ML17250B278
| ML17250B278 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 06/22/1993 |
| From: | Lazarus W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17250B273 | List: |
| References | |
| 50-244-93-10, NUDOCS 9306300191 | |
| Download: ML17250B278 (14) | |
See also: IR 05000244/1993010
Text
U. S. NUCLEARREGULATORY COMMISSION
REGION I
License: DPR-1S
Inspection Report 50-244/93-10
R. E. Ginna Nuclear Power Plant
Rochester
Gas and Electric Corporation (RG&E)
Inspection:
Inspectors:
Approved by:
April 23 through June 9, 1993
T. A. Moslak, Senior Resident Inspector, Ginna-
E. C.
utson
Resid'ent Inspector, Ginna
wiz~A>
W.
s
C
ef, Reactor Projects Section 3B
INSPECTION SCOPE
Date
Plant operations, radiological controls, maintenance/surveillance,
security, engineering/ technical
support, and safety assessment/quality
verification.
INSPECTION OVERVIEW
y~hi:Add-dy l llg
g
gl
d.R
g,ydyl
'g,
and power ascension
were well controlled.
On May 7, 1993, a controlled power reduction to
42 percent was performed to support maintenance
on a main feedwater pump.
Full power
operation
(approximately
98 percent)
resumed
on May 10,
1993,
and continued for the
remainder of the report period.
Operators demonstrated
attention-to-detail by identifying off-
normal plant conditions.
~RCh
l
l: R*ChhgM
l
'll l
d
d 'g
d
g
operations were conscientiously implemented.
ALARAcontrols for work to repair a leak on
a steam generator blowdown drain line were noteworthy.
Maintenance/
rveillance:
Rework to correct excessive
seal leakoff from the "A" main
pump
and
replacement
of the "A" service
water pump
was
required
due to
procurement program deficiencies.
However, the root cause analysis performed by the licensee
was thorough.
5ggli~:
No deficiencies
were identified during routine observations of security program
implementation.
En ineerin /Technical
Good engineering support was observed in continuing efforts
to correct feedwater control system instability.
fet
A
essment/
ualit
Verifi tion:
Failure to provide adequate
containment of sparks
generated
by metal grinding during maintenance
was an apparent violation of fire protection
program requirements.
9306300i9i
930624
ADOCK 05000244
8
TABLEOF CON'ANTS
VERVIEW
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TABLE OF CONTENTS
1.0
PLANT OPERATIONS (71707)............
1.1
Operational Experiences
1.2
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Control ofOperations..............
1.3
Observations During Power Changes
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2.0
RADIOLOGICALCONTROLS (71707).......................
2.1
Routine Observations ..............................
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3.0
. MAINTENANCE/SURVEILLANCE(62703, 61726)...........
3.1
Corrective Maintenance
3.1.1
"A" Main Feedwater Pump Excessive Seal Leakoff...
3.1.2
Steam Leak Downstream of Valve 5706 in Containment
3.1.3
Pressurizer Power Operated Relief Valve Seat Leakage
.
3.2
Surveillance Test Observations
3.3
Engineered Safety Features System Walkdown (71710)
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4.0
-. SECURITY (71707)
4.1
Routine Observations ........
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5.0
ENGINEERING/TECHNICALSUPPORT (71707, 92701)
5.1
"A" Main Feedwater Regulating Valve Oscillations
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6.0
SAFETY ASSESSMENT/QUALITY VERIFICATION (90712, 90713, 92701
40500)
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6.1
"A" Service Water Pump Replacement
6.2
Inadequate Fire Prevention Measures During Maintenance
6.3
Quality Assurance/Quality Control (QA/QC) Subcommittee Meeting
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6.4
Erosion/Corrosion (E/C) Integrated Management Team Meeting....
6.5
Corporate Management Changes
6..6
Perlodlc Reports.................................
6.7
Licensee Event Reports.............................
7
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7.0
ADMINISTRATIVE(71707, 30702, 94600)
7.1
Backshift and Deep Backshift Inspection
7..2
Exit Meetings
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DETAILS
1.0
PLANT OPERATIONS (71707)
1.1
Operational Experiences
At the beginning of the inspection period, the plant was nearing completion of the annual
refueling
and
maintenance
outage.
Reactor
coolant
system
heatup
to normal
operating
temperature (547'F) was completed on April24.
Operational testing in hot shutdown included
safety valve and control rod drop testing.
All requirements
for startup were
completed on April25, and criticality was achieved at 12:11 p.m.
Startup physics testing was
completed on April25 at 11:33 p.m. Steam plant startup was conducted and the main generator
was closed on the grid at 11:56 p.m. on.April26. Full power, approximately 98 percent, was
reached at 2:01 p.m. on May 1. On May 7, a controlled power reduction to approximately 42
percent was conducted to support corrective maintenance on the "A"main feedwater pump. Full
power operation resumed on May 10, and continued for the remainder of the inspection period.
No significant operational challenges occurred during the inspection period.
1.2
Control of Operations
Overall, the inspectors
found the R.- E. Ginna Nuclear Power plant to be operated
safely.
Control room staffing was as required.
Operators exercised control over access
to the control
room.
Shift supervisors
maintained authority over activities and provided detailed turnover
briefings to relief crews.
Operators adhered to approved procedures
and were knowledgeable
of off-normal plant conditions.
The inspectors reviewed control room log books for activities
and trends,
observed
recorder
traces for abnormalities,.assessed
compliance with technical
specifications,
and verified equipment availability was consistent with the requirements
for
existing plant conditions.
During normal work hours and on backshifts, accessible
areas of the
plant were toured.
No operational inadequacies or concerns were identified.
1.3
Observations During Power Changes
The inspectors observed portions of the reactor startup, physics testing, and power ascension
upon completion of the refueling outage,
as well as the power reduction
and escalation
performed in support of main feedwater pump maintenance.
These operations were conducted
in a professional
manner.
Communications
and supervisory involvement-were noteworthy
'trengths.
No deficiencies were noted.
2.0
RADIOLOGICALCONTROLS (71707)
2.1
Routine Observations
The inspectors periodically confirmed that radiation work permits were effectively implemented,
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dosimetry was correctly worn in controlled areas
and dosimeter
readings
were accurately
recorded, access to high radiation areas was adequately controlled, survey information was kept
current, and postings and labeling were in compliance with regulatory requirements.
Through
observations ofongoing activities and discussions with plant personnel, the inspectors concluded
that radiological controls were conscientiously implemented.
'articularly noteworthy was the planning and coordination to minimize worker exposure when
troubleshooting the steam leak downstream ofvalve 5706. Valve 5706 is located in containment
and is in a high radiation area (10-12 rem/hour) during power operations.
Prior to permitting
personnel entry into this area, the radiological control personnel
assured
that personnel were
equipped with the proper dosimetry, aware of low dose waiting areas,
and briefed on the scope
and nature of individual assignments.
3.0
MAINTENANCE/SURVEILLANCE(62703, 61726)
3.1
Corrective Maintenance
3.1.1
"A"Main Feedwater Pump Excessive Seal Leakoff
A major overhaul was performed on the "A" main feedwater pump (MFP) during the 1993
refueling outage.
On April 26, following pump startup during plant power escalation,
seal
leakoff from the "A"MFP was observed to be excessive.
This leakoff, nominally five gallons
per minute (gpm), is directed to a seal water drain tank and pumped back to the main condenser.
Seal water leakoff from the "A" MFP, however, was estimated to be approximately 60 gpm.
This exceeded
the capacity of the seal water drain tank pump, and the excess flow (estimated
at 20-30 gpm) was dumping from the tank overflow to a floor drain.
On
May 7,
1993,
the
licensee
commenced
a controlled
power
reduction
to
support
troubleshooting and repair of the "A" MFP.
When power had been reduced to less than 50
percent, the pump was secured,
cooled down, and disassembled
for inspection.
The cause of
the excessive
seal leakoff was found to be that the bolts that attach the breakdown bushing to
the pump casing were improperly sized.
The function of the breakdown bushing is similar to
that of a labrynth seal.
The hold-down bolts for the breakdown bushing were found to be too
long and prevented
the bushing from seating
against the pump casing.
This allowed high
pressure water inside the pump to be directed to the outside of the bushing, thus bypassing the
pressure
reducing channels
and traveling directly out the shaft penetration in addition to the
normal seal leakoff.
Investigation revealed that the improperly sized hold down bolts had been part of a breakdown
bushing replacement kit that had been installed during the recent pump overhaul.
The problem
had not been obvious during the overhaul reassembly,
because the bushing was brought nearly
in contact with the casing (0.017 inch clearance with the hold down bolts bottomed out in the
casing), and an 0-ring seal at the opposite end of the breakdown bushing absorbed the resultant
slight amount ofplay. No other significant problems were discovered during pump disassembly
and inspection.
The original breakdown bushing hold down bolts were subsequently
used in
pump reassembly.
The pump was returned to service on May 10, 1993.
A licensee performed root cause analysis revealed that procurement of improperly sized bolts
had caused the problem. This error, in turn, was attributed to 1) inaccuracies
in the vendor's
manual,
and 2) a change from procurement by individual part numbers to procurement by
assembly number (which does not specify the length of the hold down bolts). The licensee took
appropriate corrective actions which included returning to the practice of ordering replacement
parts by individual part numbers, and upgrading the vendor technical manual.
The inspector observed portions of the maintenance activities conducted on the "A"MFP and
noted no deficiencies.
The inspector reviewed the maintenance work package, generated under
"Feedwater Pump A - Repair Excessive
Seal Leakage."
Work was
conducted in accordance with maintenance procedure M-11.24, "A"Main Feed Pump Inspection
and Maintenance," revision 8, effective date March 30, 1991. The inspector concluded that the
work package adequately directed and documented, this maintenance and had no further questions
in this area.-,
3.1.2
Steam Leak Downstream of Valve 5706 in Containment
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On April30, 1993, while viewing the containment video monitor, on-shift operations personnel
observed intermittent wisps of steam in the vicinityof the "B" reactor coolant pump.
Although
the source of leakage could not be directly observed,
containment leakage detection
systems
confirmed that it was small in size, and containment air particulate monitor activity confirmed
that it was not reactor coolant system leakage.
Subsequent
containment entry determined that
the leak was from a pipe cap downstream ofvalve V-5706 (steam generator "B" blowdown line
drain valve).
Due to high radiation levels (10-12 rem/hour) in the area while at full power,
repair efforts were deferred for one week to coincide with the power reduction that was required
for the main feedwater pump repair (see section 3.1.1). Temporary repair using a special'clamp
assembly injected with a sealant material was successful in stopping the leak. Further corrective
action willrequire cold shutdown conditions.
The inspector observed
the steam leakage
as viewed on the control room video monitor and
concluded
that operations
personnel
had been very alert to have noted the condition.
The
inspector considered that deferring complete repair on the basis of ALARAconsiderations
was
appropriate,
and had no additional concerns on this matter.
3.1.3
Pressurizer Power Operated Relief Valve Seat Leakage
At 9:56 a.m. on April 25, 1993, main control board annunciator F-19, "Pressurizer PORV
[power operated relief valve] Outlet High Temperature 145'F," alarmed.
The PORVs (valves
PCV-430 and -431C) are designed to automatically open on abnormally high reactor coolant
system
(RCS) pressure,
directing coolant to the pressurizer
relief tank (PRT) and thereby
reducing pressure.
The purpose ofannunciator F-19 is to alert operators that actuation ofeither
or both of the PORVs has occurred.
Coolant leakage past the seats of these valves can also
produce sufficiently high outlet temperature to cause the alarm.
The PORVs do not serve a
safety
function during hot shutdown or at-power
operations.
In these
conditions,
overpressure
protection is provided by the two pressurizer
safety valves, V-434 and -435.
In
case of failure to close or excessive
seat leakage,
the PORVs can be isolated by individual
upstream block valves (MOV-516 and -515, respectively).
Operators responded by performing the appropriate portions ofalarm response procedure AR-F-
19, "Przr PORV Outlet High Temp 145'F."
PRT temperature,
pressure,
and level were
essentially constant, indicating that a PORV had not actually lifted. However, PRT temperature
was observed to be rising slowly (approximately 10'F in the first 15 minutes), suggesting that
seat leakage had developed from one of the valves.
PORV seat leakage had not been a problem
prior to the refueling outage and no maintenance
had been conducted on the valves during the
outage.
Determination of which valve was leaking was complicated by the fact that the valves
are located in the pressurizer
cubicle in the containment building (making direct inspection
difficult), as well as by the small rate of leakage (calculated to be approximately 0.025 gallons
per minute).
Due to the piping configuration and the low leakage rate, conduction of heat
between the two discharge lines allowed their temperatures to equalize and thus precluded using
PORV downstream temperature to identify which valve was leaking.
Operators attempted to eliminate the leakage by cycling the PORVs (one at a time) with their
associated block valves shut.
In addition to possibly achieving positive seating simply through
the act of being cycled, it was reasoned
that the small amount of coolant flow that would result
from depressurizing
the piping between the block valve and the PORV might clear any material
that could be fouling the seating surface.
This action, however, did not correct the
problem.'ubsequently,
a containment
entry was made to attempt to identify the cause of the high
temperature alarm by direct inspection.
Since leakage through the pressurizer
safety valve's
loop seal drain valves could, by conduction through common piping, raise temperature enough
to cause
the alarm,
these valves were verified to be fully shut.
Results of ultrasonic and
thermographic inspections in the area of the PORVs were inconclusive.
Through discussions
with the valve vendor, it was determined that proper seating may be achieved by reorienting the
valve seat and disc.
This technique was attempted on PCV-430 by rotating the valve stem/disc
90 degrees relative to the seat.
The results, however, were inconclusive, and the technique was
not attempted on the other PORV.
Operators closed the block valves in an attempt to stop the leakage.
Best success
was achieved
by maintaining the block valve for PCV-431C closed.
Although this configuration maint'ained
normal PORV outlet temperature
most of the time, the intermittent high temperature
alarm
condition continued to develop.
As of the close of the inspection period, the licensee was operating with the block valve for
PCV-431C
shut.
The
source of leakage
remained
undetermined,
although
inability to
consistently clear the PORV outlet high temperature alarm by closing both block valves suggests
that all four valves are contributing.
This leakage
does not constitute a direct operational
concern; it is contained within the system designed to collect PORV discharges
and the rate of
leakage is very low. The PORVs are not used during normal plant operations and, ifrequired
due to off-normal conditions, restoration is adequately
directed by the applicable emergency
operating procedures.
At-power operation with one (or both) PORV isolated (that is, with its
respective block valve shut) does not present a safety concern.
This configuration is allowed
by Technical Specifications, based on the requirement for both pressurizer
safety valves to be
The licensee will continue to monitor this condition and will inspect both PORVs
during the next annual outage.
The inspector considered
these actions to be appropriate.
3.2
Surveillance Test Observations
Inspectors
observed
portions of surveillance
tests
to verify proper
calibration of test
instrumentation,
use of approved procedures,
performance of work by qualified personnel,
conformance
to limiting conditions for operation
(LCOs), and correct
system
restoration
following testing.
The following surveillances were observed:
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Performance Test (PT)-34.0, "Startup Physics Test Program," revision 27, procedure
change notices (PCNs) 93T-591, 599, effective date April 16, 1993, observed April25,
1993
P
PT-34.1, "InitialCriticality and ARO [all rods out] Boron Concentration," revision 18,
PCN 93T-576, effective date April 16, 1993, observed April25, 1993
PT-12.2, "Emergency Diesel Generator 1B," revision 73, effective date May 27, 1993,
observed June 2, 1993
"The inspector determined
through observing this testing that operations
and test personnel
adhered to procedures,
test results and equipment operating parameters
met acceptance criteria,
and redundant equipment was available for emergency operation.
3.3
Engineered Safety Features System Walkdown (71710)
The inspector conducted a detailed walkdown of a representative
sample of accessible portions
of the safety injection (Sl) and containment spray (CS) systems.
Primary emphasis was placed
on inspection of system material conditions for items that might degrade plant performance.
Items examined included installation of hangers and supports, housekeeping,
material condition
of valves, correct valve positions, and component labeling.
No safety-significant deficiencies
were noted.
The inspector concluded that the material condition of the SI and CS systems was
satisfactory and verified that accessible portions of the systems were properly aligned.
4.0
SECURITY (71707)
4.1
Routine Observations
During this inspection period, the resident inspectors verified that x-ray machines and metal and
explosive detectors were operable, protected area and vital area barriers were well maintained,
personnel were properly badged for unescorted or escorted access,
and compensatory
measures
were implemented when necessary.
No unacceptable
conditions were identified.
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6.
5.0
ENGINEERING/TECHNICALSUPPORT (71707, 92701)
5.1
"A"Main Feedwater Regulating Valve Oscillations
Inspection report 50-244/92-08 discussed
advanced digital feedwater control system (ADFCS)
instabilities experienced
during the automatic mode of operation:
This problem was first
encountered
after startup from the 1992 refueling outage and, despite some improvement as a
result of troubleshooting efforts, persisted
throughout the operating cycle.
During the 1993
refueling outage, the "B" feedwater regulating valve was overhauled and the associated
control
air system was modified as further attempts to improve ADFCS stability.
During power ascension, ADFCS demonstrated good stability in controlling "B" steam generator
(SG), but developed increasingly poor characteristics
in controlling feedwater flow and water
level in the "A" SG. At full power, oscillations in feedwater flow on the order of 10 percent
were occurring over a period of several minutes.
Although normally stable within these limits,
occasionally the oscillations would rapidly increase in frequency and magnitude, to the point that
operator action was required to regain control.
Extensive troubleshooting
has been performed to determine the cause of ADFCS instability in
controlling the "A" feedwater regulating valve.
Actions have included feedwater regulating
valve lubrication and packing
adjustments,
ADFCS gain changes,
and
extensive
system
performance monitoring. It was found that satisfactory system performance could be achieved
by operating with the "A" feedwater regulating valve in manual control and its bypass valve in
automatic control. While this mode of operation adequately controls feedwater flow variations
that occur under steady state conditions, operator action would be required to maintain steam
generator water level during plant transients.
The inspector observed good engineering support and involvement in the efforts to troubleshoot
ADFCS instability.
6.0
SAFETY ASSESSM<22fT/QUALITYVERIFICATION(90712, 90713, 92701, 40500)
6.1
"A" Service Water Pump Replacement
As discussed in inspection report 50-244/93-03, the cause of excessive load on the "A" service
water pump motor was a suspected problem with the pump. During the refueling outage, testing
with the "D" service water pump motor installed on the "A", service water pump confirmed this.
The "A"service water pump was subsequently replaced.
Post-maintenance
testing demonstrated
that both motor and pump parameters
were within their expected values.
During examination
of the original pump internals, the licensee determined that the impeller first stage discharge was
oversized in diameter (1P/8 inches, as opposed to the required 10'A inches).
This impeller had been installed in February 1992, during a pump rebuild. The deficiency had
not been identified at that time,because
the procedure
did not require measurement
of the
impeller discharge.
The deficiency had not been identified during licensee receipt inspection for
the same reason.
The inspector noted that the licensee had specified the diameter of the first
stage impeller discharge on the purchase order for the impeller in question.
Based on the part
'umber,
the correct part for a Worthington service water pump had been supplied; however,
Ginna service water pump impellers had been modified in 1970, with the discharge diameter
being reduced from 11~/8 inches to 10% inches to reduce pump output.
As of the end ofthe inspection period, the licensee was evaluating this situation for 10 CFR Part
21 applicability. Corrective action included modifying both QA receipt inspection and applicable
maintenance procedures to include measurement ofimpeller discharge diameters.
The inspector
concluded that the licensee's
actions in troubleshooting problems with the "A" service water
pump had been thorough and that corrective actions for problems identified in the course of this
activity were appropriate.
6.2
Inadequate Fire Prevention Measures During Maintenance
On June 7, 1993, while in the intermediate building as part of a routine plant tour, the inspector
observed
sparks entering the intermediate building from underneath
an infrequent access
fire
door to the turbine building. The door, S-36, is located approximately three feet from 1) the
reactor trip breaker panel and 2) one of the two rod control power cabinets.
The inspector
considered that a metal grinding operation in the turbine building was the most likely cause of
the sparks.
The inspector noted that no measures
were in place to contain the sparks and that
no fire watch was present.
The inspector proceeded
to the turbine building via one of the
normal access
doors to investigate the source of the sparks.
He determined that grinding had
been in progress
at about the base of the door in question,
but that this work had been
completed.
The inspector informed licensee
management
and operations
personnel of this
observation.
As a result,
the licensee promptly stationed
a fire watch in the intermediate
building in the vicinityof door S-36.
Although no work was in progress, fire watch coverage
is required for 30 minutes following the completion of work in accordance with administrative
procedure A-905, "Open Flame, Welding and Grinding Permit (Hot Work Permit)."
Subsequent investigation revealed that the work, welding and grinding a shim on the door sill,
had been part of a maintenance package to replace door S-36. A welding and grinding permit
had been obtained in accordance with procedure A-905. The inspector noted, however, that the
requirements of this procedure
had not been effectively implemented.
Specifically, step 3.3
requires that the work area be inspected
by Fire Protection and Safety personnel prior to
commencement ofwork. Among the conditions to be verified by this inspection is that openings
into adjoining areas within a thirty-fivefoot radius be closed and/or that a second fire watch be
established.
Although door S-36 was to remain closed throughout the welding and grinding
operations,
compensatory
requirements for the gap between the door and the sill (i.e., closure
with fire retardant cloth on the intermediate building side or posting of an additional fire watch
in the intermediate building) were not specifically addressed.
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Technical specification 6.8.1 states that, "Written procedures shall established, implemented, and
maintained covering...fire protection program implementation."
In that procedure A-905 is an
implementing procedure of the fire protection program, failure to satisfy the requirements ofA-
905 prior to commencing work on door S-36 represents
a violation of technical specification 6.8.1 (50-244/93-10-01).
6.3
Quality Assurance/Quality Control (QA/QC) Subcommittee Meeting
On June
8,
1993,
the inspector
attended
the quarterly
meeting of the RG&E QA/QC
subcommittee.
The meeting addressed
the overall status, findings, and trends identified in audit
programs,
surveillance
programs,
and the various corrective action systems.
- Substantial
progress has been made in establishing cause codes to facilitate consolidation and analysis ofdata
gathered through the corrective action systems..
Using this approach,
a detailed analysis was
performed by the Quality Performance department of Audit Finding Corrective Action Reports,
Corrective Action Reports,
Identified Deficiency Reports,
Non-conformance
Reports,
Observation Reports, and QA Surveillance Observation Reports compiled from January
1, 1992
through March 31', 1993.
The results of this analysis provided definite guidance as to where
management
attention could be directed to reduce negative trends,
Through
this attendance,
the inspector concluded
that the licensee's
Quality Performance
organization is continuing to refine its techniques of performing safety assessments
and quality
verification to increase its effectiveness
as a management tool.
6.4
Erosion/Corrosion (E/C) Integrated Management Team Meeting
On June 1, 1993, the inspector attended the quarterly meeting ofthe E/C Integrated Management
Team.
Attendees
included
management
representatives
from corporate
engineering,
site
maintenance,
site
technical
engineering,
operations,
chemistry,
and
materials
inspection
departments.
The
meeting
agenda
addressed
the
scope
and
results
of nondestructive
examinations performed on large and small bore piping, elbows,
and tees during the 1993
outage, revisions to procedures implementing the E/C program, and proposed E/C activities for
the 1994 outage.
The inspector concluded that the licensee is actively carrying out an E/C program to identify and
correct potential pipe thinning problems to improve plant safety and reliability.
6.5
Corporate Management
Changes
Effective June
14,
1993, Mr. Will McCoy relinquished his responsibilities
as Department
Manager, Quality Performance, to serve on a Corporate Strategic Task Force addressing future
RG&E business
strategies.
In his absence,
the following organizational
changes
have been
made:
Thomas A. Marlow, formerly Superintendent,
Ginna Production, became Department
Manager, Quality Performance
Richard A Marchionda,
formerly Superintendent,
Support Services,
Ginna, became
Superintendent,
Ginna Production
Steven T. Adams, formerly Technical Manager, Ginna, became Superintendent,
Support
Services, Ginna
Terry R. Schuler, formerly Operations Manager, Ginna, became Technical Manager,
Ginna
Terry A. White, formerly Operations Assistant, Ginna, became Operations Manager,
Ginna
6.6
Periodic Reports
Periodic reports
submitted by the licensee
pursuant
to Technical Specification 6.9.1 were
reviewed.
Inspectors verified that the reports contained information required by the NRC, that
test
results
and/or
supporting
information were
consistent
with design
predictions
and
performance specifications,
and that reported information was accurate.
The following report
was reviewed:
Monthly Operating Report for April, 1993
No unacceptable
conditions were identified.
6.7
Licensee Event Reports
~
~
A hcensee event report (LER) submitted to the NRC was reviewed to determine whether details
were clearly reported, causes were properly identified, and corrective actions were appropriate.
The inspectors also assessed
whether potential safety consequences
were properly evaluated,
generic
implications were
indicated,
events
warranted
onsite
follow-up, and
applicable
requirements of 10 CFR 50.72 were met.
The following LER was reviewed (Note: date indicated is event date):
~
93-002, Steam Generator Tube Degradation Due To IGA/SCC, Causes Quality Assurance
Manual Reportable Limits To Be Reached (April 4, 1993)
The inspector concluded
that the LER was accurate
and met regulatory requirements.
No
unacceptable
conditions were identified.
7.0
ADMIMSTRATIVE(71707, 30702, 94600)
7.1
Backshift and Deep Backshift hispection
During this inspection period, a backshift inspection was conducted on May 7, 1993.
Deep
backshift inspections were conducted on the followingdates: April24, 25,.May 2, 8, 9, 29, 31,
and June 6, 1993.
7.2
Reit Meetings
10
At periodic intervals and at the conclusion of the inspection, meetings were held with senior
station management
to discuss the scope and findings of inspections.
The exit meeting for
inspection report 50-244/93-09 (emergency preleredness program, conducted May 17-21, 1993)
was held by Mr. Craig Gordon on May 21, 1993.
The exit meeting for followup inspection
conducted for inspection report 50-244/93-08 (service water system outage maintenance, initial
inspection conducted April 12-16, 1993 and followup inspection conducted May 24-28, 1993)
was held by Mr. Harold Gregg on May 28, 1993.
The exit meeting for inspection report 50-
244/93-10 was held on June 9, 1993.5
0:
0