ML17284A653

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Revised Pages 1-3 of Attachment 2 for Insp Rept 50-397/98-05 Correcting Two Errors.First Error Involved Identification of Initial 10CFR50.72 Rept in Both Pacific & Eastern Times
ML17284A653
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 06/02/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17284A645 List:
References
50-397-98-05, 50-397-98-5, NUDOCS 9806100421
Download: ML17284A653 (6)


See also: IR 05000397/1998005

Text

ENCLOSURE

NRC INSPECTION REPORT 50-397/98-05

ATTACHMENT2

"DETAILEDCHRONOLOGY OF MARCH 11, 1998, MAINSTEAM

LINE ISOLATIONVALVECLOSURE AND REACTOR SCRAM"

CORRECT! ON

980610042i

980602

PDR"

ADOCK 05000397

8

PDR

ATTACHMENT2

DETAILEDCHRONOLOGY OF MARCH 11, 1998

MAINSTEAM LINE ISOLATIONVALVECLOSURE AND REACTOR SCRAM

March 10

Reactor power at 100 percent

Day

March 11

The licensee noted an increase in the containment instrument air (CIA) usage

(from 1 to 1.5 SCFM) and began reviewing the potential causes for the increased

usage.

Reactor power was at 100 percent and all safety systems w'ere available and in

standby.

05:16:05

Main Steam Isolation Valve 22D fast closed on loss of containment

instrument air (CIA) nitrogen supply to the valve operator.

05:16:10

A reactor scram signal was generated

on an average power range

monitor (APRM) high flux of 118 percent.

05:16:11

Nuclear steam supply system (NSSSS) isolation and all main steam

isolation valves close on high main steam line flows.

05:16:13

Reactor pressure increases to 1085 psig and 2 safety relief valves

automatically actuate to reduce pressure.

Each safety relief valve

properly reseats.

05:16:14

The high pressure core spray diesel generator started on Level 2

(-50 inches reactor vessel level narrow range).

05:16:15

The reactor core isolation cooling and high pressure core spray systems

initiated and subsequently began injection into the reactor vessel. A main

turbine trip was initiated and the reactor closed cooling system pumps

tripped and was isolated from the drywell, resulting in a loss of drywell

cooling. A slow increase in drywell pressure begins because of the loss of

the drywell,coolers.

05:16:16

Four control rod position indications were lost, requiring operators to verify

the control rods had fullyinserted using the rod worth minimizer. All

control rods subsequently indicated full in.

05:16:38

The reactor core isolation cooling system reached maximum flow at 860

gallons per minute.

05:17:17

The reactor core isolation cooling system automatically isolated on high

reactor vessel level by closing the steam admission Valve V-45.

-2-

05:17:18

The high pressure core spray injection Valve 4 automatically closed on

high reactor vessel level.

05:19:00

The operators started residual heat removal Pump A and service water

Pump 1A in the wetwell cooling mode

.

05:26:00

The standby gas treatment system was started to reduce drywell pressure

by venting.

05:26:59

05:27:21

The reactor core isolation cooling system tripped when manually initiated.

Drywell pressure increased to approximately 1.65 psig resulting in

engineered safety feature actuation of the Division tl emergency diesel

generator.'5:28:00

The operators were able to restore the reactor closed cooling system and

established drywell cooling for pressure reduction.

05:28:29

The operator was subsequent(y able to reclose the reactor core isolation

cooling system trip and throttle valve from the control room and reinitiate

the system.

05:28:35

Drywell pressure increased to approximately 1.65 psig and resulted in the

engineered safety feature actuation of the Division I emergency diesel

generator.

05:29:08

The high drywell pressure engineered safety feature actuation signals

cleared on decreasing drywell pressure.

05:38:00

Standby gas treatment system secured.

05:54:00

High pressure core spray pump secured

05:58:00

06:00:00

The operators reset the reactor scram.

The high pressure core spray emergency diesel generator was secured.

Earlier, the emergency diesel generator restarted when the system was

shutdown prior to resetting the initiation circuitry

06:07:00

A reactor protection action signal initiated on low reactor vessel level. The

reactor core isolation-cooling system could not be operated in the

recirculation mode resulting in difficultyin controlling reactor vessel level

between plus 13 inches {lowlevel) and plus 54 inches (high level).

06:11:00

The licensee made a four hour nonemergency notification that a reactor

protection system actuation had occurred from a main generator lockout.

e

-3-

07:30:00

Pressure

and temperature indicated cooldown had exceeded the

allowable pressure and temperature curve

07:37:00

Main steam isolation valves opened (except 22D) and main turbine

bypass valves placed in auto.

07:41:00

07:44:00

07:45:00

09:00:00

09:11:00

Operators placed reactor pressure vessel level control in auto.

Reactor core isolation cooling injection secured.

Pressure

and temperature within area on the cooldown curve

Pressure

and temperature exceeds the allowable limits established by the

pressure and temperature curve

10 CFR 50.72(b)(2)(ii) 4-hour non-emergency notification of RPS

actuation (scram)

10:24:00

Reactor water cleanup system placed back in service with the

demineralizes bypassed.

10:28:00

10 CFR 50.72 (b)(2)(ii) and (iii)4-hour nonemergency notification of a

second RPS actuation and an engineered safety feature actuation

involving a reactor pressure level low level scram

10:30:00

Pressure and temperature returned to the to the right of the pressure and

temperature curve (acceptable limits) based on temperature indications

provided by the reactor water cleanup system.

11:13:00

Started reactor recirculation Pump 1A establishing forced circulation.

March 12

02:00:00

Plant entered Mode 4.

20:42:00

Event updated report to the NRC operations officer which provided

supplemental and corrected information.