ML17228B361

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Insp Repts 50-335/95-21 & 50-389/95-21 on 951029-1202. Violations Noted.Major Areas Inspected:Plant Operations Review,Maint Observation,Surveillance Observations & Plant Support
ML17228B361
Person / Time
Site: Saint Lucie  
Issue date: 12/07/1995
From: Landis K, Prevatte R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17228B359 List:
References
50-335-95-21, 50-389-95-21, NUDOCS 9512180382
Download: ML17228B361 (59)


See also: IR 05000335/1995021

Text

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UNITED STATES

t

NUCLEAR REGULATORY COMMISSION

REGION II

'01

MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Report Nos.:

50-335/95-21

and 50-389/95-21

Licensee:

Florida Power

& Light Co

9250 West Flagler Street

Miami,

FL

33102

Docket Nos.:

50-335

and 50-389

Facility Name:

St. Lucie

1 and

2

License

Nos.

DPR-67

and NPF-16

Inspection

Conducte

ctobe

through

December

2,

1995

Lead Inspector:

. Prevatte,

Senior Resi ent

Inspector

D

e Signed

Approved by:

W. Kleinsorge,

Reactor Inspector,

RII

E.

Lea, Project Engineer,

RII

M. Miller, Resident

Inspector

S.

San

'n

nior Operations Officer,

AEOD

K. Lan is,

C ief

Reactor Projects

Section

3

Division of Reactor Projects

t ~

SUMMARY

Da e

igned

Scope:

Results:

This routine resident,-.inspection

was conducted onsite in the areas

of plant operations

review, maintenance

observations,

surveillance

observations,

plant support,

and followup of previous inspection

findings.

Inspections

were performed during normal

and backshift hours

and

on

weekends

and holidays.

Plant operations

area:

Two violations involving system clearance

problems

were identified.

A non-cited violation involving the failure to maintain the

penetration

log was also identified by the licensee.

'Four

weaknesses

involving not documenting deficiencies,

weak corrective

action

and procedures

were also identified.

The above problems

are

very similar to other recent inspection findings and indicate

weaknesses

in operations ability to identify and correct

deficiencies.

Operations

response

to events involving a loss of

feedwater

and

a loss of main transformer cooling was good.

Overall

95i2i80382 951208

PDR

ADOCK 05000335

6

PDR

performance

in operations

was found to be in need of strong

management

and supervisory attention.

Maintenan'ce

and Surveillance

area:

One violation involving a missed surveillance for Reactor Coolant

System

boron concentration

was identified.

A non-cited violation

for this

same surveillance

occurred in October

1995.

This indicated.

a weakness

in the licensee corrective action program to prevent

recurrence.

A'large number of planned

and emergent

work activities

were completed during this refueling outage.

An emergent

problem

involving cracking of solder joints in Emergency Diesel

Generator

(EDG) control relay bases

added challenging corrective maintenance

on the EDG's.

Overall, outage

work quality was found to be

satisfactory.

Engineering

area:

No specific observation

worthy of noting was identified.

Plant Support area:

Performance

in this area continued to be satisfactory.

Within the areas

inspected,

the following violations were identified:

VIO 389/95-21-01,

"Failure to Follow Clearance

Procedures,"

paragraph

3.a.3)B.

VIO 389/95-21-02,

"Failure to Follow the Equipment Clearance

Order

Procedure

and ReqUire Independent Verification of a Technical

'Specification Related

Component,"

paragraph 3.d.2).

VIO 389/95-21-03,

"Failure to Perform Reactor Coolant System

Boron

'urveillance,"

paragraph

4.b.2).

Within the areas

inspected,

the following non-cited violation was

identified associated

with events reported

by the licensee:

NCV 95-21-04,

"Failure to Maintain Penetration

Logs," paragraph

3.a.4)B.

1.

Persons

Contacted

Licensee

Employees

REPORT DETAILS

  • R.
  • W.

L.

  • H.

C.

R

  • D

J.

~ H.

p.

R.

p.

K.

  • J
  • R.

W.

      • D
  • J

~ * J

. *

W.

Ball, Mechanical

Maintenance

Supervisor

Bladow, Site guality Manager

Bossinger,

Electrical Maintenance

Supervisor

Buchanan,

Health Physics Supervisor

Burton, Site Services

Manager

Dawson,

Licensing Hanager

Denver, Site Engineering

Manager

Dyer, Maintenance guality Control Supervisor

Fagley,

Construction Services

Manager

Fincher, Training Manager

Frechette,

Chemistry Supervisor

Fulford, Operations

Support

and Testing Supervisor

Heffelfinger, Protection Services

Supervisor

Harchese,

Maintenance

Manager

Olson,

Instrument

and Control Maintenance

Supervisor

Parks,

Reactor Engineering Supervisor

Pell,

Outage

Manager

Rogers,

System

and Component

Engineering

Manager

Sager,

St. Lucie Plant Vice President

Scarola,

St. Lucie Plant General

Manager

West, Operations

Manager

Wood, Operations

Supervisor

White, Security Supervisor

R. Ball, Mechanical

Maintenance Supervisor

'Other licensee

employees

contacted

included engineers,

technicians,

operators,

mechanics,

security force members,

and office personnel.

NRC'Personnel

.

H. Miller, Resident

Inspector

R. Prevatte,

Senior Resident

Inspector

S. Sandin,

Senior Operations Officer,

AEOD

E. Lea, Reactor Inspector,

Reactor Projects

Branch,

Region II

W. Kleinsorge,

Reactor Inspector,'aintenance

Branch,

Region II

E. Herschoff, Director, Reactor Projects Division, Region II

  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

Plant Status

and Activities

a.

Unit

1 entered this reporting period at

100 percent

power.

Significant changes

during the inspection period included:

.0

~

November

9

- November

13:

~

November

16

~

November

17 - November 18:

~

November

21 - November 23:

I

Reduced

power between

60 and

90

percent for main condenser

waterbox cleaning

Manual reactor trip - entered

Mode 3

Reactor startup

- entered

Mode

1

Reduced

power to 60 percent

due

to loss of main transfo'rmer lA

cooling

b.

Unit 2 entered this reporting period in Mode

6 defueled.

Milestones

during the

RFO included:

~

November

16 - November 19:

Core reload completed

~

November

20

Upper Guide Structure set

~

November

25

Reactor Vessel

Head set

~

November

27

Entered

Mode

5

c.

NRC Activity

E. Lea,

Reactor Projects

Engineer from Region II, visited the site

during the week of October 30.

His inspection efforts are

~

documented

in this report.

~ *

K. Landis,

Region II Branch Chief, St. Lucie Plant, visited the site

on November

20 and 21, reviewed resident

inspection activities

and

held meetings with senior site management.

M. Kleinsorge,'ngineering

Branch Inspector

from Region II, visited

the site during the week of November

27.

His inspection, efforts are

documented

in this report.

E. Merschoff, Director, Division. of Reactor Projects,

Region II,

visited the site

on December

1.

His a'ct,ivities included

a site

tour,

a review of resident

inspector activities

and meetings with

licensee

seni.or management.

3.

Plant Operations

'a ~

Plant Tours

(71707)

The inspectors periodically conducted plant tours to verify that

monitoring equipment

was recording

as required,

equipment

was

-properly tagged,

operations

personnel

were aware of plant

conditions,

and plant housekeeping

efforts were adequate.

The

inspectors

also determined that appropriate radiation controls were

properly established,

critical clean

areas

were being controlled in

accordance

with procedures,

excess

equipment or material

was stored

properly,

and combustible materials

and debris were disposed of

expeditiously.

During tours, the inspectors

looked for the

existence of unusual fluid leaks,

piping vibrations,

pipe hanger

and

seismic restraint settings,

various valve and breaker positions,

equipment caution

and danger tags,

component positions,

adequacy of

fire fighting equipment,

and instrument calibration dates.

Some

tours were conducted

on backshifts.

The frequency of plant tours

and control

room visits by site management

was noted.

The inspectors

routinely conducted

main flow path walkdowns of ESF,

ECCS,

and support systems.

Valve, breaker,

and switch lineups

as

well,as equipment conditions were randomly verified both l'ocally and

in the control

room.

The following accessible-area

ESF system

and

area

walkdowns were

made to verify that system lineups were in

accordance

with licensee

requirements for operability and equipment

material conditions were satisfactory:

I)

On November

13 and .14 the inspector performed

a walkdown of the

Unit

1

CCW System in the control room,

CCW surge tank area

behind Unit

1 control

room and

CCW platform area.

The walkdown

included

a review of OP 1-0310020,

Rev 43,

"Component Cooling

Water - Normal Operation,"

ONOP 1-0310030,

Rev 27,

"Component

Cooling Water - Off Normal Operation,"

and Engineering

Drawing

8770-G-083

Sh

1 -.,Flow Diagram Component

Cooling System.

Both

trains were aligned to support full power operation.

All major

flowpath valves were verified in the correct position using

both control

room and local indication,

when available.

The

following deficiencies

were identified:

A.

V14154 A-B CCW supply crosstie

header drain valve had

PWO

¹68795 tag issued

June

7 attached

due to the. stem being

broken at the handwheel

nut.

The licensee

intends to work

this valve the next outage.

B.

V14492 and V14494 Radiation Monitor supply from lA CCW HX

and

2A CCW HX, respectively,

'were described

as being

'ocated

"at monitor" on the Initial Valve Alignment of OP

1-0310020,

Step 8.1.1.A.

These

val'ves were actually

located

on top of the

CCW HXs on the

CCW Platform Upper

Level while the monitors were located in the Lower Level.

C.

V14456 was identified in the Initial Valve Alignment of OP

1-0310020,

Step 8.1.1.B,

as "PI-14-27A Isol."

The

nameplate

attached

to the valve said "lA CCW Pump Suet

Vent."

D.

V14188 Chemical

Feed

Tank drain to Liquid Waste

Management

System

was

shown in the Initial Valve Alignment of OP 1-

0310020,

Step 8.1.1.C,

as "Closed,"

rather than the

actual position of Locked Closed.

Also, Engineering

Drawing 8770-G-083

Sh

1 - Flow Diagram Component

Cool-ing

System did not show this valve as

Locked Closed.

E.

V15500 Fire Protection

System to

CCW surge tank was

shown

on Engineering

Drawing 8770-G-083

Sh

1 - Flow Diagram

Component

Cooling System

as normally closed,

rather than

the actual position of Locked Closed.

The above

items were discussed

with the Operations

Supervisor

who indicated that appropriate corrective actions

would be

taken.

2)

On November 30 the inspector performed

a walkdown of the Unit 2

CCW System in the control

room,

CCW surge tank area

behind Unit

2'ontrol

room and

CCW platform area.

The walkdown included

a

review of OP 2-0310020,

Rev 34,

"Component Cooling Mater-

Normal Operation,"

ONOP 2-0310030,

Rev 18,

"Component Cooling

Water - Off Normal Operation,"

and Engineering

Drawing 2998-6-

083

Sh I - Flow Diagram Component Cooling System.

The

CCW A

and

B train Cross

Over Valves SB14169

and

SB14439 were

LOCKED

OPEN and

SB14177

2B

CCW HX Outlet Cross

Over Isolation valve

LOCKED CLOSED due to

ICW being secured

to the

2B

CCW HX.

All

major flowpath valves were verified in the correct position

using both control

room and local indication,

when available.

The inspector

found that not all deficiencies previously

identified in IR 95-14 had

been corrected.

The following new

deficiencies

were identified:

~

A review of the control

room copy of OP 2-0310020,

Rev 34,

"Component Cooling Mater - Normal Operation"

found three

TCs attached.

Two of the

TCs cor ected deficiencies

identified in IR 95-14,

however,

the third was

a one time

use

TC writteh against

Rev 32.

This was pointed out to the

ANPS who.removed i.t from the binder

and initiated

a TC cancellation.

3)

On November 20, during a routine plant tour the inspector

identified the following. violations or deficiencies:

A.

In the Work Control Center'the

inspector

reviewed the Unit

2 Working Equipment'Clearance

Order

Log and found that the

index had not be updated

since

November

18.

OP 0010122,

Rev 60, Instruction 8.5, step

2 required that

"An up-to-date

index (similar to Figure 6) shall

be

maintained

in the log".

This was

a recurring deficiency

which was initially brought to the licensee's

attention in

IR 95-10 and,

again,

indicated

a lack of strict attention

to detail in the area of procedural

compliance.

This item was discussed

with the Operations

Supervisor.

He intends to interview the operators

involved and review

past corrective actions to prevent recurrence.

B.

In the Unit 2 steam trestle area,

the inspector

observed

that'he~osition

of V09120

2A AFW Pump to 2A SG Isol

.

valve was Closed,

vice Locked Closed

as required

by the

attached

Danger

Tag ¹13 of Equipment

Clear ance Order 2-95-

09-062.

The inspector

reviewed the clearance

which showed

that tag ¹13 was

1 of 29 Danger Tags issued

on November

17

to inspect/repair

V09305, repack V09104.

All entries

on

the Equipment Clearance

Order were properly completed

including Tag ¹13.

The inspector

informed the

NPS who, in

turn, initiated

a root cause investigation.

The inspector

concluded that the operator failed to verify

that V09120 was in<he:correct position

as specified

on

the equipment clearance

order per

OP No. 0010122,

Rev 60,

step 8.6.2..

Further, the operator performing the

independent Verification per section 3.4.4 of the

same

procedure

also failed to identify this discrepancy.

This

failure to establish

and maintain

an adequate

equipment

clearance

is

a violation, VIO 389/95-21-01,

"Failure to

Follow Clearance

P} ocedures."

C.

Unit

1 Control

Room

(1)

The inspector

was present

when one of the .station's

Fire pumps

was started for testing

and observed

operators

responding to several

alarms

due to the

voltage 'transient.

Operators

stated that these

alarms

were predictable.

The inspector

questioned

the

ANPS as to whether these

alarms

were listed as

OWAs.

The ANPS stated that they were not.

This was

confirmed by a review of the posted

OWAs.

These particular alarms were previously identified by

operators

to the Event Response

Team during the root

cause investigation of the manual reactor trip that

occurred

on November

16 (see

paragraph

3.b.3)

as well

known and predictable

occurrences.

The inspector,

questioned

the

OWA coordinator responsible for

maintaining the

OWAs if any of the

PWOs issued

as

corrective actions to this event identified these

alarms

as

an

OWA.

He stated that he did not believe

so,

however,

he stated that

he would look into this

issue.

The Operations

Supervisor later said that

this item was identified on November

20 as

an

OWA and

was in the process of being issued.

The inspector

identified this as

a weakness

in identifying and

documenting

OWAs.

(2)

Prior to the start of the Fire pump,

a

CST N, alarm

was received.'he

inspector questioned

the

ANPS

concerning the cause of the alarm.

The

ANPS said the

alarm was spurious

and that the pressure

switch which

generated

the alarm was identified by a

PWO for

repair.

The desk

RCO showed the inspector

Equipment

Clearance

Order 1-95-11-043 which tagged

closed

V29202, the isolation valve from N, feed supply to

condensate

storage

CST/23/N-2/E-24.

This clearance

was issued

November

11.

The inspector questioned

the

ANPS why the subject Annunciator was not identified

with a blue or brown dot, indicating work was

pending.

The ANPS said that this was not required

since the pressure

switch itself (PS-29-4)

was

identified by a

PWO tag.

The inspector requested

a

copy of the

PWO for review.

The

ANPS discovered that

no

PWO had

been

issued

and,

consequently,

initiated

Work Request

No. 95019464 for repairs.

The

Operations

Supervisor said that it was his

expectation that identified deficiencies

receive

prompt corrective action.

Since the pressure

source

was isolated for 9 days

with no

PWO issued,

the inspector identified thi's as

a weakness. in not taking prompt corrective action for

a known deficiency.

The inspector

posed several. questions

to the

ANPS in

an effort to identify and evaluate

the process

used

to bring deficiencies to management's

attention.

The

ANPS response

was limited to verbal

communications

only with no,reference

to the

STAR program.

The Operations

Supervisor stated that he would

address this

as

a personnel

performance

issue.

D.

Unit 2 Control

Room

(1)

t

The inspector questioned

an operator

as to why the

"B'rain

CCW sample valve showed dual position

indication.

The operator explained that this was

a

solenoid operated

valve controlled by a pressure

switch and that, with the "8" CCW header

depressurized

for outage work, it should

have

indicated closed.

He also said that

a similar

condition had

been observed

on the "A" train

CCW

sample valve during that train's outage work.

The

ANPS explained that the system engineer believed the

dual indication was attributable to less

than normal

operating temperature

effects

on the magnetic valve

position limit switch and that normal position

indication should

be verified after the system is

returned to service.

The

NPS exercised this valve to

the

Open position

and released

the pushbutton,

at

Oi

E.

which time the dual position indication reappeared.

The

ANPS dete'rmined that

a Work Request

was;-speeded,to

identify the cause of the dual indication.

The inspector identified this as

a weakness

in not

documenting

a potential deficiency.

The

recommendation

from the system engineer to verify

proper system

response

after

a return to sei vice did

not appear appropriate.

A review of the control

room

deficiency log on November

28 showed that Work

Request

No. 95019684

was issued

on November

23 for

repairs.

The Operations

Supervisor

again stated that it was

his expectation that identified deficiencies

receive

prompt corrective action.

The inspector

noted that the. Instrument Setpoint List had

been

removed from both control

rooms

and that this

information was available in the TEDB;

In the Unit I

control

room, the

ANPS was unable to provide the inspector

with the pressure

switch PS-29-4 setpoint .after reviewing

the hardcopy printout.

In the Unit 2 control'oom,

the

ANPS required approximately

15 minutes

and detailed

instructions via telephone to access

information using the

computer

TEDB.

The inspector

found that incorporating this information

into the computer'EDB without, apparently,

providing

operators with adequate

instructions and/or training for

access

was

a potential

impediment to operator

effectiveness.

In a frank discussion

with the

NPS the

inspector learned that removing other sources of

information,

such

as tech manuals,

FSAR, etc.,

was being

considered

based

on housekeeping.

The inspector concluded

that licensee

should evaluate this consideration

carefully.

The Operations

Supervisor

on November

20 issued detailed

instructions

on accessing

instrument setpoints

in the

TEDB

to operations

personnel

via electronic mail.

4)

Control

Room Log Reviews

A.

While reviewing the Unit 2

OOS log on November 27, the

inspector noted

an entry for V3536, the

A SDC warmup

valve.

The valve had

been declared

OOS on October

24 for

repacking

and actuator repair.

In the portion of the log

entry which specified the

mode or condition requiring the

valve to be in service,

operators

had specified "Prior to

draining cavity below 59'."

The inspector

noted that the

unit was in Node

5 (reactor cavity empty) at the time with

0)

the reactor cavity having been drained

below 59'n

November 23.

The inspector questioned

control

room operators

about the

subject entry and was told that the valve had

been

declared

00S because

the scheduled

work on the valve would

result in breaching the

A SDC train's pressure

boundary.

As two SDC trains would be required

below 59', operators

sought to ensure that the integrity of V3536 was restored

prior to a level reduction

below that value.

While valve

work and stroke testing

was completed

by November

14, the

valve reoiainetl in an inoperable state

pending

VOTES

testing.

The inspector

discussed

the issue with control

room

operators

and the Operations

Supervisor.

Of particular

concern to the inspector

was the fact that the

mode or

condition requiring valve operability, specified

on the

OOS log appeared

to have

been

ignored in draining down the

reactor cavity.

The inspector

was told that the

OOS log

was not modified when valve integrity was restored

because

that level of updating

was not considered

practical

from. a

programmatic

sense.

It was explained that the

OOS log was

employed mainly to identify those

items which should

be

considered prior to maneuvering

the plant through

modes

and conditions.

The formal verification of the required

conditions

was said to be accomplished via the procedures

governing

any specific evolution.

The inspector

reviewed the governing procedure for the

OOS

log,

and found that the procedure

required that the log be

kept current.

The inspector considered

the explanation

offered by operators

to fit loosely within the

requirements

of the procedure,

as the subject entry was

left in the

OOS log until valve operability was

conclusively demonstrated.

While reviewing this issue,

the inspector

noted

discrepancies

between

AP 0010145,

Rev 7,

"Shutdown Cooling

Controls,"

and

OP 2-1600023,

Rev 37, "Refueling Sequencing

Guidelines."

The discrepancies

involved the specification

of the TS-mandated

minimum reactor cavity level for the

movement of irradiated fuel

and above which only one train

of SDC was required.

Unit 2 TS required this level to be

23'bove the vessel

flange.

When this requirement

was

translated

into an overall elevation requirement, it was

alternately listed

as 58'nd 59's follows:

AP 0010145,

step 8.5, stated

the elevation to be

58'P

2-1600023 stated

the elevation

as:

~

58'n step 8.5

~

59'n Appendix A, Checksheet

1, step

2.C.,1

~

59'n Appendix A, Checksheet

3, step 1.A-

D

59'n Appendix

D

The inspector relayed the issue to the licensee,

who

stated that TCs would be generated

to establish

the

59'levation

as the consistent

standard.

The inspector

found

that the licensee's

procedures

were weak in their lack of

consistency

in TS-required values.

An additiona'I

weakness

appeared

to be involved in the recent review and approval

of OP 2-1600023

(October 26,

1995) in that the procedure

was released for use while internal inconsistencies

existed.

B.

The inspector reviewed

STAR 951930,

generated

by'gA as

a

result of an audit of Unit 2 control

room logs.

The gA

inspector

found that the penetration

log, required

by OP

2-1600023,

Rev 37, "Refueling Sequencing

Guidelines,"

was

not being maintained

as required

by step 8.4.8 of the

procedure.

The

gA inspector

found that three

penetrations,

28A, the equipment hatch,

and the personnel.

hatch,

were open,

were logged in the

OOS log, but were not=

'ogged

in the penetration

log.

Control

room staff updated

the logs when the condition was identified.

The failure of operators to maintain the penetration

log

constituted

a 'violation of plant procedures

and

NRC

. regulations.

This constitutes

a violation of minor

significance

and is being treated

as

a Non-Cited

Violation, consistent with Section

IV of the

NRC

Enforcement Policy.

.This item will be identified as,NCV

389/95-21-04,

"Failure to Maintain Penetration

Logs."

b.

Plant Operations

Review (71707)

The inspectors periodically reviewed shift logs

and operations

records,

including data sheets,

instrument traces,

and records of

equipment malfunctions.

This review included control

room logs and

auxiliary logs, operating orders,

standing orders,

jumper logs; .and

equipment tagout records.

The inspectors routinely observed

operator alertness

and demeanor during plant tours;

They observed

and evaluated

control

room staffing, control

room access',

and

operator

performance

during routine operations.

The inspectors

conducted

random off-hours inspections to ensure that operations

and

security performance

remained at acceptable

levels.

Shift turnover s

were observed

to verify that they were conducted

in accordance

with

approved licensee

procedures.

Control

room annunciator status

was

verified.

Except

as noted below,

no deficiencies

were observed.

1)

Cross

Connection of Electrical Trains during Unit 2

RFO

The inspector during routine plant tours

and inspections

found

that the licensee

had cross-connected

480V ESF Safety Related

10

Load Centers

2A2 to 2B2 through the

2AB swing load center.

Since this lineup is not discussed

in TS, the inspector

questioned

operators

as to whether electrical

separation

between electrical trains

A and

B was required in Modes

5 arid

6.

The operators

stated that they routinely use this lineup to

permit maintenance

and retain essential

equipment during

refueling outages.

STAR 2-951391

was written asking

engineerin'g to evaluate

the adequacy of this electrical

alignment.

Engineering

performed safety evaluation

JPN-PSL-SENS-95-037,

Rev.

0 "Safety Evaluation for Cross-Connecting

480V Load Center

during Modes

5 and 6" on this it'em.

This assessment

determined

that this alignment

was acceptable

and that no equipment

was

overloaded -or -exposed to additional failure as

a result of this

alignme'nt.

The inspector

reviewed this evaluation,

discussed it with an

NRR specialist

and found it to be acceptable

during refueling

outages.

However, .it appeared

that the licensee's

only

justification for this lineup

on Unit 2 was that it had

been

an

acceptable

practice

on Unit 1.

The inspector

noted that Unit

1

had

been licensed prior to any strict criteria for electrical

separation,

i.e.

RG 1.75.

2)

On November

8 the inspector reviewed the Unit 2 Appendix

C

Valve Switch,Deviation Log and identified two deficiencies:

A.

There

was

a log entry to unlock the'.normally locked closed

V-15538 Primary Water to SFP valve for

EM to washdown

equipment.

The entry was dated

and initialed on November.

7, however,.no

IV was documented.

The inspector brought

this to the attention of the

ANPS who confirmed that the

work had been

completed

and directed that the valve be

restored to the locked position, verified and the log

entry cleared.

Previous difficulties in maintaining this control

room log

were identified in IR 95-15

as violation 95-15-03,

"Failure to Follow Procedure

and Document

abnormal

valve

position in the Valve Switch Deviation Log", and in IR 95-

18.

The inspector

discussed

with the Operations

Supervisor the efficacy of the corrective actions

referenced

in IR 95-18, i.e., periodic

STA review.

The

Operations

Supervisor

noted that

a TC was in process

to

clarify the scope of the

ANPS/NWE daily log review and

that

a Night Order to all operations

personnel

had

been

issued

on November 10.

The Night Order stated:

"We are still having problems with the valve switch

deviation log.

Until further notice the valve switch

deviation log shall

be reviewed

each shift by the

ANPS.

During this review the

ANPS shall

ensure

the need for the

deviation to exist, the reason for the deviation,

and what

it will require to return the plant to

a normal

configuration.

A change to 0010125 will follow to

formalize this review.

This log should not have

many

items in it at any given time. If we are placing

a lot of .

items in this log we should question

and change

our

process."

The inspector

noted that the requirement for ANPS review

referenced

in the night order already existed in the

procedure.

The inspector

had

a followup discussion -with

=

the Operations

Supervisor

regarding the use

and

interpretation of AP 2-0010123 Administrative Control of

'alves,

Locks and Switches.

This AP, which contained

the

Appendix

C Valve, Switch Deviation

Log stated its purpose

as follows:

"This procedure

provides instructions for placing valves,

locks

and switches

under administrative control

when the

position of such valve, lock or switch is critical to the

safety of personnel

or equipment.

It also provides

instructions for periodic verification of the status of

'hese

valves,

locks

and switches

and verification of the

effectiveness

of these administrative controls."

Under Precautions

and Limits:

"The valves listed in this procedure

are the only ones

considered

to be under Administrative Control.

Other

valves found to be locked should

be referred to the

Operations

Supervisor for resolution."

Further, this

AP enumerated

the "criteria...considered

to

determine if a valve or switch should

be

added to or

deleted

from the list of Administratively Controlled

'alves

or switches".

And finally, this

AP stated that "Independent

Verifications, when required,

shall

be conducted

in

accordance with..."

The inspector questioned

the Operations

Supervisor

regarding the overall

usage of the Appendix

C Valve

Deviation Log and, specifically,

why V-15538 was

documented

in Appendix C.

This valve did not meet the

criteria specified

above requiring Administrative Control,

nor was it listed in any of the

AP Appendices.

The

Operations

Supervisor explained there were currently only

three methods of maintaining plant configuration control;

Equipment Clearance

Order, positioning

and restoring

valves

and switches within an approved

procedure or

12

documenting

by the Appendix

C Valve, Switch Deviation Log.

This applied to all valves

and switches including V-15538

Hose Station

15-55 Drain Valve which was not identified as

a valve requiring Administrative Control.

The presence

of a valve locking device

on V-15538 may have

added

some confusion for the operators.

The licensee

recently completed

a plant review of'll locked 'valves to

determine which ones

should

be under Administrative

Control.

Those valves

and switches which did not meet the

criteria had their locking devices

removed

and the

respective

PE IDs updated.

Under the Precautions

and

Limits quoted

above,

one might infer that the presence

of

a locking device

was only associated

with valves'under

Administrative Control.

The inspector

reviewed the

applicable

PAID as well as OP'-1560020

Primary Water

System

and verified that V-15538's

normal position was

closed vice locked closed.

The Operations

Supervisor

stated that it was his expectation that operations

personnel

minimize use of Appendix C.

On the question of when

an Independent Verification per

Appendix

C is required,

the Operations

Supervisor stated

this applied to all valves

and switches

under

Administrative Control

and those others which affected

safety related

components

or

systems similar to the

guidance

provided in OP-0010122

Equipment Clearance

Orders; paragraph

3.d.2.

The inspector

pointed out that

in the

9 months of reviewing Appendix

C log entries

he had

never

seen

an Independent .Verification waived.

The inspector concluded that while there

was

no violation

of any

NRC requirements,

AP 2-0010123

should

be clarified.

This AP did not currently address

maintaining

configuration control for valves

and switches which are

not under Administrative Control nor did it allow for

-waiving the'ndependent

Verification if the valve or

switch does not affect

a safety related

component or

.

system.

There were

2 log entries to close the normally open

V-

18150

and V-18710 Unit

1 to Unit 2 Instrument Air

X-tie'alves

for Safeguards

testing performed

on October

12.

Both valves were closed

by OP No. 2-0400050,

Rev

16

Periodic Test of the Engineered

Safety Features.

OP 2-0010123,

Rev 68, "Administrative Control of Valves,

Locks and Switches,"

Appendix N, "Hiscellaneous

Systems

Valve List," Part B.l, "Instrument/Station Air,"

identified the following valves for Administrative Control

by Unit 2:

(1)

V18717

(2),

V18150

(3)

V18149

13

Station Air X-tie from Unit

1

(G)

Instrument Air X-tie to Unit

1

(G)

Instrument Air from Station Air X-tie to

Unit (G)

V-18710 is not administratively controlled by Unit 2 since

it is

a Unit

1 valve physically located in the Unit

1

Turbine Building.

This valve was repositioned

by a Unit 2

test procedure

and improperly logged in the Unit 2

Appendix

C Valve Switch Deviation Log.

When this log

entry was questioned

by the inspector,

the Unit 2 ANPS

contacted

the Unit

1 ANPS, transferr ed the log entry and

filled out

a Data Sheet

No.

7 to document the discrepancy.

On November 9, the inspectoi". discussed this deficiency

with the Operations Supervisor.'he'Operations

Supervisor

stated that

a log entry was not required for

administratively controlled valves that were repositioned

and restored

by procedure.

The inspector

had reviewed the

procedure

and found no step which restored this valve.

Further, the inspector expressed

a concern that even with

all areas of each turbine building posted

"ensure you are

working on the right unit", operators

and test personnel

did not recognize

and inform the Unit

1 control

room of

this valve being repositioned.

The Operations

Supervisor

stated that

he had correcti.ve actions

under review which

may include initiating.a

STAR on the test procedure.

3)

Unit 1.Manual Reactor Trip following Feedwater Transient

On November

16,

1995, at approximately 5:35 pm, Operations

was

performing

a periodic surveillance

on the station's fire pumps.

This surveillance

involved .isolating the low fire main pressure

detector

and bleeding off pressure.to

ensure that both fire

pumps started.

At 5:40

pm the fire pumps started

and

a voltage

transient

caused

several

control

room annunciators

to alarm.

While the operators

were responding to these

alarms,

a

1B steam

generator

Low Level alarm

(51 percent

Narrow Range)

occurred.

Attempts

by operators to take manual control of the

1B MFRV and

increase

feedwater flow were. unsuccessful

and steam generator

water level continued to decrease.

At 5:41

pm, with

approximately

41 percent level in the

1B steam generator,

a

manual reactor trip was initiated to avoid the automatic

low

steam generator

water level,trip at 40 percent

steam generator

level.

All rods fully inserted

and all plant equipment,

with the

exception of the lB MFRV, responded

as expected.

The

1B MFRV

was locked in the

50 percent

open position'normally, following

a turbine trip, the

MFRVs receive

a zero

demand

and close).

Secondary safeties

momentarily lifted and reseated.

Following

the trip, operators

observed level in the

1B Steam Generator

increasing

abnormally.

The

15 percent

Feed

Bypass valves were

reset

and closed

and

a close signal

was sent to the

HFRV block

valves.

Since these

block valves require approximately

90

seconds

to close,

operators

manually tripped both

HFW pumps to

'revent

overfilling the

1B Steam Generator.

Following the trip

of the

HFW pumps,

the lA AFW pump autostarted

as designed

and

the

1B AFW pump was manually started

when level in the

1B Steam

.Generator 'decreased

to the normal

band.

After steam generator

levels stabilized,

operators

placed the

1A HFW pump back in

service to restore

normal feedflow.

A post trip review

verified that the

RCS cooldown limits were not exceeded.

The inspector attended

the operator debriefing conducted

by the

Operations

Hanager.

Operators

described

in detail their

recollection .of.-,the sequence

of events

and responses

to alarms

received.

Their actions in manually tripping both the unit and

HFPs were consistent

with current operating instructions

and

demonstrated

excellent operator

response.

Subsequent

to the trip, an Event Response

Team was formed to

determine

the root cause.

The

PGH reviewed the objectives of

the root cause evaluation with the team

and encouraged'them

to

remain focused.

The inspector

observed

team members

methodically review plant drawings,

vendor

documentation,

operator logs

and interviews

and control

room recorder traces

to eval'uate

system response

as part of their investigation.

The team was effective in developing

a plan of action which

identified the root cause

as

a degraded

24,VDC power supply

with input to'he

1B HFRV controller.

During post trip

testing,

the licensee

discovered that the this power supply was

degraded

to as low as 20.6 volts, which was';below the allowable

input of 21.6

VDC specified

by the controller manufacturer

(Fisher stated that the input voltage should

be 24

VDC + 10

percent).

The voltage

was further degraded

when the fire pumps

autostarted

causing the

1B HFRV Controll.er to malfunction.

The degraded

power supply was replaced

and

a reactor startup

commenced

at 4: 12

pm on November

17. Unit

1 returned to full

power operation at 2:10

pm on November

18 without incident.

Prior to unit restart,

the inspector

reviewed the post trip

package.

No deficiencies

or conclusions

other than those

noted

by the licensee

were identified.

4)

Downpower Due to Loss of Cooling on

1A Hain Transformer.

On November -21; the-Unit- 1- ANPO'found-a burned out indicator

lamp for the

DC power available annunciator light in the lA

main transformer cabinet.

The change

out of this lamp by the

operator created

a hard short to ground

and resulted in a loss

of all cooling fans

and

pumps

on the main transformer.

0

0

15

The control

room received annunciators,

"Hain XFHR 1A Alarm

Panel"

and "Hain XFHR 1A Alarm Panel

Emergency. Condition" at

4:30

pm.

ONOP 1-0910031

"Hain Transformer Off-Normal" was

immediately entered;

The

RCO shifted from the auxiliary to

startup transformers

and began

a downpower

as required

by the

procedure.

The

NWE and

a system protection engineer

were

dispatched

to the main transformer control panel

where they

.verified that all fans

and

pumps were off and that the

DC

control wiring was

damaged

due to overload.

The system

protection engineer

was able to mechanically actuate

several

control relays using handheld

jumpers

and restore three sets of

cooling fans

and pumps.

After some manipulation

and

use of

additional

jumpers the system protection engineer

was able to

start the three remaining sets of fans

and pumps.

At 4:45

pm,

the unit downpower was leveled off at 60 percent.

'I

At 5: 17 pm, transmission

and distribution personnel

arrived at

the scene

and

commenced

repairs to the damaged control wiring.

At about 7:00

pm, these repairs

were completed

and after

testing the transformers

were realigned

and the unit was

returned to full power.

The response

by operators

and the system protection engineer

was found to be very timely and effective.

The knowledge

and

restoration

action taken

by the system protection engineer

prevented

the potential

loss of the unit.

5)

Water Treatment

Plant Carbon Filter Changeout

During a plant tour on October 20, the inspector

noted

a number

of operators

in the area of the Water Treatment

Plant preparing

to replace

media in 4,carbon filters.

In discussing'the

~

upcoming evolution, operators

stated that they did not believe

that...they could perform the evolution with the governing

operations

department

p'rocedure

due to a lack of specificity in

the guidance.

The inspector reviewed the subject procedure

and found that it

was very vague in its requirements

and included

a requirement

for those performing the evolution to take notes to be used in

developing

a new,

more detailed revision of the procedure.

Operators

stated that this requirement

was included

when plant

management

directed that

a procedure

be effectively as-built

while experienced

operators

and maintenance

personnel

performed

the media changeout.

Operators

stated that they felt that this

method of procedure

development

was not in keeping with the

plant's

new verbatim compliance policy.

The inspector

discussed

the issue with the Operations

Supervisor,

who stated that the Water Treatment Plant was

operated

using operations

departmental

procedures

which, due to

the lack of safety significance of that area of the plant, only

16

required his signature to approve.

The direction given to

develop

a more refined procedure

by recording the steps

required to perform the changeout

was considered

appropriate

to the circumstances.

The inspector stated that he considered

the operator's

attitudes to be correct,

as the conduct of

operations

procedure

required detailed

procedures

for

evolutions conducted

in all but

a small, procedurally-defined,

,series of 'exceptions.

The Water Treatment Plant

was not among

, the current list of exceptions.

1

During the current inspection period, the inspector

revisited

the issue with the operators originally involved in the issue,

who stated that

a detailed

procedure

was developed prior to the

commencement of work on media changeout

and that the plant's

verbatim compliance policy was applied to the evolution.

The

inspector

concluded that the operators

had raised

a valid

concern regarding the appropriateness

of procedural

guidance

and that the issue

had

been satisfactorily resolved.

C.

Plant Housekeeping

(71707)

Storage of material

and components,

and cleanliness

conditions of

various

areas

throughout the facility were observed to 'determine

whether safety and/or fire hazards

existed.

Plant appearance

declined

as expected

during the RFO.. However, the licensee

had

strengthened

their management

plant walkdown program

and

as

a result

are identifying and correcting

a lot of long term minor

deficiencies.

'o

violations or deviations

were identified.

d.

Clearances

(71707)

1)

Clearance

2-95-11-018

-

125VDC to 2A

EDG control panel.

Clearance

tags

on'-'2 breakers

in

DC panel

2A.

Both tags

were in

place

and the breakers

were in the correct position.

2)

The inspector

reviewed the following effective clearances

on

the Unit- 2 Atmospheric

Dumps

and their associated

block valves:

~Primar

Clearance

~Ei

t III

N

b

HV-08-14

HV-08-17

MV-08-18A

MV-08-18B

NV-08-19A

NV-08-19B

2-95-11-152

2-95-11-128

2-95-10-170

2-95-10-168

2-95-09-258

2-95-09-261

17

OP 0010122,

Rev 59, "In-Plant Equipment Clearance

Orders,"

Step

8.3.7,

provided the detailed instructions for performing

a

SAFETY REVIEW in item 7 of the Equipment Clearance

Order.

Step

8.3.7 stated:

'The

NPS/ANPS/NWE shall circle yes or no signifying that the

following items were reviewed with respect to the clearance

requested

when item P6

(AUTHORIZED BY) is signed.

A.

B.

C.

IV Required:

A Tech.

Spec./FUSAR/Safety

related

component

or system is affected.

Containment Penetration:

Associated

clearance

involves

a

Containment Isolation Boundary.

Scope of work required

by

the

NPWO shall

be reviewed against the clearance

to verify

Containment

Boundary is maintained.

Refer to the

Open

Penetration

Log in Operating

Procedure

1 (2) - 1600023,

"Refueling Sequencing

Guidelines."

Redundancy:

Verify that the redundant

equipment/component/system

is OPERABLE.

The Equipment

Out-of-Service log and Jumper/Lifted

Lead log shall

be

utilized to verify redundancy.

D.

Mode Related:

Will a change

in MODE, up or down, require

additional surveillances

or requirements

to maintain

adherence

to Tech.

Specs.

"r

E.

Sensitive

Systems:

Work practices of.Administrative

Procedure

0010142 "Unit Reliability - Manipulation of

System

Systems."'he

safety reviews for .the above

Equipment Clearance

Orders

showed (refer to the preceding

paragraph for identification of

which item was reviewed)

A.

B.

C.

D.

E.

2-95-11-152

2-95-11-128

2-95-10-170

2-95-10-168

2-95-09-258

2-95-09-261

Y

Y

Y

N

N

N

N

Y

N

N

Y

Y

Y

Y

Y.

Y

N

Y

Y

N

Y

N

Y

Y

N

Y

N

Y

Y

N

There were several

inconsistencies

in the above safety reviews:

A.

-MV-08-17 (2-95-11-128) is a=Tech.

Spec. identified

SG

PORV

block valve which requires

an IV.

B.

MV-08-18A, MV-08-18B, MV-08-19A and MV-08-19B were all

SG

ADVs.

However, unlike the other

3

PORVs MV-08-18A (2-95-

e.

18

10-170) is identified as

a containment

penetration

and

sensitive

system.

C.

NV-08-14 and NV-08-17 are

2 of 4

SG

ADV block valves.

NV-

08-14 (2-95-11-152) is identified as

a containment

penetration

which is not mode related.

.It appeared

to the inspector the safety review criteria was

, being inconsistently applied to similar components

as

shown

above

(items

B and C).

The failure to require

an independent

verification of NV-08-17 per

OP 0010122,

as identified above,

is identified as

a violation; VIO 389/95-21.-02,

"Failure to

Follow the Equipment Clearance

Order Procedure

and Require

Independent Verification of a TS Related

Component.".

Technical Specification

Compliance

(71707J

'icensee

compliance with selected

TS

LCOs was verified. This

included the review of selected

surveillance test results.

These

verifications were accomplished

by direct. observation of monitoring

instrumentation,

valve positions,

and switch positions,

and by

review of completed

logs

and records.

Instrumentation

and recorder

traces

were observed"for abnormalities.

The licensee's

compliance

'ith

LCO action statements

was reviewed

on selected

occurrences

as

they happened.

The inspectors verified that related plant

procedures

in use were adequate,

complete,

and included the most

recent revisions.

No deficiencies

were noted.

f.

Reduced

Inventory Operations

(71707)

On November 28, Unit 2 entered

a reduced

RCS inventory condition to

support

2A2 and

2B2

RCP seal

work.

The following items were

verified prior to this evolution:

~

Containment

Closure Capability - Instructions

were issued to

accomplish this;

men and tools were

on station.

The inspector

verified that the penetration

1'og properly. indicated actions

necessary

to close the three,

logged,

open penetrations

which

were required to establish

containment integrity.

~

RCS Temperature

Indication - The inspector verified that two

normal

Node

1 CETs were available for indication.

~

RCS Level Indication - The inspector verified that independent

RCS wide and narrow range level instruments,

which indicate in

the control

room, were operable.

An additional

Tygon tube loop

level indicator in the containment

was to be manned during

level

changes

and was displayed via closed circuit television

in the control

room.

~

The inspector verified that the tygon tube was free of obvious

kinks and properly supported.

The inspector noted,

however,

19

that the tube was routed directly over the

8 hydrogen

-. recombiner.

At the time, the

A recombiner

was operating

under

a surveillance test.

Operation of the recombiners results in

high amount of heat rising from the units.

The inspector

notified the control

room, cautioning operators

not to operate

the

8 recombiner without rerouting the tygon level indicator.

~

RCS Level 'Perturbations

- When

RCS level

was altered,'

additional operational

controls were invoked.

Procedural

restrictions required, operators

to terminate

maintenance

activities that could affect

RCS level,

shutdown cooling, or

related instrumentation

and controls.

~

RCS Inventory Volume Addition Capability - The inspector

verified that one (of three)

charging

pumps

and

a HPSI

pump

were available for RCS addition.

~

RCS Nozzle

Dams - Nozzle

dams were not installed at the time.

~

Vital Electrical

Bus Availability - Operations

would not

release

busses

or alternate

power sources for work during

reduced

inventory conditions.

The lh

EDG was considered

operable

and the

18

EDG was considered

available

and was, in

fact running loaded,

as the licensee

was performing the TS-

required

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> surveillance

run, performed

each refueling on

each

EDG.

Governing procedures

prohibited switchyard work

during reduced

inventory conditions

and signs

were posted to

that affect at the switchyard.

~

Pressurizer

Vent Path - The manway atop the pressurizer

was

removed to provide

a vent path, -and

a vented

'FME device

was

attached.

The inspector reviewed

AP 0010145,

Rev 7,

"Shutdown Cooling

Controls,"

and

OP 2-160023,

Rev 38, "Refueling Sequencing

Guidelines"

and found that initial conditions either

were satisfied

at the time of the review or could be satisfied

by the time

inventory reduction

commenced.

The inspector

noted that Appendix 8,

Check Sheet I, "Surveillances

Performed During Reduced

Inventory,"

contained

a verificati'on, in step

1.E, to verify that I SG with a

level of at least

10 percent

narrow range

was available

when nozzle

dams were removed.

The step

was apparently

meant to ensure

the

possibility of natural circulation in the event of a loss of

shutdown cooling; however, it had

been established

previously that

RCS integrity and pressurization

was required to ensure

natural

circulation.

As one requirement for reducing inventory was to vent

the pressurizer,

this step

appeared

superfluous.

The inspector

questioned

operators

as to the applicability of the subject step

and

found operators

knowledgeable

on the issue,

stating that they

realized that the step

was meaningless

and stating that it was

a

holdover from previous revisions.

The

NPS stated that the procedure

would be revised to remove the subject surveillance.

Overall, the

20

inspector

found operator

knowledge of the. upcoming evolution to be

good.

A prejob briefing was held in the late afternoon of November 28.

The unit entered

reduced

inventory at 5:55

pm to perform

RCP seal

work.

The work was completed

and reduced

inventory conditions were

exited at 9:45 pm,

on November 29.

g.

Effectiveness of Licensee Controls in Identifying, Resolving,

and

Preventing

Problems

(40500)

I)

Licensee Self Assessment

-*

The inspector attended

the Management

Review Meeting held

on

November

17.

Senior

FPL Managers

including the President of

the Nuclear Division and his designated

successor

were present.

The topics covered included:

A.

Unit I manual reactor trip which occurred

on November

16

B.

Operating

Report

C.

Unit 2 Outage Status

D.

Vakious Department

Reports

~

Nuclear Materials

Management

e

Engineering,

,

~

Maintenance

~

Plant Indicators

The discussions

were lively with active participation

by senior

management.

The inspector noted that the agenda

and

present'ation

was effective in briefing senior management.

2)

gA Audit Review

The inspector reviewed

gA audit OSL-OPS-95-12 of operations

and

technical specification

compliance dated October 20,

1995.

This audit was detailed

and thorough

and identified one finding

involving inadequate

control of long term surveillance

and the

timeliness of some non-technical

specification surveillance.

Weaknesses

involving procedural

adequacy

and adherence

were

also identified.

Good performance

was noted for on-line

maintenance activity coordination,

communication, shift

turnover,

use of self verification techniques,

and supervisory

oversight of reactivity control

and risk management.

The

inspector

noted that these findings closely paralleled

those of

the

NRC.

21

h.

Outage Activities (71707,62703)

1)

Unit 2 Core Verification

Preoperational

Test Procedure

No. 32000090,

Rev 15, Step 12.9,

is

a

QA Holdpoint where

QA independently verifies the fuel

assembly,

CEA and insert configurations

per AP 0010439,

."Physical

Inventory of Nuclear Fuel Storage Areas."

On November

19, the inspector

observed

the first half of core

verification following completion of"core reload at 1:06

pm.

A

CCTV and light attached

to a pole was lowered from the

refueling bridge

and positioned initially ov'er the southwest

portion of the core.

The

CCTV signal

was received

on

2

monitors

and

a

VCR on the refueling bridge where

a

QA inspector

and Reactor Engineer independently verified the orientation of

the assembly

and recorded the serial

number.

The refueling

bridge was then moved to the next assembly,

usually in the

same

row,

and the process

repeated.

Occasionally,

the submerged

lighting intensity was adjusted to ensure

a good quality

videotape

was produced.

The overall" Cdr'e"'Verification took

approximately 4-1/2 hours with only

1 deviation noted, i.e.,

CEA 843 in assembly

L75 (core location J6)

was rotated

180

degrees.

The inspector discussed

this deviation with the

Reactor

Engineer the next day.

The Reactor Engineer pointed

out that since this was

a full length

CEA there would be no

change

in the. core physics.

This was allowed per the

instructions for Unit 2 on Figure

1 of AP 0010439,

Rev 16,

which stated

"Full length strength

CEA's 'are oriented

SW for

convenience

of verification only."

The deviation was reviewed

and accepted

by

FRG on November 20, 'at which time

a STAR. was

initiated for tracking purposes

to the next

RFO.

In the three hours that the inspector

observed

Core

Verification, communications

were good

and coordination

among

the operators

was excellent.

The

2 data recorders

agreed to a

routine whereby neither would verbalize the assembly serial

number until both said "got it" and

had entered

the data

on

2

separate

data sheets.

This ensured

independent verification of

assembly serial

numbers

and location.

2)

Reactor Vessel

Reassembly

Upon completion of core load and verification, reactor

reassembly

was started

November 20.

The head

was set

on

November

25 and tensioned

on November 27.

The inspector

observed

selected- portions- of- these- activities during routine

reactor building entries.

The inspector did not identify and

the licensee

did not encounter

any significant problems during

this evolution.

22

3)

Freeze

Seals

The inspector reviewed licensee's

procedures

and documentation

associated

with freeze

seal application,

and interviewed

licensee

personnel

concerning the freeze

seal

process.

The

inspector specifically reviewed the procedure to determine if

the licensee

had included technical

guidance

as specified in

.the

NRC inspection

manual

Part 9900, Technical

Guidan'ce-

Mechanical

Freeze

Plugs.

The inspector

concluded that the

licensee's

procedure,

GAP-10,

Rev 2, "Application Of Freeze

Seals,"

adequately

addressed

the requirement specified in part

9900 which pertain to mechanical

freeze

seal application.

The

inspector reviewed

NPWO-91-8417

and WO-95017759-01

-and

determined that many of the requirements

specified in both the

licensee's

procedure

and

NRC inspection

guidance

had

been

complied with or specified

as requirements.

Since the core

was

off-load, freeze seals

were not used to the extent originally .

anticipated

during the outage.

Followup on Previous

Operations

Inspection

Findings

(92901)

1)

IR 95-09

and 95-10 identified, during ventilation systems

walkdowns,

several

instances

where operator

aides, i.e.,

SIAS

and

CIAS donuts,

on both Unit 2 and Unit

1 control boards

were

missing.

At the time these

IRs were issued

the licensee

committed to correcting these deficiencies during

a complete

review of plant procedures

estimated to be completed within

approximately

90 days.

As followup to these

IRs the inspector confirmed that the two

missing operator aides

on Unit

1 were installed,

but that the

seven identified on Unit 2 were util'1 missing.

This was

brought to the attention of the Operations

Manager

who stated

that corrective action would be*taken.

The inspector verified

that all identified missing operator aides previously

identified in the above

IRs were inst'alled within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

2)

IR 95-14 identified deficiencies

associated

with a walkdown of

the Unit 2

CCW System in the control

room,

CCW Surge

Tank area

and the Upper and

Lower Platform levels of the

CCW structure.

The following deficiencies

have not been corrected

as of

November 30,

1995:

A.

V14101

5 V15536 were initially aligned to the

CLOSED

position;

however,

both had

a handwheel

locking device

installed with no associated

tag indicating

LOCKED CLOSED.

B.

V14438

(2A CCW HX outlet piping high point vent) omitted

from initial lineup.

C.

V14187 (Chemical

Feed Tank outlet) tag not attached.

0

3)

23

D, V14188 Aid not have

a

LOCKED CLOSED tag

as

shown in the

initial alignment.

The inspector brought this item to the attention of both the

Unit 2 ANPS and the Operations

Manager.

The

ANPS directed that

a

TC to Operating

Procedure

No. 2-0310020,

Rev. 34,

"Component

Cooling Water - Normal Operation"

be prepared to add V14438

(2A

.CCW HX outlet piping high point vent) to the initial 'lineup.

F

The inspector found that the licensee's

failure to address

minor deficiencies identified in previous

IRs

a weakness.

4.

'aintenance

and'urveillance

a.

Maintenance

Observations

(62703)

Station maintenance activities involving selected. safety-related

systems

and components

were observed/reviewed

to ascertain that they

were conducted

in accordance

with requirements.

The following items

were considered

during this review:

LCOs were met; activities were

'ccomplished

using approved

procedures;

functional tests

and/or

calibrations

were performed prior to returning components

or systems

to service; quality control records

were maintained; activities were

accomplished

by qualified personnel;

parts

and materials

used were

properly certified;

and radiological controls were implemented

as

required.

Work requests'ere

reviewed to determine the status of

outstanding jobs

and to ensure that priority was assigned

to safety-

related

equipment;

Portions of the following maintenance activities

were observed:

1)

. Inconel Alloy 600 Nozzle

and

RTD Replacement

) j

~ 'I/

In 1986,

San Onofre reported the failure of an inconel alloy

600 pressurizer

steam

space

nozzle, ht No. 54318.

FPL

determined that St. Lucie Unit 2 had four pressurizer

steam

space

nozzles,

one liquid space

nozzle

and five RCS hot leg

RTDs,

and four RCS cold leg

RTDs of the

same heat of inconel

alloy 600.

As a precaution,

St Lucie replaced

the four steam

space pressurizer

nozzles in 1987, the liquid space

nozzle,

and

the five RCS hot leg

RTDs in 1989, with inconel alloy 600 ht

No. 41501.

In 1993, the four alloy'600 steam

space pressurizer

nozzles

replaced

as

a precaution

in 1987, failed and were

replaced with inconel alloy 690 nozzles

welded with alloy 600

welding filler material

(I182).

In 1994, the steam

space

nozzles

replaced

in 1993, failed in the weld area.

These

nozzles

were removed

and reinstalled with alloy 690 welding

filler material

(I52).

FPL planned to replace the three liquid

space alloy 600 pressurizer

nozzles

in 1995,

as

a result of

previous failures of ht Nos.

NX 7630,

7387-2

and 41501.

FPL

planned to replace the five RCS hot leg

RTDs (ht No. 41501)

.

after 2003

and monitor the four RCS cold leg

RTDs (ht No.

54318).

A discussion of the

1993

and

1994 replacement activities is

contained

in

NRC Inspection

Report Nos. 50-335,389/93-08

and

50-335,389/94-10.

As

a result of both pressurizer

and hot leg penetration

failures of inconel alloy 600 ht Nos.

NX 7630

and 7387-2

reported

by San Onofre

and Palo Verde

and evidence of a St

Lucie Unit 2

RCS hot leg leak,

FPL decided to replace three

, Unit 2 pressurizer liquid space alloy 600, nozzles

and nine

RCS

instrument penetrations

with alloy 690.

As

a result of the above replacements,

all of the alloy 600 ht

Nos.

NX 7630

and 7387-2 have

been

removed from Unit 2,

and the

five hot

I'eg

RTDs of ht No.

41501 will be monitored until their

replacement.at..~

2003..

Four alloy 600 ht No. 54318

RCS cold

leg

RTDs remain in Unit 2.

Because of the lower cold leg

RCS

temperatures,

the alloy 600 ht No. 54318

RCS cold leg

RTDs are

expected to last until the

end of plant life.

None of the

alloy 600 heats

discussed

above are found in Unit l.

FPL contracted with B&W Nuclear Technologies

(B&W) to replace

the nozzles

and

RTDs under the

B&W gA program..

The applicable

Code for the nozzle

and

RTD replacement

is

ASME

B&PV Code:

Section

V - 1989 Edition with no Addenda

(89NA);

Section

IX - Edition in effect at the time of the activity; and

Section

XI -.89NA.

During the Unit 2 RFO, the licensee

implemented

PCM No. 152-295

RCS Hot Leg Instrument Nozzle Replacement for 8 flow

measurement

nozzle

J and

1 sampling nozzle

K.

These.'instrument

and

sample

nozzles

were part of the

RCS pressure

boundary

and

were

made of a specific heat treat of material

known to be

'usceptible

to

PWSCC.

Flow measurement

nozzle

J for PDT-1121B

was found to be leaking

on October

10.

The J nozzles

attached

sensing lines to the

RCS hot legs for

pressure differential transmitters

PDT-llllA, B,

C,

and

D,

PDT-

1112A,

B,

C,

and D,'nd

PDT-1124W,

X, Y, and Z.

The PDT-lllA,

B,

C and

D, and

PDT-1121A,

B,

C and

D were part of the

RPS

and

measured

the reactor coolant flow.

The

K nozzle provided

a

RCS

sampling port off the

A hot leg.

This sample port was used

by

the Primary Sampling

System

and the

PASS to check reactor

coolant chemistry

and radioactivity.

This work was being performed

by

B&W using

a

FRG reviewed

and

approved

process traveler.

This process traveler

was

a

compendium of detailed work procedures,

operating instructions,

inservice

and

NDE inspection

procedures

including

contractor/FPL

gC signoffs.

25

On November 2, the inspectors

observed

the inprocess

work for

the

-'A hot leg nozzle replacements.

This included

a visual

examination of the work site

and

a discussion

with the onsite

contractor lead engineer.

At the time, the A hot leg nozzles

had

been cut and removed

and workers were aligning the two

drill jigs prior to machining.

The inspector

was impressed

with the contractor lead engineer's

knowledge of and

familiarity with the work.

The work was controlled by the lead

.

. engineer

inside containment with closed circuit TV and radio

communications to

a trailer parked

on the west. side of the

RAB.

As steps

were completed,

the lead engineer initialed a work

copy of the procedure

and informed the contractor staff in the

trailer via radio.

After completion of work and

upon exiting

containment,

the original procedure

was signed

by those

contractor workers performing the work.

On November 3, the inspectors

reviewed the process travelers

with the contractor

gC inspector

and noted only one minor

discrepancy.

The contractor

gC inspector working the night

shift on November

2 had mistakenly dated

4 signoffs as

"10/2/95" vice "11/2/95" for the

B hot leg work.

This

.

discrepancy

was considered

minor and editorial in nature.

The

dayshift contractor

gC inspector identified the four signoffs

for'correction.

All hotleg nozzle work was completed

by November'

and the

final contractor'ecords

verification performed

on November

11.

S

On November

1'4 and

15 the inspector

reviewed the completed work

package

in gC and noted the following discrepancies:

4

A.

RC-126 location

~

Sequence

120-00:

date of gC signoff was incorrectly

identified as "10-2-95".

~

Sequence

310:

verification

BY and

DATE signoffs were

lined through

and initialed, however,

completion of

this sequence

was IV'd..

B.

RC-127 location

~

Sequence

120-00:

.date of gC signoff was incorrectly

identified as "10-2-95".

C.

RC-128 location

~

Sequence

120-00:

date of gC signoff was incorrectly

identified as "10-2-95".

~

Sequence

130:

date of worker signoff was incorrectly

identified as "10-3-95".

26

During this

same period of time,. the contractor

a]so replaced

3

pressurizer

nozzles;

I temperature

nozzle located

on the lower

pressurizer

shell

(102E),

and

2 instrument nozzles

both located

on the lower pressurizer

head

(109A and

109B) per

PCH 027-295.

All pressurizer

nozzle work was completed

by November

10 and

the final contractor records verification performed

on November

12.

A review of this 'completed

work package

performed

by the

inspector identified the following discrepancies:

A.

102E location

~

Sequence

870:

"ASD" initials of welder performing

work were not included'n Attachment

3 - Authorized

Signature Identification List.

B.

109A location

Sequences

610-00 through 630,

655-00,

and 730-00

through 750-00 were annotated

"superse'ded

by NCR 95-

00099".

Attachment

2 -

NCR Log showed

NCR 95-00099

affecting only Sequence

740.

~

Sequence

655-00

was annotated

"See

NCR0 95-00098".

Attachment

2 -

NCR Log showed

NCR 95-00098 affecting

Sequences

600 and 655.

The inspectors

discussed

with the contractor difficulties

.encountered

during the wor k, specifically, the

4 failures of

the

UT examination of the. repaired =Inconel pad.'he

contractor

noted that this was the first time they had encountered

this

problem and believe that it was related to the difficulty in

performing weld repairs

due to the pad orientation

on the lower

pressurizer shell.

The inspectors

also reviewed

PCN 027-295,

Pressurizer

Nozzle

~R1

lihi 1dd:

P

T

1

  • NOEp

d

and,reports;

STAR reports;

drawings;

Weld Control Records;

equality Control inspection reports; 'Authorized Signature

Identification Lists; heat treatment reports

and charts;

Foreign Material

and Personnel

Control Logs; nonconformance

reports;

welding material certified material test reports;

welder Performance qualification Records;

and Welding Procedure

Specifications

and their supporting. Procedure qualification

Records.

Observations

were compared with the

Code

and applicable

procedures.

27

Relative to the

PCH package

review, the inspectors

noted the

following:

Several

examples

where initials in the Authorized

Signature Identification Lists were

made in cursive

(hand

written) and the initials in the

PCM sign-off blocks were

block printed or vice versa.

The failure of sign-off

initials to match the Authorized Signature Identification

Lists initials, negates

value of the Authorized Signature

Identification Lists.

The inspectors

considered this

a

weakness.

Several

minor documentation

errors,

examples

were:

corrections

made without the

B&W gA program required

single line strike out, initial and'ate;

Weld Control

Record form was not amended to match current practice,

form required welder initials which are not

programmatically required;

missing required t'itles on

signature

blocks;

and lateral

expansion

dimensions

on

a

Welding Procedure gualification Record were reported in

mills as required,

but labeled in inches.

The licensee

made

on the spot corrections.

~

The nozzles

and

RTDs were replaced

by properly qualified

and certified welders,

gC inspectors,

and

NDE examiners

in

accordance

with properly qualified Welding Procedure

Specifications,

using properly certified welding filler

materials

and

NDE consumables.

No evidence of the non-

compliant activities of the type identified during the

1993

and

1994 nozzle replacement

outages,;were

identified

during this review.

4

The inspectors

determined that overall, this job wa's managed

very effectively and completed

on time without any significant

problems.

2)'ide

Range

SG Level Upgrade.

PCM 068-294

Wide Range

SG Level Upgrade for Reg Guide 1.97 was

also

implemented during this Unit 2 RFO.

This

Reg Guide

required that wide range

SG level instrumentation

be available

following an accident

("post accident qualified").

The

original Unit 2 design

included only I instrument per

SG whose

level transmitters

(LT-9012 .and 9022) were not qualified for a

post accident

environment.

The licensee

established

a two step

(phased

approach)

to

A.

Upgrade the environmental qualification of the existing

instrumentation,

via the previously implemented

PCN 138-

293,

and

28

B.

Add redundant

instrumentation,

with certain limitations

and exceptions

as noted in

PCH 068-294.

Work was performed

between

October

28 and November

6 by a

contractor,

under the supervision of Construction Services,

with plant testing identified as

an outstanding

item.

On

November 20, the newly installed instrumentation

was calibrated

.and placed in service.

On November

14 and

15 the inspector reviewed the completed

work

package

and did not identify any deficiencies.

This

modification also was well managed

and complete)'n

time -.,--

without any

significant;:pro5l,ems')

Emergency Diesel

Generators

The Unit 2

EDGs were taken out'of service

one at

a time to

perform routine

18 month refueling inspections

and planned

maintenance.

The following scheduled activities were

accomplished

on

EDG 2A.

~

18 month ele'ctrical

and mechanical

inspection.

'

Repair various leaks.

~ 'eplace

governor actuators.

~

Overhaul turbo lube oil motors.

~

PCH 019-295H replace water manifold. bolts.

'

PCH 156-295 delete

EDG start

on CIAS and

CSAS.

~

PCH 165-295 modify LO lube oil pressur e alarm.

~

PCH 160-295

change pre-lube check -valves to swing type

valve.

I

~

Install

new fuel oil piping from .the ..FOST to diesel oil

day

tank.'n

addition to the above planned repairs,

a problem involving

the failure of several

Curtis relay sockets

was identified.

The

18 month electrical surveillance

included removal

and bench

testing of approximately

54 relays

used in the diesel start

and

control circuitry.

After the above testing,

the, relays were

reinstalled.

During post maintenance

testing

on November 3,

EDG 2A failed to start.

Troubleshooting

found

a cracked solder

joint in the shutdown relay socket.

This socket

was replaced

and the

EDG was started.

During subsequent

testing,

the load

started

responding erratically and

was not controllable

so the

diesel

was unloaded

and shutdown.

Investigation found

a high

resistance

solder connection

on the 52Xl female relay socket.

Since this failure was similar to the above failures,

a

decision

was

made to perform resistance

testing of the

remaining

52 relay sockets.

This testing found that two

additional relay sockets,

air solenoids

(AVIA) and idle start

(R9) relays were defective.

Both of, these relay sockets

were

replaced.

k \\

29

In November 6, during the

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> surveillance run, the

operator discovered that the

EDG did not respond to i%put

control signals.

The engine

was secured

and troubleshooting

efforts again found'

problem with a relay socket solder

connection

(SSIX).

The licensee

then assigned

a team consisting of system

.engineering,

corporate

engineering,

operations,

maint'enance,

. procurement,

and materials

management

to investigate this issue

and determine the root cause

and needed corrective action.

This team found that past

and future potential failures could

be attributed to flexing of the relay base

and socket that

occurred

when the relays were removed for testing during each

refueling outage.

On Unit 2, this testing

had

been

based

on

the

EDG installation vendor recommendations

and

had

been

accomplished

each refueling outage since initial unit, startup

in 1983.

On Unit I, this testing

had started,

on

9 of 30 KPD-13

relays

based

on

INPO SER 22-87 in 1988.

The remainder of the

relays

were

added to surveillance

program in 1994.

The team's

investigation concluded that the flexing of the bases

during

relay removal

had resulted

in flexing and deforming the

receptor contacts

and cracking the solder connections of the

receptor pins to 'base or base to terminal

board connections.

The licensee

obtained

replacement

relay bases

and found that

the replacement

relays

had increased

solder buildup which led

to improved

and more rigid connections

that were less

susceptible

to the failure.

Based

on this evaluation,

the licensee

replaced all 54 relays

.

bases

in

EDG 2A control panel.

A decision

was also

made to

inspect the relay and sockets

on

EDG lA/B as they became

available

and

on

EDG 2B when it was taken out of 'service for

the

18 month inspection during the current refueling outage.

)

The installed relays were square

D, 8501 series

KPD-13 relays

with an ll pin octal type connector

base.

.The socket

base is a

Curtis, RS-ll.

The socket

assembly is rated for 10 amperes

at

250 volts and consists of a socket

and two terminal strips

mounted

on

a circuit board.

The socket

assemblies

were replaced with identical

socket

assemblies

from stores.

As noted

above,

the manufacturer

appears

to have

had

some of the

same

problems identified with

these

components

in the past

because

the replacement

bases

have

much sturdier construction

and better solder buildup.

Based

on the above,

the licensee

determined that the removal

and insertion of the relays during

18 month surveillance

testing resulted in this failure.

In addition to replacing the

sockets

on

EDG 2A, the licensee

developed

and implemented

a

special test procedure to verify satisfactory operation of the

relay and bases after the repairs

were completed.

The

30

inspector followed the above work activities

and

PWO 66/1570

under which the relay replacement

was accomplished.

It was noted that the overall

RFO repair activities

on

EDG 2A

was performed

by a combination of plant, corporate,

and vendor

support representatives.

Good procedural

compliance

was noted

during the work observations.

It was also noted that it took

,several

relay failures before the licensee

was able to

determine the root cause.

The inspector also noted 'that -.during .the24 hour endurance

run

the

16 cylinder engine governor controls appeared

to create

a

high speed oscillations in the fuel rack-mechanism;

The .system

engineer stated that this had

been the normal historical

response

of this engine

and governor control

system.'=.-.The

inspector discussed

this issue with the maintenance

qanager

arid

plant general

manager

and questioned if this could i'.'reate

excessive

stress

and

abnormal

wear on the engine control

and

led to early failure.

The plant manager indicated that

he

would have maintenance

and engineering

look into this item

further after completing the outage

maintenance

on

EDG 2B.

Since the engine successfully

completed

a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. full load

surveillance

run and

no oscillations in

EDG frequency

was

noted,

the inspector reluctantly agreed to this approach.

On November 9,

EDG IB was taken .out of service

and

.-.

relays

were inspected.

Several

relay bases

were--found with

solder defects or loose receptor connectors.

No'.deficiencies

were identified that in the licensee's

opinion would have

resulted

in a failure that could have prevented

EDG IB from

performing its safety function.

Seventeen

rel'ay sockets

were

replaced

as

a precautionary

measure.

EDG IB was -returned to

service

on November

10,

1995.

Based

on this inspection

and the

fact that the relays in Unit I have only been

removed from

testing once,

the licensee

decided to schedule

the inspections

on

EDG 1A in early December after Unit 2 has completed the

current

RFO.

The licensee's

long. term plans call for replacing

all relay bases

on Unit I during the next refueling outage.

On November ll,

EDG 2B was taken out of service to perform the

18 month surveillance,

planned corrective maintenance,

selected

modifications,

and inspection of the relay problem identified

on

EDG 2A.

The following activities were planned:

18 month electrical

and mechanical

inspection.

Repair engine oil leak.

Replace

12 and

16 cylinder governor actuators.

Replace

16 cylinder fan shaft

and bearings.

Replace fuel oil priming pump due to excessive

packing

leakage.

Meld repair

on

16 cylinder fan drive idler adjuster.

Inspect

and repair abrasions

on actuator wiring.

31

Overhaul of turbo lube oil motors.

Installed

new fuel oil line from DFOST to

EDG 2B day tank.

Calibration of I&C equipment.

PCH 019-295H install

new water manifold bolts.

PCH 160-295

change

pre-lube

check valves to swing type.

PCH 156-295 delete

EDG 2B start

on CIAS and

CSAS.

PCH 165-295 eliminate spurious

LO lube oil pressure

alarm.

Inspect,

replace defective Curtis relay

sockets.'he

inspection of Curtis relay sockets

found them in

essentially

the

same condition

as

EDG 2A.

All 54 of the relay

sockets. were subsequently

replaced.

The inspector

observed

-selected

portions of these activities which were accomplished

under

PWOs 66/1678,

66/1612,

66/1443,

and maintenance

procedure

MP 2-2200063,

Rev 19, "Periodic Test of EDG 2B," and

HP 2-

0950187,

Rev 0, ."Operation of Emergency Diesel Generator for

Haintenance

and Governor Setup Following Governor Actuator

Replacement."

The relay replacement activity was originally planned

by the

licensee to repair all sockets

and build up the solder

connectors

under guidance

provided

by engineering.

The

inspector questioned this practice

and the means of determining

acceptable

repairs,

seismic qualifications of the repair,

and

what type of post maintenance

testing

was required.

Rather

than attempt to answer these

questions,

the licensee

elected to

replace all 54 relays with new ones they were able to obtain.

The inspector then reviewed the test of the relay and

new bases

and found it to be acceptable.

After completion of the relay work,

EDG 2B was restarted

to

perform gover'nor setup

and tuning.

Problems

were encountered

in achieving the proper

response

from the

16 cylinder governor

actuator during loaded conditions.

Afte'r extensive

troubleshooting

and attempts to adjust both engines,

a problem

was discovered

in the wiring harness

to the governor actuator.

It appeared

that vibrations

had resulted

in shorting two

control wires together near the connector plug.

This short

was

in the close proximity to

a chaffing problem previously

corrected

and discussed

in IR 95-18.

Repairs

were performed

on

this wiring.

The wiring harness for the

12 cylinder governor

was also

removed.

Even though

no defects

were identified, all

connections

were resoldered

and reinsulated.

The licensee

currently plan to perform these

same inspections

on

EDG 2A and

EDGs lA/B at the earliest opportunity.

The remaining work and

governor adjustments

were completed

and the unit successfully

completed

the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> endurance

run and was returned to service

on November 29.

The inspector followed the above activities

as they occurred.

Specific observations

included, relay base

replacement

and

testing, wiring harness

repairs,

governor setup

and tuning,

32

various troubleshooting activities

and portions of the

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

endurance

run.

Overall performance

and procedural

compliance

of the craft personnel

performing the work was considered

good.

System engineering

support

was considered

good until the

assigned

engineer

became unavailable.

The initial governor

setup

and tuning appeared

to be lacking in technical

expertise.

Additional vendor support services

and the return of the system

.engineer resulted in completing these activities after

a delay

, of several

days.

The licensee notified the

NRC of the relay problem

on November

20,

and plan to submit

a

LER on this item.

4)

PCN-008-295

RPS NI,Rpyl'acement/Upgrade

The licensee

implemented this

PCN duri,ng4he current Unit 2

refueling outage.

The modifications "removed'original

CE

components

and installed replacements

developed

by

Gammametrics.

Replaced

components

included wide range

NI

detectors,

preamps

and drawers.

The .changes,

combined with a

similar

PCM to be applied to Unit I in 1996, allows

consolidation of parts,

standardization

of units,

and increased

gain sensitivities,

allowing for more accurate

indication of

flux in low leakage

cores.

The inspector reviewed the

PCH package

and'onducted

a walkdown .-

of installed,

accessible

components

with the

I&C System

Supervisor.

In viewing the Gammametrics

wide range

preamplifier boards in the Reactor Building keyway, the

inspector

noted that the cabling connecting to the -board-

included large

Ray-Chem splices

which appeared

to be securing

the cables'onnectors..to

the cables

themselves. 'he splices

were

so bulky as to prevent the cables

from being bent inside

the preamplifier cabinet to their mating connectors.

The

inspector questioned

th'e propriety of this application of the

splices.

The System Supervisor initiated STAR 951873 to

consider the question.

The STAR's resolution allowed the

cables to be used until the next refueling outage with the use

of 90'onnectors,

which precluded the need to bend the cables.

The acceptability of the splicing was based

upon .past history

of operability,

combined with satisfactory

meggar

and

continuity tests.

The inspector witnessed

portions of the post-installation

acceptance

testing performed

on the

B and

D wide range

NI

channels.

The inspector

found the procedure

and the

performance of testing to be satisfactory.

33

b.

. Surveillance

Observations

(61726)

Various plant operations

were verified to comply with selected

TS

requirements.

Typical of:these

were confirmation of TS compliance

for reactor coolant chemistry,

RWT conditions,

containment

pressure,

control

room ventilation,

and

AC and

DC electrical

sources.

The

inspectors verified that testing

was performed in accordance

with

adequate

procedures,

test instrumentation

was calibrated,

'LCOs were

met,, removal

and restoration of the affected

components

were

accomplished

properly, test results

met requirements

and were

reviewed

by personnel

other than the individual directing the test,

and that any deficiencies identified during the testing were

properly reviewed

and resolved

by appropriate

management

personnel;

"-='-"-

,

The following surveillance test(s)

were observed:

1)

OP 2-0400050,

Rev 16, "Periodic Test of the Engineered

Safety

Features."

On November

28 the licensee

continued the Integrated

Safeguards.

Test for EDG 2B Section 8.9 Diesel Generator Start

on

ESFAS

without

LOOP and 8. 10

EDG Loaded

24 Hour Run and Hot Restart.

This procedure

has several

TCs incorporated to allow for post

modification testing of

PCM 156-295

and interfacing to

OP 2-

2200050B

2B Emergency Diesel

Generator

Periodic Test

and

General

Operating Instructions.

PCM 156-295 modified the

EDG

logic to remove the

CIAS and

CSAS start signals which was.

described

in IR 95-18.

A thorough pretest briefing was conducted prior to stationing

test personnel.

The post modification testing confirmed that

the

2B

EDG did not start

on

a CIAS or

CSAS signal

and that when

paralleled to an offsite power source did not shift the

EDG to

the isochronous

Mode after receiving

a CIAS signal.

Following

completion of this portion of the test

a SIAS signal

was

inserted to verify the start of the

2B EDG. Voltage

and

frequency stabilized in the operating

range within the

10

seconds

allowed.

2B

EDG was then loaded to greater than 3800

MW for the first 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> of the

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run.

The inspector

verified that the voltage

and frequency were in spec

and that

the

EDG had stabilized load.

The inspector noted that the test

was well controlled, test

steps

were signed off as completed

and that good communication

practices

were observed.

No deficiencies

were identified.

2)

Missed Surveillance

on

RCS Boron Sample

Unit 2 Technical Specification 3. 1.2.9 required that boron

concentration

be verified consistent with shutdown margin in

Mode

5 by sampling the

RCS at

a frequency determined

by the

number of operable

charging

pumps;

The

AS requires that all

.

34

operations

involving core alterations

or positive reactivity..

changes

be suspended if the

TS requirement is not meet.

At approximately ll:45 pm on November

27 operations

discovered

.

that the required

8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

RCS chemistry surveillance with no

charging

pumps in operation

had not been

completed

since I:00

pm on November 27.

Operations

then

had Chemistry take

an

RCS

.sample.

At 12:00

pm Chemistry reported that the

RCS

'-

concentration

was within prescribed limited.

This time

exceeded

the allowable

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> +25 percent allowable extension

per

TS 4.0.2

by I hour.

I

The apparent

cause of this violation appears

to be the failure

of operations

and chemistry to identify that sampling

requirement

time changed

from 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in Mode 6 to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> in

Mode 5.

The unit had entered

Mode

5 at 3: 10

pm on November 27,

1995.

This surveillance=was

missed

on the day and peak shift

checks

and identified on the midshift.

This

same surveillance

was missed for 2 days in October

when Unit 2 entered

Mode 6 and

was identified as

NCV 389/95-18-06.

The licensee's

corrective

actions

on that item was to implement

a temporary

change to

Administrative Procedure

2-0010125

"Schedule of Periodic Tests,

Checks

and Calibrations" to require that

a Data sheet

30 of the

above procedure

be filled out to document this surveillance.

This item was also discussed

in the Operations

Department Night

Orders

on October 26.

A review of this check sheet for AP 2-

0010125 found that each shift had initialed off this step but

had not compl.eted the required data sheet.

This is

a

violation, VIO 389/95-21-03,

"Failure to Perform

RCS Boron

Surveillance."

The licensee's

investigation

had not been

completed at-the

end

of the inspection period so all corrective actions

had not been

identified.

4

3)

Eddy Current Test of Steam Genera)or

Tubing

The licensee

ECT examined the'n'it"'2

SG tubes in accordance

with Procedure

NDE 1.3,

"Eddy Current Examination of

'onferromagnetic

Tubing Using Multifrequency Techniques

MIZ18/30," Rev 7, with Field Changes

A and.B.

The examinations

were conducted

by FPL personnel

augmented

by contract personnel

under the umbrella of the

FPL gA program.

The applicable

Code

for ET examination of Unit 2

SG tubes is The

ASME B&PV Code

Section XI 89NA.

To determine

whether the licensee

conducted

ECT examinations

in accordance

with regulatory commitments

and

procedural

requirements,

the inspector

examined selected

gA

records

and 'supporting data

as desc} ibed below.

35

The

ECT examination of the Unit 2

SG tubes

included the

following:

~

Bobbin coil examination of all active tubes,

tube

end

to'ube

end.

~

Motorized Rotating

Pancake

(MRPC) examination of hot leg

transitions.

~

MRPC examination of 20 percent of cold leg tubes with

emphasis

on the stay rod and sludge pile areas.

~

MRPC examination of all dented

tube support intersections.

~

MRPC examination of selected

bobbin coil indications.

This outage,

the licensee

examined

a total of 16,355 tubes in

both

SG A and

B, identifying 383,recordable

indications

and

eight indications requiring plugging.

In addition the licensee

plugged eight tubes

as preventive maintenance.

Unit 2 Steam Generator

Tube Plug Status

SG 2A

SG-2B

Total

Tubes

Plugged Through

EOC-7

New tubes

Plugged

EOC-8

Total Tubes

Plugged through

EOC-8

269

274

198

209

467

16

483,

The inspectors

reviewed procedure

NDE 1.3, the data for the

~

plug indications,

the data for the five largest recordable

indications,

the qualification certification and visual acuity

certification documentation for ll selected

ECT examiners,

and

the calibration documentation for eight remote data acquisition

units.

Observations

were compared with the

Code

and

NDE 1.3.

The Unit 2

SG tube

ECT examinations

were conservatively

conducted

by properly qualified examiners

in accordance

with a

well written procedure.

4)

1B Emergency Diesel

Generator Periodic Test

The inspectors

observed

the performance of OP 1-2200050B,

Rev

24,

"1B Emergency Diesel

Generator

Periodic Test

and General

Operating Instructions."

OP 1-2200050B

was issued to satisfy

the 31 day surveillance

mandated

by Technical Specification

3/4.8.1.

This particular performance of Operating

Procedure

36

No.

1-2200050B,

was accomplished

to satisfy the requirements

of

AP 0010022,

Rev 0,

"Emergency Diesel

Generator Reliability

Program."

The inspectors

observed

the pre-job tail board

meeting

and the surveillance activities in the Emergency Diesel

Generator

(EDG) building.

The inspectors verified that the

latest version of the procedure

was used,

the personnel

were

properly qualified,

and tools were appropriately calibrated.

, During the performance of this surveillance the inspectors

noted the following:

~

A water valve adjacent to alarmed door 180,

and

a gage

labeled only "Water Temperature"

did not have plant

identification tags

and were not identified by a Plant

Labeling Deficiency Tag indicating that the deficiencies

were not 'formally identified by the licensee's

personnel.

Considering that the

EDG test is currently being performed

on

a

15 day periodicity, these labeling deficiencies

should

have

been identified by plant personnel.

'Replacement

bulbs were found in the log book rack on the

IB D-G.Idle Start Stop panel.

Other plants

have

experienced

plant trips as

a result of the inadvertent

installation of an incorrect panel

bulb.

Leaving

replacement

bulbs out and uncontrolled is and invitation

to trouble.

~

The water level site glass

on the

1B1 Radiator Expansion

Tank uses )-inch wide red tape to mark the high and low

water levels.

Operating

Procedure

No. I-2200050B step 8.1

4 does not specify where the water level is to be

evaluated

(above the tape,

below .the tape or behind the

tape).

l ~

~

The operators

conducting this surveillance

were

knowledgeable.

Procedure

adherence

was good.

The

coordination of this activity between the control

room. and

the

EDG building was good despite the remote location

a'nd

the high noise level.

5)

Vacuum Relief Test

The inspectors

observed

the performance of Data Sheet

24 of AP

1-0010125A,

Rev 41,

"Valve Testing Procedure."

This valve

exercise test, of the containment

vessel

to annulus

vacuum

relief valve Nos.

FCV-25-7 and

FCV 25-8, is conducted to

satisfy the requirements

of Technical Specification 3/4.6.5.

The inspectors

observed

the pre-job tail board meeting

and the

surveillance activities conducted

in the Unit I control

room.

The inspectors verified that the latest version of the

procedure

was used,

the personnel

were properly qualified,

and

tools were appropriately calibrated.

37

5.

Plant Support

(71750)

a.

Fire Protection

During the course of their normal tours, the inspectors

routinely

examined facets of the Fire Protection

Program.

The inspectors

reviewed transient fire loads,

flammable mater'ials storage,

housekeeping,

control hazardous

chemicals,

ignition source/fire risk

reduction efforts, fire protection training, fire protection

system

surveillance

program, fire barriers, fire brigade qualifications,

and

gA reviews of the program.

No deficiencies

were identified.

b.

Physic@'.-Protection

During this inspection,

the inspector toured the protected, area

and

noted that the perimeter

fence

was intact

and not compromised

by

erosion or disrepair.

The fence fabric was secured

and barbed wire

was angled

as required

by the licensee's

PSP.

Isolation zones

were

maintained

on both sides of the barrier and were free of objects

which could shield or conceal

an individual.

C.

The inspector

observed

personnel

and packages

entering the protected

area

were searched

either by special'purpose

detectors

or by a

physical

patdown for firearms, explosives

and'- contraband.

The

processing

and escorting of visitors was observed.

Vehicles were

.searched,

escorted,

and secured

as described

in the

PSP.

Lighting

of the perimeter 'and of the protected

area

met the 0.2 foot-candle

criteria.

In conclusion,

selected

functions

and equipment of the security

program were inspected

and found to comply with the

PSP

requirements.

Radiological Protection

Program

Radiation protection control activities were observed

to verify that

these activities were in conformance with the facility policies

and

procedures,

and in compliance with regulatory requirements.

These

observations

included:

Entry to and exit from 'contaminated

areas,

including step-off

pad conditions

and disposal of contaminated clothing;

Area postings

and controls;

Mork activity within radiation,

high radiation,

and

contaminated

areas;

Radiation Control Area

(RCA) exiting practices;

and;

Proper wearing of personnel

monitoring equipment,

protective

clothing,

and respiratory equipment.

V

38

1)

On November

2 the inspector

reviewed the nozzle replacement

worksite inside containment,

paragraph

4.a. l.

Prior to

entering containment,

the inspector contacted

HP in the Unit 2

RAB at approximately

10:00

am and requested

a current copy o'

both the

A and

B hot leg radiation survey maps.

HP provided

the A hot leg survey

performed at 1:00

am on November 2,

however,

was unable to locate

a current survey of the

B hot

,leg.

At the time, the inspector

understood that work'n the

A

hot leg was at the step where drilling and machining would

occur

and that scaffolding was still being erected

on the

B hot

'leg prior. to cutting and removal of the existing nozzles.

The

inspector requested

that

HP identify and provide the most

recent

B hot leg survey.

The HP'ech that the .inspector

spoke

with located

a general

area survey of the

B ho&-leg done

October

24 but believed that each shift performed this survey

and that

a more recent

one

was available.

Upon entering containment,

the inspector contacted

the

HP tech

covering the work on the A hot leg.

The

HP tech requested

the

specific

RMP used

by the inspector

and provided specific

and

detailed information on the radiation

and contamination levels

at the worksite.

.The inspector

was impressed

by the

HP techs

positive control of personnel

entering the work ar'ea

and

overall

knowledge of current radiological conditions.

On November

3 the inspector returned to the Unit 2

RAB HP

office to collect the

B hot leg survey requested

the previous

day.

The inspector

was given

a total of 4 surveys;

a general

area

survey done at 8:00

am on October 24,

a specific area

survey for removal of lead to install

a glove bag done at 2:00

am on October 31,

a general

area

survey done, at ll:00 am .on

November

2 and contamination

smears of scaffolding done at 9:30

pm on November 2.

The inspector questioned

the

HP supervisor

to determine

how often rad surveys

are required

and whether

workers entering containment

reviewed them.

The

HP supervisor

stated that radiological conditions were addressed

by HP techs

in the required prework briefings

and that only in isolated

instances

did workers request

and review rad surveys maintained

in the

HP office in the

RAB which is outside the

RCA.

The

HP

supervisor referred the inspector to the applicable

HP

procedures for how often rad surveys

are required.

The

inspector

reviewed

HPP-23 Health Physics Activities in the

Reactor

Containment Building During Shutdown

and noted three

cases

in which

a rad survey is required:

~

step 7.2.1 which was recently

changed

from

"Radiation

and

contamination surveys...should

be performed ...

once per

shift.." to "Radiation

and contamination

surveys

should

be

performed daily",

~

step 7.2.1

as directed

by the

HPSS

39

~

step 7.3.2 "All work areas

shall

be surveyed or verified

that

a curr@it survey has

been performed prior to start of

work in that area".

The fact that

a recent

documented

rad survey

on the

B hot leg

was not available for inspector review was brought to the

attention of the

HP Department

Head.

His followup indicated

-that the required surveys

were performed but not documented

and

.

that

he had instructed

HP personnel

that future surveys

were to.

be documented.

The inspector identified this as

a program

weakness.

The inspector

also reviewed HPP-I, "Radiation Work Permits,"

Rev 2, which refers to completing attachments,

e..g.,

Attachment

D prework briefing checklist.

These

attachments

were revised

and given

HPP Form Numbers only.

This editorial error was

brought to the attention of the

HP Department.

The inspector obtained

a copy of "A Layman's

Guide to Radiation

Safety" from the training department.

On page

54 in the Lesson

Titled:

Survey Naps,

appears

the statement

"Survey maps are

the best reference

to use to learn the dose rates

and

contamination levels in your work area".

The inspector could

find no requirement

or recommendation

in HPP procedures

for

radiation workers to refer to survey maps.

Radiation workers

are,

however, required to attend

prework briefin'g in which

radiological controls information is discussed

by HP.

The fact

that few, if any, workers actually, review completed

rad surveys

prior to performing work and that

HP apparently

assumes

complete responsibility in addressing

rad conditions during the

prework briefings did not reinforce the enabling objective of

RCAT training.'t

a very minimum, the licensee

may want to

consider

asking whether

any workers would like to review the

current survey.

This training and work practices

issue

was discussed

with the

HP Department

Head who said that

a STAR would be issued to

address

corrective actions.

6.

Exit Interview

The inspection

scope

and findings were summarized

on December I, 1995,

with those

persons

indicated in paragraph

I above.

The inspector

described

the areas

inspected

and discussed

in detail the inspection

results listed below.

Proprietary material is not contained

in this

repor't.

Dissenting

comments

were not received

from the licensee.

~Te

Item Number

40

Et

~0

VIO

VIO

VIO

50-389/95-21-01

50-389/95-21-02

50-389/95/21/03

Open

Open

Open

"Failure to Follow Clearance

Procedures,"

paragraph

3.a.3)B.

"Failure to Follow the

Equipment Clearance

Order

Procedure

and Require

Independent Verification of

a TS Related

Component,"

paragraph 3.d.2).

'Failure

to Perform

RCS

Boron Surveillance,'"

paragraph 4.b.2).

NCV

50=389/95-21-04

Closed

"Failure .to Haintain

Penetration

Logs,'" paragraph

3.a.4)B.

7.

Abbreviations,

Acronyms,

and Initialisms

ATTN

CC

CCTV

CCW

CE

CEA

CET

CFR

CIAS

CSAS

CST

DFOST

DPR

ECT

ECCS

EDG

EH

ESF

ESFAS

FCV

FHE

FOST

Foreign Haterial Exclusion

Fuel Oil Storage

Tank

ADV

,

Atmospheric

Dump Valve

AEOD

Analysis

and Evaluation of Operational

Data, Office for (NRC)

AFW

Auxiliary Feedwater

(system)

ANPO

Auxiliary Nuclear Plant [unlicensed]

Operator

ANPS

.

Assistant Nuclear Plant Sup'ervisor

AP

Administrative Procedure

ASHE Code American Society of Hechani'cal

Engineers 'Boiler and Pressure

Vessel

Code

.Attention

Cubic Centimeter

Closed Circuit Television

Component

Cooling Water

Combustion

Engineering

(company)

Control

Element Assembly

Core Exit Thermocouple

Code of Federal

Regulations

Containment Isolation Actuation Signal

Containment

Spray Actuation System

Condensate

Storage

Tank

Deisel

Fuel Oil Storage

Tank

Demonstration

Power Reactor

(A type of operating license)

Eddy Current test

Emergency

Core Cooling System

Emergency Diesel

Generator

Electrical Haintenance

Engineered

Safety Feature

Engineered

Safety Feature Actuation System

Flow Control Valve

FPL

FR

FRG

FSAR

GMP

HP

HPP

HPSI

HPSS

HX

I&C

ICW

i.e.

INPO

IR

IV

JPN

LCO

LER

LOOP

MFP

MFRV

MFW

MOV

MRPC

MV

MW

NCR

NCV

NDE

NI

No.

NPF

NPS

NPWO

NRC

NRR

NWE

ONOP

00S

OP

OWA

PASS

PCM

PDR

PGM

PAID

PORV

PSL

PSP

PWO

PWSCC

41

The Florida Power L Light Company

Federal

Regulation

Facility Review Group

Final Safety Analysis Report

General

Maintenance

Procedure

Health Physics

Health Physics

Procedure

High Pressure

Safety -Injection (system)

, Health Physics Shift Supervisor

Heat Exchanger

Instrumentation

and Control

Intake Cooling Water

that is

Institute for Nuclear

Power Operations

[NRC] Inspection

Report

Independent Verification

(Juno

Beach)

Nuclear Engineering

TS Limiting Condition for Operation

Licensee

Event Report

Loss of Offsite Power

Main Feed

Pump

Main Feed Regulating Valve

Main Feed Water

Motor Operated

Valve

Motorized Rotating

Pancake

Motorized Valve

Megawatt(s)

Non Conformance

Report

NonCited Violation (of NRC requirements)

Non Destructive

Examination

Nuclear Instrument

Number

Nuclear Production Facility.(a type of operati

Nuclear Plant Supervisor

Nuclear Plant Work Order

Nuclear Regulatory

Commission

NRC Office of Nuclear Reactor Regulation

Nuclear Watch Engineer

Off Normal Operating

Procedure

Out Of Service

Operating

Procedure

Operator

Work Around

Post Accident Sampling

System

Plant Change/Modification

NRC Public Document

Room

Plant General

Manager

Piping

8 Instrumentation

Diagram

Power Operated Relief Valve

Plant St.

Lucie

Physical

Security Plan

Plant Work Order

Primary Water StressCracking

Corrosion

ng license)

I

QA

QC

QI

RAB

RCAT

RCO

RCP

RCS

Rev

RFO

RG

RII

RPS

RTD

RWP

RWT

SDC

SER

SFP

SG

SIAS

St.

STA

. STAR

TC

TEDB

TS

UFSAR

VCR

VDC

'I.O;-

WO

XFHR

42

Quality Assurance

Quality Control

Quality Instruction

Reactor Auxiliary Building

Radiation Control Access Training

Reactor Control Operator

Reactor Coolant

Pump

.Reactor

Coolant System

Revision

Refueling Outage

[NRC] Regulatory Guide

Region II - Atlanta, Georgia

(NRC),

Reactor Protection

System

Resistive

Temperature

Detector

Radiation

Work Permit

Refueling Water Tank

Shut

Down Cooling

Safety Evaluation Report

Spent

Fuel

Pool

Steam Generator

Safety Injection Actuation System

Saint

'Shift Technical Advisor

St.'Lucie Action Request

Temporary

Change

Total Equipment Data

Base

Technical Specification(s)

Updated Final Safety Analysis Report

Video Cassette

Recorder

Volts Direct Current

Violation (of NRC requirements).

Work Order

Transformer