ML17264A845
| ML17264A845 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 03/25/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17264A843 | List: |
| References | |
| 50-244-97-01, 50-244-97-1, NUDOCS 9704020021 | |
| Download: ML17264A845 (50) | |
See also: IR 05000244/1997001
Text
O
U.S. NUCLEAR.REGULATORY COMMISSION
REGION
I
License Nos.
DPR-1 8
Report No.
50-244/97-01
Docket No..
50-244
Licensee:
Facility Name:
Location:
Rochester
Gas and Electric Corporation (RGSE)
R. E, Ginna Nuclear Power Plant
1503 Lake Road
Ontario, New York 14519
Inspection Period:
January 5, 1997 through February 23, 1997
Inspectors:
Approved by:
P. D. Drysdale, Senior Resident Inspector
C. C. Osterholtz, Resident Inspector
T. A. Moslak, Project Engineer,
G. S. Vissing, Project Manager,
L. T. Doerflein, Chief
Projects Branch
1
.
Division of Reactor Projects
970402002i
970325
ADQCK 05000244
8
0
lk
EXECUTIVE SUMMARY
R. E. Ginna Nuclear Power Plant
NRC Inspection Report 50-244/97-01
This integrated inspection included aspects of licensee operations,
engineering,
maintenance,
and plant support.
The report covers
a 7-week period of resident inspection.
In addition, it includes the results of announced
inspections by a regional project engineer
and the NRR Project Manager for the Ginna.Station.
~Oerations
Classroom training on Improved Technical Specifications
(ITS) implementation was
appropriate
in that it focused on an area that had been identified as a potential weakness
with operations
personnel.
The performarice of mock simulator examinations
at the
beginning of the training week was c'onsidered
a good practice in identifying specific
training concerns.
Also, the programs in place to ensure that all license'd personnel
receive
a biennial physical examination was considered
adequate.
The practice of extending
a
normal shift to meet programmatic requirements for operator proficiency has been
forwarded to NRR for further evaluation.
This item is unresolved
(URI 50-244/97-01-01).
The implementation of Priority "D" ACTION Reports to capture.low threshold incidents that
reflect possible negative performance trends was considered
a good initiative;
Nuclear Safety Audit and Review'oard (NSARB) issues were discussed'in
depth and all
.
members who participated demonstrated
a questioning attitude.
The members outside
RGRE nuclear operations were particularly active, utilizing their experiences
at other plants
to positively contribute to the discussions.
The QA/QC subcommittee
meeting provided good oversight of plant activities and audit
results.
The subcommittee
provided self-critical assessments,
focusing management
attention on the underlying root causes.
Positive measur'es
were incorporated to
improve'ata,
presentation.
The licensee had made an improvement in th'e documentation
of safety reviews, and a
heighten'ed
awareness
existed throughout'the
Ginna operation staff of the 10 CFR 50.59
process.
With one. exception, the safety review's adequately substantiated
that no
unreviewed safety question requiring a safety evaluation existed.
'aintenance
Overall, maintenance
and surveillance activities were performed effectively and were well
coordinated with all site organizations.
Maintenance technicians demonstrated
good
technical abilities and performed their work in accordance
with procedure requirements.
Maintenance
on the A-safety injection pump breaker was performed effectively. The
maintenance
technician. demonstrated
good technical abiljty arid performed the work in
accordance
with the procedure requirements.
The licensee's efforts to augment their
Executive Summary (cont'd)
inspection of Westinghouse
breaker contacts during routine breaker maintenance
were
appropriate.
The licensee appropriately responded
to plant fire alarms and effectively secured the
Control Rod Drive B-Motor Generator
(B-MG) Set.
The licensee also appeared
to identify
the cause of the MG set failure. However, the generator bearings may not h'ave received
adequate
lubrication, and the maintenance
procedure may not have provided sufficient
guidance to ensure that bearings
are adequately
lubricated.
The licensee stated that they intend to resolve excessive
vibrations in recirculation line
instrument tubing in the safety'injection system during pump operations.
The inspectors
considered this appropriate.
The licensee i'nitiated appropriate action in response
to the identified discrepancy between
the Improved Technical Specifications and the Updated Final Safety Analysis Report
regarding the operability of the auxiliary feedwater recirculation line..
Given the discrepancy between the acceptance
criteria basis assumptions,
and the ITS and
Updated Final Safety Analysis Report, the licensee's intention to re-evaluate the
acce'ptance
criteria for diesel generator compressor
check valve leakage was appropriate.
A number of discrepancies
were noted in the Training System Description.
However, the
licensee stated that the noted discrepancies
would be resolved.
h
The licensee stated that they intend to revise the emergency diesel generator periodic tests
to ensure that the proper service water pump line-up would be selected after testing was
completed.
The inspectors considered'his
appropriate.
. The licensee responded
expeditiously to secure unlocked QA storage areas.
The inspector
considered this condition t'o be an inadvertent oversight, and follow-up actions to evaluate
the processes
for modifying QA area boundaries
were appropriate.
~En ineerin
The license'e adequately
responded
to a noted increase
in reactor coolant system activity
levels and determined that the increases
were still well below the ITS limits. Continuous
monitoring of these levels for trends was appropriate.
The licensee's
aetio'ns to eliminate unnecessary
feedwater flow oscillations were effective.
No excessive oscillations occurred in.the A-train following adjustments
in its control
system.
The licensee's intention to incorporate the same change to the B-train channel
was appropriate.
The licensee took appropriate actions to correct the low temperature
conditions in the
screenhouse
bay, and to evaluate the consequences
for design basis conditions.
The
reanalysis for lower inlet temperatures
effectively demonstrated
that the consequences
of lower temperatures
would have a minimal impact under accident conditions.
A
Executive Summary (cont'd)
re-evaluation of the operability criteria for screenhouse
minimum water level and
temperature
monitor inaccuracies
at the minimum and maximum lake water inlet
temperatures
was appropriate.
Plant Su
ort
The failure to perform whole body counts on at least three in'dividuals terminated from
Ginna had minor safety significance and.represented
a failure of the licensee to meet an
administrative requirement.
The licensee had initiated adequate
corrective action.
Accordingly, this constituted
a violation of minor significance and is being treated as a non-
cited violation.
The licensee's actions to implement effective radiological work practices, to maintain
proper contamination boundary controls, and to monitor. to assure
radiological work
practices adequately prevent the spread of'ontamination have not been effective over
~
recent months.
The actions taken to identify and correct poor radiological work practices,
and to prevent the spread of potential and actual contamination have also not been
effective.
These conditions represent a'violation of 10 CFR 50, Appendix B, Criterion XVI,
"Corrective Actions," (NOV 50-244/97-01-02).
Ig
TABLE OF CONTENTS
EXECUTIVE SUMMARY
TABLE OF CONTENTS ..... ~.................., ~.....
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I. Operations
01
05
07
08
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Conduct of Operations..... ~................. ~........
01.1
General Comments
01.2
Summary of Plant Status
Operator Training and Qualification ..'. ~... ~......
05.1
Licensed Operator Training Observations
and Qualification
Review .....
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Quality'ssurance
in Operations
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07.1
Problem Identification and Resolution
07.2
Nuclear Safety Audit and Review Board (NSARB) Meeting ..
07.3
Self- Assessment
Activities
07 4
Review of 10 CFR 50.59 Activities ..................
Miscellaneous Operations Issues.........,......'; .:.....
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08.1
(Closed) LER 96-013: Circuit Breakers Closed While in Mode
Due to Personnel
Error, Resulted in Condition Prohibited by
'echnical Specifications;
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~ I. Maintenance
M1
M2
~ M3
M7
Conduct of Maintenance
M1 ~ 1
General Comments on Maintenance Activities
M1.2
General Comments on Surveillance Activities ......
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Maintenance
and Material Condition of Facilities and Equipment
M2.1
A-Safety Injection (A-Sl) Pump Breaker Maintenance
M2.2
Control Rod Drive B-Motor Generator (B-MG) Set Failure ...
M2.3
C-Safety Injection (C-Sl) Pump Quarterly Test
Maintenance
Procedures
and Documentation ....
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M3.1
B-Auxiliary Feedwater
(B-AFW) Pump Periodic Test .......
M3.2
Diesel Generator Starting Air Compressor
Discharge Check
Valve Closure Test
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M3.3
A-Diesel Generator Perio'dic Test
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Quality Assurance
in Mainte'nance Activities
M7.1
Unsecured
QA Material Storage Areas................
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.II. Engineering
E2
E8
Engineering Support of Facilities and Equipment .'..............
E2.1
RCS Total Gas Activity Increase
E2.2
Feedwater Flow Oscillations
E2.3
Temperature
Monitoring of Lake Ontario Inlet Water ~......
Miscellaneous
Engineering
Issues
E8.1
(Closed) LER 96-015: Based on Review of NRg Generic Letter 96-06, a Thermally Induced Overpressure
Transient Could
0 ccure
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IV. Plant Support ..................
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R3
Radiological Protection and Chemistry (RPSC) Procedures
and
Documentation
R3.1
Whole Body Counting for Terminated Employees
R7
Quality Assurance
in Radiological Protection and Chemistry
Activities
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Poor Radiological Work Practices and Inadequate
Contamination Area Boundary Controls
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V. Management
Meetings ..
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X1
Exit Meeting Sum'mary............
L2
Review of UFSAR Commitments
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2.4
ATTACHMENT
Attachment
1 - Partial List of Persons
Contacted
- Inspection Procedures
Used
- Items Opened, Closed, and Discussed
- List of Acronym Used
I. 0 erations
01
Conduct of
Operations'1.1
General Comments
Ins ection Procedure
The inspectors observed
plant operation on a daily basis to verify that the facility
was operated
safely and in accordance
with licensee procedures
and regulatory
requirements.
This review included tours of the accessible
areas of the facility,
verification of engineered
safeguards
features
(ESF) system operability, verification
of proper control room and shift staffing, verification that the plant was operated
in
conformance with the Improved Technical Specifications
(ITS) and appropriate
action statements
for out-of-service equipment were implemented,
and verification
that logs and,records
accurately identified equipment status or deficiencies.
01.2
Summar
of Plant Status
The plant operated at full power (approximately 100%) for the majority of the
inspection period.
On'ebruary
11, 1997, power was reduced to approximately
96% for about three hours and returned to full power.
Plant power was again
reduced.to approximately 96% on February 12 for about five hours, and then
returned to full power.
These temporary powe'r reductions'ere
performed to
maintain minimum Improved Technical Specification (ITS) temperature
limits for
service water inlet temperature without exceeding the New York State requirements
for maximum differential temperature for lake water inlet and outlet temperature
(see section E2.3). Additionally, a failure of the control rod driv'e 8-motor generator
(B-MG) set occurred on'February
18, 1997.
Plant personnel
responded
appropriately and no plant transient resulted from the failure (see section M2.2).
05
Operator Training and.Qualification
05.'1
Licensed 0 erator Trainin
Observations
.and Qualification Review
a.
Ins ection Sco
e (71707)
The inspectors observed
a classroom training session
on Improved Technical
Specifications
(ITS) implementation and simulator training on a loss-of-heat-sink
and
a small break loss-of-coolant accident (LOCA). The. inspectors
also reviewed.
records pertaining to licensed operator medical and proficiency requirements.
'Topical headings. such as 01, MS, etc., are used in accordance with the NRC standardized
reactor inspection report outline.
Individual reports are not expected to address
all outline
topics.
Observations
and Findin s
The inspectors attended
a classroom training session
on ITS implementation on
January 31, 1997.
ITS implementation by operations
personnel
had previously
been identified by the NRC as a potential weakness
(see Inspection reports (IRs)
50-244/96-11
and 50-244/96-05)
~ The training included analyses of the ITS bases
and was conducted interactively with operations
personnel
~
During the training
session, the instructor also addressed
questions from the operators concerning
specific plant scenarios
and applicable ITS requirements.
The inspectors
also observed simulator training for a licensed operating crew on a
loss-of-heat-sink
and a small break LOCA on February 3, 1997, the first day of the
training week.
The trainers initially administered
a practice examination on the crew
to identify any deficiencies that could be addressed
later in the week.
The
inspectors noted that all operator aid tags on the simulator were consistent with
tags in the plant's control room, and that the performance observations
recorded by
the licensee's training personnel were consistent with those identified by the
inspectors.
The inspectors reviewed medical records for all licensed personnel
and verified that
they all had received
a physical examination within the last two years as required by
10 CFR 55.53, "Condition of Licenses."
The inspectors
also reviewed the 1996
~ operations records for a sample of licensed operators to verify that they had
maintained their licenses active by standing
a minimum number of watches
as
specified in 10 CFR 55.53.
10 CFR 55.53(e) states,
in part, that, "To maintain
active status, the licensee shall actively perform the functions of an operator or
senior operator on a minimum of seven 8-hour or five 12-hour shifts per calendar
quarter."
The review indicated that all operators
had met the minimum number'of
total hours (56) required to maintain proficiency.
However, one instance was noted
during the second
calen'dar quarter'of 1996 where an operator stood one'regular"8-
hour shift, three regular 12-hour shifts, and then extended
a regular 8-hour shift to
12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> by relieving the watch 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> early.
His quarterly watches met the
. minimum of 56 hours6.481481e-4 days <br />0.0156 hours <br />9.259259e-5 weeks <br />2.1308e-5 months <br /> over five shifts, but it was not apparent whether the
regulatory requirements were being adequately satisfied under these circumstances.
Therefore, the inspectors forWarded theissue to The Office of Nuclear Reactor
Regulation
(NRR) for evaluation.
Conclusions
The inspectors concluded that tPe classroom training on implementing the ITS was
appropriate
in that it focused on an area that had been identified as a
potential'eakness
with operations
personnel.
The inspectors considered the performance of
mock simulator examinations at the beginning of the training week to be a good
practice in identifying specific training concerns.
Also, the programs in place to
ensure that all licensed personnel receive a biennial physical examination was
considered
adequate
in that no instance was found where the programmatic
requirements
were not met.
However, the practice of extending
a normal shift to
meet programmatic requirements for operator proficiency has been forwarded to
NRR for further ev'aluation.
Pending the results of the evaluation, this item remains
unresolved
(URI 50-244/97-01-01).
07
Quality Assurance in Operations
The inspectors
assessed
various licensee controls for identifying and correcting
problems.
This included a review of Revision 6 to IP-CAP-1, the problem reporting
procedure,
and attending
a Nuclear Safety Audit and Review Board (NSARB) QA/QC
subcommittee
meeting.
07.1
Problem Identification and Resolution
a.
Ins ection Sco
e (40500)
The inspector reviewed the licensee's
process for identifying, tracking, and
resolving problems.
b.
Observations
and Findin s
On November 11, 1996, IP-CAP-1, "Abnormal Condition Tracking Initiation or
Notification (ACTION) Report," was revised to include a lower thieshold of problem
reporting.
By management
request, ACTION Report initiation was desired for
. events or conditions that are of.very low risk, that do not require documented
investigation or corrective actions, but would provide useful precursor information if
tracked and trended for identification of repeat occurrence.
Such problems were to
be documented
with an ACTION Report and categorized
as Priority "D" by the
originator.
The PORC Chairman makes the -final determination on the appropriate
'ategory
during the daily report review.
Examples of items to be reported were
problems involving housekeeping,
administrative shortcomings,
and findings
identified duririg routine Shift Technical Advisor tours, the Supervisory Safety,
Housekeeping,
Administrative, Reliability, and Productivity (SHARP) Program tours,
and the Radiological Protection management
tours.
Management
has actively promoted use of the Priority "D" ACTION Reports through
an award/recognition
system.
The inspector examined the approximately three
dozen reports generated to date and determined that the problems described were
appropriately prioritized. The problems reflected minor lapses in the use,of 'personal
protective equipment, paperwork processing
discrepancies,
and abnormal plant.
equipment operating trends,.with no problem commonality evident.
The inspector considered the implementation of a Priority "D" ACTION Report to be
a good initiative to focus management
and'staff attention to low threshold, off
normal conditions
however, due to its-short history, the ariticipated benefits of this
initiative have not beeri realized in preventing, a more significant incident from
occurring.
c.
Conclusion
The inspector concluded that the implementation of Priority "D" ACTION Reports to
capture low threshold incidents that reflect possible negative performance trends
was a good initiative.
07.2
Nuclear Safet
Audit and Review Board
NSARB Meetin
a.
Ins
e tion Sco
e (40500)
The NRR Project Manager for the Ginna Station attended the NSARB quarterly
meeting held on January 29 and 30, 1997.
b.
Observations
and Findin s
h
The NSARB meeting was conducted
in accordance
with the Updated Final Safety
Analysis Report (UFSAR). The membership
included four individuals from outside
organizations,
as well as personnel from RGRE management.
Particular attention
was addressed. on the review of the draft letter in response to the.10 CFR 50.54(f)
letter of October 1996.
Other discussions
focused on p)ant performance,
Licensee
Event Reports (LERs), NRC inspections; the 10 CFR 50.59 process, the. proposed
modification to the spent fuel storage pool, the proposed
exemption to the
regulations relating to the low temperature
over-pressure
(LTOP) requirements,
and
the recent submittal to the NRC regarding the Probabilistic Safety Assessment.
The.
NSARB Chairman was particularly interested
in the feedback provided by outside
board'members.
Those items on the agenda
not discussed
were rescheduled
for
subsequent
meetings.
C.
Conclusions
The Project Manager concluded that the issues were discussed
in depth and all
members who participated demonstrated
a questioning attitude.
The members
outside RGKE nuclear. operations
appeared
particularly. active, utilizing their
experiences
at other plants to positively contribute to the discussions.
07.3
Self- Assessment
Activities
P
Ins ection Sco
e (40500)
The inspector assessed
the QA/QC subcommittee to the NSARB in evaluating audit
results and recommending
corrective actions.
b.
Observations
and Find n s
On January
16, 1997, the inspector attended
a meeting of the QA/QC
subcommittee to the NSARB. The meeting addressed
the status of open items from
past meetings,
a review of recently completed audit reports regarding maintenance
personnel training/qualification, the Cooperative Management Audit Program
(CMAP), and ACTION Report trending data.
The subcommittee
also addressed
the
results of a Human Performance
Enhancement
System
(HPES) evaluation relating to
an operator inappropriately closing certain safety-related
breakers
as a result of poor
communications
between the control room foreman and the operator.
The subcommittee's
discussions
were properly focused on safety and areas for
management/supervisory
improvement.
New methods of presenting ACTION
Report data to better direct attention on repetitive problems by Equipment
Identification Number/Cause
Code and by Organization/Cause
Code were discussed.
Additionally, management
directed that criteria be improved for selecting the "Top
Ten" ACTION Reports to better focus management
attention on the underlying
causes.
C.
Conclusion
The QA/QC Subcommittee
meeting provided good oversight of plant activities and
.audit results.
The subcommittee
provided self-critical assessments,
focusing
management
attention on underlying root causes.
Positive measures
were
incorporated to improve data presentation.
07.4
. Review of 10 CFR 50.59 Activities
a ~
Ins ection Sco
e (37001)
\\
The NRR Project Manager for the Ginna Station performed
a sample review of the
licensee's
10 CFR 50.59 activities.
b.
Observations
and Findin s
The Project Manager reviewed a sample of Safety Reviews of modifications
performed by the licensee
in accordance
w'ith IP-SEV-1, "Preparation,
Review and
Approval of Safety Reviews."
Additionally, since the licensee was in the process of
revising IP-SEV-1, the latest draft of this procedure was also reviewed.
It was
noted that several improvements were made, particularly in the appendices that
provided guidance
in. answering questions'that
determined if an unreviewed safety
question existed..
The Project Manager also reviewed
a selection of safety evaluations included in the
Annual Report of Facility Changes,
Tests, and Experiments Conducted Without Prio'r
Commission Approval, dated December 16, 1996.
These included:
SEV-1020, "Steam Generator Rigging and Handling"
SEV-1057, "18-Month Fuel Cycle"
SEV-1062, "Revision
1 to the.Technical Requirements
Manual"
SEV-1064, "MOV-4616 50% Open Throttling"
SEV-1020, SEV-1057, and SEV-1062 all appeared
to be comprehensive,
addressing
each of the three criteria for determining if an unreviewed safety question existed.
The Project Manager was concerned that SEV-1064 did not address the possibility
of degradation
occurring in MOV-4616 by operating it throttled at 50%.
However,
the licensee indicated that they had intended this modification to be temporary, and
the actuator for the valve was changed after approximately three months to allow
for full closure within its required time limit.
The licensee had performed an audit to assess
the adequacy of its 10 CFR 50.59
process.
The audit identified strengths
and weaknesses
and made
recommendations
accordingly.
Although the audit noted that a strength was in the
training of preparers
and reviewers, it recommended
related refresher training and
training to PORC and NSARB members regarding their specific unreviewed safety
question review responsibilities.
Other recommendations
included revising training
materials to be consistent with 10 CFR 50.59 requirements
and NRC guidance,
establishing
a process for self assessment,
and reviewing current practices
regarding the designation of inconsequential
changes.
C.
Conclusions
Based on previous inspections conducted
over the past year and interviews of
licensee personnel during this visit, the Project Manager concluded that the licensee
had made an improvement in the documentation
of safety review's.
A heightened
awareness
also existed throughout the Ginna operation staff of the 10 CFR 50.59
.process.
With the exception of SEV-1064, the safety reviews adequately
substantiated
that no unreviewed safety question requiring a safety evaluation
existed.
The Project Manager considered
one weakness
in SEV-1064 was in not
identifying the modification as temporary.
08
Miscellaneous Operations Issues (92700)
08.1
Closed
LER 96-01'3: Circuit Breakers Closed'While in Mode 3
Due to Personnel
Error Resulted in'ondition Prohibited b
Technical 'S ecifications.
LER 96-013 was submitted on November 27, 1996, as a result of an improper
closure of breakers for safety injection (Sl) pump discharge valves prior to entry into
MODE 4 during a reactor plant cooldown (see IR 50-244/96-11).
The breakers
were shut for a short period of time with the plant about 3'F above the maximum
average
RCS temperature
(Tave) allowed by the ITS for entry into MODE,.4
'<350~F).
However, this resulted in two trains of the emergency core cooling
system
(ECCS) being considered
ino'perable, which required entry into ITS limiting
condition for operation
(LCQ) 3.0.3.
'he
LER attributed the underlying cause of 'this event to personnel
error, resulting
from less than adequate
verbal communications
between the control room and in-
plant operators,
and the use of unclear supervisory methods.
The licensee
performed a Human Performance
Enhancement
System
(HPES) evaluation in.
response to this event.
The evaluation reinforced the causes
identified in the LER,
and recorr)mended that procedural, steps performed by operators
outs(de the control
room be more formally controlled.
The HPES recommended
that labels'be attached
to the Sl pump discharge
breakers to indicate the conditions under which they may
be operated.
Administrative procedure A-52.1, "Shift Organization and Responsibilities," was
revised to indicate that local operations affecting reactivity or manipulation of
safeguards
equipment shall be communicated to the control room just prior to
performance.
The licensee also indicated that condition labels would be attached to
the Sl pump discharge breakers.'he
inspectors considered that the LER and HPES
adequately described this event,.and
appropriately addressed
the root causes
and
corrective actions.
This LER is closed.
II. Maintenance
M1
Conduct of Maintenance
M1.1
General Comments on Maintenance Activities
a 0
Ins ection Sco
e 62707
The inspectors observed portions of plant maintenance
activities to verify that the
correct parts and tools were utilized, the applicable industry codes and,technical
specification reqUirements were satisfied, adequate
measures
were in place to
ensure personnel safety and prevent damage to plant structures, systems,
and
components,
and to ensure that equipment operability was verified upon completion
of post-maintenance
testing.
b.
Observations
and Findin s
the inspectors observed portions of the following maintenance
activities:
A-Safety Injection (A-Sl) pump breaker maintenance;
observed
on February
4, 1997 (see section M2.1)
Control rod drive B-motor generator
(B-'MG) set maintenance
performed in
response
to equipment failure~ observed from February 18 - February 21,
1997 (see section M2.2)
c.
Conclusions
Overall, the inspectors concluded that the observed
maintenance
activities were
performed effectively and were well coordinated between the applicable site
organizations,
Maintenance technicians demonstr'ated
good technical abilities and
performed their work in accordance
with procedure requirements.
4
8
M1.2
General Comments on Surveillance Activities
a.
Ins ection Sco
e 61726
The inspectors observed
selected surveillance tests to determine whether approved
procedures
were in use, details were adequate,
test instrumentation was properly
calibrated and used, technical specifications limiting conditions for operation
(LCOs)
were satisfied, testing was performed by qualified personnel, test results satisfied
acceptance
criteria or were properly'dispositioned,
and correct post-test system
restoration was performed.
b.
Observations
and Findin s
The inspectors observed
portions of the following surveillance tests:
~
PT-16Q-B, "AFW Pump B - Quarterly," observed
on January 31, 1997 (see
section M-3.1)
PT-2.1-0, "Safety.injection System Quarterly Test," was performed on the
C-Sl pump and observed
on February 5, 1997 (see section )VI-2.3)
PT-12.7, "Diesel Generator Starting Air Compressor
Discharge Check Valve
Closure Test," observed
on February 11, 1997 (see section M-3.2)
~
PT-12.1, "Diesel Generator A," observed
on February 19, 1997 (see section
M-3.3)
w
~
PT-12.2, "Diesel Generator B," observed
on January 27, 1997.
t
c.
Conclusions
Overall, the inspectors concluded that the observed
surveillance activities were well
controlled and coordinated with other site organizations.
Testing was performed in
accordance
with procedure requirements
and technicians demonstrated
a good
understanding
of the functional'requirements
of the equipment being tested.
M2
. Maintenance and Material Condition of Facilities and Equipment
I
l'
M2.1
A-Safet
In'ection
A-Sl Pum
Breaker Maintenance
a.
Ins ection Sco
e (62707)
The inspectors observed
and reviewed routine maintenance
associated
with the
A-Sl pump breaker.
b.
Observations
and Findin s
On February 4, 1997, the inspectors observed
routine maintenance
on the A-Sl
pump breaker in accordance with procedur'es
M-32.1.50, "DB-50 Circuit Breaker
Maintenance,"
and M-32.8, "Installation and Testing of Amptector Overcurrent
Devices for DB-25, DB-50, and'DB-75 Westinghouse Breakers."'he
technician,
performing the maintenance
noticed that two of the breaker's secondary contacts
were slightly deformed, and exhibited some slight bowing.
Additionally, these two
contacts
had much less tension (more play) when manually pressed.
The technician
replaced the two contacts with new ones.
Breaker contact deformity had recently
occurred
in other Westinghouse
breakers
in the plant (see IRs 50-224/96-11
and
50-244/96-12), but the technician indicated to the inspectors that it had not been
a
problem prior to those instances.
Other maintenance
personriel present indicated
that they were working o'n a method to verify breaker contact operability by
comparing exi'sting contacts to a predetermined
standard.
C.
Conclusions
The inspectors concluded that the breaker maintenance
was performed effectively.
The maintenance
technician performing the work demonstrated
good technical
ability in identifying the beaker contact deformity and performed the work in
accordance
with the procedure requirements.
Given the recent failures in these
components,
the inspectors
also concluded that the licensee's efforts to augment
their inspection of Westinghouse
breaker contacts during routine breaker
maintenance
were appropriate.
M2.2
a 0
Control Rod Drive B-Motor Generator
B-MG Set Failure
1
'Ins ection Sco
e (62707)
'he inspectors observed
arid reviewed corrective maintenance
associated
with a
.failure of..the control rod drive B-MG set.
b.
Observations
and Findin s
At 1:45 a.m. on February 18, 1997, the control rod drive B-MG set,was secured
due to smoke from the generator of the B-MG setting off area fire alarms.
The fire
brigade responded,
the apparent fire was extinguished,
and'the equipment secured
in approximately 10 minutes.
The licensee initially attributed the problem to bearing
failure in the generator since intermittent abnormal noises had been reported by
plant personnel
during the preceding two weeks.
After the failure, the MG was
.
dismantled and sent to an offsite repair facility the following day.
The generator
bearings were replaced and the MG was returned to the site on February 21, 1997.
At the end of the report period, the licens'ee indicated that the MG should be
returned to service early the'next week.
The inspectors reviewed Maintenance
Procedure M-1015, "Three Month Lubrication
and Maintenance
Inspection of Rotating Equipment," which provided the following
guidance for generator bearing lubrication:
"Grease Generator while running, if possible...NOTE:
DO NOT overgrease,
use discretion."
Other equipment lubricated as part of M-015 included the MG set motor bearings,
the component cooling water (CCW) pump bearings, the service water (SW) pump
'motor bearings,
and the instrument air (IA) compressor motor bearings.
The
licensee indicated that they intended to do a thorough root cause analysis in
response
to this failure.
C.
Conclusions
The inspectors concluded that the licensee appropriately responded
to the fire
alarms and effectively secured the MG set, as evidenced
by the absence
of a plant
transient, and the short period of time between fire alarm initiation and the
equipment being secured.
The licensee also appeared to identify the component
failure in the MG set.
However, the inspectors were concerned that the generator
bearings may not have received adequate
lubrication, and that the maintenance
procedure to lubricate bearings
in rotating equipment may not provide sufficient
guidance to ensure that bearings are adequately lubricated.
This was of particular
concern because
M-1015 provided similar guidance for lubrication of engineered
safety features
(ESF) equipment.
M2.3
C-Safet
In'ection
C-Sl
Pum
Quarterl
Test
a.
Ins ection Sco
e (61726)
The inspectors observed
and reviewed PT-2.1-Q, "Safety Injectioh System Quarterly
Test," for the C-Sl pump.
b.
Observations
and Findin s
\\
This periodic test was performed on February 5, 1997 to demonstrate
operability of
the C-Sl pump.
The test included verifications of pump differential pressure
and
discharge pressure,
discharge check valve operability, Sl recirculation line
operability, and pump vibration limits. During performance of the PT while the
pump was running, the inspector identified that tubing to pressure indicator Pl-915
(Sl pump recirculation flow) was vibrating and the indication on the gauge was
oscillating significantly. The inspector informed licensee test personnel that the
.vibration appeared
excessive.
Design engineering
personnel subsequently
indicated
that they intended to analyze the problem for resolutioh.
11
Conclusions
The inspectors concluded that the surveillance was performed in accordance
with
procedure
requirements
and that technicians demonstrated
a good understanding
of
the functional requirements of the equipment being tested.
The Jicensee's
intention
to resolve excessive vibrations in recirculation line instrument tubing during pump
operations was appropriate.
M3
Maintenance Procedures
and Documentation
M3.1
B-Auxiliai
B-AFW Pum
Periodic Test
Ins ection Sco
e (62716)
The inspectors observed
and reviewed portions of PT-16Q-B, "AFW Pump B-
Quarterly."
b,
I
'I
PT-16Q-B, "AFW Pump,B - Quarterly" was performed on January 28, 1997, for the
inservice test requirements
under the ASME Code,Section XI. Pump performance
was satisfactorily tested.
However, the pump's recirculation valve, AOV-4310,
failed to fully open when the pump was throttled to 40 gpm output flow per local
indication as required. by the PT. Therefore, on January 31, 1997, the PT was re-
performed in part to calibrate AOV-4310., The inspectors questioned the licensee's
practice of performing instrument calibrations as part of a periodic pump test.
However, the licensee indicated that the AFW recirculation line was not required for
pump operability in accordance
with the Improved Technical Specifications (ITS).
The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and"
noted that the function of the pump's recirculation flow was inconsistent with
the'TS
operability requirements.
Section 10.5-8 of the UFSAR stated that "The motor-
driven and turbine-driven pumps each have an automatically controlled minimum
flow recirculation system sized and periodically tested.to ensure that minimum flow
will be provided under all accident and'normal operating conditions'to prevent pump
damage from overheating."
The ITS did not have this requirement.
The licensee
generated
an ACTION Report (97-0284) to address the inconsistency.
C.
Conclusions
The inspectors concluded that the surveillance was performed in accordance
with
plant procedures
and that the technicians demonstr'ated
a good understanding
of
the functional requirements
of the equipment being tested.
The licensee initiated
appropriate action in response to the identified discrepancy between the ITS and the
UF,SAR.
0
M3.2
12
Diesel Generator Startin
Air Com ressor Dischar
e Check Valve Closure Test
a 0
Ins ection Sco
e (61726)
b.
The inspectors observed
and reviewed the performance of PT-12.7, "Diesel
Generator Starting Air Compres'sor
Discharge Check Valve'Closure Test."
Observations
and Findin
s
PT-12.7 was performed on February 11, 1997, to verify the diesel air start receivers
would not excessively depressurize
if the air compressor
separated
from its
discharge
line during a seismic event.
A check valve is installed in the air line
between the receivers and the compressor to prevent receiver depressurization.
The PT's acceptance
criteria for check valve leakage was 5 psig/min, which was
based
on an assumed
normal receiver operating pressure of 250 psig to provide
.
5 minutes for operator action to manually start the EDG before the air pressure
reached the minimum 225 psig required for. operability.
During performance" of the
PT, actual compressor check'valve leakage for both diesel generators
w'as 0 psig
over a test period of 3 minutes.
The inspectors reviewed the design basis requirements
regarding the diesel
generator air start system, consulting the UFSAR, ITS, and the Standard
Review
Plan (SRP).
The 'UFSAR specified that the compressors
will automatically start at
230 psig and automatically stop at 250 psig to keep the receivers charged.
This
appeared to be inconsistent with the assumption of 250 psig normal operating
pressure
used by the li'censee in the acceptance
criteria basis for check valve
'leakage.
The licensee indicated that they intended to re-evaluate this acceptance
criteria since 250 psig is not.the normal operating pressure,
and 5 minutes would.
only represent the maximum time available for operator action before re'aching
225 psig.
Section 9..5.6.II.4.g of the SRP (General Design Criterion 17), specified that, "As a
minimum, the air starting system should be capable of cranking a cold diesel engine
five times without charging the receivers."
Section 9.5.6 of the UFSAR, "Diesel
Generator Starting System," stated that "Testing performed'during the 1992 MODE
6 (Refueling) outage demonstrated
that with an initial pressure of 225 psig the air
start system receiver tanks was sufficient to crank the diesels for a minimum of five
starts without recharging the receivers...."
Howev'er, Section 3.8.1 of the ITS
bases stated, "Since the DGs must start and begin loading within 10 seconds,
only
one air start must be available in the air receivers as assumed
in the accident
analysis."
The inspectors
also reviewed Training System Description (TSD) RGE-S, "Standby
Generation Diesel Generators,"
and noted'the following discrepancies:
~
The TSD incorrectly stated that, "The compressors
will automatically start
at 220 psig to charge the receivers."
The compressors
actually start at
230 psig.
13.
~
The TSD incorrectly indicated
a "...normal receiver pressure of 250."
Normal
receiver pressure
actually varies continuously between 230 psig'and 250
pslg.
~
The TSD incorrectly stated that, "A relief valve set at 265 psig provides
overpressure
protection."
This was inconsistent with the UFSAR
requirement and actual setpoint of 275 psig.
Although not controlled documents,
the TSDs are used as credible reference
documents for training, and are widely used by personnel throughout the plant, and
are regarded
as essentially accurate.
C.
Conclusions
~ the licensee stated that'the note
'3.3
A-Diesel Generator Periodic Test
The inspectors concluded that the surveillance was properly performed in
accordance
with plant procedures
and that the technicians demonstrated
a good
understanding
of the functional requirements of the equipment being tested.
Given
the discrepancy between the acceptance
criteria basis assumptions
and the ITS and
the UFSAR, the inspectors considered that the licensee's intention to re-evaluate
the acceptance
criteria for diesel generator, compressor check valve leakage was
appropriate.
The inspectors were concerned with the number of discrepancies
noted in the TSD, since these documents
are widely used at the station.
However,
d discrepancies
would be revised.
a.
Ins ection Sco
e (61726)
The inspectors observed
and reviewed the performance of PT-12.1, "Diesel
Generator A."
b.
Observations
and Findin s
PT-12.1, "Diesel Generator, A," was performed on February 19, 1997, to test the
A-Emergency Diesel Generator (A-EDG) for operability.
The test verified that the
'-EDG would start from the control room and that its associated
feeder breakers to
the plant's safeguard
buses would shut.
The inspector noted that step 6.4 of,the
test procedure directed the operators to start or verify that the service water (SW)
pump currently selected for automatic safeguards
start was running.
This was to
prevent an automatic pump start when the diesel-generator
supply breaker to Bus
~ 18 was closed.
The operators placed the safeguards
selector switch from the
'-'SW
pump to the C-SW pump, since the C-SW pump was currently running.
The
'T
was then continued and the diesel-ge'nerator
was tested satisfactorily.
However,
the PT gave no direction to the operators to return the safeguard
selector switch.to
its original line-up.
The desirable line-up for automatic actuation of SW pumps was to have the non-.
running pump selected.
This line-up was preferred due to the possibility that the
14
running pump could trip on overcurrent if an undervoltage
condition preceded
a loss
of offsite power.
This would prevent the pump from restarting on an engineered
safety feature (ESF) actuation.
After the PT concluded, operations
personnel
returned the SW ESF selector switches back to their original line-up without
procedural guidance.
The licensee indicated that they intended to revise procedures
PT-12.1
(A-EDG) and PT-12.2 (B-EDG) to direct the safeguard switches be placed in
their pre-test positions following EDG testing.
C.
Conclusions
The inspectors concluded that the surveillance was performed in accordance
with
plant procedures
and that the technicians demonstrated
a good understanding
of
the functional requirements of the equipment being tested,
The inspectors
considered the licensee's intention to revise the EDG PTs was appropriate to ensure
that the proper SW pump line-up would be'selected'after
testing was completed
M7
'Quality Assurance in Maintenance Activities
M7.1
Unsecured
QA Material Stora
e Areas
a 0
b.
Ins ection Sco
e (40500)
t
The inspector review'ed the licensee's follow-up response to two QA material
storage areas in the plant that were discovered unlocked.
I
Observations
and Findin s
On February 2, 1997 (Sunday), the inspector discovered
an unlocked access
door
to the plant's QA stockroom.
Upon entering'the area, no sign of a forced entry was
apparent
and no contents of the room appeared to be disturbed.
No person was
seen inside, nor did any stockroom personnel
appear to be on duty that day.
The
inspector notified an auxiliary operator and the shift supervisor, who dispatched
the control room foreman (CRF) to lock the door.
The CRF locked the door within
10 minutes, but also found a door ajar to an adjacent QA storage enclosure.
Operations
personnel
later performed
a walk-through in the. stockroom and agreed
that nothing had been disturbed.
The following day, stock room personnel
performed
a thorough walk-through of both aieas.
Most of the QA inventory is
stored in separately locked cabinets,
and none had been disturbed.
A stockroom
'mployee
apparently left the stockroom door unlocked.
The return spring o'n the
QA storage enclosure door was weak and not able to fully latch the door when it
closed on its own.
The doors became part of the stockroom when the floor plan was modified in
February 1996 to expand the total area.
This expansion
opened
an exterior wall to
allow for another window counter, and.created
additional office space.
The area
. that was newly incorporated
included the two doors that then became additional
.
ent/ances to the stockroom.
However, the latch on one of the new entrance doors
w'as not modified to make it like the other stockroom doors which could not be
15
permanently unlocked with a key.
The following day, the lock on the stockroom
door was upgraded to the desirable type, and.the spring on the storage enclosure
door was replaced.
'I
The licensee initiated an'ACTION Report to evaluate their process for modifying the
boundaries
of designated
controlled QA storage areas,
and to determine what QA
management
reviews are appropriate for such modifications.
Although the
stockroom is temperature
and humidity controlled, it is officiallycontrolled as a level
"B" storage area (i.e., temperature
only) ~ 'It was not apparent'that this was
adequately
considered
during the modification process to ensure that the proper
level of storage was maintained.
The licensee's evaluation was in progress at the
end of the inspection period.
C.
Conclusions
The licensee responded
expeditiously to secure the unlocked QA storage areas.
The inspector considered this condition to be an inadvertent oversight, and follow-
up actions to evaluate the licensee's
processes
for modifying QA area boundaries
were appropriate.
III. En ineerin
E2
Engineering Support of Facilities and Equipment
E2.1
a 0
b.
RCS Total Gas Activit Increase
Ins ection Sco
e (37551)
'I
The inspectors reviewed the licensee's
response to an increase
system
(RCS) total gas and Iodine-1,31
(1-131) gas activities.
Observations
and Findin s
4
On January'13,
1997, the licensee observed
a notable increase
in RCS total gas
activity from an average of 0.19 micro curies per gram (pCI/gm) to 0.424 pCI/gm.
Iodine-131 activity increased from 4.15 E-3 pCI/gm to 5.05 E-3 pCI/gm.
The
licensee initiated an ACTION Report (97-0042) in response to these increases.
Based on a computer analysis, the licensee determined that the inciease was most
likely caused
by a defect in one fuel pin: The ITS limits for activity were 1.0 yCi/gm
for l-131, as well as 100/EyCI/gm (=58 yCI/gm) for RCS gross specific activity
(corresponds
to 1% failed fuel). The licensee indicated that they intend to monitor
activity levels closely for changes
or trends.
C.
Conclusions
The inspectors concluded. that the licensee adequately
responded to the noted
increase
in RCS activity levels and that the increases
were still well below ITS
limits. Continuous monitoring of these levels for trends was appropriate.
EZZ
Feedwater Flow Oscillations
16
Ins ection Sco
e (37551)
The inspectors reviewed the licensee's
response to excessive flow oscillations in
the main feedwater system.
Observations
and Findin s
Main feedwater flow oscillations had been occurring in the A-train of the feedwater
system since the reactor start up on November 12, 1996.
The A-train oscillations
occurred at irregular intervals an'd varied from between 200-300 Klbm/hr (normal
flow oscillations were between 60-80 Klbm/hr). The oscillations could be curtailed
by taking manual control of the feedwater regulating valve (FRV) and placing the
'RV
bypass valve in automatic.
The licensee indicated that the FRV bypass, valve
actuators were faster acting to feedwater system inputs, which allowed them to
respond more efficiently to system demands.
However, the licensee also indicated
that the FRV bypass valves did'not have redundant controller inputs in case of an
input failure, but that the FRVs did. Therefore, it was more desirable to analyze the
FRV actuators for possible adjustment. and.resolution.
The licensee's resolution was to reduce the gain on the A-FRV actuator by 6.5%.
~ This value was selected to reduce the sensitivity of the system to prevent the
swings from occurring, but to not reduce sensitivity to the point where the FRVs
would respond too slowly to a plant transient.
The adjustment was made on
January 25, 1997, and immediately reduced oscillations to 60-80 Klbm/hr.
No
excessive flow oscillations were noted throughout the rest of the report period.
The
licensee indicated that they intend 'to perform the same adjustment to the B-FRV in
the near future.
C.
Conclusions
. The inspectors concluded that the licensee's
actions to eliminate unnecessary
feedwater flow transients were effective in that no excessive
oscillations in the.
A-train feed flow had occurred since January 25, 1997.
The inspectors
also
concluded that the licensee's intention to incorporate the same change to the
B-train channel was appropriate
and would make both channels consistent with
each other.
E2.3
Tem erature Monitorin
of Lake Ontario Inlet Water
a 0
Iris ection Sco
e (37551)
The inspectors reviewed the licensee's
actions to evaluate discrepancies
between
the various lake inlet water temperature detectors,
and to ensure Compliance with
the ITS requirements for minimum screenhouse
inlet plenum temperature.
17
Observations
and Findin s
'he
licensee performed cold weather walkdowns on a weekly basis during the.
winter months to ensure that plant systems
are not subjected to freezing
.temperatures
and that the lake inlet water is free from ice that. could block flow'to
the circulating water (CW) and service water (SW) systems.
Administrative
procedure A-54.4.1, "Cold Weather Walkdown Procedure,"
directed plant operators
.,
to maintain a heightened
awareness
for the possible presence
of "frazil" ice in the
.
intake structure, arid to energize the intake heater voltage when lake temperature
is
less than 33
F.
ITS Basis 3.7.8 required that the screenhouse
bay temperature
be
maintained above 35'F in order to satisfy an accident analysis assumption that the
service water inlet temperature to the containment recirculation fan coolers (CRFCs)
be above the minimum temperature
used in the analysis.
Operators adjusted the
service water inlet temperature with warm recirculation flow from the circulating
water discharge that is mixed with the lake inlet water in the screenhouse
inlet
plenum.
Adjustments to the recirculation flow were made periodically to maintain a
desired service water inlet temperature
above 38
F.
During the week of January
13 -'17, 1997, the inspector noted that the plant
computer's daily recorded lake inlet temperatures
indicated betw'een 30 - 3,1
F;
however, no visual indication of ice was present on the lake or in'the'screenhouse
bay.
In addition, it was noted that the three installed instruments used for lake
temperature
monitoring did not display consistent indications, and varied over a 3-
4
F range.
The inspector questioned
the licensee about which instrument was the
most accurate, which was used for moriitoring potential icing conditions in the inlet
water, and which instrument is used to ensure that the screenhouse
bay
temperature
is maintained above 35
F.
Operators indicated that they used the one detector that inputs to the plant
computer for lake temperature
as an indication for when to regulate recirculation
flow, and they used the temperature detectors on the inlet to the condenser
waterboxes to keep the screenhouse
bay temperature
above 38'F.
A condenser
inlet temperature
above 38
F had been assumed to provide a sufficient margin to
ensure that service water inlet temperature
remained above 35'F.
The licensee
investigated the variation in temperature
indications from the three different
detectors
and determined that they had an accuracy of +2% of full calibration
range.
For the three detectors,'this tolerance could allow indications to vary from
30 to 34
F.
Based on these determinations,
it appeared that two of the
temperature detectors were reading lower than actual lake temperature.
However,
the licensee recalibrated all'three instruments to make them more consistent.
All
three of the temperature
detectors. are mounted on the north wall of the
screenhouse
close to the lake inlet flow stream before it mixes with the warm
recirculation flow. Consequently,
these detectors
read closer to the actual lake
temperature.
There is currently no temperature detector in the screenhouse
that
measures
the lake inlet mixed with the recirculation water that enters the CW and
SW inlet bays.
18
In order to obtain a more accurate indication of SW pump inlet temperature,
the SW
system engineer and operations personnel
began taking manual temperature
readings
in the SW bay using a high accuracy hand-held instrument.
On January
31, 1997, the licensee determined that some of the SW inlet water was below
35
F.
It appeared that a'"streaming" effect caused colder water in the middle of
the inlet bays to stream toward the SW pump suction.
Operators immediately
opened the recirculation gatq to increase the inlet pl'enum temperature,
and SW inlet
water was restored to above 35. F within one-half hour.
Operators later responded
to a similar occurrence
on February 11, 1997, and restored SW inlet temperature to
above 35
F within approximately 20 minutes.
Subsequent
evaluation by the licensee indicated that ITS surveillance requirement 3.7.8.1 had not been satisfied when the SW inlet temperature
dropped below 35
F,
and that represented
a condition requiring entry into ITS limiting condition for
operation
(LCO) 3.0.3.
Although a formal entry into LCO 3.0.3'was required on
both occasions,
the licensee's corrective actions were accomplished
in much less
time than the time limits permitted (6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />) for these conditions.
However, the
licensee determined that this situation was reportable to the NRC under the
requirements of,10 CFR 50,73, and initiated a Licensee Event Report (LER). At the
end of the inspection,'the
licensee anticipated the LER would be submitted in early
March 1997.
In an effort to evaluate the consequences
of th'e lower SW'temperature
on accident
conditions, the licensee's.engineering
and licensing departments
consulted with
who subsequently
recalculated the peak containment pressure
and
temperature
assuming 30
F service water inlet to the CRFCs.
The results indicated
that the lower SW temperature
Would have a minimal impact.
Since the SW piping
design analysis and s>stem design minimum terriperature is 32
F, RGRE changed
the ITS basis to a minimum temperature
of 32'F.
The inspector reviewed the
licensee's safety evaluation (SEV-1090) that supported the ITS basis change
and
found it adequate
based
on the results of the recalculated accident analysis.
A
Safety evaluation was done to support
a change to the ITS Basis to permit the
operation of SW inlet water to drop to 32
F. Also, operations procedure 0-6.13,
"Daily Surveillance Logs," was changed to direct operators to take manual readings
of the screenhouse
bay to ensure that temperatures
are maintained at )32
F.
4
The inspector'also
noted that the ITS basis for SW pump operability stated that the
pumps are operable with only 5 feet indicated water level in the screenhouse.
However, the bottom of the pump suction is exactly at the indicated 5 foot level ~
When the inspector questioned this, the licensee agreed to evaluate the
appropriateness
of this operability requirement.
The, licensee also indicated that
they intend to evaluate the possibility that inaccuracies
allowed in the screenhouse
temperature
monitors could also represent
a potential problem for lake inlet
temperature
monitoring during the summer months'when the maximum lake inlet
temperature
is limited to,80
F by the current design basis analysis.
0
C.
Conclusions
The licensee took appropriate actions to correct the low temperature
conditions in
the screenhouse
bay, and to evaluate the consequences
for design basis conditions.
The reanalysis for lower inlet temperatures
effectively demonstrated
that the
consequences
of 32
F service water would have minimal impact under accident
conditions.
A reevaluation of the operability criteria for screenhouse
minimum
water level and temperature
monitor inaccuracies
at the minimum and maximum
lake water inlet temperatures
was appropriate.
Miscellaneous Engineering Issues
E8.1
Closed
LER 96-015: Based on Review of NRC Generic Letter. 96-06
a Thermall
Induced Over ressure Transient Could Occur
'
LER 96-015 was submitted on January 22, 1997, in response to the licensee's
~ discovery that the possibility existed for a thermally induced overpressurization
that
could fail the charcoal filter dousing lines between the check valves in the cross-
connect piping for the A-.and B-containment spray (A- and B-CS) system headers.
This failure could occur from a heatup of the water-filled line inside containment
following a design basis loss-of-coolant accident:
Such an overpressurization
could
render both trains of CS incapable of performing their safety function because
of
the excessive flow diversion from the CS system through the break.
The dousing
function was not credited in the Ginna Accident Analysis, and the licensee isolated
and vented the line on December 21, 1996.
On December 23, 1996, the licensee
completed calculations confirming that a thermally induced overpressurization
in the
dousing line was possible,
and reported the condition to the NRC under 10 CFR 50.72. (b)(2)(iii)(D) as a condition that could prevent a safety function from
~ mitigating the consequences
of an accident.
On January 3, 1997; the licensee installed a thermal relief valve in the containment
spray charcoal filter dousing lines to prevent a thermal over-pressurization
of the
dousing lines; The relief valve was set for a maximum relief cap'acity of 10 gpm at
500 psig to prevent pressure fram exceeding the rated maximum piping design
pressure.
Aftei the relief valve 'was installed, the dousing line was unisolated.
The
irispectors considered that the LER adequately
described this potential event, and
~ appropriately addressed
the root causes
and corrective actions.
This LER is closed.
IV: Plant Su
ort
R3
Radiological Protection and Chemistry (RP8cC) Procedures
and Documentation
R3.1
Whole Bod
Countin
for Terminated
Em lo ees
Ins ection Sco
e
(83750)
The inspector reviewed the licensee's implementation of site procedures
regarding
conducting whole body conducting for terminated employees.
20
b.
Observation
and Findin s
The inspector reviewed licensee activities related to conducting whole body counts
(WBC) for individuals terminating their activities at Ginna.
Interviews were
conducted with the Manager, Chemistry 5 Radiological Controls and the Manager,
Dosimetry, applicable procedures
were reviewed, and dosimetry records of recently
terminated individuals were examined.
Licensee procedure
"Dosimetry Program
Administrative Procedure",
RPA-DOS, defines the requirements for internal and
external dose processing
and recording.
Paragraph
5.3.7, "Whole Body Counting
Frequency" states in part,.
~ ~"TLD badged individuals shall receive a whole body
count under the following conditions:
~ Upon termination of work activities at Ginna."
Through review of dosimetry records for individuals terminated in 1996, the
inspector determined that WBC.were not conducted
in compliance with the
procedural requirement.
Specifically, at least three individuals terminated their work
activities in 1996 at Ginna but did not have a whole body count as required by the
procedure..
However, evidence exists, in the form of'radiation w'ork permit. entries,
airborne survey data, and dates when the individuals had their an'nual whole body
count, that these individuals did not obtain an uptake of radioactive material that
.would require WBC.
The RGRE RP5C staff acknowledged
th'e'procedure
shortcoming and is presently
evaluating procedure changes to better justify when an exit WBC is needed;
in lieu
of terminating work activities at Ginna.
C.
Conclusion
This issue had minor safety significance and represented
a failure of the licensee to
meet an administrative requirement.
The licensee had initiated adequate
corrective
actions.
Accordingly, this failure constituted
a violation of minor significance and is
~
being treated as a non-cited violation, consistent'with Section IV of the enforcement
policy.
R7
R7.1
Quality Assurance in Radiological Protection and Chemistry Activities
Poor Radiolo ical Work Practices and lnade
uate Contamination Area Boundar
Controls
a 0
Ins ection Sco
e (40500)
The inspector reviewed the licensee's corrective actions associated
with ongoing
incidents where poor radiological work practices and inadequate
contamination
area
boundary controls led to the uncontrolled release of potentially and actually
contaminated
material to an uncontaminated
area..
C
21
b.
Observations
and Findin s
In December 1994, the'RC identified inconsistent. contamination
area boundary
labels, and a'loss of some contamination
area boundary controls in the auxiliary
building.
Equipment crossing contamination boundaries
was not secured
in place,
and the demarkation between contaminated
and uncontaminated
portions could'not
be identified.
These conditions were discussed
with the licensee who.indicated that
.,
the conditions would be evaluated for the appropriate corrective actions (see IR
50-244/94-29). -The NRC identified a similar situation in October 1996, where two
'instances of poor radiological work practices and inadequate
contamination
boundary controls existed inside designated
contamination
areas were not adequate
to prevent a potential spread of contamination to uncontaminated
areas
(see
IR'0-244/96-11).
Specifically, significant amounts of debris, tools, and equipment
used for maintenance
work were allowed to cross over the contamination
demarcation
boundaries
around the refueling water stor'age'tank
and around an
MOV-857A work area, without having been surveyed by radiological protection (RP)
technicians for potential contamination.
After all materials. were surveyed, it was
determined that no actual spread of contamination. resulted from these incidents.
In
September
1996, the licensee identified 12 items in the maintenance
shops
contaminated
from. 1500 to 65,000 dpm/100cm'hat
had been removed from a
radiologically controlled area without a proper contamination survey, and without
placing the"items into a controlled contamination storage area.
This was reported
on RGSE ACTION Report No. 96-0902.
All of the above iristances did not meet RGSE's
RP program requirements
or
management
expectations for radiological work or the expected contamination
area
boundary controls designed to prevent the spread of contamination.
All material
inside a designated
contamination
area at the Ginna Station is consi'dered
contaminated
until cleared by an RP technician.
In October 1996, the licensee
initiated specific corrective actions, and also identified other contaminated work
areas where radiological work practices were not meeting
RP program and
management
expectations.
The inspectors followed up on these actions to evaluate
'heir'effectiveness,
and idehtified several actions taken that were designed.to
correct these conditions.
Corrective actions included:
1) upgrading contamination
boundary labels throughout the plant, 2) Increasing the level of RP staff monitoring
of radiological work activities, and 3) conducting additional training for qualified
radiological workers and RP technicians.
However, the licensee considered that no
programmatic changes
or improvements were necessary to correct, the inadequate
work practices and barrier controls.
On February 9, 1997, the inspector observed maintenance
repairs on, the A-'Sl pump
inside desi'gnated
contamination
areas around and on the pump and its pedestal.
The contamination boundaries
were small and the workers were required to reach
into the area from outside.
During the course of the work, the inspector observed
approximately 10 rags and
a wire brush straddling the contamination boundary on
the pedestal of the pump, an. area that had been previously surveyed and
determined to have loose smearable
surface contamination above the licensee's
'imit
of 500 dpm/100cm'.
Several other tools that had been used inside the
'
22
contamination boundary around the pump bearing were laying on the floor on an
uncontaminated
surface.
The general work area was not roped off around the
pump, and tools and equipment used inside the area were not surveyed prior to
being removed:
The inspector reported the condition to the RP technician covering
the job. The technician evaluated the situation and then surveyed the tools and the
pump pedestal.
The pump pedestal
area in contact with the rags and wire brush
contained'smearable
loose surface contamination of approximately 1600
dpm/100cm'.
The inspector considered that these conditions represented
a
fundamental. disregard for boundary 'controls and the basic purposes for observing
contamination boundaries.
However, none of the tools or floor areas outside the
boundary marker were contaminated.
A larger temporary area could have controlled
the entire floor around the pumps as contamination
areas,
and the tools could have
been bagged
and surveyed at the control point.
The inspector later jnterviewed one of the mechanics involved with this job. The
mechanic could not remember the levels of contamination detected
by the HP
technician before the job started.
Other qualified radiological workers in the plant
were also interviewed.
It was apparent to the in'spector that there was wide spread
confusion and disagreement
among radiological workers regardin'g contamination
boundaries
and whether or not reaching across
a contamination boundary to work
inside an area was an acceptable practice.
Confusion also'xisted over the meaning
of radiological contamination boundary markers, i.e., ropes, tape, and signs.
One
qualified radiation worker did'not know that yellow and magenta tape represented
a
contamination boundary at Ginna.. The inspector noted several examples in the
plant where the application of boundary markers was contradictory and confusing to
plant workers.
For example:
1) contamination area tape on the floor of the
contaminated
storage'building
(CSB) threshold of all outside doors, but the CSB
floors were clean and the boundary postings specifically designated
it as a restricted
~ area/radiation
area only; -2) on the auxiliary building intermediate level near the
entrance to the CVCS resin ion exchanger
room, barrier tape was on the floor
around piping penetrations,
but a nearby. contamination barrier sign stated that'the
contamination was on the overhead
horizontal piping which extended
beyond the
vertical plane described by the tape on the floor; 3) barrier tape was not on the
floor around all edges of the spent fuel pool, but the hand railing was posted
as a
contaminated
area; 4) the penetration fan coolers in the auxiliary building were,
surrounded
by a barrier rope and floor tape, and some workers did not know if the
"contamination barrier vertical, plane" extended to the ceiling of the auxiliary
building (any a~ca more than 8 feet above
a floor, requires contact with an RP
technician prior to entry); and 5)'the area around the sink inside the radiation
chemistry laboratory was a designated'contamination
area, but several pieces of lab
equipment,
a set of tongs, an absorbent
diaper, etc, were straddling the barrier
marker.
An RP technician considered
this to be an acceptable
situation; however,
an RP supervisor did not.
The inspector reviewed al( the ACTION Reports written in 1996 that concerned..
contamination deficiencies.
Four Reports involved contaminated. material found
outside
a radiologically controlled area; six Reports involved deficient boundary
controls; two involved a spread of contamination;
and four involved miscellaneous
2'3
incidents including personal contaminations
or failure to adhere to radiological work
permit requirements.
The inspector discussed
the level of training given to qualified radiological workers
at the Ginna Station with a training department instructor who stated that if a
worker was previously a "fullyqualified radiological worker'" at another nuclear
facility, and then employed at Ginna, no requalification training is given by RGB.E.
The individual must, however, perform satisfactorily in the normal General Employee
Training (GET) given annually to qualified radiological workers.
This was also the
current process for qualified RP technicians.
RP technicians who were previously
~
certified at another facility were granted
a certification upon entering employment at
Ginna.
There was currently no periodic recertification of RP technicians at Ginna,
but these individuals also needed to pass the annual GET training.
This situation
may be related do the notable variation in radiological work practices and control
standards
among the Ginna work force.
On February 17, 1997, the inspector observed
contaminated
water dripping'rom a
fitting on the differential pres'surd transmitter at flow indicator Fl-116 (seal injection
return. flow from the B-reactor coolant pump).
A small leak had previously
developed
on December 2, 1996, and.was causing
an accumulation of boron
crystals around the fitting, but it was not large enough to form drops that would fall
to the floor. On February 17, approximately 3 drops per minute were dripping onto
an absorbent towel (i.e., a "launderable decon rag") that was placed on the
uncontaminated
floor beneath.FI-116.
It appeared that the towel was placed on the
floor to collect the drippage since it was folded into a small 6" X 6" area and placed
directly below the leaking fitting. At the time of discovery, the towel was saturated
'with water and a small stream was flowing onto uncontaminated
floor
surfaces'way
to a lowpoint where it.collected into a small puddle.
Boric acid crystals
.
approximately, 1/8 - 1/4 inch in size had formed qn the surrounding floor due to
evaporation of the fluid. The inspector contacted the RP technician on duty, who
immediately placed
a bucket under the dripping fitting and then cleaned up the
water and boron crystals.
A subsequent
survey indicated that the floor area directly
below Fl-116 was contaminated
from 700 to 2700 dpm/100cm'.
A later survey of
50 ml of the leaking water. indicated an activity level of 2.75E-3 uCi/gm.
Both the
.
RP.technician
and the RP supervisor agreed that the absorbent tbwel was not an
appropriate method to contain the dripping water and that a catch or bucket should
have been used.
It appeared that the licensee did not currently have RP program
controls that required the use of catches or buckets under potential leaks of
contaminated
water that would prevent the spread of, contamination.
Conclusions
The licensee's
actions to maintain proper contamination boundary controls, and to
monitor to assure radiological 'work practices adequately prevent the spread of
contamination have not been adequate.
Actions to identify and correct poor
radiological work practices,
and to prevent the spread of potential and..actual
contamination,
also have not been effective.
These conditions represent
a violation
of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Actions,"
(NOV 50-244/97-01-02).
V. Mana ement IVleetin s
X1
Exit Meeting Summary
The inspectors presented
the inspection results to members of licensee management
on February 25, 1997, after the <nspection was concluded.
The licensee
acknowledged
the findings presented.
The inspectors
asked the licensee whether any materials examined during the
inspection should be con'sidered
proprietary.
No proprietary information was
'dentified.
L2
Review of UFSAR Commitments
A recent discovery of a licensee operating their facility in a manner contrary to the
Updated Final Safety Analysis Report (UFSAR) description highlighted the need for a
special focused revjew that compares plant practices, procedures
and/or parameters
to the UFSAR description.
While performing the inspections discussed. in this
report, the inspector reviewed the applicable portions of the UFSAR that related to
the areas inspected.
Except in the instances
noted below, the inspector verified
that the UFSAR wording was consistent with the observed plant practices,
procedure and/or parameters.
UFSAR Section 10.5-8; AFW pump recirculation line availability was not
consistent with ITS definition of pump operability (see section M3.1).
The EDG aii start system check valve test acceptance
criteria basis was not
consistent with UFSAR Section 3.8.1 (see section M3.2).
~
e ~
ATTACHMENT 1
PARTIAL LIST OF PERSONS CONTACTED
B. Flynn
C. Forkell
G. Graus
A. Harhay
J. Hotchkiss
G. Joss
R. Marchionda
R. Mecredy
R. Ploof
R. Smith
J. Smith
J. Widay
T. White
G; Wrobel
Primary Systems
Engineering
Manager
Electrical Systems
Engineering Manager
IRC/Electrical Maintenance
Manager
Chemistry 5 Radiological Protection Manager
Mechanical Maintenance
Manager
Results and Test, Supervisor
Production Superintendent
Vice President,
Nuclear Operations
Secdndary
Systems
Engineering
Manager
.
Senior Vice President,
Customer Operations
Maintenance
Superintendent
Plant Manager
Operations
Manager
Nuclear Safety 5 Licensing
Manager.'NSPECTION
PROCEBURES USED
IP 37001:
IP 37551:
IP 40500:
IP 61726:
IP 62707:
IP 71707:
IP 71750:
IP 83750:
IP 92700:
10 CFR 50.59 Safety Evaluation Program
Onsite En'gineering
Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing
Problems
e
Surveillance Observation
Maintenance
Observation
Plant Operations
Plant Support
Occupational
Radiation Exposure
Onsite Follow-up of Written Reports of Nonroutine Events at Power Reactor
~ Facilities
ITEMS OPENED, CLOSED, AND DISCUSSED
~Oened
1) The practice of extending
a normal shift to meet programmatic requirements for
operator proficiency under 10 CFR 55.53 (URI 50-244/97-01-01).
2)
Inadequate
corrective actions for poor radiological work practices and inadequate
contamination
area 'boundary controls (NOV 50-244/97-01-02).
Closed
1)
Circuit Breakers Closed While in Mode 3, Due to Personnel
Error, Resulted in a
Condition Prohibited by Technical Specifications
(LER 96-013).
2)
Based on Review of NRC Generic Letter 96-06, a Thermally Induced Overpressure
Transient Could Occur (LER 96-015).
e
, ALARA
CFR
d/p
dpm
HPES
IFI
IR
LCO
LER
NRC
NSARB
ppm
pslg
.
. RGSE
RP5C
SEV
Sl
'RV
TSD
LIST OF ACRONYMS USED
As Low As Reasonably
Achievable
American Society of Mechanical Engineers
Component Cooling Water
Circulating Water
Code of Federal Regulations
differential pressure
disintegrations
per minute
Emergency Core Cooling Sy's tem
Emergency
Diesel Generator
Human Performance
Enhancerr}ent System
Inspection Follow-up Item
Individual Plant Evaluation
Inspection Report
Inservice Inspection
Inservice Test
Improved Technical Specifications
'imiting Condition for Operation
Licensee Event Report
Loss-of-Coolant Accident
Motor-Generator
Main Steam.Isolation Valve
Non-Cited Violation
Nuclear Regulatory Commission
Nuclear Reactor Regulation
Nuclear Safety Audit and Review Board
Peak Cladding Temperature
Plant Operations Review Committee
parts per million
Probabilistic Safety Assessment
~
Periodic Test
pounds per square inch gage
Pressurized
Water Reactor
Quality Assurance
Quality Control
Radiological Controlled Area
Rochester
Gas and Electric Corporation
Radiation Protection
Radiological Protection and Chemistry
Radiation Work Permit
Safety Evaluation
Safety Injection
Training System Description
Updated Final S'afety Analys'is Report
Violation