ML17285A106

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Insp Rept 50-397/88-24 on 880822-0902.Violations Noted. Major Areas Inspected:Maint,Engineering & QA Activities Re Emergency Diesel Generator Sys & Nuclear Steam Supply Shutoff Sys
ML17285A106
Person / Time
Site: Columbia 
Issue date: 11/15/1988
From: Dangelo A, Fiorelli G, Paul Prescott, Richards S, Samworth R, Tatum J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17285A104 List:
References
50-397-88-24, NUDOCS 8812120003
Download: ML17285A106 (40)


See also: IR 05000397/1988024

Text

4

U. S.

NUCLEAR REGULATORY COMMISSION

REGION

V

Report No.

Docket No.

50-397/88-24

50-397

License

No.

Licensee:

Facility Name:

Inspection at:

NPF-21

Washington Public Power Supply System

P. 0.

Box 968

Richland,

Washington

99352

Washington Nuclear Project No.

2 (WNP-2)

WNP-2 Site,

Benton County, Washington

Inspection conducted:

August

2 - September

2,

1988

Inspectors:

.

D

nge o,

n>or

es> ent

nspector

Team Leader

il rs

E/'e

gne

Approved By:

J.

atum,

ess

ent Inspector

lore

s,

e

s

t

nspector

NP7

rescott,

R

amwort

,

Other Accompanying Personnel:

B. L. Collins,

NRC Contractor,

INEL

sc

ar s,

)e

,

ngsneersng

ection

i> - is -88

ate

sgne

ll- 8'-88

ate

Soigne

l/ / ~ f'J

a

e

sgne

d'P

te

sgne

ate

sgne

Ins ection

Summar

Ins ection

on Au ust

22 - Se tember

2

1988

Re or t No. 50-397 88-24

~AI

I:

A I 11,

I

I I

I

I I

maintenance,

engineering

and

QA activities

as they relate primarily to the

EDG

system

and the Nuclear Steam Supply Shutoff System.

SSi2120003

88i123

PDR

Anger.v n~nnnzev

Results:

General

Conclusions

and

5 ecific Findin s:

1.

Control of work activities and operations is weak resulting in activities

being conducted

and documented in an informal manner.

2.

Plant problems

are not being adequately identified at the working level.

3.

The followup of identified plant problems is not aggressive..

Additionally, see Appendix B, Areas Inspected

and Results

Summar

of Violations Identified:

1.

Failure to follow procedures

when revising a surveillance procedure.

2.

Failure to report to the

NRC two Reactor Protective

System actuations.

3.

Failure to follow procedures

in reterminating electrical

connections

during maintenance.

~

~

~

~

~

~

~

~

~

4.

Failure to promptly determine the affect of the out of calibration status

of testing equipment.

0 en Items

Summar

Four new items open,

none closed.

4

>>

DETAILS

1.

Persons

Contacted

a.

Washin ton Public Power

Su

1

S stem

"C.

M. Powers,

Plant Manager

"R.

L. Webring, Manager, Assistant Maintenance

"A. L. Oxsen, Assistant

Managing Director, Operations

"J.

W. Baker, Assistant

Manager,

Nuclear Plant

"M. R. Wuestefeld,

Supervisor,

Plant Engineering

"G.

D. Bouchey, Director, Licensing and guality Assurance

"A. G. Hosier, Manager,

Project Licensing

WNP2

"L. T. Harrold, Manager,

Generation

Engineering

"W. D. Shaeffer,

Assistant

Manager,

Operations

Nuclear Plant

"S.

L. McKay, Manager,

Operation Nuclear Plant

D.

S.

Feldman,

Supervisor,

Mechanical

Maintenance

E.

R.

Ray, Supervisor,

Instrument Maintenance

T.

W. Albert, Engineer,

Instrument Maintenance

J.

0.

Cooper,

Engineer,

Mechanical

Maintenance

S.

L. Gupta,

Engineer,

Principal guality Control

B. Pesek,

Engineer,

Systems

b.

USNRC

"B. F. Faulkenberry,

Deputy Regional Administrator,

RV

"S.

A. Richards,

Chief, Engineering Section,

RV

Denotes

those attending the final exit meeting

on September

2, 1988.

The inspectors

also contacted

licensee

operators,

engineers,

technicians,

and other personnel

during the course of the inspection.

2.

Sco

e and Pur ose of the Ins ection

This team inspection evaluated

the material condition, performance,

maintenance,

design modifications

and operating procedures

of WNP-2 as

they relate primarily to two selected

systems.

The Emergency Diesel

4

Generator

(EDG) system

and the Nuclear Steam Supply Shutoff System

(NS )

were selected

by the team for review.

Generic precursor data associated

with the systems

under review was evaluated

by the team to determine if

the lessons

learned 'regarding potential

system degraded

performance

had

been addressed

by the licensee.

Observations

of operator performance

both inside and outside of the

control

room were conducted

by the team.

Maintenance

and surveillance

activities were observed for compliance with written instructions

and

procedures,

and for documentation of work which was actually performed.

The material condition of the plant was assessed

by comparing the as

found equipment status with documented

procedures,

drawings,

specifications,

vendor data

and past documented

industry experience.

3.

Performance

of the 0 eratin

Crews

The team performed several

plant tours

and verified the operability of

the emergency

diesel

generator

system,

reviewed the tag out log,

operators'ogs

and verified proper return to service of components.

Particular attention

was given to housekeeping,

examination for potential

fire hazards,

and fluid leaks.

The team observed that operational activities were conducted in a

professional

manner,

and the operations staff appeared

to be dedicated

and displayed

a good attitude towards the performance of their duties.

Although the licensed operators

appeared

to be very experienced,

the team

observed

'a number of weaknesses

in the execution of the licensee's

programs.

Additional definition of this concern is included in

paragraphs

3.a through 3.d below:

The team reviewed the Control Operator

and Shift Manager log entries

and verified that logs were being kept in accordance

with

Administrative Procedure 1.3.4, titled "Operating Data and Logs"

(Revision

9 dated April 17, 1987),

and verified that Technical

Specification action requirements

and mode restraints

were complied

with for selected

safety related

components.

Although no

discrepancies

were identified, the team noted the following

weaknesses:

Entries in the Control Operator's

log were often abbreviated

and did not provide much detail, making subsequent

log reviews

cumbersome

and time consuming.

Significant plant problems

and inoperable

equipment which could

have

some impact on Technical Specification requirements

were

not highlighted and carried forward, such that this information

was not readily available.

A formal system did not exist for tracking inoperable

equipment

to assure

compliance with Technical Specification action

statements

and mode restraints.

The team discussed

these observations

with the Operations

Manager,

who acknowledged the team's

comments

and stated that programmatic

improvements in these

areas

were currently being considered.

During review of the control

room logs, the team observed that the

following actuations of the reactor protection system

(RPS) occur red

and were not reported to the

NRC:

At 0844 on May 29, 1988, during Mode 5 operation,

an

RPS

actuation

occurred during initial testing of the alternate

rod

insertion (ARI) system.

The

RPS actuation occurred

when air

pressure

bled off the scram valves after the ARI system

was

placed in the test

mode

and the scram air header

was isolated.

Although the Shift Manager's

log stated that this action is

normal with supply air off during the initial testing of ARI,

it appeared

that this conclusion

was reached after the

RPS

actuation occurred.

The team reviewed the procedure

which was

used for testing the ARI system

(TP 8.3.94)

and discussed

the

actuation with the cognizant engineer.

The team concluded that

the

RPS actuation

was not anticipated in the test procedure,

and control rod drive air system

leakage

was

an abnormal

condition which resulted

from undocumented air system leaks.

At 1553 on August 26, 1988, during Mode

5 operation,

an

RPS

actuation occurred

when Division II RPS power was transferred

from alternate to normal.

The Shift Manager's

log made

reference to nonconformance

report

(NCR) 288-379,

and the

Control Operator's

log stated that the actuation

was

due to

switch over-travel.

NCR 288-379 stated that this event was not

reportable

because it occurred during equipment testing.

The

Operations

Manager stated that a similar event was reported to

the

NRC which had occurred

on August 25 when Division I RPS

power was transferred

from alternate to normal.

The

RPS

actuation that occurred

on August 26 was

due to subsequent

testing

and was not felt to be reportable.

The team observed

that the control

room logs did not indicate that testing

was

in'rogress

at the time of the

RPS actuation,

and the licensee

could not produce

a maintenance

work order or other

documentation to demonstrate

that testing

was in progress

during the August 26 event.

10

CFR 50.72 requires the licensee to report

RPS actuations

which

are not part of a preplanned

sequence within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of actuation.

The licensee's

assessment

of the reportability of these

events

was

incorrect,

and the required 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> reports

were not made to the

NRC.

Failure to report these

events is an apparent violation

(50-397/88-24-01).

Housekee in /Material Plant Condition

While making rounds with equipment operators

and during general

plant tours, the team

made the following observations

relative to

housekeeping

and material plant condition:

The team toured the drywell during the inspection.

The drywell

was accessible

because

the unit was shutdown for an unscheduled

outage.

Equipment in the drywe11 did not appear to be well

preserved

in that there appeared to be excessive

rust on piping

and other

components.

Following the last scheduled

outage,

miscellaneous

debris

such

as fire retardant

covers,

a plastic

bag fashioned into a seat cushion,

and a pair of goggles,

had

not been identified and removed from the drywell.

The team

also observed that a grounding cable

had been left attached to

one of the reactor vessel

instrument nozzles.

It was

apparently

a remnant from startup testing.

The cap was noted

to be missing from an electrical

connector for temperature

element

CMS-TE"52 used to measure

upper return ring header air

temperature

in the drywell at the 575 foot elevation.

With the

exception of the rust and the grounding cable,

the licensee

stated that these conditions would be corrected prior to

startup

from the current outage.

Felt tip pen was

used extensively for component identification.

In addition, graffiti was prevalent throughout the plant.

Licensee

management

acknowledged

the teams

concern

and stated

that a program was being developed to address

plant labeling.

In addition, painting of the facility was in process

during the

inspection.

Electrolyte levels for many of the batteries

used for emergency

lighting were not properly maintained.

For example, batteries

441/2

~ 441/7 ) 441/8 j 441/9 )

SWA7 1X )

SWA7 2X )

SWA5 6

SWA6 4

and

SWS3-3 were all low on electrolyte level.

The team noted

that Electrical Maintenance

Procedure

10.25.63, titled

Emergency Lighting Inspection

(Rev.

3 dated

June 17, 1988)

identified batteries

SWA7-1X and

SWA7-2X as 8-hour units

required to satisfy the requirements

of 10CFR50 Appendix R.

The licensee

stated that Electrical Maintenance

Procedure

10.25.63 would be changed to include verification of proper

battery electrolyte level.

Housekeeping

deficiencies

outside the drywell included several

instances

where ladders

were not properly stowed,

one instance

where a liquid nitrogen bottle was left on a dolly unsecured

and unattended,

a large accumulation of trash

on the 467'evel

of the radwaste building, and many observations

where tools

were not properly stored.

Transformer TR-7A-A (DIV 1) circuit lM-7AA-150-1 was missing

a

condulet cover,

and a grounding cable

near

MCC-8C-A was not

secured.

Handwheels

were not secured

on valves

RHR-PI-VX-74A,

RHR-PI-VX-74B and HPCS-V-69.

Breaker indicating lights were not working for high pressure

core spray

(HPCS) diesel

generator

(DG) room fan DMA-FN-31 and

HPCS

DG oil transfer

pump DO-P-2.

The licensee

stated that the

indicating lights were burned out and that the bulbs were

subsequently

replaced to resolve the problem.

The team discussed

these observations with station management,

noting that a program for maintaining adequate

plant material

condition did not appear to have been established.

Although the

licensee

had undertaken

maintenance efforts to repair

known

deficient conditions

and

had begun to paint the power block,

no

comprehensive

program exists to establish

minimum requirements for

maintaining of material plant conditions.

d.

Formalit

and Attention to Detail

In addition to the housekeeping

and material plant condition

observations

discussed

in paragraph

2.c above,

the team identified

the following examples of informality and inattention to detail:

The shift brief that was conducted

by the Control

Room

Supervisor

on August 27, 1988, included mention of a

waterhammer that occurred in the residual

heat

removal

(RHR)

system.

The team observed that the cognizant engineer

was

present in the control

room evaluating this event.

While making

rounds with the equipment operator later during the shift, the

team observed that a waterhammer

occurred

when

RHR pump

B was

started.

The team also observed that

RHR pump

B was rotating

backwards for a pe} iod of time when the system

was being

aligned initially for operation.

Although the cognizant

engineer

was

made

aware of the

RHR waterhammer

problem, the

team observed that a log entry was not made regarding this

problem and resolution of the problem was not being pursued in

a formal manner.

In addition,

upper station

management

was not

made

aware of the waterhammer

events in a timely fashion.

In response

to the team's

concern over the pump shaft rotating

backwards

and the apparent water hammer,

the licensee

began

an

'nvestigation

which included the disassembly

and inspection of

the

RHR pump discharge

check valve.

The licensee

discovered

during the internal valve inspection that the disk of the check

valve was in the open position and did not close.

The

RHR pump discharge

check valves are tilting disk Anchor

Darling valves.

The disk of these

valves rotates

about

a pin,

such that the disk remains in the flow stream.

However,

upon

rotation the cross sectional

area of disk which obstructs

flow

is reduced to a minimum.

When fluid flow is reduced or

stopped,

the buoyant force which had been acting on the disk is

reduced or removed.

This would cause the disk to rotate or

tilt back into the closed position.

The check valve disk, when opened

by fluid flow, is pressed

against

a stop which was designed to ensure

the disk's center

of mass is always

ahead of the disk pin.

Therefore the disk

would tend to close

based

on the disk's

own deadweight.

During

the valve inspection,

the licensee

discovered that the disk

stop did not interrupt the disk travel until the disk's center

of mass

was apparently directly over the disk pin.

This

apparently

caused the disk to become balanced

on the disk pin

and when fluid flow stopped,

the disk did not close.

In

addition, the disk remained

open against reverse flow which

apparently occurred

when the

RHR pump's shaft was observed to

be rotating backwards.

When clearance

order 88-8-106 was being implemented,

the

equipment operator could not locate

a fuse that was called out

as part of the clearance.

The inspector observed that drawing

24E005

(Rev 7) indicated that the fuse was located in

instrument rack 67, but the fuse was subsequently

found in a

terminal

box associated

with instrument rack 67.

The inspector

also observed that approximately

12 circuits were left

abandoned

in instrument rack 67,

and the circuits were not

labeled

as to their current status.

Actions were not taken

by

operations

personnel

to formally document

and resolve these

discrepancies.

During emergency diesel

generator

(DG) ¹1 surveillance testing

that was conducted

on August 26, 1988, the inspector

observed

that

a yellow oil-like substance

was floating in the cooling

water of the

DG cooling water expansion

tank sight glass.

The

inspector also observed that after the diesel

was started,

the

governor oil levels did not drop to the sight glass midpoint

scribe mark which was the nominal level specified by the

surveillance

procedure

(a tolerance

band was not specified).

These conditions were not questioned

and were not documented

by

the equipment operator.

The team discussed

the above observations

with the licensee.'t

appeared

that the licensee

recognizes

the

need for more aggressive

program

development

and implementation.

Recent

changes

in station

management

have

been

made in an effort to improve performance,

and programmatic

improvements

are currently being considered.

One violation was identified as discussed

in paragraph

3.b above.

4.

Surveillance Activities

The team observed

in"process surveillances

on the diesel

generator

and

the drywell sump flow monitor for attention to detail in following the

written instructions provided and in recording the data obtained

from the

surveillance.

There appeared

to be a rigorousness

by the control room

personnel

in following surveillance procedures.

However,

a surveillance

and in-process trouble shooting was observed

by the team for the drywell

sump monitor where such rigor was not apparent.

a 0

Diesel Generator ¹I Monthl

Surveillance

On August 26, 1988, the team observed the monthly operational

surveillance of the ¹1 emergency diesel

generator

(DG).

The

surveillance

was conducted in accordance

with Surveillance

Procedure

7.4.8. 1. 1.2.1, titled "Diesel Generator ¹1 - Monthly Operability

Test"

(Rev. ll dated August 25, 1988).

Although the surveillance

was performed satisfactorily, the team observed that a yellow

oil-like substance

was floating in the

DG cooling water expansion

tank sight glass.

The team also observed that after the diesel

was

started,

the governor oil levels did not drop to the sight glass

midpoint scribe

mar k which was the nominal level specified by the

surveillance

procedure

(a tolerance

band was not specified).

These

conditions were not questioned

and were not documented

by the

equipment operator (also discussed

in paragraph

3.d of this report).

In order to resolve the teams'oncerns,

maintenance

work request

I

b.

(MWR) AT6682 was initiated to remove any foreign substance

from the

DG cooling water system

and the

DG was started

so that adjustments

could be made to the governor oil levels.

The licensee

stated that

the surveillance

procedure

would be changed to provide more

definitive guidance with regard to the governor oil levels.

Dr well

Sum

Flow Monitor Calibration

On August 24, 1988, the team observed that instrument

and control

(I8C) technicians

were making adjustments

to the drywell sump flow

monitor calibration.

Procedure 7.4.4.3.1.4, titled "Drywell Sump

Flow Monitors - CC" (Rev. 3, including Deviation 88-538 dated

June.

ll, 1988),

was being used to perform this activity.

The licensee

had determined that the flow indicated by the monitor was

inaccurate.

The actual flow rate from the drywell sump

was being

measured periodically by liquid collection techniques.

The team

observed that the procedure

was being marked

up as the calibration

was being performed.

There did not appear to be any administrative

control of the revisions

made to the procedure.

The maintenance

supervisor stated that there were

some problems with the procedure

such that the flow totalizer did not give accurate

indication when

the calibration was completed

and that the procedure

was being

troubleshot

and corrected

as part of the calibration activity that

was currently being performed.

When questioned,

the Shift Manager

stated that he was not advised of the changes that were being

made

to the calibration procedure.

The licensee's

Administrative Procedure 1.2.3, titled "Use of

Procedures"

(Rev.

12 dated

September

18, 1987), requires

procedures

to be followed in the performance of plant activities.

When

procedures

cannot

be followed, a revision to the procedure or a

procedure deviation must be completed.

In the case of a procedure

deviation,

documentation prior to its implementation is not required

providing the deviation

has

been approved

by two members of plant

management/supervisory

staff, and the Shift Manager is of the

opinion that the work must continue.

During calibration of the

drywell

sump flow monitor, these administrative controls were not

complied with. The maintenance

supervisor initiated nonconformance

report

(NCR) 288-373 to address

the team's

concern.

This is an

apparent violation (50-397/88-24-02).

One violation was noted in this area during the inspection.

5.

Maintenance

Pro

ram Im lementation

a 0

Or anization/Pro

ram

The Maintenance organization consists of a staff of approximately

210 and is directed

by a maintenance

manager

who reports directly to

the plant manager.

In addition to the normal

complement of

craftsmen

and supervisors,

the organization includes groups of

maintenance

engineers

who provide both technical

and work

coordination support to the individual craft groups.

The

maintenance

engineers

are the principal developers

of the work

instructions

and work package

planning sheets

which identify the

critical elements of a maintenance effort.

In an effort to provide

stronger direction and improve the quality of the maintenance

work

at the plant,

reassignments

were recently

made in the positions of

maintenance

manager,

assistant

maintenance

manager

and mechanical

maintenance

supervisor.

The systems for identifying, controlling, documenting

and

determining work requirements

are established

in plant procedure

1.3.7,

"Maintenance

Work Request"

(NWR).

During the review of this

procedure,

the team noted that a maintenance

work procedure is not

required

when tightening the packing

on pumps or changing

a fuse

when it has blown for the first time.

Apparently this is considered

"mundane" work and the procedure

has

been written to allow this work

to be completed

by various organizations.

The team discussed this

with the licensee

and pointed out that the referenced

items,

when

associated

with safety related

equipment,

could represent

a

significant problem with the system (in the case of a blown fuse) or

require the discipline of an operating

check (tightening of pump

packing)

and should require the use of a maintenance

request.

The

licensee

representative

acknowledged

the comment

and stated that

this matter was already under review and subject to a program

change.

The

NWR procedure

describes

the following 3 types of maintenance

work requests;

a normal

MWR which is intended to control

a

"one-of-a-kind" equipment failure,

a standing

NWR whichis intended

to control repetitive maintenance

tasks,

and

a vital

NWR which is

intended to control maintenance activities

on equipment which, if

left unrepaired,

could result in a potential Technical Specification

violation, a reportable

occurrence,

a safety hazard,

or could affect

plant reliability.

The quality of instructions

and records

associated

with the later

NWR type was considered to be poor and is

addressed

in paragraph

5.b.

Additionally it was noted that the use

of the vital work request

exceeded

the intent of the maintenance

work request

procedure

and was routinely used

even when

no imminent

safety problem existed.

Document Review

After reviewing approximately

20 work packages

which were related to

the emergency diesel

generators

and the containment isolation system

and which were completed during the past

1 1/2 years,

the team

made

the following observations:

1.

An inconsistency in the work packages

was noted in the

identification of components

associated

with Technical

Specification requirements.

The

NWR form contains

a check box

to identify the equipment

on the

NWR as technical specification

equipment.

There appeared

to be a lack of formality in

checking the box correctly for equipment

on which work was

being performed.

~

A

I

The team noted Maintenance

Work Requests

where work

instructions

to craftsmen

were considered to be minimal.

One

case involved the troubleshooting of safety related isolation

valve RCIC-V66, which is a check valve with position indication

in the control

room.

The valve is the closest isolation valve

to the reactor vessel for RCIC injection water.

The valve had been discovered with an open indication in the

control

room, contrary to its required closed position.

An

activity had been

undertaken

by the licensee to establish

a

valve lineup which would cause

a lower pressure

region upstream

of the check valve and thereby tend to reseat

the valve.

The record after troubleshooting

the problem did not indicate

the reason

why the valve was open,

when it should

have

been

closed.

Also, there

was

no indication that retesting

was

required.

The inspector later confirmed that the valve had

been retested

as part of a generic surveillance test involving

other isolation valves.

Another case

involved the repacking of

RCIC-V63.

The instruction stated,

"Valve Leaking -, Repack".

No

detail, procedure

reference,

vendor manual, or torquing

requirements

were listed.

In one case,

a vital

MWR involved the reassembly of the

4

cylinder valve bridge and rocker arm assembly

as well as the

installation of the oil lines onto the rocker arms of emergency

diesel

1A.

Three torquing operations

were to be performed.

Due to informal communications

between Quality Control

(QC) and

Maintenance,

QC did not inspect the torquing operation in

accordance

with its internal guidance.

The vital

MWR did

permit the torquing step to be bypassed if QC was not available

at the time of the call to witness.

However, the inspector

noted that the torquing step

was not performed until the next

day, at which time

QC was not called again to witness the step.

Two cases

were noted where the maintenance

records

associated

with maintenance

work on the main steam isolation valve

solenoid pilot valves

and the

RHR-V53B valve indicated that

a

cable involved in each of the jobs had not been reterminated.

The retermination control sheet in the

MWR had not been

completed.

The changes

in the instructions

had not been

authorized

by the Plant Manage

as required by administrative

procedure 1.3.9, "Control of Electrical

and Mechanical

Jumpers

and Lifted Leads".

This is considered

a violation of

regulatory requirements

(50-397/88-24-03).

Three instances

were noted where the evaluation

and disposition

of out-of-calibration measuring

and test equipment

(t4kTE)

associated

with two torque wrenches

and a piece of leak rate

testing equipment were not completed in a timely manner.

In

the case of the two torque wrenches,

the out-of-calibration

notices

had been issued in August 1987 and were still open.

The out-of-calibration notice for the leak rate detection

instrument also was still open

and had been issued in

c

10

March 1987.

The failure to complete in a timely manner the

evaluation of the impact on performance of the equipment

on

which testing

was performed using out of calibration NTE is

considered

a violation of regulatory requirements

(50-397/88-24-04).

6.

On June 14, 1988,

RHR-V-9 would not close

when operated

remotely from the control

room.

The Shift Manager initiated

vital maintenance

work request

(MWR) AV1733 to address this

problem.

During subsequent

troubleshooting of the valve,

RHR

pump RHR-P-2A tripped and nonconformance

report

(NCR) 288-258

was issued to address this problem.

The

NCR concluded that the

probable

cause for the

RHR-P-2A failure was the initiation of a

pump trip signal during RHR"V-9 troubleshooting activities.

A

less than full open indication from RHR-V-9 sends

a trip signal

to RHR-P-2A for loss of suction protection.

The team reviewed

vital

MWR AV1733 and

NCR 288-258 and

made the following

observations:

The work instructions provided

on the

MWR appeared

to be

very qualitative (i.e. troubleshoot problem),

and no

caution

was provided regarding the potential to trip the

operating

RHR pump.

A continuation sheet

was

added to the work instruction

after the work instruction was initially prepared,

and

there did not appear to be any administrative controls

governing this type of change to a

MWR.

The work

performed section of the

MWR did not include documentation

of the date

and time when the work was started.

RHR-P-2A tripped on June 15, 1988, at 1253.

Work

associated

with MWR AV1733 was completed

on June

14 at

1605.

The licensee's

conclusion

documented

on

NCR

288-258, which indicates that RHR-P-2A tripped while

maintenance

was being performed

on RHR-V-9, does not

appear to be well founded.

No further root cause

determination

had been attempted to reconcile the apparent

mismatch of dates

between the

MWR being completed the day

before the

pump trip.

Observation of Work

The team observed portions of work in progress

associated

with the

following maintenance activities:

o

Pressure

decay test of the main steam re'Iief valve tail pipe

associated

with valve MS-RV-28 (MWR¹ AT 6632).

o

Replacement of a pressure

switch on one of the recirculation

valve controls

(MWR¹ AT 6053).

o

Repacking of the RCIC-63 valve

(MWR¹ AV 1810).

l

~

0

o

Modification of the moisture separator

level transmitter

on the

containment

atmosphere

control system

(HWR8 AT 6245).

The team noted during the observation of work that maintenance

work

requests

had been written for the work in progress.

Where

measurements

were being taken,

instrumentation calibrations

were

current.

gC was noted to be present

when the work activity required

gC presence.

Radiation precautions

were considered

adequate

for the

work in progress

and procedures

appeared

to be followed.

During the

performance of one maintenance, job involving the repacking of

RCIC-V63, the team observed that maintenance

personnel

were having

difficulty installing the

new packing into the valve stuffing box.

The team also noted that the maintenance

personnel

determined that

the packing was the wrong size

and stopped

the work.

The problem

with the packing was found to be associated

with the dye used to cut

the inner diameter.

The dye was

stamped with the wrong size.

Proper sized packing was produced

and the work completed.

An ASME

Section XI test

had been identified as

a retest

requirement

following maintenance.

Two violations were identified in this area of inspection.

6.

Emer enc

Diesel Generators

EDG

DG-1 and

DG-2

During the inspection the team performed

a field walkdown of the

EDG

skids

and associated

support systems.

These

systems

included, in part,

the

EDG air start system,

EDG jacket water cooling system,

governor

control system,

EDG pre-heat

lube oil modification and service water

cooling system.

Verifying such items

as support locations, orientation,

and correct piping configurations,

the team performed

a limited as-built

configuration inspection of the subject

systems utilizing the applicable

design configuration drawings.

An operational test in which the team

was

able to observe

the various operating parameters

of the

EDG system

such

as temperatures,

pressures,

and fluid levels, (i.e. exhaust

gas outlet

temperature,

jacket water and lube oil pressure

and levels)

was also

performed for

EDG engine 81Al.

The following is a description of the

system material condition,

any observations

or deficiencies

noted,

and

the potential

impact the deficiencies

could have

on the safe

and reliable

operation of the system.

Also included is a description of the

licensee's

corrective actions for the deficiencies identified during the

team's

walkdown of the

EDG systems.

EDG Startin

Air and Servomotor

Pneumatic

Tubin

Lines

During the inspection the team performed

a limited as-built

configuration inspection of the

EDG pneumatic tubing lines which

supply air to the starting air motors, the servomotor,

and

associated

starting air piping and components.

During an emergency

start actuation,

a solenoid valve is energized,

allowing air from

the starting air tanks to pass

through the solenoid valve to the

pinion gear

end of the starting motors.

The entry of air through

the pneumatic tubing lines moves the pinion gear forward to engage

with the engine ring gear.

In addition to maintaining gear

engagement,

the air opens the air start valve, releasing

the main

1

~

~~,, l\\.

12

starting air supply.

Starting air passes

through the air start

valve and into the flexible hose

assembly

attached to each air

starting motor.

The multivane starting motors drive the pinion

gears,

rotate the ring gear,

and crank the engine.

During the starting sequence,

at the

same time that starting air is

applied to the starting motors, air is also applied to the bottom of

the governor booster.

This drives the booster piston up, forcing

oil under pressure

into the governor.

The governor power piston is

moved in the "increase fuel" direction and fuel is supplied to the

injectors for starting the engine.

The

EDGs are supplied with two

redundant

banks of air start motors

and servomotor shuttle valves.

During the field walkdown, the team identified approximately

20 feet

of the pneumatic starting air line on

EDG engine

01A1 to be

unsupported

and noted that additional

spans of tubing appeared

to be

unsupported

on the other

EDGs as well.

The team identified this

condition to the licensee's

design engineering staff and to the

EDG

system engineer to determine if there were any analyses

or

documentation indicating that the existing condition was acceptable.

The licensee

personnel

were unable to present

the team with an

analysis that the existing condition met the design criteria for

allowable tubing stress.

Licensee

personnel

were also unable to

identify any design control documentation

specifying the location

of'he

required vibration/seismic

supports for the pneumatic tubing

lines.

A postulated failure of these lines (if left unsupported)

could potentially result in a loss of starting air to the

EDG or a

loss of air to the servomotor during normal vibration or during a

seismic event.

The licensee

performed the following corrective actions.

The

licensee

issued plant deficiency report No. 288-380 which documented

the as-found condition of the starting air pneumatic tubing.

The

immediate disposition of the plant deficiency report recommended,

in

patt, performing an analysis to demonstrate

the ability of the

pneumatic tubing to withstand

a seismic event, evaluating the need

to add additional supports,

and requesting

design engineering staff

to provide design direction for the installation of the supports.

As a result, the design engineering staff issued basic design

change

(BDC) No. 88-0299-04.

This

BDC included the installation and

qualifying stress

calculations with references

to the analyses

assessing

the as-found condition of the starting air pneumatic

tubing.

The analyses

affirmed that no seismic

induced failure would

have occurred for the worst case

as-found condition.

However, prior

to the conclusion of the inspection,

design engineering did provide

design direction for the installation of additional supports to

improve seismic capability.

13

EDG Coolin

Water Pi

e Cou lin

During the field walkdown of the external

EDG cooling piping on

EDG-2, engine

181, the team identified that safety-related

flex

coupling No.

DLW FLX-llB1, located

on the cooling water line between

the engine

and thermostat

valve on the auxiliary skid, was

misaligned approximately 5.5

.

The team identified this condition

to the licensee to determine if there

had been

any analyses

performed or documentation reflecting that the existing condition

was

an acceptable

installation.

The licensee

personnel

stated that

this condition may have resulted

from the R-1 outage in July of

1986,

when it was noted that

EDG engines lA and

1B were not doweled

(aligned) in accordance

with the

EDG manufacturer's

recommendations.

The licensee

also stated that the original

EDG alignment problem had

been corrected

and documented

per plant modification record

No. 02-86-0329-0.

However, licensee

personnel

were unable to

demonstrate

that the present

excessive

angularity of the cooling

water flex coupling was acceptable.

Because

a postulated failure of the flex coupling during a seismic

event could result in the loss of EDG cooling water and potentially

render the

EDG inoperable,

the licensee

performed the following

actions.

The licensee first performed angularity field measurements

on the flex coupling and determined the maximum angularity to be

~

5. 5

.

The licensee

also measured

the length of pipe insertion into

the flex coupling to assure that the minimum insertion criteria of

1.86 inches

had not been affected

due to the excessive

angularity.

Upon review of the manufacturer's

(Airoquip) catalog,

the licensee

determined that the coupling's as-found condition was outside the

manufacturer's

maximum angularity criteria of 4 .

Upon disassembly of the coupling in the field, the licensee

discovered that the actual

minimum insertion was 1.66 inches or .2

inch less than the manufacturer's

stated

minimum.

This situation

was discussed

with the licensee

and the manufacturer,

and was

determined to not render the

EDG inoperable for the following

reasons:

1.

The 1.66 inch penetration into the coupling is sufficient to

provide

a good contact surface

between the gasket

on the end of

the coupling and the pipe.

The end of the pipe is far enough

beyond the gasket not to interfere with the seal.

2.

The application normally involves

no pipe movement or very

small, infrequent

movement of the piping.

Consequently,

even

if contact

had been

made between the end of the pipe and the

coupling wall, the movement would not have been expected to

wear the coupling wall to an extent that the coupling would

have failed.

3.

The coupling is designed for 150 psig internal pressure

but

operates

at approximately

10 psig.

The licensee reinstalled the flex coupling to meet the required

angularity and insertion criteria as specified in the manufacturer's

catalog

and documented

the as-found condition per plant deficiency

report

(PDR) No. 288-382.

Bent Coolin

Water Vent Line Nozzle

While performing a limited as-built configuration inspection of the

external

EDG cooling water piping for EDG lA1 and 181, the team

identified two bent nozzles

(1/2 inch x 4 inches long) on diesel

cooling water

(DCW) tanks

181 and 2Bl. It appeared

that the nozzles

were bent 1/4 inch off center (worst case)

as

a result of being

stepped

on while personnel

were performing various work activities

in the

EDG rooms.

This condition had not been previously identified

in the licensee's

problem identification tracking system.

The

nozzles

were associated

with the

EDG cooling water vent lines,

and

failure of the nozzles

could result in a loss of EDG cooling water,

potentially rendering the

EDG inoperable.

The licensee

performed

the following corrective actions.

The licensee

performed

a field

walkdown of all associated

cooling water vent lines and performed

field measurements

to determine which

DCW tank nozzle was most

affected.

The licensee

also issued plant deficiency report

(PDR)

No. 288-392 to document the deficiency and performed

a calculation

to assess

the (worst case) existing condition. It was determined in.

the calculation that the bend was

on the 4 inch vertical lead of

pipe (tank nozzle)

because this section of piping consisted of sch.

40 pipe while the rest of the associated

piping is sch.

160. It was

also determined that there

was

no deformation

near

the

DCW tank weld

and since the weld is a full penetration

weld, non-destructive

examination of the weld was not required.

The disposition of the

PDR and calculation was that the slight bend in the

DCW tank nozzle

had

no effect on the serviceability of the pipe.

Service Water Valve No.

SW-V-4A

During a field walkdown of DG room DG-1, the

NRC inspectors

identified an incomplete thread

engagement

condition on the packing

gland nuts for safety-related,

8-inch line, motor-operated

service

water valve No.

SW-V-4A.

The team identified this condition to the

licensee to determine if there

was any documentation reflecting the

existing condition.

The licensee

was unable to present

any

documentation

which reflected the existing condition.

However,

because

of the potential for a loss of service water which is used

as secondary cooling for the

EDG jacket water and lube oil systems,

the licensee

performed the following corrective actions.

The

licensee

issued

maintenance

work request

(HWR) No.

AT 6667.

The

MWR

work instructions stated in part to (1) obtain clearance for work,

(2) remove all necessary

packing to obtain proper thread

engagement,

(3) repack

SW-V-4A per maintenance

procedure

No. 10.2.7,

and (4)

ensure

SW-V-4A stokes

manually with proper thread

engagement.

The

NRC inspectors

were notified that the work was performed prior to

the conclusion of the inspection.

15

Deformation of EDG Su

ort Footin

s

During the field walkdown of EDG skids

and associated

components,

the team identified a deformed support footing on the east side of

engine

1B2.

The team identified this condition to the licensee

personnel

to determine if there

was any documentation reflecting the

existing condition.

The licensee

stated that the deformed support

foot had been

documented

upon receipt inspection (material

damage

report

No. B-022 dated

December

13, 1978)

and was dispositioned

accept-as-is,

touch

up with paint as required.

However, after

a

secondary

visual inspection of the subject support foot and the

discovery of an additional

deformed foot on the west side of engine

1B2 by the team, the licensee

performed the following additional

corrective actions:

The licensee

issued plant deficiency report

(PDR) No. 288-393,

which

stated

in part that the condition was caused

by an excessive

load

being placed

on the jacking screws which were used to obtain the

proper alignment for the

EDGs.

The

PDR further stated that the

operations

and maintenance

manual

would be modified to warn

personnel

performing

EDG alignments to exercise

care in using the

jacking bolts,

such

as not to deform the support footings.

The

licensee

also performed mechanical

evaluation

(M.E.) No. 02-88-58

for the west support foot which was determined to have the worst

case deformity.

The evaluation stated in part that based

on the

engine alignment, bolting arrangement,

visual weld examinations,

the

use of gusset plates

on either side of the support footings,

and

previous main bearing examinations

which showed

no perceptible

wear,

it was concluded that the support footing deformations

appeared

to

be localized,

and would have

no effect on the serviceability of the

engine.

Missin

Su

ort on Lube Oil Circulatin

Pum

Suction Line

The team performed

a limited as-built configuration inspection of a

vendor

recommended

modification (MI 9644), which the licensee

had

implemented

on the high pressure

core spray diesel

engine

and all

four EDG engines.

The purpose of the modification is to provide

an

improved immersion heater

lube oil circulating system that will

consistently

supply lube oil to the engine's

turbocharger

and

crankshaft in anticipation of an emergency start.

During a walkdown of the emergency diesel

engine lA1 modification,

the team identified a missing seismic support bracket

on the lube

oil circulating pump suction line.

The team identified this

condition to the licensee to determine if there

was any

documentation reflecting this condition.

The licensee

presented

the

team with as-built configuration drawing No. 02-332-002 which

identified the support

as part of the modification (item 90).

However,

because

the support

was missing

on engine

1A1, potentially

affecting the seismic capability of the lube oil piping, the

licensee

issued

PDR No. 288-393 to document the condition.

The

immediate disposition of the

PDR stated that,

based

on a span chart

criteria (ANSI B31.1) the missing seismic support would not affect

~

~

16

the seismic qualification of the suction line.

The licensee

also

performed

a physical inspection of the subject line and installed

the support per maintenance

work request

(MWR) No.

AT 6629 prior to

the conclusion of the inspection.

EDG Governor

Lube Oil Level

During a walkdown of the

EDG skid for engine

1A1, the team noted

that the lube oil level in the external sight glass for the

EDG

governor

was out of sight high with the

EDG in the standby

mode of

operation.

The team also reviewed the station

EDG surveillance

procedure

No. 2.7.3-7 (Step 15) and was unable to determine the

required governor oil levels during standby or normal operation of

the

EDG.

The team identified this concern to the licensee to

determine what criteria the equipment operators

were utilizing for

the governor lube oil levels, while performing their surveillance

inspections

of the

EDGs and high pressure

core spray engines.

The

failure to identify a high oil level in the governor during

operation could potentially result in foaming of the lube oil

causing erratic operation of the engines.

On August 25,

1988 the licensee

contacted

the

EDG governor

manufacturer

(Woodward Governor) via telephone for guidance

on

determining the optimum governor oil level for standby

and normal

~

operation of the engines.

The

EDG governor manufacturer

recommended

that the governor oil level be monitored,

and if needed,

be adjusted

after the engine

has

been operating for such

a time span that the

engine is warm.

The governor manufacturer further stated that the

the intended

normal governor oil level

be determined (via the

external sight glass) with the engine running.

As a result, the licensee

performed

an operational test of EDG 1Al

to assure that the governor oil level dropped within tolerance

during operation.

Excess oil was drained

so that a level could be

observed

in the external sight glass during normal operation of the

engine.

The licensee

also revised the station surveillance

procedures

prior to the conclusion of the inspection.

Vendor Manual

Review

The licensee's

emergency diesel

engines

were manufactured

by General

Motors, Electromotive Division (EMD).

The diesels

are 20 cylinder

turbocharged

engines.

There are two diesel

engines driving each

emergency

generator.

The inspector reviewed the vendor manual

recommendations

applicable to the diesel

engines,

and made the

following observations:

The vendor manual stated that the governor oil level should

be

checked

and adjusted to the midpoint scribe mark in the

sightglass

shortly after the diesel is started.

As discussed

above, the licensee's

surveillance procedure did not provide

specific instructions in this regard.

E

c

~

17

For the oil fog lubricators located

upstream of the air start

motors, the vendor manual

speci fies

an oi 1 dr ip rate whi ch is

dependent

on the nominal air velocity through the air start

piping.

The licensee's

procedures

did not address

this vendor

recommendation.

Based

on the team's

observations, it appears that the licensee

has

not established

a program to address

and implement (as appropriate)

vendor recommendations.

Licensee

personnel

could not identity where

the vendor recommendations

had been incorporated.

However, they

would evaluate

the recommendations

for possible insertion into the

appropriate

procedure.

Because

the above identified concerns

did not result in a direct safety

issue

and because it would be difficult to determine the cause of the

deficiencies in most cases (ie, construction activities versus

recent

operational activities), the team did not consider enforcement

appropriate.

However the number of discrepancies

noted does indicate

that licensee

personnel

need to be more aggressive

in identifying and

documenting discrepancies.

ASCO Solenoid Valves

Used Within Nuclear Steam

Su

1

Shutoff

S stem

NS

During the inspection,

the team reviewed the licensee's

evaluation of NRC

=

information notice No. 88-43, entitled "Solenoid Valve Problems."

The

information notice was issued to alert licensees

to a series of solenoid

valve failures that have occurred at several

nuclear

power plants.

The

notice discussed

in part various licensee

investigations

which isolated

the cause for two main steam isolation valve (MSIV) failures to Automatic

Switch Company

(ASCO) Model

NP 8323AZOE dual solenoid operated

valves

(SOVs).

The failure mechanism(s)

could not be positively identified.

However, the most likely cause of the two failures

was determined to be,

in part,

a degradation

of the ethylene propylene diene

monomer

(EPDM)

elastomer

seats,

due to exposure to high temperature

environments,

and

a

yellowish sticky film which acts like an adhesive

and prevents

the core

assembly

from shifting to the de-energized

position,

and which lies

between the core assembly

and plugnut assembly of the solenoid valve.

It

was later stated that the film substance

closely resembled

the

Dow 550

lubricant with which ASCO routinely lubricates the core and plugnut

assemblies

to reduce noise

and wear associated

with a 60 cycle

hum.

In discussions

with the licensee,

the team discovered that WNP-2 had

experienced

one failure of their MSIVs during testing and

had established

an extensive

program to determine the root cause of the problem.

The

licensee attributed the cause of the failure to be sticking of the "A" or

upper core assembly of a SOV.

Two analyses,

one in-house

by licensee

personnel

and another by an outside consulting firm, were performed.

The

analyses

were based

on

SOV internal scrapings

which were found to be

primarily si'licon in nature.

The licensee

concluded that the sticking of

the "A" core assembly

was associated

with the

Dow 550 lubricant.

The

licensee

then issued

a maintenance

work request to reinstall all new MSIV

solenoid control valves without the

Dow 550 lubricant and is presently

operating with the MSIV solenoid valves in this configuration.

When the

licensee notified the solenoid valve manufacturer of their conclusion,

. ~

18

the manufacturer

stated that they did not concur with that postulated

failure mechanism.

The licensee

stated that the manufacturer

indicated that there

was

a

possibility that the lower exhaust

core assembly

was sticking due to the

introduction of hydraulic fluid leaking back through the air lines from

the MSIV closure control mechanism.

The licensee's

engineering

opinion

is that due to the torturous path the hydraulic fluid had to follow to be

introduced into the lower exhaust

core assembly, this possibility

appeared

to be unlikely.

The licensee's

engineering analysis

appears

to

be adequate

and supported

by chemical analysis of valve internals

residue.

Trouble-shooting

was initially performed

on the solenoid valve,

however,

the licensee

had not required

a controlled disassembly

in the field.

This effort, had it been performed,

could have preserved

any evidence of

hydraulic fluid within the piping system.

8.

Desi

n Process

Review

The licensee's

design processes

were evaluated for technical

accuracy

and

attention to detail.

Three (3) Plant Modification Requests

(PHRs)

and

their associated

Design

Change

Packages

(DCPs), Field Change

Requests

(FCRs),

and Maintenance

Work Requests

(HWRs) were reviewed

fear plant

modifications to the Nuclear Steam Supply Shutoff System

(NS ) and the

Emergency Diesel Generators.

In the design packages,

no discrepancies

which had not already

been

addressed

by the licensee

were identified.

However,

some activities associated

with the design

packages

exhibited

weaknesses

where designs

were being performed or documented

in an

informal manner.

a ~

PHR 02-85-0466-0

RWCU Surveillance Test Switch

Design package

DCP 85-0466-OA was generated

to install test switches

to enable the performance of surveillance testing of the reactor

water clean

up

(RWCU) delta flow function without the use of

temporary jumpers.

The design

package

contained

both drawing

changes

and wire termination lists.

These

two items did not agree

with each other, i.e., the drawings were correct but the wire

termination lists were incomplete

and inaccurate.

The wire

termination lists were corrected

by the technical staff with a

DCP

revision

(DCP 85-0466-0B).

The design engineer prepared

the revised

DCP with the wiring list corrections.

However, the package

was not

released

since engineering

procedures

do not require the wire

termination lists to be a part of the controlled design package.

The wire termination lists, however, are required in the

MWR and

therefore the lists corrected

by the technical staff were included

in the

MWR.

The maintenance

department

reviewed the wire

termination list and discovered that the termination lists were

still incomplete.

Maintenance

personnel

made further corrections to

the wire lists.

The team's

concern

was that the wire termination

list is required to be contained within the

MWR.

However, there is

apparently

no clear procedure

requirement for someone to generate

19

the document.

In addition, for this

DCP review, it was not clear

that revisions

made to the wire termination list were checked.

Licensee

management

acknowledged

the concern

and stated that the

wire termination list would be required

by the appropriate

procedure.

Although the test switches

have

been installed

and operate

as

intended,

the informal design

and documentation

process left areas

where mistakes

and errors could have

been

made.

Since engineering

and the technical staff only receive the cover sheet of the

MWRs,

they had

no indications that the scope of the corrections to the

wire termination lists

had changed

from the

DCP.

b.

PMR 02-85-0383-0 Diesel

En ine Governor

S stem

Design packages

DCP 85-0383-OA and

DCP 85-0383-0B were generated

to

replace the diesel

engine governor controls with an electronic

governor allowing the diesels to be operated at a slow idle.

The

design

was intended to be a vendor supplied "black box" replacement

for the old governor controls.

This apparently simple 'plant

modification required

2 DCPs

and 15

FCRs to complete.

Of the 15

FCRs, at least

9 could be attributed to errors,

omissions,

or

incompleteness

of the design.

Furthermore,

a licensee

gA audit

(Surveillance

Report 2-88-203) identified 6 deficiencies

and 14

observations

associated

with the design

and installation of this

work package.

These

examples

are indicative of a less than rigorous approach to the

controls

placed

on the development

and implementation of design

packages

for plant modifications.

The licensee

has recently committed to

improving their program for design

changes.

Since

no design activities

were reviewed which would have been developed

under the

new programs, it

can not,

as yet,

be determined if the weaknesses

observed

by the

inspector

have been addressed

or eliminated by the licensee.

9.

Plant Oversi ht Grou

s

The team examined the involvement of the licensee's

oversight groups in

formulating corrective actions in response

to internal

and external

events

having potential safety significance.

To determine the

effectiveness

of the oversight groups,

the review considered initiatives

of the groups

and ultimate corresponding

actions of the licensee.

The

team generally found the work of the review groups to be thorough.

Instances

were found where followup of review group findings was

incomplete.

a 0

Nuclear Safet

Assurance

Grou

The Nuclear Safety Assurance

Group

(NSAG) functions to examine unit

operating characteristics,

NRC issuances

such

as bulletins and

notices,

industry advisories,

Licensee

Event Reports,

and other

sources of unit design

and operating experience

information

(including units of similar design) which may indicate areas for

20

improving unit safety.

The

NSAG makes detailed

recommendations f'r

revised procedures,

equipment modifications,

maintenance activities,

operations activities, or other means of improving unit safety.

NSAG

reports to the Director of Licensing and Assurance.

Specific

requirements for the group are set forth in Technical Specification 6.2.3.

The licensee's

procedures

under which this group operates

are found in PPM 1.10.4.

The team looked at NSAG's reviews of events

on emergency )iesel

generators

and

on nuclear

steam supply shutoff system

(NS )

components.

The number of reports

on external

events

reviewed by

NSAG is large.

There were roughly 100 events

reviewed

on diesel

generators

and roughly 40 reviewed

on

NS

components.

The team examined

NSAG reports

on a representative

number of events.

The analyses

were found to be thorough

and the recommendations

for

action were clear and concise.

NSAG recommendations

are subject to

review,

and thus modification, by other organizational

units prior

to implementation.

However, the team found that the

NSAG

recommendations

were well respected

and any modifications appeared

to have rational

bases.

Although NSAG maintains

cognizance of their recommendations

through

ultimate disposition,

the team noted that a small percentage

of

items were lost from the tracking system without documentation of

closeout

and furthermore were apparently not implemented.

For

example, in a report dated

November 26, 1984,

NSAG recommended

increasing the air receiver capacity of the air start system for the

HPCS diesel

generator in order to improve reliability.

Subsequently,

engineering

recommended

an alternative for achieving

the improvement in reliability.

The recommendation

is no longer in

the

NSAG tracking system.

However,

no action was taken to improve

diesel

generator reliability.

The alternative action is on a

different plant tracking system

(as

PMR 02 85 0093-1) but is

dormant.

This appears

to be a defect in the tracking system rather

than an indication that

NSAG is not functioning. Nevertheless,

to be

fully effective at its function, followup of review group

recommendations

is essential.

Cor orate Nuclear Safet

Review Board

The Corporate Nuclear Safety Review Board

(CNSRB) is appointed

by

the Managing Director from his senior technical staff and from

personnel

outside the Supply System.

At the time of the inspection,

three outsiders

served

on the Board. This group serves to provide

independent

review and audit of activities designated

in Technical Specification section 6.5.2 and advises

the Managing Director of

their findings and recommendations

from these

reviews and audits.

The team reviewed the minutes from the last four regularly scheduled

quarterly meetings of the

CNSRB (meetings

87-11, 88-01, 88-07,

and

88-09).

CNSRB also'meets

intermittently as needed,

for example, to

review proposed

changes

to technical specifications.

The inspection

team reviewed the minutes from one recent special

meeting (meeting

~ ~

21

p, ~

kc

88-05) to gain understanding

of the

CNSRB input to this process.

These special

meetings often do not include the complete

CNSRB

membership.

The inspector also interviewed the

CNSRB Chairman

and

the former recording secretary.

The team found the minutes to be quite detailed

and therefore very

helpful in providing insight into the depth of discussion occurring

at the quarterly meetings.

Presumably

because

of the focus

on the

need for management

involvement,

CNSRB recommendations

were usually

directed toward longer range safety

improvements

involving policies,

programs

and procedures,

rather than toward resolution of technical

problems.

However,

recommendations

gener ally would result in

actions for operations.

The

CNSRB maintains its own tracking system.

The team looked at

followup to recommendations

made at earlier meetings.

A number of

the recommendations

had been closed out and it generally appeared

that

CNSRB was making

a significant contribution to safe operation

of WNP-2.

However, the minutes often include recommendations

or

commitments which are not entered into the

CNSRB tracki,ng system

and

do not appear

to be closed out methodically by CNSRB. It appears

that the effectiveness

of the

CNSRB could be enhanced

by expanding

their tracking system to capture all recommendations

and

commitments.

C.

Plant

0 erations

Committee

The Plant Operations

Committee

(POC) functions to advise the Plant

Manager

on all matters related to nuclear safety.

Specific

responsibilities

detailed in the technical specifications

(Section

6.5.1) essentially

include review of changes

to hardware or

procedures

having potential safety ramifications,

review of events

which may convey safety lessons,

and review of operations

to detect

potential safety hazards.

The technical specifications

require

monthly meetings to address

these matters.

However, the

POC has

found it necessary

to schedule regular weekly meetings

and

frequently holds additional

meetings to discharge its

responsibilities.

The team reviewed minutes from POC meetings for most of the past

year and attended

one

POC meeting.

The team also talked with POC

members

about

POC procedures.

POC maintains their independent

tracking system for followup of certain specified action items.

Review of the minutes,

as well as observations

at the one meeting

attended,

indicate that the

POC meeting

agendas

are dominated

by the

mandatory reviews of design

and procedural

changes,

of licensing

actions,

and of event reports.

In order to accommodate

the large

number of such actions to be acted

on by POC, coordination problems

and technical

and safety concerns

must be resolved before the

meeting.

Discussion of these

items is minima) at the meetings.

Meeting minutes often are limited to identification of the items.

acted

upon with indication of the action taken.

Nevertheless, it

22

would appear that the formality of the

POC process for approval of

these

items results in resolution of safety concerns.

Review of the

POC minutes also sought records of discussion of unit

operations

and of evolving operational

problems to identify and

determine the effectiveness

of the group in advising the Plant

Manager of pending safety concerns.

Specifically sought out, for

example,

were minutes of meetings

addressing

drywell leakage

and

drywell temperature

problems,

both before

and after the recent

refueling outage.

The minutes were brief, but gave the general

impression that the discussion at

POC centered

around solving the

immediate

complex technical

problems, rather than

on the safety

ramifications of the problems

and alternative solutions.

An unexpected plant shutdown early in the inspection period afforded

the team

an opportunity to enter the drywell.

The team noted that

some outage work areas

apparently

had not been cleaned

up prior to

restarting after the last refueling outage.

Because of the role of

the

POC in implementing the restart plan, the

POC minutes for

meetings

near the end of the outage

were reviewed.

Minutes for the

June

1988

POC meeting (888-22.2) which reviewed the containment

closeout inspection,

indicated that housekeeping efforts were still

in progress

but would be completed prior to restart.

This was not

an item for the

POC tracking system

and was not addressed

in

subsequent

minutes prior to startup.

Based

on the team's

review of POC documentation, it is not apparent

that the

PDC had addressed

the long term safety implications of the

drywell leakage

and temperature

problems

or the drywell cleanliness

prior to restart.

No documentation

which addressed

the long term

effects of the higher than normal temperature

of the drywell on

electrical

equipment environmental qualification was found.

Drywell cleanliness

problems

were reviewed by the

POC during the

committee's

review of startup requirements.

However,

no followup

action appeared

to have been taken by the committee to ensure

acceptable

drywell cleanliness

standards

were met.

The licensee

acknowledged

the team's

concern

and stated that the

POC

appears

to become involved in problem solutions rather than review

and oversight functions.

ualit

Assurance Activities

The team examined quality assurance

activities in cogjunction with

modifications to the diesel

generators

and to the

NS

.

The team

also reviewed

a recent audit more broadly addressing

design

modifications

and associated

activities (Audit 88-434) prepared

by

the Corporate

Licensing and Assurance staff.

The inspection

considered

the scope of the gA review,

as well as actions taken in

response

to gA findings, to ascertain

the effectiveness

of this

review group

on plant safety.

23

Audit 88-434

made

a number of findings regarding design

modifications which demonstrate

the thoroughness

of their

examinations

as well as their willingness to be candid to their

management

regarding their results.

A number of their findings focus

on problems identified in previous

NRC inspection reports

(87-19 and

88-02).

In accordance

with licensee

procedures,

the organization

whose work areas

were audited

was to respond to the audit,

identifying actions to be taken to correct deficiencies

noted in the

audit.

The effectiveness

of the audit activities will not be determinable

until corrective actions

have been fully implemented.

Audit

responses

addressed

specific plant components

called into question

by the audit,

and corrective actions

were taken where appropriate.

Additionally, a number of procedural

changes

were identified in

responses

to the audit.

Procedural

improvements

should enhance

performance of future design modifications.

The team expressed

some concern with follow up to audit findings by

the audit group.

Licensee

procedures

resulted in an apdit being

closed out on the basis of responses

received.

Thus specific audit

findings are not tracked by Corporate

Licensing and Assurance.

For

example,

the inspector

noted that at least

one item appeared

to have

been

dropped without significant procedural

changes

being

considered.

guality Finding Report

No. 4 stated that failure of

design engineers

to visit a jobsite

may have contributed to design

deficiencies.

In response

to this finding, the existing policy for

walkdowns was restated.

Although subsequent

discussions

with the

licensee

have provided additional insight on the particularities of

the deficiencies

referenced

in the audit, it remains to be

demonstrated

that walkdowns are being utilized effectively to

produce quality design modifications.

Based

on a review of records the licensee

supplied, it is not apparent

that recommendations

of the oversite

groups are adequately

tracked

through implementation.

This may result in some recommendations

being

dropped or deferred without formal documentation.

In some instances,

discussion with plant management

identified additional resolution,

although little documentation

had been generated

by the plant to support

the closeout of the issue.

On September

2, 1988,

an exit meeting

was held with the licensee

representatives

identified in paragraph

1.

The team summarized the

inspection

scope

and findings as described

in this report.