Similar Documents at Ginna |
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LER-1980-005, /01T-0:on 800603,during Performance of Monthly Verification Procedure,Loop a Accumulator Injection Circuit Breaker Found in on Position.Cause Not Stated.Breaker Returned to Off Position |
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| 2441980005R01 - NRC Website |
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NRC FQRM 366
{7~77)
.'07 7
8 CON'T
~01
~LQB 0
5 0
0 0
2 4
4 Qj 0
6 0
3 8
0 QB 0
6 1
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0 Qg 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES 10 During performance of monthly verification rocedure S-30.1, A loo accumulator 7
8 iniection MOV-855 circuit breaker was found in ON position.
(T.S. 3.3.l.l.g) 4 The accumulator was available to erform its intended function as MOV was in safe-U. S. NUCLEAR REGULATORY COMMISSION 0
ICENSEE EVENT REPORT CONTROL BLOCK:
Q1 (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION)
I 6
NYREG I,.Q300-00000-00Q341111Q~QR 9
LICENSEE CODE 14 15 LICENSE NUMBER 26 LICENSE TYPE 30 57 CAT 58
~Q6 guards position, open.
Redundant accumulator was also available with proper ower arrangement.
~08 7
8 9
80
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8 o
SYSTEII'I
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE Q1 Q>>
~ZQ>>
O K
T B
R K
Q4
~Q70
~ZQ70 9
10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERiRQ EVENT YEAR REPORT NO.
CODE TYPE NO.
Q>>
017007
~80
+
~00 5
QW
~01
+T
QO 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP.
CahIPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.
SUPPLIER hIANUFACTURER
~QQ70 ~ZQ70
~ZQ30
~ZQ>>
0 0
0 0
~Y Q33
~NQ34
~NQ30 W
1 2
1 Qto 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 Breaker was immediately returned to OFF.
All breakers in S-30 series were reverified as in correct position.
Review of records showed docuinentation of proper position at 3 different times on 5/21/80, date of heatup.
Frequency of breaker position checks 7
8 9
FACILITY
~3P METHO STATUS
% POWER OTHER STATUS ~
DISCO 5
~E Qos ~10 0
Qto NA
~B 7
8 9
10 12 13 44 45 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ3 liE Mz Q33 z
Q34 NA 7
8 9
10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Ag 7 ~00 0
Q17 Z
Qos 7
8 9
11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41 0 ~00 0
Q4o NA 7
8 9
11 12 LOSS OF OR DAMAGETO FAGILITYQ TYPE
DESCRIPTION
z Q42 NA ISSUED DESCRIPTION Q46 8 006 1 9 0 g
y
~NQ NA 8
9 10 D OF VERY Q31 Performing 46 80 DISCOVERY DESCRIPTION
@32 verification procedure 80 LOCATIONOF RELEASE Q36 NA 80 45 80 80 80 NRC USE ONLY 40 1
80 4s 0ft 68 69 PHDNE.
3 15/524-4446 Carl H. Peck NAME OF PREPARER 4
has been increased per change to procedure 0-9.1 Shift Relief Turnover-Aux.Operator.
4 1
I 1,
Attachment to LER 80-005/01T-0 Rochester Gas and Electric Corporation R. E. Ginna Nuclear Power Plant, Unit No.
1 Docket No. 50-244 During monthly performance of procedure S-30.1 Safety Injection Valve Position Verification on June 3, 1980 at 0645 hours0.00747 days <br />0.179 hours <br />0.00107 weeks <br />2.454225e-4 months <br /> it was discovered that the circuit breaker for the A Loop Accumulator injection MOV-865 was in the ON position.
This is contrary to Technical Specification section 3.3.1.1.g which calls for removal of A.C. power for certain valves in the open position.
The valve position was verified as proper and the breaker was immediately returned to the required position.
Allbreakers listed in
'he S-30 series of verification procedures were reverified as in the correct position.
A review of the records shows that the breaker was placed in the correct position on May 21, 1980 per procedure 0-1.1, Plant Heatup from Cold Shutdown to Hot Shutdown.
This correct position was confirmed later the same day by Procedure 0-1.1C, Precritical Technical Specification Check Sheet.
The correct position was then verified later the same day by Procedure S-30.1, Safety Injection System Valve Position Verification.
The frequency of circuit breaker checks 'has been increased by amending procedure 0-9.1 Shift Relief Turnover-Auxiliary Operator to include checks by each shift.
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| 05000244/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000244/LER-1980-001-03, /03L-0:on 800118,while Performing PT-12.1, Emergency Generator 1A Would Not Accept Nameplate Steady Load Rating.Caused by Adjusting Governor Setting to Incorrect Value Indicated on Dynotape Sticker Setting Mod | /03L-0:on 800118,while Performing PT-12.1, Emergency Generator 1A Would Not Accept Nameplate Steady Load Rating.Caused by Adjusting Governor Setting to Incorrect Value Indicated on Dynotape Sticker Setting Mod | | | 05000244/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000244/LER-1980-002-03, /03L-0:on 800331,during Review of Special Instructions,Discovered That Time from Previous Boron Concentration Sample Exceeded 75 Days.Caused by Inadequate Guidance for Bimonthly Sampling Schedule.Schedule Changed | /03L-0:on 800331,during Review of Special Instructions,Discovered That Time from Previous Boron Concentration Sample Exceeded 75 Days.Caused by Inadequate Guidance for Bimonthly Sampling Schedule.Schedule Changed | | | 05000244/LER-1980-003-01, /01T-0:on 800414,during Steam Generator Inservice Insp,One Tube in a Steam Generator & 34 Tubes in B Generator Showed Pluggable Indications.Probably Caused by Concentration of Caustics in Crevices | /01T-0:on 800414,during Steam Generator Inservice Insp,One Tube in a Steam Generator & 34 Tubes in B Generator Showed Pluggable Indications.Probably Caused by Concentration of Caustics in Crevices | | | 05000244/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000244/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000244/LER-1980-004-01, /01T-0:on 800506,during post-installation Test of Reactor Vessel Head Vent,Dc Power Switches for Both Trains of Low Temp Overpressurization Protection Found in Off Position W/No RCS Vent Open.Cause Unknown | /01T-0:on 800506,during post-installation Test of Reactor Vessel Head Vent,Dc Power Switches for Both Trains of Low Temp Overpressurization Protection Found in Off Position W/No RCS Vent Open.Cause Unknown | | | 05000244/LER-1980-005-01, /01T-0:on 800603,during Performance of Monthly Verification Procedure,Loop a Accumulator Injection Circuit Breaker Found in on Position.Cause Not Stated.Breaker Returned to Off Position | /01T-0:on 800603,during Performance of Monthly Verification Procedure,Loop a Accumulator Injection Circuit Breaker Found in on Position.Cause Not Stated.Breaker Returned to Off Position | | | 05000244/LER-1980-005, Forwards LER 80-005/01T-0 | Forwards LER 80-005/01T-0 | | | 05000244/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000244/LER-1980-006-01, /01T-0:on 800711,during Routine Analysis of Boric Acid Tank Samples,Concentration Exceeded Tech Spec Limit on Three Occasions.Caused by Entry of Ascarite Into Tank. Reagent Check Now Performed W/Sampling | /01T-0:on 800711,during Routine Analysis of Boric Acid Tank Samples,Concentration Exceeded Tech Spec Limit on Three Occasions.Caused by Entry of Ascarite Into Tank. Reagent Check Now Performed W/Sampling | | | 05000244/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000244/LER-1980-007-03, /03L-0:on 800829,controller TC-402R for Channel II Did Not Respond to Change in Input.Caused by Faulty Main Amplifier Bridge Assembly & Low Limit Transmitter.Controller Replaced & Calibr | /03L-0:on 800829,controller TC-402R for Channel II Did Not Respond to Change in Input.Caused by Faulty Main Amplifier Bridge Assembly & Low Limit Transmitter.Controller Replaced & Calibr | | | 05000244/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000244/LER-1980-008-03, /03L-0:on 800910,during PT-12.2 Test for B Emergency Generator,Bus 16 Breaker Did Not Close.Caused by Guide Pin Split End Opening & Binding Control Relay Antipump Release Lever.Split End Closed | /03L-0:on 800910,during PT-12.2 Test for B Emergency Generator,Bus 16 Breaker Did Not Close.Caused by Guide Pin Split End Opening & Binding Control Relay Antipump Release Lever.Split End Closed | | | 05000244/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000244/LER-1980-009-03, /03L-0:on 801003,during Performance of PT-12.1 to Verify Operability of 1A Emergency Generator,Part from Barring Device Seen to Fly Out.Caused by Bearings Not Designed to Withstand Operation W/Generator Running | /03L-0:on 801003,during Performance of PT-12.1 to Verify Operability of 1A Emergency Generator,Part from Barring Device Seen to Fly Out.Caused by Bearings Not Designed to Withstand Operation W/Generator Running | | | 05000244/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000244/LER-1980-010-03, /03L-0:on 801125,pinhole Leak Found in Weld on RHR Thermowell.Caused by Poor Quality Weld.Weld Repaired | /03L-0:on 801125,pinhole Leak Found in Weld on RHR Thermowell.Caused by Poor Quality Weld.Weld Repaired | | | 05000244/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000244/LER-1980-011-03, /03L-0:on 801211,bus 17 Breaker from 1B Emergency Generator Failed to Close.Cause Not Stated.Testing Interval Shortened to Verify Operability 810106 | /03L-0:on 801211,bus 17 Breaker from 1B Emergency Generator Failed to Close.Cause Not Stated.Testing Interval Shortened to Verify Operability 810106 | |
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