ML17250A931
| ML17250A931 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 08/10/1989 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17250A932 | List: |
| References | |
| 50-244-87-99, NUDOCS 8908230040 | |
| Download: ML17250A931 (64) | |
See also: IR 05000244/1987099
Text
ENCLOSURE
BOARD REPORT
U. S.
NUCLEAR REGULATORY COMMISSION
REGION I
SYSTEMATIC ASSESSMENT
OF LICENSEE
PERFORMANCE
BOARD REPORT 50-244/87"99
ROCHESTER
GAS AND ELECTRIC CORPORATION
R.
E.
GINNA NUCLEAR POWER
PLANT
50-244
ASSESSMENT
PERIOD:
December
1,
1987 -
May 31,
1989
BOARD MEETING:
July 11,
1989
3003230040
35'03/0
ADOCK 05000244
O
TABLE OF CONTENTS
PAGE
I.
INTRODUCTION...............
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II.
SUMMARY OF RESULTS...................................................
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II.A
Overviewt
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II.B
Facility Performance Analysis Summary.
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III. PERFORMANCE ANALYSIS.................................................
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III.A
III.B
III.C
III.D
IIIi E
III.F
III.G
Plant Operations..............
Radiological Controls.........
Maintenance/Surveillance.....
Emergency Preparedness........
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Engineering/Technical
Support.
Safety Assessment/guality
Veri
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SUPPORTING
DATA AND SUMMARIES
A.1
Licensee Activities.........
A.2
Direct Inspection
and Review Activities............
B
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C.
Unplanned
Shutdowns,
Plant Trips and Forced
Outages
D.
Enforcement Activity...............................
E.
Inspection
Hour Summary.....
F.
Licensee
Event Report Casual Analysis..............
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o SD/S 8
TABLES
Table
1 - Enforcement/Severity
Level
Table
2 - Inspection
Hour Summary
Table
3 - Listing of LERs by Functional
Area
I.
INTRODUCTION
The Systematic
Assessment
of Licensee
Performance
(SALP) is an integrated
NRC
staff effort to collect the available observations
and data
on
a periodic basis
and to evaluate
licensee
performance
based
upon this information.
The program
is supplemental
to normal regulatory processes
used to ensure
compliance with
NRC rules and regulations.
It is intended to be sufficiently diagnostic to
provide a rational basis for allocating
NRC resources
and to provide meaningful
feedback to the licensee's
management
regarding the NRC's assessment
of their
facility's performance
in each functional area.
A NRC SALP Board,
composed of the staff members listed below,
met on July 15,
1989 to review the observations
and data
on performance,
and to assess
the lic-
ensee
performance
in accordance
with Chapter
"Systematic
Assessment
of Licensee
Performance".
The guidance
and evaluation criteria are
summarized
in Section III of this report.
The Board's findings and recommendations
were
forwarded to the
NRC Regional Administrator for approval
and issuance.
This report is the NRC's assessment
of the licensee's
safety performance at
R.
E. Ginna Nuclear Power Plant for the period December
1,
1987 through
May 31,
1989.
The
SALP Board for R.
E. Ginna Nuclear
Power Plant was composed of:
Chairman:
W. Kane, Director, Division of Reactor Projects
(DRP)
S. Collins, Deputy Director,
DRP (part-time)
Members:
B. Boger, Acting Director, Division of Reactor Safety
(ORS)
J. Joyner,
Division Project Manager, Division of Radiation Safety
and Safe-
guards
(DRSS)
R.
Wessman,
Director, Project Directorate I-3,
A. Johnson.
Project Manager,
PD I-3,
E. Wenzinger,
Chief, Projects
Branch
No 1,
ORP
C. Cowgill, Chief, Reactor Projects
Section
lA, DRP
C. Marschall,
Senior
Resident
Inspector,
Ginna
Other Attendees
N. Perry,
Resident
Inspector,
Ginna
C. Amato,
Emergency
Preparedness
Specialist,
ORSS
T. Dragoun,
Senior Radiation Specialist,
DRSS
O.
Haverkamp,
Chief, Reactor Projects Section
3B,
ORP
J. Johnson,
Chief, Projects
Branch
No. 3,
R. Keimig, Chief, Safeguards
Section,
DRSS
J. Prell, Senior Operations
Examiner,
E. Sylvester,
Senior
Reactor
Engineer,
ORSS
2
II.
SUMMARY OF RESULTS
II.A Overview
The licensee
operated
the Ginna Station safely throughout the period.
Senior
corporate
management's
commitment to safety is evident
and
a number of staffing
changes
have
been
made both at the corporate office and plant to strengthen
the
organization.
Overall performance,
however,
has not yet reflected the results
of these
changes.
A significant strength continues to be the technically competent
and knowledge-
able plant and corporate staff.
Personnel
exhibited professionalism
and pride
in their performance,
and station
management
strongly relies
on this asset.
However, this reliance
has resulted in weak administrative controls
and plant
procedures.
Additionally, corporate
and site
management
have not effectively
used the guality Assurance
and guality Control organization
as
a management
tool to improve station performance.
Operator performance
and professionalism
continue to be
a strength during nor"
mal plant operations
and in emergency situations.
The operator. degree
program
is a positi
e initiative which has
been well received
by the operations staff
and'upported
by management.
Constructive
and effective daily staff meetings
have improved communication
between departments.
There is a lack of observation of staff activities by department
and first line
supervision
as evidenced
by weak adherence
to procedures
and continuing house-
keeping deficiencies.
Additionally, a lack of aggressive
response
to NRC,
INPO,
and self-audit findings was noted.
The licensee
has
made
several at-
tempts to improve the effectiveness
of the Quality Assurance
organization.
However, performance
during this period
has not shown
improvement
and there
have
been
several
areas
where
NRC findings were
made that had not been identi-
fied by the licensee's
quality organization.
Performance
in the Security area
was rated Category
1 during the last SALP.
Performance
in this area
was assessed
as Category
2 during this period due
a
lack of management
oversight
and support.
Specifically noted were inattention
to the continuing
need for security system
maintenance
and failure to maintain
a current
and effective Security Plan.
A consistent
strength in this area con-
tinues to be competent
and well trained security force.
Force
members continue
to be professional
and knowledgeable
and morale is high.
In summary,
the licensee
senior
management
is committed to excellence
in per-
formance
and improving programs to maintain
safe
and efficient operation of the
facility.
Use of quality organizations
remains
weak and;.the reliance
on the
technical
competence
of the staff has hindered
improvement in overall perform-
ance.
Improving supervisory oversight of activities, strengthening
admini"
strative controls at the station,
and improving the systems
used
by management
for identifying and correcting deficiencies at the station are necessary
to
attain
a significant improvement in performance.
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II.B Facilit
Performance
Anal sis
Summar
This SALP report incorporates
the recent
NRC redefinition of the assessment
functional areas.
Changes
include combining the previously separate
Mainten-
ance
and Surveillance
areas
and addition of the Safety Assessment/guality
Veri-
fication area.
The Safety Assessment/guality
Verification section is largely
a
synopsis of observations
in other functional areas.:
Additionally, the Fire
Protection,
Licensing, Refueling/Outage,
Training and Assurance
of guality
areas
have
been
incorporated into the remaining functional areas
as appro-
priate.
Functional
Area
Rating
Last
Period"
Rating
This
Period""
Trend
A.
Plant Operations
B.
Radiological Controls
C.
Maintenance/Surveillance""*
2/1
D.
Emergency
Preparedness
E.
Security
F.
Engineering/Technical
Support
G.
Safety Assessment/equality
Verification
H.
Licensing Activities
I.
Training 5 qualification Effectiveness
J.
Assurance of guality
June
1,
1986 to November 30,
1987
- "
December
1,
1987 to May 31,
1989
""* Previously addressed
as separate
areas.
Not addressed
as
a separate
area.
NOTE: It is important to note that
a major revision of the
SALP Manual Chapter
has
been
made which combined
some
areas
and
made
changes
to the attributes
in
the functional areas.
Therefore,
a direct comparison of the functional area
grades
cannot
be made
between
the previous
SALP and the current
one.
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III. PERFORMANCE ANALYSIS
III.A
Plant 0 erations
(2517 Hours,
52K)
III.A.I
A~nal
sos
The previous
SALP report rated this area
Category
2 with a need to assess
the
plant operations
and corporate
engineering
interface.
Strengths
noted were the
strong support of operator training improvement programs,
good operator
exam
results,
overall operator
performance
improvement,
and high plant availability.
Weaknesses
noted were the interface between plant operations
and corporate
engineering
and the lack of aggressive
management
attention toward housekeep-
ing.
This evaluation is based
on routine resident
and specialist
inspections
and
an
Integrated
Performance
Assessment
Team (IPAT) inspection.
Management oversight
and control of operations
was inconsistent
during this
SALP period.
Management
support of the college degree
program
and Morning Pri-
ority Action Required
(MOPAR) meetings
was strong;
however, control of house-
keeping
remained
a problem.
Well-qualified operators
exhibited consistent,
good performance,
but an ineffective independent verification program mani-
fested itself when valves were found out of position.
Weaknesses
were iden-
tified with training in the fire protection program.
The previously noted weak interface
between plant operations
and corporate
engineering
was addressed
through frequent attendance
at daily MOPAR meetings
by corporate
engineers.
Additionally, operation
and engineering
personnel
are
working together closely
on
a
P&ID upgrade
process.
The previously noted weak-
nesses
were not observed
during this assessment
period with the exception of
problems relating to modifications performed in the
1989 r'efueling outage which
is discussed
in the Engineering/Technical
Support analysis.
Plant management
continued to effectively use
MOPAR daily meetings,
where prob-
lems
and daily activities were discussed.
Implementation of a
Human Perform-
ance Evaluation
System
(HPES) process
by operations
management
was
a positive
initiative to improve root cause identification for human performance errors.
Another positive initiative was implementation of a six shift, forward rotating
schedule after the
1988 annual refueling outage.
Input on the
new rotation
schedule
was obtained
from operators prior to implementation;
the
new schedule
was well accepted.
The licensee
has
an effective training program for preparing operators for writ-
ten and operating examinations.
Ten of the eleven candidates
were issued lic-
enses.
Candidates
performed well on sections of the written examination cover-
ing fundamental
nuclear theory,
thermodynamics,
and components.
All candidates
exhibited weakness
during. the operations
phase of the examination;
they did not
correctly identify the proper prioritization and
use of Emergency Operating
Procedures
(EOPs).
Examples of individual weaknesses
included
improper priori-
tization and
use of "Reactor Trip on Safety Injection" and "Loss of All AC
5
Power"
EOPs.
Candidates
were also unable to properly prioritize the Functional
Restoration
Procedures.
However, inplant use of the
was performed
smoothly
and effectively during a loss of normal offshift power,
and following the June
I, 1989 plant trip.
Disposition of EOP change
requests
was
an identified weakness;
approximately
400 outstanding
proposed
changes
were not resolved or dispositioned
in a timely
manner.
In response,
the licensee
developed
and assigned
a task force to as-
sist the
EOP Committee in resolving the backlog of outstanding
EOP change re-
quests.
The validation process for the recently enhanced
was completed;
however,
implementation will not occur until July 1989, after the annual re-
fueling outage,
due to required training of operators.
.An inspection of the
licensed operators training records indicated records
were maintained
as de-
scribed in their procedures
and specific tasks
such
as complicated surveillance
tests,
major pl'ant systems tests,
refueling operations,
and abnormal
and emer"
gency operations
were addressed
with the personnel.
Operator'raining for modifications
and other plant conditions was,
in general,
effective and well-documented.
Training in preparation for the
1989 annual
.refueling outage
was comprehensive,
especially with respect to operations at
low loop levels.
However, while starting the plant
up after the
1988 refueling
outage,
a lack of training on
an unusually positive moderator temperature
co-
efficient resulted
in a plant trip.
Additionally, the plant tripped from 53
percent-',power
on June
1, 1989,
because
of an incomplete understanding
of the
ATWS Mitigation System Actuation Circuitry (AMSAC), a
1989 refueling outage
modification.
Problems
in communicating modification-related
information from
engineering to operations
personnel
are further discussed
in the Engineering/
Technical
Support Section.
Management
support of the college degree
program continued to be
a strength,
with eight licensed operators
earning degrees
during this assessment
period.
Presently
29 plant personnel
are enrolled in the program.
Control
room operators effectively dealt with four plant trips and'everal
plant transients.
Operator actions
were timely, appropriate
and procedures
were
used effectively.
In particular, operator actions dealing with two steam
generator
pressure
transmitter
sensing
lines freezing,
were conservative
and in
the interest of safety.
Weakness
were identified in the licensee's
program for verifying and tracking
proper implementation of corn'mitments,
and administrative controls for handling
and tracking valve positions.
Operators
were manipulating valves without pro-
per tagging
and adequate
independent verification of alignments
was not rou-
tinely performed
and
a commitment, addressing
verification of pr'oper system
alignment per
was not properly interpreted
and implemented.
Control of housekeeping,
identified as
a weakness
in the prior SALP report,
continued to be
a weakness.
Plant management
was deficient in touring plant
spaces
including safety-related
areas;
plant conditions reflected the weak man-
agement
involvement and low management
standards
for housekeeping.
During both
6
refueling outages,
housekeeping
was cyclic in the Containment
and Auxiliary
Buildings.
Though improved since the Auxiliary Building was
opened to access
in street clothes in November
1988, control of extraneous
materials
remains
a
problem.
To address this problem management
is constructing
a Contaminated
Storage Building addition to the Auxiliary Building.
New programs
were
implemented to enhance plant operations.
A PAID upgrade pro-
cess
was initiated requiring
a coordinated effort between
engineering
and opera-
tions personnel.
The initial phases
are complete.
A labeling program, to at-
tach permanent
labels to all plant components
was developed.
Operations
man-
agement
receives
monthly status
reports of labeling progress.
Although the.
labeling program is
a positive initiative, lack of label verification is consi-
dered
a weakness
in the labeling program.
A partially implemented computerized
tagging hold system is in the main control
room and is expected to be fully
implemented late in 1989.
At the close of the
SALP period,
a process
was for-
malized for operations
personnel
to implement
an internal self-check of opera-
tions activities.
While these
programs
are considered
positive initiatives
their effectiveness
has not been
assessed.
Two weaknesses
were identified in the fire protection
program indicating
a de-
ficiency in management
support.
were not installed to design
specification criteria and installation was not verified; this is addressed
in
the Engineering
and Technical
Support section.
Preplanned
quarterly fire
drills Here not conducted
during three quarters
in 1988; 'credit was documented
for responding to false alarms.
The fire protection
program does
not account
for a staff with varying levels of fire training and expertise.
Individuals
with no previous fire fighting experience
were expected
to fight fires after
receiving only four hours of hands
on practice; this is considered
very mini-
mal.
However, fire brigade
members exhibited
a good knowledge of fire fighting
system operations.
Management
support of the college degree
program
and effective use of MOPAR
meetings continued to be licensee
strengths.
Operator training, license
exam
results,
and overall operator
performance
were also noted
as licensee
strengths'oor
housekeeping
persisted
and management
tours,
which could have identified
the problem,
were few.
Control of system alignments
and independent verifi-
cation program weaknesses
were identified as problems.
The fire protection
program also evidenced
some training weaknesses.
III.A.2
Performance
Ratin
- Category 2.
III.A.3
Recommendations
Licensee:
Assess
the adequacy of housekeeping
standards
expected
by management,
and the effectiveness
of the communication of those
standards
to the
staff.
NRC:
None.
7
Radiolo ical Controls (229 Hours,
5X)
III.B.I
~Anal sls
The Radiological Controls Program
was rated category
2 last assessment
period.
Although the program was judged to be effective, overall weaknesses
included
the ineffective policies
and procedures
to control activities,
and the lack of
challenging
exposure
goals in the
ALARA Program.
III.8
During the current assessment
period, three radiation protection inspections
(two outage
reviews,
one review of ALARA and
open items) were conducted.
The
resident inspectors
also routinely reviewed the radiation protection area.
One
inspection
was conducted of the radwaste
and transportation
program.
The area
of chemistry
and effluents was reviewed
as part of the
IPAT team inspection.
The licensee's
Radiological Protection
(RP) organization
was stable
and well-
qualified.
The level of staffing was adequate
to support implementation of the
RP program during routine operations.
Weaknesses
were noted,
however, with the
level of
RP management
oversight of field activities during the
1988 and
1989
refueling outages.
Tours of the work areas
by
RP supervision
and management
were infrequent.
The licensee's
contractor technician workforce, brought in to
support the
1988 outage,
exhibited weakness
in technical
knowledge
and perform-
ance.
While the licensee's
training programs partially addressed
the technical
knowled)e area, it could not make
up for weaknesses
in technician experience.
These
weaknesses
cont> ibuted to observed deficiencies
in procedural
compliance,
High Radiation Area (HRA) control,
and radiological posting
and labeling during
the
1988 outage.
For the extended
1989 outage the licensee
applied
more re-
strictive qualification criteria for hiring technicians
and implemented
a pre-
test screening
program to more effectively train technicians.
As
a result,
contractor technician
performance
improved.
However,
management
oversight of
field activities remained
weak.
Audits of the
RP area
are performed
by the
gA group, with technical
assistance
from the corporate
HP staff and consultants.
Scope of the audits
was adequate.
However,
response
of the
RP group to the gA audit findings, as well as
NRC in"
spection findings,
was often delayed or inappropriate.
NRC concerns with in-
strument'ation
control charts
had previously been identified in repeated lic-
ensee audits,
but not corrected.
Also, NRC-identified weaknesses'ith
job-
related
survey procedures
remained
unresolved
since the previous )ALP.
And the
RP group revised the wrong procedure
in an attempt to correct
NRC identified
deficiencies
regarding calculation
and recordkeeping
of extremity doses.
Five procedural
violations were noted in the
RP area during the assessment
period.
These
included violations of the Special
Work Permit
(SWP)
'and
controls,
and routine survey
and counting instrument
gC procedures.
This ap-
pears
due,
in part, to
a failure by
RP management
to require procedural
com-
pliance.
Weaknesses
were also noted regarding
procedure
adequacy;
specific-
ally, the lack of procedural
guidance relating to the performance
and documen-
tation of job-related
surveys.
8
Insufficient management
oversight
and weakness
in procedural
compliance re-
sulted in repeated
instances
of improper posting
and labeling of radiological
areas
during the
1988 outage.
Specific examples
included the inconsistent
posting of the containment
HRA access,
and the obscuring of significant 'radio-
logical signs
(HRA, Airborne area) with additional postings or tape.
Signi-
ficant improvements
in postings
were noted during the operational
period after
the
1988 outage
and-during the
1989 outage.
The improvements
were
a direct
,
result of the licensee's
response
to
NRC concerns.
The licensee's
training program for contractor
HP technicians
and radiation
workers was satisfactorily implemented.
Lesson
plans were noted to be gene-
rally adequate.
One strength
was noted in that all levels of radiation worker
training (i.e., initial and requalification) include
a practical factor seg-
ment.
As noted above,
for the
1989 outage the licensee initiated pretesting
as
a method to evaluate
and screen contractor
HP technicians
in order to better
focus training.
Late in the period, after significant decontamination
and survey efforts, the
licensee
released
the major ity of the Auxiliary and Intermediate Buildings from
contaminated
area controls.
This substantial
licensee effort, which came about
after
NRC and
INPO had identified the problem and strongly urged corrective
action, allowed easier
access
and better oversight of work activities while
reducing hazards to workers.
Licensee
performance
in the ALARA area
showed
improvement since the last as-
sessment.
The licensee's
1988 exposure
goal of 300 man-rem
was noted to be
more aggressive
than the
1987 goal of 375 man-rem.
Licensee
actual
exposure
for 1988 equaled
approximately
270 man-rem,
the lowest recorded
annual
exposure
for a full operational
year at Ginna.
Although the licensee exhibited excel-
lent planning
and control of repetitive work, such
as
inspec-
tion, goal setting
and planning for one-time-jobs,
such
as plant modifications,
were routinely found to be weak.
Oqe reason for the poor planning during the
1989 outage
was that engineering
packages
for plant design
changes
arrived
on
site just before the start of the outage,
allowing little time to mock-up the
job and train workers.
In addition, illness caused
the loss of the highly ex-
perienced
ALARA Program Coordinator
who had
been
responsible for program im-
plementation.
The licensee'continued
to maintain
an effective transportation
and solid rad-
waste
programs.
Improvements
were
made in the Quality Control
(QC) procedures
for resin dewatering
and in a proceduralized
retraining program for radwas'te
workers.
These
were areas identified during the previous
assessment
period
as
being minor weaknesses.
Ouring the
IPAT inspection,
the
NRC identified
a persistent
weakness
regarding
QC surveillance of chemistry activities.
As part of the corrective action, the
licensee
recently created
the position of QC Specialist
in order to strengthen
the laboratory
QC/QA program.
A noted licensee
strength
was the control of
9
chemistry.
The program established
by the licensee
includes,
items
such
as the
Steam Generator Reliability Committee,
the installation of a
catalytic oxygen removal
system,
and
a secondary
plant data trending
system.
The licensee'
Radiological Controls programs
were adequately
implemented dur-
ing the current period.
Weaknesses
were noted in management
oversight of field
activities,
ALARA planning during the
1989 outage,
resolution of identified
problems,
and procedural
compliance.
The licensee's
use of pretesting to evalu-
ate
and screen
contractor
HP technicians
was
a good initiative.
Training of
radiation wor kers, particularly by use of a practical factors
segment,
was
a
strength.
Control of steam generator
chemistry was another
noted strength,
as
was implementation of the
ALARA program during 1988.
III.B.2
Performance
Ratin
Category 2.
III.B.3
Recommendations:
Licensee:
None.
NRC:
Conduct
a special
inspection of the licensee's
corrective action programs.
III.C
Maintenance/Surveillance
(802 Hours,
17%)
III.C.I
~Anal
sos
Maintenance
and Surveillance
were evaluated
in separate
sections of previous
SALP reports.
This section
has
been created
to consolidate
the two sections
and to assess
all activities associated
with diagnostic,
predictive, preventive
or corrective maintenance
of plant structures,
systems
and components.
It
evaluates
procurement,
control
and storage of components;
installation of plant
modifications;
and maintenance
of the plant physical condition.
It also in-
-'cludes surveillance testing
as well as Inservice Inspection
and Testing acti-
vities.
In the previous
SALP, maintenance
was rated category 2, improving; surveillance
was rated category
1.
Maintenance
weaknesses
included two failures to control
maintenance activities,
a need for continued aggressive
implementation of main-
tenance training, insufficient operations
involvement in outage
and maintenance
planning,
and further progress
needed
in programs for maintenance
upgrade.
Positive steps
taken to upgrade
the maintenance
program
and improve its effec-
tiveness,
and aggressive
management
atte'ntion to maintenance
were noted strengths.
Surveillance
weaknesses
identified were personnel
errors resulting in a missed
test
and poor test control; supervisory level review and data trending,
strong
management
involvement,
and the Inservice Inspection
program were strengths.
This evaluation is based
on routine resident
and specialist .inspections,
a re-
start
team inspection,
a'special
team inspection for Inservice Testing,
and
an
Integrated
Performance
Assessment
Team ( IPAT) inspection.
The
1988 (34 days)
and
1989 (74 days) refueling outages
were completed during the current assess-
ment period.
10
Maintenance
management
was strengthened
during the current
SALP period through
reorganization
under the Superintendent,
Ginna Support Services,
and
a newly
appointed
Maintenance
Manager.
The maintenance
Superintendent
and Manager are
formerly SRO licensed,
have extensive
experience,
and
have
a stated
goal. of
"achieving the highest
long term equipment reliability and unit availability
consistent with achieving
a low forced outage rate, while not compromising nuc-
lear safety,
and maintaining radiation exposures
As Low As Reasonably Achiev-
able."
Overall, control of outage related
maintenance
and surveillance activi-
ties
was
a licensee
strength
although failure to identify defects during eddy
current testing in the
1988 refueling outage resulted in a forced outage to
plug additional tubes.
Few difficulties were attributed to maintenance
or sur-
veillance activities during restart after the
1989 refueling outage.
Observa-
tions of maintenance
and surveillance activities indicated personnel
were
thoroughly qualified and technically competent.
In addition, staffing levels,
considered
adequate
in the previous
SALP, have increased
during the current
assessment
period.
Two trips, two unplanned
shutdowns
and one generator trip attributed to
maintenance activities occurred during this
SALP period.
A trip on low steam
generator
level with steam flow/feed flow mismatch
was caused
by a blown fuse.
The licensee
does
not have
a formal program to address
component
ag'.'ng,
and did
not investigate the possibility of an age-related
failure until prompted
by the
NRC.
An unplanned
shutdown also occurred
when
a bushing failed in the main
substation.
Formal preventive maintenance
in the substation
could have
identified failure of the bushing oil level indicator.
The main generator
tripped because
of the failure to properly install the sliding links following
the
1989 outage.
Licensee
weaknesses
in programmatic control of preventive
maintenance
may have caused
both of unplanned
outages
and the generator trip.
Management reliance
on technical
competence
and pride in performance within
maintenance
and surveillance organizations
contributed to lack of cooperation
at times with the Quality Control
and Quality Assurance
departments.
An ex-
ample is the problem identified during tensioning of the 'B'team Generator
manways,
when lack of management
support for activities of the site
QC organi-
zation resulted
in a delayed reactor restart.
The reluctance
to accept
and
integrate findings by Quality Control personnel
was
a problem identified in the
previous
SALP and has not yet been adequately
addressed.
Reliance
on highly motivated
and technically capable
personnel
also resulted
in
weak administrative control over safety-related activities.
In many areas
procedures
and controls were not specific and required extensive
knowledge
and
experience
to be properly implemented.
Examples of these. problems include:
surveillance
procedures,
previously considered well-written, needed
change;
maintenance
procedures
required extensive rewrite,
and multiple instances
of
failure to adhere to procedures
were observed.
Corporate
and senior station
management
acknowledged
the problem.
However,
some middle level
and lower
level managers
and workers did not acknowledge
the importance of strong
administrative controls of activities.
The maintenance
backlog
was small;
however,
a manual tracking system,
used to manage
the backlog,
was not always
11
current,
and did not provide useful information to managers.
The g-list was
inadequate,
as identified by the
NRC; licensee
long. term response
was appro-
priate; however,
interim measures
to provide
a means of determining
g parts
was not considered until prompted
by the
NRC.
Inadequate
reviews resulted
in
several
safety related
valves being omitted from the IST program,
inadequate
testing of the main steam line check valves,
and escalated
enforcement.
Physics testing
performed during cycle
18 start-up
was closely coordi nated with
the reactor engineer,
operations,
testing,
I&C and Westinghouse
test personnel.
Direction and control of rod drop measurements,
initial criticality, all rods
out boron concentration
measurement,
moderator
temperature coefficient measure-
ment and control rod worth testing,
by the assigned
reactor engineer
was
a
noted licensee
strength.
Licensee action in response
to identified weaknesses
was generally timely and
thorough.
In response
to procedural
adherence
failures, instructions providing
clarification were issued
and training was conducted for plant personnel;
a
comprehensive
procedures
upgrade
program, requiring several
years for comple-
tion, was undertaken
to rewrite calibration
and maintenance
procedures;
compu-
terized systems to track the maintenance
backlog are under development;
an in-
terim instruction
was written to supplement
the g-list unt-:1 a rewrite is com-
pleted;
a schedule
for corrective action in response
to Inservice Testing (IST)
program inadequacies
was formulated
and reported to the
NRC within five days of
the inspection exit meeting.
In some cases,
identification of technical
issues
was weak in the area of sur-
veillance.
Examples:
inadequate
engineering
support for the IST program re-
sulted in check valves test procedures
which were not consistent with require-
ments of ASME Section XI; inadequate
plant reviews resulted in several
safety
related valves being omitted from the
IST program;
and inadequate
testing
was
performed
on main
steam line check valves.
However, surveillance test proce-
dures developed
to implement the IST program were generally well written and
easy to follow.
During the IST program test personnel
were knowledgeable
and experienced
as
demonstrated
during the turbine-driven Auxiliary Feedwater
pump test.
Opera-
tional performance of the staff was
a licensee
strength.
Licensee
implementa-
tion of the Inservice Inspection (ISI) program,
including twenty-year ISI acti-
vities, conducted during the
1989 refueling,
Qas thorough
and well-controlled.
Overall the licensee
has effectively conducted
Maintenance
and Surveillance
activities at the plant.
Personnel
additions
and
changes.
have
been
made to
strengthen
the organization.
The maintenance
staff is experienced
and com-
petent.
Maintenance
backlog is low and there are
few missed surveillances.
Technical
competence
of maintenance
and surveillance
personnel
was
a strength
tempered
by weakness
in administrative control of safety-related activities.
The identified procedural
weaknesses
are being addressed
through
a general
up-
grade of procedures.
Lack of supervisory observation
of surveillance
and main-
tenance activities was
a weakness,
while aggressive
management
and established
goals
were
a strength.
Although valves omitted from the IST program resulted
in escalated
enforcement,
IST surveillance
implementation
was
a licensee
12
strength.
The ISI program
was thorough,
and reactor
physics testing
was well-
controlled and coordinated.
Staffing was adequate,
training effective,
and
efforts to continue training program upgrades
were
a strength..
Licensee re-
sponse
to
NRC concerns
was, in general,
timely and appropriate.
III.C.2
Performance
Ratin
- Category 2.
III.C.3
Recommendations:
None.
III.D
Emer enc
Pre aredness
(103 Hours,
2X)
III.D.I
~Anal sls
During the previous
assessment
period, licensee
performance
in this area
was
rated category
1.
This rating was based
upon evaluation of performance
made
during
a full and
a partial participation exercise,
and the results. of two
routine safety inspections.
No exercise
weaknesses
were identified.
The lic-
ensee
demonstrated
good emergency
response
capability.
Results of the routine
inspections
indicated the licensee
was taking steps to improve emergency re-
sponse capability.
The emergency
preparedness
staff consisted
of one person
supported
by other plant and corporate
personnel.
During the current assessment
period,
a partial participation exercise
was ob-
served
and one routine safety inspection
was conducted.
Personnel
of the
New
York State
Emergency
Management Office, Monroe and
Wayne Counties participated
in the exercise.
Operators
recognized
symptoms
and events,
and correctly
selected
Abnormal
and
Emergency Operating
Procedures.
Accident classification
was correct, offsite notifications were
made within the prescribed
time and
State
and local government participants
were involved in the development of
Protective Action Recommendations.
A Notice of Violation was issued
in the
EP area during the assessment.
The
licensee did not include in the
EP (Emergency
Preparedness)
Program Audit an
evaluation of the adequacy
of State
and local government interface for a number
of years
and did not make these results available to the State
and Counties for
several
years
when this audit was performed.
A review of EP implementing pro-
cedures
revealed that field procedures
that would be
used for collection of
iodine'amples
during off site releases
specifies
inordinately long collection
times.
While this appears
to be conservative, it fails to recognize that ex-
cessive
exposures
to field team .members'nd
that excessive
sample activity
could incapacitate
a laboratory analyzer.
The licensee
could not provide
a
basis
document for this procedure at the time of the inspection,
but committed
to develop
one.
However, at the time of this report,
the basis
document still
was not available.
This delayed
response
to an
NRC concern is considered
iso-
lated and not indicative of a programmatic degradation.
13
The licensee
has demonstrated
several
good initiatives with respect
to the
(Emergency Operations Facility).
for example,
during construction
by the
Rochester City Government in the vicinity of the
EOF, the licensee
took appro-
priate interim steps to maintain
EOF functionality.
To further improve the
EOF, the licensee
recently reconfigured it and increased its area.
An evaluation of licensee
response
to an actual
Unusual
Event involving Secur-
ity and Operations
Departments
indicated that plant staff responded well.
Security officers recognized
the event
and reported it to the control
room,
and
the reactor operator s accurately classified it as
an Unusual
Event.
These ac-
tions demonstrated
effective Security-Operations
interface
and effective train-
ing of security officers in non-security event
response
actions.
The response
by operations
personnel
to this and other Unusual
Events indicates that train-
ing has
been effective.
The plant simulator
has
been
improved with the addition of communications
equipment to permit its use for training drills and exercises.
This eliminates
the risk'of exercise
players
impacting normal operations
and enable
reactor
operators to place real
and simulated calls to off site authorities while
undergoing training.
The result is enhance
exercise
and drill realism.
EP remains
a staff function performed
by one person
supported
by site organi-
zation and licensee
management.
As a short term response
to
NRC concern re-
garding'the
EP staffing, the licensee
recently created
the position of Direc-
tor, Corporate
Radiation Protection.
This position also
has responsibility for
EP and has
been filled by a Health Physicist experienced
in EP.
While
excellent past
performance
in the
EP area did not decline during this
evaluation period, consideration
should
be given to additional staffing in this
area,
as previously
recommended
by a licensee
audit committee.
In summary,
the licensee
maintains
an overall excellent
EP program.
Training
of the emergency
response
personnel
and emergency
response facility operation
is adequate
as demonstrated
during the exercise
and response
to actual
events.
The licensee
does
need to assure
that
EP procedures
are given adequate
review
to provide
a basis
document justifying or revising current field sampling
procedures
for iodine.
An isolated instance of lack of management
control
was
indicated
by the fai lure to provide local governments
copies of audit reports.
III.D.2
Performance
Ratin
- Category l.
III.D.3
Recommendations:
None.
14
III.E
~Secur<t
(187 Hours,
4%)
III.E.1
A~oa1
sos
During the previous
assessment
period, the licensee's
performance
was rated
Category 1.
No major regulatory issues
in the area of physical protection were
identified by either region-based
or resident
inspectors.
During this assessment
period, there were two routine unannounced
security in"
spections
performed
by region-based
inspectors.
Routine inspections
by the
resident inspectors
continued throughout the period.
As a result of the in-
spections,
five Severity Level IV violations were identified involving alarm
system testing, vital area barriers (2), alarm assessment
and inattentive
security officers.
The licensee
took timely and effective action to correct
the alarm system testing deficiency,
and has
scheduled
modifications to upgrade
the barrier at one vital area.
Corrective actions for the other deficiencies
are currently under review by the licensee.
It is not apparent that corporate security management
has continued to ade-
quately monitor the site security program.
There are indications that the suc-
cess of the program in previous
as.'essment
periods
may have resulted in a com-
, placent attitude
by the licensee.
The onsite licensee
security staff is com-
posed of a supervisor
and
a training coordinator,
both of whose strengths
and
efforts!appear
to be directed toward effectively supervising
the training and
performance of the contract guard force.
Because
of the lack of effective cor-
porate
management
oversight
and the emphasis
placed
on the personnel-related
aspects
of the program by onsite licensee
security personnel,
attention to the
performance
and maintenance
of the physical security
systems
have
been
inade-
quate.
No major upgrades
were
made to security
systems
during this assessment
period,
and
some
systems,
notably those related to intrusion alarm assessment,
have
been neglected
to the point that they are marginally effective,
For ex-
ample,
a major degradation
of the assessment
system
was identified by instru-
mentation/control
personnel
and contract security force members
about three
years
ago.
The correction of this problem was not pursued
by onsite licensee
security personnel,
and apparently
no system is in place for either corporate
management
or the onsite supervision to track such degradations
or other
security-related
issues.
Onsite licensee
management
continued to be effective in supe'rvising
the con-
tract security force.
This is evidenced
by the positive attitude toward secur-
ity displayed,
and the support afforded to the security organization
by all
plant personnel.
The site security organization maintains
an active liaison
with the local
law enforcement
agencies,
and conducts
an annual orientation
and
briefing for Federal,
State
and local law enforcement officers.
Effective
security supervision is demonstrated
in personnel-related
aspects
of the secur-
ity program, especially with regard to the development
and implementation of
physical protection procedures,
security force training and personnel
access
control.
However,
systems
and equipment
and the security plan appear to have
been neglected.
15
The annual audit of the security program,
performed
by the licensee's
quality
assurance
group, identified no program deficiencies.
This is in contrast to
the concerns identified by
NRC personnel.
The licensee
committed to evaluate
the effectiveness
of the audit process
and the security expertise
of the audi-
tors in the course of the contractor review of the security program.
Review of the licensee's
security event reports
and reporting procedures
found
them to be consistent with the NRC's regulation,
and implemented
by personnel
knowledgeable
of the reporting requirements.
Three reports
were
aade during the assessment
period.
One involved a loss of security
system
power supply,
and the other two were related to inattentive security force mem-
bers while on post.
The licensee's
and contractor supervisor's
actions in each
case
were prompt and appropriate,
and reflected proper management
involvement
and excellent contingency training.
However, the reports did not identify the
root cause for the inattentive officers or long term corrective actions.
Licensee
management
of the contract security force continued to be effective,
as evidenced
by the continued
low turnover rate (8X), high morale,
a profes-
sional attitude toward job performance
by members of the security force and
good enforcement
record relative to the performance of security force members.
Staffing of the contract security force is sufficient to meet the commitments
of the NRC-approved security plan.
However, during certain shifts,
guard
staffing could be strained
because
of the assignment
of security force members
to collateral duties.
The security force training and requalification program is well developed
and
effectively administered.
This is apparent
from the excellent job knowledge
demonstrated
by securi .y force members during interviews by
NRC personnel
and
few on-the-job errors.
As part of its efforts to assess
security program im-
plementation,
the licensee
also conducted
numerous
Safeguards
Contingency
Plan
drills.
Such drills further demonstrate
the licensee's
desire to maintain
an
effective security force.
During this assessment
period,'he
licensee
submitted three revisions to the
Security Plan in accordance
with the provisions of 10 CFR 50.54(p).
Two of the
revisions were reviewed by the
NRC and found to be acceptable,
although
a resub-
eitta1
was required in one case to provide more complete information.
The
third revision is currently under review by the
NRC,
The licensee
also sub-
.
mitted revisions to the'.Security
Plan in response
to the
10 CFR 73.55, Mis-
cellaneous
Amendments
and Search
Requirements.
The revisions contained
com-
mitments which meet the objectives of the rule change
and were
found to be ac-
ceptable.
The accuracy of the exit<'ng Security Plan
was also reviewed during on-site
inspections
by
NRC personnel,
and inconsistencies
in the Plan were identified.
From these
reviews,
there are indications that'he
licensee
does
not fully
understand
the importance of maintaining
a clear consistent
Security Plan
and
the
need to submit timely and accurate
revisions.
The licensee
has initiated
a review of their plan to address
this concern,
but the effectiveness
of this
review has not been
assessed.
16
The licensee
has,
in general,
maintained
an effective security program.
There
are
some indications,
however, of a lack of management
oversight
and support to
the continuing
need for security
system
upgrades
and modernization,
and for
maintaining
an effective Security Plan
~
As in the .past,
the strongest
areas
in
the security program are the training program for the security force and the
performance of the security force members.
However, the staffing level of the
contract security force, at times,
could be strained.
Also, the weakness
in
managerial
expertise
in physical security
systems
have contributed to the
decline in overseeing
the proper operation of systems
and equipment
and the
quality of the security plan.
III.E.2
Performance
Ratin
Category
2.
III.E.3
Recommendations:
Licensee:
Evaluate
the adequacy of the management
system to monitor and track
security
system
and equipment
performance.
IIIsF
En ineerin /Technical
Su
ort (311 Hours,
6X)
III.F.I
A~nal sls
In the prior assessment
period,
Engineering/Technical
support
was rated
as
a
Category 2.
The board noted problems
such as:
staffing shortages
causing
en-
gineering to operate
in a reactive
mode, limited routine support to the plant,
ineffective prioritization of projects,
weak interface
between corporate
and
site resulting in delays in resolving issues,
inadequate
assessments
of safety
significant issues
and omissions of safety evaluations,
and weak management
control in Equipment gualification activities.
Several
positive factors noted
by the board were:
the nucleus of competent
corporate
engineering
personnel,
aggressiveness
in the fire protection activity, and
good engineering training.
The board
recommended
a reexamination
in the depth of the engineering staff to
ensure
resources
are available to enhance plant performance
by the conduct of
proactive initiatives.
The following evaluation is based
on assessments
of engineering
support effec-
tiveness
from routine
and special
inspections
performed during this assessment
period.
Assessments
also related to the licensee's
activities in response
to
the prior assessment
comments.
Corporate
and site organizational
changes
have
been
made.to define account-
ability and improve management's
capability to assess
and resolve engineering
issues.
The separation
of the corporate
engineering
nuclear
and non-nuclear
functions was
a noted
improvement.
Creating
two new supervisory positions that
oversee all plant activities and report to the plant manager
was considered
a
positive action.
These
changes
have improved management
involvement in assur-
ing quality.
17
In response
to staffing shortages
identified in the previous
SALP, increases
were evident at both corporate
and site engineering.
In corporate
engineering
there
was
an increase
of 22 engineers
with present
approval for 12 more.
At
the site the technical
group staff was increased
from thirteen to twenty"six.
The staffing increases
at both locations
has aided the effectiveness
in com-
munications
between
corporate
and site.
It was also noted that two
PRA engi-
neers
have recently
been hired and
PRA reliability analyses
are planned.
The
above staffing increases
indicate
management
commitment to improve the quality
of the engineering
support to the plant.
Despite the above
improvements,
the licensee
performance
in this area
has
been
mixed.
Inadequate
engineering
support of the
pump and valve inservice test
program led to testing omissions
and inadequate
testing of safety
system
com-
ponents
and resulted
in a level III violation with a civil penalty.
The
licensee
has
made rapid and significant progress
in addressing
this deficiency.
The site technical
group staffing increase
aided in the licensee's
quick cor-
rective action.
During the startup
from the
1989 refueling outage,
operators
were not fully
aware of the status of the SI and
AMSAC modifications.
Failure of the engi-
neering groups to ensure
operators
were formally notified of changes
imple"
mented resulted
in a plant trip and
a forced shutdown.
The licensee
has
been aggressive
in attempting to correct
10 CFR 50.59 problems
by instituting training, placing additional
departmental
overview in the formal
review process,
and discussing daily modification work at the morning meetings
as
an informal review process.
However,
weaknesses
in 10 CFR 50.59 reviews
and
engineering
reviews continued to exist.
Typical examples
included inappropri-
ate evaluation of: condensate
storage
tank capacities
that used incorrect tem-
perature
and did not consider the tap location; the
CST level indication modi-
fication that used
tygon tubing; the spent fuel pool modification and the
block valve replacement
that did not fully establish
the operability and quali-
fication of the
new valves.
A licensee
program to address
these
weaknesses
was
in place at the
end of the
SALP period, but had not yet been evaluated.
Fire Protection activities, previously identified as
a strength,
have
shown
some problems during this assessment
period.
Weaknesses
were identified in
inadequately installed fire barrier wrap, fire door closure
problems, fai lure
to consider
the
need to wrap cable tray supports,
and as mentioned in the Plarit
Operations Analysis.
Another issue
not fully addressed
involves availability
of compensatory
measures
to be taken
on loss of city water supply
on
a loss of
screen
house
and
AC power supply scenario.
On
'h'e positive side,
the licensee
has exhibited initiative in the innovative
redesign of the large
supports
which eliminated the need for 6
of the 8 hydraulic snubbers.
The use of sophisticated
computer
codes to ensure
proper pipe sizing and established
test procedures
to assure
required flows and
~
18
discharge
pressures
demonstrated
good engineering
and planning for the licen-
see's
submittals to
NRR regarding
the modification of recirculation lines for
the
Engineering
has provided significant support for the
installation of a second
station transformer.
Modification packages
from corporate
engineering
do not always get to the plant
within sufficient time to properly plan the activities.
The licensee's
program, for instance,
has suffered
because
of this.
However, with this excep-
tion, outage planning
was
a coordinated
team effort that was competently
directed.
Major modification efforts included the safety injection and resi-
dual
heat
removal recirculation piping upgrade,
turbine trip system
ATWS modi-
fication, offsite power reconfiguration work, steam generator
snubber replace-
ment,
and
blowdown system upgrade.
Considerable
additional
work was also performed concurrent with the major modifications
and included:
inspection
and sleeving,
ten year ISI reactor vessel
inspec-
tion, high and low pressure
turbine overhaul,
primary heat exchanger
inspec-
tions,
and
many maintenance activities.
The licensee recently developed
an-
alytical.basis for prioritizing modifications and other activities; the program
is presently being
used to determine priorities for the next refueling outage.
T'>e licensee's
inspection
and sleeving activities was especially
noteworthy.
The licensee
performed
an inspection of all active tubes in both
to determine
the actual condition of tubes.
The licensee
de-
veloped<a training program for qualification and certification of visual ex-
aminers that exceeds
the
ASME Code requirements,
and includes
hardware
mock-ups
of actual plant equipment,
and implemented effective automation for sleeve in-
sertion
and welding in order to minimize personnel
radiation exposure.
The
reactor pressure
vessel
inspection
was well planned
and it used state of the
art techniques.
The licensee
also
has
an effective erosion-corrosion
control
program.
The effectiveness
of this program was evident in the identification
and replacement of several
components
before problems occurred.
The technical capability and the professional
conduct of the engineering staff
continues to be
a licensee
strength.
Staffing corrective
measures
have
been
instituted.
Management attention
should
be given .to assure effective use of
the staff in performing thorough engineering
evaluations
and reducing the ex-
isting backlog.
A pertinent observation of the
IPAT inspection
was that over-
reliance
on experienced
and qualified personnel
was not adequately
balanced
with programs
and procedures
and that Engigeering is not as proactive
as
needed
to assure
top quality performance.
In conclusion,
improvements
have
been
made in engineering staffing and the
technical capability of the engineering staff continues to be
a strength.
A
1=.i.k of formal communication
from engineering
groups to the operations
group
was evident throughout the modification process for both SI and
AMSAC modifi-
cations during the
1989 refueling outage.
A number of problems
were encoun-
tered during the first half of this
SALP period and
may be attributed in part
to past staffing inadequacies,
weaknesses
in management
over sight and
ineffective use of gA.
The backlog of work projects
remains
high and needs
to
be addressed.
The licensee
has
been aggressive
in correcting
NRC identified
19
issues.
Management
changes
were
made in the later half of the assessment
period and
a more proactive
management
stance
and commitment to assurance
of
quality engineering
support
has
been evident.
III.F.2
Performance
Ratin
- Category 2.
III.F.3
Recommendations:
None.
III.G
Safet
Assessment/ ualit
Verification (202 Hours,
4%)
III.G.I
A~nal sl s
In previous
SALP reports,
Assurance of guality and Licensing Activities were
evaluated
in separate
sections of the report.
This
new section'(Safety
Assess-
ment/guality Verification) has
been created
not only to consolidate
those
two
sections,
but also to encompass
activities
such
as safety reviews,
responses
to
NRC-generated initiatives such
as generic letters, bulletins, information
notices,
and resolution of TMI items.
This section, continues to encompass lic-
ensee
revi,ew activities associated
with licensee
amendment
requests
and Tech-
nical Specification
change.s;
activities related to the resolution of safety
issues;
treatment of unreviewed safety questions;
self-assessment
activities;
analyses
related to industry operational
experience;
root cause
analyses
of
plant events;
and
use of feedback
from plant quality reviews.
This section
provides
a broad
assessment
of the licensee's ability to identify and correct
problems related to nuclear
safety.
This includes
the effectiveness
of the
licensee's
quality verification function in identifying and correcting
sub-
standard
or anomalous
performance
and in monitoring the overall performance
of
the plant.
This constitutes
the first assessment
of this functional area.
For the pre-
vious
SALP report,
Assurance of guality was rated
Category
2 and Licensing Ac-
tivities was -rated Category
1.
During this assessment
period the licensee
made
a
number of changes
to plant
,
programs,
organizational
structure,
and corporate
management
alignments to
better focus
on problem areas identified in previous
SALP periods.
RG&E has
hired
a number of engineering
and professional staff members to augment the
RG&E staff at plant and corporate offices.
In addition goals
and commitment to
safety
have
been
promulgated
by Senior corporate officers.
In response
to identified problems
RG&E strengthened
the, process for making
changes
to the facility in accordance
with the provi sions of 10 CFR 50.59.
RG&E Staff guidance is being rewritten
and major efforts are
underway
on up-
grading "g" Lists and plant drawings.
The
new guidance
has
strengthened
RG&E's
treatment of any unreviewed safety questions with regard to any probability/
consequences
of malfunction of plant equipment
and its respective
margin of
safety.
~
20
In general
the licensee
continued to provide high quality licensing submittals
to the
NRC,
many of which involved complex issues.
The submissions
were. gene-
rally timely, technically sound,
and responses
to requests
for information were
complete.
Examples
include:
responses
to Loss of Decay Heat
Removal Generic
Letter, Inservice Inspection
program,
the Bulletins relating to rapid propagat-
ing fatigue cracks in steam generator
tubes
and potential safety-related
pump
loss.
However,
one notable exception to this performance
was related to the
steam driven Auxiliary Feedwater
(AFW) Pump.
Substantial
NRC involvement was
required to effect appropriate
corrective actions including a change to the
facility Technical Specifications.
Although the licensee
agreed to a conser-
vative operating
philosophy for the
AFW system in December
1988,
a technical
specification
change
supporting this philosophy was not submitted until May
1989.
Midway through the cycle the licensee
made changes
to improve the credibility
and utilization of the quality organizations.
One action
was the creation of a
new position, Director of Quality Assurance/Quality
Control.
The Director of
QA/QC reports to the President
and Chief Operating Officer, and is responsible
for site and corporate quality organizations.
The position was filled by the
former Ginna Outage Coordinator,
an
SRO licensed
engineer with significant
operating experience.
Although the
new Director of QA/QC left
REISE in April
1989 and the position was not filled at the end of the
SALP period,
he com-
pleted
a self-assessment
of the site quality organization.
He also provided
a
plan to<improve quality effectiveness.
Although this was
a positive initi-
ative, to date,
implementation of the quality plan
has lost momentum,
as poor
corrective actions indicating continued
QA department
ineffectiveness
has
been
evidenced
by the .following examples:
Audits of the radiological protection organization,
performed
by the
QA group,
assisted
by the corporate
HP staff,
as discussed
in the Radiological Controls
section, identified weaknesses
during the early part of the
SALP period, but
evidenced
no improvement with respect
to required corrective actions
by the
second audit in September
1988.
Corrective action,
as
a result of NRC security inspections
which identified
four violations,
was delayed
due to the lack of QA management
attention (refer
to Section III.E.1).
Control
and documentation
of receipt,
storage
and handling of materials
and
components
also displayed
some weaknesses.
The, present
documentation
system
does
not appear
able to assure
shelf life is considered
in selection
and
use
of parts
and materials
stored in the stockroom
system.
Significant IST deficiencies
were identified during the period.
The licensee
vigorously pursued
the issue to correct the deficiencies during the refueling
outage to ensure
implementation of an acceptable
program that would meet
NRC
requirements.
The effort by the
RG&E staff produced
a good. IST program
and
developed
a thorough understanding
by the plant and engineering staff of NRC
requirements with regard to IST.
RG&E was
one of the first licensees
to re-
spond to
NRC Generic Letter 89-04, providing
a comprehensive
program for IST.
p
rr
~
21
Although the licensee's
corrective actions
were aggressive,
previous audits
had
not identified the problems
(as discussed
in Maintenance/Surveillance).
During this
SALP period
RG&E took appropriate
action
by their multi-plant ac-
tion (MPA) management
team to closeout
TMI Action Items III.A.1.2 and III.A.2
with regard to the Ginna emergency
response facilities (ERF).
RG&E proposed,
scheduled,
and completed
an upgrade
program for meteorological
measurements
and
analyses.
RG&E installed
a second
100 percent station service transformer
(second
source
of preferred
power)
as
a conservative
action that will increase offsite power
reliability.
The engineering effort for this modification has
been extensive.
During an event in December
1988,
a plant shutdown
was initiated due to freez"
ing of a two steam generator
pressure
sensing lines.
The anticipated
Safety
Injection (SI) activation
was negated
by use of a simulated signal.
The plant
operator's
actions
were appropriate
to the circumstances
as actions were car-
r'ied out
~ after shift supervisory
and shift technical
advisor judgement con"
sidered the safety implications.
In response
to
NRC concerns,
RG&E has pro-
ceduralized
the supervisory
and operator's
actions to ensure that all safety
implications are considered
when
such actions
by the plant operator are taken.
Although management
was very responsive
to the safety implications of this
event;
they failed to assure
adequate
corrective action
was taken after
a
similar>line freezing event which occurred
several
years earlier.
The 1989, Cycle
19 refueling outage
was
a complex outage,
longer than antici-
pated
in which active senior
RG&E management
involvement was observed.
Major
activities at Ginna during the Cycle
19 refueling outage which exemplified
a
high caliber of management
oversight
and technical capability were: ISI exami-
nation of the reactor vessel utilizing new techniques,
sleeving
tubes in the peripheral
sections with newly developed tools and procedures;
modifications to SI
pump recirculation lines;
and implementation of the newly
approved
IST program which required the disassembly
of major valves for inspec-
tion and testing.
However,
some engineering
packages
were not,completed with
sufficient lead time for adequate
ALARA planning.
Inadequate
ALARA planning
resulted
in missed opportunities for total dose
savings during the outage
period.
Also, insufficient post-maintenance
testing of the SI
pump recircu-
lation lines resulted in having to reset
the valve positions after the restart
from the outage.
Also,
a plant trip, caused
by a locked-in; relay from prior
testing,
occurred
as
a result of an inadvertent ASS Mitigation System Actu-
ation Circuitry (AMSAC) initiation.
In response
to
NRC identified weaknesses,
the licensee
developed
several
man-
agement tools to improve plant management
effectiveness.
These include:-a
tracking system for Non-Conformance
Reports
(NCR), the Identified Deficiency
Report (IDR), and
a
new reporting
system for non-safety-related
deficiencies.
A tracking system for IORs similar to the system for NCRs was also developed.
Effectiveness
of these
new tools
has not yet been
assessed.
22
In summary,
changes
were
made in corporate
and plant programs,
management,
and
staffing during this assessment
period which resulted in a significant change
in corporate
philosophy.
However, the heavy reliance
on technically competent
individuals,
has resulted in weak administrative controls,
and continued lack
of effectiveness
of quality organizations
as
a management
tool.
During this
SALP period, senior
management
was actively involved in licensing activities
and technical
issues
which ensure
a high quality of licensee
support perfor-
mance.
III.G.2
Performance
Ratin
- Category 2.
III.G.3
Recommendation:
Licensee:
Meet with the
NRC staff to describe overall approach
to assure
that
quality organizations will be effectively used
as
a management
tool
to assure
safe station operation.
NRC:
None.
~ I)Pi
SUPPORTING
DATA AND SUMMARIES
A.l. Licensee Activities
At the beginning of the assessment
period, the plant was operating at full
power.
On February
5,
1988, while the plant was being
shutdown for the annual
refueling outage,
a reactor trip occurred
due to high counts,
when the source
range detectors
energized.
Faulty connectors
were determined to be the root
cause of the high counts.
Outage activities included refueling, plugging 74
tubes,
repairing
B main
steam isolation valve,
a reactor cool-
ant
pump seal
inspection,
boric acid system piping upgrade,
and emergency
diesel generator
fuel oil system piping modifications.
The plant was started
up on March 9,
1988, but tripped
on March 10,
1988 from 25 percent
power due to
low steam generator
level with a
steam flow-feed flow mismatch.
During the
start-up, operators
experienced
system temperature
control
problems
due to the slightly positive moderator
temperature coefficient.
The plant was returned to power on March 12,
1988,
but
tube
leak forced
a shutdown
on March 14,
1988 from 89 percent
power.
Nine tubes
were plugged during this forced outage.
The plant was returned to power
on
March 24, 1988.
On June
1, 1988, the reactor tripped from full power due to a low steam
gene-
rator level caused
by the
random failure of a feedwater flow transmitter fuse.
A safety injection signal
was generated
due to low pressurizer
pressure.
The
plant was returned to power on June
5,
1988.
A substation
breaker
failure and fire forced
a shutdown
from full power
on July 16,
1988.
The plant
was returned to power
on July 17,
1988.
A turbine runback occurred
on August
25,
1988 when
a power range detector
dropped
rod rod stop bistable failed.
The
plant was stabilized at approximately
70 percent
power and was returned to full
power after the bistable
was replaced.
Two steam generator
pressure
sensing
lines froze
on December
11,
1988 causing
plant personnel
to initiate
a technical
specification required plant shutdown.
Power was reduced to sixty-three percent
before the sensing lines were returned
to operable.
The plant was returned to full power later the
same
day.
Operators
manually tripped the turbine from 48 percent
power
on January
21,
1989 when turbine load was lost during intercept
and reheat
stop valve testing.
Plant power was reduced to repair main condenser
tube leaks.
A short circuit
during the test caused all valves to close
when only one should
have closed
momentarily.
The plant was returned to power the following day.
On February
6,
1989,
a spike in the vital
DC system
caused
a turbine runback.
The plant was stabilized at approximately
72 percent
power and was returned to
full power later the
same day.
The plant was
shutdown for the annual refueling
and maintenance
outage
on March 17,
1989.
SD/D-1
Outage activities included refueling, ten year inservice inspection,
safety
injection system
and residual .heat
removal
system recirculation modifications,
and
tube recovery, consisting partly of peripheral
tube sleev-
ing.
The reactor
was taken critical on May 29,
1989 and operators
attempted to syn-
chronize the generator
to the grid on May 30,
1989.
The generator
breaker
im-
mediately
opened
when closed
and the turbine tripped due to open slide links
at the main transformer."
The generator
was successfully
synchronized
to the
grid on
May 30,
1989, after the links were closed.
A reactor trip occurred
on June
1,
1989 from 53 percent
power due to
a turbine
trip.
The turbine tripped due to an unanticipated
actuation of the
ATWS Miti-
gation System Actuation Circuitry (AMSAC).
A.2. Direct Ins ection
and Review Activities
Two
NRC resident
inspectors
were assigned
to the site throughout the assessment
period.
The total inspection time for the assessment
period was 4859 hours0.0562 days <br />1.35 hours <br />0.00803 weeks <br />0.00185 months <br />
(resident
and region based) with a distribution in the appraisal
functional
area
as
shown with each functional area.
This equates
to 3241 hours0.0375 days <br />0.9 hours <br />0.00536 weeks <br />0.00123 months <br />
on
an an-
nual basis.
Special!inspections
included the following:
Refueling outage
team inspection to assess
readiness
for restart
(February
22-26.
19889).
Special
team inspection to assess
the adequacy
and verify adherence
to
regulatory requirements
and license
commitments for the implementation of
the IST program
(May 16-20,
1988).
Special
inspection of June
1,
1988 reactor trip with complications
(June
1-4, 1988).
Integrated
Performance
Assessment
Team Inspection
(September
8-22,
1988).
The annual
emergency
preparedness
exercise
was held
on October
19,
1988.
Special
inspection to assess
the safety significance of the December ll,
1988
frozen pressure
sensing
lines
(December
11-21,
1988).
B.
Criteria
Licensee
performance
is assessed
in selected
functional areas,
depending
on
whether the facil.ity is in a construction,
preoperational,
or operating
phase.
Each functional area
normally represents
areas significant to nuclea~ safety
and the environment,
and are
normal
programmatic
areas.
Special
areas
may be
added to highlight significant observations.
SD/D-2
The following evaluation criteria,
where appropriate,
were used to assess
each
functional area:
l.
Assurance of quality, including management
involvement and control;
2.
Approach to resolution of technical
issues
from a safety standpoint;
3.
Responsiveness
to
NRC initiatives;
4.
Enforcement history;
5.
Operational
events (including response
to, analyses
of, reporting of and
corrective actions for)
6.
Staffing (including management),
and
7.
Effectiveness of training and qualification program.
On the basis of the
NRC assessment,
each functional area evaluated is rated
according to three
performance
categories.
The definitions of these
perform-
ance categories
are
as follows:
~Cate or
1.
Licensee
management
attention
and involvement are readily evident
and place
emphasis
on superior performance
of nuclear safety or safeguards
ac-
tivities, with the resulting performance substantially
exceeding
regulatory
requirements.
Licensee
resources
are
ample
and effectively used
so that
a high
level of plant and personnel
performance
is being achieved.
Reduced
NRC at-
tention
may be appropriate.
~Cate or
2.
Licensee
management
attention to and involvement in the perform-
ance of nuclear safety or safeguards
is good.
The licensee
has attained
a
level of performance
above that needed
to meet regulatory requirements.
Lic-
ensee
resources
are
adequate
and reasonably
allocated
so that good plant and
personnel
performance
is being achieved.
NRC attention
may be maintained at
normal
levels'atecaCorr
3
Licens.ee
management
attention to and involvement in the perform-
ance of nuclear safety or safeguards
activities are not sufficient.
The lic-
ensee's
performance
does
not significantly exceed that needed to meet minimal
regulatory requirements.
Licensee
resources
appear to be strained or not ef-
fectively used.
NRC attention
should
be increased
above
normal levels.
The
SALP Board may assess
a functional area to compare
the licensee's
perform-
ance during the last quarter of the assessment
period to that during the entire
period in order to determine the recent', trend.
The
SALP trend categories
are
as follows:
The trend, if used,
is defined as:
~Im rovin
Licensee
performance
was determined
to
be improving near the close
.
of the assessment
period.
~geclinin
Licensee
performance
was determined to be declining near the close
of the assessment
period and. the licensee
had not taken mean'ingful
steps
to
address
this pattern.
A trend is assigned
only when, in the opinion of the
SALP Board,
the trend is
significant enough to be considered
indicative of a likely change
in the per-
formance'category
in the near. future.
For example,
a classification of "Cate-
gory 2, Improving" indicates
the clear potential for "Category I" performance
in the next
SALP period.
It should
be noted that Category
3 performance,
the lowest category,
represent
acceptable,
although minimally adequate,
safety performance.
If at any time
the
NRC concluded that
a licensee
was not achieving
an adequate
level of safety
performance, it would then
be incumbent
upon
NRC to take prompt appropriate
action in the interest of public health
and safety.
Such matters
would be
dealt with independently
from, and
on
a more urgent
schedule
than,
the
process.
It should also
be noted that the industry continues
to be subject to rising
performance
expectations.
NRC expects
licensees
to use industry-wide and
plant-specific operating
experience
actively in order to effect performance
improvement.
Thus,
a licensee's
safety performance
would be expected
to show
improvement over the years
in order to maintain consistent
SALP ratings.
C.
Un lanned
Shutdowns
Plant Tri
s and Forced Outa
es
Power
Root
Functional
Date
,
Leve1
Cause
Area
Descri tion
2/5/88
OX
Personnel
Error
Maintenance/
Surveillance
A reactor trip occurred
on Source
Range
Hi Flux
during
a planned shut-
down for the annual
re-
fueling outage.
The
source
range instruments
reenergized
prematurely
as
a result of connec-
tors apparently
damaged
during previous mainten-
ance activities.
3/10/88
25K
Personnel
Error
Operations
A reactor trip occurred,
during plant start-up,
on low steam generator
level coincident with
steam flow-feed flow
mismatch.
A lack of
operator training 'with
positive moderator
tem-
perature coefficient
caused
system temperature
and
level
control problems.
SD/D-4
Date
Power
Level
Root
Cause
Functional
Area
Descri tion
3/14/88
89
Personnel
Error
Maintenance/
Surveillance
tube leak
).1
gpm forced plant shut-
down.
The licensee failed
to correctly identify a de-
fect in the leaking tube
during
Eddy Current data
analysis
performed during
the refueling outage.
6/1/88
100K
7/16/88
100%
1/21/89
48K
Component Failure
Maintenance/
Surveillance
Component Failure
Maintenance/
Survei'.lance
Component Failure
N/A
A reactor trip occurred
on
low steam generator
level
coincident with steam flow-
feed flow mismatch.
A fuse
in the controlling feed flow
channel
power supply blew
causing
feed flow and
steam
generator
level swings.
A
safety injection signal
was
caused
by operators
over-
feeding the
causing reactor coolant sys-
tem pressure
to drop.
A breaker
bushing failure
in the plant's
main sub-
station
caused
a loss of
normal offsite power.
The
bushing's oil level
was broken
and oil level
decreased
causing internal
arcing
and subsequent
bushing failure.
The plant
was
shutdown to effect re-
pairs to the substation.
While repairing main con-
denser
tube leaks,
opera-
tors manually tripped the
turbine when load was lost
during testing of the inter-
cept
and reheat
stop .valves.
A short circuit caused all
valves to close
when only
one should
have closed
momentarily.
The rector
was taken subcritical to
effect repairs to the
turbine control
system.
Date
Power
Level
Root
Cause
Functional
Area
Descri tion
6/I/89
53%
Personnel
Error
Engineering/
Tech Support
A reactor trip occurred
on
a turbine trip due to
actuation of AMSAC.
Operators
unblocked
AMSAC without first
totally resetting
the
system.
A procedural
inadequacy
resulted
from
a deficiency in the
training material
sup-
plied by engineering for
the modification.
D.
Enforcement Activit
Functional
No. of Violations in Ea"h Severity Level
V
IV
III
II
I
Total
A.
Plant Operations
1
4
B.
Radiological Controls
2
4
C.
Maintenance/Survei
1 1 ance
1
P
D.
Emergency
Prepar edness
E.
Security
1
1
F.
Engineering/Technical
Support
1
1
G.
Safety Assessment/guality
1
Verification
H.
Other
Total
6
20
1
27
SD/D-6
E.
Ins ection
Hour
Summar
Functional
Area
Plant Operations
Radiological Controls
Maintenance/Surveillance
Emergency
Preparedness
Security
Engineering/Technical
Support
Safety Assessment/equality
Yerification
Other
Actual
2517
229
802
103
187
311
202
508
Annualized
Hours
1678
153
535
69
125
207
135
339
Percent
52
17
10
TOTAL
4859
3241
100
SD/0-7
F.
Licensee
Event
Re ort Casual
Anal sis
Functional
Area
Number By Cause
Code
A
8
C
0
E
X
Total
Plant Operations
Radiological Controls
Maintenance/Surveillance
Emergency
Preparedness,
1
1
Security
Engineering/Technical
Support
Safety Assessment/guality
Verification
Other
4
4
Totals
4
2
1
6
13
Cause
Codes
A - Personnel
Error
8 - Design, Manufacturing,
Construction or Installation Error
C External
Cause
0 - Defective Procedures
E - Component Failure
X - Other
SD/0-8