ML17278A964

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Insp Rept 50-397/86-21 on 860601-0712.Violation Noted:Tools & Equipment Used During Performance of Maint Not Inventoried,Inventory Sheet Not Maintained & Log Not Maintained for Personnel Working Near or on Open Sys
ML17278A964
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 07/24/1986
From: Rebecca Barr, Dodds R, Johnson P, Toth A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17278A962 List:
References
50-397-86-21, NUDOCS 8608130328
Download: ML17278A964 (24)


See also: IR 05000397/1986021

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION U

Report No: 50-397/86-21

Docket No: 50-397

Licensee:

Washington Public Power Supply System

P.

O. Box 968

Richland,

WA. 99352

Facility Name:

Washington Nuclear Project No.

2

(WNP-2)

\\ )

Inspection at:

WNP-2 Site near. Richland,

Washington

I

Inspection

Conducted:

June l - July 12,

1986

Inspectors:

R.

T

odd

Senior Resident Inspector

Date Signed

A.

D

oth, Reactor Inspector

June

- 13,

1986

Approved by:

P.

H. J

Reacto

nson,

Chief

rojects Section

3

R.

C.

arr, Resident Inspector

~

~

Date Signed

/ Md0

Date Signed

>(~ ri

Date Signed

Summary:

Ins ection on June

1 - Jul

12

1986 (50-397/86-21)

Areas Ins ected:

Routine inspection by the resident inspectors

and

a regional

inspector of control room operations,

engineered

safety feature

(ESF) status,

surveillance program,

maintenance

program, licensee

event. reports,

special

inspection topics,

and licensee action on previous inspection findings.

During this inspection,

Inspection Procedures

30703,

39701,

42700,

61707,

61726,

62703,

71707,

71710,

71711,

72700,

90712,

92700,

92701,

92702,

92703,

and 93702 were utilized for guidance.

Results:

Two violations or deviations

were identified pertaining to radiation

controls

and tool and equipment accountability during the repair of an

RHR

system valve (paragraph 6).

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DETAILS

Persons

Contacted

D.

J.

-C.

J.

-R.

R.

K.

J.

R.

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M.

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-S.

L.

Mazur, Managing Director

Martin, Assistant

Managing Director for Operations

Powers,

Plant Manager

Baker, Assistant Plant Manager

Corcoran,

Operations

Manager

Beardsley,

Assistant Operations

Manager

Cowan, Technical Manager

Harmon, Maintenance

Manager

Graybeal, Health Physics

and Chemistry Manager

Feldman, Plant equality Assurance

Manager

Peters,

Administrative Manager

Powell, Licensing Manager

Wuesterfeld,

Reactor Engineering Supervisor

Walker, Outage

Manager

Williams, BPA, Nuclear Engineer

Shockley,

HP/Chemistry

Webring, Plant Technical

Hedges,

Maintenance

McKay, Assistant Operation Manager

Davison,

Compliance Engineer

Harrold, Engineering

Manager

>Personnel in attendance

at exit meeting July 11,

1986

An interim presentation

regarding follow-up of previously identified

inspection findings was conducted

June

13,

1986 in conjunction with an

exit meeting by a regional inspector (ref.

NRC Inspection Report 86-22).

The inspectors

also interviewed various control room operators, shift

supervisors

and shift managers,

engineering,

quality assurance,

and

management

personnel relative to activities in progress

and records.

General

Supply System

Management

continued the practice of assigning

an

experienced

licensed senior operator

as the Assistant Operations

Manager

(AOM).

Mr. S.

McKay recently replaced

Mr. R.'Beardsley in that position.

The

AOM position was established

to strengthen interaction between plant

operations

and its support organizations.

Also, the

AOM provides

an

additional technical resource

to the Technical Support Center staff

during an emergency.

'

1

At the beginning of the period the reactor 'was shutdown with repairs to

uninterruptible power supply IN-l,in progress.

The reactor

was restarted

on June 4,

1986.

Training for,prospective-'licensed

operators

was

conducted

on June

4 and 5.

Start-up testing

and surveilla'nces

were

performed from-June

4 through June '20. 'n',June

10,

1986 an unplanned

L

1

V

~'

V

(

)C

reactor

scram occurred while shifting digital electro-hydraulic

(DEH)

control modes of the main turbo-generator.

On June 21,

1986 the reactor

was shut

down when MK-V-53B was determined to be leaking by the seat in

excess

of Technical Specification allowed limits.

On June 29,

1986 the

reactor

was restarted

and achieved

100'/ power on July 4,1986.

On July 10,

while performing

a ground isolation, the reactor

scrammed

due to

de-energizing

a relay that indirectly provides input to the turbine

governor valve control system.

The reactor

was restarted that evening

and

on July 12 was at 82/ thermal power.

0 erations Verifications

The resident inspectors

reviewed the control room operator

and shift

manager log books

on a daily basis during this report period.

Reviews of

the Jumper/Lifted Lead Log, the Clearance

Order Iog and the the

Nonconformance

Log were also performed to verify operations

were being

conducted per Technical Specifications

and licensing requirements.

Events involving unusual

equipment conditions were discussed

with

on-shift control room operators

and were evaluated for safety

significance.

The licensee's

adherence

to Limiting Conditions for

Operations

(LCO's) was observed.

The inspectors

routinely took note of

activated annunciators

on control panels

and ascertained

that control

room operators

were familiar with the reason

and the significance of each

active annunciator.

The inspectors

observed

access

control, manning,

nuclear instrument operability and availability of on-site

and off-site

electrical power.

The inspectors

made regular tours of accessible

areas

to evaluate

equipment conditions,'adiological

controls,, s'ecurity, safety

and adherence

to regulatory requirements.,

n

Detailed reviews of Control Room..Operators'nd

Shift Managers'ogs

and

Clearance

Order Logs were conducted to evaluate

the effectiveness

of

management

actions directed at ~improving. the quality of these

documents.

The omission of significant off-normal conditions from the'ontrol

room

logs--e.g.

frequent venting of the "B" RHR"Loop'due.,to'leakage

from

RHR-V-53B--continue to persist.

Management actions ',to; eliminate

previously noted deficiencies in'he Equ'ipment Clearance

'and Tagging

Procedure

(PPM 1.3.8) (e.g. redundant'erifications

not performed

and

pink sheets

remaining in the active log subsequent

to hanging tags)

have

been effective.

(86-06-02,'Closed).

Future, ins'pections will focus on

licensee efforts to improve the quality of the control room logs

(86-06-04).

No violations or deviations

were identified.

Surveillance

Pro

ram Im lementation

The inspectors

ascertained

that surveillance 'of,safety-related

systems

or

components

was being conducted in accordance

with license

requirements.

In addition to witnessing

and verifying daily control panel instrument

checks,

the inspectors

observed portions of several surveillance tests

by

operators

and instrument

and control technicians.

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PPM 7.4.44.1

PPM 7.4.1.4.1.1

PPM 7.4.8.21.20

PPM 7.4.3.1.1.1

T.P. 8.2.100

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Reactor Coolant 'PH, Chloride and Conductivity

Analysis

Rod Worth Minimizer Pre-Critical Check

Weekly Battery Testing

Intermediate

Range Monitor-.Ch. A-CFT

RCIC Overspeed

Test

Late preparation

and questionable

quality of T..P.8.2.100

(RCIC Over'speed

Test)

caused

the Shift, Manager to reject the initial proposed test.

Additionally, the initial procedure

taken to the Shift Manager

had not

been approved

by the Plant Operating

Committee.

When performed,

the test

was conducted successfully.

No violations or deviations

were

identified.'onthl

Maintenance

Observation

Portions of selected

safety-related

systems

maintenance activities were

observed."

By direct observation

and review of records

the inspectors

evaluated

maintenance activities to be consistent with LCOs and proper

administrative controls.

Maintenance

Work, Request

(MWR) AU0746,

RHR-V-53B repair,

was examined in detail.

The plant was

shutdown

on June

21,

1986 to repair RHR-V-53B which had

seat

leakage in excess of technical specification allowed limits.

Work,

document

MWR AU 0746 established

the requirements

and conditions for

conduct of the repair.

The work instructions did not refer to, as they

should have,

the use of plant procedure

PPM 1.3.18,

Tool and Equipment

Accountability Around Open Plant Systems.

PPM 1.3.18 requires stringent

tool accountability

and work practices

when working on open reactor or

Emergency

Core Cooling Systems.

These controls were not being used in

the repair of MiR-V-53B.

Prior to completing the repair,

the potential

for entry of foreign objects into the system existed particularly when no

actual maintenance

was being performed.

Only a yellow polyethylene

bag

stuffed in the valve body served

as

a boundary.

The work area

was

extremely cluttered

and disorganized.

Tools, rags,

spray

cans

and

miscellaneous

debris were strewn throughout the work area.

The globe of

an overhead light had been broken during the repair and glass

fragments

were scattered

throughout the work area.

The globe had not been replaced

prior to recommencing repairs.

The exposed light bulb represented

an

electrical shock hazard to the workers.

Lanyards

were not being used

on

tools when working over the open valve.

Controls to prevent the entry of

foreign material in the reactor

and

RHR system were not in use.

These

conditions were identified as

an apparent violation of Techni'cal

Specification 6.8.1 (86-21-01).

Radiation Work Permit

(RWP) 286-00-280 established

health physics

and

contamination control requirements for the repair of RHR-V-53B.

The

RWP

required continuous health physics

coverage

when breaching

the system

boundary

and during grinding, welding, machining

and wire brushing,

activities.

Additionally, the

RWP required use'of

a face shield or

respirator during work when the system

was open. During grinding of

RHR-V-53B, continuous health physics;,coverage

was not provided nor was

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the required protective respirator/face

shield worn as required by the

RQP.

Good contamination control work practices

also were not being used during

the maintenance.

The potentially contaminated poly bag that was stuffed

in the valve body to prevent foreign objects

from entering the system

was

frequently removed from the valve and placed

on scaffolding, lagging or

piping during maintenance.

Potentially contaminated tools used during the

maintenance

were not segregated

from those that were not contaminated.

The containers for the discarded protective clothing (PC's)

were too far

from the step off pad requiring the throwing of PC's

6 to 8 feet from the

step off pad to the container.

The container for used PC's

was overfilled

and required emptying.

These conditions were identified as

an apparent

violation of Technical Specification 6.11.

(86-21-02)

Two apparent violations were identified.

7.

En ineered Safet

Feature Verification

This inspection

was performed

as part of the team inspection

and will be

discussed

in inspection report 86-11.

8.

Start-u

Testin /Refuelin

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Control Rod Drive Scram Time Tests

On June 8,

1986,

the inspectors

examined the computer printout of

control rod scram tests that were conducted at rated pressure

and

temperature

pursua'nt to P.P.M. 7.4.1.3.2.

Data were not collected

on two rods and,the

scram times for three other rods were longer

than normal.

These control rod hydraulic systems

were vented to

remove any gas in the hydraulic system.

On June )3,

1986, the

inspector

observed

a portion of the testing of these

rods. All but

one of the five rods

(34-51) met the acceptance

criteria of 3.497

seconds

from the fully withdrawn position to position 5 for the

average

scram insertion time of all operable control rods.

Rod 34-51 had

a measured

time of 3.569 seconds,

well under the

individual scram time limit of 7 seconds.

b.

Local Power Range Monitor (LPRM) Calibration

c ~

The inspector

observed portions of the initial calibration of LPRM

panel meters

and individual power supplies.

He also observed

the

initial traversing in-core probe (TIP) configuration verification

relative to fuel position and the subsequent

full-core flux mapping

(performed at 30/ percent power) that was used to determine the

LPRM

gain adjustments.

The tests

were'"conducted

pursuant to P.P.M.

7.4.3.1.1.70,

LPRM Gain Calibration and Setpoint Check.

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Reactor Recirculation

Pump "B" (RRC-P-B) Testing

The inspector

observed

the initial 60Hz,'0% reactor power testing

of RRC-P-B.

Due to excessive vibration,

RRC-P-,B had been replaced

during the refueling outage.

The maximum pump shaft vibratio'n on

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June

13,

1986 was found to be 6.3 mils at

a Slow of 10,000

gpm.

The

shaft vibration decreased

to about 5.5 mils as

pump flow was

increased

to rated flow during power ascension.

These vibration

levels were within the manufacturer's

recommendations

and,the

pump

was returned to service.

d.

Shutdown Margin Determination

The inspectors

reviewed Surveillance

Procedure 7.4.1.1.,

Shutdown

Margin Determination

(SDM), which utilizes the In Sequence

Method,

and found the procedure technically adequate.

The inspectors

also

observed

the performance of and reviewed the results of the Shutdown

Margin Determination.

The calculations

were verified accurate

and

the surveillance results

were within Technical Specification limits.

The shutdown margin,

however, differed significantly (1'/ delta k)

from the fuel vendor's

(Exxon Nuclear

Company-ENC) calculated value.

ENC, after reviewing their calculations at the licensee's

request,

determined incorrect bias values

had been used in calculating the

shutdown margin.

After using the correct bias values,

the

calculated

shutdown margin closely agreed with the actual

shutdown

margin.

e.

Procedural

Controls

The licensee in Administrative Procedure

P.P.M. 1.2.3.,Plant

Procedure

Control, establishes

the requirements for procedural

use

and compliance.

Step-by-step

performance is used only when the

procedure

being used specifically states

that sequenced

step-by-step

performance is required.

While observing

two reactor start-ups

this reporting period,

the inspectors

observed that the steps within

the procedure

were not being performed in a defined

sequence

and by

not doing so contributed to the complexity and delayed the start-up.

In one instance

the steps for opening the main steam isolation

valves

and having an operating Digital Electro-Hydraulic Control

System were skipped

and not signed off as part of the start-up

checkoff list. Subsequently,

the "verify start-up checklist" block

of the Start-up Procedure,

P.P.M.3.1.2.,

was incorrectly signed off

as completed without a qualifying or explanatory statement.

When

the reactor

reached

190 degrees F., the start-up

was delayed

due to

the inoperability of the

DEH system.

The inspector noted that the

licensee

should reevaluate

the guidance provided in P.P.M. 1.2.3 for

using plant procedures

(86-21-03).

No violations or deviations

were identified.

9.

Residual Heat Removal

S stem Ba'ck-I,eaka

e

Following the refueling outage, trains A'and

B of the

RHR system were

pressurizing

due to back-leakage

from the primary system;

This.

necessitated

frequent venting of each train.

Examination, of local

leakage

rate test data performed during the outage

showed 'the isolation

valves to be well within the test acceptance

criteria.

By'June

19,

1986,

train B needed to'e vented

a'bout every

8 minutes'to,preclude

actuation

of the system pressure relief valves, whil'e trainA needed to be vented

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about every hour.

Accordingly, Temporary Procedure 8.3.4.2,

RHR System

Sack-leakage

Test,

was drafted

and approved by the the Plant Operations

Committee.

The inspector

observed part of the testing conducted

on

June 20,

1986.

The tests

showed the leakage

through RHR-V-53B to be 1.3

gpm, exceeding

the Technical Specification limit, of 1.0 gpm.

The

licensee promptly commenced

a reactor

shutdown in accordance

with

Technical Specification Action Statement 3.4.3.2.c,

achieving "hot

shutdown" within ll hours

and "cold shutdown" within the next

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

Tests of the valve following shutdown

showed the leakage rate to be

equivalent to that measured

at power.

The associated

"B" Train inside

containment isolation check valve was still well within leakage

rate

limits as were the corresponding

valves in train A.

RHR-V-53B was

subsequently

disassembled

and repaired.

Following return to power

operation both train A and

B RHR containment isolation valves exhiMted

minimal back-leakage.

No violations or deviations

were identified other than those associated

with the valve repair itself (see paragraph

6).

Iicensee

Event Re orts

The resident inspectors

reviewed the following reports

and supporting

information on site to verify that licensee

management

had reviewed the

events,

corrective action had been taken,

no unreviewed safety questions

were involved and violations of regulations

or Technical Specification

conditions

had been identified.

LER-85-23

(Open) - Cable Tray Cover Omissions -

As noted in NRC

inspection report 85-37, the licensee

had deferred installation of

missing covers pending evaluation of need via testing by Wylie

Iaboratories.

Hourly fire tours of susceptible

areas

have been

implemented

as compensatory interim measures.

The Hylic Laboratories

testing has

now been

completed

and documented in a test report dated

January

30,

1986.

The licensee

stated that identification of trays with

missing covers

and determination of which do not need covers

and which

still require covers is documented in design

change

package

DCP-85-352,

revisions

OA, OB, and

OC.

The licensee

provided the inspector with a

copy of the Wylie Laboratories test report for review by NRC.

In a January

31,

1986 letter to NRC Nuclear Reactor Regulation

(G02-86-121)

the licensee

advised that

a spray-on non-flammable coating

would be used in lieu of tray covers to meet requirements

of Regulatory

Guide 1.75.

Physical work was found to be in-progress in conjunction

with corrective actions for 10 CFR 50 Appendix R discrepancies

identified

during

a recent

NRC inspection.

The licensee

stated that July 31,

1986

was the target date for completion of all corrective work relative to the

cable tray cover omissions.

This item is considered

an open issue pending

NRC review of,the test

report,

examination of the design

changes

which i.dentify,which trays will

not be covered,

and completion of corrective actions planned by July 31,

1986.

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No violations or deviations

were identified.

11.

IE Bulletin Follow-u

For the IE Bulletin listed below, the inspector verified the bulletin was

received by licensee

management,

that

a review for applicability was

performed,

and that. if the bulletin were applicable to the facility,

appropriate

corrective actions

were taken.

IB-85-02

UV Trip Attachments of DB-50 RT Breakers

(The DB-50 Westinghouse electrical breaker is not used at WNP-2.

This

breaker is frequently used in PWR's

as

a scram breaker.)

12.

IE Circulars

and Notices

For the IE Circulars/Notices listed below, the inspectors verified that

the Circular/Notices

were received,

that an applicability review was

performed,

and that if applicable to the facility, appropriate

corrective

actions

were taken.

IC-80-21

Regulation of Refueling Crews

IC-81-14

Evaluate

MSIV Programs

and Propose

Changes

to

Minimize Problems

13.

WNP-2 has developed

and implemented

an effective computerized

system for

logging and tracking the status of IE Bul'letins, Circulars

and Notices.

However, if the item is found to be applicable to the facility,

appropriate corrective actions

are frequently slow to be identified and

implemented.

Recently, all open external,",commitments

were integrated

into a

common data base to aid management in tracking open commitments.

To date, little improvement has been observ'ed,in

the closing of long

standing

open information notices

(86'-21,-04).

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Xicensee Actions

On Previous

NRC Ins ection Findin s

The inspectors

reviewed records,

interviewed'personnel,

and i.nspected

plant conditions relative to licensee

actions

on previously identified

inspection findings:

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(Closed) Follow-up Item (84-35-01) - Omission of small diameter vent

and drain valves from containment integrity checklist.

NRC inspections

(reports

84-35

and 84-37) identified vents

and

drains which did not appear

on surveillance checklists.

This

matter, subject of a subsequent

notice of violation (report 85-11,

item 85-11-03)

was resolved

as described in'eport 85-36.

A

Technical Specification

change to section 4.6.1.1.b

(Amendment No.

22) clarified that small diameter vents

and drains

need not be

secured in place

and verified on 31 day cycles.

The previously

noted omissions of such valves from the surveillance checklists is

now a closed issue.

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(Closed) Follow-up Item (84-36-01) - Potent~al'deficiency

in

cable crimp connections

of battery chargers

(identified at another

,reactor facility).

Inspection report 85-12 (Paragraph

6.'a) recognized

the licensee's

efforts to assess

the performance of electrical power connectors in

equipment throughout the plant, using infra-red detectors.

The

licensee

has recently procured

such equipment for repeated

use

and

has

conducted additional surveys

and corrective actions.

The

electrical maintenance

supervisor stated that the battery charges

had been subject to maintenance

which involved tightening of the

connections,

and no problems

have been noted with the crimp

connectors.

(Closed) Follow-up Item (85-36-02) - Minor loss of control of

weld filler material by craft's.

The January

1-May 10,

1986 Quality Assurance

surveillance report

2-86-085

documented part of the refueling outage. It included field

checks of locked and unlocked tool boxes

and associated

work areas

in the reactor plant,

and determined that uncontrolled filler

material was not being retained

by crafts.

The audits apparently

had the effect of sensitizing the crafts to management

concern in

this area

and eliminated the practice of retaining miscellaneous

weld electrodes for use in weld joint fit-ups and other non-welding

purposes.

The inspectors

noted

no instances

of uncontrolled weld

material during routine tours of work areas.

(Open) Follow-up Item (85-12-01) - Improvement In Identifying

and Correcting Drifting Setpoints of Instruments.

Inspectors

noted in reports

85-12 and 85-36 that the licensee's

calibration activities had identified setpoint drift which in some

cases

exceeded

est:ablished

tolerances,

but for which corrective

actions

appeared

confined to simply adjusting the instrument.

It

appeared

advisable to establish

methods to identify and assess,,

instrument drift prior to exceeding

tolerances

permitted by

technical specifications

thus assuring that the instruments

would

not be out of specification for prolonged periods of time between

calibrations.

It was noted that corrective measures

could include

incre'asing

the frequency of calibration beyond that required by the

technical specifications

or repair/replacement

of the instruments.,

Subsequently,

the licensee

established

a simple computer program

data base

which will print, a graph of the setpoint calibration

history of each principal instrument

and display 'technical

specificat:ion

and more conservative administrative limits.

Currently, the ISC engineer,

who is responsible for review of

completed calibration data,

enters

the current calibration data into

the computer

and identifies items which exceed

the administrative

limit.

d'or such out-of-calibration items, he obtains a,printout of

the history for that instrument

and forwards it to the Technology

department instrument engineer for'evaJuation

and action.,b-

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For the specific items previously identified by the

NRC inspectors

(HCU and CIA pressure

switches)

the printouts demonstrated

that

corrective action was taken to increase

the calibration frequency to

correct the setpoints

before technical specification limits were

exceeded.

The licensee

program included Static 0-Ring differential pressure

transmitters

used for reactor vessel level measurement.

Printouts

showed that setpoint drift had not exceeded

technical specification

tolerances,

as determined

by the calibration technique

being used,

in those

areas

examined by the inspector

(WPPSS pressure/level

transmitter calibrations involve isolation of the instrument

and

application of fluid pressure

to the actual mechanical

components of

the sensors).

The licensee

program is still under development

and all instruments

have not yet been included in the data base.

Procedures

have not yet

been established

to define responsibilities,

interfaces,

action

thresholds,

and other management

expectations

such

as corrective

action alternatives.

This licensee

program will be subject to

further NRC review as it is developed.

(Closed) Violation (85-37-02) - Vent and Drain valves were

found unlocked without record in the locked valve checklist.

The licensee

corrective action was documented in letter to NRC dated

January

10,

1986. Additionally, the locked valve checklist procedure

(PPM-1.3.29)

has been revised to clarify control of deviations.

The

specific valves in question,

(RFW-45A and 458) have been deleted

from locked valve requirements,

consistent with the resolution of

item 84-35-01

(above).

(Open) Zollow-up Item (85-37-03) -

Licensee initiatives to reduce

backlogs of nonconformance

reports.

In November

1985 the inspector noted licensee efforts to reduce

and

control backlogs of nonconformance

reports.

Additional continuation

of this licensee effort was noted in plant internal memoranda

and

memoranda

to the corporate Assistant

Managing Director for

Operations,

during the September

through December

1985 period.

Initiatives and follow-up included directions to plant technical

supervisors

expressing

management

expectations

for periodic review

of outstanding

NCRs, including review for validity and alternative

corrective actions for each

NCR. Additional guidance

was included

for separating

long term design

improvement related corrective

measures

from the interim, short term actions necessary

to correct

the immediate nonconforming condition.

The Quality Assurance

department is currently the final approval authority for close-out

of nonconformance

reports

and interview of the Quality Assurance

Manager

showed that he appeared

to be, sensitive toassuring that

NCRs are not prematurely or improper'ly 'closed

.He had limited NCR

closure review and approval authority to only a few of his'enior

level staff members,

and had monitored their activities through

personal

and corporate office audits...Various plant management

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supervisors

stated that

a concerted effort had been

made prior to

the recent refueling outage to identify NCRs which should be

included for corrective action during the outage.

The inspector

examined the current Plant Tracking Log (PTL) for all

open

NCRs originating from time of issuance

of the operating license

through mid 1985

((283-0167,, through 285-372).

Of these

84 NCRs,

20

were examined to determine

the appropriateness

of their, current lack

of resolution.

Most of these

appeared

to-be of low:significance or

had other elements

which appea'red 'to'justify, deferral

due to

prioritization of resources.

However<" three of these

unresolved

NCRs appeared

overdue without good

cau'se

and reflected

need for

continued

management

emphasis, on ba'cklogs:

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285-020 QCII tubing installed in a QCI in'strument rack

(Originated January

15,

1985') ~,"'-'

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285-228 Improper installation of anchor bolts in spray pond header

drain piping supports

(Originated May 14,

1985)

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285-267 Failure to obtain/record specific quarterly surveillance

information to meet,

ASME in-service te'st, requirements

(Originated April 22,

1985)

The inspector did not identify any long-standing unresolved

NCRs

with significant safety implications.

However, the inability to

effect timely resolution of issues

appears

to be an indicator of

adequacy of technical support resources.

This aspect will be

considered

during future

NRC inspections

and the issue of backlogs

is considered

a continued

open item.

(Open) Follow-up Item (85-38-02) - Absence of management policy

regarding long-standing activated annunciators.

The Operations

Department

implemented

a procedure requiring

clearance

order tagging of malfunctioning annunciators.

The

temporary procedure

change

system permits

changing annunciator

response

procedures

to clarify operator actions for malfunctioning

annunciators.

According to the Operations

Manager, Shift Managers

should utilize this procedure

(e.g. specify frequency of repeated

verification of alternative information to assure that spuriously

activated annunciators

do not mask actual

abnormal conditions)

when

annunciators

repeatedly malfunction.

This policy is not currently

documented

and such actions

have been

at, the discretion of

individual Shift Managers.

This will remain an open item until licensee's

management

expectations

are

documented

or sufficient inspection data are

compiled to support effective policy implementation.

(Open) Follow-up Item (85-38-04) - Lifted leads,

authorized

under

a

long suspended

work request,

were found on the spray pond level

transmitter barometric

compensators.

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When this finding was identified, the licensee

committed to an audit

of open,

long-standing

work requests

to determine if similar

jumpers or lifted leads existed.

During the current inspection,

the

licensee

maintenance

manager

said such

a review had been

conducted

but was not documented.

He also stated

a review was conducted of

the Jumper/Lifted Lead Logs and all unnecessary

jumpers

and lifted

leads

were removed.

To improve future controls in this area

a

revision of the Jumper

8 Iifted I,ead administrative procedure

was

submitted to the Plant Operations

Committee for consideration.

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(Closed) Follow-up Item (86-04-02) - Chemistry Department

technicians failed to verify or record that they verified use of the

current revision.

The licensee

issued

nonconformance

reports

286-021

and

022 to

prescribe corrective action.

The

January

24,

1986 memorandum to

chemistry staff reiterated

the importance of surveillance procedure

verification prior to use.

This action is considered

appropriate to

alert technicians

and data reviewers to the requirement.

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(Open) Violation (86-06-01) - Improperly stored high pressure

nitrogen bottles

(May 23, 1986).

Licensee corrective actions

included:

1)

revising P.P.M. 1.3.19,

Housekeeping,

to clarify gas cylinder

storage

requirements

2)

committing to training plant and contractor personnel

on gas

cylinder storage

requirements

(not yet implemented)

During a tour, the inspector noted six cylinders in the reactor

building not secured at the base,

as prescribed

by the newly issued

procedure.

When brought to a

maintenance

supervisor's

attention he

took immediate corrective action.

This discrepancy is an element of

general

housekeeping

and is addressed

in more detail in inspection

report 86-22.

This item remains

open pending completion of the

licensee'raining definition and implementation

and reinspection of

plant conditions.

12.

Mana ement Meetin

During this time the inspectors

met periodically with plant management

and discussed

inspection findings.

On July 11,

1986 the inspectors

met

with the Plant Manager

and members of his staff,

as noted in paragraph

1,

to discuss

inspection f'indings.

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