ML17251A471

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Insp Rept 50-244/89-04 on 890313-17.Violations Noted.Major Areas Inspected:Engineering Organization & Function at Site & Corporate Ofc,Design Activities,Outage Planned Mods,Work Backlog & Project Prioritization
ML17251A471
Person / Time
Site: Ginna 
Issue date: 04/27/1989
From: Eapen P, Gregg H, Moy D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17251A469 List:
References
50-244-89-04, 50-244-89-4, NUDOCS 8905110209
Download: ML17251A471 (14)


See also: IR 05000244/1989004

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION I

Report

No.

50-244/89-04

Docket No.

50-244

License

No.

DRP-18

Licensee:

Rochester

Gas

& Electric

Com an

49 East Avenue

Rochester

New York

14649

Facility Name:

R.

E. Ginna Nuclear

Power Plant/Cor orate

En ineerin

Office

Inspection At:

Ontario

New York/Rochester

New York

Inspection

Conducted:

March 13-17

1989

Inspectors:

Daniel

T.

oy,

Rea

Engineer

date

Harold

.

regg,

Seni r Reactor

Engineer

d te

Approved by: P..

Eapen,

Chief, Special

est

Program

Section

date

Ins ection

Summar

Routine

unannounced

ins ection

on March 13-17

1989 throu

h A ril 20

1989.

Ins ection

Re ort No. 50-244/89-04

T

T

T

d <<T

T

d

function at the site

and corporate office.

Specific reviews of design

activities,

outage

planned modifications, work backlog,

and project prioritiza-

tion were performed during the inspection.

The inspection also included

observations

of two attended training sessions

and observations

from plant

walkdowns.

Results:

One violation pertaining to

PORV block valve replacement

was

identified.

Three inspection findings were designated

as unresolved

items.

3905110209

390423

PDR

ADOCK 05000244

Q

PDC

DETAILS

1.0

Persons

Contacted

1. 1

Rochester

Electric and

Gas

Com an

R.

E. Ginna Site Personnel

  • S. Adams, Technical

Manager

J.

Bodine, Nuclear Assurance

Manager

"T. Harding, Modification Support Coordinator

  • R. Marchionda, Director of Outage

Planning

T. Marlow, Superintendent

Ginna Support Services

"S. Spector,

Plant Manager

Ginna Station

  • J. Widay, Superintendent

Ginna Production

Cor orate

En ineerin

Personnel

R. Mecredy,

General

Manager Nuclear Production

  • B. Snow, Chief Engineer

G. Voci, Manager,

Mechanical

Engineering

"P.

Wi lkens, Director, Nuclear Engineering

Services

G. Wrobel, Manager,

Nuclear Safety

and Licensing

1.2

U.S. Nuclear

Re viator

Commission

C. Marschall, Senior Resident

Inspector

N. Perry,

Resident

Inspector

"Denotes

those

present at exit meeting

on March 17,

1989.

2.0

Objective

The objective of this inspection

was to review and evaluate

the

engineering

organization

and function at the site

and corporate office.

The review of staffing, personnel

capability,

planned

and completed

activities, project status

and backlog, interface

between organizations

and management

control was included in the inspection plan.

Both site and corporate

engineering

have

undergone

recent organizational

changes.

At the site,

the technical

and modification support groups were

separated

and are

headed

by two new supervisory positions that report

directly to the plant manager.

At the corporate office, nuclear

and

non

nuclear engineering

were separated.

1,

0

Site engineering

is performed

by two groups,

the modification support

group and the technical

group.

Modification support

has

10 engineers,

5 are

RGE and

5 are contract personnel.

Staffing levels

have

remained

constant,

several

personnel

transfers

have occurred,

and the work backlog

remains

high.

This group reviews

and inputs major modification details,

interfaces with corporate

engineering,

and is cognizant

and involved with

the modification installation.

This group also interfaces with mainte-

nance

and the site technical

group.

The other site engineering

group,

the

technical

group,

performs minor modifications,

temporary modifications,

and operational

trouble report related work.

Present

staffing of this

group is

7 engineers

plus

2 test

and results

engineers

whereas prior

staffing was

4 engineers total.

Corporate

engineering

recently reorganized

as nuclear engineering

services

and consists

of mechanical,

electrical,

nuclear safety

and licensing

disciplines.

The cur rent staff is 72 engineers

and there are

12 newly

approved

vacancy positions.

Prior to the reorganization

the staff was

70

engineers,

of which 20 had

non nuclear functions.

In summary,

the inspector

concluded that the site and corporate

engineering

organizational

changes

implemented

by the licensee

are beneficial

and are

established

to improve responsibility and accountability of nuclear

engineering activities.

Staffing levels at corporate

engineering

have

been substantially

increased

and filling the

12 vacancies will further

improve this organization's

capability,

however,

the current project backlog

remains extremely large.

The staffing increase

in the site technical

group

was viewed positively and their work completion

appears

to be timely.

The

modification support group was

found proficient. and capable

in handling

their assignments,

however, their staff has not increased

and their work

burden is high.

In each of the engineering

areas,

constant

communications

and interfacing were evident

between

the site

and corporate

engineering

functions.

4.0

Review of Major Modifications

Several

major modification project design criteria and safety analysis

details

were reviewed

by the inspector.

These projects were:

Offsite Power Reconfiguration

EWR 4525.

(Permanent

installation

of second station transformer to improve system reliability and

eliminate susceptabi lity of single failure loss of all

AC power.)

Safety Injection

pump recirculation loop -

EWR 3881. (Increasing

the

loop piping size to increase

minimum pump flow and replacement

of

currently blocked

open air operated

valves with environmentally

qualified motor operated valves).

RHR pump recirculation

loop EWR 4675.

(Installing separate

recirculation

loops in response

to

NRC Information Notice (IN) 85-09

and Bulletin (BU) 88-04.

The

BU and

IN described

the problem of two

pumps discharging into

a

common

header resulting in restricted flow

or dead

heading

the weaker

pump).

PORV block valve Upgrade -

EWR 3755.

(Existing Velan gate valve seats

had been

machined

many times and little seat material is left.

The

two PORV block valves are being replaced with Anchor Darling double

disc gate valves).

Review of Desi

n Criteria

The inspector noted that the design criteria was brief in all cases

other than the offsite power reconfiguration which had more detail.

It was determined

the reason

the criteria was brief was that this

was

an initial project document

and precise details of the

modification may not be

known at the time.

The inspector verified

that corporate

engineering

does

document

subsequent

design

reviews

and analysis

and other descriptive

documentation detail is available.

4.2

Safet

Analysis

The inspector

reviewed the safety analysis for each of the above

modification projects.

The inspector

noted that in each

case

the

safety analysis describes

and assesses

the proposed modification

consequences

and concludes with preliminary safety evaluation

statements

reflecting

some of the provisions of 10 CFR 50.59.

The

inspector's

noted that the assessment

and the 50.59 provisions

are not linked and it is difficult to relate the assessment

to the

10 CFR 50.59 provi sion.

For example,

the

RHR recirculation

upgrade

safety analysis

narrates

the intent of the modification and

references

design criteria to show non-adverse

performance.

The

analysis

concludes with individual

10 CFR 50.59 provisions

as being

met.

The inspector

concluded that the analysis

would be improved if

each of the

10 CFR 50.59 provisions

had

a narrative justification.

4.3

PORV Block Valve

Re lacement

The design criteria and safety analysis for replacement

of the two

3" Velan wedge gate valves with two 3" Anchor Darling double disc

gate valves were reviewed during the inspection.

The reason

the valves

are being replaced is to enable

minimum seat

leakage

to be maintained.

Prior seat machinings

have limited the seat

surface available for

further remachining.

However, the design criteria and safety analysis

did not describe

or provide any justification for the operational

qualification of the replacement

valves that are

a different design

and manufacturer

than the original valves.

Operational qualification

of PORV block valves

was specified in

NUREG 0737 as

TMI Action Plan

Item II.D.1,

The licensee

committed to this TMI action plan item as

confirmed in the

NRC Order issued

on July 10,

1981.

The original

Velan valves

had

been qualified for operation

and

a safety evaluation

report for these

valves issued

by the

NRC.

However, at the time of

the inspection it was determined that requirements

relative to oper-

ability of the Anchor Darling replacement

valves

had not been fully

addressed

or documented

by the licensee for the approved modification.

0

Due to concerns of the safety significance of this modification

several

additional

conference

telephone calls were

made

and

some

preliminary information was obtained.

The licensee

was requested

to

provide documentation

demonstrating

that the valves are qualified

for operation prior to restart of the plant.

The failure to adequately

evaluate

operational qualification of the

replacement

PORV block valves is

a violation of 10 CFR 50, Appendix B,

Design Control requirements

(50-244/89-04-01).

5.0 ~P

The planned activities for the refueling outage

scheduled

March 17,

1989

to May 11,

1989 were discussed

with the outage director.

Many major

modifications are planned

since this is

a

10 year ISI outage

and the core

will be unloaded.

Major modifications include:

safety injection and

residual

heat

removal recirculation piping upgrade,

turbine trip system

ATWS

modification, offsite power reconfiguration,

steam generator

snubber

replacement,

and

steam generator

blowdown system

upgrade.

Many other

major activities are planned concurrent with the major modification work

and include:

steam generator

inspection,

"A" reactor coolant

pump motor

replacement,

primary valve maintenance,

high and low pressure

turbine

overhaul,

primary heat exchanger

inspections,

and

many maintenance

related activities.

Outage

plans

and schedule

milestones

were reviewed

by

the inspector

and verification was

made that outage

planning meetings

were effective.

The inspector

concluded that the outage project schedule

was comprehensive

and the planning

and training for the outage

appears

effective.

6.0

Modification Project Prioritization

The inspector

noted that the major project listing contains approxi-

mately 250 projects

and based

on discussions

with engineering

personnel

the backlog continues to increase.

The inspector

was concerned

about

the large project backlog

and its implication that insufficient resources

.may be allocated to major project work,

some of which may have

significant safety significance.

This issue is unresolved

pending

the licensee's

evaluation of the project listing (50-244/89-04-02).

6.2

New Prioritization

S stem

The licensee

has recently developed

a new method of prioritizing

modifications

and other activities.

The

new system considers

the

attributes of safety, operability, regulation, plant improvement,

and corporate objectives

in decreasing

order.

Various elements of

each attribute are rated

and assigned

a numerical

value

and the

aggregate

numerical

value provides the level of priority.

The

higher the total, the higher the priority.

The inspector

viewed the

new prioritization system

as far improved over the old judgmental

approach that had

been

used,

and

a worthwhile licensee effort.

The

inspector

noted that the project prioritization currently in place

for 1989

and

1990 still utilizes the old system.

7.0

Use of PRA Techni

ues

The licensee

has not had any significant

PRA involvement to date.

Two

PRA engineers

were recently hired and the licensee

plans to perform

PRA

reliability analyses utilizing plant data.

Currently the licensee

has

not committed to

a schedule of PRA planned activities.

8.0

Trainin

Observations

8. 1

Safet

Evaluations

During the inspection,

the inspector attended

a,10 CFR 50.59 Safety

Evaluation training session

being conducted

by an outside contractor.

The training was well attended

and the inspector considered

the

effort worthwhile.

The inspector also noted that site engineering is

striving to eliminate past

problems of maintenance

performing design

modifications without a safety evaluation.

This is being accomplished

through closer ties

and communications with maintenance

and the

routing of trouble reports

through qC, the maintenance

supervisor,

and maintenance

planner.

Additionally, maintenance

goes over the

details of their work plans at the morning meeting where further

staff review is obtained.

8.2

Steam Generator

Maintenance

The inspector

observed

plant personnel

being trained

by Combustion

Engineering

in preparation for the

steam generator

sleeving during

the outage.

The

steam generator

mock-up was being utilized and the

plant personnel

were training

on the installation of the sleeving

elevator

and its attachment

to the manipulator

arm.

The inspector

viewed the training as effective,

however,

there

was

a concern that

the trainees

were not in PCs or masks.

The licensee's

representative

stated that this training was preliminary and that later training is

to be done in PCs

and masks.

9.0

Plant Walkdown Observations

Inspections

were

made in the plant of the safety injection pumps

and

blocked

open

AOVs, main steam safety valves,

main steam isolation valves,

spent. fuel pool cooling

pump installation,

and feedwater

(FW) piping and

valves.

The inspector

noted

numerous

valves in the turbine building that

had the

appearance

of neglect.

Manual

FW valves

3978

and

3979

had packing leaks,

MOV 3976

and

3977

had packing residue

on the stem,

small valves

1960 and

1961

had considerable dirt and dust inside the yoke posts,

valve 3527 had

a gland leak,

and valve 3872 appeared

to have

some packing extrusion.

The

general

condition of the valves in this area

was evidence of non uti liza-

tion of general

valve maintenance

practice.

This matter is unresolved

pending the,licensee's

evaluation of these

concerns

(50-244/89-04-03).

The inspector

noted problems with the closure capability of fire doors

F13,

14 and

15 in the turbine building at the mezzanine

level

and door S65

in the auxiliary building.

In each

case

the automatic door closer would

not fully close the door.

It was noted that door S65 was

an alarmed door

and personnel

would latch it, however,

in the case of the other doors,

they

were left partially open.

It was noted that several

of these

same doors

were identified as problems in prior inspection report 88-24.

This item

is unresolved

pending the licensee's

evaluation

and correction of the

problem (50-244/89-04-04).

10.0 Unresolved

Items

deviations.

and two in

fl

Unresolved

items are matters

about which more information is required in

order to ascertain

whether they are acceptable

items, violations or

Three unresolved

items are discussed;

one in paragraph

6. 1,

paragraph

9.0.

The inspector

met with the licensee's

representatives

at the conclusion

of the inspection

on March 17,

1989.

During the inspection,

the inspector did not provide any written material

to the licensee.

The licensee

representatives

did not indicate that this

inspection

involved any proprietary information.

14

s

I

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