ML17229A506

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Insp Repts 50-335/97-10 & 50-389/97-10 on 970727-0906. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support
ML17229A506
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 10/06/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17229A504 List:
References
50-335-97-10, 50-389-97-10, NUDOCS 9710230026
Download: ML17229A506 (67)


See also: IR 05000335/1997010

Text

U.S.

NUCLEAR REGULATORY COHHISSION

REGION II

Docket Nos: 50-335,

50-389

License

Nos:

DPR-67,

NPF-16

Report

Nos: 50-335/97-10,

50-389/97-10

Licensee:

Florida Power

Im Light Co.

Facility:

St. Lucie Nuclear Plant.

Units

1

& 2

Location:

6351 South

Ocean Drive

Jensen

Beach,

FL

34957

Dates:

July 27 - September

6

~

1997

Inspectors:

H. Hiller. Senior Resident

Inspector

J.

Munday, Resident

Inspector

D. Lanyi, Resident

Inspector

M. Thomas,

Regional

Inspector

(Sections

E7. 1.

E8. 1,

and E8.2)

.

S. Ninh, Project Engineer

(Sections

08. 1, 08.2. 08.3.

~

08.4,

and 08.5)

Approved by:

K. Landis. Chief. Reactor Projects

Branch

3

Division of Reactor Projects

97i0230026 97i006

PDR

ADQCK 05000335

8

PDH

EXECUTIVE SUMMARY

St. Lucie Nuclear Plant, Units

1 5 2

NRC Inspection Report 50-335/97-10,

50-389/97-10

This integrated

inspection included aspects

of licensee operations'ngineer-

ing, maintenance,

and plant support.

The report covers

a 6-week period of

resident inspection;

in addition, it includes the results of region based

inspections

in the areas of engineering

and operations.

~Ocr ati ons

Actions taken by operators to terminate

a reactor

power increase,

experienced

while placing

a Chemical

and Volume Control System ion

exchanger'in

service,

were swift and correct.

The proper level of

attention

was afforded this critical evolution.

(Section 01.2)

A leaking condenser

tube was identified quickly by Chemistry personnel.

Actions taken to minimize'the event were timely and in accordance

with

applicable plant procedures.

(Section 01.3)

An Auxiliary Feedwater

System periodic surveillance

was performed

satisfactorily with no discrepancies

rioted.

(Section 01.4)

Operator

response

to a dropped Control

Element Assembly during testing

was professional.

The inspector

noted good communications

between

Operations

and Reactor Engineering.

The management

decision to de1ay

the test until Xenon conditions were stabilized

was both appropriate

and

conservative.

(Section 01.5)

A routine walkdown of the control

room ventilation system revealed only

minor deficiencies.

The inspector

found the response

and corrective

actions for a refrigerant leak adequate.

(Section 02. 1)

Although the procedure

upgrade

program was found to be on schedule.

the

volume of.procedures

remaining will present

a challenge to the licensee.

The prioritization of procedure

revisions

was appropriate.

(Section

03.1)

A non-cited violation was identified for failure to revise a.Quality

Instruction after the Nuclear Watch Engineer position was determined to

be optional.

(Section 03.1)

Overall. site procedures

were found to be adequate

to perform their

intended functions, availability of current revisions

was good,

and the

procedures

were usable, particularly the upgraded

versions.

As an

example,

although the licensee

had issued only a small percentage

of

upgraded

Annunciator Response

Procedures,

the inspector

noted that they

were

a significant improvement over the older versions.

(Section 03. 1)

The inspector

noted that an operator aligning the Gas

Decay Tank system

was careful

and methodical

in performing the evolution.

Although the

operator misread

one step,

overall procedural

adherence

was good.

(Section 04. 1)

Maintenance

The

1B ion exchanger

resin was discharged

according to procedure with no

major problems

noted by the inspector.

Good coordination

was noted

between the groups involved in the activity. (Section Ml. 1)

The experience

and knowledge of the technicians calibrating

2A High

Pressure

Safety Injection discharge

pressure

instrument resulted in

timely repair of a unique problem.

(Section M1.2)

The simultaneous

performance of maintenance

and surveillance

was

considered

a strength in reducing unnecessary

starts

and periods of

inoperability of the

2B diesel

generator.

(Section Hl.3)

The 2A charging

pump accumulators

were charged properly in accordance

with site procedures.

(Section H1.4)

The inspector

noted the technicians

were knowledgeable

about both the

equipment

and the procedures

being used during Reactor Protection

System

survei llances.

(Section Hl.6)

Although plant cleanliness

was generally acceptable,

more attention

was

warranted.

(Section

M2. 1)

~

A Quality Assurance audit on

Gai -tronics system problems

was well

performed.

The conclusions

were well founded

and the recommendations

were appropriate.

The inspector

concluded that the licensee's

response

to QA audit findings was proper,

and the programs in place should

maintain the Gai-tronic system acceptably.

(Section

M7. 1)

The inspector

concluded that the licensee

was actively and methodically

working to locate

and isolate

OC grounds

associated

with a nuisance

alarm.

(Section

H8. 1)

~E

Quality Assurance

audits

and assessments.

and the Site Engineering self

assessment

efforts were effective in providing oversight of Engineering

activities

and identifying areas for improvement

and increased

management

attention.

(Section

E7. 1)

The findings identified by the licensee during the UFSAR/Procedure

'onsistency

Review were documented.

processed,

and being tracked in

accordance

with the licensee's

corrective action program

and

NRC

regulations.

(Section

E8. 1)

The inspector

concluded that, for the condition reports

reviewed, Site

Engineering generally provided acceptable

responses

to address

the

concerns identified in the applicable condition reports.

(Section

E8.2)

3

~

A violation was identified for failure to update the

UFSAR with the

latest information developed to describe the design basis.

Enforcement

discretion

was granted for three

examples of UFSAR descrepancies

that

would more than likely have been identified by the license's

UFSAR

review program.

An NCV was identified for these

examples.

(Section

E8.3)

The inspector's

review of issues

surrounding the containment radiation

monitors identified potential deficiencies

associated

with the design

basis.

as defined by calculation, operability of the system,

UFSAR

inaccuracies.

and timeliness of completing design basis calculations.

An Unresolved

Item was opened

pending further review of these

issues.

(Section

E8.3)

1

Plant

Su

ort

Although several

DC emergency lights were noted to need replacement,

work had

been planned

and replacement

batteries

were on order.

The

Preventative

Maintenance

program for the

DC emergency lighting system

was found to be adequate

to detect

any problems with the lights within

approximately

one month of fai lure.

(Section

FZ. 1)

With two exceptions,

the inspector

found the fire suppression

system

properly aligned

and maintained.

A pump discharge

pipe support

was

found not supporting the pipe and

a recently repai red check valve was

left uncoated

and exposed to the environment.

Other minor deficiencies

were noted

and corrected or planned to be corrected.

(Section F2.2)

Summar

of Plant Status

Re ort Details

Unit

1 entered the period at approximately

90 percent

power following recovery

from a condenser

tube leak.

On July 27. the unit experienced

a reacti vity

transient during power ascension

due to inadequate

flushing of a Chemical

and

Volume Control System

Ion Exchanger.

The next day,

power was reduced to about

90 percent

due to

a dropped Control

Element Assembly

(CEA).

The unit was

returned to full power early on July 29.

The unit experienced

one other

dropped

CEA on August 21.

Power was reduced to 88 percent for a short time to

allow for recovery.

The unit remained at full power for the remainder of the

period.

Unit 2 remained essentially at full power for the entire period.

I. 0 erations

01

,

Conduct of Operations

01.1

General

Comments

71707

Using Inspection

Procedure

71707, the inspectors

conducted

frequent

reviews of ongoing plant operations.

In general: the conduct of opera-

tions was professional

and safety-conscious;

specific events

and

noteworthy observations

are detailed

in the sections

below.

01.2

Unit

1 Reactivit

Increase

When Placin

Ion Exchan er In Service

71707

a.

Ins ection Sco

e

C

On July 27, reactor

power increased

2 percent

and Reactor

Coolant System

(RCS) cold leg temperature

increased

2.5

F after the

1A Chemical

Volume

and Control System

(CVCS) Ion Exchanger (IX), was placed in service.

The inspectors

reviewed Condition Report

(CR) 97-1492 which documented

the event;

as well as the procedures

used during the evolution.

b.

Observations

and Findin s

On July 25, the resin in the

1A IN was replaced.

On July 25 and 26,

steps

were taken to equalize the boron concentration of the

IN with the

RCS,

a process

known as "rinsing in."

This was accomplished

by simply

routing

RCS fluid through the

IX allowing the boron to be deposited

in

the resin.

Because

the boron concentration of the

RCS fluid leaving the

IX was reduced,

the effluent was routed to a holding tank rather than

returned to the

RCS.

This cycle is repeated until the

IN effluent boron

concentration is within 25 parts per million (ppm) of RCS concentration.

On July 26, approximately

1700 gallons of RCS fluid was diverted through

the IX. and

a chemistry sample taken at 2:00 p.m. indicated

a final

boron concentration of 655 ppm.

At 3:32 a.m.

~ on July 27. the rinsing

in process

was again

begun.

The initial boron concentration

sample

indicated

233 ppm, which was thought to be in error,

based

on the

previous

sample results.

A second

sample

was drawn which indicated the

concentration

was

633 ppm.

At 5:02 a.m.,

another rinse of the

IX was

performed with the resulting boron concentration

indicating

721

ppm.

RCS boron concentration

at that time was

717

ppm so the decision

was

made to place the

IX in service.

This was completed

by 5:45 a.m..

Because

small uncertainties

in the boron sample analysis

can result in

small reactivity changes'perators

anticipated

having to make

corrections

as necessary.

Additionally. the reactivity change, if one

occurred,

would not occur immediately because

the

IX effluent is

directed first to the Volume Control Tank

(VCT) prior to being

pumped to

the reactor.

At 6:ll a.m.,

the board operator

added

10 gallons of boric

acid and

20 gallons of water to the suction of the charging

pumps to

counteract

a slowly increasing

RCS temperature.

At 6:25 a.m., the

IX

was bypassed

when the

RCS temperature

continued to rise.

RCS

temperature

increased

2.5

F from 546 to 548.5

F.

Reactor

power

increased

2 percent

from 87 percent to 89 percent.

Operations

then

added additional boric acid to reduce

RCS temperature

to the pre-event

values.

The licensee

immediately initiated an Event Response

Team (ERT)'to

determine the root cause

and provide corrective actions.

The team

concluded the root cause

was that the samples

were actually taken

when

the

IX was bypassed.

This resulted in sampling reactor coolant rather

than

IX effluent.

-This occurred

because

the operating

procedure

controlling the evolution,

OP 1-0210020,

Revision 43,

"Charging and

Letdown

- Normal Operation," did not provide enough detail to adequately

coordinate the operation of the system

and the drawing of the sample.

As corrective action, the licensee

generated

temporary

changes

(TC) to

both units operating

procedures

to add additional

steps to better

coordinate the activity.

These

changes

were documented

in TC 1-97-071

for Procedure

OP 1-0210020

and 2-97-136 for 2-0210020.

The licensee

followed up the TCs with a permanent

change to the

same procedures.

The inspector

reviewed the event

and discussed

the details with the

involved personnel

and considered

the licensee's

root cause to be

accurate.

~ The procedure

revisions were reviewed

and were determined to

provide enough detai l to adequately

control this evolution.

Conclusions

The inspector

concluded that the actions taken

by the operators to

terminate this event were swift and correct.

The proper level of

attention

was being placed

on the evolution during this critical time.

The revision made to the appropriate operating

procedures

should prevent

this event from occurring again.

Unit

1

Down ower Oue to Condenser

Tube Leak

71707

Ins ection

Sco

e

On July 26, Unit 1 experienced

a condenser

tube leak which resulted in a

manual

power decrease

to approximately

75 percent.

The inspector

reviewed

CR 97-1490 which was written to document the event

and

determine corrective actions.

In additions

the inspector discussed

the

01.4

event with various Operations

and Chemistry personnel.

The inspector

also reviewed Off-Normal Operating

Procedure

ONOP-1-0610030.

Revision

13 'Secondary

Chemistry-Offnormal."

Observations

and Findin s

On July 26, at approximately 6:45 a.m.,

Chemistry personnel

notified the

Nuclear Plant Supervisor

(NPS) that Steam Generator

(SG) cation

conductivity was 0.4 umho/cm on both

SGs

and increasing.

Procedure

ONOP

1-0610030

was entered

and

SG blowdown was increased.

The

ONOP indicated

that the plant was initially in an Action Level

1 condition which

allowed one week to reach

normal chemistry values.

Shortly thereafter,

Chemistry reported that the analysis

indicated the conductivity increase

was due to sea water intrusion.

Operations

commenced

reducing reactor

power at 7:37 a.m. to remove the suspect

181 waterbox from service.

However, at 8:05 a.m., Action Level

2 was reached

when conductivity

exceeded

2 umhos/cm,

and

a power reduction to less than

30 percent

within four'ours

was

commenced

in accordance

with the

ONOP.

At 8:10

a.m., the

181 Circulating Water

pump was secured

which terminated the

sea water inleakage.

By 8:30 a.m.,

waterbox conductivities were

decreasing

and

SG conductivities

had stabilized.

By 9:00 a.m., the

SG

conductivities

began to decrease.

A clearance

was

hung on the waterbox

for maintenance

to commence work.

The power decrease

was halted at 75

percent.

Maintenance

personnel

searched

for the tube leak using helium and

a

helium detector but were not successful.

However,

four plugs were noted

to be missing when comparisons

were made with the waterbox tube plugging

map.

The missing plugs were replaced

and the plant was brought back to

100 percent

power.

Secondary plant conductivities

remained within

normal

range.

Conclusions

The leaking condenser

tube was identified quickly by Chemistry

personnel.

Actions taken were timely and in accordance

with applicable

plant procedures.

Unit 2 Auxiliar

Feedwater

AFW

Periodic Test

61726

Ins ection

Sco

e

~ The inspector witnessed

the performance of Procedure

OP 2-0700050,

Revision

48 'Auxiliary Feedwater

Periodic Test."

Observations

and Findin s

The inspector

attended

the pre-job brief and observed portions of the

surveillance

in both the main control

room and locally at the pump.

The

procedure

was verified to be of'he current revisions

the Measuring

and

Test Equipment

(%TE) was within its calibration due dates,

and the

operators

were qualified to perform the task.

No discrepancies

were

identified dur ing the performance of this activity.

Conclusi ons

The surveillance

was performed satisfactorily with no discrepancies

noted.

Dro

ed Control

Element

Assembl

93702

Ins ection

Sco

e

On August 21, the inspector

responded to the Unit

1 control

room in

response

to

a dropped

CEA during Full Length,CEA testing.

The inspector

observed

the rod recovery

and subsequent

power ascension.

Observations

and Findin s

At 8:45 a.m..

on August 21, Unit

1 experienced

a dropped

CEA (A-47)

during Full Length

CEA Testing per Procedure

OP 1-0110050,

Revision 35,

"Control Element Assembly Periodic Exercise."

The operators

responded

immediately in accordance

with Off-Normal Operating

Procedure

ONOP 1-

0110030,

Revision 38,

"CEA Off-Normal Operation

and Realignment."

The

operators

reduced

power to approximately

88 percent.

This dropped

rod

was different from most since it was

a dual

rod shutdown

CEA positioned

near the

"D" linear power range nuclear instrument (NI).

This caused

a

large rod shadow

on that NI, and

a large axial flux shape variation.

In

fact, the large

power shift caused

the operators

some minor problems

maintaining the opposite side T in the normal

band.

18C personnel

quickly determined that

a power switch had failed,

allowing the

CEA to drop.

By 9:05 a.m.,

18C had repaired the problem

and Operations

had verified CEA operability.

Operators

had fully

withdrawn .the rod by 9:25 a.m.

The Operations staff acted

professionally throughout the event.

The

NPS and Assistant

Nuclear

Plant Supervisor

(ANPS) minimized extraneous

control

room activity

during the recovery.

The inspector

noted

good communications

between

Operation

and Reactor

Engineering

(RE).

RE support

was appropriate

and

timely.

The inspector noted that the recovery to full power 'was

deliberate to al'low core power to equalize.

The conservative

management

decision to delay the Full Length

CEA test for twenty-four hours

was

appropriate.

Conclusions

Operator

response

to a dropped

CEA during testing

was professional.

The

inspector

noted

good communications

between

Operations

and

RE.

The

management

decision to delay the test

a day after

CEA recovery

was both

appropriate

and conservative.

V

02

02.1

Oper ational Status of Facilities

and Equipment

Walkdown of Control

Room Ventilation

71707

Ins ection

Sco

e

The inspector

performed

a routine walkdown of both units'ontrol

room

air conditioning systems.

In additions

the inspector followed up on

maintenance

associated

with a refrigerant leak that occurred

on the Unit

2 3A air conditioning unit.

Observations

and Findin s

The inspector

used

Drawings 2998-G-879

SH 2, Revision

16 and 8770-G-852,

Revision .22 to perform

a system walkdown of the air conditioning

systems.

Also, Procedures

1-1900020,

Revision 12,

"Reactor Auxiliary

and Control

Room Ventilation Operation,"

and 2-1900020, Revision'0.

"Reactor Auxiliary and Control

Room Ventilation Operation," were

reviewed by the inspector to verify system line up.

The inspector

found

only minor drawing discrepancies

that had already

been identified to the

system engineer.

In May, Maintenance

noticed that the Unit 2 air conditioning unit

2HVA/ACC-3A had

a pinhole leak at the shell side threaded inlet fitting

of the water cooled condenser.

A Condition Report

(CR 97-1044)

was

written identifying that

27 pounds of refrigerant

had been

added

and

identifying the apparent

location of the leak.

By the middle of June,

Engineering dispositioned the

CR by identifying the repai r.

At that

point. the work was placed

on the Plan of the

Day

(POD) to be worked in

July.

The licensee started

a surveillance

run of the Unit 2 3A air

conditioner

on the evening of July 4.

Within a few hours, the

ANPS

determined that the unit was not cooling properly, declared

the unit

inoperable,

and generated

a high priority work request to repai r the

unit.

The repai rs were completed July 5 with 60 pounds of refrigerant

added.

On July 22, Maintenance

evacuated

the Unit 2 3A air conditioner to

repair the leak.

They verified the system pressure

gages

and the

pumping unit pressure

gages

showed that no more refrigerant

was present.

They then unbolted

a solenoid valve bonnet

and refrigerant

gas

escaped

into the ventilation room.

All personnel

were evacuated

from the

ventilation room, located directly behind the control

room.

The doors

from the control

room were opened to vent the control

room and vent room

areas.

The causes

of the event were determined to be the following:

A lack of procedural

guidance.

The licensee

considered

evacuating

refrigerant within the skill of the craft and

no detailed

procedure existed.

Inadequate

Maintenance training.

The crew that performed this

work activity had been recently certified to service air

conditioning units.

The training was inadequate

as it did not

include site specific information about the air conditioning

units.

Inadequate

information in the work package.

The work package

did

not include the schematic

drawing of the equipment

layout that

would have

shown the craft that

a check valve between the

condenser

heat exchanger

and the closed solenoid valve was

installed which prevented

the reclamation 'of refrigerant in the

lines.

Short term corrective actions

included adding guidance to the generic

air conditioning work order to ensure

evacuation of all piping.

Long

term corrective actions

included development of a procedure to control

all air conditioning maintenance.

Maintenance

also completed

repai r of

the leak and restored

the unit to operation.

c.

Conclusions

The inspector

found only minor deficiencies

in the control

room

ventilation system.

The system engineer

was already

aware of these

problems.

The inspector

found the response

and corrective actions to

the refrigerant leak adequate.

03

Operations

Procedures

and Documentation

03. 1

Procedure

Review

42700

a.

Ins ection

Sco

e

The inspector

reviewed the licensee's

procedures

for developing,

implementing.

and revising plant procedures.

Also, the inspector

evaluated

the licensee's

procedure

upgrade

program,

procedure

change

backlog,

and library maintenance.

Finally, the inspector

surveyed

a

sample of.Administrative, Operations,

Maintenance,

Chemistry,

and Health

Physics

procedures

for usability, accuracy,

and conformance with the

site Writer's Guide.

b.

Observations

and Findin s

The inspector

reviewed the following:

Both units'echnical

Specification

(TS) Sections

6.5 and 6.8

The Topical Quality Assurance

Report

(TQAR) Section 5.0. Revision

12. "Instructions,

Procedures,

and Drawings"

Quality Instruction QI 5-PSL-1,

Revision 2, "Preparation,

Revision,

Review/Approval of Procedures"

Quality Instruction'I 5-PR/PSL-3,

Revision

14, "Verification

Guide for Emergency Operating

Procedures"

Quality Instruction QI 6-PR/PSL-1.

Revision 32,

"Document Control"

Procedure

ADM 11.02,

Revision 0, "St. Lucie Procedure Writer'

Guide"

Procedure

ADM 11.03,

Revision 1,

"Temporary Change to Procedures"

The inspector also conducted

interviews with several

procedure writers,

their management,

and procedure

users to determine the overall

effectiveness

of the St. Lucie procedure

program.

Several

years

ago the licensee identified that its procedures

being used

in the field were less than adequate.

Sufficient detail

was lacking to

ensure that minimally qualified personnel

could perform

a task in a

repeatable

and acceptable

way.

About two years

ago the licensee

began

a

procedure

upgrade

program designed to improve and standardize all plant

procedures

by the year 2000.

At the end of this report period, the

inspector estimated that approximately

15 percent of the upgraded

procedures

had been

issued with another five percent

nearing completion.

The licensee

had not yet identified what the final population of

procedures

would be.

One Procedure Writer noted that

some procedures

would be combined while others would be subdivided into separate

procedures. 'herefore.

a final count would be difficult to ascertain.

Based

upon the information provided by the Procedures

Group supervision,

the inspector estimated that about thi rty-six hundred procedures still

required

a significant amount of work prior to being issued.

This

number included

2350 Annunciator Response

Procedures

(ARPs).

The

licensee

acknowledged that their resources

were less than adequate.

The

large number of procedures

to upgrade

by the end of 1999 combined

with'he

"normal" duties of revising and reissuing

procedures,

posed

a large

challenge to the Procedures

Group with its limi.ted resources.

The St. Lucie site maintained

two main libraries,

one in the South

Service Building

(SSB)

and the other in the North Service Building.

The

Technical

Support Center

(TSC),

and both libraries all have

a complete

set of controlled procedures.

Several satellite areas

also have

controlled copies.

For example,

the diesel

generator

rooms

have

portions of controlled Off-Normal Operating

Procedures

(ONOPs). the hot

shutdown panel

rooms

have controlled copies of the

ONOPs

and Emergency

Operating

Procedures

(EOPs),

and the maintenance

area of the D-13

building had

some controlled procedures.

Each library location

contained

"For Information Only" procedure title lists.

However.

according to Quality Instruction QI 6-PR/PSL-1,

Revision 32,

"Document

Control," Section 4.5, the user

was to verify controlled copies

by using

the on-line Passport

D150 panel.

The inspector verified that the diesel

room procedures

and the hot shutdown

panel

room procedures

were the

current revision and ensured that

a sample of the D-13 procedures

was

current.

The inspector

noted

no discrepancies.

The inspector

randomly

verified twelve operations

and administrative procedures

in both control

rooms.

No deficiencies

were noted.

The inspector

randomly selected

52

procedures

from all disciplines

and verified that they were current in

the two main libraries.

The inspector

found one deficiency that the

licensee concurrently identified.

Maintenance

Procedure

MP-0940061,

Revision 22,

"Maintenance of Thermal Overload Devices," still existed in

the

SSB files although

EMP-100.01,

Revision 0,

"Maintenance of Thermal

Overload Devices."

had superseded it in March.

The licensee identified

the problem in Condition Report 97-1651.

The inspector

reviewed fifteen procedures

from various disciplines:

Operations,

Administrative, Maintenance.

Health Physics

(HP).

and

Chemistry.

These included both upgraded

and non-upgraded

procedures.

Overall, the inspector

noted that the upgraded

procedures

were more

uniform in appearance

than the non-upgraded

versions.

However the

HP

and Chemistry upgraded

procedures

routinely departed

from the Writer'

Guide recommendations.

All non-upgraded

procedures

reviewed

had been

revised within the past year for either clarity, technical

content or

both.,

The inspector

compared the procedural

steps to the plant

configuration,

where applicable.

and determined that the procedures

would accomplish their intended function and were usable.

The inspector

concluded that the format of the upgraded

procedures

was improved but

technical

content

was comparable to the non-upgraded

procedures.

However, the consistent

use of nomenclature

and format did make the

procedures

more usable.

During the review, the inspectors

observed

one discrepancy.

On August

5

~ the inspector

found that procedure

QI 1-PR/PSL-2,

Revision 32,

"Operations Organization," still described

the Nuclear Watch Engineer

(NWE) as required for minimum crew manning.

Since mid-June,

the

licensee

had allowed the

NWE position to remain

unmanned

as

a temporary

response to Violation 50-335,389/97-04-02,

"Routine Use of Heavy

Operator Overtime."

The licensee identified the needed

revision on June

19 and started the procedure

change

process.

Because

Procedure

ADM

11.03 'evision

1

~

"Temporary Change to Procedures."

did not permit QI's

to be processed

as temporary changes,

the licensee

was forced to perform

a normal procedure revision.

The revised procedure

was approved

by the

Facility Review Group and signed

by the Plant General

Manager

on July

14.

On August 5,

Document Control issued the procedure.

putting it into

effect.

The Operations Assistant Supervisor stated that

he did not

place

a higher priority on the change

because

he did not believe that it

was warranted.

His primary focus

was to get the procedures

that were

used regularly changed.

He understood that the operations staff rarely

read

QI 1-PR/PSL-2

and did not affect the routine of the Operations

Department.

Section 4.2 of Procedure

QI 1-PR/PSL-2,

Revision 32, stated,

"The

Operations

group consists of five (5) or more shifts with a Nuclear

Plant Supervisor

in charge of each shift.

Each shift consists of the

required

operators

discussed

in Section 5.2 of this procedure."

Section

5.2.5 stated that

a Nuclear Watch Engineer

was

a requi red position to be

manned.

The licensee routinely left the

NWE position unmanned

since

June 9.

For both units, Technical Specification 6.8. l.a requi red that

procedures

recommended

in Appendix A of Regulatory Guide 1.33,

Revision

2, including minimum shift staffing,

be maintained

and followed.

This

failure constitutes

a failure of minor significance,

and is being

treated

as

a Non-Cited Violations consistent with Section

IV of the

NRC

Enforcement

Manual,

NCV 50-335,389/97-10-01 'Failure to Update

a

Procedure."

The inspector also noted that the licensee

issued the first set of ARPs

in the Unit 1 control

room.

Each annunciator

panel still had

a response

procedure

book associated

with it.

Each

book now contained

a specific,

one-page

response

procedure for each annunciator

window.

This was

a

significant improvement over the old ARPs.

Operators

stated that the

new procedures

were more useable

and accurate

than the old procedures.

They liked the ability to revise

a single annunciator

response

without

revising the entire book.

A brief audit of the Controlled Wiring

Diagram

(CWD) references

by the inspector

revealed

a significant

improvement in their accuracy.

Of the ten

ARPs reviewed,

the inspector

found no deficiencies

in the references.

The licensee

scheduled

the

ARP

upgrade for completion by December

1998.

The inspector

reviewed the procedure revision process.

The licensee

could change their procedures

in two ways.

The simplest

method

was

a

temporary change.

As described

in Procedure

ADH 11.03.

Revision

1,

"Temporary Changes to Procedures,"

personnel

should generate

a

TC when

they could not perform 'a procedure

as written and time constraints

would

not allow revision via the normal procedure

change

process.

The

procedure

change

could not change the intent of the original procedure.

requi re

a Facility Review Group

(FRG) review. or was not

a Quality

Instruction,

Emergency

Plan Implementing Procedure,

or an Emergency

Operating

Procedure.

Furthermore the procedure

required the following:

A qualified reviewer perform

a

10 CFR 50.59 screening

on the

TC

A member of plant management staff review the procedure

change to

determine if a cross-disciplinary

review was required

A member of plant management staff verification that no change of

intent was involved

A member of plant management staff verification of technical

adequacy

Another member of plant management staff to review the forms and

determine the need for a

FRG

Technical Specification 6.8 also requi red the review by two members of

plant management

and by the

FRG within fourteen days.

The inspector

reviewed fifteen recent

TCs.

No discrepancies

were noted.

The licensee

performed

normal procedure

changes

according to procedure

QI-5-PSL-1, Revision 2, "Preparation.

Revision,

Review/Approval of

Procedures."

This procedure

requi red those appropriate

subcommittee

reviews,

10 CFR 50.59 screenings,

UFSAR reviews,

and

FRG reviews

be

performed.

The inspector

reviewed nineteen

recently approved

procedures

from Operations,

Haintenance,

Administrative,

Emergency Operating

Procedures,

and

Emergency

Plan Implementing Procedures.

The inspector

reviewed

them for agreement

with licensing documents

and for

administrative compliance.

The inspector

found no deviations.

The licensee actively tracked the procedure

backlogs,

the number of

procedure

changes

due to technical

inaccuracies,

and the number of

active

TCs as indicators of their performance.

The inspector noted

a

positive trend in all areas for the last few months.

At the beginning

of July. the procedure

backlog was approximately

76 items.

They were

equally distributed

among word processing,

proofreading,

and

~7

04

04.1

10

administrative holds such

as training.

At the beginning of August the

backlog was

down to 42 items.

This time, however,

about half the

backlog was for an administrative hold.

Technical

inaccuracies

were

down during 1997 over

a comparable

period last year.

Most notably, the

licensee

reduced the inaccuracy rate for the improved procedures

to

about

2 percent of the issued

improved procedures.

This was

down from

approximately

6 percent the year before.

The non-improved procedures

also had

an inaccuracy rate of about

2 percent for 1997.

Conclusions

The procedure

upgrade

program at St. Lucie was scheduled to continue

into December

1999.

The prioritization of upgrading

was generally

appropriate.

However. the licensee

may not have allocated sufficient

resources

to attain the completion date

as evidenced

by the large

percentage of'he project remaining combined with the burden of normal,

non-upgrade

revision of the remaining procedures.

Overalls the

inspector

determined that the procedures

were adequate

to perform their

intended function, availability of current revisions

was good,

and the

procedures

were usable, particularly the upgraded

versions.

Although

the licensee

had issued only a small percentage

of upgraded

ARPs, the

inspector

noted that they were

a significant improvement over the older

versions.

The inspector determined that control of procedure

changes

was adequate.

The inspector

found

a positive trend in procedure

backlog

reduction.

One

NCV was identified for failure to properly revise

a

procedure to update the Operations staffing requirements

following a

change to those requirements.

Operator

Knowledge and Performance

0 erations

Swa

in

Gas

Deca

Tanks

71707

Ins ection

Sco

e

The inspector witnessed

an operator

remove the

1B Gas

Decay tank

(GDT)

from service

and place the

1A GDT in service.

In addition, the waste

gas analyzer

was aligned for service.

Observations

and Findin s

On July 30, the inspector witnessed

an operator

remove the

1B GDT from

service

and place the

1A GDT in service.

The operator

had

and followed

the appropriate

procedure.

The inspector

noted that when the operator

had questions

about the evolution, control

room operators

were contacted

for resolution.

While performing the valve lineup for placing the waste

gas analyzer in service,

the inspector

noted that the operator verified

= a valve closed rather

than open

as required

by procedure.

When

questioned

by the inspector

the operator .reviewed the procedure,

noted

the error,

and opened the valve.

Additionally. the inspector

noted

several

tools inside the panel

housing the waste

gas analyzer.

It

appeared

as though they were left by maintenance

personnel.

The

.It

11

appropriate

licensee

representative

was notified and the tools were

removed.

Conclusions

The inspector

noted that the operator

was careful

and methodical

in

performing this evolution.

Although the operator misread

one step,

overall procedural

adherence

was good.

Full Len th Control

Element

Assembl

Test

61726 71707

On August 22, the licensee

performed

a Full Length Control Element

Assembly test

on Unit 1 per Procedure

OP 1-0110050,

Revision 35,

"Control Element Assembly Periodic Exercise."

This test

had been

originally started the previous

day but was delayed after dropping

a

CEA.

The inspector noted that the actual testing

was being performed

by

an operator -in-training and supervised

by a qualified operator.

An

extra operator

was assigned

to the shift to allow the operators

performing the test to concentrate

on the test.

The operators

performed

the test according to the procedure

and kept the

ANPS informed of the

status

at all times.

Operator attention to the test

was good.

The pre-

job briefing was adequate

for the task.

Miscellaneous

Operations

Issues

Closed

LER 50-389/96-001-00

"Manual Reactor Tri

Due to Hi

h Main

Generator

Cold Gas

Tem erature"

92901

On January

5,

1996, Unit 2 was manually tripped by utility licensed

operators

due to an increasing

main generator

cold gas temperature.

The

primary cause of this event

was the fai lure of Temperature

Control Valve

(TCV) TCV-13-15 to automatically regulate cooling water flow from the

main generator

hydrogen coolers following local closure of the

TCV

bypass

valve.

A subsequent

inspection

showed that the valve controller

derivative setting

was incorrectly adjusted.

Post maintenance testing

performed after recent controller maintenance

was insufficient to assure

proper

system operation.

A contributing factor was the failure of

Operations

personnel

to adequately

monitor the evolution and ensure that

system

response

was as expected

following the local actions.

Several

unexpected

SG low level indications were received following the trip and

were subsequently

found to be caused

by partial sensing line blockage

from accumulated

corrosion products.

Corrective actions for this event included 'the following:

2)

3)

The TCV controllers setting

was adjusted prior to returning Unit 2

to service.

Additional controllersin other plant systems

were inspected for

proper operation.

Post maintenance

testing of controllers

was reviewed for adequacy.

4)

5)

6)

7)

8)

12

Operations

evaluated

generic implications and required additional

oversight for this evolution in the future.

Controller setpoints

were reviewed f'r inclusion into a data

base.

Unit 2

SG level instrumentation

sensing line blockage

was cleared,

and instrument performance

was revi ewed for Unit 1.

SG level sensing lines

and others

deemed susceptible will be blown

down in the future as part of a preventative

program.

Plant procedures

were revised to facilitate early detection of

instrumentation

discrepancies.

The inspector

reviewed the licensee's

corrective actions

and determined

that they had been completed satisfactorily.

Therefore, this item is

closed.

Closed

LER 50-335/96-003-00

"Containment Particulate

and Gaseous

Monitor Out of Service Resultin

in a Condition Prohibited

b

Technical

S ecifications

Due to Personnel

Error"

9Z901

This subject

LER documented

a

HP technician failing to return

a throttle

valve to its open position after

a containment air sample

was obtained

on February

22,

1996.

The root cause of this event

was personnel

error

attributed to the

HP technician for not following procedure.

Subsequently,

VIO 50-335/96-04-01,

"Failure to Follow Procedures

Lead to

Unit 1 Containment

PIG Inoperability," was issued for this event.

The

details of this incident were previously discussed

in Inspection

Report

97-06,

Paragraph

08. 1.

The inspector

reviewed the licensee's

corrective

actions for this event

and found that they had been satisfactorily

implemented.

Therefore, this

LER is closed.

Closed

LER 50-335/96-004-00

"Inadvertent

Manual Start of the

1A

Emer enc

Diesel Generator

Due to Personnel

Error"

9Z901

Ins ection Sco

e

On February

27,

1996,

an inadvertent

manual start of the lA Emergency

Diesel Generator

(EDG) was initiated when an Instrumentation

& Control

(I&C) technician,

working inside the

1A EDG control cabinet.

accidentally

bumped the actuating

stem on

a relay mounted

on the inside

of the cabinet.

The inspector

reviewed the event

and the subject

LER.

Observations

and Findin s

The investigation determined that the root cause of this event

was

personnel

error.

The Nuclear Plant Work Order

(NPWO) recommended that

a

clearance

be used.

A sign was posted

on the front of the

EDG control

cabinet

door warning that there

was equipment inside the cabinet which

could cause

an

EDG start.

The

I&C Supervisor did not request

a

clearance

before scheduling

work to commence in the

EDG control cabinet.

The acting control

room supervisor authorized

work to commence in the

1A

EDB control cabinet without a clearance.

Corrective actions were

inclusion of the

EDG control cabinet

under requirements of Procedure

AP

0010142,

"Unit Reliability-Manipulation of Sensitivity Systems,"

13

personal

discussion of the incident and its importance with the

responsible

parties

by the licensee

management.

and

a special training

bulletin to all maintenance

and operations

personnel

that reinforced the

~

importance of using clearances

to avoid inadvertent actuation of plant

equipment

The inspector

reviewed the licensee's

corrective actions for this event

and found that all corrective actions

had been satisfactorily

implemented.

However, the inspector

found that Procedure

AP 0010142

'Unit

Reliability-Hanipul.ation of Sensitivity Systems."

was later

deleted

and incorporated into Procedure

ADH 0010432,

"Nuclear Plant Work

Orders."

Subsequently,

the inspector

reviewed the following plant

procedures

and discovered that they still referenced

Procedure

AP

0010142.

Operations

Policy OPS-502,

Revision 0, "Pre-Evolution Briefs"

AP 0010532,

Revision 6, "Relay Work Orders"

ADH 08.01,

Revision 6,

"On-Line Leak Sealant

Procedure"

AP 0010460,

Revision

10, "Critical Maintenance

Hanagement"

AP 0005758,

Revision 7, "Electrical Maintenance

New Employee

Indoctrination Guidelines"

ADH 17.07,

Revision 3,

"Flow Accelerated

Corrosion Inspection

Implementation

Program"

The discrepancies

were brought to the licensees'ttention

and

subsequently,

a Condition Report 97-1584 was initiated to perform root

cause evaluation

and to determine

any potential generic implications

and

corrective actions.

The fai lure by the licensee to remove

a reference

of Procedure

AP 0010142

from the affected plant procedures

was

identified as

a weakness

in the licensee's

procedure

upgrade

program.

Conclusion

The inspector determined that the licensees'orrective

actions

were

appropriate to avoid

a repeat

event.

However, the failure by the

licensee to remove

a reference of AP 0010142 from the affected. plant

procedures

was identified as

a weakness

in the licensee's

procedure

upgrade

program.

08.4

Closed

VIO 50-335 389/96-11-04

"Preconditionin

of Valves Prior to

Surveillance"

92901

This violation documented

the failure of the licensee to ensure that the

procedures

(AP 1-0010125A,

Revision

39 and

AP 2-001025A,

Revision 43)

were performed

under suitable environmental

conditions.

Specifically,

these

.two procedures

allowed four containment

spray valves to be

lubricated prior to being tested:

The details of this incident and the

08.5

M1

Ml. 1

licensee's

cor rective actions

were previously discussed

in Inspection

Report 96-11,

Paragraph

E2. 1.

The inspector

reviewed the licensee's

corrective actions

as specified in the Florida Power

& Light (FPL)

response to the subject Notice of Violation (NOV), dated

September

27,

1996.

The inspector verified that all corrective actions were properly

implemented.

Therefore, this item is closed.

Closed

VIO 50-335 389/96-16-02

"Failure to Control

0 eration

Ke s"

~92901

This violation addressed

the licensee's

failure to properly control the

keys used for the electrical isolation of the Power Operated Relief

Valves

(PORVs)

as required

by Procedure

AP 2-0010123,

"Administrative

Control of Valves,

Locks and Switches."

The inspector

reviewed the

licensee's

corrective actions

as specitied in the

FPL response

to the

subject

NOV, dated October

18 '996.

The inspector verified that

ail'orrective

actions

were properly implemented.

Therefore, this item is

closed.

II. Maintenance

Conduct of Maintenance

Chemical

and

Volume Control

S stem Ion Exchan er Resin Oischar

e

62707

Ins ection Sco

e

The inspector

observed portions of the Chemical

and Volume Control

System

Ion Exchanger

Resin Oischarge

on Unit 1.

The inspector

reviewed

the radiological controls in place

and operator

procedural

conformance

and knowledge of the evolution.

Observations

and Findin s

Resin discharge

was

done in accordance

with Procedure

OP 1-0520020.

Revision 36.

"Radioactive Resin Replacement"

in conjunction with Health

Physics

Procedure

HP-40, Revision 43,

"Shipment of Radioactive

Material."

The licensee

discharged

the resin to a shipping container

staged

outside the Reactor Auxiliary Building (RAB).

The container

was

then sealed

and shipped offsite for burial at an approved site.

On July 29. the inspector

observed

the discharge of the

1B CVCS

purification ion exchanger.

The inspector

noted

good coordination.

between Operations

and Health Physics.

All personnel

appeared

to be

fami liar with the procedures'nd

communications

were generally good.

The inspector

did notice

a short period when communications

between the

shipping container

and inside the

RAB were lost.

An extra person

was

dispatched

from the container into the

RAB to inform them that the radio

was not working at that location.

The resin discharge

and flush were

completed without further problems.

'

e

Conclusions

15

The

1B ion exchanger

resin was discharged

according to procedure with no

major problems

noted by the inspector.

Good coordination

was noted

between the groups involved in the activity.

Calibration of the

2A Hi

h Pressure

Safet

In ection Dischar

e Pressure

Indicator

62707

Ins ection

Sco

e

The inspector witnessed

I8C personnel

calibrate the

2A High Pressure

Safety Injection (HPSI) discharge

pressure

indicator in accordance

with

Work Order

(WO) 97010910

and

I8C Procedure

2-140064P,

Revision 36,

"Installed Plant Instrumentation Calibration (Pressure)."

Observations

and Findin s

On July 30, the inspector witnessed

I8C perform portions of a

transmitter calibration.

The inspector verified the proper procedure

was being used,

the

M&TE was calibrated

and control led,

and the

appropriate prerequisites

had been completed.

After the transmitter

was

isolated

and the test equipment attached.

the technicians

noted the

pressure

indication increasing

on the test meter.

With the transmitter

isolated.

the pressure

should not have increased.

The test equipment

was

removed,

a valve lineup of the transmitter

completed

and the

equipment

reattached.

The transmitter again indicated

an increasing

pressure.

The technicians

manually increased

the pressure with an

installed pressure

source

and noted

an erratic response

from the

transmitter.

The technicians initially thought the transmitter

had

failed but noted that neither of them had ever seen

one fail in that

manner.

After several

minutes of discussion

one of the technicians

recalled having seen

a similar problem when Neolube was accidently

dropped

on the circuit board located inside the transmitter.

The

transmitter

was opened

and Neolube was found on the board.

Neolube is

a

conductive lubricating material that is applied to the threads of the

end caps

on the transmitter.

Prior to starting the calibration, the

technicians

had opened the transmitter to perform another part of the

procedure.

While applying the Neolube,

the technician accidently

brushed

a small

amount onto the circuit board.

After cleaning the

neolube

from the board,

the transmitter

was successfully calibrated.

Conclusions

The experience

and knowledge of the technicians calibrating this

instrument resulted in timely repair of a unique problem.

16

Governor Maintenance

and Load Run on 28 Diesel Generator

61726

62707

Ins ection

Sco

e

On August 28, the licensee

scheduled

preventive maintenance

on the

28

Emergency Diesel Generator to occur just prior to the monthly load run.

The inspector

observed

the coordination

between

maintenance

and

operations

and portions of the subsequent

load run.

Observations

and Findin s

On July 10, the

2A EDG experienced erratic behavior

due to set screws

on

the mechanical

governor vibrating loose.

The licensees'epair

was to

install the set screws with lock-tite.

On August 28, the licensee

scheduled

the 28

EDG for its monthly load run and determined that this

would also be an ideal opportunity to perform the maintenance

on this

diesel's

governors.

Because

the diesel

is inoperable for a period when

the Senior Nuclear Plant Operator

(SNPO) jacked the machine.

the

licensee

planned to perform the maintenance

then.

Shortly after the start of peak shift on August 28, the

ANPS held

a

brief with the crew.

The briefing consisted of those individuals

involved in the evolution and covered the precautions of the operating

procedure

and contingency actions for possible failures.

The ANPS 'also

covered the maintenance activity allowing the System

Engineer

time to

discuss

the job and the reason

behind it.

Overall the inspector judged

the brief to be above average.

At 4:45 p.m., the

SNPO entered

the

EDG room to begin work, the

electrician

was already in the room near the 281

EDG governor.

They

performed the maintenance

in accordance

with Work Order 97017209

01.

The procedure

had the electrician

remove each of the three set screws

one at

a time and reinstall with lock-tite.

Any problems were to be

resolved with the System Engineer

who was

on station.

The work did not

begin until the

SNPO disabled the diesel for jacking purposes.

This was

essentially

a tagout without paper.

The inspector questioned

the

Quality Assurance

(QA) Manager,

who was present for the evolution.

about

the need for a clearance.

He brought in the System Engineer to explain

why no tags were needed.

He explained that this was just an extra

precaution,

no tags would be needed

at all for his safety since

he was

not near

any rotating equipment.

Although the Equipment Clearance

Procedure

is not clear for this case,

the inspector

was satisfied that

the worker's safety

was not in jeopardy.

The

QA Manager initiated

a

Condition Report

(CR 97-1668) to clarify the issue.

The maintenance

was

performed

per the work order and in a timely manner.

The inspector

judged this to be an effective use of the inoperable diesel time.

The licensee, started

and ran the 28

EDG according to Procedure

OP 2-

22000508,

Revision 30,

"28 Emergency Diesel Generator

Periodic Test and

General

Operating Instructions."

The inspector

noted that the

SNPO

appeared

very familiar with the machine,

and followed the procedure

as

written.

The inspector did not see

any anomalies with the load run.

Conclusions

17

The inspector

observed

maintenance activity on the 28

EDG followed by

the monthly load run.

The combination of the maintenance

and load run

was considered

a strength in reducing unnecessary

starts

and periods of

inoperability of the diesel.

Unit 2 Char in

Pum

Accumulator Pressure

Checks

62707

Ins ection Sco

e

The inspector witnessed

the licensee

charge the suction

and discharge

pressure

accumulators

for the

2A charging

pump.

Observations

and Findin s

This maintenance

was performed in accordance

with WO 97015744

and

Procedure

HP-2-H-0018,

Revision 52,

"Charging

Pump Accumulators

2A,

2B,

and

2C Pressure

Check/Recharge."

The inspector verified the proper

revision of the procedure

was used,

the

H&TE calibration of the

instrumentation

was current,

and the prerequisites

had been completed

prior to starting work.

The nitrogen supply was from installed piping connected

to the plant

nitrogen system.

To charge the accumulators,

the licensee

simply

connected

high pressure

hoses

and

a small

pump between the installed

piping and the accumulators.

The maintenance

personnel

were very

familiar with performing this work and completed the task

satisfactorily.

The only discrepancy

noted by the inspector

was also identified by the

licensee

and promptly corrected.

One of the maintenance

workers

slightly stepped into the roped off contamination

zone.

The health

physics technician

assigned to monitor the work, saw this occur and

instructed the worker to step back.

A survey was conducted

and the area

was found to be clean.

Conclusions

The 2A charging

pump accumulators

were charged properly in accordance

with site procedures.

Oia nostic Testin

of 2-V2525

Boron Load Control Valve

62707

Ins ection Sco

e

The inspector witnessed

portions of the performance of Haintenance

Procedure

0940079,

Revision 6,

"VOTES 100 System Operating," which was

used to perform testing for the 2-V2525.

Observations

and Findin s

18

This valve was being tested

monthly because

Engineering

had previously

identified that the thrust at the torque switch trip was less than

requi red.

This information was documented

in CR 97-1190

and the testing

was being tracked

by PHAI 97-06-282.

The

CR concluded that the problem

was

a result of inadequate

lubrication at the stem/stem

nut interface.

This area

was cleaned

and relubricated.

The

CR required testing

was to

be performed monthly for six months to monitor the condition.

The inspector

reviewed the

WO that actually contained the work

instructions

and noted that all the prerequisites

had been completed.

The procedure

was reviewed

and noted to have several

missing signatures.

Discussion with the personnel

performing the activity, revealed that

-tables at the back of the procedure

contained the

same signoffs

as those

in the body of the procedure.

The signoffs in the table had been

completed.

Upon discovery,

the duplicate steps

in the body of the

procedure

were signed

as well.

The inspector witnessed

the valve being stroked

and data being taken.

After the data

was reviewed,

the analyst

concluded that the valve was

operating properly and

no additi'onal testing or maintenance

was

required.

Conclusions

The inspector

concluded that the personnel

observed

performing this task

were qualified and knowledgeable

about diagnostic testing.

No

discrepancies

were identified with this evolution.

Unit 2 Reactor

Protection

S stem Testing

61726

ti

S

The inspector witnessed

portions ot the performance of two Reactor

Protection

System

(RPS) survei llances,

I8C Procedure

2-1400160.

Revision

13.

"Channel Calibration delta

T power

- Quarterly,"

and 2-1400198,

Revision 4,

"RPS Channel Calibration Variable High Power Quarterly."

Observations

and Findin s

The inspector

observed

two technicians

perform the Channel

A portions of

each of these tests.

The procedures

were noted to have

been well

written and required little interpretation.

The technicians

were

observed to follow the procedure

verbatim.

In addition, the inspector

noted that the technicians

were extremely knowledgeable

about the

equipment

being tested

and the procedures

being used.

Conclusions

The inspector noted the technicians

were knowledgeable

about both the

equipment

and the procedures

being used during these survei llances.

In

addition, the procedures

were noted to have

been well written and easy

to follow.

C

M2

Maintenance

and Material Condition of Facilities and Equipment

M2. 1

Material Condition of Plant

62707

71707

a.

Ins ection Sco

e

During routine tours

and maintenance

inspections,

the inspectors

identified

a number of items impacting the overall material condition of

the plant.

b.

Observations

and Findings

During routine plant tours

and inspections,

the inspectors identified

the following items:

On July 7, tools were found inside of the Unit

1 waste

gas

analyzer

panel

On August 21,

on Unit 1,

an unsecured

ladder

was found wedged

between the

1B battery

room wall and the

125 volt DC load test

panel in the cable spreading

room.

On August

21 and September

5,

on Unit 1,

an unsecured

ladder

was

found leaning against the 480 volt load center

1A2.

On August 21,

on Unit 2,

Door

RA84, located

on the 19.5 ft

elevation of the

RAB was found blocked open.

A sign attached to

the door stated that people exiting were to ensure the door

was

closed.

On August 27; fire locker 4, located

on the 43 ft elevation of the

Unit

1 RAB, contained four flashlights

used

as emergency lighting

by the fire brigade.

One of the flashlights contained

a dead

battery

and the other three flashlights were extremely dim.

On August 27,

on Unit 2, fire door 43, located

on the 19.5 ft

elevation of the

RAB, was found blocked open.

On August 28,

on Unit 2,

an unsecured

ladder was

f'ound leaning

against the wall in the

CVCS hallway,

on the 19.5 ft el'evation of

the

RAB.

On September

3, the access

doors to the

1A and

1B LPSI

pump rooms

were found to have

been secured

by only one latch.

Each door has

eight latches.

On September

3,

an unsecured

ladder

was found erected

over -the

2B

containment

spray

pump instrumentation.

M7

M7.1

20

Each of these conditions were brought to the licensees'ttention

and

were promptly corrected.

In addition,

on August 29, scaffold located in the Unit I fuel transfer

canal

was found suspended

by carbon steel

cables.

Procedure

QI 13-

PR/PSL-2,

Revision 31,

"Housekeeping

and Cleanliness

Control Measures,"

Step 9.D.8, states

that materials fabricated

from carbon steel shall not

be stored in the pool.

However, the procedure

did not specifically

apply the

same restriction to the fuel transfer canal.

Reactor

Engineering

and Chemistry were contacted to determine if this was

a

concern.

The Chemistry supervisor stated that carbon steel

components

were not allowed in the spent fuel pool because

the boric acid solution

would cause

the component to deteriorate.

He stated that although.

on

occasions

the fuel transfer canal

and the spent fuel pool communicate

with one another.

the cable would not be

a problem as long as it did not

remain there underwater for an extended

period of time.

The inspector

verified that the maintenance activity was performed in a dry atmosphere

and therefore would not be

a concern with respect to boric acid induced

degradation.

Conclusions

While plant cleanliness

was generally acceptable,

more attention

was

warranted.

Quality Assurance in Maintenance Activities

Lon standin

Gai -troni cs Defici enci es

62707

Ins ection Sco

e

In July, Quality Assurance

issued

an audit report

(QSL-EP-97-05) that

documented

several

Emergency

Plan deficiencies.

QA's first finding

discussed-the

licensee's

ineffectiveness

in resolving longstanding

audibility problems of the Gai-tronics public address

system.

The

inspector

reviewed QA's finding and the licensee's

response

to correct

the problem.

Observations

and Findin s

The

Gai -tronics system

was the St. Lucie site's

primary means of

notification to personnel

in case of an emergency.

Section 4.6 of the

Emergency

Plan,

Revision 32, stated,

"The LPublic Address]

(PA) system,

with speakers

strategically located throughout the Protected

Area,

provides for the transmission of warning and instructions in the event

oi an emergency."

The licensee

concluded that, "... the Gai-tronics

system

has not received the necessary priority and attention to maintain

acceptable

system performance."

QA further concluded,

"Corrective

actions to address

Gai-tronics deficiencies

have not been successful

in

resolving long term problems."

'

21

In November

1994, the licensee initiated St. Lucie Action Report

(STAR)

0-94110315 to assess

the

PA coverage at the site and to make necessary

improvements to the system.

The licensee

issued

Plant Manager's Action

Item (PMAI) PM 96-02-423 to close out the

STAR and carry out corrective

actions.

Initially, a due date of April 1,

1996,

was assigned

but was

later changed to September

1,

1996.

In November

1996,

Inspection Report

50-335,389/96-18

documented

a licensee

weakness

in failing to ensure the

implementation of timely corrective actions, specifically fai ling to

correct Gai-tronic audibility deficiencies identified in STAR 0-

94110315.

In December

1996, the licensee

audited the site wide audibility of the

Gai-tronics system,

identifying several

deficiencies.

The licensee

issued

a Nuclear Plant Work Order,

WO 97001256 to address

these

deficiencies.

At the time of the

QA audit,

some items

had been repaired

but the work order remained

open.

QA identified that the system ground

readings

were low. troubleshooting

was difficult, and other maintenance

priorities were taking precedence.

The audit went on to discuss

several

other

documented

problems with the

Gai-tronics system identified by plant personnel.

Condition Report 97-

0296 identified the lack of speakers

in the Management

Information

System office area.

Condition Report 97-0589 discussed

a loud hum from

the system in the control

room.

In May,

CR 97-0787 identified that

PA

announcements

were not heard in the Unit 2 containment.

Finally,

Condition Reports

97-0998

and

CR 97-1009 identified the lack of working

speakers

in the North Service Building.

QA concluded that this finding was another

example of a weakness

previously identified by the licensee with less than effective

corrective action implementation

and follow through.

QA recommended

three actions.

First, the licensee

should commit the necessary

time and

resources

to promptly address

the problems.

Seconds

the licensee

should

start

a preventative

maintenance

program to periodically test

and repai r

the plant page system.

Third, the licensee

should review the impact of

additional

page stations prior to installation.

The inspector

found the

audit finding thorough.

the conclusions

accurate,

and the

recommendations

appropriate.

In June

1997, the licensee

formed

a task team to address

the

PA system

concerns identified in CR 97-0998

and

CR 97-1009.

The team's

recommendations

were not issued until after the

QA audit and therefore

included input from the audit.

NPWO 5306/67 identified which stations

were broken.

PMAI 97-07-119

was issued to track paging station repairs.

All repairs

were completed

by August 15.

The licensee established

a

surveillance

program for the system

on August 29.

The first test

occurred

on September

4.

The area tested

was in the turbine buildings

and steam trestles.

Although overall the test

was satisfactory.

several

discrepancies

were noted.

The licensee

captured the information in a

NPWO and repair work began that afternoon.

Last, the licensee

issued

PMAI 97-07-122 to develop

a tracking mechanism for the paging system

performance.

This was completed

on September

5.

Senior licensee

M8

H8. 1

a.

22

management

was holding those responsible for the completion of the items

accountable.

No due dates

were allowed to be extended without the

QA

Manager's

and Site Vice-President's

approval.

The inspector

concluded

.

that the licensee

had committed the resources

to properly resolve the

. problems with the

Gai -tronic system.

The inspector

randomly verified the operability of Gai -tronic stations

in the power block.

All units checked

were operable.

Also the

inspector

ensured that the plant telephones

were working.

No problems

were noted.

Conclusions

The

QA audit on the Gai-tronics

problems

was well performed.

The

inspector

found the conclusions to be well founded

and the

recommendations

to be appropriate.

The inspector concluded that the

licensee's

response

was proper,

and the programs in place should

maintain the

Gai -tronic system acceptably.

Miscellaneous

Haintenance

Issues

Licensee Control of Nuisance

or Fre uentl

Alarmin

Annunciators

62707

37551

Ins ection Sco

e

The inspector

reviewed the licensees list of annunciators

in alarm. the

controlling procedure,

AP 0010120

~ Revision 94, "Conduct of Operations,"

associated

work orders,

and condition reports, to determine if the

licensee

was adequately

addressing this issue.

Observations

and Findin s

The inspector

reviewed the activities associated

with three

CRs

concerning

nuisance

annunciators.

Procedure

AP 0010120 defined

a

frequently alarming annunciator

as

one which was unexpected

and alarmed

at least twice in a twenty-four hour period.

It stated that action

should be initiated to correct the cause of the alarm.

This procedure

defined

a nuisance

annunciator

as

one which was unexpected

and alarmed

greater than or equal to eight times in any eight hour period.

The

procedure

stated that immediate corrective action was to be taken to

correct the cause of nuisance

annunciators,

up to the point of calling

out the necessary

personnel

to correct the cause.

CR 97-1178

was written to document that when the Unit 2 station air

compressor

was started,

annunciator

F-14, "Station Air Compressor

Temp

Hi/Overld/Trip," would alarm.

WO 97008404

was written to troubleshoot

and repair.

Maintenance

determined

the problem to be associated

with

the overload trip/alarm contacts

on the 480

V breaker.

A scope

change

was

made to the

WO which allowed the alarm setpoint to be increased.

However, the setpoint

was still within the acceptable

limits previously

established

in the procedure.

The, work was successfully

completed in

e

23

accordance

with Procedure

HP 0920070,

Revision

10, "Periodic Maintenance

of 480 Volt ITE- Circuit Breakers,"

Section 4.0.

CR 97-1417

was written to document that Unit

1 annunciator

N-25 was

a

frequent alarm.

This alarm was caused

by the reactor

drain tank

(RDT)

pressure

transmitter intermittently failing low.

Maintenance

performed

initial troubleshooting

in accordance

with WO 97013779,

which determined

the problem to be

a fai ling transmitter.

Because

the transmitter is

located in a high radiation area it was scheduled for replacement

during

the upcoming refueling outage.

The third issue involved annunciator

A-10.

"125 Volt DC Bus

1B Ground,"

which was continuously alarming

and was identified as

a nuisance

alarm

on June 8,

1997.

CRs 97-1265

and 97-0496 were written to document this

recur ring problem.

Initially Haintenance

located

grounds in the fire detection

system heat

detectors for the turbine lube oil and hydrogen seal oil systems.

WO 97007805

was written to locate the faulty detectors

and replace

as

necessary.

This activity was completed 'on the turbine lube oil system

and the hydrogen

seal oil system

has

been scheduled for repair.

In addition,

a ground was found on

a wire associated

with the start

circuit for the

1A2 reactor coolant

pump.

This ground was isolated

by

lifting the affected wire.

This activity was documented

in temporary

system alteration

(TSA) 1-97-012.

Additional grounds still existed

on the system that have not yet been

located.

Engineering

concluded that the grounds

being detected

were

small

and not of major concern.

As

a result,

TSA 1-97-017

was developed

which disabled the annunciator

and installed

a voltage meter in the main

control

room.

Operations

personnel

monitored the meter hourly and if a

ground of a predetermined

magnitude

was detected,

the annunciator

response

procedure

was

implemented.

In addition, the sensitivity for

the ground alarm relays associated

with the

1B and

1BB battery chargers

was reduced in accordance

with engineering

evaluation

JPN-PSL-SEEJ-90-

029 and plant specific guidance.

At the end of this report period,

Engineering

was reviewing the ground detection

system to determine if it

needed to be modified to make it more effective.

Because

grounds still existed

on the system,

various circuits supplied

by the

1B bus,

were routinely monitored in an attempt to isolate

and

locate the remaining grounds.

The inspector

reviewed the

WOs and

TSAs associated

with the

aforementioned

problems.

Discussions

were held with numerous operators,

engineers.

and maintenance

personnel

regarding this problem.

In

addition, the inspector

reviewed the applicable

procedures

concerning

TSAs and nuisance

annunciators.

No discrepancies

were identified.

In addition;

CR 97-1265 indicated that corrective action to

repair/disable

annunciator

A-10 was not taken,. in that personnel

E7

E7.1

24

necessary

to correct the problem were not called to the plant because

.

the event occurred

on

a weekend.

The inspector discussed this

CR with

Operations,

Maintenance,

and Engineering

management

and concluded that

the actions

taken were prudent.

The licensee stated that the personnel

knowledgeable

on the system were unavailable to respond

and searching

for electrical

grounds

was too risky to be performed without adequate

planning

and the proper staff.

However, sufficient staff was available

to determine that the grounds

causing the alarm were not sufficiently

large to warrant immediate .attention.

The inspector questioned

the licensee

about

why the annunciator

was not

disabled to prevent the operators

from being unnecessarily

challenged

and burdened

by it being in a constant state of alarm.

The licensee

stated that

a process

did not exist which would allow annunciators

to be

disabled without first being subjected to

a lengthy review process.

At

that time, annunciators

were being disabled

by the use of Procedure

AP

0010124,

Revision 43,

"Temporary System Alteration Control."

However,

this process

requi red

a large amount of review/work by the system

engineer.

Because this person

was unavailable

when the annunciator

was

in constant

alarm, disabling the annunciator

was not considered

an

immediate option.

At the end of the report period, the licensee

was in

the process of developing

a procedure

which would allow the on shift

operators to disable annunciators,

upon successful

completion of a

screening

process.

This would result in a more timely response to

nuisance

annunciators.

Conclusions

The inspector concluded that frequent

and nuisance

annunciators

place

an

unnecessary

burden

on the board operators.

The ability to rapidly

resolve annunciator

problems is crucial to ensure that

a valid

annunciator is not masked

by one which is in a constant state of alarm.

In the examples

discussed

above,

the inspector concluded that the

licensee

was actively and methodically working to locate

and isolate

grounds 'associated

with this

DC bus.

The effectiveness

of rapidly

resolving nuisance

annunciators will be enhanced with the implementation

of the proposed

procedure for disabling nuisance

annunciators.

III. En ineerin

Quality Assurance in Engineering Activities

ualit

Assurance

Audits and Assessments

40500

Ins ection Sco

e

The inspector

reviewed selected daily quality reports,

audit reports,

and techni ca 1 revi ew acti vity reports.

These vari ous reports

documented

oversight activities of the Site Quality Assurance

Department.

The

inspector also reviewed selected self assessment

activities performed

by

Site Engineering.

The inspector

reviewed the audits

and assessments

to

I

25

determine if findings were documented

and processed

in accordance

with

the licensee's

corrective action program

and

NRC regulations.

Observations

and Findin s

The inspectors

noted that Site

QA had observed

various activities which

involved Site Engineering.

These observations

were documented

in QA

Quality Reports.

Site

QA had issued over 20 Quality Reports since

January

1997.

The inspector

noted that nearly 50 percent of the

QA

Quality Reports

found unsatisfactory results for activities related to

Site Engineering.

Site

QA issued condition reports to document the

unsatisfactory results.

Site Engineering

had initiated actions to

address

the

QA observations.

The inspector

reviewed

QA Audit Report QSL-EFF-97-01.

During this

review, the inspector

noted that one of the audit findings identified

configuration control concerns

regarding quality related equipment (fire

prot'ection equipment

as

an example) that were not clearly identified as

quality related in the Total Equipment

Data

Base

(TEDB).

Condition

Report 97-0592 documented

other quality related

equipment that was not

properly identified in the

TEDB.

Site Engineering initiated corrections

to address this

QA finding.

The inspector also reviewed

QA Audit Report

08.03.MKFOHV.97. 1*.

This

audit was

a limited scope audit performed

on the Steam Generating

Team

Ltd.

(SGT) design control process.

SGT is

a Morrison Knudsen

Corporation

and

Duke Engineering

& Services,

Inc.,

company which the

licensee

had contracted with for the engineering

and replacement of the

Unit

1 steam generators.

This audit was performed

by the quality

assurance staff put in place

by the licensee to provide oversight of the

Steam Generator

Replacement

Project

(SGRP) activities.

The inspector

noted that the audit team identified four findings.

The audit findings

were being addressed

by SGT management.

The inspector also reviewed selected

QA Technical

Review Activity

Reports.

These monthly reports provided

a summary of oversight

activities completed

by the Technical

Review and Assessments

(TRA) group

within Site

QA.

The inspector

noted that the

TRA group was responsible

for performing the independent

technical

review function that had been

performed previously by the Independent

Safety Engineering

Group (ISEG).

The

ISEG function was transferred to the

QA organization

as

a result of

a licensee

Technical Specification

amendment

request that was approved

by the

NRC on December

22,

1994.

The inspector

reviewed

TRA monthly

reports for the period January

1997, through July 1997,

and focused

on

the engineering activities reviewed by the

TRA group.

The inspector

noted that the

TRA group identified

a number of findings and initiated

'several

CRs

as

a result of the activities observed.

The inspector

noted

that Site Engineering

was taking actions to address

the findings

identified by the TRA group.

In addition to reviewing the

QA audit and assessment

efforts. the

inspector also reviewed the results. of the Site Engineering self

E8

26

assessment

for the second quarter of 1997.

This self assessment

covered

the performance of Site Engineering for the months of March, April. and

May.

and was centered

around the St.

Lucie Unit 2 Cycle

10 refueling

outage activities.

The inspector

noted that the self assessment

of Site

Engineering

found areas of strength,

areas that were acceptable.

and

areas for improvement.

Site Engineering

had initiated actions to

address

the areas for improvement.

Conclusion

The inspector

concluded that the

QA audits

and assessments,

and the Site

Engineering self assessment

efforts were effective in providing

oversight of Engineering activities

and identifying areas

for

improvement

and increased

management

attention.

The inspector verified

that findings identified by the licensee during the audits

and

assessments

were documented

and processed

in accordance

with the

licensee's

corrective action program requi rements

and

NRC regulations.

Miscellaneous

Engineering

Issues

U dated Final Safet

. Anal sis

Re ort Review Pro

ram

37550 40500

Ins ection Sco

e

The inspector

reviewed the results of the licensee's

Updated Final

Safety Analysis Report

(UFSAR)/Procedure

Consistency

Review effort to

determine if the findings identified by the licensee

were documented

and

processed

in accordance

with the licensee's

corrective action program

and

NRC regulations.

The inspector also reviewed the status of the

licensee's

efforts to conduct

a graded

review of the St. Lucie Unit

1

and Unit 2 UFSARs.

Observations

and Findin s

UFSAR/Procedure

Consistenc

Review

The licensee,

initiated this

UFSAR review as part of the corrective

actions for a violation issued

by the

NRC for the St.

Lucie Unit

1 Boron

Dilution Event of January

22,

1996.

In a letter dated April 23,

1996,

FPL committed to review the Unit 1 and Unit 2 UFSARs and plant

procedures

for mutual consistency.

This review was to be completed

by

December

31,

1996.

The Site Engineering

Department

was assigned

the lead to perform the

review of'he

UFSARs and procedures.

The licensee

formed

a

UFSAR

project team in August 1996 'hich consisted of personnel

from Site

Engineering,

Operations,

and

QA.

Quality Instruction

ENG-QI 6.7,

"FSAR

Reviews,"

was followed for the classification of the review findings.

All chapters of the

UFSAR for both units were reviewed by Engineering

and Operations

personnel.

Procedures

and procedural

processes

that were

mentioned in the

UFSAR were identified.

Mutual consistency

between the

procedures

and the

UFSAR was established

and the inconsistencies

were

27

identified and documented.

After the licensee

completed both

UFSAR

reviews. the inspector

noted that recommendations

for UFSAR corrections,

procedure

changes,

and plant modifications (if required)

were

prioritized and scheduled for disposition.

The inspector

noted that the results of the St. Lucie Unit

1

UFSAR/Procedure

Consistency

Review were documented

in FPL inter-office

correspondence

JPN-SPSL-96-0560 'ated

December

30,

1996.

This review

resulted in a total of 41 CRs,

129 PHAIs,

206 Procedure

Change

Requests

(PCR),

and

80

FSAR Change

Packages

(FCP) being issued to document

and

track the findings.

There were no Unit

1 modifications required

as

a

result of this review.

The inspector noted that the results of the St. Lucie Unit 2

UFSAR/Procedure

Consistency

review were documented

in FPL inter-office

correspondence

JPN-SPSL-96-0562,

dated

December

31,

1996.

This review

resulted

in

a total of 26 CRs,

181 PHAIs,

228

PCRs,

and approximately

65

FCPs being issued to document

and track the findings.

The inspector

noted that there

was one Unit 2 modification which resulted

from this

review.

A condition was identified by the licensee

where

an

UFSAR

commitment

had not been

met by the plant design in that the control

power for the primary and the back-up protection for the Reactor

Coolant

Pump

(RCP) feeders

was being provided from the same battery.

The

licensee initiated Plant Change/Hodification

(PC/H) 97015 'CP Relaying

Hodification

~ to address this finding.

This

PC/H was classified

by the

licensee

as being non-nuclear safety related.

The inspector further

noted during review of the licensee's

results that

completion of the corrective actions for the

UFSAR findings was not tied

to the December

31,

1996,

NRC commitment date.

The licensee

had

developed workoff curves

and schedules

to track completion of all the

findings.

The inspector

concluded that the findings identified by the licensee

during the UFSAR/Procedure

Consistency

Review were documented.

processed,

and being tracked in accordance

with the licensee's

corrective action program and

NRC regulations.

UFSAR Graded

Review

The inspector

reviewed the FPL's letter L-97-180, Voluntary Initiative

to Review Final Safety Analysis Reports,

dated July 11,

1997.

In this

letter,

FPL committed to conduct

a graded

review of the St. Lucie Unit

1

and Unit 2 UFSARs.

This review by the licensee

was being performed in

accordance

with the revisions that the

NRC published to its General

Statement of Policy

and Procedures

for Enforcement

Actions'Enforcement

Policy),

(NUREG 1600) to address

issues

associated

with

departures

from the

UFSAR.

These revisions were published in the

Federal

Register

(61 FR 54461)

by the

NRC on

October

18,

1996.

28

In the July 11.

1997 letter,

FPL indicated that the reviews would be

prior itized according to risk significance

(based

on probabilistic

safety assessment

methods) of the systems

described

in the

UFSAR

sections.

The licensee

had established

four priority levels.

The

licensee

further indicated that the discovery phase of the Priority l.

2.

and

3 reviews

was expected to be completed

by October

18,

1998, but

some of the walkdowns that requi re access

to the containment buildings

may be completed during the Unit 2 refueling outage in 1998 and the Unit

1 refueling outage in 1999.

The licensee

indicated that the Priority 4

systems

may be reviewed,

pending the outcome of the Priority 1, 2,

and

3

reviews.

The inspector

noted that the project scope for performing the

UFSAR

reviews

was still being developed

by the licensee at the conclusion of

this inspection.

The inspector

noted that the scope

document, titled

"Review of Risk-Significant

UFSAR Systems."

dated July 16,

1997,

was

still in draft form.

The inspector discussed

the project scope with

Site Engineering

personnel

who indicated that the

UFSAR fire protection

systems

(which were described

as Priority 2 systems

in the July 11,

1997, letter) would be covered in a separate

scope

document.

The inspector

concluded that the specific details of the licensee's

plan

to perform

a graded

review of the

UFSAR systems

according to risk

significance

(as discussed

in the licensee's

letter to the

NRC dated

July ll, 1997) were being developed.

Conclusion

The inspector

concluded that the findings identified by the licensee

during the UFSAR/Procedure

Consistency

Review were documented.

processed,

and being tracked in accordance

with the licensee's

corrective action program and

NRC regulations.

The inspector also concluded that the details of the licensee's

plan to

perform

a graded

review. of the

UFSAR systems

according to risk

significance

(as discussed

in the licensee's

letter to the

NRC dated

July 11 '997) were being developed.

Condition

Re ort Review

40500

Ins ection

Sco

e

The inspector

reviewed selected

CRs assigned to Site Engineering to

assess

the adequacy

and timeliness of the corrective actions

proposed

by

Engineering.

Observations

and Findin s

The inspector

reviewed the

CRs listed below that were assigned

to Site

Engineering for resolution.

The inspector

noted that Engineering

had

not responded to some of these

CRs because

the 30 day response

due dates

had not been

reached at the time of this inspection.

CR 97-0494

CR 97-0592

CR 97-1399

CR 97-1422

CR 97-1429

CR 97-0524

CR 97-1211

CR 97-1414

CR 97-1428

CR 97-1460

29

During review of CR 97-1422.

the inspector

noted that this

CR was

written to document

a concern that plant drawings were not revised

when

the Unit 2 PC/M 008-295,

RPS NI Safety Channel

Replacement,

was revised

during implementation via Change

Request

Notice

(CRN) 008-295-5600.

Site Engineering

responded

to the

CR by issuing Drawing Change

Request

(OCR) 97-0127 to resolve the drawing configuration issue.

The

Engineering

response to this

CR also included corrective actions to

address

generic implications and actions to prevent recurrence.

These

actions

included

a

PMAI (PM97-08-053)

assigned

to Engineering to review

the

CRNs, drawings.

and manuals for both the Unit

1 and Unit 2 Nuclear

Instrumentation

(NI) modifications

(PC/M 009-195

and

PC/M 008-295,

respectively).

The inspector considered that the corrective actions for

this

CR were of sufficient depth

and scope to address

the issue

identified.

Howevers

during further review of this

CR. the inspector

noted that the due date for completion of the

PMAI was March 30,

1998.

The inspector discussed

this

CR with licensee

personnel

and questioned

the timeliness for completion of this PMAI, given the Unit 2 drawing

configuration issues identified with implementation of CRN 008-295-5600,

and the conf'iguration control issues identified during implementation of

the Unit

1

PC/M (discussed

in NRC Inspection

Report 50-335,389/96-22)

in

the Uni't

1 refueling outage in 1996.

Subsequent

to the discussions

with

the inspector,

the licensee

revised the completion due date for PMAI

PM97-08-053 from March 30,

1998 to November 30,

1997.

The inspector

informed the licensee that after the licensee

completes

the actions for

PMAI PM97-08-053.

the inspector will review the results during-a

subsequent'nspection.

Followup of this issue

was identified as

Inspector

Followup Item, IFI 50-335,389/97-10-02,

"Completion of

Corrective Actions for Condition Report 97-1422 Regarding Plant Drawing

Revisions."

During review of the other

CRs, the inspector

noted that Engineering

generally provided acceptable

responses

to address

the concerns

identified in the applicable

CR.

Conclusions

The inspector concluded that, for the condition reports

reviewed, Site

Engineering generally provided acceptable

responses

to address

the

concerns identified in the applicable condition reports.

However, the

initial due date for completing the corrective actions for

CR 97-1422

was not considered timely.

The completion date

was revised

by the

licensee

and

an IFI was identified to review the completed corrective

actions.

30

E8.3

Closed

URI 50-335 389/96-04-09

"Failure to

U date

UFSAR"

Closed

URI 50-335 389/96-15-05

"Inade uate

Desi

n Basis

Documentation"

Closed

URI 50-335/96-16-04

"FSAR Descri tion of Installed

Instrumentation

on Unit

1

HSDP"

92903

The inspector

reviewed the NRC-identified

UFSAR inaccuracies

detailed in

Table

1 in accordance

with the Enforcement Policy as updated

by

Enforcement

Guidance

Hemorandum

(EGM)96-005,

"Enforcement

Issues

Associated with FSARs, Section

8. 1.3 Enforcement of FSAR Commitments."

With respect to the items in the table below, the inspector

reviewed the

licensee's

planned

UFSAR review effort to determine whether it was

reasonable

to conclude that the inaccuracies

would have

been identified

by the licensee's

review program.

The inspector

had the following

findings associated

with the items

on the table:

,With respect to item 1, the inspector

noted that,

although the

deficiency was identified to the licensee

in an inspection report

dated April 29,

1996, the inaccuracy

was not corrected

in a

UFSAR

amendment

submitted in January,

1997.

The licensee's

failure to

update the

UFSAR in this case

was found to be one example of a

violation of 10 CFR 50.71(e),

which requi red that the

UFSAR be

periodically updated to include, the latest material

developed

(VIO

50-335,389/97-10-03,

"NRC Identified UFSAR Inaccuracies" ).

With respect to items

2 through

16 the inspector concluded that

the inaccuracies

would not have

been identified by the licensee's

documented

UFSAR review effort and were, therefore,

subject to

enforcement action per the subject

EGN.

The inspector

found that

the subject

items represented

additional

examples of violations of

'10 CFR 50.71(e)

(VIO 50-335,389/97-10-03,

"NRC Identified UFSAR

Inaccuracies" ) .

With respect to item 17, the inspector

concluded that the item was

identified shortly after

a modification was affected that created

the subject inaccuracy.

The licensee

subsequently

incorporated

the change appropriately.

With respect to item 18, the inspector concluded that because

manual operation of these

components

was only allowed under test

conditions.

an inaccuracy in the

UFSAR did not exist.

With respect to item 19. the licensee

provided additional

information indicating the

UFSAR requirements

were met.

With respect to items 20,

21,

and 22, the inspector concluded that

the licensee's

program to review the

UFSAR was of sufficient scope

to identify these

examples.

In accordance

with the Enforcement

Policy, the fai lure to update the

UFSAR normally would be

categorized

as

a Severity Level

IV violation.

However, as-

'discussed

in Section VII.B.3 of the Enforcement Policy, the

NRC

may refrain from issuing

a Notice of Violation (Notice) for a

31

violation that involves

a past

problem,

such

as

an old

engineering,

design,

or installation deficiency,

provided that

certain criteria are met.

After review of this violation the

NRC

has concluded that while a violation did occur,

enforcement

discretion is warranted in this case.

Therefore,

to encourage

~licensee efforts to identify and correct

UFSAR discrepancies.

no

Notice is being issued in this case.

The specific bases for this

decision were (1) the licensee's

UFSAR review program,

as

described in paragraph

E8. l.b of'his report.

would likely have

identified the violation in light of the defined scope,

thoroughness

and schedule;

(2) there

had been

no prior notice

where the licensee

could have reasonably identified the violation

earlier;

(3) timely and appropriate corrective action was taken or

planned;

(4) timely and effective long-term corrective acti'ons

are

being implemented to review and identify any similar design

deficiencies:

(5) the design deficiency was considered

an old

design issue;

and,

(6) the yiolatIon was not willful. This issue

will be documented

as Non-Cited Violation (NCV)

50-335.389/97-10-06:

Failure to Update

UFSAR.

With respect to item 23. the inspector

noted that the inaccuracy

appeared

to represent

an inaccuracy of material significance.

The

issue's

resolution

has

been tied to the resolution of a generic

concern for the operability of containment

leak detection

radiation monitors.

The issue will be tracked

as

a part of a

separate

URI, as discussed

below.

URI 50-335,389/96-04-09

is

closed.

URI 50-335/96-'6-04 is closed.

TABLE 1

Item

IR

96-004

96-006

96-006

96-006

96-006

96-006

96-006

96-006

Para

raph

X1

Xj.j

X1.1

Xj.j

X1.1

X1.1

X1.2

X1.2

Oiscrepanc

Unit 1 UFSAR Table 6.2-22

showed Unit 1

NaOH concentration

as 30-32 w/o.

TS 3.6.2.2.a correctl

specified the concentration

as 28.5-30.5 w/o.

Unit 1 UFSAR Table 7.3-2 incorrectly designated

NV-21-2 as relating to

the A ICW train rather than the 8

ICW train.

Unit 1

UFSAR Figure 9.2. la was not revised following modifications to

the intake coolin

water lube oil cooler

erformed under

PC/N 341-192.

Unit 1 UFSAR Table 7.4-1

~ Intake Cooling Water System.

was not revised

to delete lubricating water pressure

switches

FIS-21-3A,

3B,

3C. 30.

3E

and 3F (non-safet

) which had been

removed

b

modification.

Unit

1 UFSAR figures 7.4-9.

19'nd

11 were not revised to remove

annunciator

E-15 lo ic. which was

s ared out.

Unit 2 UFSAR Table 7.3-2 incorrectly designated

NV-21-2 as relating to

the A ICW train rather than the 8

ICW train.

Unit

1 UFSAR Section 4.2.3.2.3(b)(1)

indicated

a minimum CEA drop time

of 2.5 seconds

plus 0.5 seconds totalling 3.0 seconds

which was

inconsistent with the 3. 1 seconds listed in TS 3. 1.3.4

and

UFSAR Table

4.2-1.

An audit of Unit 2 fire extinguishers identified three fire

extinguishers

~ at locations T-13. T-16.

and T-18 of the Turbine

Building.that were not the types of fire extinguishers

described in Unit

2 UFSAR Table 9.5A-BD.

32

Item

10

12

14

15

16

17

18

19

20

21

IR

96-008

96-008

96-015

96-015

96-015

96-015

97-006

97-006

96-004

96-006

96-006

96-022

URI

96-16-04

IR 96-16

Para

ra h

Xj

X1

E3.1

E3.1

E3.1

E3.1

E8.8

E8.8

X1

X1.1

X1.1

X.1

02.3.6-

Discrepanc

Unit 2 UFSAR'able 7.5-3 for windows LA-9 and LB-9 incorrectly showed

actuation devices

as LS-17-552A/553A and LS-17-552B/553B.

The correct

actuation devices

were LS-59-009A/014A and LS-59-218/28B.

Unit 2 UFSAR Table 7.5-3 indicated that windows LA-4 and LB-4. "Lube

Water Supply Strainers'igh Differential Pressure,

were safety related.

The system

had been

downgraded

to non-safety related status

by PC/M 268-

292.

Unit 1

UFSAR Section 5.2.4.5.b,

1 incorrectly stated that the level

detector which measured

leakage

flow through the containment

sump weir

was non-seismic.

The detector

was in fact seismically qualified.

[This

section also stated that the recorder would have

a full scale

range of 0

to 11

.

The recorder.

FR-07-03.

in fact had

a ran

e of 0 to 12 gpm.7

Unit

1

UFSAR Section 5.2.4.5.b.2

stated that the Containment

Atmosphere

Radiation Monitoring System took isokinetic samples of air from the

containment cooling system ductwork.

Section

12.2..4. 1 stated that the

sample nozzles

were designed

such that the sampling velocity was the

same

as that in the ventilation system

so that preferential particulate

selection did not occur.

The licensee

indicated that the system flow

rate was greater

than the sample flow rate: therefore the system

was not

isokinetic.

Unit

1 UFSAR Table 5.2-11,

Reactor Coolant Leak Detection Sensitivity.

item (1). referenced

Figure 5.2-36 which did not exist.

[The Average

Rate of Change

and the Time for Scale to Move did not correspond for

entries

2 and 3 of Table 5.2-117.

[Human factors decrepancies

were

identified in that the instrument

ranges in Item (2) for the quench tank

water level.

Item (3) for Safety Injection Tank water level were

specified in units that did not correspond to units used in the plant

instrumentation.

Also, item (3) indicated that the Safety Injection

Tank pressure

instruments

ranged

from 0 to 250 psig when plant

instruments

indicated

from 0 to 300 psig.7

[The licensee identified

that the average

rate of change did not corres[pond to item 2 and 3 of

Table 5.2-jj.j

Unit

1

UFSAR Section 12.2.4. 1 stated that containment

atmosphere

sample

flow was regulated

and indicated by independent

mass flow meters.

While

the flow was indicated

by independent

mass flow meters. it was not

regulated.

The system flow was dependent

only on the capability of the.

Um

Unit 1 UFSAR Table 8.3-5 did not match the battery load profile shown in

calculation PSL-1-F-J-E-90-0015

and

UFSAR Fi ure 8.3-14.

UFSAR Table 9.2-5. Operating

Flow Rates

and Calculated

Heat Loads for

Auxiliary Equipment Cooled by Component Cooling Water.

was not changed

to reflect

a 1993 accident

reanal

sis of these

arameters.

Unit 2 UFSAR Table 7.3-4 listed

EDGs as starting

on a CSAS:

a feature

removed in the Unit 2 outa

e

revious to the findin ..

Unit 1 and

2 UFSAR descriptions of TCV 14-4A and

4B operation

assume

the

valves to be automatic.

et

rocedur es allow manual

o eration.

Unit 2 UFSAR Section 9.2. 1.2 stated that

an alarm would alert operators

if blowdown heat exchanger

ICW isolation valves were reopened

during

a

SIAS.

The desi

n of the alarm was unclear.

PC/M 009-195 deleted the rod drop turbine ru0back feature in Unit 1 NI

circuitry. but

UFSAR Section 7.7. 1.4 was not updated to reflect the

deletion

Unit 1 UFSAR Section 7.4. 1.8 listed one control switch for the

pressurizer auxiliary spray valve as installed

on the Hot Shutdown

Panel.

Two switches were actually installed.

33

Item

22

23

IR

URI

96-16-04

IR 96-16

96-015

Para

raph

02.3.6

E3.1

Oiscre

anc

Unit

1

UFSAR Section 7.4. 1.8 Hot Shutdown Panel

contained

two source

range

and two wide range Nls.

The UFSAR failed to list the existence of

these in lists of installed indicators.

Unit 1

UFSAR Section 5.2.4.6 stated that the rate of chan'ge in

indication of the various leak detection

parameters

provides the

necessary

information to identify and estimate

reactor coolant system

leakage rates for a 1.0 gpm leak.

Table 5.2-11 lists the amount of time

for a

1 gpm leak to be detected

as evidenced

by a 10 percent deviation

in the normal readings.

The inspector

observed

the Containment

Radiation Particulate

and Gaseous

meters

channels

31 and 32.

respectively.

to deviate

by more than

10 percent normally. without a

1

gpm leak.

URI 50-335,389/96-15-05.

"Inadequate

Design Basis Documentation."

was opened

to track the resolution of questions

raised over both units'eak

detection

system containment radiation monitors

( Item 23 in Table, 1).

The issue

was

raised

when the inspectors

noted that no basis existed for containment

particulate

and gaseous air sampling high radiation alarm setpoints.

Since

the original inspection of this issue,

the inspectors

continued to review the.

subject systems'escriptions

in the

UFSAR and the licensee's

actions relative

to the systems.

In the course of the inspection,

the inspectors

noted that

the licensee

had no analytical

basis for the information in the

UFSAR.

Consequently,

in October,

1996 'he licensee

began performing calculations to

demonstrate

the performance characteristics

of both units'etector s.

The

inspectors identified discrepancies

as described

in Table

2 below:

TABLE 2

Unit

Source

1

UFSAR

5.2.4.1

Discrepant

Information

"The leakage

detection

systems

are consistent

upwith

the recomnendations

in R.G. 1.45..."

Oiscussion

Referenced

Regulatory Guide stated that the sensitivity of each

leakage detection

system should be adequate

to detect

a leakage

rate of 1 gpm in

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

UFSAR information. described in items

below. indicated that the

UFSAR might be inaccurate

in this regard.

A Task Interface Agreement

(TIA) on the subject

was forwarded to

NRR for review.

The accuracy of the

UFSAR statement will be

judged,

in the context of the requirements of 10 CFR 50.9.

based

upon the response

to the TIA.

34

Unit

Source

1

UFSAR

5.2.4.5

2

UFSAR

5.2.5

UFSAR

5.2.5

Discrepant

Information

"The time that

a 1.0

gpm reactor

coolant

boundary leak takes

to cause

a

10

percent deviation in

the normal readings

of various

monitoring systems

is listed in Table

5.2-11."

The subject Table

indicated that:

The time for the

gaseous

monitor to

deviate

10 percent

was 15. 1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

The time for the

particulate monitors

to deviate

10

percent

was 18.1

hours

"The leakage

detectiqn

system is

capable of detecting

unidentified leakage

equivalent to 1.0

gpm or less within

one hour."

Table 5.2-14

indicated that

detection time for

both the particulate

and gaseous

monitors

to deviate

10

percent

from normal

readings

were

">62

minutes."

"The leakage

detection

system is

consistent with the

recommendations

of

Regulatory Guide 1.45..."

Discussion

The inspectors

found that normal deviations experienced

in the unit

resulting from fluctuations in background level exceeded

10 percent

over several

minutes.

The accuracy of the

UFSAR in indicating that

a

10 percent deviation was both indicative of a

1 gpm leak and was.

in fact. identifiable given background variability. wi 11

be

evaluated in the context of 10 CFR 50.9.

Calculation PSL-1FSN-96-002.

Revision 0, which evaluated

gaseous

monitor sensitivity. indicated that

a

10 percent

increase

in.

detector output could. mathematically.

occur in 2. 1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

assuming

a higher percentage

of failed fuel than currently existed in the

plant.

The calculation also stated that "It is unacceptable

to use

an alarm setpoint of two times background

as

an indication of a 1.0

gpm step increase

in RCS leakage since the time to an alarm would

be too long...[based

on realistic

RCS chemistry]."

Estimates of

times required to identify a

1 gpm leak based

on typical chemistry.

a 100 percent

increase

in indication.

and initial leak rate (prior

to a

1 gpm step increase)

varied from 19 hours2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br /> to 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />.

The

corresponding

times for a

10 percent

change

ranged

from 2. 1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

to 19.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.

The calculation results

(Section 6.2 of the

calculation) stated that. given current

RCS chemistry performance,

"...there would be insufficient activity available in the

containment

atmosphere for the containment

gaseous

monitor to

noticeably respond to a

1 gpm step increase

in RCS leakage."

Calculation PSL-1FSN-96-001.

Revision 0, which evaluated

particulate monitor sensitivity. indicated that

a 100 percent

increase in detector output could. mathematically.

occur in 70

minutes.

The calculation also stated that the use of the

10

percent deviation as indicative of 1 gpm

RCS leakage

was "difficult

given the current

o crating environment."

Calculation PSL-2FSN-96-003.

Revision 0. performed to evaluate

the

containment particulate monitor, concluded that. for typical

chemistry conditions.

105 minutes

were required for detector output

to double.

As in the case of Unit 1.

a

10 percent

increase

in

output was found. in the field. to be masked

by the natural

variability of background levels.

The accuracy of the subject

statement will be reviewed against

the requirements of 10 CFR 50.9.

The inspectors

noted that the referenced

Regulatory Guide stated

that the sensitivity of each

leakage detection

system should be

adequate

to detect

a leakage rate of

1 gpm in

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

UFSAR

information, described in items below. indicated that the

UFSAR

might be inaccurate

in this regard.

A TIA on the subject

was

forwarded to NRR for'eview.

The accuracy of the

UFSAR statement

will be judged, in the context of the requirements of 10 CFR 50.9.

based

upon the response

to the 'TIA.

35

In addition to the discrepancies

identified above,

the inspectors .identified

a

potential operability concern relating to the detectors.

The applicable

TS

stated:

3.4.6.1

The following RCS leakage detection

systems

shall

be

OPERABLE:

a.

The reactor cavity sump inlet flow monitoring system;

and

b.

One containment

atmosphere

radioactivity monitor

(gaseous

or

particulate).

APPLICABILITY:

HODES 1, 2, 3,

and 4.

The inspectors

noted that

an obvious operability issue would exist if the

licensee is found to be out of agreement

with the Regulatory Guide referred to

in the

UFSARs.

However, the inspectors

also questioned

whether the monitors

could be cohsidered

operable if RCS activity levels were less than that

assumed

in the

UFSAR (.1 percent failed fuel).

Specifically:

~

Current chemistry results indicate that the units are performing

much better, relative to failed fuel, than

assumed

in the

UFSAR.

Calculations referred to above indicate that the low level of RCS

activity presents

a challenge in the ability of the detectors

to

identify leakage.

~

Both units'articulate

monitor calculations credit Rubidium-88

(Rb-88) alone

as providing the activity detected.

Rb-88 has

a

half-life of approxiqately

18 minutes.

Given this short half-

life, the inspectors

questioned

the ability of the particulate

monitors to indicate leakage

when the unit is in Hodes

3 and 4.

For example,

a simple decay

law estimation indicated that Rb-88

activity levels

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after shutdown would reduced

by a factor

of approximately 8E-25.

When asked for a basis for Hode 3 and

4 operability, the licensee stated that

meeting the recommendations

of Regulatory Guide 1.45 as stated in the

UFSAR

and accepted

in two NRC Safety Evaluation Reports

was sufficient to establish

operability regardless

of plant mode.

Additionally. the licensee

stated that

surveillance

requirements

of the subject

TS were met (the monitors were

calibrated

and channel

checks

were performed

as required),

thus indicating

operability.

The inspectors

noted that the Bases for TS 4.03 stated,

in part,

"Under the provisions of this specification,

systems

and components

are

assumed to be

OPERABLE when Surveillance

Requirements

have

been satisfactorily

performed within the specified time interval.

However, nothin

in this

rovision is to be construed

as

im

1 in

that s stems

and

com onents

are

OPERABLE when the

are found or known to be ino erable althou

h still meetin

the Surveillance

Re ui rements

[emphasis

addedj."

The operability of the

subject monitors will be resolved

as

a part of the overall .issue.

'n

addition to the issues

above,

the inspectors

noted that, while the lack of

calculations

which supported

statements

made in the

UFSAR was identified to

the licensee in October of 1996 'he'icensee

had, at the close of the current

36

inspection period. failed to complete the calculations.

The calculations for

Unit

1 were completed

on October

24,

1996.

The calculation for the Unit 2

particulate monitor was completed

on February 4,

1997.

The licensee

stated

that the Unit 2 gaseous

monitor calculation

was not scheduled to be completed

unti l approximately January,

1998.

The inspectors

asked whether Safety

Evaluations

under

10 CFR 50.59 had been performed for the noted

UFSAR

discrepancies.

The licensee stated that none had been performed

and that they

would not be performed unti 1 the calculations

were complete.

The timeliness

of the licensee's

corrective actions

(completion of calculations

which support

UFSAR data

and operability and the performance of 10 CFR 50.59 Safety

Evaluations) will be reviewed for conformance to 10 CFR 50 Appendix B,

Criterion XVI, to determine whether the licensee's

actions

were of appropriate

promptness.

The issues

described

above will be tracked

as

one

URI (URI 50-335.389/97-10-

04,

"RCS Leakage Detection Radiation Honitor Acceptability and Operability" ).

URI 50-335,389/96-15-05,

"Inadequate

Design Basis Documentation," will be

'losed, in deference to the new URI, which incorporates

design basis,

operability,

UFSAR accuracy,

and corrective action issues.

IV. Plant

Su

ort

F2

Status of Fire Protection Facilities

and Equipment

F2.1

Emer enc

DC Li ht

71750

a.

Ins ection Sco

e

The inspector

performed

a walkdown of the Emergency

DC lights within the

Radiological Controlled Area .(RCA) and observed portions of the monthly

emergency lighting preventive maintenance.

b.

Observations

and Findin s

e

On September

3. the inspector

performed

a partial walkdown of the

RCA

emergency lights, concentrating

mainly on both

RABs and the

EDG rooms.

The inspector

noted deficiency tags

on several

lights, however,

none of

the tags

noted were more than two months old.

The following day, the

inspector noticed

an electrician performing the August checks

per

Procedure

HP 0940066 'evision

20 'Portable

Emergency Lighting

Haintenance

and Inspection,"

and Work Order 97017406.

The results

o'

the checks

observed

were satisf'actory.

The inspector

reviewed the last two months of inspections

performed

by

Electrical

Haintenance

(EH).

In July, four lighting units were found to

be inoperable in Unit 1 and replaced

(EL-1-36-001,

EL-1-36-004,

EL-1-47-

002,

and EL-1-7-006).

EH found nine emergency lights that needed

replacement

in Unit 2.

Planning

has

issued

a work order to replace

these l'ights when replacement

batteries

become available.

The inspector

noted that the generic work order to check the lights also allowed

replacing lights.

In fact

~ one step stated that ten spares

should

be on

hand.

When the inspector questioned

why there were no spares,

the

EM

37

supervisor

and the planner stated that the had

an unusually high usage

recently

and all spares

had been

used.

Conclusions

The

PM program for the

DC emergency lighting system is adequate

to

detect

any problems with the lights within approximately

one month of

failure.

Several

lights were noted to need replacement,

work had been

planned

and replacement

batteries

were on order.

Fire

Pum

Halkdown

71750

Ins ection Sco

e

On August 26 'he inspector

performed

a detailed

walkdown of the fire

pump area.

The inspector

was looking for any detrimental conditions,

system lineups

and licensing document

conformance.

Observations

and Findin s

The inspector

had questions

about multiple items,

most of'hich the

licensee

proved acceptable

to the inspector.

However, the licensee

did

agree that several

items required

some type of corrective action.

The

inspector identified that all of the large Motor Operated

Valves

(MOV)

had equalizing valves installed around the

MOV.

Drawing 8770-G-084

SH.

1 did not show the equalizing lines

and valves.

Engineering verified

that the original design included one inch bypass

valve features,

and

therefore

no design

non-conformance

or operability concerns

existed.

CR

97-1670

documented

the drawing problem and requested

Engineering

and

Operations

Support to initiate a revision to the drawing.

The inspector also noticed that the large

MOVs were all locked open or

closed.

Drawing 8770-G-084

SH.

1 did not show any locking devices

present.

.Protection Services

recognized that this question

had been

asked in the past.

Inspection Report 95-21 noted t'hat V15500 was

shown

closed,

but the actual position was locked closed.

At that time, the

licensee initiated

STAR 960264 to investigate.

The response

indicated

that this was

an acceptable

practice.

Nuclear Engineering Standard.

STD-D-13.5.

Paragraph

6.12 stated that.

"Valves shall

be indicated

as

locked open or locked closed

when as

a Design Baseline,

locks are

necessary

for nuclear or personnel

safety.

Valves locked

administratively for equipment security and other similar purposes

are

not to be addressed

on Flow Diagrams."

The STAR further stated that the

licensee

locks the valves to meet Nuclear

Mutual Limited Insurance

Standards

and National Fire Protection Association Standards.

Since

no

design baseline exists to maintain these

valves in a locked position for

nuclear or personnel

safety,

the drawings .do not need to show the valves

as locked.

The inspector noted that both pumps

had discharge

pressure

switches

(PS-

15-20 for 1A and PS-15-21 for 1B) and pressure

gages

(PI-15-24A for 1A

and PI-15-24B for 1B) that had several

temporary valves associated

with

38

them.

The Protection Services

Supervisor

agreed that the valves were

necessary

to use the system

and that they would not remove them.

An

Engineering

review revealed that these

valves

met the definition of a

temporary valve per Operations

Ipstruction 0-0I-99-09, Revision 0.

"Labeling/Tagging of Plant Equipment,"

and they were properly labeled.

The inspector observed

what appeared

to be caulking around the base of

three

18 fire pump pipe supports.

Protection Services

stated that the

caulking was placed

around the edge to keep water from corroding the

support flange from underneath.

The inspector questioned if the

concrete

support

pad actually

made contact with the pipe support.

The

inspector

and the Protection Services

Manager probed behind the caulk

and found that the support flange on the discharge of the

18 pump was

not in contact with the concrete support.

The Protection Services

Supervisor wrote

a

CR (97-1695) to determine the operability of the

system.

Engineering

determined that the support

was not required

and

that the system

was operable.

The preliminary analysis

showed that all

pipe stresses

were within allowable limits and no operability concerns

existed.

Engineering

was planning to continue their investigation to

learn

how the piping was left in this condition.

The inspector

performed

an independent

investigation in an attempt to

determine the reason

for this nonconformance.

In October,

1996, the

licensee

replaced the

18 pump casing

due to excessive

corrosion

according to

PRO 69 5085.

Although the workers

remember

some

"difficulty"in pipe/pump flange alignment,

the Journeyman's

notes only

discussed

shimming the

pump to meet the discharge

flange.

The licensee

completed

a similar replacement

on the lA pump in February,

1997.

Again

the workers noted

some pipe fitup problems,

and again they documented

shimming the pump.

None of the maintenance

personnel

interviewed by the

inspector

remembered

noticing the gap between the support

and the

support

base.

The inspector

was unable to determine

when the support

was lifted, but it may have

been prior to the

pump casing

replacement.

The inspector

spoke with the painter who caulked

and painted the

supports.

He stated that his painting guidelines

di rected

him to caulk

any cracks prior to painting.

He further stated that he did not

consider that

a prob'lem might exist if the support did not rest

on the

base.

Once the painter painted the support,

the inspector concluded

that it was unlikely that

a casual

observer

would notice that the

supports

were caulked

and painted.

The inspector noticed that the pipe around the

18 recirculation check

valve V15121 was not painted

and was heavily corroded.

The licensee

confirmed that they had recently performed work on the check valve and

they never

repainted

the carbon steel

pipe.

The licensee corrected the

condition.

c.

Conclusions

The inspector

found the overall condition of the fire pumps to be

acceptable.

The system

was properly lined up for standby actuation.

39

One deficiency was identified due to a pipe support

found not supporting

the pipe.

Some other minor deficiencies

were noted

and corrected or

planned to be corrected.

With the exception of leaving

a repaired

check

valve exposed to the environment,

the inspector

found the material

condition generally good.

F5

Fire Protection Staff Training and Qualification

F5. 1

Closed

URI 50-335 389/97-06-13 "Failure to Man the Fire Bri ade

as

Re ui red

b

Procedure"

92904

This Unresolved

Item involved an Auxiliary Nuclear Plant Operator

(ANPO)

filling a position on the fire brigade

team which was specifically

designated

as requi ring a Senior Nuclear Plant Operator.

The procedure

was not changed prior to allowing the

ANPO to assume

the SNPO's fire

brigade duties.

Further investigation determined that the

ANPO did meet

the intent of the procedure;

he had been trained in Safe'Shutdown

System

fire fighting and was

a qualified brigade

member.

Operations

supervision did not question the one specific requirement

that the

~

position was to be filled by a

SNPO.

Procedure QI-5-PSL-l, Revision 2,

"Preparation,

Revision,

Review/Approval of Procedures."

Section 4.7. 1,

required verbatim compliance with procedures.

This fai lure to follow

the procedure constitutes

a violation of minor significance

and is being

treated

as

a Non-Cited Violation,

NCV 50-335.389/97-10-05.

"Failure to

Man the Fire Brigade as Required

by Procedure."

consistent with Section

IV of the

NRC Enforcement Policy.

This item was inadvertently reported

in the items opened

and closed section of Inspection Report 97-06 as

a

NCV. It was unresolved at the end of that report period.

This

Unresolved

Item is now closed.

V. Mana ement Meetin s and Other

Areas

Xl

Exit Meeting Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on September

12,

1997.

An interim exit meeting

was held on August 22,

1997, to discuss

the

findings of Region based

inspection.

The licensee

acknowledged

the

findings presented.

The inspectors

asked the licensee

whether any materials

examined during

the inspection

should

be considered proprietary.

No proprietary

information was identified.

PARTIAL LIST OF

PERSONS

CONTACTED

Licensee

H. Allen. Training Manager

C. Bible, Site Engineering

Manager

W. Bladow, Site Quality Manager

G. Boissy, Materials

Manager

H. Buchanan,. Health Physics Supervisor

D. Fadden,

Services

Manager

R. Heroux,

Business

Manager

H. Johnson,

Operations

Manager

J.

Marchese,

Maintenance

Manager

C. Marple. Operations

Supervisor

J. Scarola,

St. Lucie Plant General

Manager

A. Stall, St. Lucie Plant Vice President

E.

Weinkam, Licensing Manager

W. White, Security Supervisor

Other licensee

employees

contacted

included office. operations,

engineering,

maintenance.

chemistry/radiation,

and corporate

personnel.

4

INSPECTION

PROCEDURES

USED

IP 37550:

IP 37551:

IP 40500:

IP 42700:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 92901:

IP 92903:

IP 92904:

IP 93702:

Engineering

Onsite Engineering

Effectiveness of Licensee Controls in Identifying, Resolving,

and

Preventing

Problems

Plant Procedures

Surveillance

Observations

Maintenance

Observations

Plant Operations

Plant Support Activities

Followup - Plant Operations

Followup - Engineering

Followup - Plant Support

Prompt Onsite Response

to Events at Operating

Power Reactors

ITEMS OPENED,

CLOSED.

AND DISCUSSED

~0ened

50-335,389/97-10-01

NCV

"Failure to Update

a Procedure"

(Section

03. 1)

50-335,389/97-10-02

50-335,389/97-10-03

50-335,389/97-10-04

50-335,389/97-10-05

50-335,389/97-10-06

IFI

"Completion of Corrective Actions for Condition

Report 97-1422" (Section E8.2)

VIO

"NRC Identified UFSAR Inaccuracies"

(Section

E8.3)

URI

"RCS Leakage Detection Radiation Monitor

Acceptability and Operability" (Section 08.3)

NCV

"Failure to Man the Fire Brigade as Required

by

Procedure"

(Section

F5. 1)

NCV

"Failure to Update

UFSAR" (Section

E8.3)

Closed

50-389/96-001-00

50-335/96-003-00

50-335/96-004-00

50-335.389/96-11-04

50-335,389/96-16-02

50-335.389/96-04-09

50-335,389/96-15-05

50-335/96-16-04

50-335,389/97-06-13

Discussed

50-335/96-04-01.

41

LER

"Manual Reactor Trip Due to High Main Generator

Cold Gas Temperature"

(Section 08. 1)

LER

"Containment Particulate

and Gaseous

Monitor Out

of Service Resulting in a Condition Prohibited

by Technical Specifications

Due to Personnel

Error" (Section 08.2)

LER

"Inadvertent

Manual Start of the

1A Emergency

Diesel Generator

Due to Personnel

Error"

(Section 08.3)

VIO

"Preconditioning of Valves Prior to

Surveillance"

(Section 08.4)

VIO

"Failure to Control Operation

Keys" (Section

08.5)

URI

"Failure to Update

UFSAR" (Section E8.3)

URI

"Inadequate

Design Basis Documentation"

(Section

08.3)

URI

"FSAR Description of Installed Instrumentation

on Unit 1 HSDP" (Section

E8.3)

URI

"Failure to Man the Fire Brigade

as Required

by

Procedure"

(Section

F5. 1)

VIO

"Failure to Follow Procedures

Lead to Unit 1

Containment

PIG Inoperability" (Section 08.2)

50-335,389/96-15-05

URI

"Inadequate

Design Basis Documentation"

(Section

08.2)

50-335,389/97-04-02

VIO

"Routine Use of Heavy Operator

Overtime"

(Section 03.1)

LIST OF ACRONYMS USED

ADM

AFW

ANPO

ANPS

AP

ARP

ATM

CEA

Administrati ve Procedure

Auxil iary Feedwater

Auxi'liary Nuclear Plant [unlicensedj

Operator

Assistant

Nuclear Plant Supervisor

Administrati ve Procedure

Annunciator Response

Procedures

Attention

Control

Element Assembly

42

CFR

CR

CRN

CSAS

CVCS

CWD

DC

OCR

DPR

DWG

EA

EDG

EGM

EM

EMP

ENG

EOP

EP

ERT

FCP

FPL

FR

FRG

FSAR

GDT

HP

HPSI

HSDP

IBC

ICW

IFI

I.P

IR

ISEG

IX

JPN

LER

LPSI

LS

M8TE

MOV

NaOH

NCV

NI

NOV

NPF

NPO

NPS

NPWO

NRC

NUREG

NWE

Code of Federal

Regulations

Condition Report

Change

Request

Notice

Containment

Spray Actuation System

Chemical

8 Volume Control System

Control Wiring Diagram

Direct Current

Drawing Change

Request

Demonstration

Power Reactor

(A type of op

Drawing

Enforcement Action

Emergency Diesel Generator

Enforcement

Guidance

Memorandum

Electrical Maintenance

~ Electrical Maintenance

Procedure

Engineering

Emergency Operating

Procedure

Engineering

Package

Event Response

Team

UFSAR Change

Package

The Florida Power

8 Light Company

Federal

Regulation

Facility Review Group

Final Safety Analysis Report

Gas

Decay Tanks

Health Physics

High Pressure

Safety Injection (system)

Hot Shutdown

Panel

Instrumentation

and Control

Intake Cooling Water

[NRC] Inspector

Followup Item

Inspection

Procedure

[NRC] Inspection

Report

Independent

Safety Engineering

Group

Ion Exchanger

(Juno

Beach)

Nuclear Engineering

Licensee

Event Report

Low Pressure

Safety Injection (system)

Level Switch

Measuring

5 Test Equipment

Motor Operated

Valve

Sodium Hydroxide

Non Cited Violation (of NRC requirements)

Nuclear Instrument

Notice of Violation (of NRC requirements)

Nuclear Production Facility (a type of op

Nuclear Plant Operator

Nuclear Plant Supervisor

Nuclear Plant

Work Order

Nuclear Regulatory

Commission

Nuclear Regulatory

(NRC Headquarters

Publ

Nuclear Watch Engineer

crating license)

crating license)

ication)

ONOP

OP

PA

PC/M

PCR

PDR

PIG

PM

PMAI

PORV

ppm

Pslg

PSL

PWO

QA

QC

QI

QSL

RAB

Rb-88

RCA

RCP

RCS

RDT

RE

RII

RPS

SG

SGRP

SGT

SIAS

SNPO

St.

SSB

STAR

TC

TCV

TCW

TEDB

T

TIA

TQAR

TRA

TS

TSA

TSC

UFSAR

umho/cm

URI

USNRC

V

VCT

43

Off Normal Operating

Procedure

Operating

Procedure

Public Address

Plant Change/Modification

Procedure

Change

Request

NRC Public Document

Room

Particulate-Iodine-Noble

Gas Monitor

Preventive

Maintenance

Plant Management Action Item

Power Operated Relief Valve

Parts

per Million

Pounds

per square

inch (gage)

Plant St. Lucie

Plant Work Order

Quality Assurance

Quality Control

Quality Instruction

Quality Surveillance Letter

Reactor Auxiliary Building

Rubidium-88

Radiologically Controlled Area

Reactor

Coolant

Pump

Reactor

Coolant System

Reactor Drain Tank

Reactor

Engineering

Region II - Atlanta, Georgia

(NRC)

Reactor Protection

System

Steam Generator

Steam Generator

Replacement

Project

Steam Generating

Team.

Ltd

Safety Injection Actuation System

Senior Nuclear Plant [unlicensed] Operator

Saint

South Service Building

St. Lucie Action Request

Temporary

Change

Temperature

Control Valve

Turbine Cooling Water

Total Equipment

Data

Base

RCS Hot Leg Temperature

Task Interface Agreement

Topical Quality Assurance

Report

Technical

Review and Assessment

Technical Specification(s)

Temporary System Alteration

Technical

Support Center

Updated Final Safety Analysis Report

Micromhos per centimeter

[NRC] Unresolved

Item

United States

Nuclear Regulatory

Commission

Volt(s)

Volume Control Tank

VIO

VOTES

WO 44

Violation (of NRC requirements)

Valve Operation Test Evaluation System

Work Order

rg