team found the

STAIF calculations were appropriately utilized and agreed with the licensee's

determination that unstable power oscillations would not have been likely if the

manual scram had not been performed.

A review of the plant data also indicated

that unstable power oscillations did not occur prior to the scram.

Conclusions

The reactor core operating data confirmed that Region A was not entered.,

Although plant conditions were approaching

Region A, the reactor remained stable

and power oscillations were unlikely. The operator actions in this instance were

appropriate to maintain core stability and the scheduled

long-term solution

implementation date was adequate

given the operator's demonstrated

sensitivity to

core instability concerns.

Review of En ineerin

Anal sis in Su

ort of Ad'ustable

S eed Drive Modification

Ins ection Sco

e

92903

The team reviewed the engineering

analysis used, in part, to support the adjustable

speed drive modification.

Comparisons

were performed between the previous

recirculation system flow control valve design and adjustable

speed drive operating

characteristics.

This also included the licensee's activities to integrate the other

significant plant modifications, power-up rate and digital feedwater level control

system initiated during the same period, for plant performance

and transient

response.

Observations

and Findin s

Com arison of Reactor Recirculation

S stem Runback Rates

The team compared the plant test data from the 1984 initial power ascension

feedwater pump trip test to the data obtained from the March 27, 1997, feedwater

pump trip test.

The team calculated that the rates of total core-flow reduction

during a recirculation system runback were approximately 4.2 percent/sec for the

new adjustable

s'peed drive configuration and approximately 11.0 percent/sec

for

the previous recirculation system configuration with flow control valves.

The core-

flow runback rate was approximately 75 percent of the drive flow rate (i.e., a drive-

flow reduction from 100 to 0 percent results in a core-flow reduction from 100 to

24 percent, the natural circulation rate); thus, the team estimated that the

recirculation loop drive-flow runback rates were approximately 5.5 percent/sec

for

the adjustable

speed drive configuration and approximately 14.5 percent/sec

for the

flow control valve configuration.

The team found that the runback rate in the

adjustable

speed drive configuration was approximately 2.5 times slower than in the

flow control valve configuration.

The overall effect of the slower adjustable

speed

drive runback rate was reviewed with the licensee

and assessed

using the

licensee's

RETRAN licensing model code.

1

En ineerin

Anal sis to Determine Im act of Power-u

Rate and Ad'ustable

S eed

Drive Modification on Recirculation S stem Performance

The team reviewed

a number of calculations performed by General Electric with

their licensing Code REDY, and sensitivity analysis performed by the licensee's staff

with their RETRAN licensing model.

The REDY calculations were documented

in

Letter GENE-208-12-0793 ("WNP2 Power Up Rate Supplement for the WNP-2

Control System Design report, Incorporating the Adjustable Speed

Drive Reactor

Recirculation System" ), and the RETRAN calculations were summarized

in internal

licensee memorandums.

The core flow predicted by both of these simulations

compared well with the actual core flow from the March 27 recirculation flow

runback.

The primary purpose of the REDY calculations in Letter GENE-208-12-0793 was to

evaluate the impact of the new power level and control systems

on the reactor

water level following a number of transients.

The analyses

were performed to

demonstrate

analytically that a reactor scram on either low or high vessel level

would not occur, as had been demonstrated

during the initial startup testing

program.

The licensee identified, following the March 27, 1997, test, that the

analysis performed prior to the feedwater pump trip test did not address the

recirculation loop temperatures

and differential temperature

cavitation interlock

margin.

The RETRAN calculations were performed in December 1996 to evaluate the impact

of the different flow runback rates between the adjustable

speed drive and flow

control valve systems.

As with the above REDY calculations, the RETRAN results

were evaluated to determine the impact on water level transient behavior, but

margins to the pump cavitation interlock were not investigated.

Following the

March 27 event, the licensee's staff evaluated the RETRAN-calculated recirculation

loop temperature

and determined that the simulation had predicted the cavitation

interlock but was not recognized prior to the event.

J

The licensee's

event evaluation team identified that the differential temperature

cavitation interlock had been set at 9.9

F in 1984 and that the setpoint had not

been changed to 10.7

F when the power-up rate was implemented

as

recommended

by General Electric.

The team reviewed the basis for the differential

temperature

cavitation setpoint and requested

any analysis which provided for

maintaining the setpoint at 9.9

F. The team was subsequently

provided with

General Electric Letter 94-PU-0013, dated March 18, 1994, which specified, in

part, that the 10.7

F recirculation system differential temperature

cavitation

setpoint was consistent with the analysis in support of the power-up rate project.

The letter stated that, "(s)hould the Supply System request additional analysis

in

support of the 9.9'F setpoint, General Electric will do so as a change notice to the

current power-up rate contract since this constitutes

a change from the agreed upon

power-up rate recirculation system design basis."

The power-up rate modification (Technical Specification Amendment 137) became

effective on May 2, 1995, with the recirculation system cavitation interlock setpoint

established

at 9.9

F.

The team found that the power-up rate design basis was not

correctly translated for the recirculation system differential temperature

cavitation

setpoint following the power-up rate.

The licensee implemented the power-up rate

in May 1995, and operated the plant for two cycles without changing the setpoint,

without performing additional testing, and without additional analyses.

The team

identified this to be a violation of Criterion III, "Design Control," of Appendix B to

10 CFR Part 50 (50-397/9710-01).

The team also considered

the design basis for the 15-second

delay before the

differential temperature

cavitation interlock would actuate.

No specific design basis

was found; however, the licensee's staff believed the delay time was chosen to

avoid spurious pump speed reductions,

based on engineering judgement using

empirical data, and was consistent with similar delay times in other plants.

The team reviewed the written safety evaluation performed to support the

installation of the adjustable

speed drives (Safety Evaluation Control 93-200, dated

July 11, 1995).

The team found that the recirculation system design basis

information used to support development of the safety evaluation was not adequate

to provide the basis that an unreviewed safety question did not exist.

Specifically,

the licensing basis implementing determination for Plant Modification

Request 87-0244 did not provide a comprehensive

review for the design and testing

of the reactor recirculation system adjustable

speed drive.

The licensing basis

impact determination did not identify that the reactor recirculation system cavitation

interlock would actuate during a planned loss of a feedwater pump.

This resulted in

a second recirculation pump runback and reactor operation near the power-to-flow

instability Region A, an area of operation prohibited by Technical Specifications.

This plant response

was not recognized

and reviewed.

The licensee did not

establish

an adequate

design basis for the recirculation system to determine that the

adjustable

speed drive modification did not result in an unreviewed safety question.

The team identified this to be a violation of 10 CFR 50.59

(50-397/9710-02).

The licensee subsequently

performed Safety Evaluation SE 97-078, "Recirculation

Flow Control System Digital Feedwater

Level Control System Feedwater

Pump Trip

Test Followup 10 CFR 50.59 Safety Evaluation," Revision 0. This safety evaluation

provided an integrated review based

on the results observed from the feedwater

pump trip test.

The licensee's safety evaluation appropriately considered

the

differential temperature

cavitation interlock actuation and associated

reactor

recirculation pump runback, plant operation in or near Region A, and the digital

feedwater level control system response.

The licensee determined that the

integrated plant response

did not result in an unreviewed safety question.

10

Prior to the March 27 test, the licensee conducted

operator training using the plant

simulator.

The simulator modeling of the test failed to predict the differential

temperature

cavitation interlock would actuate.

The team reviewed the simulator

calculation and the licensee ran the simulation again during the inspection with the

same results.

The team reviewed the licensee's

evaluation, which attributed the

failure to predict the cavitation, interlock to a 4'F steady state mismatch between

the predicted and measured

recirculation loop temperatures.

Because of this 4'F

mismatch, the 9.9'F cavitation setpoint was not reached

in the simulation.

The

licensee was continuing to evaluate the cause of the 4'F mismatch at the end of the

inspection.

The team agreed with the licensee's

assessment

that the WNP-2

training simulator had not been modeled to validate detailed engineering

analysis.

Contributin

Factors to the Differential Tem erature Cavitation Interlock Actuation

The team found that the differential temperature

cavitation interlock actuation

during the feedwater pump trip test was attributable,

in part, to reactor recirculation

system design changes

resulting from the adjustable

speed drive modification and

power-up rate.

The team identified three factors as contributors to the reduction in

the recirculation differential temperature

cavitation interlock margin:

(1)

The drive flow runback rate was reduced from approximately

15 percent/sec

(using the recirculation flow control valves) to approximately 5 percent/sec

(with the adjustable

speed drive design).

The RETRAN simulation showed

the flow control valves resulted in a faster transient, with the differential

temperature

cavitation interlock actuating for a shorter period of time.

The

RETRAN simulations always indicated

a reduction in the cavitation interlock

margin with the adjustable

speed drive system.

The magnitude of the margin

reduction ranged from 10 percent to 30 percent depending

of the

methodology used for data interpretation.

Similar results using the NRC's

TRAC model were obtaine'd by the team.

(2)

The final drive-flow setpoint following the runback was reduced significantly.

In the flow control valve system, the runback resulted in approximately

60 percent core flow; the adjustable

speed drive system runback to 27 hertz

resulted in approximately 48 percent core flow. This significant reduction in

final core flow resulted in a lower dome pressure,

lower saturation

temperature,

and reduced margin to the differential temperature

cavitation

interlock.

In addition, the power-up rate modification implemented

in 1994

resulted in a higher operating pressure

and suction side recirculation system

operating temperatures,

which also contributed to the reduced margin to the

cavitation interlock actuation.

(3)

The cavitation interlock logic was modified for the adjustable

speed drive

system.

The new logic was more conservative

in actuating the differential

temperature

cavitation interlock because

it selected the lower of the two

measured

saturation temperatures

and the highest of the four measured

recirculation loop temperatures.

The adjustable

speed drive cavitation

interlock logic had the effect of reducing the steady state cavitation margin.

11

c.

Conclusions

The engineering

analysis tools (REDY and RETRAN) were adequate

to predict the

integrated plant response

to the feedwater pump trip test; however, the licensee

failed to consider the recirculation differential temperature

cavitation interlock during

their analysis.

Several recirculation system operating characteristics

were effected

by the design modifications, which resulted in the unexpected

recirculation system

pump runbacks

and plant operation

in or near Region A.

Two violations were identified involving failures to appropriately incorporate

recirculation system design information.

The first violation involved the failure

to incorporate the power-up rate modification analyzed recirculation differential

temperature

cavitation interlock setpoint into the plant.

The second violation

involved the failure to adequately

establish the recirculation system design basis, for

the adjustable

speed drive modification, to determine that an unreviewed safety

question did not exist.

E1.3

Inte rated Plant Testin

of Ad'ustable

S eed Drive and Di ital Feedwater

Level

Control S stem

Ins ection Sco

e 92903

The team reviewed:

the 1996 post-adjustable

speed drive and digital feedwater

level control system modification testing, the power ascension test results and the

1984 power ascension test results; problem evaluation requests

associated

with the

adjustable

speed drive and digital feedwater level control system since their

implementation;

and, internal licensee correspondence.

This included the software

testing associated

with the adjustable

speed drive and digital feedwater level control

system related to reactor recirculation pump differential temperature cavitation

interlock and the reactor feedwater Turbine A governor valve controls.

b.

Observations

and Findin

s

Inte rated ad'ustable

s eed drive and Di ital Feedwater

Level Control S stem

~Testin

The team found the post-modification and power-ascension

testing, performed prior

to the March 27 loss-of-feedwater

pump trip test, provided appropriate

loop

verification of adjustable

speed drive and digital feedwater level control system

control functions and sufficient overlap of the control systems.

The power

ascension test Procedure 8.3.339 encompassed

the Final Safety Analysis Report

requirements

and was consistent with verifying the adjustable

speed drive system

as described

in the safety evaluation by the Office of Nuclear Reactor Regulation

(Amendment 145 for the replacement

of the reactor recirculation flow control

system with an adjustable

speed drive system).

12

A licensee report on the power-ascension

program was developed

in December

1996.

The report found the testing criteria had been met for the adjustable

speed

drive and digital feedwater level control system.

In addition, the report provided

a

basis for delaying the performance

of the feedwater pump trip test.

The team

identified that the written safety evaluation performed to support the deferral of

power ascension

testing (Safety Evaluation Control 96-106, dated December

12,

1996) was not adequate

to provide the basis that an unreviewed safety question

did not exist.

The team found that the recirculation system design basis information

used to support development

of the safety evaluation was not adequate.

As

previously discussed,

the plant response

was not recognized

and reviewed.

The

failure to establish the recirculation system design basis for evaluating the deferral

of the power ascension

test, to provide the 10 CFR 50.59 evaluation basis that an

unreviewed safety question did not exist, was identified by the team as a second

example of Violation 50-397/9710-02.

Inte rated Plant Di ital Feedwater

and Ad'ustable

S eed Drive Software Review

The software associated

with the instrumentation

and controls for the digital

feedwater level control system and the reactor recirculation system performed

as

designed

during the feedwater pump trip test.

The unanticipated

second runback of

the reactor recirculation pump was found to be a design deficiency (unanticipated

differential temperature

interlock actuation) rather than a software implementation

error.

The feedwater pump governor valve software operated correctly during the

test prior to the failure to close upon demand

and no software errors were found

which would have caused the digital feedwater level control system failure.

NRC Inspection Report 50-397/96-07 documented

concerns associated

with the

design and installation of the digital feedwater level control system.

This inspection

found that some of these concerns

had manifested

as problems.

Problem Event

Report 296-0624, pertaining to which processor was to control and which was to

be the backup, and Work Order CXH6, pertaining to cable replacement,

were

generated

to correct problems, which had been previously identified by the vendor

(GE-FANUC). The team identified that no surveys or audits were performed by the

licensee on the GENE design prior to the factory acceptance

test to identify these

types of problems.

The team also determined that the GE-FANUC programmable

controllers were not

registered with GE-FANUC and as such the licensee would not receive any

notifications of errors or design changes.

The team found that the prime contractor

(GENE) had not registered the product and the licensee did not register the product

until operation such that there were several years where error reports or design

changes

were not reported to GENE or the licensee.

The licensee was not aware of

the number or significance of any notifications that may have been issued by

GE-FANUC while they were not registered.

The team reviewed Procedure

1.4.14, "WNP-2 Software Control," Revision 0, used

to maintain software configuration control for the feedwater and recirculation

systems.

Changes

made by the vendors were controlled by the vendor procedures.

13

The team noted that this procedure defined the methods used for the development,

maintenance,

production, use, and retirement of software.

The procedure

was

applicable to both safety- and selected nonsafety-related

systems.

The feedwater

and recirculation systems

(nonsafety-related)

were not specifically identified in the

procedure;

however, the licensee stated that the procedure

was applicable to these

systems.

As a software configuration control document for nonsafety systems,

the

team found that the procedure

had several deficiencies.

The procedure

did not

identify interface controls with vendors and subcontractors

and did not address

security, inspections

and audits, tools, techniques

and methodologies,

o training

documents.

As a safety-related software development

plan, the team found the

proc'edure to be inadequate.

The procedure

did not specify or reference

a software

management

plan, a software development

plan, a software quality assurance

plan,

a software safety plan, verification and validation methodology, training,

programming standards,

hardware/software

integration, installation procedures

or

maintenance.

The team verified that this procedure

had not been used for the

development

or modification of any safety-related

software.

The licensee

representative

stated that they had no plans for doing so.

The team'reviewed

Problem Event Report 296-0625, which included

a "Design

review of adjustable

speed drive and DFW systems" performed in August 1996 and

the event evaluation report, which evaluated the March 27 runback test event.

These reports included many software-related

conclusions

and recommendations.

A

summary table of the actions planned,

as a result of the event evaluation report,

was provided to the team during this evaluation; however, the team noted that

there were many specific recommendations

from the August 1996 report that were

not included in the action plan.

The team found the adjustable

speed drive and digital feedwater level control

system engineers

knowledgeable

about systems software and were proactive about

reviewing changes to the software.

This included detailed interactions with the

equipment suppliers.

Conclusions

The post-modification and power-ascension

testing performed prior to the March 27

loss of feedwater pump trip test provided appropriate

loop verification of adjustable

speed drive and digital feedwater level control system control functions and

sufficient overlap of the control systems.

A second example of a 10 CFR 50.59 violation was identified for the failure to

establish the design basis for the recirculation system in evaluating the deferral of

the power ascension

test and ensure that an unreviewed safety question did not

exist.

14

The licensee had limited involvement in the original design of both the feedwater

and recirculation digital retrofit. Several equipment failures occurred, which may

have been preventable with more active involvement by the licensee during the

original design.

The team concluded that the licensee staff had subsequently

become knowledgeable

about these systems.

I

The deficiencies noted in the software control procedure indicated that software

procedure controls were weak.

The procedure was determined to be inadequate

for

the developmer..

or management

of software for safety-related

applications.

The

licensee had not utilized the software configuration control procedure

on any safety-

related applications.

The design review and the event evaluation reports contain many specific and

programmatic recommendations

that should further enhance

the feedwater and

recirculation systems performance.

E7

Quality Assurance

in Engineering

E7.1

Licensee Root-Cause

Investi ation

Followu

Activities and Corrective Actions

a

~

Ins ection Sco

e

92703

The team reviewed the licensee's

event investigations'performed

by the event

evaluation team and the independent

evaluation team.

This review included

evaluating the depth of the event evaluation team's review, technical basis for the

event evaluation team's recommendations

and findings, and their resolution.

The

independent

evaluation team was reviewed for its independence

and overall scope

of review of the event evaluation team findings and conclusions.

The initial and

supplemental

reports issued by the event evaluation team and independent

evaluation team were reviewed.

The team also followed up on the licensee's

responses

to the additional questions identified during the May 30, 1997, public

meeting regarding the reactor feedwater pump trip test.

b.

Observations

and Findin s

The licensee's April 9, 1997, letter to Mr. E. W. Merschoff defined the scope of the

event evaluation team and independent

evaluation team activities regarding the

March 27, 1997, reactor scram.

On April 3, the licensee committed to provide the

results of the evaluations prior to the plant startup from the spring 1997

maintenance

and refueling outage.

The event evaluation team, composed

principally of licensee personnel were tasked with: evaluating the analytical results

of the testing performed on March 27, 1997; the performance of the onshift

personnel

leading up to, during, and immediately following the manual reactor scram

on March 27; the performance of the adjustable

speed drive and digital feedwater

level control system; the adequacy

of the design integration for installation of the

reactor power-up rate, adjustable

speed drive, and digital feedwater level control

system modifications; and, the adequacy

of the power ascension

test procedure.

The primary assurance

was to be that the licensee had a thorough understanding

of

15

the events surrounding the March 27 test, reactor scram and any needed corrective

actions.

The independent

evaluation team, which was composed

principally of non-

licensee personnel,

was also tasked with providing a critical re'view of the event and

the investigation performed by the event evaluation team.

The team noted that Licensee Event Report 97-004-00, "Technical Specification

Required Manual Scram Due to Entry Into Region A of the Power-to-Flow Map,"

dated April 28, 1997, did not provide a comprehensive

review of the March event.

The licensee event report was issued prior to completion of the event evaluation

team and independent

evaluation team activities.

The license representative

stated

that they intend to provide a revised licensee event report to include the findings

~

from the event evaluation team and independent

evaluation team.

Licensee Event Evaluation Team Activities

The initial event evaluation team report was issued on May 9, 1997, and addressed

each of the items identified in the charter.

Each of the event evaluation team

recommendations

was specifically identified in Problem Evaluation Report 97-0244.

The team found the event evaluation team's findings and recommendations

to be

good.

However, the team was concerned that the event evaluation team had not

evaluated

each of the operating parameters

effected by the power-up rate,

adjustable

speed drive, and digital feedwater modifications.

For example, the team

identified differences in the adjustable

speed drive, and flow control valve runback

rates, which the event evaluation team did not appear to have considered.

In

addition, the design integration of the adjustable

speed drive, power-up rate, and

digital feedwater systems were not comprehensively

addressed.

These issues were

subsequently

reviewed following the licensee's

response

to questions identified

during a May 30, 1997, public meeting with the licensee.

The event evaluation team subsequently

issued an addended

report (Event

Evaluation Team Addendum

1), which provided additional information regarding

additional analyses that were performed during and following the event evaiuation

team activities.

The event evaluation team was able to demonstrate,

qualitatively

and quantitatively, based

on these additional analyses,

the overall cumulative

impact of the adjustable

speed drive, power-up rate, and digital feedwater

modifications on the differential temperature

cavitation interlock margin.

Sensitivity

studies performed on six case descriptions provided

a quantitative assessment

of

the different changes

resulting from the power-up rate, adjustable

speed drive and

digital feedwater modifications.

These cases involved:

final power-to-flow

conditions; flow control valve and adjustable

speed drive runback rates; combined

power-up rate and digital feedwater; and, the effect of the conservative

FANUC trip

logic. The event evaluation team. concluded that, of the case sensitivity reviews

performed, the addition to the conservative

logic and the final condition (power-to-

flow) of the runback provided the largest contributors to reducing the differential

temperature

cavitation interlock margin.

Each of the sensitivity studies showed the

effect of each modification was to decrease

the margin to a differential temperature

cavitation interlock trip. The event evaluation team did not identify any further

recommendations

based

on the additional analyses that were performed.

16

The team noted that the event evaluation team addended

report provided

a

comprehensive

review of the event, which was well supported

by analyses.

The

event evaluation team and the team found that the overall effect of the power-up

rate, adjustable

speed drive, and digital feedwater modifications resulted in a

reduced margin to the differential temperature

cavitation interlock trip.

Inde endent

Evaluation Team Activities

The team was concerned that the independent

evaluation team, as documented

in

the initial report dated

May 9, 1997, concluded,

in part that, "although there was

considerable

agreement

between the independent

evaluation team and event

evaluation team, the independent

evaluation team concluded that the event

evaluation team preliminary report was not acceptable

in its entirety.

The

independent

evaluation team review found the event evaluation team developed

plausible causes

for the event but had not fully validated these causes

by analysis."

Specifically, the independent

evaluation team (based on review of the preliminary

event evaluation team report) found that the event evaluation team report provided

an unconvincing evaluation of the adequacy of the design integration for the

installation of the power-up rate, adjustable

speed drive, and digital feedwater

modifications.

These independent

evaluation team findings did not provide

assurance

that the licensee had

a thorough understanding

of the events surrounding

the March 27, 1997, reactor scram, and developed

the appropriate corrective

actions.

The NRC addressed

the concern that the independent

evaluation team's findings

resulted in not accepting the event evaluation team report in its entirety during the

May 30 public meeting.

The licensee identified that the independent

evaluation

team would perform an additional review of the event evaluation team final report

and provide the results of that review to the team.

On June 20, the independent

evaluation team issued

a report addressing

the independent

evaluation team review

of the event evaluation team report and Addendum

1.

In addition, the independent

evaluation team reviewed the licensee's

response

to the NRC's June 4, 1997, letter

regarding additional questions for the reactor feedwater pump trip test event.

The

independent

evaluation team concluded that final event evaluation team report and

the associated

addendum

adequately

addressed

the independent

evaluation team's

concerns.

The addended

event evaluation team report provided the necessary

analysis to validate the. causes for the event.

The licensee's

planned actions, with

respect to the independent

evaluation team identified startup issues, were found to

adequately

resolve the remaining issues that would prevent plant'startup.

The

independent

evaluation team noted that the original safety evaluations for the

modifications should be reviewed to ensure their continued applicability and ensure

that an unreviewed safety question did not exist.

These actions were completed by

the licensee and reviewed by the team.

No unreviewed safety questions

were

identified.

17

Licensee

Res

onse to Additional Questions

Re ardin

Reactor Feedwater

Pum

Tri

Test and Corrective Actions

The licensee's

response

to the NRC letter dated June 4, 1997, T. P. Gwynn to

J. V. Parrish, "Summary of Meeting with Washington

Public Power Supply System

(WNP-2) on May 30, 1997," appropriately addressed

each of the six items and/or

concerns pertaining to the reactor feedwater pump test.

The specific items

involved:

followup actions planned by the event evaluation team and independent

evaluation team to address

apparent divergent findings or recommendations;

the

licensee's

plans for a thorough review of the integrated engineering

and/or

operational design feature review of the modifications; actions to be taken to

integrate the independent

evaluation team and event evaluation team findings and

recommendations;

an accounting of each independent

evaluation team and event

evaluation team recommendation;

whether an unreviewed safety question existed

because

of the adjustable

speed drive modification; and the licensee's

plans for

performing the reactor feedwater pump trip test.

The NRC raised the above described six items because

of concerns with the event

evaluation team's basis for its conclusions

and recommendations

and the

independent

evaluation team's overall conclusion that the event evaluation team

report could not be accepted

in its entirety.

Prior to the May 30 public meeting, the

team had not been provided with the licensee's

actions to resolve the differences

between the event evaluation team and independent

evaluation team

recommendations

and what additional reviews the independent

evaluation team

would perform to provide assurance

of the completeness

of the event evaluation

team's activities.

The team found that the licensee performed extensive additional efforts to resolve

the independent

evaluation team's concerns.

These efforts were documented

in the

event evaluation team addended

report as discussed

previously.

These additional

efforts were reflected in the licensee's

response

to the six items. The team

reviewed both the event evaluation team addended

report and the independent

evaluation team supplemental

report and found the event evaluation team

appropriately addressed

the independent

evaluation team report concerns

and

validated the causes for the event.

The licensee's

and GENE's engineering

operational design feature reviews did not identify any additional adverse effects on

the operating parameters

with the exception of the differential temperature

cavitation interlock. The licensee's

background information provided to the team

supported this finding.

Integration of the event evaluation team and independent

evaluation team findings

with regard to the adjustable

speed drive and digital feedwater level control system

was accomplished

through the problem evaluation report process.

Additional

RETRAN simulations identified that the digital feedwater level control system had

operated

properly and that the system performance would not prevent a Level 8

high reactor vessel water trip after a scram.

The concerns with the sluggish

feedwater pump turbine governor relay valve operation were addressed

through the

problem evaluation report process.

Corrective maintenance

was performed to clean

18

and polish the relay valves.

Additional tuning of the hydraulic control system was

performed; however, the licensee determined that additional modifications were are

needed to the system to improve the responsiveness

of the governor controller

following a reactor scram.

The team reviewed the licensee's

actions and'proposed

actions for each of the

event evaluation team and independent

evaluation team recommendations.

Each

recommendation

was being addressed

by the licensee through the problem

evaluation report process.

The licensee's safety evaluation to determine whether an

unreviewed safety question existed because

of the adjustable

speed drive

modification was well supported

and the team agreed with the licensee's

determination that an unreviewed safety question did not exist.

However, the team

was concerned

with the incomplete basis provided for Safety Evaluation 97-075

performed to modify the differential temperature

cavitation setpoints.

The licensee

identified changes to the differential temperature

setpoints, differential time delay to

runback, and alarm features.

The team found that the safety evaluation provided to

the plant operating committee was not well supported with regard to the

justification for the setpoint changes.

The increase

in the setpoint to 10.7

F was

based

on a previous General Electric analysis; however, the basis for increasing the

differential time delay to 10 minutes from 15 seconds

was based

on the justification

in a draft General Electric memorandum to the licensee.

The team reviewed the

plant operating committee meeting minutes, dated June 25, 1997, where Safety

Evaluation 97-075 was reviewed.

The team found the plant operating committee

had identified similar concerns with the basis supporting the differential time delay

increase to 10 minutes.

The plant operating committee conducted

extensive

discussions

with the engineering staff and GENE.

The team also discussed

the

basis for the time increase with the engineering staff and GENE.

The team found

-that the jet pump usage factors, fatigue factors and jet pump set screw gap

concerns

had been considered

in the establishing the increased time differential

limit. The safety evaluation was accepted

based

on the supplemental

information

obtained during the plant operating committee meeting to support the. safety

evaluation.

The team found the licensee had appropriately identified the event evaluation team

and independent

evaluation team recommendations,

which were required to be

completed prior to plant restart.

The team verified that each of the restart

recommendations

had been completed.

The feedwater pump trip retest was

successfully. completed on July 23. The adjustable

speed drive system ran the

recirculation pumps back to 30 hertz (revised based

on WNP-2 Cycle 13 power-to-

flow map) and the digital feedwater level control system maintained level between

the low and high reactor vessel level trip setpoints.

Conclusions

The initial event evaluation team and independent

evaluation team activities did not

provide the assurance

that the event and corrective actions were well understood

or

that the bases for the recommendations

were well supported

by analyses.

The

additional event evaluation team and independent

evaluation team activities to

19

provide this assurance

were not undertaken

until after the public meeting on

May 30, 1997, with the NRC. However, the final event evaluation team and

independent

evaluation team activities provided

a thorough understanding

of the

event and the conditions leading to it, as well as, establishing the root cause and

recommending

comprehensive

corrective actions.

The event evaluation team and independent

evaluation team plant restart issues

were appropriately identified and resolved prior to criticality following the refueling

outage.

The integrated adjustable

speed drive and digital feedwater level control

system testing demonstrated

the plant operating setpoints

had been properly

implemented.

The additional analyses

provided the assurance

that the integrated

power-up rate, adjustable

speed drive and digital feedwater level control system

operational characteristics

(in'eluding transient response)

were well understood.

E8

Miscellaneous Engineering Issues

E8.1

Control Rod Position Indications

a.

Ins ection Sco

e 92903

The team reviewed control rod position indication concerns

and apparent position

discrepancies.

The review included:

(1) frequency of control rod indication

problems;

(2) cause of the observed

"bounce" phenomenon

and resolution; and

(3) licensee actions based

on industry experience.

b.

Observations

and Findin s

The licensee had identified and tracked various rod position indication problems, at

an average of approximately one per month, during plant operations for fuel

Cycle 12.

During the plant response

to the manual reactor scram following the

performance of a reactor feedwater pump trip test, three control rods were not

verified by the plant computer to be at their full-in position.

This concern was

documented

in Problem Evaluation Request 297-0244.

Plant operators verified that

all rods were inserted by full core display and auto scram timer data.

The licensee

included the rod position indication concern in with other related issues documented

in Problem Evaluation Requests

297-0153 and 297-0187.

The team noted

a combination of three reed switches provided rods-in position

indication; two switches were located at the normal latched position and a third

switch corresponding

to just beyond full-in position.

The licensee was unable to

determine the specific control rods from the operator logs or interviews conducted

with control room personnel.

The team found that a new data system, currently in

a test mode, indicated that all control rods were full-in immediately following the

scram, but several control rods sporadically lost indication at various times.

20

Problem Evaluation Request 297-0187 documented

that during the performance of

scram time testing of Control Rod 1415, the respective

blue scram light and green

full-in light failed to illuminate.

The licensee identified that after the scram test

switches were reset, an unusually long period of time elapsed

before flow

movement noises

in the hydraulic control unit ceased;

at which time rod position

indications had returned to normal.

The tearri noted that the blue scram light

provided indication that both scram valves were in the fully open position, providing

full accumulator flow to the hydraulic control unit to rapidly insert the control rod

into the core.

The team observed that the green light provided indication that the

control rod was at the fully inserted position of the core.

Troubleshooting

efforts by plant personnel

identified the cause of the blue scram

light indication problem to be a limit switch failure.

The team found that the limit

switches for the scram valves of Hydraulic Control Unit 1415 had been

, subsequently

replaced.

Post-maintenance

testing resulted in all normal indications,

including the blue scram light response

regarding scram test switch operation.

No

additional problems regarding the blue scram light indications have occurred since

the replacement

of the limit switches for the effected scram valves.

The license

determined that the scram valves for the effected control rod should be refurbished

at the next available opportunity to ensure normal response

characteristics

while

closing.

The team determined that no safety function was provided while resetting

or closing the scram valves.

General Electric provided Service Information Letter 532, dated March 27, 1991,

regarding full-in control rod position indication.

This service information letter

stated that several boiling water reactors have temporarily lost "full-in"control rod

indication during reactor scrams.

Although not verified, General Electric postulated

that following a reactor scram, the position sensing magnet was subjected to

temperature

excursions,

which reduced its magnetic strength until cooling water

had been restored.

The letter recommended

modifying the rod position information

system logic to indicate full-in if any one of the three reed switches monitoring the

corresponding

position was closed.

Plant personnel

had implemented

a similar

modification 2 years prior to the service information letter submitted by General

Electric to.minimize spurious data fault indications.

The licensee had performed the

modification in accordance

with Maintenance Work Request AT5718 by changing

the programmable

read only memory locations corresponding

to the full-in logic

portion of the position indication probe data processing

cards.

With this change,

either of the two normal latch position switches combined with the full-in position

switch would provide the green full-in and data fault indication.

The team noted

that this modification did not prevent the momentary loss of full-in position

indication during the manual scram during the reactor feedwater pump trip test.

The team observed that scram valves for Control Rod 1415 were scheduled

for

refurbishment during Refueling Outage 12, in addition to replacement of position

indicator probes with identified problems during the last operating cycle.

The team

observed that, as a part of the corrective action plan, during control rod testing all

21

control rod position indications were verified to operate properly, including each of

the full-in and full-out position reed switches.

The team found that the licensee

staff had not implemented

a replacement

plan for scram valves, scram limit

switches, or position indicator probes, prior to failure.

c.

Conclusions

The licensee's

corrective actions following the position reed switch failures were

conservative

and demonstrated

an aggressive

approach

in tracking and r.solving

past rod position indication problems.

IV. Mana ement Meetin s

X1

Public Meeting and Exit Meeting Summary

A public meeting was held in the Region IV office on May 30, 1997, to review the

events leading to the March 27, 1997, reactor feedwater pump test, the safety

implications of resulting events, the post-event reviews performed by the event

evaluation team and independent

evaluation team, and the corrective actions being

implemented or proposed.

The team presented

the inspection results to members of licensee management

after the conclusion of the inspection on July 30, 1997.

The licensee

acknowledged

the findings presented.

During the inspection the licensee identified

that certain material details examined should be considered

proprietary.

None of

these details are contained

in the report.

22

ATTACHMENT 1

Supplemental

Information

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Arbuckle, Licensing Engineer

R. Barbee, Assistant Manager System Engineering

P. Bemis, Vice President for Nuclear Operations

R. Burk, System Engineer

A. J. Fonstock, Training Supervisor

P. Inserra, Licensing Engineer

R. Libra, Systems

Engineering Supervisor

D. Mand, Manager, Design and Projects

D. Mano, Design Engineer Manager

M. Monopoly, Operations Manager

B. Pesek, Supervisor Major Projects

G. Shindehite, Technical Specifications

G. Smith, Plant General Manager

J. Swailes, Engineering Director

D. Swank, Regulatory Affairs Manager

R. Webring, Vice President Operations Support

D. Whitcomb, Principal Engineer

INSPECTION PROCEDURES USED

IP 52001:

IP 52002:

IP 92901:

IP 92903:

Digital Retrofits Receiving Prior Approval

Digital Retrofits without Prior Approval

Followup - Operations

Followup - Engineering

50-397/9710-01

VI0

50-397/9710-02 VIO

ITEMS OPENED

Design Criterion III (Section E1.2)

Two examples of inadequate

10 CFR 50.59 reviews

(Sections E1.2 and E1.3)

LIST OF DOCUMENTS REVIEWED

Letter from Mr. P. R. Bemis, Vice President

Nuclear Operations,

dated June 25, 1997,

Nuclear Plant WNP-2, "Operating License NPF-21-Reactor

Feedwater

Pump Trip Test

Response

To Questions"

Plant Operating Committee Meeting 97-24.02, dated June 28, 1997, background

material

Plant Operating Committee Meeting 97-24 Meeting Minutes, dated June 25, 1997

Procedure 4.602.A6, "602.A6 Panel Alarms," Revision 8, and procedure revision form,

dated June 24, 1997

Safety Evaluation 97-078, "Recirculation Flow Control System Digital Feedwater

Level

Control System Feedwater

Pump Trip Test Followup 10 CFR 50.59 Safety Evaluation,"

Revision 0

Y

PMR 87-0244-6, "RRC-ASD-Interconnection 5 Control Room Mods, dated January 31,

1996

ASD-DFWLC Testing Overview

Procedure 4.12.4.7, "Unintentional Entry Into Region of Potential Core Power Instabilities,"

Revision 14

Problem Event Report 297-0244," Following RFW Pump B and Expected

RRC Runback to

27 Hz, a Second Unexpected DiffTemp Cavi Runback Occurred" dated March 27, 1997,

and associated

corrective action plans

Problem Event Report 297-0246, "Following Manual Reactor Scram Reactor Feedwater

Control System Did Not Reactor Level Below Level 8," dated March 27, 1997, and

associated

corrective action plans

PMR 91-0438-0, Field Change Request 91-0438-0-08, "The Power Ascension Test portion

of the Test Requirement Summary needs to be revised to include additional testing required

by POC," dated November 17, 1995

GE SIL 380, "Control of Neutron Flux Noise in Low Damped Operating Conditions"

Licensee Letter, "WNP-2 Operating License NPF-2, Evaluation of March 27, 1997 Reactor

Scram," dated April 9, 1997

Work Task Order BST8, RRCTT01 Suet Temp LOOP Cals, dated December 23, 1996

Procedure 8.3.339, "Test Instructions-Reactor

Recirculation Adjustable Speed

Drive and

Reactor Digital Feedwater

Control Power Ascension Test Program," Revision 3 and

Temporary Change Notice 97-108

Procedure 8.3.375, "Reactor Feedwater Turbine Digital Retrofit Preoperational

Test,"

Revision 0

1996 Power Ascension Test Report, Dated December 31, 1996

Procedure 8.3.386, "Test Instructions-RFW Governor'ost Maintenance

Retest and

Tuning," Revision

1

Procedure 8.3.376, "Test Instructions-Reactor

Recirculation Adjustable Speed

Drive

Preoperational

Test," Revision 0

Problem Event Report 296-0624, "DFWLC," dated August 11, 1996

Procedure 8.2.23.c, "Feedwater System-Feedwater

Pump Trip Test," dated January

16,

1984

Independent

Evaluation Team Report dated May 9, 1997

Independent

Evaluation team Review of Final EET Report and Addendum

1, dated June 20,

1997

Event Evaluation Team Report issued May 9, 1997, and Addended Report 1, issued June

1997

Safety Evaluation Report, Amendment dated June 3, 1996 (GI2-96-137)

Licensed Operators/STA Requalification Training for ASD and DFWLC

General Electric Letter 94-PU-0013, dated March 18, 1994

Safety Evaluation Control 93-200, dated July 11, 1995

Safety Evaluation Control 96-106, dated December

12, 1996

Procedure

1.4.14, "WNP-2 Software Control," Revision 0

WNP-2 Reactor Trip Report 97-1

Prebrief Check-off Sheet for March 27, 1997, planned reactor feedwater pump trip test

(OI-22, Revision B)

Procedure 4.12.4.7, "Unintentional Entry into Region of Potential Core Power Instabilities,"

Revision 14

BWROG Stability interim Corrective Actions and licensee's

response

GENE-208-12-0793,

"WNP-2 Power Up Rate Supplement for the WNP-2 Control System

Design Report, Incorporating the Adjustable Speed rive Reactor Recirculation System"

Plant Modification Request 87-0244

NRC letter dated June 4, 1997, T. P. Gwynn to J. V. Parrish, "Summa'ry of Meeting with

Washington Public Power Supply System (WNP-2) on May 30, 1997

Plant Operating Committee Meeting Minutes, dated June 25, 1997,

.Cycle 012 Core Operating Limits Report

Problem Evaluation Request 297-0187

General Electric provided Service Information Letter 532, dated March 27, 1991

ATTACHMENT2

Letter G02-97-131

Licensee Response

to Supplemental

Ouestions

dated June 25, 1997

WASHINGTON PUBLIC POWER SUPPLY SYSTE!vI

PO. Box 968

~ Richlnuit, iYashingtou 99352-0968

Docket No. 50-397

U. S. Nuclear Regulatory Commission

Attn: Document Control Desk

Washington, D. C.

20555

Gentlemen.'ubject:

NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21

REACTOR Fl<3<3)WATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Reference:

Letter, dated June 4, 1997, TP Gwynn (NRC) to JV Parrish (SS), "Summary of

Meeting with Washington Public Power Supply System (WNP-2) on May 30,

1997"

This letter provides our response to the requested information in the referenced letter pert'uning

to the reactor feedwater pump trip test and reactor scram which occurred on March 27, 1997.

The Supply System was requested

to address certain items prior to WNP-2 leaving Operational

Mode 4 and entering Operational Mode 2 for startup.

Our response

consists of this letter and Attachments A and B. In Attachment A, responses

to

each of the six items pertaining to the reactor feedwater pump test are provided.

Attachment

B consists of a listing of recommendations

from the Event Evaluation Team (EET) and the

Independent Evaluation Team (IET) and the planned response

to these recommendations.

As a result of divergent findings or recommendations

resulting from the IET review of

preliminary results from the EET, an additiona1 evaluation of plant response to the event was

performed.

The results of this evaluation were incorporated as an addendum to the final ~MT

report.

Additional insight into the factors that contributed to the differential temperature

cavitation

interlock trip which preceded

the manual scram is provided in the addendum.

The major

contributors were the effect of the conservatism

in the trip logic implemented

during the

Adjustable Speed Drive (ASD) modification and the final power and flow conditions of the

Reactor Recirculation

(RRC) System pump runback.

These

were estimated

to reduce

the

~

~

differential temperature

margin by 1.5 to 2.0 degrees Fahrenheit and 1.5 degrees Fahrenheit,

respectively.

REACTOR FEI<3)WATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Page 2 of 2

Also evaluated was the effect of power uprate and digital feedwater on differential temperature

reduction.

These

were shown to be less

significant', at 0.5 and 0.3 degrees

Fahrenheit

respectively.

Finally, the impact of the difference in runback rates between flowcontrol valve

and ASD runback rates were confirmed to be a smaller contributor to loss of differential

temperature margin. Details of the various parameters

that potentially could have impacted the

differential temperature

cavitation interlock are contained in the addendum

to the final EET

report.

Should you have any questions or desire additional information pertairung to this letter, please

call me or P.J. Inserra at (S09) 377-4147.

Respectfully

P..

s

Vi

President, Nuclear Operations

Mail Drop PE23

Attachment

CC:

EW Merschoff - NRC RIV

KE Perkins, Jr. - NRC RIV, Walnut Creek Field Office

TG Colburn - NRC NRR

NRC Senior Resident Inspector - 927N

DI. Williams - BPA/399

PD Robinson - Winston & Strawn

IL

I

( ~

REACTOR FEEDWATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 1 of 13

The Supply System

was requested

to address

the following items prior to WNP-2 leaving

Operational Mode 4 and entering Operational Mode 2 for startup.

For ease of reference,

a

restatement of each item is provided.

Item 1

"When willthe IET review of the final EKT report be completed?"

On June 20, 1997 the IET completed its review of the final EET report along

with the report addendum and the proposed responses

to items one through four

of this attachment.

The IET concluded that the subsequent followup effort resulting in the finalEET

report and associated

addendum adequately

addresses

the concerns identified in

the IET report.

Specifically, the EET has provided information to v'alidate the

causes fox the event.

With respect to the IET recommendations,

the Supply System has accepted

the

recommendations

and has provided a schedule forresolving them. The two issues

which could potentially impact reactor startup (i.e., rerun ofthe reactor feedwater

pump test and analyze plausible causes for the event) are considered closed as a

result of actions taken and planned by the Supply System.

The planned actions

for the remaining recommendations will be adequately

resolved

as part of the

ongoing activities related to the event.

A separate

assigned

team,

including a supervisor,

has

been

established

to

implement and close all open issues related to the ASD and DFWLC systems.

Xtem 2

S

"Based on questions raised by the IET regarding the thoroughness

of the

a<gustable speed drive transient analysis with respect to the modifications,

please

provide your actions or plans for a thorough engineering and/or

operational design feature review of the digital feedwater and acgustable

speed drives and the power uprate modification.

This integrated review

should

ensure

that other operating

parameters,

simjtlar to the reactor

recirculation

system

delta

temperature

cavitation interlock,

were

not

impacted by these changes."

The original design and analysis for the Adjustable Speed Drive (ASD) and

reactor power uprate (RPU) modifications were performed

as

an integrated

product.

Letter

GE-NE-189-33-0392,

"Preliminary

Design

of WNP-2

Recirculation Adjustable Speed Drive," dated March 1992,

states in the first

paragraph of the Introduction Section,

"The preliminary design of the ASD

implementation for the WNP-2 Reactor, Recirculation System is developed to be

consistent with the ASD &Power Uprate projects."

As such, the integration of

REACTOR FEEDWATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 2 of 13

these two projects started during the preliminary design phase.

In fact, separation

ofthe two projects had to be made to allow RPU to be implemented in 1995 with

the ASD modification implemented in 1996.

This split was performed due to a

lack of sufficient resources

to complete both projects within the same year and

during the same refueling outage.

During the design phase of the Digital

Feedwater Level Control System (DFWLC), design inputs considered that both

the ASD and RPU modifications were in place.

The Supply System's Event Evaluation Team~ performed a review of the

design

requirements

for the DFWLC and ASD systems.

The Independent

Evaluation Team (IET) reviewed the EET preliminary results and questioned the

thoroughness of the work completed at that time, particularly with respect to the

evaluation of the integration of the DFWLC, ASD and RPU changes

made at

WNP-2. A description of the additional integrated review performed is provided

below.

The Supply System's

EET reviewed

the impact of the DFWLC and ASD

modifications, verses

the analog

feedwater level control system

and

analog

recirculation flow control system,

on plant design.

In particular,

the EET

evaluated the followingtransients, anticipated operational occurrences,

and events

and the potential impact of the ASD and DFWLC systems on these events:

ao

b.

C.

d.

e.

f.

g.

h.

Transient MCPR Control - FCV Failure

Transient

MCPR Control - Idle Recirculation

Pump

Start-

up/Recirculation Speed Changes

Recirculation Pump Trip System

SCRAM Avoidance - Core Flow Increases

SCRAM Avoidance - Loss Of Reactor Feedwater Pump

Equipment Protection - Cavitation Interlocks

Equipment Protection - Valve Interlocks

Loop Mismatch

Maintain Core Circulation - Reactor Recirculation System (RRC)

60 Hz Trip

Anticipated Transient Without SCRAM (ATWS)

In response

to an IET concern

regarding

the completeness

of the review

performed by the Supply System's EET, the Supply System, in conjunction with

senior members of the General Electric Nuclear Engineering

(GENE) staff,

performed a review of other operating parameters

to ensure that they were not

REACTOR FEEDWATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 3 of 13

negatively impacted by the ASD/DFWLC/RPU modifications in a manner not

evaluated as part of the modifications.

Specifically, based on direction provided

by the Supply System's Engineering organization, GENE engineers performed a

review and submitted their preliminary results to the Supply System for review

and comment.

Following Supply System comments,

additional evaluation was performed by

GENE and the final results and concerns were provided to the Supply System.

For each of the operating parameters

reviewed, consideration was given to the

integrated impact of the three modifications. The results ofthe GENE review are

consistent with those obtained during Supply System reviews.

For the RPU modification, the review group looked at the following operating

parameters.

Each of these parameters were included in the RPU analyses

as part

of the RPU modification.

APRM flow biased simulated thermal power-high scram setpoint

Reactor vessel steam dome pressure-high

setpoint

APRMflowbias simulated thermal power-upscale scram setpoint equation

Neutron flux-upscale control rod block trip setpoint equation

Main steam line high pressure setpoint

Rod Block Monitor instrument flow biased setpoint

Revised Group l SRV setpoints and the setpoint maximum tolerances to

reflect the RPU and SRV setpoint analyses

. Revised reactor pressure vessel pressure-temperature

curves for RPU

Required number of ADS valves required reduced by one for RPU

Turbine first stage pressure

scram bypass remains at 30% reactor power

Main steam line flow differential pressure setpoint revised

Reactor pressure vessel operating steam dome pressure raised

Reactor power raised to 3486 MWt

REACTOR F<E%2)WATER %AMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 4 of 13

Credited operating pressure for High Pressure

Core Spray (HPCS) was

raised

Rated feedwater flow was evaluated

Rated steam flow was evaluated

The runback rate for the Extended Load Line Limitwas analyzed as part

of the RPU and again as part of the ASD modification

For each of the RPU impacted operating parameters

listed above,

the review

group evaluated the parameters relative to changes caused by DFWLC and ASD.

No additional impacts were identified.

For the DFWLC and ASD modifications,

the review group looked at the

following:

ao

The recirculation fiow runback characteristics

were changed

since they

were previously based on flow control valve position and closure speed

With the ASD modification, these

characteristics

are based

on pump

speed.

This change was previously analyzed and determined to have no

appreciable effect.

b.

An ASD overfrequency trip was added to terminate the flowrunout event.

There is a separate overfrequency trip circuit for each of the RRC pumps.

This should have no effect on the other parameters or events since it stops

a transient from progressing.

C.

Cavitation Interlock changes

Setpoints - no changes

2.

Logic - designed

to be more conservative

since the worst case

differential temperature

is selected,

this is conservative from a

cavitation prevention point of view, but it also results in a slight

increase in the probability of a recirculation pump runback to 15

Hz and entry into Region A of the Power-to-Flow Map.

The

cavitation runback is a non-safety-related

equipment protection

feature.

3.

Removed the feedwater flow cavitation runback logic

REACTOR FEEDWATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 5 of 13

4.

Changed from an analog design to a more accurate digital design

as part of the ASD modification

d.

The single feedwater pump trip recirculation pump runback endpoint and

rate of runback were changed from flow control valve position and rate

of change to a recirculation, pump speed

end point and rate of change.

The setpoints were developed through a series of parametric studies

as

part of the ASD design effort.

e.

Added ASD equipment protection trips.

These should have no effect on

other parameters

since they are bounded by the recirculation pump trip

analysis.

The recirculation pump trip is an anticipated

operational

occurrence

that does not result in a plant scram or have other adverse

operational impacts.

One channel runback capability for loss of a single channel in one ASD.

This does not effect any other parameters in an unanalyzed way since it

is bounded by the recirculation pump trip analysis.

The recirculation

pump trip is an anticipated operational occurrence that does not result in

a plant scram or have other adverse operational impacts.

g.

Jet pump sensing line clamps were added for the variable pump speeds

(and thus pump vane passing

frequencies)

that would be encountered.

This does not effect the other parameters.

h.

The recirculation flow control valves were locked open.

The ASD

analysis was performed with the ASDs instead of the fiow control valves

providing flow control.

Electrical bus harmonics were evaluated to determine the effects of the

ASDs.

Acceptable conditions were verified for the electrical distribution

system and connected equipment.

J ~

The recirculation system runback lower limitfor a single feedwater pump

trip was lowered.

This impacted the cavitation interlock.

None of the

other operating parameters

were impacted.

An evaluation of the effect of fault logic or signal noise (transition to

single element flow control) was not specificaQy analyzed.

However,.

these changes were implemented to reduce the impact ofequipment failure

or degradation,

and

thus provide for improved system

performance.

Operation in single element control is a condition that was previously

analyzed.

REACTOR HU~MWATERPUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 6 of 13

1

The DFWLC system

was designed

to fully open the feedwater pump

minimum flow bypass

valves back to the condenser

for 30 seconds

followinga scram and then to ramp these valves closed.

This change was

implemented to reduce the potential for a high reactor water level gevel

8) due to swell following a scram.

This change was evaluated as part of

the 10CFR50.59 Safety Evaluation for the DFWLC system.

Additional

analysis has recently been performed and it was deterinined that this valve

action has littleeffect in avoiding the Level-8 trip, and does not adversely

impact plant performance following a scram.

m.

The quasi-steady

state behavior of the differential temperature cavitation

interlock was previously analyzed.

However, the dynamic evaluation of

the instrument system was not previously analyzed for impact from ASD,

DFWLC, and RPU. Significant analysis has now been performed and an

interim modification to the differential temperature

cavitation interlock

will be implemented prior to plant restart from the current maintenance

and refueling outage.

This includes a change to the current time delay

from 15 seconds to 10 minutes. Plant procedures willbe revised to reflect

this change and to provide plant personnel with the information necessary

to ensure that the fatigue usage of 15 minutes for the remaining lifeof the

plant for the jet pumps

is not exceeded

due

to cavitation.

This

modification may become permanent

pending

the results of followup

cavitation logic change review efforts.

The differential temperature

setpoint willbe increised from 9.9 degrees

Fahrenheit to 10.7 degrees

Fahrenheit.

Although original evaluations

resulted in a setpoint of 10.7 degrees Fahrenheit, it was determined based

on initialpower ascension

testing results that 9.9 degrees Fahrenheit was

acceptable.

Subsequent

increased

core flow and power uprate analyses

concluded

that the original evaluations

remain valid and no setpoint

changes

were required.

Based on followup assessments,

the setpoint is

. being changed to 10.7 degrees Fahrenheit.

As discussed above, the evaluations of the operating parameters

and the potential

impact of the ASD, DFWLC and RPU modifications did not identify adverse

effects to these parameters

not previously evaluated,

except for the delta T

cavitation interlock.

Apreliminary review has been completed and did not identify any additional tests

that need to be re-run to validate the initial startup test program results.

In

addition, after startup an evaluation willbe completed of the FSAR Chapter 14

initialpower accession

startup test program acceptance criteria to ensure that the

changes

implemented by ASD, DFWLC and RPU did not impact the initial

REACTOR FEEDWATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 7 of 13

startup test program results and conclusions.

Item 3

"VVhat evaluations willbe performed to integrate the IET and EET findings

regarding the adjustable speed drive modification and the digital feedwater

problems identified in Problem Evaluation Report (PER) 297-0246?"

The concern regarding occurrence of the post-scram high water Level-8 trip was

specifically not part of the EET charter and has not been addressed

by the EET

or IET. Resolution of this problem is being tracked by the Problem Evaluation

Request (PER) process.

i

Since initialstartup ofWNP-2, several design changes have been implemented to

improve the chances ofavoiding a Level-8 trip following a scram.

These include

setdown'of the vessel level setpoint followinga scram, reduction ofthe muiiinum

steady-state

feedwater

pump governor

speeds

and,

most recently, with the

addition of the DFWLC system,

momentary opening of the feedwater pump

minimum Qow bypass to condenser valves upon a scram to reduce the vessel refill

rate.

Preliminary evaluations

determined

that each of the design

change

features

operated correctly and sluggish governor valve actuation had caused the Level-8

trip.

General Electric and Lovejoy Controls, Inc., assisted

Supply System

Engineering in reviewing the feedwater turbine response.

Based on available

data, it was concluded

that the Digital Feedwater

Level Control (DFWLC)

System appeared

to function correctly. Initial analyses indicated that a sluggish

relay valve was the most likely cause ofvessel level reaching Level-8.

Based on

the recommendations,

testing and intrusive investigations were completed

and

found the relay valves in both Reactor Feedwater Pump Turbines A and B to be

sluggish and scored.

The relay valves were removed, polished and cleaned and

confirmed to be working properly. Arepresentative from Lovejoy Controls, Inc.,

was on site during the relay valve work effort. The cause ofthe problem appears

to be less than adequate filtration in the feedwater pump turbine oil system.

To further determine

the most likely cause of the Level-8 trip, computer

(RETRAN) simulations,

specific to WNP-2, were recently completed by the

Supply System to evaluate the effectiveness of these enhancements

as well as to

quantify the effect of the sticking relay valve.

Results determined that each had

minimal effect in either causing, or avoiding, the Level-8 trip point. In fact, the

only

effective

means

of avoiding

vessel

overfill was

determined

to

be

improvement in the responsiveness

of the governor controller following a scram.

The required changes are complex.

These changes willcontinue to be evaluated

after reactor startup and a remedy implemented at the first future window of

REACTOR FEEDWATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 8 of 13

appropriate plant conditions.

ln order to assess

the impact of continued

operation of the plant without

resolution of this problem,

an

assessment

of the

safety

significance

was

performed.

Results determined that a post-scram Level-8 trip of this type does

not represent

a safety concern.

Additional actions may be required to preclude

or recover from a Level-8 trip.

However, plant operators

are trained that a

Level-8 trip followinga scram may occur. This training includes actions that can

be taken to either avoid the trip or respond accordingly should a trip occur.

Item 4

"Provide an accounting for each ofthe EET and IET recommendations.

This

accounting should provide a direct correlation between the recommendation,

its acceptance

or denial, whether the action is complete or its status, and

whether the recommendation

actions will be implemented prior to plant

restart."

The Supply System response

to this question is provided as Attachment B and

contains the EET and IET recommendations.

In each case, the recommendations

have been accepted and entered into the Plant Tracking Log. Completed actions

have been identified as well as those which willbe completed prior to reactor

startup.

The criteria for completion before startup include items that would adversely

affect plant safety or clearly decrease plant reliability or capability.

Corrective

actions that met this criteria are identified as items that require completion before

the end of the R-12 Maintenance and Refueling Outage.

Item 5

"Determine whether the instaHed a@ustable speed drive modification resulted

in an unreviewed safety question and whether an additional submittal will

need to be reviewed by the NRC modifying the previous safety evaluation.

Your response

should also include whether the planned delta T cavitation

interlock setpoint resolution willrequire NRC review and approval."

1. Plant Response to the Event

For the purposes of an unreviewed safety question determination, the activity is

defined as the plant response to the reactor feedwater pump trip test event.

This

includes

the differential temperature

cavitation interlock trip and

associated

reactor recirculation pump runback, indicated entry into Region A of the Power-

to-Flow Map, and water level response.

REACTOR H~MDWATERPVMP TRIP TEST

RESPONSE TO QVESTIONS

Attachment A

Page 9 of 13

The cavitation interlock protects

the recirculation pumps and jet pumps from

cavitation damage.

The interlock signal is the differential temperature between

the steam dome temperature

(derived from steam dome pressure

measurement)

and the recirculation pump suction temperature.

Increasing the pump speed above

the minimum value is prevented ifthe temperature

difference is less than the

setpoint.

Similarly, the pumps are automatically run back to the minimum speed

ifthe setpoint is reached.

Minimum speed is below the cavitation threshold.

Followup sensitivity evaluations were performed that considered

the effect of

changes

in various

parameters

and

plant

characteristics

as

a

result

of

implementation ofpower uprate and the ASD and DFWLC modifications. These

analyses

further defined. the extent to which final test conditions,

a more

conservative trip logic, and other variables, combined to reduce overall operating

margin during the trip test.

However, initiation of the interlock and subsequent

runback of the RRC pumps

to

15 Hz is bounded by the more severe

and

previously-analyzed trip of two recirculation pumps transient.

Reactor recirculation system flow run-back and recirculation pump trip events

leading to entry into stability Region A of the WNP-2 Power-to-Flow Map were

considered in establishing the stability region boundaries.

Response to entry into

Region A of the Power-to-Flow Map is controlled by Technical Specification 3.4.1, "Recirculation Loops Operating.

Compliance with the limitingcondition

for operation action statements in this specification, in the event of entry into

Region A, assures

that a USQ does not exist.

It was

recognized

during development of the stability region that there is

reasonable

probability that unplanned

operational

occurrences,

most notably

recirculation pump trips and run-backs,

could lead to entry into the stability

region.

The region definitions account for entry into the region as a result of a

core flow reduction,

independent of the probability of occurrence of such a

reduction in core flow.

As an aside, the Supply System has committed to implement Stability Solution

Enhanced Option I-A. General Electric Licensing Topical Report NEDO-32339-

A, "Reactor Stability Long-Term Solution: Enhanced Option I-A,"Revision 0,

was developed to provide a methodology for prevention of reactor instabilities.

The NRC determined that Enhanced Option I-A was acceptable for referencing

in license applications to the extent specified, and under the limitations delineated

in NEDO-32339 and the associated NRC technical

evaluation.'etter

and Safety Evaluation, RC Jonea (NRC-NRR) to RAFinelli (BWROG), Acceptance forRcferencing ofTopical Repott NEDO- 32339, Reactor StabiTity Long tcrtn Solution: Enhanced Option I-Ag'AC M89222),

dated April24, 199$

REACTOR mt~WATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 10 of 13

In the Topical Report, it was recognized that the establishment of the Exclusion

and Restricted

Regions

assures

stability at anticipated

terminal reactor

state

conditions following plant transients.

It was stated in the report that transients

that result in limiting reactor stability conditions are loss of feedwater and core

flow reduction events.

'vents

whose

reactor

state

trajectories

would enter

the Exclusion Region

terminate with automatic reactor scram at the region boundary.

The treatment of

events that teaninate within the Restricted Region depends upon whether they

initiate inside or outside of the Restricted Region.

In a followup to the Topical Report, it was also recognized that flow reduction

events

may

have

a

significant effect

on reactor

stability

performance.'xamples

of flow reduction events are one or two reactor recirculation pump

trips, reactor recirculation pump runbacks, and reactor recirculation flowcontrol

valve runbacks.

However, the specific mechanism causing these events is irrelevant.

Reasonably

limiting flow reduction events considering the combination of all parameters

affecting stability performance

are defined for the stability region boundary

validation analyses.

The ASD and DFWLC system response pre-scram to the feedwater pump trip and

subsequent recirculation fiowrunback was as expected with regards to the reactor

vessel water level and did not result in a Level-3 scram.

As the feedwater flow

stabilized out, the reactor vessel level swelled and peaked

at slightly over 51

inches, avoiding a Level-8.

Initiation of a feedwater pump trip not initiating a

reactor trip indicates

that the control system

response

does not increase

the

probability ofa more severe transient resulting &om an operational event.

Other,

less limiting, operational events are analyzed in the General Electric ASD control

system report and are shown not to degrade due to ASD and DFWLC system

response.

Therefore, less limiting transients do not become additional transients

for FSAR analysis.

The post-scram response is not dissimilar to what would have been seen with the

previous analog system.

Since the Level-8 trip was reached post-scram,

there

was no adverse impact on the fuel thermal limits. For long term cooling and

inventory make-up,

the High Pressure

Core Spray (HPCS) System would be

available once the water level lowered to the initiation setpoints.

Therefore, the

NEDO-32339, ReviYion i,

Licensing Topical Report - Rcactoe

StabiTity Long-Tcrtn Solution: Enhanced

Option I-h,

dated

December 1996

REACTOR H~3H)WATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 11 of 13

transients in the FSAR are stillbounding and, as a result, the consequences of an

accident as analyzed in the FSAR were not increased.

The Reactor Core Isolation

Cooling (RCIC) System would also be available once the water level lowered.

In conclusion, this situation does not result in a condition where 1) the probability

of occurrence or the consequences

of an accident or malfunction of equipment

important to safety previously evaluated in the safety analysis report may be

increased, or 2) a possibility for an accident or malfunction of a different type

than any evaluated previously in the safety analysis report may be created, or 3)

the margin of safety as defined in the basis for any technical specification is

reduced.

2. Differential Temperature Cavitation Interlock

With regard to the cavitation interlock, the following changes to the differential

temperature

logic for reactor

recirculation flow control

system

cavitation

protection are planned:

Differential Temperature Setpoint

The differential temperature setpoint willbe increased from 9.9 degrees

Fahrenheit to 10.7 degrees Fahrenheit.

Differential Temperature Setpoint Reset

'he

differential temperature

setpoint reset will be increased

from 10.9

degrees Fahrenheit to 11.2 degrees Fahrenheit.

Differential Time Delay to Runback

The differential time delay to runback willbe increased from 15 seconds

to ten minutes.

~

Alarm Features

Alarm annunciation willbe changed from actual runback initiation to the

start of the timing period.

The cavitation interlock protects

the recirculation pumps and jet pumps from

cavitation damage.

The interlock signal is the differential temperature

between

the steam dome temperature

(derived from steam dome pressure

measurement)

and the recirculation pump suction temperature.

Increasing the pump speed above

the minimum value is prevented if the temperature

difference is less than the

REACTOR FEEDWATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Attachment A

Page 12 of 13

setpoint. Similarly, the'pumps are automatically run back to the minimum speed

ifthe setpoint is reached.

The cavitation interlock setpoint is being changed to reflect calculated values,

includes margin, and accounts for the high cavitation conditions which would be

experienced

under increased core flow. Increasing the existing time delay will

result in the avoidance of unnecessary

reactor recirculation system pump speed

runbacks.

The alarm logic is being changed'to

initiate the alarm when the

cavitation setpoint is exceeded,

rather than the current design of after the time

delay.

Although original evaluations resulted in a setpoint of 10.7 degrees Fahrenheit,

it was determined based on initialpower ascension testing results that 9.9 degrees

Fahrenheit was acceptable.

Subsequent

increased

core fiow and power uprate

analyses

concluded that the original evaluations remain valid and no setpoint

changes

were required.

Based on followup assessments,

the setpoint is being

changed to 10.7 degrees Fahrenheit.

The allowable 10-minute time foroperating under cavitation conditions at WNP-2

is based on the measured

test results during a cavitation event at a BWR-4 plant

with a 251-inch diameter vessel, and additional conservatisms to allow for the test

results being consistent with a BWR-5.

It was concluded from testing and

calculations

that the cumulative time allowable for cavitations would be

15

minutes (cumulative for each pump for the reniaining life of the plant), taking

into account the presence ofjet pumps with set screw gaps in the past.

The recirculation fiowcontrol system does not perform any active safety function.

The primary relation of the system to the licensing basis analysis is as an initiator

of events.

The proposed

modification changes

provide adequate

equipment

protection against cavitation damage.

The proposed

change

does not alter assumptions

made in the licensing basis

documents

pertaining to reactor recirculation

system

pump response

during

transients or accidents.

The jet pumps are part ofthe reactor recirculation system

and are designed to provide forced circulation through the core to remove heat

from the fuel.

Because

the jet pump suction elevation is at two-thirds core

height, the vessel can be reflooded and coolant level maintained at two-thirds core

height even with the complete break of the recirculation loop pipe that is located

below the jet pump suction elevation.

The capability of reflooding the core to two-thirds core height is dependent upon

the structural integrity of the jet pumps.

Structural failure or system degradation

could adversely affect the water level in the core during the refiood phase of a

REACTOR FEW)WATER PUMP TRIP TEST

RESPONSE TO QUESTIONS

Qi

Attachment A

Page 13 of 13

Loss'of Coolant Accident (LOCA), as well as the assumed blowdown Qow during

a LOCA.

However,

a malfunction of a jet pump

is

considered

in the

Technical

Specifications.

The

Technical

Specifications

include

daily

surveillance

requirements

which are designed to detect jet pump failure and provide action

statements

should a jet pump failure be indicated.

The presence of cavitation

would not impact the ability of the surveillance to detect a jet pump failure.

The changes,

which were proposed

and accepted

by the Supply System

and

endorsed by General Electric, provide for avoiding recirculation pump runbacks

caused

by false indication of cavitation conditions or by a setpoint that is

inappropriate during some operating conditions.

This willalso allow Control

Room Operators time to validate the alarm and determine ifit is the result of an

actual condition or the result of spurious component failures or other problems.

In conclusion, this situation does not result in a condition where 1) the probability

of occurrence or the'consequences

of an accident or malfunction of equipment

important to safety previously evaluated in the safety analysis report may be

increased,

or 2) a possibility for an accident or malfunction of a different,type

than any evaluated previously in the safety analysis report may be created, or 3)

the margin of safety as defined in the basis for any technical specification is

reduced.

Therefore, prior NRC review would not be required.

Item 6

"WiHthe reactor feedwater pump trip test be rerun? Ifyes, then at what

initialconditions and on what schedule?"

The Supply System plans to rerun the feedwater pump trip test. Initialconditions

willbe consistent with those from the WNP-2 Power Ascension Test Program,

i.e., greater than 95 percent of thermal power.

The testing is planned to be

performed as a part of power ascension

testing at the completion of the R-12

Maintenance

and Refueling Outage

and in accordance

with Plant Procedure

(PPM) 8.3.339, "Test Instruction - Reactor Recirculation Adjustable Speed Drive

and Reactor Digital Feedwater Control Power Ascension Test Program."

The current sequence in the power ascension

testing schedule for this test is as

soon as practical after the completion of stable fullpower operation and required

100-percent-power calibrations and tests.

Att

tB

Response to Item 4

Page I of7

The listing below contains all EET and IET recommendations.

In all cases the recommendatlons

have been accepted

and entered

into the Plant

Tracking Log. Completed actions have been identified as well as those which will be completed prior to reactor startup (RXSU). Other actions wIII be

completed after startup (ARXSU).

The criteria for completion before startup include items that would adversely affect plant safety or clearly decrease

plant reliability or capability.

Corrective actions that met this criteria are Identified as items that require completion before the end of the R12 outage.

Recommendations

Item

Recomm end atioas

1.

hT Cavitation Setpoint and Methodology

Date

RXSU

The GE Factory Automatic Numeric Controls (FANUC) system compares

Inputs from the four RTD's suction temperatures

with Inputs

from two reactor steam dome pressure

Inputs.

The

FANUC determines

the differential temperature

(hT) by selecting the highest

temperature

input and the lowest pressure

Input. The following actions are recommended

with respect to the

9.9'F setpolnt and the

methodology:

a. Given the capability inherent in the ASD system, evaluate whether a more effective hT cavltatlon protection method can be designed

and implemented.

b. If a more effective hT cavltatlon protection method cannot be provided,

then evaluate through analysis whether to use the 10.7'F

setpoint

recommended

by GE or the 9.9'F setpoint determined by the Supply System ln the Interim and document the basis for this

decision.

Further, determine whether or not a higher setpolnt can be implemented to provide greater operating

margin while still

providing protection to the Jet pumps.

c. Need to decide or clarifywhether the setpolnt is a trip setpolnt or an analytical limit.

d. Ifit is a setpoint, the analytical limitand the accuracy/drift for the temperature and pressure loops need to be defined.

e. Ifit is an analytical limit, a calculation needs to be performed to determine the trip setpoint.

Att

tB

Respond

to Item 4

Page2of7

15 Second Time Delay

RXSU

Analysis needs to be performed to evaluate increasing the time delay and provide justification that the resulting time delay is short

enough to prevent excessive damage to the Jet pumps from cavitation and long enough for the system to stabilize following a transient

which could activate the cavitation interlock.

Alarm Logic

RXSU

The alarm logic should be changed to annunciate the alarm when the time delay timer starts, not when the time out Is completed. This will

give Operations some wamlng of a potential runback. The alarm coupled with a longer time delay could also allow Operations time to Insert

control rods and possibly avoid Region A should the runback occur after the time delay. Add the operator response

when the alarm ls

received In the annunciator response procedure (e.g., Is the alarm real or due to a human error).

Runback Value of 15 Hi

ARXSU

The runback value of 15 Hz should be reviewed for possible revision based on the Issue of core stability. The original cavitation logic was

developed prior to the concern over core Instability In regions of high power and low core flow. The present logic allows for a spurious or

unnecessary

runback to place the reactor Into such a condition.

Varying these

parameters

may allow avoidance of Region A.

This

evaluation should also consider single loop operation.

Cavitatlon Logic Change

ARXSU

Recommend

considering a modification to allow the logic to vary the time delay (dependent

upon sensed

conditions) as a long term

approach to improve the cavitation interlock. The current cavitation logic has a number of issues that together indicate that assessment

of a change to the logic would be beneficial to the plant. Issues Identifie during this review are:

a. Adding setpolnt margin to the interlock setpolnt will make it necessary to achieve a higher thermal power in power ascension

before

the speed can be Increased above 15 Hz. This will make It more difficultto avoid the stability increased awareness

zone at the low end

of the thermal power core flowmap (see Figure 1) during power ascension.

b.

The Interlock ls based

on the dNerential temperature

conditions that exist at high core flow and low thermal power.

The single

setpolnt causes the intertock to be excessively conservative at lower core fiows and thermal powers making it necessary to raise thermal

power to high values before speed can be Increased.

c. The interlock setpolnt Is based on two loop operation and does not Initiate a runback when needed for a region of the thermal power-

Att

tB

Response to Itein 4

Page3 of7

core flow map in single loop operation.

Operator action is needed in single loop operation to avoid entry into the region not covered by

the cavitation interlock.

d.

Increasing the allowable time for cavltatlon although It may be acceptable

in that it will not cause excessive

equipment damage

Is

conceptually the non-conservative direction. Analyses should establish acceptable limits and recommendations for minimizing this risk.

An interlock change that would allow changing the setpolnt of the interlock versus core flow, thermal power (e.g., feedwater flow) and the

number of operating loops would be more accurate and allow Increasing speed at lower rod lines during power ascension.

The possibility of a flow biased delta temperature interlock trip should be evaluated as another means of avoiding a delta temperature trip

during a transient.

TR 650 Temperature Values

Complete

As indicated in Figure 12, the values recorded on TR 650 are significantly lower than the RTD values due to the MV/I converter.

The

calibration of the converter should be adjusted to provide values that are more consistent with the actual RTD readings.

A further review of the Simulator model Is required to determine why it did not sufficiently model the feedwater flow rates, temperatures

and

ARXSU

reactor water level controller. Recommend that the Simulator staff fullyreview these differences.

The 5% / second rate limiter In the ASD speed control logic did not limit the ASD speed Increase during the January 1997 flow transients

ARXSU

which resulted from the Phase

Lock Loop (PLL) faults. Mechanisms

independent

of the ASD to limit RRC pump runback should

be

evaluated.

10.

Document the basis for the 1% / second and 5% / second rate limitersetting.

ARXSU

Simulator Staff evaluate the simulator ASD model versus the plant ASD for the Delta-T cavitatlon logic. Additionally, evaluate the simulator

ARXSU

recirc loop temperature and dome pressure/temperature

response to this transient.

Develop and Implement corrective actions as necessary.

4

Engineering General Manager work with the Nuclear Training Manager to enhance existing procedures for design and system engineering to

ARXSU

provide Information to the Simulator group to Identify deficiencies and improve the fidelityof the Simulator

12.

To provide clear guidance for the Simulator group, the Engineering General Manager and the Nuclear Training Manager, need to develop a

ARXSU

procedure, or enhance existing procedures such as P.P.M. 1.4.1, with acceptance

guide lines for who is responsible for gathering the plant

data and provide an acceptable time frame for updating the Simulator. Currently ANSI standard 3.5 allows 1 year to up grade the Simulator

Au

tB

ResIN

to Item 4

Page 4 of7

after change ln the plant Is made. This guidance should also address that in preparing for a special test, engineering should provide and the

Simulator group should implement the necessary

information to allow the Simulator to correctly model the proposed test.

13.

The Simulator group and Operations should set up a ",priority meeting'hich would allow setting the priorities for which Simulator up grades

ARXSU

should be made immediately and those that are not as Important, can be delayed. This meeting could be Incorporated

In into the TAG

meeting or be separate.

14.

Discuss with operations trainers, that when providing training for evolution's of this type, Nuclear Training should enhance the quality of the

ARXSU

training by conducting a refresher of all the trips and Interlocks for the component being tested.

15.

The Engineering General Manager should develop a task force, consisting of an Operations representative,

a System Engineer, a Design

ARXSU

Engineer, and a Training representative

to review P.P.M. 4.12.4.7 for possible lnstrumentatlon,

procedure,

and training enhancements

to

provide the operators improved guidance and greater flexibilityln maxlmizlng plant operations white avoiding stability region "A".

17.

Perform Feed Turbine test again to demonstrate the integrated plant response.

18.

Develop an appropriate method of properly Identifying critlcal parameters to compare, before and after conditions of systems that are to be

modified.

Consider adding this guidance to Engineering document PDS-9 when developed.

16.

Implement Corrective Actions associated with PER 29T-0248 (Feedturbine trip following SCRAM). PER 297-0248 tracks to completion.

ARXSU

ARXSU

ARXSU

19.

Develop a better means of establishing clear design bases for new modifications and provide a means to compare the new bases with older

ARXSU

bases.

Add this guidance to the appropriate Engineering Instruction.

20.

21.

Develop more comprehensive

modeling systems to better predict test results, prior to running the actual tests when practicable.

When not

practicable, model limitations must clearly be defined and understood.

Consider the following:

Know what parameters are going to change.

Know what Interlocks are influenced by these parameters.

Know ifwe can accurately predict that the interlocks willbe activated during the test and Ifthey cannot be modeled.

Know how we willmanage the issue In the test.

Review and consider the benefits of developing a tool such as

flow/tree diagrams that would list potential system Interactions during PMT.

The diagrams could be used to brainstorm ail predicted system responses

and then determine what steps should be taken to revise the

design or mitigate transients.

Ensure

that testing

Is completed

for both the grounding scheme

(FCR &T-0244-0-20) and the watt transducer

(FCR 87-02444-43)

modifications.

ARXSU

RXSU

At

tB

Respo

to Item 4

Page 5 of7

22.

The impact of the DFWLC setpoint modification (Work OQer ¹DDN2) on plant operation should be reviewed by reactor engineering and

Complete

operations to determine whether a revision to these setpoints is needed)

23.

Recommend

that engineering

ensure

that all ASD/DFW modifications planned for this outage

(Identified in section

7, Analysis) are

ARXSU

thoroughly reviewed using PDS-9 guidance including consideration of the recommendations from this Event Evaluation Report.

24.

Discuss the Impact of the causal factors of this event at an Engineering AllHands meeting.

Include the following in this discussion:

An event overview including fiindings of cause

The need for comprehensive review of Vendor supplied modifications,

How our mind set and other factors Impacted our ability to challenge certain assumptions during the ASD/DFW design phase,

Impact of the recent improvements in expectations for creating a challenging environment including positive reinforcement for staff

response to date,

Any changes to various Engineering Instructions or policies resulting from this review, and

Any other recommendations

deemed appropriate by management.

ARXSU

25.

As a part of Its overall Strategic Planning process,

Engineering

should (after the outage

concludes)

conduct a review session

using

brainstorming techniques to identify other potential mind set barriers that exist within the organization which hinder progressive thinking.

This session should include various levels of engineering staff and be designed to reward both the Identification of limiting assumptions and

suggestions to overcome those potential barriers.

The outcome should be documented

and functional suggestions

should be Incorporated

into engineering guidance documents and/or the Engineering Strategic Plan as appropriate.

ARXSU

Following (or as a part of) the session discussed

above, a review of current major modifications should be conducted to Identify any Impact

from the mind sets identified.

Design Engineering should review current engineering guidance documents (especially Engineering Standards

Manual PDS-9,) to ensure

ARXSU

that adequate guidance exists for reviewing:trip setpoints of interfacing systems, and industry experience with similar modifiicatlons

27.

While the Engineering Strategic Plan (as weil as recent changes to Project Review Group and Design Scoplng procedures)

establishes

a

foundation for improved standards

In this area, prior to initiating any major system tests Engineers and Operations should meet early ln the

design phase to identify and agree

on acceptable

standards

for the outcome of the test.

This guidance should be Incorporated

into

applicable procedures.

ARXSU

28

PDS-9 (put In place after the time frame discussed

here) addresses

the current expectatlons for the analysis and planning of new design

ARXSU

modifications.

Elsewhere

ln this report are suggested

changes to enhance

PDS-9.

Management

must ensure that PDS-9 Is properly

applied.

'T

~pe

Att

nt B

Response to Item 4

Page6of7

29.

Supply System personnel have become extremely knowledgeable on ASD/DFW through research, training, and experience over the life of'RXSU

the project. GE personnel contacted for this report described Supply System personnel as "some of the most knowledgeable ln the

Industry't

this point. The Team re'commends sending the system engineer to ASD school at the next available opportunity.

30

31

Engineering should review the existing Engineering Instructions to ensure that adequate

guidance ls provided regarding Supply System

ARXSU

involvement and overslgnt of vendor modifications. To be worked In conjunction with item 24 above.

Engineering and Training management

should review and agree to standards of Control Room Simulator fidelity. We recognize that the

ARXSU

Simulator was not intended as a modeling tool, but rather as a training tool and as such needs only to provide sufficient fidelityas to support

high quality training.

32

The Engineering Support Personnel Training Advisory Group (ESP TAG) should consider the benefit of training Design/Project Engineers on

ARXSU

the Impact of and considerations for changing a component design from a low precision (or analog) design to a high precision (or digital)

design.

Recommendations

from the IET

Item

33

Recommen dation

Date

Take action to inform the nuclear Industry, particularly the BWR 5 and 6 designs, of this potential via INPO networks and evaluate

its

ARXSU

reportability In accordance with regulatory requirements

34

The RRC pump cavltatlon protection requirements

and any modifications need to be reviewed consistent

with the plant operations

ARXSU

requirements and the experience gained as a result of the feedwater pump trip test.

The mind set that 'more conservative setpolnts are

better" needs to be carefully evaluated on a case by case basis.

Engineering should be tasked with the development of revised Interiock

setpolnt and or the time delay values to ensure design Intent Is achieved.

35

Engineering and operations perform a review of the design features of the DFW and ASD/RRC system under similar transient conditions to

ARXSU

ensure other operating parameters were not impacted by these changes.

36

Rerun Section 8.15 of PPM 8.3.339 after setpolnt modifications.

t'7

Response: The Supply System plans to rerun the feedwater pump trip test.

Initial conditions will be consistent with those required

by the WNP-2 Power Ascension Test Program, l.e. greater than 95% of thermal power. The testing Is planned to be performed as a

At

B

Res

Item 4

Page7 of7

part of power ascension

testing at the completion of Refueling Outage

12 and In accordance

with PPM 8.3.339.

The present

sequence

in the power ascension

testing schedule for this test Is as soon as practical after the completion of stable full power

operation and required 100% power calibrations and tests.

37

Senior management

should require accountability for the success of failure or functions or projects under their cognizance.

This should be

ARXSU

an element of each strategic plan as well as each short term task plan.

Senior management must set policy and performance expectations ln all areas and recognize the challenge ln Integrating complex changes

and interfacing with outside organizations.

38

The EET should analyze the plausible causes for the event and validate their findings.

RXSU