05000244/LER-1979-019-03, /03L-0:on 790919,loose Nuts on Anchor Bolts Were Found on Pipe Supports & on Svc Water Piping to Standby Auxiliary Feedwater Pump.Caused by Nuts Working Loose During Sys Operation.Nuts Were Torqued to Current Requirement

From kanterella
(Redirected from ML17261A145)
Jump to navigation Jump to search
/03L-0:on 790919,loose Nuts on Anchor Bolts Were Found on Pipe Supports & on Svc Water Piping to Standby Auxiliary Feedwater Pump.Caused by Nuts Working Loose During Sys Operation.Nuts Were Torqued to Current Requirement
ML17261A145
Person / Time
Site: Ginna Constellation icon.png
Issue date: 10/19/1979
From: St Martin J
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17249A212 List:
References
LER-79-019-03L, LER-79-19-3L, NUDOCS 7910220354
Download: ML17261A145 (2)


LER-1979-019, /03L-0:on 790919,loose Nuts on Anchor Bolts Were Found on Pipe Supports & on Svc Water Piping to Standby Auxiliary Feedwater Pump.Caused by Nuts Working Loose During Sys Operation.Nuts Were Torqued to Current Requirement
Event date:
Report date:
2441979019R03 - NRC Website

text

U. S. NUCLEAR REGULATORY COMMISSION NT REPORT

~

(OAR 1339)

{PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION)

NRC FORM 366 I7-77) r f

79-019/

CENSEE EVE CONTROL BLOCK:

Qi 1

6 N Y R

B G 1Q20 0 -

0 0

0 0

0 0

0 Q34 1

1 1

1 QE~QE 9

LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 [oat 7

8 CON'T

~8 7

8 REDRT ~LQB 0

5 0

0 0

2 4

4 7

0 9

1 9

7 9

B 1

0 1

9 7

9 QB 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES +10 During inspections required by IE Burietin 79-14, loose nuts on anchor bolts were

~o3 found on pipe supports SW-1 4 1, - 1 42, -1 43,

-. 1 45, and 1 46, on service water piping

~o4 to the "D" standby auxiliary feedwater pump.

Although the pump was declared

'I ~os inoperable (T ~ S

~ 3 ~ 4 ~ 2. d) all three auxiliary feedwater pumps and the alternate

~OB standby auxiliary feedwater pump were operable.

7

~O7

~OS 80 7

8 9

~OB 7

8 SYSTEM

CAUSE

CAUSE COMP.

VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~OH Q77.

~B Q72

~O Q73 9

U P 0 R

T Q74

~B Q78

~Z QE 9

10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.

CODE TYPE NO, Q17 REPoRT ~79

~

~01 9

+r

~03

~L

+

+0 21 22 23 24 26 27 28 29 30 31 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP.

COMPONENT TAKEN ACTION ON PLANT METHOD HOURS l@2 SUBMITTED FORM SUB.

SUPPLIER MANUFACTURER Q18 ~Z Q18

~ZQ20

~Z Q27 0

0 0

0

~N Q23

~N Q24

~A Q28 G

1 9

0 Q28 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o

Construction requirements at the time of installation (1975-1977) did not detail anchor bolt torqueing requirements.

Nuts worked loose during system operation.

Nuts were torqued to current requirements, and pump was then declared operable.

These anchor 3

bolts willcontinue to be inspected in accordance with the station ISI program.

4 7

8 9

FACILITY STATUS

% POWER OTHER STATUS Q E

1 0

0 NA 44 METHOD OF DISCOVERY GR ~Q28

~CQ31 7

8 9

10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITY 6

~Z Q33

~ZQ34 NA 7

8 9

10 11 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 7

~0000 00Q3 7 Z

Q38 NA 7

8 9

11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41 8 ~00 OQR NA DISCOVERY DESCRIPTION Q32 IE Bulletin 79-14 LOCATIONOF RELEASE 80 80 80 80 7

8 7

8 o

7 8

9 11 12 LOSS OF OR DAMAGETO FACILITY 43 TYPE

DESCRIPTION

Z Q4, NA 9

IO PUBLICITY ISSUED DESCRIPTION~

~NQ44 NA 9

10 80 80 79102203~

NRC USE ONLY Tohn T. St Martin NAME OF PREPARER 7

68 69 80 ER PHDNE.7 1 6/546-2700, ext ~ 29 1-253