ML17292A803

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Insp Rept 50-397/97-04 on 970210-14.Violations Noted.Major Areas Inspected:Review of Tripping of Standby Service Water Pump 1A Due to Incorrect Overcurrent Relay Setting & Installation of Drywell Pressure Instruments
ML17292A803
Person / Time
Site: Columbia 
Issue date: 04/11/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17292A800 List:
References
50-397-97-04, 50-397-97-4, NUDOCS 9704170093
Download: ML17292A803 (16)


See also: IR 05000397/1997004

Text

NCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION I.V

Docket No.:

License No.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-397

NPF-21

50-397/97-04

Washington Public Power Supply System

Washington Nuclear Project-2

3000 George Washington Way

Richland, Washington

February 10-14, 1997

G. W. Johnston,

Senior Project Inspector

D. G. Acker, Senior Project Inspector

H. J. Wong, Chief, Reactor Projects Branch E

Attachment:

Supplemental

Information

9704K 70093 97041 i

PDR

ADOCK 05000397

8

PDR

EXECUTIVE SUMMARY

Washington Nuclear Project-2

NRC Inspection Report 50-397/97-04,

~En ineerin

~

A nonconservative

and erroneous

plant modification record (PMR) resulted in a

violation.

Design personnel failed to consider, during initial design, the safety

requirements

associated

with ensuring service water (SW) Pump 1A and the low

pressure

core spray (LPCS) pump would operate when required.

The licensee did

not act on available technical information which indicated that the associated

instantaneous

overcurrent (IOC) trips were set too low (Section E8.1).

~

After issuing the PMR, engineering

personnel twice noted conflicts with the UFSAR,

but took no action to review th'e PMR for additional conflicts, until one was noted

by the inspector (Section E8.1)

~

~

The installation of replacement

High Pressure

Core Spray (HPCS) initiation drywell

pressure switches without the required substitution evaluation was a violation .of

facility procedural requirements

(Section E8.2).

~

The'licensee staff had several opportunities to identify the deficient conditions for

both the overcurrent trip setpoints

and the replacement

HPCS initiation drywell

pressure switches.

These opportunities reflect on'the ability of licensee staff to

'ecognize

potential problems prior to their occurrence

(Sections

E8.1 and E8.2).

~

..

The licensee's

immediate corrective actions for both issues were prompt

(Sections E8.1 and E8.2).

Re ort Details

This inspection involved review of two events:

(1) the tripping of Standby Service Water

Pump 1A due to an incorrect overcurrent relay setting; and 2) the installation of drywell

pressure instruments which were not properly vented and resulted in degraded

performance.

III. E

ineerin

ES

Miscellaneous Engineering Issues (92902)

E8.1

Closed

Licensee Event Re ort

LER 50-397 96-009:

miscalculation of

instantaneous.overcurrent

relay settings resulting in inoperability of safety-related

equipment.

The licensee identified that the supply circuit breaker to the motor for Standby

Service Water (SW) Pump 1A tripped on December 20, 1996, during a routine

attempt to start the pump.

The licensee determined that the circuit breaker was

tripped due to actuation of the circuit bre'aker's

IOC relay.

The licensee determined

that the setpoint for the IOC relay had.been

reset in

November 1996 based on calculations using an ina'ccurate locked rotor current and

nonconservative

selection of.a multiplication factor.

Between November 1996,

when the IOC was reset, and the December 20, 1996; failure, the pump had been

successfully started seven times.

Postmaintenance

testing included bench

testing'f

the, relays and a successful

pump start,

The licensee reset the IOC relay trip

setpoint and successfully started the pump.

The licensee identified the root cause

as use of inappropriate design input for

determining the IOC setpoint.

As a result of the trip of SW Pump 1A, the licensee requested

and,the NRC

approved the use of enforcement discretion to discontinue repetitive testing of

emergency diesel generators.

This'approval was documented

in a letter to the

licensee dated Decemb'er 24, 1996.

a.

Ins ection Sco

e

The inspector reviewed the LER, the plant modification associated

with the initial

change

in the IOC relay setpoint, associated

calculations and circuit breaker

coordination studies, industry standards for selection of IOC setpoints,'he

licensee's operability and root cause evaluations,

and discussed

this information

with licensee employees.

b.

Observations

and Findin s

The inspector noted that normal plant electrical protective device coordination

requires IOC relays for tripping individual pump circuit breakers for pump and cable

faults.

Proper coordination requires that the IOC relays be set to trip the pump

0

-2-

circuit breaker before circuit breaker(s) supplying the entire bu's trips.

However, the

IOC relays needed to be set high enough to ensure that they did not trip during

starting of the pump.

Starting current for pumps is normally estimated

using vendor

locked rotor test data, general motor design data, or actual starting current

measurements.

Based on past licensee evaluations.and

NRC inspections,

the licensee determined

that the coordination of their plant circuit breakers could be improved.

On

January 30, 1996, the licensee approved

PMR 85-0528-0, "Protective Relay

Coordination Study and Installation," to reset or change

a number of protective

relays to improve overall plant protection from electrical faults.

This PMR was

based

on calculations issued in 1993.

The licensee stated that they received locked rotor current test data from General

Electric (GE) for a number of plant pumps.

Some of this data was'locked rotor

current for a test at 20 percent of rated voltage, some of it was locked rotor current

data at 80 percent voltage, and some of the data was GE's projecte'd locked rotor

current at full voltage based

on tests and an unspecific'd multiplication factor.

For the SW Pump 1A, GE'provided

a locked rotor current (LRC) value at

approximately 20 percent rated voltage.

The licensee extrapolated the locked rotor

current at 100 percent voltage by multiplying the current at 20 percent voltage by a

linear factor and de'termined the LRC was 960 amps.

Motor starting c'urrent is dependent

on the locked rotor current and additional

variables such as direct current offset and line voltage.

Therefore,

IOC trips 'are set

at some value above locke'd,rotor current that will ensure that the IOC trips "willnot

activate during pump starting.'merican-National

Standards

Institute/Institute of

Electrical and Electronics Engineers

(IEEE) C37.96-1988,

"IEEE Guide for AC

[alternating current] Motor Protection," recommends

th'at the IOC trips be set at

locked rotor. current multiplied by 1.65 to 1.875.

Other technical guides

'ecommend

use of locked rotor current multiplied by.1.7 to 1.8.

The licensee chose

to use 1.65 times locked rotor current for their safety-related

and balance-of-plant

pumps.

As noted above, SW Pump 1A tripped on IOC during a routine start

attempt after its IOC relay trip value was lowered.

Data was available to the licensee which indicated that the setting chosen by the

licensee co.:ld be too low including:

IEEE Standard 112-1991,

"IEEE Standard Test Procedure for Polyphase

Induction Motors and Generators,"

states that locked rotor current taken at

low voltage levels could not simply be multiplied by a linear factor to

determine locked rotor current at 100 p'ercent voltage due to changes

in"

reactance.

3

The motor nameplate

and design drawings provided for the SW Pump 1A

motor indicated locked rotor current was 1330 amps or approximately

'0

per'cent higher than the value calculated by the licensee.

The value of locked rotor current calculated by the licensee provided

a ratio

of locked rotor current to running'current which was approximately 4.5, a

very low value for this size and type of motor.

The licensee was operating the motors at 4160 volts nominal, while their

calculated lock rotor current was based on 4000 volts.

Since the starting

current will increase with increased

voltage, the calculated IOC.trip point

was based

on a voltage which was approximately five percent low.

The licensee was using the lowest multiplication factor (1.65) recommended

by industry.

The inspector reviewed the above information with the licensee,

The licensee

acknowledged that they had information which could have alerted them to the

potential for improper setting of the SW Pump 1A IOC relay.

However, licensee

representatives

stated that they believed the primary root cause of the problem was

that in attempting to provide the best circuit breaker coordination, they lost sight of

fhe fact that the important safety function of SW Pump 1A was to operate

and that

they should have set the IOC at a higher industry recommend

value, which would

also provide adequate

circuit breaker coordination.

The inspector agreed that this

was an important contributor to the event.

I

The licensee subsequently.

measured

the starting current for SW Pump 1A.and

determined that it was approximately 1350 amps,

The inspector determined that IOG trip setting was incorrectly set in that the setting

would not always ensure that SW Pump 1A would start when required, and had

caused the pump.to fail and be declared inoperable on December 20, 1996.

Failure

to correctly set the'OC relay to ensure SW Pump 1A operability is a violation of

10 CFR Part 50, Appendix B, Criterion III, Design Control (Violation 50-397/97-04-

01).

The inspector noted that the IOC for the LPCS Pump was set as low as SW

Pump 1A and was potentially susceptible to tripping during pump starting.

The

licensee reset the IOCs.

There were no other IOCs for. safety-related

pumps set as

low as these two pumps, partly since no safety-related

pump IOCs had been 'reset

for Train B safety-related

pumps.

The inspector reviewed circuit breaker

coordination associated

with the SW 1A and LPCS pumps and concluded, that the

, new IOC settings provided adequate

circuit breaker coordination with bus supply

~

circuit breakers.

-4-

After the trip, the licensee had reset the IOC for SW Pump 1A to 2100 amps;

approximately 1.5 times the measured

locked rotor current of 1350 amps.

The

inspector reviewed the UFSAR and determined that Section 8.3.1.1 stated that the

IOCs were set to trip at approximately two times locked rotor current.

The

inspector considered that this was not the sa'me as described

in the UFSAR.

The

IOC for the LPCS Pump was also set lower than two times locked rotor current.

The inspector reviewed PMR 85-0528-0 and the licensee's

design control

procedures

and determined that the design control procedures

required a.review of

'he

UFSAR to determine if the design affected anything in the UFSAR; however, in

January 1996 licensee personnel checked

a step in'dicating that the UFSAR was not

affected by the PMR. The inspector considered that since the licensee's objective

on thesetpoint change was to provide improved breaker coordination, lowering the

IOC setpoint would be an expected result. At most, a more complete review of the

UFSAR would have most likely resulted in only an updated

UFSAR page and not a

more accurate calculation of the IOC setpoint.

The inspector reviewed changes

associated

with the PMR and noted that two

separate

changes,

issued in 1996, identified two other conflicts between the PMR

and the UFSAR, which the licensee resolved.

The inspector discussed

review of the

UFSAR with licensee personnel.

The licensee issued

a problem evaluation

request

(PER) to compare the PMR to the UFSAR and resolve any differences.

c.

Conclusion

The inspector concluded that the present IOC setpoints for SW Pump 1A and the

LPCS Pump were coordinated with upstream circuit breakers, but were

nonconservative

with respect to motor testing currents.

The inspector concluded that the original PMR was flawed in that licensee design

personnel failed"to consider, during initial design, the safety requirements

associated

with ensuring SW Pump 1A arid LPCS pumps would 'operate when required and did

not act on available technical information which indicated that the associated

IOC

trips were set too low. Failure to establish appropriate circuit breaker trip setpoints

to ensure reliable operation of SW Pump 1A is a violation of 10 CFR Part 50,

Appendix B, Criterion III, Design Control.

'n

addition, after initial issue of. the PMR, engineering

personnel twice n'oted

conflicts with the UFSAR, but took no action to review the PMR for additiorial

conflicts, until one was noted by the inspector.

In summary, the inspector concluded that engineering

performance associated

with

this PMR was weak.

-5-

E8.2

Closed

LER 50-397 96-008:

failure.to comply with a Technical Specification

action requirement for the emergency

core cooling system actuation instrumentation

due to unidentified inoperability condition.

The licensee identified that drywell pressure switches, designed to initiate the High

Pressure

Core Spray (HPCS) on high drywell pressure,

had exceeded

their Technical

Specification allowable values on several occasions

during the period from June'10

through November 24, 1996.

The original pressure switches had been replaced by newer models in April 1996,

during

Refueling'Outage

R11.

The switches that were installed had a loss-of-

coolant accident (LOCA) seal and a vent plug installed on the instrument housing.

The vent plug had not been removed as required for the instaflation.

It was

subsequently

determined that the failure to remove the vent plug allowed

temperature

variations in the reactor building to affect the setpoint of the pressure

switches.

The licensee determined the root cause of the event to be an administrative

deficiency in the control on the issuance

o'f the p'ressure switches for use.

A PMR

had been initiated in 1984 that would have initiated the engineering

analysis of the

replacement

pressure switches; however, the PMR was cancelled in 1989.

With no

process tie between the PMR and the pressure switches, the installation in 1996

went forward without an engineering

ev'aluation of the substitution.

ao

Ins ection Sco

e

The irispector reviewed the LER, the'MR associated

with the installation of the

,. drywell pressure switches, the substitution evaluations performed, design

documents,

work packages

associated

with the installation of the pressure

switches, the licensee's

operability and root cause evaluations,

and discussed

this

information with licensee employees.

b.

Observations

and Findin s

The licensee performed an evaluation of setpoint drift on December 5, 1996, related

to drywell Pressure

Switches MS-PS-47B and 47C (used for actuation of HPCS on

high drywell pressuie).

The evaluation was prompted by several instances where

the switches failed administrative calibration limits during surveillance tests and

were required to be recalibrated.

The evaluation was documented

in PER 296-

0829.

The PER determined that 'the drywell pressure switches were installed with

the instrument cover vent plugs left in place.

The PER also determined that the

switches were operable at the time of the evaluation.

However, the PER indicated

they had possibly been inoperative during several periods since their installation;

Due to that evaluation,

LER 50-397/96-008 was issued.

-6-

In 1984,'PMR 8'4-1125-0 was written to replace

a Static 0-Ring (SOR)

12NAA5X10TT.(referred to hereafter as TT) pressure switch installed as a drywell

pressure switch for actuation of the HPCS System.

The TT switch could not be

procured as a Quality Class

1 component.

However, SOR Pressure

Switch 12N6BB4NXCIAJJTTX6 (referred to hereafter as X6) was available as a

- Quality Class

1 component.

The primary difference between the switches was the

provision for a loss-of-coolant accident seal or an air tight conduit connection

and a

vent plug installed on'the instrument case for the X6 switch.

In 1988, SOR

Corporation issued

a I art 21 notification"for the X6 switch due to

process'ermeation

through the kapton diaphragm that affected setpoint drift. A revised

version of SOR 12N6BB4NXCIAJJTX12 (hereafter referred to as X12) replaced the

kapton diaphragm with a stainless steel diaph'ragm.

March 9, 1989, Substitution Evaluation 567, Revision.0; was issued to evaluate the

difference between the'stook of X6 switches and the newer X12 model.

The

.

evaluation noted that a PMR was re'quired to install the X12 version.

No procedural

requirement existed at that time to place

a limitation on use in the Material

Management

System (MMS)..

Subsequently,

on August 3, 1989, PMR 02-84-1125-0 was voided.

A note on the

PMR states

"SOR being revised to SS diaph. per RFTS 89-03-094" and "will

address switch replacement

as required."

No reason was given for cancellation of

the PMR.

Later, on February

1'2, 1990, a purchase

order was issued to return three

X6 switches, have them modified to X12 versions, and acquire eight new X12

, switches.

On June 'l5, 1991, Procedure

SPES-1, Section 7.47; was issued, requiring that a

limitation on use be placed on any item being procured as part of a PMR prior to a

Basic Design Change being approved.

This would place in.the MMS a notation that

the item required an engineering review prior to its use in the plant.

This procedure

change would, under current circumstances,

require that any equipment proc'ured

~ for replacement stock that was not identical to the installed equipment be restricted

with a limitation on use.

On December, 8, 1995, four X12 switches were issued for replacement of installed

, drywell pressure switches under work orders (WO) YT4401 and WO YT4501.

These WOs were generated

on April 17, 1996, as routine replacement for

environmental qualification requirements.

The inspector examined the WO,

identifying that the task required

a replacement of flexible conduit for the

'nstallation

of the new switch.

This is becaus'e the TT model installed in the plant

does not have a sealed electrical conduit connection.

The inspector noted that the

WOs requirement for extra work, specifically the conduit. replacement,

provided an

opportunity for the preparer to identify'the possible need for an engineering

evalu'ation.

-7-

Two more opportunities occurred in June 1996 for identifying the need for

engineering

evaluations.

June 4, 1996, Substitution Evaluation 2293, Revision 0,

was issued to address the replacement of the now obsolete X12 pressure switch

with an newer version.

This substitution evaluation was released for review

January 30, 1996.

While recognizing that the preparer was not required to evaluate

prior substitution evaluations

or review previous limitations on use, had the'preparer

of this substitution evaluation noted that Substitution Evaluation 567 required a

PMR for installation, the necessity for a limitation on use in the MMS may have

become apparent.

Further,

a revision to setpoint Calculation E/I-02-92-1072 for

the'PCS

drywell pressure switches, was issued on June 6, 1996, that reflected

changes

due to the replacement of the pressure switches.

The previous calculation

(for the installed switches) stated that the switches were subjected to a walkdown

to verify a vent path existed.

The licensee noted that although the walkdown

comment was included in the revision barred section of the calculation, no

verification walkdown was conducted.

Although the configuration of the original

pressure switches included the vent plug, a walkdown may have noted the need for

a vent path due to the inclusion of the LOCA seal in the replacement

switches'.

Therefore

a walkdown may have resulted in the identification of the need to vent

the instrument housing.

WO YT4401 was signed off as completed. for installation April 29; 1996, for

Instruments MS-PS-47A and 47C.

Final signoff occurred June 6, 1996.

WO YT4501 for installation of Instruments MS-PS-47B and 47D signed as

completed on April 26, 1996, and final sign off occurred July 7, 1996.

The

inspector examined the WOs and fou'nd them to be complete:

Initial calibrations

were done for both sets of switches'with no notations of a problem in either case.

There was no information supplied in either package of a substitution evaluation.

Further, it appeared

that no reliance was made of prior substitution evaluations.

The requirement to perform substitution evaluations

is described

in Plant Procedure

Manual (PPM) 1.15.12, Section 8.4, Revision 0, "Substitution Evaluation," and a

subtier Procedure

SPES-1, Sect)on 6.7, Revision 1, ".Substitution Evaluations."

PPM 1.15.12 states,

in part, under 8.4.2, "Determination of Need," "Where

desirable or necessary

to procure or use substitute items, it is the responsibility of

the user to request an evaluation by. Material, Technical and Quality prior to

procurement or use

~ .." Further, Procedure

SPES-1, Section 6.7.A, states,

in part,

that "Substitution evaluations

are performed on safety-related

and augmented

quality class (other than'Flag 1M) items per PPM 1.15.12 to assure the alternative

replacement

item is an acceptable

substitute."

Contrary to this, a substitution

evaluation was not requested

to be performed for the installation on April26 and

29, 1996, of replacement

HPCS drywell pressure Switches MS-PS-47A, 47B, 47C,

and 47D. This is a violation of the requirements of Technical Specification 6.8.1a

for failure to implement the requirements

of PPM 1.15.12 (Violation 50-397/97-04-

02).

0

0

-8-

Following installation of the X1.2 replacements,

the switches were subjected

periodic surveillance tests in accordance

with Surveillance Procedures

7.4.3.3.1.53

"HPCS Initiation Drywell Pressure

High A & C - Channel Function Test/Channel

Check (CFT/CC)," and 7.4.3.3.1.54

"HPCS Initia'tion Drywell Pressure

High B 5, D-

CFT/CC." These procedures

had administrative limits of 38.0 to 49.0 inches of

water (1.37 psi and 1.77 psi respectively), with a nominal setpoint of 45.7 inches

of water (1.65 psi).

T. S. 3.3.3 specifies an allowable actuation setpoint of

1.85 psig.

For the period from April 1996 through November 1996 there were six

. occasions

when a switch failed to meet the administrative limits. In four of those

occurrences,

a switch failed to meet the administrative limit by being over the

acceptance

criteria.

On two occasions the switches were below the acceptance

criteria.

Only one occurrence

on June 30, 1996, involving Switch MS-PS-47C, was

over the Technical Specification requirement of 1.85 psi, at 1.899 psi ~

Corrective Actions - Following the determination on December 5, 1996, that the

reliability of the HPCS drywell pressure switches was.questionable,

the licensee

took immediate action to remove the vent plugs. from the instrument cases

and

verify the setpoints in'accordance with the Channel Functional Test Surveillance

Procedures

7.4.3.3.1.53

and 7.4.3.3.1.54.

The licensee's

actions restored the

~

instrument to their intended configuration.

Other instruments

in the facility were

also inspected to assure the proper venting for similar instruments;

none were

deficient.

PER 296-0829 and,the corrective action'plans associated

with the, PER were

reviewed by the 'inspector to de'termine the adequacy

of the scope of the evaluation

of the event and the long term corrective actions.. The licensee indicated that all

open or voided PMR's, which required procurement of c'omponent level materials to

implement, will be reviewed to determine if there were materials requiring

substitution evaluations that were not captured

in the, Material Management

System

with limitations on use.

These actions appear to address the significant issues

related to the installation of replacement components

by ensuring that similar

circumstances

are not repeated.

P

Conclusion

The inspector concluded the licensee had several opportunities to.capture the fact

that replacement

HPCS initiation drywell switches had not been subjected to

engineering

analysis for substitution.

These opportunities reflect on the ability of

licensee staff to recognize potential problems prior to their occurrence.

The installation of replacement

HPCS initiation drywell pressure switches without

the required substitution evaluation was a violation of procedure

PPM 1.15.12.

The licensee's

immediate corrective actions were prompt and effective.

Long-term

corrective actions'appear

to provide assurance

that possible similar situations will

'be appropriately identifiqd.

1

-9-

IV. IVlana ernent IVleetin s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management

after

the conclusion of the.inspection on March 19, 1997.

The licensee acknowledged

the

.

findings presented.

The inspectors

asked the licensee whether any materials examined during the inspection

should be considered

proprietary.

No proprietary information was identified.

ATTACHMENT

Supplemental

Information

PARTIAL LIST OF PERSONS CONTACTED

Licensee

P. Bemis, Vice President for Nuclear Operations

R. Webring, Vice President Operations Support

L. Fernandez,

Licensing Manager

B. Pfitzer, Licensing Engineer

G. Smith, Plant General Manager

J. Swailes, Engineering Director

D. Swank, Regulatory Affairs Manager

INSPECTION PROCEDURES USED

IP 92903

Followup - Engineering

ITEMS CLOSED

LER 50-397/96-008

LER 50-397/96-009

LIST OF ACRONYMS USED

CFT/CC

FSAR

GE

HPCS

IOC

'LER

LPCS

MMS

NRC

'PER

PMR

PPM

SW

UFSAR

WNP-2

WO

channel functional test/channel

check

Final Safety Analysis Report

'eneral Electric

high pressure

core spray

instantaneous

overcurrent

licensee event report

low pressure

core spray

material management

system

U.S. Nuclear Regulatory Commis'sion

problem evaluation request

plant modification record

plant procedure

manual

service water

Updated Final Safety Analysis Report

Washington Nuclear Project-2

work order